05000366/LER-1982-041: Difference between revisions

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| document report number = LER-82-041-03L-01, LER-82-41-3L-1, NUDOCS 8206110207
| document report number = LER-82-041-03L-01, LER-82-41-3L-1, NUDOCS 8206110207
| package number = ML20054E433
| package number = ML20054E433
| document type = LICENSEE EVENT REPORT (SEE ALSO AO,RO), TEXT-SAFETY REPORT
| document type = LICENSEE EVENT REPORT (SEE ALSO AO RO), TEXT-SAFETY REPORT
| page count = 2
| page count = 2
}}
}}

Revision as of 14:36, 15 March 2020

LER 82-041/03L-0:on 820516,during Cold Shutdown,Pipe Clamp Found Removed from Core Spray B Loop Test Line to Torus. Clamp Hold Pipe Restraint 2E21-CS-R106 in Place.Caused by Personnel Error.Clamp Reinstalled
ML20054E438
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 06/03/1982
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20054E433 List:
References
LER-82-041-03L-01, LER-82-41-3L-1, NUDOCS 8206110207
Download: ML20054E438 (2)


LER-2082-041,
Event date:
Report date:
3662082041R00 - NRC Website

text

NRC FORM 3665 U. S. NUCLEAR REGULATORY COMMISSION (7 77) .

LICENSEE EVENT REPORT (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

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EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h i o gj l On May 16, 1982, while Unit Two was in cold shutdown a pipe clamp was l o 3 l found removed from the Core Spray "B" Loop Test Line to the Torus by a l g o i,; l Plant Equipment Operator. The subject clamp holds pipe restraint I io m i 2E21-CS-R106 in place. Plant operation was not affected. There were l y a is l l no effects upon public health and safety due to this non-repetitive event. I lo lil I I l O ITl i I

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JJ 34 35 36 3/ 40 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h io l The cause of this event was attributed to personnel error since no l l3 li l l Maintenance Request (MR) was generated to remove the clamp initially. l

,, l The clamp was reinstalled and inspected per MR-2-82-2861 by May 18, i iiial 1 1982. l 1: 141 I l 7 8 9 80 ST S  % POWE R OTHE R STATUS dis OV RY DISCOVERY DESCRIPTION I1 l'> l l Gl@ l 01010 l@l NA l lBl@l ODerator observatinn l A TiVITY CONTENT HELEASED OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELEASE li 16 l [ Zj @ [Z_j@l NA I l NA l PERSONNEL EXPOS ES NuveeR TYPE DESCRIPTION @

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  • DESCRIPTION U PDR ADOCK 05000366
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NAVE OF PHEPARER R. T. Nix, Supt. of Maintenance pgong. 912-367-7781

LER No.: 50-366/1982-041 Licensee: Georgia Power Company

-Facility: Edwin I. Hatch Docket No.: 50-366 Narrative Report for LER 50-366/1982-041 On May 16, 1982, while Unit Two was in cold shutdown, a pipe clamp was found removed from the "B" Core Spray Loop Test Line to the Torus by a Plant Equipment Operator. The subject clamp holds pipe restraint 2E21-CS-R106 in place. Plant operation was not affected. There were no effects upon public health and safety due to this non-repetitive event.

The cause of this event was attributed'to personnel error since no Maintenance Request (MR) was generated to remove the clamp initially.

The clamp was reinstalled and inspected per MR-2-82-2861 by May 18, 1982. ,

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