IR 05000348/2017004: Difference between revisions
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
||
(4 intermediate revisions by the same user not shown) | |||
Line 3: | Line 3: | ||
| issue date = 02/12/2018 | | issue date = 02/12/2018 | ||
| title = NRC Integrated Inspection Report 05000348/2017004 and 05000364/2017004 | | title = NRC Integrated Inspection Report 05000348/2017004 and 05000364/2017004 | ||
| author name = Blamey A | | author name = Blamey A | ||
| author affiliation = NRC/RGN-II/DRP/RPB2 | | author affiliation = NRC/RGN-II/DRP/RPB2 | ||
| addressee name = Madison D | | addressee name = Madison D | ||
| addressee affiliation = Southern Nuclear Operating Co, Inc | | addressee affiliation = Southern Nuclear Operating Co, Inc | ||
| docket = 05000348, 05000364 | | docket = 05000348, 05000364 | ||
Line 18: | Line 18: | ||
=Text= | =Text= | ||
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION | {{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION ary 12, 2018 | ||
==SUBJECT:== | |||
JOSEPH M. FARLEY NUCLEAR PLANT - NUCLEAR REGULATORY COMMISSION INTEGRATED INSPECTION REPORT 05000348/2017004 AND 05000364/2017004 | |||
==Dear Mr. Madison:== | ==Dear Mr. Madison:== | ||
On December 31, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Joseph M. Farley Nuclear Plant, Units 1 and 2. On January 23, 2017, NRC inspectors discussed the results of this inspection with you and other members of your staff | On December 31, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Joseph M. Farley Nuclear Plant, Units 1 and 2. On January 23, 2017, NRC inspectors discussed the results of this inspection with you and other members of your staff. | ||
NRC inspectors documented three findings of very low safety significance (Green) in this report. Two findings involved violations of NRC requirements. In addition, the inspectors documented a licensee-identified violation which was determined to be of very low safety significance in this report. The NRC is | The results of this inspection are documented in the enclosed report. | ||
NRC inspectors documented three findings of very low safety significance (Green) in this report. Two findings involved violations of NRC requirements. In addition, the inspectors documented a licensee-identified violation which was determined to be of very low safety significance in this report. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy. | |||
If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. | If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. | ||
Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555- 0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC resident inspector at the Joseph M. Farley Nuclear Plant, Units 1 and 2. | Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC resident inspector at the Joseph M. Farley Nuclear Plant, Units 1 and 2. | ||
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the | If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC resident inspector at the Joseph M. Farley Nuclear Plant, Units 1 and 2. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding. | ||
Director, Office of Enforcement; and the NRC resident inspector at the Joseph M. Farley Nuclear Plant, Units 1 and 2. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, | |||
Sincerely, | Sincerely, | ||
/RA/ | /RA/ | ||
Alan Blamey, Chief Reactor Projects Branch 2 | Alan Blamey, Chief Reactor Projects Branch 2 Division of Reactor Projects Docket Nos.: 50-348, 50-364 License Nos.: NPF-2, NPF-8 | ||
===Enclosure:=== | |||
IR 05000348/2017004, 05000364/2017004 w/Attachment: Supplemental Information | |||
License Nos.: NPF-2, NPF-8 | REGION II== | ||
Docket Nos.: 50-348, 50-364 License Nos.: NPF-2, NPF-8 Report No.: 05000348/2017004; and 05000364/2017004 Licensee: Southern Nuclear Operating Company, Inc. | |||
Facility: Joseph M. Farley Nuclear Plant Location: Columbia, Alabama Dates: October 1, 2017 through December 31, 2017 Inspectors: P. Niebaum, Senior Resident Inspector K. Miller, Resident Inspector B. Collins, Reactor Inspector (1R08) | |||
W. Pursley, Health Physics Inspector (2RS1) | |||
B. Caballero, Senior Operations Engineer (1R11) | |||
Approved by: Alan Blamey, Chief Reactor Projects Branch 2 Division of Reactor Projects Enclosure | |||
Facility: Joseph M. Farley Nuclear Plant | |||
Location: Columbia, Alabama | |||
Dates: October 1, 2017 through December 31, 2017 | |||
Inspectors: P. Niebaum, Senior Resident Inspector K. Miller, Resident Inspector B. Collins, Reactor Inspector (1R08) | |||
W. Pursley, Health Physics Inspector (2RS1) B. Caballero, Senior Operations Engineer (1R11) | |||
Approved by: Alan Blamey, Chief Reactor Projects Branch 2 Division of Reactor Projects | |||
=SUMMARY= | =SUMMARY= | ||
IR 05000348/2017004; and 05000364/2017004, October 1, 2017, through December 31, 2017; | IR 05000348/2017004; and 05000364/2017004, October 1, 2017, through December 31, 2017; | ||
Joseph M. Farley Nuclear Plant, Units 1 and 2, Fire Protection, Refueling and Other Outage Activities, Problem Identification and Resolution. | Joseph M. Farley Nuclear Plant, Units 1 and 2, Fire Protection, Refueling and Other Outage Activities, Problem Identification and Resolution. | ||
The report covered a 3-month period of inspection by resident inspectors and regional inspectors. There are two NRC-identified and one self-revealing violations documented in this report. The significance of inspection findings are indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, | The report covered a 3-month period of inspection by resident inspectors and regional inspectors. There are two NRC-identified and one self-revealing violations documented in this report. The significance of inspection findings are indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC)0609, Significance Determination Process (SDP) dated April 29, 2015. If a cross-cutting area was assigned include the following: The cross-cutting aspects are determined using IMC 0310, | ||
Aspects within the Cross-Cutting Areas dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy dated November 1, 2016. The NRCs program for overseeing the safe operations of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 6. | |||
Documents reviewed by the inspectors which are not identified in the Report Details are identified in the Attachment. | |||
===Cornerstone: Mitigating Systems=== | ===Cornerstone: Mitigating Systems=== | ||
: '''Green.''' | : '''Green.''' | ||
A self-revealing finding was identified for the | A self-revealing finding was identified for the licensees failure to evaluate the impacts to the Unit 2 Reactor Coolant Pump (RCP) 2C oil collection system when a service water (SW) leak was identified on the Unit 2 RCP motor air coolers. As a result, a strategy was not implemented to prevent service water from collecting in the 2C RCP oil collection system drain tank which impacted its design function while the plant was in Mode 1. The licensees failure to evaluate the potential impacts to the Unit 2 RCP 2C oil collection system during the operability/functionality evaluation of the SW leak associated with RCP motor air coolers was a performance deficiency. The licensee initiated condition reports (CRs) 10420400 and 10422562 and replaced the 2C RCP motor and leaking air cooler. | ||
The finding was more than minor because it was associated with the protection against external factors (fires) and adversely affected the mitigating systems cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, failure to maintain adequate capacity in the RCP 2C Oil Spillage Protection System (OSPS) oil collection tank presented a degradation of a fire confinement component which has a fire prevention function of not allowing an oil leak to reach hot surfaces. The significance of this finding was evaluated using IMC 0609, Appendix F, "Fire Protection Significance Determination Process, | The finding was more than minor because it was associated with the protection against external factors (fires) and adversely affected the mitigating systems cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, failure to maintain adequate capacity in the RCP 2C Oil Spillage Protection System (OSPS) oil collection tank presented a degradation of a fire confinement component which has a fire prevention function of not allowing an oil leak to reach hot surfaces. The significance of this finding was evaluated using IMC 0609, Appendix F, "Fire Protection Significance Determination Process, dated September 20, 2013, because the performance deficiency affected fire protection defense-in-depth strategies involving fire confinement. | ||
Using IMC 0609, Appendix F, Attachment 1, | Using IMC 0609, Appendix F, Attachment 1, Fire Protection Significance Determination Process Worksheet, the inspectors determined that the finding was of very low safety significance (Green) because the exposed fire area contained no potential damage targets that are unique from those in the exposing fire area. The inspectors determined the finding had a cross-cutting aspect of Evaluation in the problem identification and resolution area because the licensee did not fully evaluate the impacts of the RCP motor air cooler SW leak on the Unit 2 RCP oil collection systems. [P.2] (Section 1R05) | ||
: '''Green.''' | : '''Green.''' | ||
An NRC-identified NCV of 10 CFR 50.48(c) and National Fire Protection Association Standard 805 (NFPA 805), Section 3.3.12, was identified for the | An NRC-identified NCV of 10 CFR 50.48(c) and National Fire Protection Association Standard 805 (NFPA 805), Section 3.3.12, was identified for the licensees failure to maintain the Unit 2 RCP 2B oil collection system in an operable condition to perform its design function. Specifically, the licensee failed to ensure that the RCP 2B OSPS oil lift system enclosure collected all oil leakage from all potential leakage sites, including the oil lift system. The licensees failure to maintain the Unit 2 RCP 2B oil collection system in an operable condition to perform its design function was a performance deficiency. The licensee initiated CR 10428611, and determined an oil leak was not active. Another CR was initiated (10446206) to inspect and, if needed, repair this area at the next available opportunity. | ||
OSPS oil lift system enclosure collected all oil leakage from all potential leakage sites, including the oil lift system. The | |||
The finding was more than minor because if left uncorrected, the performance deficiency would have the potential to become a more significant safety concern. Specifically, failing to ensure that the RCP 2B Oil Spillage Protection System oil lift system enclosure collected all oil leakage from all potential leakage sites, including the oil lift system, presented a degradation of a fire confinement component which has a fire prevention function of not allowing an oil leak to reach hot surfaces. The significance of this finding was evaluated using IMC 0609, Appendix F, "Fire Protection Significance Determination Process, | The finding was more than minor because if left uncorrected, the performance deficiency would have the potential to become a more significant safety concern. Specifically, failing to ensure that the RCP 2B Oil Spillage Protection System oil lift system enclosure collected all oil leakage from all potential leakage sites, including the oil lift system, presented a degradation of a fire confinement component which has a fire prevention function of not allowing an oil leak to reach hot surfaces. The significance of this finding was evaluated using IMC 0609, Appendix F, "Fire Protection Significance Determination Process, dated September 20, 2013, because the performance deficiency affected fire protection defense-in-depth strategies involving fire confinement. Using IMC 0609, | ||
Appendix F, Attachment 1, | Appendix F, Attachment 1, Fire Protection Significance Determination Process Worksheet, the inspectors determined that the finding was of very low safety significance (Green) because the exposed fire area contains no potential damage targets that are unique from those in the exposing fire area. The inspectors determined the finding had a cross-cutting aspect of Design Margins in the human performance area because the licensee did not maintain fire protection defense-in-depth by ensuring the Unit 2 RCP 2B oil collection system was in an operable condition to perform its design function. (H.6) (Section 1R20) | ||
: '''Green.''' | : '''Green.''' | ||
A self-revealing NCV of Technical Specification (TS) 5.4.1.a, | A self-revealing NCV of Technical Specification (TS) 5.4.1.a, Procedures, was identified when the Unit 1 Turbine Driven Auxiliary Feedwater (TDAFW) uninterruptible power supplies (UPS) swapped to a bypass power source during maintenance on November 5, 2017. As a result, the TDAFW pump was rendered inoperable. Failure to follow licensee procedure FNP-1-EMP-1352.01, TDAFW UPS Battery Weekly Battery Inspection, Version 19, as written was a performance deficiency. The operability of the TDAFW pump UPS was restored after approximately 3 hours. The licensee entered this issue into their Corrective Action Program (CAP) as Condition Report (CR) 10427370. | ||
The finding was more than minor because it was associated with the equipment performance attribute of the mitigating system cornerstone and adversely affected that cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences since the TDAFW pump was rendered inoperable. The significance of this finding was evaluated using | The finding was more than minor because it was associated with the equipment performance attribute of the mitigating system cornerstone and adversely affected that cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences since the TDAFW pump was rendered inoperable. The significance of this finding was evaluated using IMC 0609, Appendix A, The Significance Determination Process (SDP) for findings at Power, dated June 19, 2012. This finding was determined to be of very low safety significance (Green) because all of the mitigating systems screening questions were answered NO. The inspectors determined the finding had a cross-cutting aspect of Avoid Complacency in the Human Performance area because the individuals involved in this maintenance did not recognize or plan for the possibility of mistakes and appropriate error reduction tools were not implemented. [H.12] (Section 4OA2.3) | ||
Violations of very low safety significance that were identified by the licensee have been reviewed by the NRC. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. These violations and corrective action tracking numbers are listed in Section 4OA7 of this report. | |||
=REPORT DETAILS= | =REPORT DETAILS= | ||
Line 102: | Line 84: | ||
===Summary of Plant Status=== | ===Summary of Plant Status=== | ||
Unit 1: | Unit 1: Unit 1 started the report period at approximately 100 percent rated thermal power (RTP). Unit 1 maintained approximately 100 percent RTP through the end of the report period. | ||
Unit 2: | Unit 2: Unit 2 started the report period at approx. 100 percent RTP. On October 15, 2017, Unit 2 shutdown for a refueling outage. Following completion of the outage on November 15, 2017, Unit 2 achieved 100 percent RTP on November 19, 2017. Unit 2 maintained approximately 100 percent RTP through the end of the report period. | ||
==REACTOR SAFETY== | ==REACTOR SAFETY== | ||
Cornerstones: | Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity {{a|1R01}} | ||
{{a|1R01}} | |||
==1R01 Adverse Weather Protection== | ==1R01 Adverse Weather Protection== | ||
{{IP sample|IP=IP 71111.01}} | {{IP sample|IP=IP 71111.01}} | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Impending Adverse Weather Conditions: | Impending Adverse Weather Conditions: The inspectors reviewed the licensees preparations to protect risk-significant systems from adverse weather conditions (Tropical Storm/Hurricane Nate) expected on site October 7 and 8, 2017. The inspectors evaluated the licensees implementation of adverse weather preparation procedures and compensatory measures, including operator staffing, before the onset of the adverse weather conditions. The inspectors verified that operator actions specified in the licensees adverse weather procedure maintain readiness of essential systems. | ||
The inspectors also verified that the licensee implemented periodic equipment walkdowns or other measures to ensure that the condition of plant equipment met operability requirements. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R04}} | ||
{{a|1R04}} | |||
==1R04 Equipment Alignment== | ==1R04 Equipment Alignment== | ||
{{IP sample|IP=IP 71111.04}} | {{IP sample|IP=IP 71111.04}} | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Partial Walkdown: | Partial Walkdown: The inspectors verified that critical portions of the following systems were correctly aligned by performing partial walkdowns. The inspectors determined the correct system lineup by reviewing plant procedures and drawings listed in the | ||
. | . | ||
* Unit 2, | * Unit 2, 2B emergency diesel generator (EDG) | ||
* Unit 2, | * Unit 2, 2B penetration room filtration system The inspectors reviewed corrective action documents, including condition reports and outstanding work orders, to verify the licensee was identifying and resolving equipment alignment discrepancies. The inspectors also reviewed periodic reports containing information on the status of risk-significant systems, including maintenance rule reports and system health reports. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R05}} | ||
{{a|1R05}} | |||
==1R05 Fire Protection== | ==1R05 Fire Protection== | ||
{{IP sample|IP=IP 71111.05AQ}} | {{IP sample|IP=IP 71111.05AQ}} | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Quarterly Inspection: | Quarterly Inspection: The inspectors evaluated the adequacy of fire plans by comparing the fire plans to the defined hazards and defense-in-depth features specified in the fire protection program for the following fire areas. | ||
* Unit 2, Room 2-055 - Containment Building, Fire Area 2-055, Fire Zone 2-CTMT | * Unit 2, Room 2-055 - Containment Building, Fire Area 2-055, Fire Zone 2-CTMT | ||
* Unit 1 and 2, Room 401, Common Main Control Room, Room, Fire Area 044, Fire Zones 0401-U1 & 0401-U2 | * Unit 1 and 2, Room 401, Common Main Control Room, Room, Fire Area 044, Fire Zones 0401-U1 & 0401-U2 The inspectors assessed the following: | ||
The inspectors assessed the following: | |||
* control of transient combustibles and ignition sources | * control of transient combustibles and ignition sources | ||
* fire detection systems | * fire detection systems | ||
Line 148: | Line 125: | ||
* passive fire protection features | * passive fire protection features | ||
* compensatory measures and fire watches | * compensatory measures and fire watches | ||
* issues related to fire protection contained in the | * issues related to fire protection contained in the licensees corrective action program | ||
* material condition and operational status of fire protection equipment | * material condition and operational status of fire protection equipment | ||
Line 154: | Line 131: | ||
=====Introduction:===== | =====Introduction:===== | ||
A Green Self-Revealing finding was identified for the | A Green Self-Revealing finding was identified for the licensees failure to evaluate the impacts to the Unit 2 Reactor Coolant Pump (RCP) 2C oil collection system when a service water (SW) leak was identified on the Unit 2 RCP motor air coolers. As a result, a strategy was not implemented to prevent service water from collecting in the 2C RCP oil collection system drain tank which impacted its design function while the plant was in Mode 1. The licensees failure to evaluate the potential impacts to the Unit 2 RCP 2C oil collection system during the operability/functionality evaluation of the SW leak associated with RCP motor air coolers, was a performance deficiency. | ||
=====Description:===== | =====Description:===== | ||
On October 17, 2017, the inspectors performed a Unit 2 containment building inspection while the plant was in Mode 5. The inspectors noted that one of the RCP 2C motor air cooling coils had been leaking service water and some of that water was dripping from inside the motor housing into the oil catch-basin below the lower motor bearing oil reservoir. The licensee had previously noted an increasing rate of Unit 2 containment sump in-leakage, beginning on September 21, 2017, and operating personnel made a containment entry on September 27 to look for possible leak sources in low-dose accessible areas, concluding that an RCP motor air cooling coil was likely leaking service water. By October 9, 2017, the Unit 2 containment sump in-leakage rate was approximately 0.75 gpm. Plant operators evaluated the operational impact on October 10, 2017, associated with CR 10411954, but the evaluation did not consider the possible impact on the oil spillage protection system (OSPS) functionality. A 300-gallon capacity OSPS oil collection tank is provided on the 105 | On October 17, 2017, the inspectors performed a Unit 2 containment building inspection while the plant was in Mode 5. The inspectors noted that one of the RCP 2C motor air cooling coils had been leaking service water and some of that water was dripping from inside the motor housing into the oil catch-basin below the lower motor bearing oil reservoir. The licensee had previously noted an increasing rate of Unit 2 containment sump in-leakage, beginning on September 21, 2017, and operating personnel made a containment entry on September 27 to look for possible leak sources in low-dose accessible areas, concluding that an RCP motor air cooling coil was likely leaking service water. By October 9, 2017, the Unit 2 containment sump in-leakage rate was approximately 0.75 gpm. Plant operators evaluated the operational impact on October 10, 2017, associated with CR 10411954, but the evaluation did not consider the possible impact on the oil spillage protection system (OSPS) functionality. A 300-gallon capacity OSPS oil collection tank is provided on the 105-6 elevation of the containment for each RCP and each RCP motor contains 265 gallons of lubricating oil. Each tank is provided with an open vent of 2-inch schedule 40 piping at the top of the tank. Following the containment inspection on October 17, 2017, the licensee drained the contents of each oil collection tank and found approximately 137 gallons of water in the 2C RCP oil collection drain tank. With this amount of water in the tank, there would not be sufficient capacity in the tank to contain the full inventory of the RCP 2C motor lubricating system. | ||
procedure NMP-AD-012, | The tank would only be able to accept approximately 163 gallons of oil, leaving up to 102 gallons of oil that would spill out onto the reactor containment building floor. Licensee procedure NMP-AD-012, Operability Determinations and Functionality Assessments, Ver. 13.1, section 4.2.3 required (in part) the licensee to evaluate the effects on other components if the condition could affect other components. Contrary to those requirements, the licensee failed to consider the impacts on the U2 RCPs oil collection system, during the operability/functionality evaluation of the RCP air motor SW leak. | ||
The licensee initiated CRs 10420400 and 10422562 and replaced the 2C RCP motor and leaking air cooler. | The licensee initiated CRs 10420400 and 10422562 and replaced the 2C RCP motor and leaking air cooler. | ||
=====Analysis:===== | =====Analysis:===== | ||
The | The licensees failure to evaluate the potential impacts to the Unit 2 RCP 2C oil collection system during the operability/functionality evaluation of the SW leak associated with RCP motor air coolers was a performance deficiency. The finding was more than minor because it was associated with the protection against external factors (fires) and adversely affected the mitigating systems cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, failure to maintain adequate capacity in the RCP 2C OSPS oil collection tank presented a degradation of a fire confinement component which has a fire prevention function of not allowing an oil leak to reach hot surfaces. The significance of this finding was evaluated using IMC 0609, Appendix F, "Fire Protection Significance Determination Process, dated September 20, 2013, because the performance deficiency affected fire protection defense-in-depth strategies involving fire confinement. Using IMC 0609, Appendix F, Attachment 1, Fire Protection Significance Determination Process Worksheet, the inspectors determined that the finding was of very low safety significance (Green) because the exposed fire area contains no potential damage targets that are unique from those in the exposing fire area. The inspectors determined the finding had a cross-cutting aspect of Evaluation in the problem identification and resolution area because the licensee did not fully evaluate the impacts of the RCP motor air cooler SW leak on the Unit 2 RCP oil collection systems. [P.2] | ||
=====Enforcement:===== | =====Enforcement:===== | ||
Line 173: | Line 150: | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Non-Destructive Examination | Non-Destructive Examination Activities and Welding Activities From October 23 - October 27, 2017, the inspectors conducted an onsite review of the implementation of the licensees inservice inspection (ISI) program for Unit 2. The ISI program is designed to monitor degradation of pressure retaining components in vital system boundaries. The scope of this program includes components within the reactor coolant system boundary, risk-significant piping boundaries, and containment system boundaries. | ||
The inspectors either directly observed or reviewed the following non-destructive examination (NDE) activities. These activities were mandated by the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (Code of Record: | The inspectors either directly observed or reviewed the following non-destructive examination (NDE) activities. These activities were mandated by the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (Code of Record: | ||
2001 Edition with 2003 Addenda). The inspectors evaluated the NDE activities for compliance with the requirements in Section XI and Section V of the ASME Code. The inspectors also evaluated if any identified indications or defects were dispositioned in accordance with either the ASME Code or an NRC-approved alternative requirement. | 2001 Edition with 2003 Addenda). The inspectors evaluated the NDE activities for compliance with the requirements in Section XI and Section V of the ASME Code. The inspectors also evaluated if any identified indications or defects were dispositioned in accordance with either the ASME Code or an NRC-approved alternative requirement. | ||
requirements. | Additionally, the inspectors reviewed the qualifications of the NDE technicians performing the examinations to determine if they were in compliance with ASME Code requirements. | ||
* Ultrasonic Examination (UT) of APR1-4302-12-RB and -13-RB, 12 | * Ultrasonic Examination (UT) of APR1-4302-12-RB and -13-RB, 12 OD, ASME Class 1, Safety Injection system pipe-to-elbow and elbow-to-pipe welds (observed) | ||
* Liquid Penetrant Testing (PT) of Q2-P16-HCB-9, 6 | * Liquid Penetrant Testing (PT) of Q2-P16-HCB-9, 6 OD, ASME Class 2, Service Water system valve-to-pipe weld (reviewed) | ||
* PT of Q2-P16-HCB-9, 6 | * PT of Q2-P16-HCB-9, 6 OD, ASME Class 2, Service Water system valve-to-pipe weld (repair weld) (reviewed) | ||
The inspectors either directly observed or reviewed the following welding activities. The inspectors evaluated these activities for compliance with site procedures and the requirements in Section IX and Section XI of the ASME Code. Specifically, the inspectors reviewed the work orders, repair or replacement plans, weld data sheets, welding procedures, procedure qualification records, welder performance qualification records, and NDE reports. | The inspectors either directly observed or reviewed the following welding activities. The inspectors evaluated these activities for compliance with site procedures and the requirements in Section IX and Section XI of the ASME Code. Specifically, the inspectors reviewed the work orders, repair or replacement plans, weld data sheets, welding procedures, procedure qualification records, welder performance qualification records, and NDE reports. | ||
* WO SNC 849902, Replacement of 6 | * WO SNC 849902, Replacement of 6 Service Water valve Q2P16V072, ASME Class 2 (reviewed) | ||
PWR Vessel Upper Head Penetration Inspection Activities The inspectors verified that the licensee did not identify any indications that were accepted for continued service. Additionally, the inspectors verified that the licensee did not perform any welding repairs to the upper head penetrations since the last Unit 2 refueling outage. | PWR Vessel Upper Head Penetration Inspection Activities The inspectors verified that the licensee did not identify any indications that were accepted for continued service. Additionally, the inspectors verified that the licensee did not perform any welding repairs to the upper head penetrations since the last Unit 2 refueling outage. | ||
Boric Acid Corrosion Control Inspection Activities The inspectors reviewed the | Boric Acid Corrosion Control Inspection Activities The inspectors reviewed the licensees boric acid corrosion control program (BACCP)activities to determine if they were implemented in accordance with program requirements, applicable regulatory requirements, and industry guidance. Specifically, the inspectors performed the following activities: | ||
* Reviewed applicable procedures and the results of the | * Reviewed applicable procedures and the results of the licensees most recent containment walkdown inspection. | ||
* Interviewed the BACCP owner. | * Interviewed the BACCP owner. | ||
* Conducted an independent walkdown of accessible areas of the Unit 2 reactor building containment pipe chase. | * Conducted an independent walkdown of accessible areas of the Unit 2 reactor building containment pipe chase. | ||
* Verified that degraded or nonconforming conditions, such as boric acid leaks, were properly identified and corrected in accordance with the | * Verified that degraded or nonconforming conditions, such as boric acid leaks, were properly identified and corrected in accordance with the licensees BACCP and the CAP. | ||
* Reviewed engineering evaluations of components with boric acid leakage which verified that minimum wall thickness of those components was maintained. | * Reviewed engineering evaluations of components with boric acid leakage which verified that minimum wall thickness of those components was maintained. | ||
Steam Generator Tube Inspection Activities The inspectors reviewed the Unit 2 steam generator maintenance program. The inspectors verified that no steam generator tube inspection activities were required this refueling outage. This inspection schedule was verified with the requirements of the ASME Code, the | Steam Generator Tube Inspection Activities The inspectors reviewed the Unit 2 steam generator maintenance program. The inspectors verified that no steam generator tube inspection activities were required this refueling outage. This inspection schedule was verified with the requirements of the ASME Code, the licensees Technical Specifications, and applicable industry guidance. | ||
the plant. | Identification and Resolution of Problems The inspectors reviewed a sample of ISI-related issues entered into the corrective action program. The inspectors evaluated if the licensee had appropriately described the scope of the problem and had initiated corrective actions. The review also included the licensees consideration and assessment of operating experience events applicable to the plant. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R11}} | ||
{{a|1R11}} | |||
==1R11 Licensed Operator Requalification Program and Licensed Operator Performance== | ==1R11 Licensed Operator Requalification Program and Licensed Operator Performance== | ||
{{IP sample|IP=IP 71111.11}} | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Resident Inspector Quarterly Review of Licensed Operator Requalification: | Resident Inspector Quarterly Review of Licensed Operator Requalification: | ||
The inspectors observed simulator scenarios conducted for training of an operating crew for requalification on November 21, 2017 and December 13, 2017. | The inspectors observed simulator scenarios conducted for training of an operating crew for requalification on November 21, 2017 and December 13, 2017. | ||
Line 220: | Line 189: | ||
* simulator performance Resident Inspector Quarterly Review of Licensed Operator Performance The inspectors observed licensed operator performance in the main control room for the following evolutions: | * simulator performance Resident Inspector Quarterly Review of Licensed Operator Performance The inspectors observed licensed operator performance in the main control room for the following evolutions: | ||
* Unit 2 power ascension to 100% during a Southern Company System Alert on October 10, 2017 | * Unit 2 power ascension to 100% during a Southern Company System Alert on October 10, 2017 | ||
* Unit 2 | * Unit 2 transition to Mode 1 and subsequent power ascension following a refueling outage from November 13 to November 16, 2017 The inspectors assessed the following: | ||
* use of plant procedures | * use of plant procedures | ||
* control board manipulations | * control board manipulations | ||
Line 227: | Line 196: | ||
* use of human error prevention techniques | * use of human error prevention techniques | ||
* documentation of activities | * documentation of activities | ||
* management and supervision oversight Annual Review of Licensee Requalification Examination Results: | * management and supervision oversight Annual Review of Licensee Requalification Examination Results: | ||
On June 29, 2017, the licensee completed the annual requalification operating examinations required to be administered to all licensed operators in accordance with Title 10 of the Code of Federal Regulations 55.59(a)(2), Requalification Requirements, of the NRCs Operators Licenses. The inspectors performed an in-office review of the overall pass/fail results of the individual operating examinations and the crew simulator operating examinations in accordance with Inspection Procedure (IP) 71111.11, Licensed Operator Requalification Program. These results were compared to the thresholds established in Section 3.02, Requalification Examination Results, of IP 71111.11. | |||
On June 29, 2017, the licensee completed the annual requalification operating examinations required to be administered to all licensed operators in accordance with Title 10 of the Code of Federal Regulations 55.59(a)(2), | |||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R12}} | ||
{{a|1R12}} | |||
==1R12 Maintenance Effectiveness== | ==1R12 Maintenance Effectiveness== | ||
{{IP sample|IP=IP 71111.12}} | {{IP sample|IP=IP 71111.12}} | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors assessed the | The inspectors assessed the licensees treatment of the issues listed below to verify the licensee appropriately addressed equipment problems within the scope of the maintenance rule (10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants). The inspectors reviewed procedures and records to evaluate the licensees identification, assessment, and characterization of the problems as well as their corrective actions for returning the equipment to a satisfactory condition. The inspectors also interviewed system engineers and the maintenance rule coordinator to assess the accuracy of any performance deficiencies and extent of condition. | ||
* Quality Control - Unit 2, repair of load sequencer Q2R43E0001B - replacement of electrical DG1 diode with new commercially dedicated item | * Quality Control - Unit 2, repair of load sequencer Q2R43E0001B - replacement of electrical DG1 diode with new commercially dedicated item | ||
* Unit 2 train | * Unit 2 train A service water strainer degraded backwash piping reviewed under structural monitoring program for the maintenance rule | ||
====b. Findings==== | ====b. Findings==== | ||
A licensee-identified violation was identified. See section | A licensee-identified violation was identified. See section 4OA7 for details. {{a|1R13}} | ||
{{a|1R13}} | |||
==1R13 Maintenance Risk Assessments and Emergent Work Control== | ==1R13 Maintenance Risk Assessments and Emergent Work Control== | ||
{{IP sample|IP=IP 71111.13}} | {{IP sample|IP=IP 71111.13}} | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed the maintenance activities listed below to verify that the licensee assessed and managed plant risk as required by 10 CFR 50.65(a)(4) and licensee procedures. The inspectors assessed the adequacy of the | The inspectors reviewed the maintenance activities listed below to verify that the licensee assessed and managed plant risk as required by 10 CFR 50.65(a)(4) and licensee procedures. The inspectors assessed the adequacy of the licensees risk assessments and implementation of risk management actions. The inspectors also verified that the licensee was identifying and resolving problems with assessing, and managing maintenance-related risk using CAP. Additionally, for maintenance resulting from unforeseen situations, the inspectors assessed the effectiveness of the licensees planning and control of emergent work activities. | ||
* Unit 2, October 18, 2017 - U2 shutdown safety assessment with reduced inventory in the reactor vessel | * Unit 2, October 18, 2017 - U2 shutdown safety assessment with reduced inventory in the reactor vessel | ||
* Unit 1, October 22, 2017 - Insulator replacement in low voltage switchyard | * Unit 1, October 22, 2017 - Insulator replacement in low voltage switchyard | ||
Line 258: | Line 221: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R15}} | ||
{{a|1R15}} | |||
==1R15 Operability Determinations and Functionality Assessments== | ==1R15 Operability Determinations and Functionality Assessments== | ||
{{IP sample|IP=IP 71111.15}} | {{IP sample|IP=IP 71111.15}} | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Operability Determinations and Functionality Assessments Review: | Operability Determinations and Functionality Assessments Review: | ||
The inspectors selected the operability determinations or functionality evaluations listed below for review based on the risk-significance of the associated components and systems. The inspectors reviewed the technical adequacy of the determinations to ensure that technical specification operability was properly justified and the components or systems remained capable of performing their design functions. To verify whether components or systems were operable, the inspectors compared the operability and design criteria in the appropriate sections of the technical specification and updated final safety analysis report to the licensees evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with operability evaluations. | |||
The inspectors selected the operability determinations or functionality evaluations listed below for review based on the risk-significance of the associated components and systems. The inspectors reviewed the technical adequacy of the determinations to ensure that technical specification operability was properly justified and the components or systems remained capable of performing their design functions. To verify whether components or systems were operable, the inspectors compared the operability and design criteria in the appropriate sections of the technical specification and updated final safety analysis report to the | |||
* CR10415220, component cooling water (CCW) heat exchangers tube leakage | * CR10415220, component cooling water (CCW) heat exchangers tube leakage | ||
* Work Order (WO) SNC841458, Unit 1 turbine driven auxiliary feedwater pump and turbine oil samples | * Work Order (WO) SNC841458, Unit 1 turbine driven auxiliary feedwater pump and turbine oil samples | ||
Line 274: | Line 235: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R18}} | ||
{{a|1R18}} | |||
==1R18 Plant Modifications== | ==1R18 Plant Modifications== | ||
{{IP sample|IP=IP 71111.18}} | {{IP sample|IP=IP 71111.18}} | ||
Line 284: | Line 244: | ||
* confirmed the modifications did not degrade the design bases, licensing bases, and performance capability of risk significant structures, systems and components. | * confirmed the modifications did not degrade the design bases, licensing bases, and performance capability of risk significant structures, systems and components. | ||
* verified modifications performed during plant configurations involving increased risk did not place the plant in an unsafe condition. | * verified modifications performed during plant configurations involving increased risk did not place the plant in an unsafe condition. | ||
* evaluated whether system operability and availability, configuration control, | * evaluated whether system operability and availability, configuration control, post-installation test activities, and changes to documents, such as drawings, procedures, and operator training materials, complied with licensee standards and NRC requirements. | ||
* reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with modifications. | * reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with modifications. | ||
Line 291: | Line 251: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R19}} | ||
{{a|1R19}} | |||
==1R19 Post-Maintenance Testing== | ==1R19 Post-Maintenance Testing== | ||
{{IP sample|IP=IP 71111.19}} | {{IP sample|IP=IP 71111.19}} | ||
Line 301: | Line 260: | ||
* WO SNC904009, repair of load sequencer Q2R43E0001B | * WO SNC904009, repair of load sequencer Q2R43E0001B | ||
* WO SNC391170, diagnostic test of Q2B31PCV445A | * WO SNC391170, diagnostic test of Q2B31PCV445A | ||
* WO SNC376715, | * WO SNC376715, packing leak on Unit 2 TDAFW governor valve The inspectors evaluated these activities for the following: | ||
* Acceptance criteria were clear and demonstrated operational readiness. | * Acceptance criteria were clear and demonstrated operational readiness. | ||
* Effects of testing on the plant were adequately addressed. | * Effects of testing on the plant were adequately addressed. | ||
Line 312: | Line 271: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|1R20}} | ||
{{a|1R20}} | |||
==1R20 Refueling and Other Outage Activities== | ==1R20 Refueling and Other Outage Activities== | ||
{{IP sample|IP=IP 71111.20}} | {{IP sample|IP=IP 71111.20}} | ||
Line 335: | Line 293: | ||
=====Introduction:===== | =====Introduction:===== | ||
A Green NRC-identified NCV of 10 CFR 50.48(c) and National Fire Protection Association Standard 805 (NFPA 805), Section 3.3.12, was identified for the | A Green NRC-identified NCV of 10 CFR 50.48(c) and National Fire Protection Association Standard 805 (NFPA 805), Section 3.3.12, was identified for the licensees failure to maintain the Unit 2 Reactor Coolant Pump (RCP) 2B oil collection system in an operable condition to perform its design function. Specifically, the licensee failed to ensure that the RCP 2B Oil Spillage Protection System (OSPS) oil lift system enclosure collected all oil leakage from all potential leakage sites, including the oil lift system. The licensees failure to maintain the Unit 2 RCP 2B oil collection system in an operable condition to perform its design function was a performance deficiency. | ||
=====Description:===== | =====Description:===== | ||
On November 8, 2017, while the plant was in Mode 5, the inspectors performed a Unit 2 containment building closeout inspection. The inspectors observed RCP oil leaking out of the bottom of the oil lift system support plate through mounting bolt holes for the 2B RCP. Oil was dripping off the threaded fasteners penetrating the lift system horizontal mounting plate onto the motor air cooling coil, then from the coil onto | On November 8, 2017, while the plant was in Mode 5, the inspectors performed a Unit 2 containment building closeout inspection. The inspectors observed RCP oil leaking out of the bottom of the oil lift system support plate through mounting bolt holes for the 2B RCP. Oil was dripping off the threaded fasteners penetrating the lift system horizontal mounting plate onto the motor air cooling coil, then from the coil onto an electrical box. The RCP 2B lift system had apparently been leaking oil while the associated lift pump was in operation. The lift oil system operates at a pressure in excess of 550 psig. The lift pump is not required to operate once the RCP has started, but the lift pump is restarted when the RCP is stopped. The control room log noted the oil lift pump was operated for twelve minutes on November 3, and again on November 4, 2017, for ten minutes while starting RCP 2B at 0405. The inspectors asked the licensee to determine why the oil was leaking out of the oil lift system enclosure. The licensee initiated CR 10428611, and determined an oil leak was not active. Another CR was initiated (10446206) to inspect and, if needed, repair this area at the next available opportunity. | ||
an electrical box. The RCP 2B lift system had apparently been leaking oil while the associated lift pump was in operation. The lift oil system operates at a pressure in excess of 550 psig. The lift pump is not required to operate once the RCP has started, but the lift pump is restarted when the RCP is stopped. The control room log noted the oil lift pump was operated for twelve minutes on November 3, and again on | |||
=====Analysis:===== | =====Analysis:===== | ||
The | The licensees failure to maintain the Unit 2 RCP 2B oil collection system in an operable condition to perform its design function was a performance deficiency. The finding was more than minor because if left uncorrected, the performance deficiency would have the potential to become a more significant safety concern. Specifically, failing to ensure that the RCP 2B Oil Spillage Protection System (OSPS) oil lift system enclosure collected all oil leakage from all potential leakage sites, including the oil lift system, presented a degradation of a fire confinement component which has a fire prevention function of not allowing an oil leak to reach hot surfaces. The significance of this finding was evaluated using IMC 0609, Appendix F, "Fire Protection Significance Determination Process, dated September 20, 2013, because the performance deficiency affected fire protection defense-in-depth strategies involving fire confinement. | ||
Using IMC 0609, Appendix F, Attachment 1, | Using IMC 0609, Appendix F, Attachment 1, Fire Protection Significance Determination Process Worksheet, the inspectors determined that the finding was of very low safety significance (Green) because the exposed fire area contained no potential damage targets that are unique from those in the exposing fire area. The inspectors determined the finding had a cross-cutting aspect of Design Margins in the human performance area because the licensee did not maintain fire protection defense-in-depth by ensuring the Unit 2 RCP 2B oil collection system was in an operable condition to perform its design function. (H.6) | ||
=====Enforcement:===== | =====Enforcement:===== | ||
Farley Nuclear Plant, Unit 2, Operating License Condition 2.C.(6), required, in part, that the licensee shall implement and maintain in effect all provisions of the approved fire protection program (FPP) that comply with 10 CFR 50.48(c), as specified in the license amendment requests dated September 25, 2012; April 25, 2016; and supplements dated December 20, 2012; September 16, 2013; October 30, 2013; November 12, 2013; April 23, 2014; May 23, 2014; July 3, 2014; August 11, 2014; August 29, 2014; October 13, 2014; January 16, 2015; and as approved in the safety evaluation reports (SER) dated March 10, 2015 and October 17, 2016. The 2001 Edition of NFPA-805, Section 3.3.12, Reactor Coolant Pumps, required that the oil collection system shall be designed and installed such that leakage from the oil system is safely contained for off normal conditions such as accident conditions or earthquakes. | Farley Nuclear Plant, Unit 2, Operating License Condition 2.C.(6),required, in part, that the licensee shall implement and maintain in effect all provisions of the approved fire protection program (FPP) that comply with 10 CFR 50.48(c), as specified in the license amendment requests dated September 25, 2012; April 25, 2016; and supplements dated December 20, 2012; September 16, 2013; October 30, 2013; November 12, 2013; April 23, 2014; May 23, 2014; July 3, 2014; August 11, 2014; August 29, 2014; October 13, 2014; January 16, 2015; and as approved in the safety evaluation reports (SER) dated March 10, 2015 and October 17, 2016. The 2001 Edition of NFPA-805, Section 3.3.12, Reactor Coolant Pumps, required that the oil collection system shall be designed and installed such that leakage from the oil system is safely contained for off normal conditions such as accident conditions or earthquakes. | ||
Leakage points on a reactor coolant pump motor to be protected shall include, but not be limited to the lift pump and piping, overflow lines, oil cooler, oil fill and drain lines and plugs, flanged connections on oil lines, and the oil reservoirs, where such features exist on the reactor coolant pumps. The leakage shall be collected and drained to a vented closed container that can hold the inventory of the reactor coolant pump lubricating oil system. Contrary to the above, the licensee failed to comply with the NFPA 805 code requirements for the Unit 2 RCP oil collection system. Code requirements for oil collection systems for reactor coolant pumps specify the leakage shall be collected and drained to a vented closed container that can hold the inventory of the reactor coolant pump lubricating oil system. The OSPS cannot be relied upon to meet these requirements if it is not maintained in an operable condition to perform its design function. Because the licensee included this deficiency in their corrective action program as CR 10428611 and because the deficiency had low safety significance, this finding will be treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy and is identified as NCV 05000364/2017004-02, Failure to maintain an operable Oil Collection System on RCP 2B. | Leakage points on a reactor coolant pump motor to be protected shall include, but not be limited to the lift pump and piping, overflow lines, oil cooler, oil fill and drain lines and plugs, flanged connections on oil lines, and the oil reservoirs, where such features exist on the reactor coolant pumps. The leakage shall be collected and drained to a vented closed container that can hold the inventory of the reactor coolant pump lubricating oil system. Contrary to the above, the licensee failed to comply with the NFPA 805 code requirements for the Unit 2 RCP oil collection system. Code requirements for oil collection systems for reactor coolant pumps specify the leakage shall be collected and drained to a vented closed container that can hold the inventory of the reactor coolant pump lubricating oil system. The OSPS cannot be relied upon to meet these requirements if it is not maintained in an operable condition to perform its design function. Because the licensee included this deficiency in their corrective action program as CR 10428611 and because the deficiency had low safety significance, this finding will be treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy and is identified as NCV 05000364/2017004-02, Failure to maintain an operable Oil Collection System on RCP 2B. | ||
Line 356: | Line 312: | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed the surveillance tests listed below. The surveillance test was either observed directly or test results were reviewed to verify testing activities and results provide objective evidence that the affected equipment remain capable of performing their intended safety functions and maintain their operational readiness consistent with the | The inspectors reviewed the surveillance tests listed below. The surveillance test was either observed directly or test results were reviewed to verify testing activities and results provide objective evidence that the affected equipment remain capable of performing their intended safety functions and maintain their operational readiness consistent with the facilitys current licensing basis. The inspectors evaluated the test activities to assess for: | ||
* preconditioning of equipment, | * preconditioning of equipment, | ||
* appropriate acceptance criteria, | * appropriate acceptance criteria, | ||
Line 363: | Line 319: | ||
* equipment alignment following completion of the surveillance. | * equipment alignment following completion of the surveillance. | ||
Additionally, the inspectors reviewed a sample of significant surveillance testing problems documented in the | Additionally, the inspectors reviewed a sample of significant surveillance testing problems documented in the licensees corrective action program to verify the licensee was identifying and correcting any testing problems associated with surveillance testing. | ||
Routine Surveillance Tests | Routine Surveillance Tests | ||
Line 369: | Line 325: | ||
* FNP-2-STP-101, Low Power Reactor Physics Testing, Ver. 29 | * FNP-2-STP-101, Low Power Reactor Physics Testing, Ver. 29 | ||
* FNP-2-STP-22.27, 2B Auxiliary Feedwater Pump Cold Shutdown Inservice Test & | * FNP-2-STP-22.27, 2B Auxiliary Feedwater Pump Cold Shutdown Inservice Test & | ||
Preservice Test, Ver. 27.0 | Preservice Test, Ver. 27.0 In-Service Tests (IST) | ||
In-Service Tests (IST) | |||
* FNP-1-STP-23.8, Component Cooling Water Valve Inservice Test, Ver. 51.0 Containment Isolation Valve | * FNP-1-STP-23.8, Component Cooling Water Valve Inservice Test, Ver. 51.0 Containment Isolation Valve | ||
* FNP-2-STP-627.0, Local Leak Rate Testing of Containment Penetrations, Ver. 60 | * FNP-2-STP-627.0, Local Leak Rate Testing of Containment Penetrations, Ver. 60 | ||
Line 378: | Line 332: | ||
No findings were identified. | No findings were identified. | ||
===Cornerstone: | ===Cornerstone: Emergency Preparedness=== | ||
{{a|1EP6}} | {{a|1EP6}} | ||
==1EP6 Drill Evaluation== | ==1EP6 Drill Evaluation== | ||
Line 384: | Line 338: | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors observed the emergency preparedness training drill conducted on December 14, 2017. The inspectors observed licensee activities in the simulator and/or technical support center to evaluate implementation of the emergency plan, including event classification, notification, dose assessment, and protective action recommendations. The inspectors evaluated the | The inspectors observed the emergency preparedness training drill conducted on December 14, 2017. The inspectors observed licensee activities in the simulator and/or technical support center to evaluate implementation of the emergency plan, including event classification, notification, dose assessment, and protective action recommendations. The inspectors evaluated the licensees performance against criteria established in the licensees procedures. Additionally, the inspectors attended the post-exercise critique to assess the licensees effectiveness in identifying emergency preparedness weaknesses and verified the identified weaknesses were entered in the corrective action program. | ||
====b. Findings==== | ====b. Findings==== | ||
Line 390: | Line 344: | ||
==RADIATION SAFETY== | ==RADIATION SAFETY== | ||
(RS) | (RS) {{a|2RS1}} | ||
==2RS1 Radiological Hazard Assessment and Exposure Controls (Seven Inspection Samples== | |||
Completed) | |||
====a. Inspection Scope==== | |||
== | Hazard Assessment and Instructions to Workers. During facility tours, the inspectors directly observed radiological postings and container labeling for areas established within the radiologically controlled area (RCA) of the Unit 2 (U2) containment building, Unit 1 (U1) and U2 auxiliary building and radioactive waste processing and storage locations. The inspectors independently measured radiation dose rates or directly observed conduct of licensee radiation surveys for selected RCA areas. The inspectors reviewed survey records for several plant areas including surveys for airborne radioactivity, gamma surveys with a range of dose rate gradients, surveys for alpha-emitters and other hard-to-detect radionuclides, and pre-job surveys for upcoming tasks. | ||
The inspectors also discussed changes to plant operations that could contribute to changing radiological conditions since the last inspection. The inspectors attended pre-job briefings and reviewed Radiation Work Permit (RWP) details to assess communication of radiological control requirements and current radiological conditions to workers. | |||
Control of Radioactive Material. The inspectors observed surveys of material and personnel being released from the RCA using small article monitor, personnel contamination monitor, and portal monitor instruments. The inspectors discussed equipment sensitivity, alarm setpoints, and release program guidance with licensee staff. | |||
The inspectors also reviewed records of leak tests on selected sealed sources and discussed nationally tracked source transactions with licensee staff. | |||
Hazard Control. The inspectors evaluated access controls and barrier effectiveness for selected High Radiation Area (HRA), Locked High Radiation Area (LHRA), and Very High Radiation Area (VHRA) locations and discussed changes to procedural guidance for LHRA and VHRA controls with Radiation Protection (RP) supervisors. The inspectors reviewed implementation of controls for the storage of irradiated material within the spent fuel pool. Established radiological controls, including airborne controls and electronic dosimeter (ED) alarm setpoints, were evaluated for selected U2 Refueling Outage 25 (U2R25) job tasks. In addition, the inspectors reviewed licensee controls for areas where dose rates could change significantly as a result of plant shutdown and refueling operations. The inspectors also reviewed the use of personnel dosimetry including extremity dosimetry and multibadging in high dose rate gradients. | Hazard Control. The inspectors evaluated access controls and barrier effectiveness for selected High Radiation Area (HRA), Locked High Radiation Area (LHRA), and Very High Radiation Area (VHRA) locations and discussed changes to procedural guidance for LHRA and VHRA controls with Radiation Protection (RP) supervisors. The inspectors reviewed implementation of controls for the storage of irradiated material within the spent fuel pool. Established radiological controls, including airborne controls and electronic dosimeter (ED) alarm setpoints, were evaluated for selected U2 Refueling Outage 25 (U2R25) job tasks. In addition, the inspectors reviewed licensee controls for areas where dose rates could change significantly as a result of plant shutdown and refueling operations. The inspectors also reviewed the use of personnel dosimetry including extremity dosimetry and multibadging in high dose rate gradients. | ||
Radiation Worker Performance and RP Technician Proficiency. Occupational workers | Radiation Worker Performance and RP Technician Proficiency. Occupational workers adherence to selected RWPs and RP technician proficiency in providing job coverage in radiologically significant areas were evaluated through direct observations and interviews with licensee staff. Jobs observed included maintenance work in the reactor cavity including transfer tube removal, seal filter pump room valve cutouts and RVLIS detector removal. The inspectors also evaluated worker responses to dose and dose rate alarms during selected work activities. | ||
Problem Identification and Resolution. The inspectors reviewed and assessed condition reports (CR) associated with radiological hazard assessment and control. The inspectors evaluated the | Problem Identification and Resolution. The inspectors reviewed and assessed condition reports (CR) associated with radiological hazard assessment and control. The inspectors evaluated the licensees ability to identify and resolve the issues in accordance with licensee procedures. The inspectors also reviewed recent self-assessment results. | ||
Inspection Criteria. RP activities were evaluated against the requirements of Updated Final Safety Analysis Report (UFSAR) Section 12, Technical Specifications (TS) | Inspection Criteria. RP activities were evaluated against the requirements of Updated Final Safety Analysis Report (UFSAR) Section 12, Technical Specifications (TS) | ||
Sections 5.4 and 5.7, 10 CFR Parts 19 and 20, and approved licensee procedures. Licensee programs for monitoring materials and personnel released from the RCA were evaluated against 10 CFR Part 20 and IE Circular 81-07, | Sections 5.4 and 5.7, 10 CFR Parts 19 and 20, and approved licensee procedures. | ||
Licensee programs for monitoring materials and personnel released from the RCA were evaluated against 10 CFR Part 20 and IE Circular 81-07, Control of Radioactively Contaminated Material. Documents and records reviewed are listed in the Attachment. | |||
====b. Findings==== | ====b. Findings==== | ||
Line 420: | Line 378: | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed a sample of the performance indicator (PI) data, submitted by the licensee, for the Unit 1 and Unit 2 PIs listed below. The inspectors reviewed plant records compiled between November 2016, and October 2017, to verify the accuracy and completeness of the data reported for the station | The inspectors reviewed a sample of the performance indicator (PI) data, submitted by the licensee, for the Unit 1 and Unit 2 PIs listed below. The inspectors reviewed plant records compiled between November 2016, and October 2017, to verify the accuracy and completeness of the data reported for the station. The inspectors verified that the PI data complied with guidance contained in Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, and licensee procedures. The inspectors verified the accuracy of reported data that were used to calculate the value of each PI. | ||
. The inspectors verified that the PI data complied with guidance contained in Nuclear Energy Institute 99-02, | |||
data. | In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with PI data. | ||
===Cornerstone: | ===Cornerstone: Mitigating Systems=== | ||
* high pressure injection system (Units 1 and 2) | * high pressure injection system (Units 1 and 2) | ||
* emergency AC power system (Units 1 and 2) | * emergency AC power system (Units 1 and 2) | ||
Line 431: | Line 388: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. {{a|4OA2}} | ||
{{a|4OA2}} | |||
==4OA2 Problem Identification and Resolution== | ==4OA2 Problem Identification and Resolution== | ||
{{IP sample|IP=IP 71152}} | {{IP sample|IP=IP 71152}} | ||
===.1 Routine Review=== | ===.1 Routine Review=== | ||
The inspectors screened items entered into the | The inspectors screened items entered into the licensees CAP in order to identify repetitive equipment failures or specific human performance issues for followup. The inspectors reviewed condition reports, attended screening meetings, or accessed the licensees computerized corrective action database. | ||
repetitive equipment failures or specific human performance issues for followup. The inspectors reviewed condition reports, attended screening meetings, or accessed the | |||
====b. Findings and Observations==== | ====b. Findings and Observations==== | ||
Line 447: | Line 401: | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors performed a review of issues entered in the | The inspectors performed a review of issues entered in the licensees CAP and reviewed associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors focused their review on missed surveillance testing, but also considered the results of inspector daily condition report screenings, licensee trending efforts, and licensee human performance results. The review nominally considered the six-month period beginning in July 2017, through December 2017, although some examples extended beyond those dates when the scope of the trend warranted. The inspectors compared their results with the licensees analysis of trends. Additionally, the inspectors reviewed the adequacy of corrective actions associated with a sample of the issues identified in the licensees trend reports. | ||
The inspectors also reviewed corrective action documents that were processed by the licensee to identify potential adverse trends in the condition of structures, systems, and/or components as evidenced by acceptance of long-standing nonconforming or degraded conditions. | The inspectors also reviewed corrective action documents that were processed by the licensee to identify potential adverse trends in the condition of structures, systems, and/or components as evidenced by acceptance of long-standing nonconforming or degraded conditions. | ||
The inspectors performed a search of the CAP database and found 22 examples of condition reports initiated since the beginning of 2017 associated with missed surveillance testing. The licensee identified a cognitive trend in missed surveillance testing and initiated a trend CR (10401365) on August 23, 2017, citing four CRs as examples and noted that the trend had continued over the previous | The inspectors performed a search of the CAP database and found 22 examples of condition reports initiated since the beginning of 2017 associated with missed surveillance testing. The licensee identified a cognitive trend in missed surveillance testing and initiated a trend CR (10401365) on August 23, 2017, citing four CRs as examples and noted that the trend had continued over the previous 41 days. Since that time there were at least an additional seven CRs initiated for issues associated with missed surveillance testing. The licensee nuclear oversite organization also initiated CR 10393974 on August 2, 2017, addressing inadequate engagement in the surveillance program. The licensee initiated Corrective Action Report (CAR) 270723, completing the disposition on December 15, 2017, in an effort to resolve the negative trend, but it is not apparent the licensees corrective actions were effective since the negative trend continues. The inspectors continue to monitor this issue. | ||
====b. Findings and Observations==== | ====b. Findings and Observations==== | ||
Line 460: | Line 414: | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors conducted a detailed review of the following condition report: | The inspectors conducted a detailed review of the following condition report: | ||
* CR10427370, Unit 1 TDAFW inoperability The inspectors evaluated the following attributes of the | * CR10427370, Unit 1 TDAFW inoperability The inspectors evaluated the following attributes of the licensees actions: | ||
* complete and accurate identification of the problem in a timely manner | * complete and accurate identification of the problem in a timely manner | ||
* evaluation and disposition of operability and reportability issues | * evaluation and disposition of operability and reportability issues | ||
Line 472: | Line 426: | ||
=====Introduction:===== | =====Introduction:===== | ||
A Green self-revealing non-cited violation (NCV) of Technical Specification (TS) 5.4.1.a, | A Green self-revealing non-cited violation (NCV) of Technical Specification (TS) 5.4.1.a, Procedures, was identified when the Unit 1 TDAFW uninterruptible power supplies (UPS) swapped to a bypass power source during maintenance on November 5, 2017. As a result, the TDAFW pump was rendered inoperable. Failure to follow licensee procedure FNP-1-EMP-1352.01, TDAFW UPS Battery Weekly Battery Inspection, Version 19, as written was a performance deficiency. | ||
=====Description:===== | =====Description:===== | ||
Maintenance performed a preventive maintenance task on the Unit 1 TDAFW UPS in accordance with work order SNC860880 and licensee procedure FNP-1-EMP-1352.01, | Maintenance performed a preventive maintenance task on the Unit 1 TDAFW UPS in accordance with work order SNC860880 and licensee procedure FNP-1-EMP-1352.01, TDAFW UPS Battery Weekly Battery Inspection, Ver. 19 on November 5, 2017. While making an adjustment to the primary charger float potentiometer, a step was performed out of sequence. This caused the charger failure light to come on locally at the UPS and annunciator JH4 TDAFWP UPS FAULT in the main control room. This also caused the UPS to swap from the primary UPS charger to the secondary UPS charger. The missed step was then performed which opened the battery input breaker to the secondary UPS and caused both UPS to swap to a bypass source. According to the licensee, this action rendered the TDAFW pump inoperable. | ||
10427370. | The TDAFW pump UPS consists of two separate full capacity UPS connected in a primary/secondary arrangement. Both UPS are normally in operation with the primary UPS supplying all of the loads. The operability of the TDAFW pump UPS was restored after approximately 3 hours. The licensee entered this issue into their CAP as CR 10427370. | ||
=====Analysis:===== | =====Analysis:===== | ||
The failure to follow licensee procedure FNP-1-EMP-1352, Ver. 19.0 as written during maintenance on the Unit 1 TDAFW pump UPS on November 5, 2017 was a performance deficiency. Specifically, steps in section 4.7.a were performed out of sequence which resulted in an unavailable UPS and an inoperable TDAFW pump. The finding was more than minor because it was associated with the equipment performance attribute of the mitigating system cornerstone and adversely affected that cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences since the TDAFW pump was rendered inoperable. The significance of this finding was evaluated using IMC 0609, Appendix A, | The failure to follow licensee procedure FNP-1-EMP-1352, Ver. 19.0 as written during maintenance on the Unit 1 TDAFW pump UPS on November 5, 2017 was a performance deficiency. Specifically, steps in section 4.7.a were performed out of sequence which resulted in an unavailable UPS and an inoperable TDAFW pump. The finding was more than minor because it was associated with the equipment performance attribute of the mitigating system cornerstone and adversely affected that cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences since the TDAFW pump was rendered inoperable. The significance of this finding was evaluated using IMC 0609, Appendix A, The Significance Determination Process (SDP) for findings at-Power, dated June 19, 2012. This finding was determined to be of very low safety significance (Green) because all of the mitigating systems screening questions were answered NO. | ||
dated June 19, 2012. This finding was determined to be of very low safety significance (Green) because all of the mitigating systems screening questions were answered NO. | |||
The inspectors determined the finding had a cross-cutting aspect of Avoid Complacency in the Human Performance area because the individuals involved in this maintenance did not recognize or plan for the possibility of mistakes and appropriate error reduction tools were not implemented. | The inspectors determined the finding had a cross-cutting aspect of Avoid Complacency in the Human Performance area because the individuals involved in this maintenance did not recognize or plan for the possibility of mistakes and appropriate error reduction tools were not implemented. [H.12] | ||
=====Enforcement:===== | =====Enforcement:===== | ||
Technical Specification 5.4.1.a, | Technical Specification 5.4.1.a, Procedures, required, in part, that written procedures shall be established, implemented and maintained covering the applicable procedures recommended in Regulatory Guide (RG) 1.33, Revision 2, Appendix A. Section 9.a of RG 1.33, Appendix A, stated in part that maintenance that can affect the performance of safety-related equipment should be properly preplanned and performed in accordance with written procedures. Contrary to the above, on Nov. 5, 2017, licensee procedure FNP-1-EMP-1352.01, TDAFW UPS Battery Weekly Battery Inspection, Version 19 was performed out of sequence during maintenance the Unit 1 TDAFW UPS which rendered the TDAFW pump inoperable. The licensee entered this issue into their corrective action program (CAP) as condition report (CR) 10427370. The operability of the TDAFW pump UPS was restored after approximately 3 hours. | ||
Because this finding is of very low safety significance and has been entered into the CAP, this violation was treated as an NCV, consistent with the Enforcement Policy. NCV 05000348/2017004-03 | Because this finding is of very low safety significance and has been entered into the CAP, this violation was treated as an NCV, consistent with the Enforcement Policy. NCV 05000348/2017004-03 Failure to Follow Procedure Resulted in Inoperable TDAFW pump. | ||
{{a|4OA3}} | {{a|4OA3}} | ||
==4OA3 Follow-up of Events== | ==4OA3 Follow-up of Events== | ||
{{IP sample|IP=IP 71153}} | {{IP sample|IP=IP 71153}} | ||
===1. (Closed) Licensee Event Report (LER) 05000348/2016-007-02: Plant Shutdown Required by Technical Specifications due to Inoperable Steam Flow Transmitters | ===1. (Closed) Licensee Event Report (LER) 05000348/2016-007-02: Plant Shutdown=== | ||
Required by Technical Specifications due to Inoperable Steam Flow Transmitters | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
During the | During the licensees engineering review of cycle full power scaling values for steam flow normalization at the beginning of a new fuel cycle for Unit 1 while in Mode 1 at 99 percent reactor power, three steam flow channel values were found to be non-conservative and outside of +/- 2.5% delta pressure scan. This non-conservatism would allow steam flow to exceed the TS trip set-point before a steam line isolation would occur. Unit 1 initiated a plant shutdown on November 17, 2016, at 6:59 p.m. in accordance with Limiting Condition for Operation (LCO) 3.0.3 for having no operable steam flow channels for the C Steam Generator (SG). The two steam flow channels did not meet acceptance criteria for TS 3.3.2. On November 18, 2016, at 12:41 a.m., the Unit 1 plant shutdown was completed and the plant entered Mode 3, as required by LCO 3.0.3. The steam flow transmitters were restored to operable status by calculating new scaling data and rescaling the channels. LER 05000348/2016-007-02 is closed. | ||
====b. Findings==== | ====b. Findings==== | ||
A severity level IV violation was identified in inspection report 2017-009. See section 4OA2.1.c.1 of that report for details. | A severity level IV violation was identified in inspection report 2017-009. See section 4OA2.1.c.1 of that report for details. | ||
{{a|4OA5}} | {{a|4OA5}} | ||
Line 519: | Line 472: | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed the | The inspectors reviewed the licensees response to VIO 05000348/2016008-01, 05000364/2016008-01, EA-16-110 and determined that the reason, corrective actions taken and planned to address recurrence, and the date when full compliance was achieved for this violation is adequately addressed and captured on the docket. | ||
Documents reviewed are listed in the attachment. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. | ||
{{a|4OA6}} | |||
==4OA6 Meetings, Including Exit== | |||
On January 23, 2018, the resident inspectors presented the inspection results to Dennis Madison and other members of the licensees staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection period. | |||
{{a|4OA7}} | |||
==4OA7 Licensee-Identified Violations== | |||
The following violations of very low safety significance (Green) or Severity Level IV were identified by the licensee and are violations of NRC requirements which meet the criteria of the NRC Enforcement Policy, for being dispositioned as a non-cited violation. | |||
* 10 CFR 50.55 (a)(b)(5)(i) required in part that licensees must apply the most recent version of ASME BPV Code cases listed in Regulatory Guide 1.147, Revision 17. | |||
* 10 CFR 50.55 (a)(b)(5)(i) required in part that licensees must apply the most recent version of ASME BPV Code cases listed in Regulatory Guide 1.147, Revision 17. | |||
CR 10416364. | Contrary to the above, the licensee failed to perform augmented re-examinations on a 30-day periodicity as required by ASME Code Case N-513-3. A through-wall pinhole leak on the Unit 2 Train A Service Water strainer backwash piping was documented in condition report (CR) 10234480 on June 10, 2016. The service water system provides a heat sink for the removal of process and operating heat from safety related components during a Design Basis Accident (DBA) or transient. The backwash piping is safety-related ASME Section III, Class 3 piping. An Immediate Determination of Operability Evaluation (IDO) was performed declaring the strainer operable but degraded non-conforming (OBDN). The licensee followed the guidance of ASME Code Case N-513-3, Evaluation Criteria for Temporary Acceptance of Flaws in Moderate Energy Class 2 or 3 Piping, Section XI, Division 1. The code case requires that an additional five similar susceptible locations be identified and inspected to ensure that another flaw does not exist. In addition to the expanded scope, the code case requires that frequent periodic inspections of no more than 30-day intervals shall be used to determine if the flaws are growing to an unacceptable size. An additional CR (10236417) was initiated on June 15, 2016, to request work orders for inspection of these five locations. A total of three examinations were performed on a 30-day periodicity, the last being completed on August 22, 2016. CR 10416364 was initiated on October 5, 2017, documenting that no re-examinations on a 30-day periodicity were performed on the original leak location and the five additional locations since August 22, 2016. The ultrasonic examination was completed on October 5, 2017, and the degraded backwash piping was removed and replaced with new piping by WO SNC795917 on October 28, 2017. This finding was determined to be of very low safety significance (Green) because it was not a design or qualification deficiency, it did not represent a loss of system safety function of a single train for greater than its TS allowed outage time, and it did not screen as potentially risk significant due to seismic, flooding, or severe weather initiating events. This finding was entered into the licensees CAP as CR 10416364. | ||
ATTACHMENT: | ATTACHMENT: | ||
=SUPPLEMENTAL INFORMATION= | =SUPPLEMENTAL INFORMATION= | ||
Line 543: | Line 498: | ||
===Licensee Personnel=== | ===Licensee Personnel=== | ||
: | : | ||
: [[contact::K. Baity]], Site Design Manager | : [[contact::K. Baity]], Site Design Manager | ||
: [[contact::S. Briggs]], Plant Manager | : [[contact::S. Briggs]], Plant Manager | ||
: [[contact::J. Carroll]], Engineering Plant Support Manager | : [[contact::J. Carroll]], Engineering Plant Support Manager | ||
: [[contact::D. Erb]], Assistant Maintenance Director | : [[contact::D. Erb]], Assistant Maintenance Director | ||
: [[contact::B. Freeman]], Engineering Supervisor | : [[contact::B. Freeman]], Engineering Supervisor | ||
: [[contact::S. Harris]], Shift Operations Manager | : [[contact::S. Harris]], Shift Operations Manager | ||
: [[contact::J. Horn]], Operations Director | : [[contact::J. Horn]], Operations Director | ||
: [[contact::N. Koteel]], Operations | : [[contact::N. Koteel]], Operations | ||
: [[contact::D. Madison]], Site Vice President | : [[contact::D. Madison]], Site Vice President | ||
: [[contact::R. McAdams]], Engineering Director | : [[contact::R. McAdams]], Engineering Director | ||
: [[contact::J. Short]], Maintenance Director | : [[contact::J. Short]], Maintenance Director | ||
: [[contact::D. Simmons]], EP Supervisor | : [[contact::D. Simmons]], EP Supervisor | ||
: [[contact::G. Surber]], Licensing Supervisor | : [[contact::G. Surber]], Licensing Supervisor | ||
: [[contact::C. Welch]], Assistant Engineering Director | : [[contact::C. Welch]], Assistant Engineering Director | ||
: [[contact::R. Wells]], Site Projects Manager | : [[contact::R. Wells]], Site Projects Manager | ||
: [[contact::E. Williford]], Regulatory Affairs Manager | : [[contact::E. Williford]], Regulatory Affairs Manager | ||
: [[contact::D. Brown]], Site NDE Level III | : [[contact::D. Brown]], Site NDE Level III | ||
: [[contact::S. Champion]], Site ISI Coordinator | : [[contact::S. Champion]], Site ISI Coordinator | ||
: [[contact::K. King]], BACCP Owner | : [[contact::K. King]], BACCP Owner | ||
: [[contact::W. Truss]], Steam Generator Program Manager | : [[contact::W. Truss]], Steam Generator Program Manager | ||
==LIST OF REPORT ITEMS== | ==LIST OF REPORT ITEMS== | ||
Line 570: | Line 525: | ||
FIN | FIN | ||
: 05000364/2017004-01 Failure to Evaluate Impacts on the 2C RCP Oil Collection System (Section 1R05) | : 05000364/2017004-01 Failure to Evaluate Impacts on the 2C RCP Oil Collection System (Section 1R05) | ||
NCV | NCV | ||
: 05000364/2017004-02 Failure to maintain an operable Oil Collection System on RCP 2B (Section 1R20) | : 05000364/2017004-02 Failure to maintain an operable Oil Collection System on RCP 2B (Section 1R20) | ||
NCV | NCV | ||
: 05000348/2017004-03 Failure to Follow Procedure Resulted in Inoperable TDAFW pump (Section 4OA2.3) | : 05000348/2017004-03 Failure to Follow Procedure Resulted in Inoperable TDAFW pump (Section 4OA2.3) | ||
===Closed=== | ===Closed=== | ||
: 05000348/2016-007-02 Plant Shutdown Required by Technical Specifications due to Inoperable Steam Flow Transmitters (Section | LER | ||
: 05000348/2016-007-02 Plant Shutdown Required by Technical Specifications due to Inoperable Steam Flow Transmitters (Section 4OA3.1) | |||
: 05000348/2016008-01 | VIO | ||
: 05000348/2016008-01 Inaccurate Training Records (Section 4OA5.2) | |||
: 05000364/2016008-01 | VIO | ||
: 05000364/2016008-01 | |||
==LIST OF DOCUMENTS REVIEWED== | ==LIST OF DOCUMENTS REVIEWED== | ||
}} | }} |
Latest revision as of 02:25, 19 December 2019
ML18043A031 | |
Person / Time | |
---|---|
Site: | Farley |
Issue date: | 02/12/2018 |
From: | Alan Blamey NRC/RGN-II/DRP/RPB2 |
To: | Madison D Southern Nuclear Operating Co |
References | |
IR 2017004 | |
Download: ML18043A031 (40) | |
Text
UNITED STATES NUCLEAR REGULATORY COMMISSION ary 12, 2018
SUBJECT:
JOSEPH M. FARLEY NUCLEAR PLANT - NUCLEAR REGULATORY COMMISSION INTEGRATED INSPECTION REPORT 05000348/2017004 AND 05000364/2017004
Dear Mr. Madison:
On December 31, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Joseph M. Farley Nuclear Plant, Units 1 and 2. On January 23, 2017, NRC inspectors discussed the results of this inspection with you and other members of your staff.
The results of this inspection are documented in the enclosed report.
NRC inspectors documented three findings of very low safety significance (Green) in this report. Two findings involved violations of NRC requirements. In addition, the inspectors documented a licensee-identified violation which was determined to be of very low safety significance in this report. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.
If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S.
Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC resident inspector at the Joseph M. Farley Nuclear Plant, Units 1 and 2.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement; and the NRC resident inspector at the Joseph M. Farley Nuclear Plant, Units 1 and 2. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Alan Blamey, Chief Reactor Projects Branch 2 Division of Reactor Projects Docket Nos.: 50-348, 50-364 License Nos.: NPF-2, NPF-8
Enclosure:
IR 05000348/2017004, 05000364/2017004 w/Attachment: Supplemental Information
REGION II==
Docket Nos.: 50-348, 50-364 License Nos.: NPF-2, NPF-8 Report No.: 05000348/2017004; and 05000364/2017004 Licensee: Southern Nuclear Operating Company, Inc.
Facility: Joseph M. Farley Nuclear Plant Location: Columbia, Alabama Dates: October 1, 2017 through December 31, 2017 Inspectors: P. Niebaum, Senior Resident Inspector K. Miller, Resident Inspector B. Collins, Reactor Inspector (1R08)
W. Pursley, Health Physics Inspector (2RS1)
B. Caballero, Senior Operations Engineer (1R11)
Approved by: Alan Blamey, Chief Reactor Projects Branch 2 Division of Reactor Projects Enclosure
SUMMARY
IR 05000348/2017004; and 05000364/2017004, October 1, 2017, through December 31, 2017;
Joseph M. Farley Nuclear Plant, Units 1 and 2, Fire Protection, Refueling and Other Outage Activities, Problem Identification and Resolution.
The report covered a 3-month period of inspection by resident inspectors and regional inspectors. There are two NRC-identified and one self-revealing violations documented in this report. The significance of inspection findings are indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC)0609, Significance Determination Process (SDP) dated April 29, 2015. If a cross-cutting area was assigned include the following: The cross-cutting aspects are determined using IMC 0310,
Aspects within the Cross-Cutting Areas dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy dated November 1, 2016. The NRCs program for overseeing the safe operations of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 6.
Documents reviewed by the inspectors which are not identified in the Report Details are identified in the Attachment.
Cornerstone: Mitigating Systems
- Green.
A self-revealing finding was identified for the licensees failure to evaluate the impacts to the Unit 2 Reactor Coolant Pump (RCP) 2C oil collection system when a service water (SW) leak was identified on the Unit 2 RCP motor air coolers. As a result, a strategy was not implemented to prevent service water from collecting in the 2C RCP oil collection system drain tank which impacted its design function while the plant was in Mode 1. The licensees failure to evaluate the potential impacts to the Unit 2 RCP 2C oil collection system during the operability/functionality evaluation of the SW leak associated with RCP motor air coolers was a performance deficiency. The licensee initiated condition reports (CRs) 10420400 and 10422562 and replaced the 2C RCP motor and leaking air cooler.
The finding was more than minor because it was associated with the protection against external factors (fires) and adversely affected the mitigating systems cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, failure to maintain adequate capacity in the RCP 2C Oil Spillage Protection System (OSPS) oil collection tank presented a degradation of a fire confinement component which has a fire prevention function of not allowing an oil leak to reach hot surfaces. The significance of this finding was evaluated using IMC 0609, Appendix F, "Fire Protection Significance Determination Process, dated September 20, 2013, because the performance deficiency affected fire protection defense-in-depth strategies involving fire confinement.
Using IMC 0609, Appendix F, Attachment 1, Fire Protection Significance Determination Process Worksheet, the inspectors determined that the finding was of very low safety significance (Green) because the exposed fire area contained no potential damage targets that are unique from those in the exposing fire area. The inspectors determined the finding had a cross-cutting aspect of Evaluation in the problem identification and resolution area because the licensee did not fully evaluate the impacts of the RCP motor air cooler SW leak on the Unit 2 RCP oil collection systems. [P.2] (Section 1R05)
- Green.
An NRC-identified NCV of 10 CFR 50.48(c) and National Fire Protection Association Standard 805 (NFPA 805), Section 3.3.12, was identified for the licensees failure to maintain the Unit 2 RCP 2B oil collection system in an operable condition to perform its design function. Specifically, the licensee failed to ensure that the RCP 2B OSPS oil lift system enclosure collected all oil leakage from all potential leakage sites, including the oil lift system. The licensees failure to maintain the Unit 2 RCP 2B oil collection system in an operable condition to perform its design function was a performance deficiency. The licensee initiated CR 10428611, and determined an oil leak was not active. Another CR was initiated (10446206) to inspect and, if needed, repair this area at the next available opportunity.
The finding was more than minor because if left uncorrected, the performance deficiency would have the potential to become a more significant safety concern. Specifically, failing to ensure that the RCP 2B Oil Spillage Protection System oil lift system enclosure collected all oil leakage from all potential leakage sites, including the oil lift system, presented a degradation of a fire confinement component which has a fire prevention function of not allowing an oil leak to reach hot surfaces. The significance of this finding was evaluated using IMC 0609, Appendix F, "Fire Protection Significance Determination Process, dated September 20, 2013, because the performance deficiency affected fire protection defense-in-depth strategies involving fire confinement. Using IMC 0609,
Appendix F, Attachment 1, Fire Protection Significance Determination Process Worksheet, the inspectors determined that the finding was of very low safety significance (Green) because the exposed fire area contains no potential damage targets that are unique from those in the exposing fire area. The inspectors determined the finding had a cross-cutting aspect of Design Margins in the human performance area because the licensee did not maintain fire protection defense-in-depth by ensuring the Unit 2 RCP 2B oil collection system was in an operable condition to perform its design function. (H.6) (Section 1R20)
- Green.
A self-revealing NCV of Technical Specification (TS) 5.4.1.a, Procedures, was identified when the Unit 1 Turbine Driven Auxiliary Feedwater (TDAFW) uninterruptible power supplies (UPS) swapped to a bypass power source during maintenance on November 5, 2017. As a result, the TDAFW pump was rendered inoperable. Failure to follow licensee procedure FNP-1-EMP-1352.01, TDAFW UPS Battery Weekly Battery Inspection, Version 19, as written was a performance deficiency. The operability of the TDAFW pump UPS was restored after approximately 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />. The licensee entered this issue into their Corrective Action Program (CAP) as Condition Report (CR) 10427370.
The finding was more than minor because it was associated with the equipment performance attribute of the mitigating system cornerstone and adversely affected that cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences since the TDAFW pump was rendered inoperable. The significance of this finding was evaluated using IMC 0609, Appendix A, The Significance Determination Process (SDP) for findings at Power, dated June 19, 2012. This finding was determined to be of very low safety significance (Green) because all of the mitigating systems screening questions were answered NO. The inspectors determined the finding had a cross-cutting aspect of Avoid Complacency in the Human Performance area because the individuals involved in this maintenance did not recognize or plan for the possibility of mistakes and appropriate error reduction tools were not implemented. [H.12] (Section 4OA2.3)
Violations of very low safety significance that were identified by the licensee have been reviewed by the NRC. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. These violations and corrective action tracking numbers are listed in Section 4OA7 of this report.
REPORT DETAILS
Summary of Plant Status
Unit 1: Unit 1 started the report period at approximately 100 percent rated thermal power (RTP). Unit 1 maintained approximately 100 percent RTP through the end of the report period.
Unit 2: Unit 2 started the report period at approx. 100 percent RTP. On October 15, 2017, Unit 2 shutdown for a refueling outage. Following completion of the outage on November 15, 2017, Unit 2 achieved 100 percent RTP on November 19, 2017. Unit 2 maintained approximately 100 percent RTP through the end of the report period.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection
a. Inspection Scope
Impending Adverse Weather Conditions: The inspectors reviewed the licensees preparations to protect risk-significant systems from adverse weather conditions (Tropical Storm/Hurricane Nate) expected on site October 7 and 8, 2017. The inspectors evaluated the licensees implementation of adverse weather preparation procedures and compensatory measures, including operator staffing, before the onset of the adverse weather conditions. The inspectors verified that operator actions specified in the licensees adverse weather procedure maintain readiness of essential systems.
The inspectors also verified that the licensee implemented periodic equipment walkdowns or other measures to ensure that the condition of plant equipment met operability requirements.
b. Findings
No findings were identified.
1R04 Equipment Alignment
a. Inspection Scope
Partial Walkdown: The inspectors verified that critical portions of the following systems were correctly aligned by performing partial walkdowns. The inspectors determined the correct system lineup by reviewing plant procedures and drawings listed in the
.
- Unit 2, 2B emergency diesel generator (EDG)
- Unit 2, 2B penetration room filtration system The inspectors reviewed corrective action documents, including condition reports and outstanding work orders, to verify the licensee was identifying and resolving equipment alignment discrepancies. The inspectors also reviewed periodic reports containing information on the status of risk-significant systems, including maintenance rule reports and system health reports.
b. Findings
No findings were identified.
1R05 Fire Protection
a. Inspection Scope
Quarterly Inspection: The inspectors evaluated the adequacy of fire plans by comparing the fire plans to the defined hazards and defense-in-depth features specified in the fire protection program for the following fire areas.
- Unit 2, Room 2-055 - Containment Building, Fire Area 2-055, Fire Zone 2-CTMT
- Unit 1 and 2, Room 401, Common Main Control Room, Room, Fire Area 044, Fire Zones 0401-U1 & 0401-U2 The inspectors assessed the following:
- control of transient combustibles and ignition sources
- fire detection systems
- water-based fire suppression systems
- gaseous fire suppression systems
- manual firefighting equipment and capability
- passive fire protection features
- compensatory measures and fire watches
- issues related to fire protection contained in the licensees corrective action program
- material condition and operational status of fire protection equipment
b. Findings
Introduction:
A Green Self-Revealing finding was identified for the licensees failure to evaluate the impacts to the Unit 2 Reactor Coolant Pump (RCP) 2C oil collection system when a service water (SW) leak was identified on the Unit 2 RCP motor air coolers. As a result, a strategy was not implemented to prevent service water from collecting in the 2C RCP oil collection system drain tank which impacted its design function while the plant was in Mode 1. The licensees failure to evaluate the potential impacts to the Unit 2 RCP 2C oil collection system during the operability/functionality evaluation of the SW leak associated with RCP motor air coolers, was a performance deficiency.
Description:
On October 17, 2017, the inspectors performed a Unit 2 containment building inspection while the plant was in Mode 5. The inspectors noted that one of the RCP 2C motor air cooling coils had been leaking service water and some of that water was dripping from inside the motor housing into the oil catch-basin below the lower motor bearing oil reservoir. The licensee had previously noted an increasing rate of Unit 2 containment sump in-leakage, beginning on September 21, 2017, and operating personnel made a containment entry on September 27 to look for possible leak sources in low-dose accessible areas, concluding that an RCP motor air cooling coil was likely leaking service water. By October 9, 2017, the Unit 2 containment sump in-leakage rate was approximately 0.75 gpm. Plant operators evaluated the operational impact on October 10, 2017, associated with CR 10411954, but the evaluation did not consider the possible impact on the oil spillage protection system (OSPS) functionality. A 300-gallon capacity OSPS oil collection tank is provided on the 105-6 elevation of the containment for each RCP and each RCP motor contains 265 gallons of lubricating oil. Each tank is provided with an open vent of 2-inch schedule 40 piping at the top of the tank. Following the containment inspection on October 17, 2017, the licensee drained the contents of each oil collection tank and found approximately 137 gallons of water in the 2C RCP oil collection drain tank. With this amount of water in the tank, there would not be sufficient capacity in the tank to contain the full inventory of the RCP 2C motor lubricating system.
The tank would only be able to accept approximately 163 gallons of oil, leaving up to 102 gallons of oil that would spill out onto the reactor containment building floor. Licensee procedure NMP-AD-012, Operability Determinations and Functionality Assessments, Ver. 13.1, section 4.2.3 required (in part) the licensee to evaluate the effects on other components if the condition could affect other components. Contrary to those requirements, the licensee failed to consider the impacts on the U2 RCPs oil collection system, during the operability/functionality evaluation of the RCP air motor SW leak.
The licensee initiated CRs 10420400 and 10422562 and replaced the 2C RCP motor and leaking air cooler.
Analysis:
The licensees failure to evaluate the potential impacts to the Unit 2 RCP 2C oil collection system during the operability/functionality evaluation of the SW leak associated with RCP motor air coolers was a performance deficiency. The finding was more than minor because it was associated with the protection against external factors (fires) and adversely affected the mitigating systems cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, failure to maintain adequate capacity in the RCP 2C OSPS oil collection tank presented a degradation of a fire confinement component which has a fire prevention function of not allowing an oil leak to reach hot surfaces. The significance of this finding was evaluated using IMC 0609, Appendix F, "Fire Protection Significance Determination Process, dated September 20, 2013, because the performance deficiency affected fire protection defense-in-depth strategies involving fire confinement. Using IMC 0609, Appendix F, Attachment 1, Fire Protection Significance Determination Process Worksheet, the inspectors determined that the finding was of very low safety significance (Green) because the exposed fire area contains no potential damage targets that are unique from those in the exposing fire area. The inspectors determined the finding had a cross-cutting aspect of Evaluation in the problem identification and resolution area because the licensee did not fully evaluate the impacts of the RCP motor air cooler SW leak on the Unit 2 RCP oil collection systems. [P.2]
Enforcement:
The inspectors did not identify a violation of regulatory requirements associated with this finding. FIN 05000364/2017004-01, Failure to evaluate impacts on the 2C RCP oil collection system.
1R08 Inservice Inspection Activities
a. Inspection Scope
Non-Destructive Examination Activities and Welding Activities From October 23 - October 27, 2017, the inspectors conducted an onsite review of the implementation of the licensees inservice inspection (ISI) program for Unit 2. The ISI program is designed to monitor degradation of pressure retaining components in vital system boundaries. The scope of this program includes components within the reactor coolant system boundary, risk-significant piping boundaries, and containment system boundaries.
The inspectors either directly observed or reviewed the following non-destructive examination (NDE) activities. These activities were mandated by the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (Code of Record:
2001 Edition with 2003 Addenda). The inspectors evaluated the NDE activities for compliance with the requirements in Section XI and Section V of the ASME Code. The inspectors also evaluated if any identified indications or defects were dispositioned in accordance with either the ASME Code or an NRC-approved alternative requirement.
Additionally, the inspectors reviewed the qualifications of the NDE technicians performing the examinations to determine if they were in compliance with ASME Code requirements.
- Ultrasonic Examination (UT) of APR1-4302-12-RB and -13-RB, 12 OD, ASME Class 1, Safety Injection system pipe-to-elbow and elbow-to-pipe welds (observed)
- Liquid Penetrant Testing (PT) of Q2-P16-HCB-9, 6 OD, ASME Class 2, Service Water system valve-to-pipe weld (reviewed)
- PT of Q2-P16-HCB-9, 6 OD, ASME Class 2, Service Water system valve-to-pipe weld (repair weld) (reviewed)
The inspectors either directly observed or reviewed the following welding activities. The inspectors evaluated these activities for compliance with site procedures and the requirements in Section IX and Section XI of the ASME Code. Specifically, the inspectors reviewed the work orders, repair or replacement plans, weld data sheets, welding procedures, procedure qualification records, welder performance qualification records, and NDE reports.
- WO SNC 849902, Replacement of 6 Service Water valve Q2P16V072, ASME Class 2 (reviewed)
PWR Vessel Upper Head Penetration Inspection Activities The inspectors verified that the licensee did not identify any indications that were accepted for continued service. Additionally, the inspectors verified that the licensee did not perform any welding repairs to the upper head penetrations since the last Unit 2 refueling outage.
Boric Acid Corrosion Control Inspection Activities The inspectors reviewed the licensees boric acid corrosion control program (BACCP)activities to determine if they were implemented in accordance with program requirements, applicable regulatory requirements, and industry guidance. Specifically, the inspectors performed the following activities:
- Reviewed applicable procedures and the results of the licensees most recent containment walkdown inspection.
- Interviewed the BACCP owner.
- Conducted an independent walkdown of accessible areas of the Unit 2 reactor building containment pipe chase.
- Verified that degraded or nonconforming conditions, such as boric acid leaks, were properly identified and corrected in accordance with the licensees BACCP and the CAP.
- Reviewed engineering evaluations of components with boric acid leakage which verified that minimum wall thickness of those components was maintained.
Steam Generator Tube Inspection Activities The inspectors reviewed the Unit 2 steam generator maintenance program. The inspectors verified that no steam generator tube inspection activities were required this refueling outage. This inspection schedule was verified with the requirements of the ASME Code, the licensees Technical Specifications, and applicable industry guidance.
Identification and Resolution of Problems The inspectors reviewed a sample of ISI-related issues entered into the corrective action program. The inspectors evaluated if the licensee had appropriately described the scope of the problem and had initiated corrective actions. The review also included the licensees consideration and assessment of operating experience events applicable to the plant.
b. Findings
No findings were identified.
1R11 Licensed Operator Requalification Program and Licensed Operator Performance
a. Inspection Scope
Resident Inspector Quarterly Review of Licensed Operator Requalification:
The inspectors observed simulator scenarios conducted for training of an operating crew for requalification on November 21, 2017 and December 13, 2017.
The inspectors assessed the following:
- licensed operator performance
- the ability of the licensee to administer the scenario and evaluate the operators
- the quality of the post-scenario critique
- simulator performance Resident Inspector Quarterly Review of Licensed Operator Performance The inspectors observed licensed operator performance in the main control room for the following evolutions:
- Unit 2 power ascension to 100% during a Southern Company System Alert on October 10, 2017
- Unit 2 transition to Mode 1 and subsequent power ascension following a refueling outage from November 13 to November 16, 2017 The inspectors assessed the following:
- use of plant procedures
- control board manipulations
- communications between crew members
- use and interpretation of instruments, indications, and alarms
- use of human error prevention techniques
- documentation of activities
- management and supervision oversight Annual Review of Licensee Requalification Examination Results:
On June 29, 2017, the licensee completed the annual requalification operating examinations required to be administered to all licensed operators in accordance with Title 10 of the Code of Federal Regulations 55.59(a)(2), Requalification Requirements, of the NRCs Operators Licenses. The inspectors performed an in-office review of the overall pass/fail results of the individual operating examinations and the crew simulator operating examinations in accordance with Inspection Procedure (IP) 71111.11, Licensed Operator Requalification Program. These results were compared to the thresholds established in Section 3.02, Requalification Examination Results, of IP 71111.11.
b. Findings
No findings were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
The inspectors assessed the licensees treatment of the issues listed below to verify the licensee appropriately addressed equipment problems within the scope of the maintenance rule (10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants). The inspectors reviewed procedures and records to evaluate the licensees identification, assessment, and characterization of the problems as well as their corrective actions for returning the equipment to a satisfactory condition. The inspectors also interviewed system engineers and the maintenance rule coordinator to assess the accuracy of any performance deficiencies and extent of condition.
- Quality Control - Unit 2, repair of load sequencer Q2R43E0001B - replacement of electrical DG1 diode with new commercially dedicated item
- Unit 2 train A service water strainer degraded backwash piping reviewed under structural monitoring program for the maintenance rule
b. Findings
A licensee-identified violation was identified. See section 4OA7 for details.
1R13 Maintenance Risk Assessments and Emergent Work Control
a. Inspection Scope
The inspectors reviewed the maintenance activities listed below to verify that the licensee assessed and managed plant risk as required by 10 CFR 50.65(a)(4) and licensee procedures. The inspectors assessed the adequacy of the licensees risk assessments and implementation of risk management actions. The inspectors also verified that the licensee was identifying and resolving problems with assessing, and managing maintenance-related risk using CAP. Additionally, for maintenance resulting from unforeseen situations, the inspectors assessed the effectiveness of the licensees planning and control of emergent work activities.
- Unit 2, October 18, 2017 - U2 shutdown safety assessment with reduced inventory in the reactor vessel
- Unit 1, October 22, 2017 - Insulator replacement in low voltage switchyard
- Unit 2, November 6, 2017 - 1C diesel generator outage and power range nuclear instruments trip setpoint adjustments
b. Findings
No findings were identified.
1R15 Operability Determinations and Functionality Assessments
a. Inspection Scope
Operability Determinations and Functionality Assessments Review:
The inspectors selected the operability determinations or functionality evaluations listed below for review based on the risk-significance of the associated components and systems. The inspectors reviewed the technical adequacy of the determinations to ensure that technical specification operability was properly justified and the components or systems remained capable of performing their design functions. To verify whether components or systems were operable, the inspectors compared the operability and design criteria in the appropriate sections of the technical specification and updated final safety analysis report to the licensees evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with operability evaluations.
- CR10415220, component cooling water (CCW) heat exchangers tube leakage
- Work Order (WO) SNC841458, Unit 1 turbine driven auxiliary feedwater pump and turbine oil samples
- CR10424737, Loss of Unit 2 B-Train Service Water during performance of FNP-2-STP-40.0B
- CR10429121, Q2N12HV3235A, Steam leak past valve pressure seal
- CR10441286, 1A reactor coolant pump degraded #2 seal
b. Findings
No findings were identified.
1R18 Plant Modifications
a. Inspection Scope
For the following plant modifications listed below, the inspectors;
- verified that the modifications did not affect the safety functions of important safety systems.
- confirmed the modifications did not degrade the design bases, licensing bases, and performance capability of risk significant structures, systems and components.
- verified modifications performed during plant configurations involving increased risk did not place the plant in an unsafe condition.
- evaluated whether system operability and availability, configuration control, post-installation test activities, and changes to documents, such as drawings, procedures, and operator training materials, complied with licensee standards and NRC requirements.
- reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with modifications.
Plant Modification:
- Limited design change package (LDCP) SNC728696, Unit 2 service water to reactor coolant pump motor operated valve Q2P16MOV3131 replacement
b. Findings
No findings were identified.
1R19 Post-Maintenance Testing
a. Inspection Scope
The inspectors either observed post-maintenance testing, or reviewed the test results for the maintenance activities listed below to verify the work performed was completed correctly, and the test activities were adequate to verify system operability and functional capability.
- WO SNC904009, repair of load sequencer Q2R43E0001B
- WO SNC391170, diagnostic test of Q2B31PCV445A
- WO SNC376715, packing leak on Unit 2 TDAFW governor valve The inspectors evaluated these activities for the following:
- Acceptance criteria were clear and demonstrated operational readiness.
- Effects of testing on the plant were adequately addressed.
- Test instrumentation was appropriate.
- Tests were performed in accordance with approved procedures.
- Equipment was returned to its operational status following testing.
- Test documentation was properly evaluated.
Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with post-maintenance testing.
b. Findings
No findings were identified.
1R20 Refueling and Other Outage Activities
a. Inspection Scope
For the Unit 1 refueling outage from October 15, 2017, through November 15, 2017, the inspectors evaluated the following outage activities:
- outage planning
- fatigue management
- shutdown, cooldown, refueling, heatup, and startup
- reactor coolant system instrumentation and electrical power configuration
- reactivity and inventory control
- decay heat removal and spent fuel pool cooling system operation
- containment closure The inspectors verified that the licensee:
- considered risk in developing the outage schedule
- controlled plant configuration in accordance with administrative risk reduction methodologies
- developed work schedules to manage fatigue
- developed mitigation strategies for loss of key safety functions
- adhered to operating license and technical specification requirements Inspectors verified that safety-related and risk-significant structures, systems, and components not accessible during power operations were maintained in an operable condition. The inspectors also reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with outage activities.
b. Findings
Introduction:
A Green NRC-identified NCV of 10 CFR 50.48(c) and National Fire Protection Association Standard 805 (NFPA 805), Section 3.3.12, was identified for the licensees failure to maintain the Unit 2 Reactor Coolant Pump (RCP) 2B oil collection system in an operable condition to perform its design function. Specifically, the licensee failed to ensure that the RCP 2B Oil Spillage Protection System (OSPS) oil lift system enclosure collected all oil leakage from all potential leakage sites, including the oil lift system. The licensees failure to maintain the Unit 2 RCP 2B oil collection system in an operable condition to perform its design function was a performance deficiency.
Description:
On November 8, 2017, while the plant was in Mode 5, the inspectors performed a Unit 2 containment building closeout inspection. The inspectors observed RCP oil leaking out of the bottom of the oil lift system support plate through mounting bolt holes for the 2B RCP. Oil was dripping off the threaded fasteners penetrating the lift system horizontal mounting plate onto the motor air cooling coil, then from the coil onto an electrical box. The RCP 2B lift system had apparently been leaking oil while the associated lift pump was in operation. The lift oil system operates at a pressure in excess of 550 psig. The lift pump is not required to operate once the RCP has started, but the lift pump is restarted when the RCP is stopped. The control room log noted the oil lift pump was operated for twelve minutes on November 3, and again on November 4, 2017, for ten minutes while starting RCP 2B at 0405. The inspectors asked the licensee to determine why the oil was leaking out of the oil lift system enclosure. The licensee initiated CR 10428611, and determined an oil leak was not active. Another CR was initiated (10446206) to inspect and, if needed, repair this area at the next available opportunity.
Analysis:
The licensees failure to maintain the Unit 2 RCP 2B oil collection system in an operable condition to perform its design function was a performance deficiency. The finding was more than minor because if left uncorrected, the performance deficiency would have the potential to become a more significant safety concern. Specifically, failing to ensure that the RCP 2B Oil Spillage Protection System (OSPS) oil lift system enclosure collected all oil leakage from all potential leakage sites, including the oil lift system, presented a degradation of a fire confinement component which has a fire prevention function of not allowing an oil leak to reach hot surfaces. The significance of this finding was evaluated using IMC 0609, Appendix F, "Fire Protection Significance Determination Process, dated September 20, 2013, because the performance deficiency affected fire protection defense-in-depth strategies involving fire confinement.
Using IMC 0609, Appendix F, Attachment 1, Fire Protection Significance Determination Process Worksheet, the inspectors determined that the finding was of very low safety significance (Green) because the exposed fire area contained no potential damage targets that are unique from those in the exposing fire area. The inspectors determined the finding had a cross-cutting aspect of Design Margins in the human performance area because the licensee did not maintain fire protection defense-in-depth by ensuring the Unit 2 RCP 2B oil collection system was in an operable condition to perform its design function. (H.6)
Enforcement:
Farley Nuclear Plant, Unit 2, Operating License Condition 2.C.(6),required, in part, that the licensee shall implement and maintain in effect all provisions of the approved fire protection program (FPP) that comply with 10 CFR 50.48(c), as specified in the license amendment requests dated September 25, 2012; April 25, 2016; and supplements dated December 20, 2012; September 16, 2013; October 30, 2013; November 12, 2013; April 23, 2014; May 23, 2014; July 3, 2014; August 11, 2014; August 29, 2014; October 13, 2014; January 16, 2015; and as approved in the safety evaluation reports (SER) dated March 10, 2015 and October 17, 2016. The 2001 Edition of NFPA-805, Section 3.3.12, Reactor Coolant Pumps, required that the oil collection system shall be designed and installed such that leakage from the oil system is safely contained for off normal conditions such as accident conditions or earthquakes.
Leakage points on a reactor coolant pump motor to be protected shall include, but not be limited to the lift pump and piping, overflow lines, oil cooler, oil fill and drain lines and plugs, flanged connections on oil lines, and the oil reservoirs, where such features exist on the reactor coolant pumps. The leakage shall be collected and drained to a vented closed container that can hold the inventory of the reactor coolant pump lubricating oil system. Contrary to the above, the licensee failed to comply with the NFPA 805 code requirements for the Unit 2 RCP oil collection system. Code requirements for oil collection systems for reactor coolant pumps specify the leakage shall be collected and drained to a vented closed container that can hold the inventory of the reactor coolant pump lubricating oil system. The OSPS cannot be relied upon to meet these requirements if it is not maintained in an operable condition to perform its design function. Because the licensee included this deficiency in their corrective action program as CR 10428611 and because the deficiency had low safety significance, this finding will be treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy and is identified as NCV 05000364/2017004-02, Failure to maintain an operable Oil Collection System on RCP 2B.
1R22 Surveillance Testing
a. Inspection Scope
The inspectors reviewed the surveillance tests listed below. The surveillance test was either observed directly or test results were reviewed to verify testing activities and results provide objective evidence that the affected equipment remain capable of performing their intended safety functions and maintain their operational readiness consistent with the facilitys current licensing basis. The inspectors evaluated the test activities to assess for:
- preconditioning of equipment,
- appropriate acceptance criteria,
- calibration and appropriateness of measuring and test equipment,
- procedure adherence, and
- equipment alignment following completion of the surveillance.
Additionally, the inspectors reviewed a sample of significant surveillance testing problems documented in the licensees corrective action program to verify the licensee was identifying and correcting any testing problems associated with surveillance testing.
Routine Surveillance Tests
- FNP-2-STP-608.0, Main Steam Safety Valve Operational Test, Ver. 41 for valve Q2N11V011A
- FNP-2-STP-101, Low Power Reactor Physics Testing, Ver. 29
- FNP-2-STP-22.27, 2B Auxiliary Feedwater Pump Cold Shutdown Inservice Test &
Preservice Test, Ver. 27.0 In-Service Tests (IST)
- FNP-1-STP-23.8, Component Cooling Water Valve Inservice Test, Ver. 51.0 Containment Isolation Valve
- FNP-2-STP-627.0, Local Leak Rate Testing of Containment Penetrations, Ver. 60
b. Findings
No findings were identified.
Cornerstone: Emergency Preparedness
1EP6 Drill Evaluation
a. Inspection Scope
The inspectors observed the emergency preparedness training drill conducted on December 14, 2017. The inspectors observed licensee activities in the simulator and/or technical support center to evaluate implementation of the emergency plan, including event classification, notification, dose assessment, and protective action recommendations. The inspectors evaluated the licensees performance against criteria established in the licensees procedures. Additionally, the inspectors attended the post-exercise critique to assess the licensees effectiveness in identifying emergency preparedness weaknesses and verified the identified weaknesses were entered in the corrective action program.
b. Findings
No findings were identified.
RADIATION SAFETY
(RS)
2RS1 Radiological Hazard Assessment and Exposure Controls (Seven Inspection Samples
Completed)
a. Inspection Scope
Hazard Assessment and Instructions to Workers. During facility tours, the inspectors directly observed radiological postings and container labeling for areas established within the radiologically controlled area (RCA) of the Unit 2 (U2) containment building, Unit 1 (U1) and U2 auxiliary building and radioactive waste processing and storage locations. The inspectors independently measured radiation dose rates or directly observed conduct of licensee radiation surveys for selected RCA areas. The inspectors reviewed survey records for several plant areas including surveys for airborne radioactivity, gamma surveys with a range of dose rate gradients, surveys for alpha-emitters and other hard-to-detect radionuclides, and pre-job surveys for upcoming tasks.
The inspectors also discussed changes to plant operations that could contribute to changing radiological conditions since the last inspection. The inspectors attended pre-job briefings and reviewed Radiation Work Permit (RWP) details to assess communication of radiological control requirements and current radiological conditions to workers.
Control of Radioactive Material. The inspectors observed surveys of material and personnel being released from the RCA using small article monitor, personnel contamination monitor, and portal monitor instruments. The inspectors discussed equipment sensitivity, alarm setpoints, and release program guidance with licensee staff.
The inspectors also reviewed records of leak tests on selected sealed sources and discussed nationally tracked source transactions with licensee staff.
Hazard Control. The inspectors evaluated access controls and barrier effectiveness for selected High Radiation Area (HRA), Locked High Radiation Area (LHRA), and Very High Radiation Area (VHRA) locations and discussed changes to procedural guidance for LHRA and VHRA controls with Radiation Protection (RP) supervisors. The inspectors reviewed implementation of controls for the storage of irradiated material within the spent fuel pool. Established radiological controls, including airborne controls and electronic dosimeter (ED) alarm setpoints, were evaluated for selected U2 Refueling Outage 25 (U2R25) job tasks. In addition, the inspectors reviewed licensee controls for areas where dose rates could change significantly as a result of plant shutdown and refueling operations. The inspectors also reviewed the use of personnel dosimetry including extremity dosimetry and multibadging in high dose rate gradients.
Radiation Worker Performance and RP Technician Proficiency. Occupational workers adherence to selected RWPs and RP technician proficiency in providing job coverage in radiologically significant areas were evaluated through direct observations and interviews with licensee staff. Jobs observed included maintenance work in the reactor cavity including transfer tube removal, seal filter pump room valve cutouts and RVLIS detector removal. The inspectors also evaluated worker responses to dose and dose rate alarms during selected work activities.
Problem Identification and Resolution. The inspectors reviewed and assessed condition reports (CR) associated with radiological hazard assessment and control. The inspectors evaluated the licensees ability to identify and resolve the issues in accordance with licensee procedures. The inspectors also reviewed recent self-assessment results.
Inspection Criteria. RP activities were evaluated against the requirements of Updated Final Safety Analysis Report (UFSAR) Section 12, Technical Specifications (TS)
Sections 5.4 and 5.7, 10 CFR Parts 19 and 20, and approved licensee procedures.
Licensee programs for monitoring materials and personnel released from the RCA were evaluated against 10 CFR Part 20 and IE Circular 81-07, Control of Radioactively Contaminated Material. Documents and records reviewed are listed in the Attachment.
b. Findings
No findings were identified.
OTHER ACTIVITIES
4OA1 Performance Indicator Verification
a. Inspection Scope
The inspectors reviewed a sample of the performance indicator (PI) data, submitted by the licensee, for the Unit 1 and Unit 2 PIs listed below. The inspectors reviewed plant records compiled between November 2016, and October 2017, to verify the accuracy and completeness of the data reported for the station. The inspectors verified that the PI data complied with guidance contained in Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, and licensee procedures. The inspectors verified the accuracy of reported data that were used to calculate the value of each PI.
In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with PI data.
Cornerstone: Mitigating Systems
- high pressure injection system (Units 1 and 2)
- emergency AC power system (Units 1 and 2)
- heat removal system (Units 1 and 2)
b. Findings
No findings were identified.
4OA2 Problem Identification and Resolution
.1 Routine Review
The inspectors screened items entered into the licensees CAP in order to identify repetitive equipment failures or specific human performance issues for followup. The inspectors reviewed condition reports, attended screening meetings, or accessed the licensees computerized corrective action database.
b. Findings and Observations
No findings were identified.
.2 Semi-Annual Trend Review
a. Inspection Scope
The inspectors performed a review of issues entered in the licensees CAP and reviewed associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors focused their review on missed surveillance testing, but also considered the results of inspector daily condition report screenings, licensee trending efforts, and licensee human performance results. The review nominally considered the six-month period beginning in July 2017, through December 2017, although some examples extended beyond those dates when the scope of the trend warranted. The inspectors compared their results with the licensees analysis of trends. Additionally, the inspectors reviewed the adequacy of corrective actions associated with a sample of the issues identified in the licensees trend reports.
The inspectors also reviewed corrective action documents that were processed by the licensee to identify potential adverse trends in the condition of structures, systems, and/or components as evidenced by acceptance of long-standing nonconforming or degraded conditions.
The inspectors performed a search of the CAP database and found 22 examples of condition reports initiated since the beginning of 2017 associated with missed surveillance testing. The licensee identified a cognitive trend in missed surveillance testing and initiated a trend CR (10401365) on August 23, 2017, citing four CRs as examples and noted that the trend had continued over the previous 41 days. Since that time there were at least an additional seven CRs initiated for issues associated with missed surveillance testing. The licensee nuclear oversite organization also initiated CR 10393974 on August 2, 2017, addressing inadequate engagement in the surveillance program. The licensee initiated Corrective Action Report (CAR) 270723, completing the disposition on December 15, 2017, in an effort to resolve the negative trend, but it is not apparent the licensees corrective actions were effective since the negative trend continues. The inspectors continue to monitor this issue.
b. Findings and Observations
No findings were identified.
.3 Annual Followup of Selected Issues
a. Inspection Scope
The inspectors conducted a detailed review of the following condition report:
- CR10427370, Unit 1 TDAFW inoperability The inspectors evaluated the following attributes of the licensees actions:
- complete and accurate identification of the problem in a timely manner
- evaluation and disposition of operability and reportability issues
- consideration of extent of condition, generic implications, common cause, and previous occurrences
- classification and prioritization of the problem
- identification of root and contributing causes of the problem
- identification of any additional condition reports
- completion of corrective actions in a timely manner
b. Findings
Introduction:
A Green self-revealing non-cited violation (NCV) of Technical Specification (TS) 5.4.1.a, Procedures, was identified when the Unit 1 TDAFW uninterruptible power supplies (UPS) swapped to a bypass power source during maintenance on November 5, 2017. As a result, the TDAFW pump was rendered inoperable. Failure to follow licensee procedure FNP-1-EMP-1352.01, TDAFW UPS Battery Weekly Battery Inspection, Version 19, as written was a performance deficiency.
Description:
Maintenance performed a preventive maintenance task on the Unit 1 TDAFW UPS in accordance with work order SNC860880 and licensee procedure FNP-1-EMP-1352.01, TDAFW UPS Battery Weekly Battery Inspection, Ver. 19 on November 5, 2017. While making an adjustment to the primary charger float potentiometer, a step was performed out of sequence. This caused the charger failure light to come on locally at the UPS and annunciator JH4 TDAFWP UPS FAULT in the main control room. This also caused the UPS to swap from the primary UPS charger to the secondary UPS charger. The missed step was then performed which opened the battery input breaker to the secondary UPS and caused both UPS to swap to a bypass source. According to the licensee, this action rendered the TDAFW pump inoperable.
The TDAFW pump UPS consists of two separate full capacity UPS connected in a primary/secondary arrangement. Both UPS are normally in operation with the primary UPS supplying all of the loads. The operability of the TDAFW pump UPS was restored after approximately 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />. The licensee entered this issue into their CAP as CR 10427370.
Analysis:
The failure to follow licensee procedure FNP-1-EMP-1352, Ver. 19.0 as written during maintenance on the Unit 1 TDAFW pump UPS on November 5, 2017 was a performance deficiency. Specifically, steps in section 4.7.a were performed out of sequence which resulted in an unavailable UPS and an inoperable TDAFW pump. The finding was more than minor because it was associated with the equipment performance attribute of the mitigating system cornerstone and adversely affected that cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences since the TDAFW pump was rendered inoperable. The significance of this finding was evaluated using IMC 0609, Appendix A, The Significance Determination Process (SDP) for findings at-Power, dated June 19, 2012. This finding was determined to be of very low safety significance (Green) because all of the mitigating systems screening questions were answered NO.
The inspectors determined the finding had a cross-cutting aspect of Avoid Complacency in the Human Performance area because the individuals involved in this maintenance did not recognize or plan for the possibility of mistakes and appropriate error reduction tools were not implemented. [H.12]
Enforcement:
Technical Specification 5.4.1.a, Procedures, required, in part, that written procedures shall be established, implemented and maintained covering the applicable procedures recommended in Regulatory Guide (RG) 1.33, Revision 2, Appendix A. Section 9.a of RG 1.33, Appendix A, stated in part that maintenance that can affect the performance of safety-related equipment should be properly preplanned and performed in accordance with written procedures. Contrary to the above, on Nov. 5, 2017, licensee procedure FNP-1-EMP-1352.01, TDAFW UPS Battery Weekly Battery Inspection, Version 19 was performed out of sequence during maintenance the Unit 1 TDAFW UPS which rendered the TDAFW pump inoperable. The licensee entered this issue into their corrective action program (CAP) as condition report (CR) 10427370. The operability of the TDAFW pump UPS was restored after approximately 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />.
Because this finding is of very low safety significance and has been entered into the CAP, this violation was treated as an NCV, consistent with the Enforcement Policy. NCV 05000348/2017004-03 Failure to Follow Procedure Resulted in Inoperable TDAFW pump.
4OA3 Follow-up of Events
1. (Closed) Licensee Event Report (LER) 05000348/2016-007-02: Plant Shutdown
Required by Technical Specifications due to Inoperable Steam Flow Transmitters
a. Inspection Scope
During the licensees engineering review of cycle full power scaling values for steam flow normalization at the beginning of a new fuel cycle for Unit 1 while in Mode 1 at 99 percent reactor power, three steam flow channel values were found to be non-conservative and outside of +/- 2.5% delta pressure scan. This non-conservatism would allow steam flow to exceed the TS trip set-point before a steam line isolation would occur. Unit 1 initiated a plant shutdown on November 17, 2016, at 6:59 p.m. in accordance with Limiting Condition for Operation (LCO) 3.0.3 for having no operable steam flow channels for the C Steam Generator (SG). The two steam flow channels did not meet acceptance criteria for TS 3.3.2. On November 18, 2016, at 12:41 a.m., the Unit 1 plant shutdown was completed and the plant entered Mode 3, as required by LCO 3.0.3. The steam flow transmitters were restored to operable status by calculating new scaling data and rescaling the channels. LER 05000348/2016-007-02 is closed.
b. Findings
A severity level IV violation was identified in inspection report 2017-009. See section 4OA2.1.c.1 of that report for details.
4OA5 Other Activities
.1 Operation of an Independent Spent Fuel Storage Installation (ISFSI) (60855.1)
a. Inspection Scope
The inspectors performed a walkdown of the onsite ISFSI on December 22, 2017. The inspectors also reviewed surveillance records to verify that daily surveillance requirements were performed as required by technical specifications.
b. Findings
No findings were identified.
.2 (Closed) Violation (VIO)05000348/2016008-01, 05000364/2016008-01, Inaccurate
Training Records
a. Inspection Scope
The inspectors reviewed the licensees response to VIO 05000348/2016008-01, 05000364/2016008-01, EA-16-110 and determined that the reason, corrective actions taken and planned to address recurrence, and the date when full compliance was achieved for this violation is adequately addressed and captured on the docket.
Documents reviewed are listed in the attachment.
b. Findings
No findings were identified.
4OA6 Meetings, Including Exit
On January 23, 2018, the resident inspectors presented the inspection results to Dennis Madison and other members of the licensees staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection period.
4OA7 Licensee-Identified Violations
The following violations of very low safety significance (Green) or Severity Level IV were identified by the licensee and are violations of NRC requirements which meet the criteria of the NRC Enforcement Policy, for being dispositioned as a non-cited violation.
- 10 CFR 50.55 (a)(b)(5)(i) required in part that licensees must apply the most recent version of ASME BPV Code cases listed in Regulatory Guide 1.147, Revision 17.
Contrary to the above, the licensee failed to perform augmented re-examinations on a 30-day periodicity as required by ASME Code Case N-513-3. A through-wall pinhole leak on the Unit 2 Train A Service Water strainer backwash piping was documented in condition report (CR) 10234480 on June 10, 2016. The service water system provides a heat sink for the removal of process and operating heat from safety related components during a Design Basis Accident (DBA) or transient. The backwash piping is safety-related ASME Section III, Class 3 piping. An Immediate Determination of Operability Evaluation (IDO) was performed declaring the strainer operable but degraded non-conforming (OBDN). The licensee followed the guidance of ASME Code Case N-513-3, Evaluation Criteria for Temporary Acceptance of Flaws in Moderate Energy Class 2 or 3 Piping,Section XI, Division 1. The code case requires that an additional five similar susceptible locations be identified and inspected to ensure that another flaw does not exist. In addition to the expanded scope, the code case requires that frequent periodic inspections of no more than 30-day intervals shall be used to determine if the flaws are growing to an unacceptable size. An additional CR (10236417) was initiated on June 15, 2016, to request work orders for inspection of these five locations. A total of three examinations were performed on a 30-day periodicity, the last being completed on August 22, 2016. CR 10416364 was initiated on October 5, 2017, documenting that no re-examinations on a 30-day periodicity were performed on the original leak location and the five additional locations since August 22, 2016. The ultrasonic examination was completed on October 5, 2017, and the degraded backwash piping was removed and replaced with new piping by WO SNC795917 on October 28, 2017. This finding was determined to be of very low safety significance (Green) because it was not a design or qualification deficiency, it did not represent a loss of system safety function of a single train for greater than its TS allowed outage time, and it did not screen as potentially risk significant due to seismic, flooding, or severe weather initiating events. This finding was entered into the licensees CAP as CR 10416364.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
- K. Baity, Site Design Manager
- S. Briggs, Plant Manager
- J. Carroll, Engineering Plant Support Manager
- D. Erb, Assistant Maintenance Director
- B. Freeman, Engineering Supervisor
- S. Harris, Shift Operations Manager
- J. Horn, Operations Director
- N. Koteel, Operations
- D. Madison, Site Vice President
- R. McAdams, Engineering Director
- J. Short, Maintenance Director
- D. Simmons, EP Supervisor
- G. Surber, Licensing Supervisor
- C. Welch, Assistant Engineering Director
- R. Wells, Site Projects Manager
- E. Williford, Regulatory Affairs Manager
- S. Champion, Site ISI Coordinator
- K. King, BACCP Owner
- W. Truss, Steam Generator Program Manager
LIST OF REPORT ITEMS
Opened and Closed
- 05000364/2017004-01 Failure to Evaluate Impacts on the 2C RCP Oil Collection System (Section 1R05)
- 05000364/2017004-02 Failure to maintain an operable Oil Collection System on RCP 2B (Section 1R20)
- 05000348/2017004-03 Failure to Follow Procedure Resulted in Inoperable TDAFW pump (Section 4OA2.3)
Closed
LER
- 05000348/2016-007-02 Plant Shutdown Required by Technical Specifications due to Inoperable Steam Flow Transmitters (Section 4OA3.1)
- 05000348/2016008-01 Inaccurate Training Records (Section 4OA5.2)