IR 05000348/2022003

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Integrated Inspection Report 05000348/2022003 and 05000364/2022003
ML22299A015
Person / Time
Site: Farley  Southern Nuclear icon.png
Issue date: 10/28/2022
From: Alan Blamey
Division Reactor Projects II
To: Gayheart C
Southern Nuclear Operating Co
References
IR 2022003
Download: ML22299A015 (12)


Text

SUBJECT:

JOSEPH M. FARLEY NUCLEAR PLANT - INTEGRATED INSPECTION REPORT 05000348/2022003 AND 05000364/2022003

Dear Cheryl Gayheart:

On September 30, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Joseph M. Farley Nuclear Plant. On October 18, 2022, the NRC inspectors discussed the results of this inspection with Mr. Delson Erb, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Alan J. Blamey, Chief Reactor Projects Branch 2 Division of Reactor Projects Docket Nos. 05000348 and 05000364 License Nos. NPF-2 and NPF-8

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000348 and 05000364

License Numbers:

NPF-2 and NPF-8

Report Numbers:

05000348/2022003 and 05000364/2022003

Enterprise Identifier:

I-2022-003-0014

Licensee:

Southern Nuclear Operating Company, Inc

Facility:

Joseph M. Farley Nuclear Plant

Location:

Columbia, AL

Inspection Dates:

July 01, 2022 to September 30, 2022

Inspectors:

J. Bell, Health Physicist

K. Kirchbaum, Operations Engineer

N. Lacy, Operations Engineer

P. Meier, Senior Resident Inspector

S. Temple, Resident Inspector

Approved By:

Alan J. Blamey, Chief

Reactor Projects Branch 2

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Joseph M. Farley Nuclear Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

PLANT STATUS

Unit 1 began the inspection period at approximately 100 percent rated thermal power (RTP). On August 3, 2022, the unit was automatically shut down due to an automatic shutdown of the main turbine/generator. The turbine/generator shutdown was caused by a maintenance activity that inadvertently isolated the main generator from the 230 kilovolt (kV) bus no. 1. The unit was restarted on August 5, 2022 and returned to approximately 100 percent RTP on August 7, 2022.

On August 21, 2022, power was reduced to approximately 97 percent RTP to address a feedwater heater valve. The unit was returned to approximately 100 percent RTP on August 24, 2022. On August 27, 2022, the unit began coasting down until approximately 80 percent RTP was achieved on September 18, 2022. The unit was then shutdown on September 18, 2022 for a planned refueling outage (1R31) and remained there through the end of the report period.

Unit 2 began the report period at approximately 100 percent RTP and remained at or near 100 percent RTP through the end of the report period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

External Flooding Sample (IP Section 03.03) (1 Sample)

(1) The inspectors evaluated the Farley severe weather procedure on intense precipitation or site flooding emergency during the week of July 18, 2022.

(per procedure FNP-0-AOP-21.0)

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 1 'A' train of penetration room filtration during 'B' train equipment outage for charcoal sampling on July 27, 2022 (FNP-1-SOP-60.0A)
(2) Unit 1 turbine driven auxiliary feed water following unit trip and maintenance on steam admission valves during the week of August 15, 2022 (work order (WO) 1358833 and FNP-1-SOP-22.0)

(3)1B, 2B, 1-2A, and 1C emergency diesel generators and associated electrical distribution in advance of expected 2C diesel generator (station blackout generator)outage on August 23, 2022 (FNP-0-SOP-38.0A,B,C,E)

(4) Unit 1 component cooling water system during 'C' component cooling water pump planned maintenance outage on September 12, 2022 (FNP-1-SOP-23.0, D175002)

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the unit 1 auxiliary feedwater system from July 13 -18, 2022 (FNP-1-SOP-22.0A).

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas (FAs):

(1) Unit 1 component cooling water heat exchanger room (FA 1-006) on September 13, 2022 (FNP-1-FPP-1.0)
(2) Unit 1 'A' train electrical penetration room (FA 1-035) on September 13, 2022 (FNP-1-FPP-1.0)
(3) Unit 1 'A' train service water intake switchgear room (FA 76) on September 13, 2022 (FNP-1-FPP-1.0)
(4) Unit 1 hallway and local hot shutdown panel room (FA 1-012) on September 13, 2022 (FNP-1-FPP-1.0)
(5) Unit 1 residual heat removal heat exchanger room (FA 1-001) on September 13, 2022 (FNP-1-FPP-1.0)
(6) Diesel generator room 2C (FA 057) on September 13, 2022 (FNP-0-FPP-2.0)

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)

The inspectors evaluated internal flooding mitigation protections in the:

(1) Unit 1 and unit 2 'B' train pull boxes (inaccessible underground power cabling),

B1M47 and B2M47, that include safety related service water equipment cabling on July 5, 2022 (WO SNC1161367)

71111.11B - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Requalification Program (IP Section 03.04) (1 Sample)

The inspectors completed an inspection to verify the licensee's ability to evaluate the performance of their licensed operators during the conduct of examinations, to assess their ability to properly develop and administer requalification annual operating tests and biennial written examinations, to evaluate the performance of the control room simulator and their testing and maintenance of the simulator, to ensure that licensed individuals satisfy the conditions of their licenses, and to assess their effectiveness in ensuring that operator license conditions are satisfied.

(1) Biennial Requalification Written Examinations The inspectors evaluated the quality of the licensed operator biennial requalification written examination, 2022 Biennial Week 3, administered on May 26, 2022.

Annual Requalification Operating Tests The inspectors evaluated the adequacy of the facility licensees annual requalification operating test.

Administration of an Annual Requalification Operating Test The inspectors evaluated the effectiveness of the facility licensee in administering requalification operating tests required by 10 CFR 55.59(a)(2) and that the facility licensee is effectively evaluating their licensed operators for mastery of training objectives.

Requalification Examination Security The inspectors evaluated the ability of the facility licensee to safeguard examination material, such that the examination is not compromised.

Remedial Training and Re-examinations The inspectors evaluated the effectiveness of remedial training conducted by the licensee, and reviewed the adequacy of re-examinations for licensed operators who did not pass a required requalification examination.

Operator License Conditions The inspectors evaluated the licensees program for ensuring that licensed operators meet the conditions of their licenses.

Control Room Simulator The inspectors evaluated the adequacy of the facility licensees control room simulator in modeling the actual plant, and for meeting the requirements contained in 10 CFR 55.46.

Problem Identification and Resolution The inspectors evaluated the licensees ability to identify and resolve problems associated with licensed operator performance.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the Control Room during
(1) unit 1 dilution and operator response to a fire drill on July 14, 2022,
(2) unit 1 startup on August 5, 2022 following an unplanned trip on August 3, 2022, and
(3) portions of the unit 1 shutdown on September 18, 2022, in preparation for a planned refueling outage.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated licensed operator just-in-time training at the simulator in preparation for the unit 1 shutdown for the fall 2022 refueling outage (1R31) on September 12 and 13, 2022.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (1 Sample)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components remain capable of performing their intended function:

(1) Overall health of the Farley radiation monitoring systems (condition reports (CRs)

===10887483, 10855827)

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01)===

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Work in the high voltage switch house and unit 1 'A' train residual heat removal pump breaker planned maintenance and quarterly test on August 16, 2022. (WOs SNC1141529 and SNC1357707)
(2) Unit 2 'B' residual heat removal system outage resulting in yellow risk configuration on August 30, 2022. (WO SNC1236955)
(3) Unit 2 'B' 125 volt direct current (VDC) vital electrical bus ground emergent work on September 7, 2022, (NMP-DP-001)
(4) Unit 1 turbine driven auxiliary feedwater pump unavailability due to testing coincident with outage preparation work in the high voltage and low voltage switchyards on September 15, 2022, (NMP-GM-021)

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (6 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Unit 2 safety injection 'B' cold leg exceeding thermal stratification limit identified on June 30, 2022, (CR10891595)
(2) Unit 2 turbine driven auxiliary feedwater pump high thrust bearing temperature during surveillance run on bypass flow identified on July 7, 2022, (CR10893072)
(3) Unit 1 turbine driven auxiliary feedwater pump uninterruptible power supply battery cracks identified on June 20, 2022, (CR10889042)
(4) Unit 1 particulate radiation monitor, R11, alarming following filter replacement identified on July 21, 2022, (CRs10895715 and 10896105)
(5) Containment average air temperature calculation in accordance with the unit 1 and unit 2 operations daily and shift surveillance requirements (FNP-1/2-STP-1.0, CR

===10898368)

(6) Unit 2 'B' emergency diesel generator service water leak at the lube oil heat exchanger outlet service water side drain identified on August 22, 2022, (CR10902677)

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01)===

The inspectors evaluated the following post-maintenance testing activities to verify system operability and/or functionality:

(1) Unit 1 'B' emergency diesel generator start air system planned maintenance outage on July 5, 2022, (WO SNC892197)
(2) Unit 1 'C' component cooling water heat exchanger equipment outage and inspection performed during the week of July 12 and 18, 2022, (WOs SNC1140560 and SNC1139298)
(3) Work on circuit breaker for motor operated valve Q2N23MOV3764B, motor driven auxiliary feed water pumps to 2B steam generator, on August 1, 2022, (WOs SNC973092, SNC445588, and SNC996414)
(4) Cell replacement on #3 service water battery on August 3, 2022, (WO SNC1111648)
(5) Train 'B' control room filtration system maintenance inspection on July 25 and 26, 2022, (WOs SNC1083429 and SNC1086094)

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities to verify system operability and/or functionality:

Surveillance Tests (other) (IP Section 03.01) (3 Samples)

(1) Unit 1 'B' RHR pump quarterly surveillance test on July 5, 2022, (FNP-1-STP-11.2)
(2) Unit 1 'A' RHR pump quarterly surveillance run on August 16, 2022, (FNP-1-STP-11.1)
(3) Unit 2 'B' motor driven auxiliary feedwater pump quarterly surveillance run on July 28, 2022, (FNP-2-STP-22.2)

Inservice Testing (IP Section 03.01) (1 Sample)

(1) Unit 2 'A' RHR pump quarterly surveillance performed on July 19, 2022, (FNP-2-STP-11.1)

Reactor Coolant System (RCS) Leakage Detection Testing (IP Section 03.01) (1 Sample)

(1) Unit 2 identified leakage issues due to potential leakage on a letdown relief valve and a pressurizer safety valve identified on July 8, 2022, (CR10893201)

FLEX Testing (IP Section 03.02) (1 Sample)

(1) FLEX (i.e., diverse and flexible coping strategies) diesel generator testing and steam generator FLEX pump testing on July 26, 2022, (WOs SNC1170308 and SNC1133233)

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

MS05: Safety System Functional Failures Sample (IP Section 02.04)===

(1) Unit 1 (July 1, 2021 through June 30, 2022)
(2) Unit 2 (July 1, 2021 through June 30, 2022)

BI01: RCS Specific Activity Sample (IP Section 02.10) (2 Samples)

(1) Unit 1 (July 1, 2021 through June 30, 2022)
(2) Unit 2 (July 1, 2021 through June 30, 2022)

BI02: RCS Leak Rate Sample (IP Section 02.11) (2 Samples)

(1) Unit 1 (July 1, 2021 through June 30, 2022)
(2) Unit 2 (July 1, 2021 through June 30, 2022)

71152A - Annual Follow-up Problem Identification and Resolution Annual Follow-up of Selected Issues (Section 03.03)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Longstanding issue with all 3 phases of vital 120VAC alternate transformers 'fan failure' lights lit. (CRs 10816309, 368169, 368170, and 10896743)
(2) Corrective actions associated with a fire main rupture that occurred on February 11, 2021 (CR10773474)

71152S - Semiannual Trend Problem Identification and Resolution Semiannual Trend Review (Section 03.02)

(1) The inspectors reviewed the licensees corrective action program for potential adverse trends of unit 2 'B' residual heat removal pump oil additions and leaks that might be indicative of a more significant safety issue (CR10887730).

INSPECTION RESULTS

No findings were identified.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On October 18, 2022, the inspectors presented the integrated inspection results to Mr. Delson Erb, Site Vice President, and other members of the licensee staff.

THIRD PARTY REVIEWS Inspectors reviewed a World Association of Nuclear Operators peer review report regarding a review performed in February 2022.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Corrective Action

Documents

CR 10883142

Licensed Operator change in medical condition was not

reported to the NRC within 30 Days

05/24/2022

22 Biennial

Week 3

RO and SRO Written Exam

05/25/2022

CRO-333C, CRO-

358C, SO-296A,

SO-484, SO-

610E, SS-138D,

Crew 2 (Week 1) JPMs

06/21/2022

CRO-336B, CRO-

346 MOD, SO-

090, SO-551A,

SO-610C, SS-

138AA

Crew 5 (Week 4) JPMs

06/27/2022

Medical Records

Licensed Operator Medical Records (9)

July 2022

Reactivation

Records

Licensed Operator Reactivation Records (3)

July 2022

Scenario 21

200330 and

Peer 1

Crew 5 (Week 4) Simulator Scenarios

06/24/2022

Miscellaneous

Scenario 31-

20180517 and

Scenario 42-

200228

Crew 2 (Week 1) Simulator Scenarios

06/16/2022

NMP-OS-026

License Administration

Version 2.2

NMP-TR-100

SNC Conduct of Training

Version 14.2

NMP-TR-416

Licensed Operator Continuing Training Program

Administration

Version 12.3

71111.11B

Procedures

NMP-TR-424

License Operator Continuing Training Exam Development

Version 7.3