IR 05000352/2006002: Difference between revisions

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=Text=
=Text=
{{#Wiki_filter:May 01, 2006Mr. Christopher M. CranePresident and CNO Exelon Nuclear Exelon Generation Company, LLC 200 Exelon Way Kennett Square, PA 19348SUBJECT:LIMERICK GENERATING STATION - NRC INTEGRATED INSPECTIONREPORT 05000352/2006002 AND 05000353/2006002
{{#Wiki_filter:==SUBJECT:==
LIMERICK GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000352/2006002 AND 05000353/2006002


==Dear Mr. Crane:==
==Dear Mr. Crane:==
On March 31, 2006, the United States Nuclear Regulatory Commission (NRC) completed aninspection at your Limerick Generating Station Units 1 and 2. The enclosed integrated reportdocuments the inspection results which were discussed on April 11, 2006, with Mr. R. DeGregorio and other members of your staff. This inspection examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.
On March 31, 2006, the United States Nuclear Regulatory Commission (NRC) completed an inspection at your Limerick Generating Station Units 1 and 2. The enclosed integrated report documents the inspection results which were discussed on April 11, 2006, with Mr. R. DeGregorio and other members of your staff.


The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. This report documents one self-revealing finding of very low safety significance (Green). Thisfinding was determined to involve a violation of an NRC requirement. Additionally, a licensee-identified violation which was determined to be of very low safety significance is listed in this report. However, because of the very low safety significance, and because it is entered into your corrective action program, the NRC is treating this finding as a non-cited violations (NCV),in accordance with Section VI.A.1 of the NRC's Enforcement Policy. If you contest the NCV inthis report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001; with copies to the Regional Administrator Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Limerick facility.In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, itsenclosure, and your response (if any) will be available electronically for public inspection in the C. Crane2NRC Public Document Room or from the Publicly Available Records (PARS) component of theNRC's document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
This inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
 
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
 
This report documents one self-revealing finding of very low safety significance (Green). This finding was determined to involve a violation of an NRC requirement. Additionally, a licensee-identified violation which was determined to be of very low safety significance is listed in this report. However, because of the very low safety significance, and because it is entered into your corrective action program, the NRC is treating this finding as a non-cited violations (NCV),
in accordance with Section VI.A.1 of the NRCs Enforcement Policy. If you contest the NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001; with copies to the Regional Administrator Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Limerick facility.
 
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,
Sincerely,
/RA/James M. Trapp, ChiefProjects Branch 4 Division of Reactor ProjectsDocket Nos: 50-352; 50-353License Nos: NPF-39; NPF-85Enclosure:Inspection Report 05000352/2006002 and 05000353/2006002w/Attachment: Supplemental Informationcc w/encl:Chief Operating Officer, Exelon Generation Company, LLC Site Vice President - Limerick Generating Station Plant Manager, Limerick Generating Station Regulatory Assurance Manager - Limerick Senior Vice President - Nuclear Services Vice President - Mid-Atlantic Operations Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Director - Licensing and Regulatory Affairs, Exelon Generation Company, LLC Manager, Licensing - Limerick Generating Station Vice President, General Counsel and Secretary Associate General Counsel, Exelon Generation Company Correspondence Control Desk J. Johnsrud, National Energy Committee Chairman, Board of Supervisors of Limerick Township R. Janati, Chief, Division of Nuclear Safety, Pennsylvania Bureau of Radiation Protection J. Bradley Fewell, Assistant General Counsel, Exelon Nuclear D. Allard, Director, Dept. of Environmental Protection, Bureau of Radiation Protection (SLO)
/RA/
James M. Trapp, Chief Projects Branch 4 Division of Reactor Projects Docket Nos: 50-352; 50-353 License Nos: NPF-39; NPF-85 Enclosure: Inspection Report 05000352/2006002 and 05000353/2006002 w/Attachment: Supplemental Information cc w/encl:
Chief Operating Officer, Exelon Generation Company, LLC Site Vice President - Limerick Generating Station Plant Manager, Limerick Generating Station Regulatory Assurance Manager - Limerick Senior Vice President - Nuclear Services Vice President - Mid-Atlantic Operations Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Director - Licensing and Regulatory Affairs, Exelon Generation Company, LLC Manager, Licensing - Limerick Generating Station Vice President, General Counsel and Secretary Associate General Counsel, Exelon Generation Company Correspondence Control Desk J. Johnsrud, National Energy Committee Chairman, Board of Supervisors of Limerick Township R. Janati, Chief, Division of Nuclear Safety, Pennsylvania Bureau of Radiation Protection J. Bradley Fewell, Assistant General Counsel, Exelon Nuclear D. Allard, Director, Dept. of Environmental Protection, Bureau of Radiation Protection (SLO)


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
IR 05000352/2006-002, 05000353/2006-002; 01/01/2006 - 03/31/2006; Limerick GeneratingStation, Units 1 and 2; Operator Performance During Non-Routine Plant Evolutions and Events.The report covered a 3-month period of inspection by resident inspectors and announcedinspections by a regional health physicist inspector and a reactor inspector. The inspectors identified one Green non-cited violation (NCV). The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter 0609, "Significance Determination Process" (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeingthe safe operation of commercial nuclear power reactors is described in NUREG-1649,"Reactor Oversight Process," Revision 3, dated July 2000. Reactor Safety A.
IR 05000352/2006-002, 05000353/2006-002; 01/01/2006 - 03/31/2006; Limerick Generating
 
Station, Units 1 and 2; Operator Performance During Non-Routine Plant Evolutions and Events.
 
The report covered a 3-month period of inspection by resident inspectors and announced inspections by a regional health physicist inspector and a reactor inspector. The inspectors identified one Green non-cited violation (NCV). The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649,
Reactor Oversight Process, Revision 3, dated July 2000.
 
Reactor Safety


===NRC-Identified and Self-Revealing Findings===
===NRC-Identified and Self-Revealing Findings===
Line 35: Line 52:
===Cornerstone: Initiating Events===
===Cornerstone: Initiating Events===
: '''Green.'''
: '''Green.'''
A self-revealing NCV was identified for the licensee's failure to comply withTechnical Specification (TS) 3.9.2, "Instrumentation.Plant operations staffinappropriately started core alterations after the loss of all Unit 2 source range monitor audible alarms. Core alterations were stopped when Exelon management was informed of the problem. The source range monitor audible alarm was fixed prior to moving fuel in the reactor and this issue was entered into Exelon's corrective action program.This finding is greater than minor because it affected the Initiating Events cornerstoneobjective of limiting the likelihood of those events that challenge critical safety functions during shutdown conditions. This finding is of very low safety significance because it did not increase the likelihood of a loss of reactor coolant system inventory, it did notdegrade the ability to terminate a leak or add inventory to the reactor cool ant system,and it did not degrade the ability to recover decay heat removal capability if lost.  (Section 1R14)
A self-revealing NCV was identified for the licensees failure to comply with Technical Specification (TS) 3.9.2, Instrumentation. Plant operations staff inappropriately started core alterations after the loss of all Unit 2 source range monitor audible alarms. Core alterations were stopped when Exelon management was informed of the problem. The source range monitor audible alarm was fixed prior to moving fuel in the reactor and this issue was entered into Exelon's corrective action program.


===B. Licensee-Identified Violations===
This finding is greater than minor because it affected the Initiating Events cornerstone objective of limiting the likelihood of those events that challenge critical safety functions during shutdown conditions. This finding is of very low safety significance because it did not increase the likelihood of a loss of reactor coolant system inventory, it did not degrade the ability to terminate a leak or add inventory to the reactor coolant system, and it did not degrade the ability to recover decay heat removal capability if lost.
Violations of very low safety significance, which were identified by the licensee havebeen reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. One licensee identified violation and associated corrective actions are listed in Section 4OA7 of this report.


Enclosure
        (Section 1R14)
 
===Licensee-Identified Violations===
 
Violations of very low safety significance, which were identified by the licensee have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. One licensee identified violation and associated corrective actions are listed in Section 4OA7 of this report.
 
iii


=REPORT DETAILS=
=REPORT DETAILS=
Summary of Plant StatusUnit 1 began this inspection period at full rated thermal power and operated at full power untilJanuary 13, 2006, when operators decreased power to approximately 70 percent for power suppression testing. Unit 1 returned to full power on January 17. On February 7, 2006, Unit 1 entered reactor power end-of-cycle coastdown. On March 6, operators shutdown Unit 1 for aplanned refueling and maintenance outage (1R11). The reactor achieved criticality on March 23, and following repairs to the 1C reactor feed pump, Unit 1 returned to full rated thermal power on March 28, 2006.Unit 2 began this inspection period at full rated thermal power. Unit 2 shut down onFebruary 23, 2006 for a planned maintenance outage to replace three safety relief valves (SRVs.)   Unit 2 returned to full rated thermal power on February 26, 2006 and operated at or near full rated thermal power for the rest of the inspection period.
 
===Summary of Plant Status===
 
Unit 1 began this inspection period at full rated thermal power and operated at full power until January 13, 2006, when operators decreased power to approximately 70 percent for power suppression testing. Unit 1 returned to full power on January 17. On February 7, 2006, Unit 1 entered reactor power end-of-cycle coastdown. On March 6, operators shutdown Unit 1 for a planned refueling and maintenance outage (1R11). The reactor achieved criticality on March 23, and following repairs to the 1C reactor feed pump, Unit 1 returned to full rated thermal power on March 28, 2006.
 
Unit 2 began this inspection period at full rated thermal power. Unit 2 shut down on February 23, 2006 for a planned maintenance outage to replace three safety relief valves (SRVs.) Unit 2 returned to full rated thermal power on February 26, 2006 and operated at or near full rated thermal power for the rest of the inspection period.


==REACTOR SAFETY==
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity1R01Adverse Weather Protection (71111.01 - 1 sample)
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
 
{{a|1R01}}
==1R01 Adverse Weather Protection==
{{IP sample|IP=IP 71111.01|count=1}}


====a. Inspection Scope====
====a. Inspection Scope====
Since snow storms were forecasted in the vicinity of the facility for early February 2006,the inspectors reviewed Exelon's overall preparations and protection for the expected weather conditions. The inspectors walked down portions of procedure SE-14, "Snow,"
Since snow storms were forecasted in the vicinity of the facility for early February 2006, the inspectors reviewed Exelons overall preparations and protection for the expected weather conditions. The inspectors walked down portions of procedure SE-14, Snow, including applicable portions of the emergency diesel generators and the condensate storage tank system. The inspectors also reviewed various related issue reports (IRs)and action requests (ARs). This inspection satisfied one inspection sample for overall preparations and protection for expected adverse weather conditions. Documents reviewed for each applicable section of this report are listed in the Attachment.
including applicable portions of the emergency diesel generators and the condensate storage tank system. The inspectors also reviewed various related issue reports (IRs)and action requests (ARs). This inspection satisfied one inspection sample for overall preparations and protection for expected adverse weather conditions. Documents reviewed for each applicable section of this report are listed in the Attachment.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|1R04}}
{{a|1R04}}
==1R04 Equipment Alignment (71111.04)==
==1R04 Equipment Alignment==
.1   Partial Walkdown (71111.04Q - 3 samples)
{{IP sample|IP=IP 71111.04}}
===.1 Partial Walkdown===
{{IP sample|IP=IP 71111.04Q|count=3}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed a partial walkdown of the following three systems to verify theoperability of redundant or diverse trains and components when safety equipment wasinoperable. The inspectors attempted to identify any discrepancies that could impact the function of t he system, and, therefore, potentially increase risk. The inspectors 2Enclosurereviewed applicable operating procedures, walked down control systems components,and verified that selected breakers, valves, and support equipment were in the correct position to support system operation. The inspectors also verified that Exelon hadproperly identified and resolved equipment mitigation problems that could cause initiating events or impact the capability of mitigating systems or barriers and enteredthem into the corrective action program.
The inspectors performed a partial walkdown of the following three systems to verify the operability of redundant or diverse trains and components when safety equipment was inoperable. The inspectors attempted to identify any discrepancies that could impact the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, walked down control systems components, and verified that selected breakers, valves, and support equipment were in the correct position to support system operation. The inspectors also verified that Exelon had properly identified and resolved equipment mitigation problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program.
* Unit 2 Reactor Core Isolation Cooling (RCIC) System During High Risk HighPressure Coolant Injection (HPCI) System Testing* D12, D13, and D14 Emergency Diesel Generators (EDGs) During D11 EDGPlanned Maintenance* Unit 1 Reactor Recirculation System Following Refueling Outage.2     Complete System Walkdown (71111.04S - 1 sample)
* Unit 2 Reactor Core Isolation Cooling (RCIC) System During High Risk High Pressure Coolant Injection (HPCI) System Testing
* D12, D13, and D14 Emergency Diesel Generators (EDGs) During D11 EDG Planned Maintenance
* Unit 1 Reactor Recirculation System Following Refueling Outage
 
===.2 Complete System Walkdown===
{{IP sample|IP=IP 71111.04S|count=1}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors conducted one complete walkdown of the Unit 2 residual heat removal(RHR) system to verify the functional capability of the system. The inspectors usedExelon procedures and other documents listed in the Attachment to verify proper systemalignment. The inspectors also verified electrical power requirements, operator workarounds, hangers and support installation, and associated support systems status. The walkdown also included evaluation of the system piping and supports against thefollowing considerations:*Piping and supports did not show evidence of water hammer*Oil reservoirs appeared normal
The inspectors conducted one complete walkdown of the Unit 2 residual heat removal (RHR) system to verify the functional capability of the system. The inspectors used Exelon procedures and other documents listed in the Attachment to verify proper system alignment. The inspectors also verified electrical power requirements, operator workarounds, hangers and support installation, and associated support systems status.
*Snubbers did not appear to be leaking hydraulic fluid
 
*Hangers were functional
The walkdown also included evaluation of the system piping and supports against the following considerations:
*Component foundations were not degradedThe inspectors performed a review of outstanding issue reports, action requests, andwork orders to ensure that the deficiencies did not affect RHR design function and toverify that Exelon was appropriately identifying and resolving any equipment alignment problems.
* Piping and supports did not show evidence of water hammer
* Oil reservoirs appeared normal
* Snubbers did not appear to be leaking hydraulic fluid
* Hangers were functional
* Component foundations were not degraded The inspectors performed a review of outstanding issue reports, action requests, and work orders to ensure that the deficiencies did not affect RHR design function and to verify that Exelon was appropriately identifying and resolving any equipment alignment problems.


====c. Findings====
====c. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|1R05}}
==1R05 Fire Protection==


3Enclosure1R05Fire Protection.1Fire Protection - Tours (71111.05Q - 9 samples)
===.1 Fire Protection - Tours===
{{IP sample|IP=IP 71111.05Q|count=9}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors conducted a tour of the areas listed below to assess the materialcondition and operational status of fire protection features. The inspectors verified that combustibles and ignition sources were controlled in accordance with Exelon's administrative procedures, fire detection and suppression equipment was available for use, and that passive fire barriers were maintained in good material condition. The inspectors also verified that station personnel implemented compensatory measures for out-of-service, degraded, or inoperable fire protection equipment in accordance with Exelon's fire plan.
The inspectors conducted a tour of the areas listed below to assess the material condition and operational status of fire protection features. The inspectors verified that combustibles and ignition sources were controlled in accordance with Exelons administrative procedures, fire detection and suppression equipment was available for use, and that passive fire barriers were maintained in good material condition. The inspectors also verified that station personnel implemented compensatory measures for out-of-service, degraded, or inoperable fire protection equipment in accordance with Exelons fire plan.
* Unit 1 Refuel Floor During New Reactor Fuel Inspections* Unit 1 Elevation 253' During Refuel Outage Preparations
* Unit 1 Refuel Floor During New Reactor Fuel Inspections
* Unit 1 Elevation 253' During Refuel Outage Preparations
* D11 EDG Room During Maintenance Overhaul
* D11 EDG Room During Maintenance Overhaul
* Unit 1 Elevation 269' During Refuel Outage Preparations
* Unit 1 Elevation 269' During Refuel Outage Preparations
Line 86: Line 131:
====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|1R07}}
{{a|1R07}}
==1R07 Heat Sink Performance (71111.07A - 1 sample)==
==1R07 Heat Sink Performance==
{{IP sample|IP=IP 71111.07A|count=1}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed portions of Exelon's "1A" residual heat removal (RHR) heatexchanger transfer test to ensure the heat exchanger could perform its design function.
The inspectors observed portions of Exelons 1A residual heat removal (RHR) heat exchanger transfer test to ensure the heat exchanger could perform its design function.


The inspectors observed the heat transfer test from the main control room and locally in the Reactor Building. The inspectors reviewed Exelon's final heat exchanger test data to ensure the as-found heat transfer values were within design limits. The inspectors also walked down the "1A" RHR heat exchanger to assess its material condition.
The inspectors observed the heat transfer test from the main control room and locally in the Reactor Building. The inspectors reviewed Exelons final heat exchanger test data to ensure the as-found heat transfer values were within design limits. The inspectors also walked down the 1A RHR heat exchanger to assess its material condition.
* RT-2-012-390-1, "1A Residual Heat Removal Heat Exchanger Transfer Test"
* RT-2-012-390-1, 1A Residual Heat Removal Heat Exchanger Transfer Test


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.


4Enclosure1R08Inservice Inspection Activities (71111.08 - 1 sample)
{{a|1R08}}
==1R08 Inservice Inspection Activities==
{{IP sample|IP=IP 71111.08|count=1}}


====a. Inspection Scope====
====a. Inspection Scope====
Inspectors selected a sample of non-destructive examination (NDE) activities for reviewfrom the Unit 1 refueling outage (RFO) 11 examination plan to assess the effectiveness of the inservice inspection (ISI) program for monitoring degradation of containment, the reactor coolant system (RCS), and risk-significant piping system pressure boundaries. The inspection consisted of interviews with plant personnel, observations of nondestructive examinations and calibrations of nondestructive equipment, and review of procedures, examination results, calibration documentation, and qualification certifications. The inspector verified that Exelon performed these activities in accordance with the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code requirements.The inspector reviewed the modification package for the replacement of the 16 inch'B' loop RHR containment spray outboard isolation valve to verify that the design basisand performance of the valve was not degraded as a result of the modification. The inspector verified that Exelon performed the radiography of the pipe to elbow weld FW 1301, the pipe to valve weld FW 5, and the pipe to valve weld SW 6 in accordance with the ASME Boiler and Pressure Vessel Code and that the welds met the ASME Code acceptance criteria. The inspector verified the welding procedure and the welder qualifications met the requirements of the ASME Code.The inspector observed and reviewed several visual examinations associated with thein-vessel visual inspection (IVVI) including jet pump set screw tack welds, wedge wear, restrainer bracket adjustment screw gap measurement, riser pipe to riser brace circumferential weld, and core spray 'A' loop shroud pipe to collar weld, P8aC. The inspector verified the camera calibration and examination met the ASME requirements for VT-1 visual examinations.The inspector observed portions of the magnetic particle inspection of the reactor vesselskirt weld in order to evaluate examiner skill and examination technique. The inspectorverified the calibration of the AC electromagnetic yoke, that the examiner was properly qualified, and that the examination procedure was followed. Examination results werereviewed for recordable indications. The inspector observed a portion of the ultrasonic examination of 4 inch RCIC weldsDBA-107-1FW54 (RC012) and DBA-107-1FW4 (RC013) in order to evaluate examiner skill, test equipment performance, and examination environment (condition of weldsurface). The inspector verified the calibration and examination were performed in accordance with approved procedures and that the examiners were properly qualified.
Inspectors selected a sample of non-destructive examination (NDE) activities for review from the Unit 1 refueling outage (RFO) 11 examination plan to assess the effectiveness of the inservice inspection (ISI) program for monitoring degradation of containment, the reactor coolant system (RCS), and risk-significant piping system pressure boundaries.
 
The inspection consisted of interviews with plant personnel, observations of nondestructive examinations and calibrations of nondestructive equipment, and review of procedures, examination results, calibration documentation, and qualification certifications. The inspector verified that Exelon performed these activities in accordance with the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code requirements.
 
The inspector reviewed the modification package for the replacement of the 16 inch B loop RHR containment spray outboard isolation valve to verify that the design basis and performance of the valve was not degraded as a result of the modification. The inspector verified that Exelon performed the radiography of the pipe to elbow weld FW 1301, the pipe to valve weld FW 5, and the pipe to valve weld SW 6 in accordance with the ASME Boiler and Pressure Vessel Code and that the welds met the ASME Code acceptance criteria. The inspector verified the welding procedure and the welder qualifications met the requirements of the ASME Code.
 
The inspector observed and reviewed several visual examinations associated with the in-vessel visual inspection (IVVI) including jet pump set screw tack welds, wedge wear, restrainer bracket adjustment screw gap measurement, riser pipe to riser brace circumferential weld, and core spray A loop shroud pipe to collar weld, P8aC. The inspector verified the camera calibration and examination met the ASME requirements for VT-1 visual examinations.
 
The inspector observed portions of the magnetic particle inspection of the reactor vessel skirt weld in order to evaluate examiner skill and examination technique. The inspector verified the calibration of the AC electromagnetic yoke, that the examiner was properly qualified, and that the examination procedure was followed. Examination results were reviewed for recordable indications.
 
The inspector observed a portion of the ultrasonic examination of 4 inch RCIC welds DBA-107-1FW54 (RC012) and DBA-107-1FW4 (RC013) in order to evaluate examiner skill, test equipment performance, and examination environment (condition of weld surface). The inspector verified the calibration and examination were performed in accordance with approved procedures and that the examiners were properly qualified.
 
The inspector reviewed the exam reports for recordable indications.


The inspector reviewed the exam reports for recordable indications.The inspector verified the scope of the ultrasonic examination of the core shroud weldswas in accordance with the guidance from the Electric Power Research Institute (EPRI)
The inspector verified the scope of the ultrasonic examination of the core shroud welds was in accordance with the guidance from the Electric Power Research Institute (EPRI)
Boiling Water Reactor Vessel Inspection Program 76 (BWRVIP-76). The data from the 5Enclosureultrasonic examination of the horizontal welds H-3, H-4, H-5 and vertical welds V-15,V-16, V-17, and V-18 of the core shroud was reviewed for recordable indications.
Boiling Water Reactor Vessel Inspection Program 76 (BWRVIP-76). The data from the ultrasonic examination of the horizontal welds H-3, H-4, H-5 and vertical welds V-15, V-16, V-17, and V-18 of the core shroud was reviewed for recordable indications.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|1R11}}
{{a|1R11}}
==1R11 Licensed Operator Requalification Program (71111.11 - 1 sample)Resident Inspector Quarterly Review==
==1R11 Licensed Operator Requalification Program==
{{IP sample|IP=IP 71111.11|count=1}}
Resident Inspector Quarterly Review


====a. Inspection Scope====
====a. Inspection Scope====
On January 30, 2006, the inspectors observed a medium pipe break loss of coolantaccident (LOCA) simulator scenario to assess licensed operator performance and the evaluator's critique. The simulator evaluation was performed during the licensed operator annual examination. The inspectors discussed the results with operators, operations management, and training instructors.
On January 30, 2006, the inspectors observed a medium pipe break loss of coolant accident (LOCA) simulator scenario to assess licensed operator performance and the evaluators critique. The simulator evaluation was performed during the licensed operator annual examination. The inspectors discussed the results with operators, operations management, and training instructors.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|1R12}}
{{a|1R12}}
==1R12 Maintenance Effectiveness (71111.12 - 2 samples)==
==1R12 Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12|count=2}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the two samples listed below for items such as:
The inspectors reviewed the two samples listed below for items such as:
: (1) appropriatework practices;
: (1) appropriate work practices;
: (2) identifying and addressing common cause failures;
: (2) identifying and addressing common cause failures;
: (3) scoping in accordance with 10 CFR 50.65(b) of the maintenance rule (MR);
: (3) scoping in accordance with 10 CFR 50.65(b) of the maintenance rule (MR);
: (4) characterizing reliability issues for performance;
: (4) characterizing reliability issues for performance;
: (5) trending key parameters for condition monitoring;(6) charging unavailability for performance;
: (5) trending key parameters for condition monitoring;
: (7) classification and reclassification inaccordance with 10 CFR 50.65 (a)(1) or (a)(2); and
: (6) charging unavailability for performance;
: (8) appropriateness of performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2)and/or appropriateness and adequacy of goals and corrective actions for SSCs/functions classified as (a)(1). Items reviewed included the following:* Unit 1 and 2 Safety Relief Valve Leakage* Emergency Core Cooling System (ECCS) Room Cooler Failures due to Silting in theEmergency Service Water (ESW) System
: (7) classification and reclassification in accordance with 10 CFR 50.65 (a)(1) or (a)(2); and
: (8) appropriateness of performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2)and/or appropriateness and adequacy of goals and corrective actions for SSCs/functions classified as (a)(1). Items reviewed included the following:
* Unit 1 and 2 Safety Relief Valve Leakage
* Emergency Core Cooling System (ECCS) Room Cooler Failures due to Silting in the Emergency Service Water (ESW) System


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.


6Enclosure1R13Maintenance Risk Assessments and Emergent Work Control (71111.13 - 7 samples)
{{a|1R13}}
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13|count=7}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the following seven activities to verify that Exelon performedthe appropriate risk assessments prior to removing equipment for work. The inspectors verified that Exelon performed accurate and complete risk assessments as required by 10 CFR 50.65 (a)(4). When the station performed emergent work, the inspectors verified that the plant risk was promptly reassessed and managed in accordance with Exelon's risk assessment tool and risk categories.
The inspectors reviewed the following seven activities to verify that Exelon performed the appropriate risk assessments prior to removing equipment for work. The inspectors verified that Exelon performed accurate and complete risk assessments as required by 10 CFR 50.65 (a)(4). When the station performed emergent work, the inspectors verified that the plant risk was promptly reassessed and managed in accordance with Exelons risk assessment tool and risk categories.
* 101 Transformer Tap Changer Failed to Tap Following Modification*Unit 1 Reactor Core Isolation Cooling (RCIC) System High Turbine Oil Level
* 101 Transformer Tap Changer Failed to Tap Following Modification
*Unit 1 Risk During D11 EDG Planned Maintenance Concurrent with Maintenance onHPCI/RCIC Full-Flow Test Valve*Unit 1 'A' and 'B' Outboard MSIVs Exceeded Max Close Stroke Time (A1554743)
* Unit 1 Reactor Core Isolation Cooling (RCIC) System High Turbine Oil Level
*Unit 1 RCIC Turbine Oil Contained Bearing Material (IR 463640)
* Unit 1 Risk During D11 EDG Planned Maintenance Concurrent with Maintenance on HPCI/RCIC Full-Flow Test Valve
*HV-049-1F007 Failed to Close (A1554514)
* Unit 1 A and B Outboard MSIVs Exceeded Max Close Stroke Time (A1554743)
*High Unit 1 Reactor Conductivity and Chlorides During Start-Up from  
* Unit 1 RCIC Turbine Oil Contained Bearing Material (IR 463640)
{{a|1R11}}
* HV-049-1F007 Failed to Close (A1554514)
==1R11 Refueling Outage
* High Unit 1 Reactor Conductivity and Chlorides During Start-Up from 1R11 Refueling Outage


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|1R14}}
{{a|1R14}}
==1R14 Operator Performance During Non-Routine Evolutions and Events==
==1R14 Operator Performance During Non-Routine Evolutions and Events (71111.14 -==
==
 
{{IP sample|IP=IP 71111.14|count=2}}
2 samples)


====a. Inspection Scope====
====a. Inspection Scope====
For the non-routine events described below, the inspectors reviewed operator logs, plantcomputer data, and other documentation to determine what occurred and how theoperators responded, and to determine if the response was in accordance with plant procedures. *On March 12, 2005, the inspectors reviewed operator and station response to theloss of an alarm horn supplying audible indication for a number of Unit 2 main control room (MCR) alarms. The inspectors reviewed the applicable Technical Specification (TS) requirements, off-normal operating procedures, and Limerick's Emergency Plan. The inspectors also conducted interviews with operators and supervisors. An NRC followup review of this issue was performed prior to finaldocumentation.*On February 22, 2006, the inspectors observed a reactor shutdown on Unit 2 inpreparation for a short-duration maintenance outage to replace three leaking safety relief valves (SRVs). The inspectors observed operator actions in the control room, 7Enclosurereviewed logs and outage work schedules, and monitored portions of thesubsequent start-up and return to full power.
For the non-routine events described below, the inspectors reviewed operator logs, plant computer data, and other documentation to determine what occurred and how the operators responded, and to determine if the response was in accordance with plant procedures.
* On March 12, 2005, the inspectors reviewed operator and station response to the loss of an alarm horn supplying audible indication for a number of Unit 2 main control room (MCR) alarms. The inspectors reviewed the applicable Technical Specification (TS) requirements, off-normal operating procedures, and Limericks Emergency Plan. The inspectors also conducted interviews with operators and supervisors. An NRC followup review of this issue was performed prior to final documentation.
* On February 22, 2006, the inspectors observed a reactor shutdown on Unit 2 in preparation for a short-duration maintenance outage to replace three leaking safety relief valves (SRVs). The inspectors observed operator actions in the control room, reviewed logs and outage work schedules, and monitored portions of the subsequent start-up and return to full power.


====b. Findings====
====b. Findings====


=====Introduction.=====
=====Introduction.=====
A Green self-revealing non-cited violation (NCV) was identified of TS3.9.2, "Instrumentation," because Limerick started core alterations after the loss of allUnit 2 source range monitor (SRM) audible alarms.Description. On the morning of March 12, 2005, while performing an annunciator checkin the MCR, the horn for several MCR panels sounded continuously and could not be reset. At the time, Limerick Unit 2 was shutdown for a planned refueling outage. The control room operators entered procedure ON-122, "Loss of Main Control Room Annunciators," and removed power to the alarming horn. The disabled horn provided the audible alarms for the SRMs, among others. As a compensatory measure, a dedicated operator was stationed in the MCR to monitor the panels without audiblealarms.Limerick TS 3.9.2 requires that at least two SRM channels be operable and inserted tothe normal operating level with audible alarm indication available for at least one SRM.
A Green self-revealing non-cited violation (NCV) was identified of TS 3.9.2, Instrumentation, because Limerick started core alterations after the loss of all Unit 2 source range monitor (SRM) audible alarms.
 
=====Description.=====
On the morning of March 12, 2005, while performing an annunciator check in the MCR, the horn for several MCR panels sounded continuously and could not be reset. At the time, Limerick Unit 2 was shutdown for a planned refueling outage. The control room operators entered procedure ON-122, Loss of Main Control Room Annunciators, and removed power to the alarming horn. The disabled horn provided the audible alarms for the SRMs, among others. As a compensatory measure, a dedicated operator was stationed in the MCR to monitor the panels without audible alarms.
 
Limerick TS 3.9.2 requires that at least two SRM channels be operable and inserted to the normal operating level with audible alarm indication available for at least one SRM.


If these conditions are not met, TS 3.9.2 requires that core alterations be suspended.
If these conditions are not met, TS 3.9.2 requires that core alterations be suspended.


At the time the alarm function of the SRMs was lost, fuel bundle movement in the reactor core was not in progress at Unit 2. However, at 12:11 p.m. on March 12, following consultation with the Outage Control Center (OCC), Limerick shift management authorized fuel movements to commence. While corrective actions for the failed alarm function were being planned, the horn was st ill inoperable at that time. Fuel movement continued until 8:58 p.m., when a supervisor on the night shiftrecognized that a violation of TS 3.9.2 may have occurred. The Shift Manager ordered fuel movements to be suspended and informed the OCC and Limerick senior management. The Shift Manager, Shift Operations Superintendent, and Control Room Supervisor then made the decision that the compensatory measures in place for theinoperable horn were adequate to meet the intent of the TS, and at 9:11 p.m., thestation recommenced fuel movement. Operations did not coordinate this decision through the OCC. When the OCC learned that fuel movement had been resumedwithout the audible SRM alarm function, they notified the Operations Director, and heordered fuel movements stopped at 9:39 p.m. Station personnel repaired the SRMaudible alarm prior to moving additional fuel bundles.
At the time the alarm function of the SRMs was lost, fuel bundle movement in the reactor core was not in progress at Unit 2. However, at 12:11 p.m. on March 12, following consultation with the Outage Control Center (OCC), Limerick shift management authorized fuel movements to commence. While corrective actions for the failed alarm function were being planned, the horn was still inoperable at that time.
 
Fuel movement continued until 8:58 p.m., when a supervisor on the night shift recognized that a violation of TS 3.9.2 may have occurred. The Shift Manager ordered fuel movements to be suspended and informed the OCC and Limerick senior management. The Shift Manager, Shift Operations Superintendent, and Control Room Supervisor then made the decision that the compensatory measures in place for the inoperable horn were adequate to meet the intent of the TS, and at 9:11 p.m., the station recommenced fuel movement. Operations did not coordinate this decision through the OCC. When the OCC learned that fuel movement had been resumed without the audible SRM alarm function, they notified the Operations Director, and he ordered fuel movements stopped at 9:39 p.m. Station personnel repaired the SRM audible alarm prior to moving additional fuel bundles.


=====Analysis.=====
=====Analysis.=====
The inspectors determined that Exelon's non-compliance with therequirements of TS 3.9.2 is a performance deficiency. Additionally, once the non-compliance was identified, Limerick operations staff incorrectly determined that compensatory measures could be used to meet the TS 3.9.2 requirements, andsubsequently recommenced fuel moves. Traditional enforcement does not apply because the issue did not have any actual safety consequences or potential for impacting the NRC's regulatory function, and was not the result of any willful violationof NRC requirements or Exelon procedures.
The inspectors determined that Exelons non-compliance with the requirements of TS 3.9.2 is a performance deficiency. Additionally, once the non-compliance was identified, Limerick operations staff incorrectly determined that compensatory measures could be used to meet the TS 3.9.2 requirements, and subsequently recommenced fuel moves. Traditional enforcement does not apply because the issue did not have any actual safety consequences or potential for impacting the NRCs regulatory function, and was not the result of any willful violation of NRC requirements or Exelon procedures.
 
This finding is greater than minor because it was associated with the Configuration Control attribute of shutdown equipment alignment, and affected the Initiating Events Cornerstone objective of limiting the likelihood of events challenging critical safety functions during shutdown operations. Inspectors assessed this finding using Phase 1 of the Shutdown Operations Significance Determination Process. Inspectors determined this finding to be of very low safety significance (Green), because while the finding represented a non-compliance with a core alteration TS, it did not increase the likelihood of a loss of reactor coolant system (RCS) inventory, it did not degrade the ability to terminate a leak or add inventory to the RCS, and it did not degrade the ability to recover decay heat removal capability if lost.
 
=====Enforcement.=====
TS 3.9.2, Instrumentation, requires that at least two SRM channels be operable and that at least one has an audible indication in the MCR. If this condition is not met, TS 3.9.2 requires that core alterations be immediately suspended. Contrary to the above, on March 12, 2005, Limerick Unit 2 operators continued to perform core alterations for over nine hours following the loss of all Unit 2 SRM audible annunciators.


8EnclosureThis finding is greater than minor because it was associated with the ConfigurationControl attribute of shutdown equipment alignment, and affected the Initiating Events Cornerstone objective of limiting the likelihood of events challenging critical safety functions during shutdown operations. Inspectors assessed this finding using Phase 1 of the Shutdown Operations Significance Determination Process. Inspectors determined this finding to be of very low safety significance (Green), because while the finding represented a non-compliance with a core alteration TS, it did not increase the likelihood of a loss of reactor coolant system (RCS) inventory, it did not degrade theability to terminate a leak or add inventory to the RCS, and it did not degrade the abilityto recover decay heat removal capability if lost.Enforcement. TS 3.9.2, "Instrumentation," requires that at least two SRM channels beoperable and that at least one has an audible indication in the MCR. If this condition is not met, TS 3.9.2 requires that core alterations be immediately suspended. Contrary tothe above, on March 12, 2005, Limerick Unit 2 operators continued to perform core alterations for over nine hours following the loss of all Unit 2 SRM audible annunciators.
Because this issue is of very low safety significance and has been entered into Exelons corrective action program (IR 312046), this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000353/2006002-01, Unit 2 Core Alterations Without Audible Source Range Monitor Alarms.


Because this issue is of very low safety significance and has been entered into Exelon's corrective action program (IR 312046), this violation is being treated as an NCV,consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV05000353/2006002-01, Unit 2 Core Alterations Without Audible Source RangeMonitor Alarms.
{{a|1R15}}
{{a|1R15}}
==1R15 Operability Evaluations (71111.15 - 6 samples)==
==1R15 Operability Evaluations==
{{IP sample|IP=IP 71111.15|count=6}}


====a. Inspection Scope====
====a. Inspection Scope====
For the six operability evaluations listed below, the inspectors evaluated the technicaladequacy of the evaluations to ensure that Exelon properly justified Technical Specification operability and the subject component or system remained available suchthat no unrecognized increase in risk occurred. The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR) to verify that t he system or component remainedavailable to perform its intended function. In addition, the inspectors reviewed compensatory measures implemented to verify that the compensatory measures workedas stated and that Exelon adequately controlled these measures. The inspectors alsoreviewed a sampling of issue reports to verify that Exelon identified and corrected any deficiencies associated with operability evaluations.
For the six operability evaluations listed below, the inspectors evaluated the technical adequacy of the evaluations to ensure that Exelon properly justified Technical Specification operability and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR) to verify that the system or component remained available to perform its intended function. In addition, the inspectors reviewed compensatory measures implemented to verify that the compensatory measures worked as stated and that Exelon adequately controlled these measures. The inspectors also reviewed a sampling of issue reports to verify that Exelon identified and corrected any deficiencies associated with operability evaluations.
* Unit 1 RCIC High Turbine Oil Level (IR 436635)*HV-51-148B (RHR Heat Exchanger Bypass) Did Not Close (IR 437503)*HV-011-201H Failed Stroke Time (IR 442139)
* Unit 1 RCIC High Turbine Oil Level (IR 436635)
*Unit 1 RCIC Steam Admission Valve (HV-50-1F045) Operability due to Wiring Issue (IR 442831)*TE-041-213B Fluctuating (2B SRV) (IR 439845)
* HV-51-148B (RHR Heat Exchanger Bypass) Did Not Close (IR 437503)
*20 Station Auxiliary Bus Voltage Outside Normal Band (IR 450906)
* HV-011-201H Failed Stroke Time (IR 442139)
* Unit 1 RCIC Steam Admission Valve (HV-50-1F045) Operability due to Wiring Issue (IR 442831)
* TE-041-213B Fluctuating (2B SRV) (IR 439845)
* 20 Station Auxiliary Bus Voltage Outside Normal Band (IR 450906)


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|1R17}}
{{a|1R17}}
==1R17 Permanent Plant Modifications (71111.17 - 1 sample)==
==1R17 Permanent Plant Modifications==
{{IP sample|IP=IP 71111.17|count=1}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the engineering documentation for the Unit 1 residual heatremoval (RHR) shutdown cooling check valve modification. In addition, the inspectorsperformed a walkdown of the modification in the drywell during initial component installation and after station personnel completed the pipe and valve work. Exelon performed the modification to eliminate intermittent check valve motion with the plant at full power operation. The check valve motion has led to valve damage and degraded internal leakage in the past.* Unit 1 Residual Heat Removal Shutdown Cooling Check Valve Modification,ECR LG-05-00621
The inspectors reviewed the engineering documentation for the Unit 1 residual heat removal (RHR) shutdown cooling check valve modification. In addition, the inspectors performed a walkdown of the modification in the drywell during initial component installation and after station personnel completed the pipe and valve work. Exelon performed the modification to eliminate intermittent check valve motion with the plant at full power operation. The check valve motion has led to valve damage and degraded internal leakage in the past.
* Unit 1 Residual Heat Removal Shutdown Cooling Check Valve Modification, ECR LG-05-00621


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|1R19}}
{{a|1R19}}
==1R19 Post-Maintenance Testing (71111.19 - 6 samples)==
==1R19 Post-Maintenance Testing==
{{IP sample|IP=IP 71111.19|count=6}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the post-maintenance tests listed below to verify thatprocedures and test activities ensured system operability and functional capability. Theinspectors reviewed Exelon's test procedures to verify that the procedures adequately tested the safety function(s) that may have been affected by the maintenance activity, that the acceptance criteria in the procedure were consistent with information in theapplicable licensing basis and/or design basis documents, and that the procedure had been properly reviewed and approved. The inspectors also witnessed the test or reviewed the test data to verify that the results adequately demonstrated restoration ofthe affected safety function(s).* D11 EDG Initial Start and Parallel to the Electrical Grid After a Major Overhaul,RT-6-092-315-1*Diesel Driven Fire Pump Flow Test, ST-6-022-252-0, after Control SwitchReplacement*ADS Drywell Pressure Bypass Timer Calibration/Functional Test, ST-2-042-661,Following Relay Replacement*Unit 2 'B' Safety Relief Valve Test Following Valve Replacement, ER-AA-330-001 and ST-4-041-470-2*D13 Diesel Generator 4KV Safeguard Loss of Power and Outage Test after Bus Work, ST-6-092-117-1 10Enclosure*Testing Following Repairs on Unit 1 'D' Residual Heat Removal Pump MinimumFlow Valve
The inspectors reviewed the post-maintenance tests listed below to verify that procedures and test activities ensured system operability and functional capability. The inspectors reviewed Exelons test procedures to verify that the procedures adequately tested the safety function(s) that may have been affected by the maintenance activity, that the acceptance criteria in the procedure were consistent with information in the applicable licensing basis and/or design basis documents, and that the procedure had been properly reviewed and approved. The inspectors also witnessed the test or reviewed the test data to verify that the results adequately demonstrated restoration of the affected safety function(s).
* D11 EDG Initial Start and Parallel to the Electrical Grid After a Major Overhaul, RT-6-092-315-1
* Diesel Driven Fire Pump Flow Test, ST-6-022-252-0, after Control Switch Replacement
* ADS Drywell Pressure Bypass Timer Calibration/Functional Test, ST-2-042-661, Following Relay Replacement
* Unit 2 B Safety Relief Valve Test Following Valve Replacement, ER-AA-330-001 and ST-4-041-470-2
* D13 Diesel Generator 4KV Safeguard Loss of Power and Outage Test after Bus Work, ST-6-092-117-1
* Testing Following Repairs on Unit 1 D Residual Heat Removal Pump Minimum Flow Valve


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|1R20}}
{{a|1R20}}
==1R20 Refueling and Other Outage Activities (71111.20 - 1 sample)==
==1R20 Refueling and Other Outage Activities==
{{IP sample|IP=IP 71111.20|count=1}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the outage plan for the Unit 1 refueling outage (1R11),conducted March 6 - 24, 2006, to confirm that Exelon had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured maintenance of defense-in-depth. During therefueling outage, the inspectors observed portions of the shutdown and cooldown processes and monitored licensee controls over the outage activities listed below.*Configuration management, including maintenance of defense-in-depthcommensurate with the outage plan for key safety functions and compliance with the applicable Technical Specifications when taking equipment out-of-service.*Implementation of clearance activities and confirmation that tags were properly hungand equipment appropriately configured to safely support the work or testing.*Installation and configuration of reactor coolant pressure, level, and temperatureinstruments to provide accurate indication and instrument error accounting.*Controls over the status and configuration of electrical systems and switchyardactivities to ensure that Technical Specifications were met.*Monitoring of decay heat removal processes.
The inspectors reviewed the outage plan for the Unit 1 refueling outage (1R11),conducted March 6 - 24, 2006, to confirm that Exelon had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured maintenance of defense-in-depth. During the refueling outage, the inspectors observed portions of the shutdown and cooldown processes and monitored licensee controls over the outage activities listed below.
 
* Configuration management, including maintenance of defense-in-depth commensurate with the outage plan for key safety functions and compliance with the applicable Technical Specifications when taking equipment out-of-service.
*Controls to ensure that outage work was not impacting the ability of the operators tooperate the spent fuel pool cooling system.*Reactor water inventory controls, including flow paths, configurations, alternativemeans for inventory addition, and controls to prevent inventory loss.*Controls over activities that could affect reactivity.
* Implementation of clearance activities and confirmation that tags were properly hung and equipment appropriately configured to safely support the work or testing.
 
* Installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication and instrument error accounting.
*Maintenance of secondary containment as required by Technical Specifications.
* Controls over the status and configuration of electrical systems and switchyard activities to ensure that Technical Specifications were met.
 
* Monitoring of decay heat removal processes.
*Refueling activities, including fuel handling and sipping to detect fuel assemblyleakage.*Startup and ascension to full power operation, tracking of startup prerequisites, and walkdown of the drywell (primary containment) to verify that debris had not been left which could block emergency core cooling system suction strainers.*Identification and resolution of problems related to refueling outage activities.
* Controls to ensure that outage work was not impacting the ability of the operators to operate the spent fuel pool cooling system.
* Reactor water inventory controls, including flow paths, configurations, alternative means for inventory addition, and controls to prevent inventory loss.
* Controls over activities that could affect reactivity.
* Maintenance of secondary containment as required by Technical Specifications.
* Refueling activities, including fuel handling and sipping to detect fuel assembly leakage.
* Startup and ascension to full power operation, tracking of startup prerequisites, and walkdown of the drywell (primary containment) to verify that debris had not been left which could block emergency core cooling system suction strainers.
* Identification and resolution of problems related to refueling outage activities.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.


11Enclosure1R22Surveillance Testing (71111.22 - 6 samples)
{{a|1R22}}
==1R22 Surveillance Testing==
{{IP sample|IP=IP 71111.22|count=6}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors witnessed six surveillance tests and/or reviewed test data of selectedrisk significant structures, systems, or components (SSCs) to assess, as appropriate,whether the SSCs met the requirements of the Technical Specifications and theUFSAR. The inspectors also determined whether the testing effectively demonstrated that the SSCs were operationally ready and capable of performing their intended safety functions.
The inspectors witnessed six surveillance tests and/or reviewed test data of selected risk significant structures, systems, or components (SSCs) to assess, as appropriate, whether the SSCs met the requirements of the Technical Specifications and the UFSAR. The inspectors also determined whether the testing effectively demonstrated that the SSCs were operationally ready and capable of performing their intended safety functions.
* ST-6-012-231-0, 'A' Loop RHRSW Pump, Valve, and Flow Test*ST-6-051-233-2, 'C' RHR Pump, Valve, and Flow Test*ST-2-042-933-2, RPS and NSSSS Rx Vessel Water Level Low, Level 3, Channel 'B'Response Time Test*RT-2-056-404-2, Unit 2 HPCI Turbine Exhaust Pressure High Calibration /Functional Test*ST-6-051-231-2, 'A' RHR Pump, Valve, and Flow Test*ST-6-041-202-1, MSIV Cold Shutdown Valve Test
* ST-6-012-231-0, A Loop RHRSW Pump, Valve, and Flow Test
* ST-6-051-233-2, C RHR Pump, Valve, and Flow Test
* ST-2-042-933-2, RPS and NSSSS Rx Vessel Water Level Low, Level 3, Channel B Response Time Test
* RT-2-056-404-2, Unit 2 HPCI Turbine Exhaust Pressure High Calibration /
Functional Test
* ST-6-051-231-2, A RHR Pump, Valve, and Flow Test
* ST-6-041-202-1, MSIV Cold Shutdown Valve Test


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.
{{a|1R23}}
{{a|1R23}}
==1R23 Temporary Plant Modifications (71111.23 - 1 sample)==
==1R23 Temporary Plant Modifications==
{{IP sample|IP=IP 71111.23|count=1}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the temporary modification listed below, the associated10 CFR 50.59 screening, and compared each against the UFSAR and Technical Specifications to verify that the modification did not affect operability or availability of theaffected system. The inspectors ensured that each modification was in accordance withthe modification documents and reviewed post-installation and removal testing to verify that Exelon adequately verified the actual impact on perm anent systems by the tests.*S51.7.B, "Defeating the RHR Shutdown Cooling Auto Isolation"
The inspectors reviewed the temporary modification listed below, the associated 10 CFR 50.59 screening, and compared each against the UFSAR and Technical Specifications to verify that the modification did not affect operability or availability of the affected system. The inspectors ensured that each modification was in accordance with the modification documents and reviewed post-installation and removal testing to verify that Exelon adequately verified the actual impact on permanent systems by the tests.
* S51.7.B, Defeating the RHR Shutdown Cooling Auto Isolation


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.


12Enclosure2.RADIATION SAFETYCornerstone:Occupational Radiation Safety2OS1Access Control to Radiologically Significant Areas (71121.01 - 21 samples)
==RADIATION SAFETY==
 
===Cornerstone: Occupational Radiation Safety===
 
2OS1 Access Control to Radiologically Significant Areas (71121.01 - 21 samples)


====a. Scope====
====a. Scope====
During the periods of January 9 - 13, 2006, and March 13 - 17, 2006, the inspectorconducted the following activities to verify that Exelon implemented physical, administrative, and engineering controls for access to locked high radiation areas and other radiologically controlled areas, and that workers were adhering to these controls when working in these areas during power operations and during the Unit 1 refueling outage (1R11). The inspector reviewed implementation of these controls against the criteria contained in 10 CFR 20, applicable industry standards, and Exelon procedures.
During the periods of January 9 - 13, 2006, and March 13 - 17, 2006, the inspector conducted the following activities to verify that Exelon implemented physical, administrative, and engineering controls for access to locked high radiation areas and other radiologically controlled areas, and that workers were adhering to these controls when working in these areas during power operations and during the Unit 1 refueling outage (1R11). The inspector reviewed implementation of these controls against the criteria contained in 10 CFR 20, applicable industry standards, and Exelon procedures.
 
Completion of ten samples during the January 9 - 13 inspection period and 11 samples during the March 13 - 17 inspection period completes the annual inspection requirement of 21 samples for inspection procedure 71121.01.
 
Plant Walkdowns and Radiation Work Permit (RWP) Reviews The inspector identified exposure significant work areas in Units 1 and 2, including areas of the Reactor Buildings, Control Structure, Radwaste Building, and Turbine Building. The inspector reviewed survey maps and RWPs for these areas to determine if the associated controls were acceptable.
 
The inspector toured accessible radiological controlled areas in both Units, and with the assistance of a radiation protection technician performed independent radiation surveys of selected areas to confirm the accuracy of survey maps and the adequacy of postings.
 
In evaluating the RWPs, the inspector reviewed electronic dosimeter (ED) dose/dose rate alarm set points to determine if the set points were consistent with the survey indications and plant policy. The inspector verified that workers were knowledgeable of the actions to be taken when the ED alarms or malfunctions for tasks being conducted under selected RWPs. Work activities reviewed included radiographic examinations performed in the Unit 1 reactor building, Unit 2 reactor feed pump turbine exhaust expansion joint inspections, control room chiller maintenance, and preparing/repairing control rod drive equipment in the Unit 2 control rod drive rebuild room. Work activities reviewed during 1R11 included removal of spent filters from the suppression pool, repair of the regenerative heat exchanger end bell, installation of permanent drywell shielding, and installation of the RHR shutdown cooling check valve differential pressure modification. Additionally, the inspector reviewed dose and dose rate alarm reports to determine if the set points were appropriate for the radiological conditions experienced by the worker, and that Exelon entered the alarms into their corrective action program for further evaluation.
 
The inspector examined the airborne monitoring instrumentation, air sampling results, respiratory protection evaluations, and engineering controls for potential airborne radioactivity areas. Through review of relevant documentation, the inspector confirmed that no worker received an internal dose in excess of 50 mrem due to airborne radioactivity for 2005, including during the Unit 1 refueling outage and the Unit 2 maintenance (2M36) outage.
 
The inspector examined the physical and programmatic controls for highly activated/contaminated components stored in the spent fuel pools. The inspector verified that stored materials were properly secured.
 
Identification and Resolution of Problems The inspector reviewed elements of Exelons corrective action program related to controlling access to radiologically controlled areas and evaluating dose and dose rate alarms, completed since the last inspection of this area, to determine if problems were being entered into the program for resolution. Details of this review are contained in Section 4OA2 of this report.


Completion of ten samples during the January 9 - 13 inspection period and 11 samples during the March 13 - 17 inspection period completes the annual inspection requirement of 21 samples for inspection procedure 71121.01.Plant Walkdowns and Radiation Work Permit (RWP) ReviewsThe inspector identified exposure significant work areas in Units 1 and 2, includingareas of the Reactor Buildings, Control Structure, Radwaste Building, and Turbine Building. The inspector reviewed survey maps and RWPs for these areas to determine if the associated controls were acceptable.The inspector toured accessible radiological controlled areas in both Units, and with theassistance of a radiation protection technician performed independent radiation surveys of selected areas to confirm the accuracy of survey maps and the adequacy of postings.In evaluating the RWPs, the inspector reviewed electronic dosimeter (ED) dose/doserate alarm set points to determine if the set points were consistent with the survey indications and plant policy. The inspector verified that workers were knowledgeable of the actions to be taken when the ED alarms or malfunctions for tasks being c onductedunder selected RWPs. Work activities reviewed included radiographic examinations performed in the Unit 1 reactor building, Unit 2 reactor feed pump turbine exhaust expansion joint inspections, control room chiller maintenance, and preparing/repairingcontrol rod drive equipment in the Unit 2 control rod drive rebuild room. Work activities reviewed during 1R11 included removal of spent filters from the suppression pool, repair of the regenerative heat exchanger end bell, installation of permanent drywell shielding, and installation of the RHR shutdown cooling check valve differential pressuremodification. Additionally, the inspector reviewed dose and dose rate alarm reports to determine if the set points were appropriate for the radiological conditions experienced by the worker, and that Exelon entered the alarms into their corrective action program for further evaluation.
Jobs-In-Progress Review The inspector observed aspects of various maintenance activities being performed during the inspection periods to verify that radiological controls, such as required surveys, area postings, job coverage, locked high radiation area controls, and pre-job RWP briefings were implemented; personnel dosimetry was properly worn; and that workers were knowledgeable of work area radiological conditions. Tasks observed included control room chiller maintenance and radiographic examinations. Tasks observed during 1R11 included regenerative heat exchanger repairs, removal of suppression pool cleanup filters, and installation of permanent drywell shielding.


13EnclosureThe inspector examined the airborne monitoring instrumentation, air sampling results,respiratory protection evaluations, and engineering controls for potential airborneradioactivity areas. Through review of relevant documentation, the inspector confirmed that no worker received an internal dose in excess of 50 mrem due to airborne radioactivity for 2005, including during the Unit 1 refueling outage and the Unit 2 maintenance (2M36) outage.The inspector examined the physical and programmatic controls for highlyactivated/contaminated components stored in the spent fuel pools. The inspectorverified that stored materials were properly secured. Identification and Resolution of ProblemsThe inspector reviewed elements of Exelon's corrective action program related tocontrolling access to radiologically controlled areas and evaluating dose and dose rate alarms, completed since the last inspection of this area, to determine if problems were being entered into the program for resolution. Details of this review are contained in Section
During the January 9 - 13 inspection period, the inspector attended pre-job briefings for radiographic examinations that station personnel performed on various components located in the Unit 1 reactor building, and a Chemistry Department planning meeting regarding preparations for conducting power suppression testing. During 1R11, the inspector attended pre-job briefings for regenerative heat exchanger repairs and for removal of suppression pool filters. The inspector assessed the adequacy of information presented during these briefings and the interdepartmental coordination required in completing these tasks.
{{a|4OA2}}
 
==4OA2 of this report. Jobs-In-Progress ReviewThe inspector observed aspects of various maintenance activities being performedduring the inspection periods to verify that radiological controls, such as required==
High Risk Significant, High Dose Rate HRA, and VHRA Controls The inspector and the Radiation Protection Supervisor discussed High Dose Rate (HDR) areas and Very High Radiation Area (VHRA) controls and procedures. The inspector verified that any changes made to relevant Exelon procedures did not substantially reduce the effectiveness and level of worker protection. Controls of significant high risk areas reviewed during the inspection periods included the Unit 1 and Unit 2 drywells and Traversing Incore Probe (TIP) rooms.
 
Keys to Unit 1 and Unit 2 locked high radiation areas (LHRA) and very high radiation areas (designated A and B keys) were inventoried and 172 LHRAs were verified to be properly secured and posted during plant tours. In addition, selected Unit 1 LHRAs were verified to be properly secured and posted during plant tours during 1R11.


surveys, area postings, job coverage, locked high radiation area controls, and pre-job RWP briefings were implemented; personnel dosimetry was properly worn; and that workers were knowledgeable of work area radiological conditions. Tasks observedincluded control room chiller maintenance and radiographic examinations. Tasksobserved during 1R11 included regenerative heat exchanger repairs, removal of suppression pool cleanup filters, and installation of permanent drywell shielding. During the January 9 - 13 inspection period, the inspector attended pre-job briefings forradiographic examinations that station personnel performed on various components located in the Unit 1 reactor building, and a Chemistry Department planning meeting regarding preparations for conducting power suppression testing. During 1R11, the inspector attended pre-job briefings for regenerative heat exchanger repairs and for removal of suppression pool filters. The inspector assessed the adequacy of information presented during these briefings and the interdepartmental coordination required in completing t hese tasks.High Risk Significant, High Dose Rate HRA, and VHRA ControlsThe inspector and the Radiation Protection Supervisor discussed High Dose Rate(HDR) areas and Very High Radiation Area (VHRA) controls and procedures. Theinspector verified that any changes made to relevant Exelon procedures did not substantially reduce the effectiveness and level of worker protection. Controls of significant high risk areas reviewed during the inspection periods included the Unit 1 and Unit 2 drywells and Traversing Incore Probe (TIP) rooms.
Radiation Worker/Radiation Protection Technician Performance During both inspection periods, the inspector assessed radiation worker and radiation protection technician performance by attending a pre-job briefing for radiographic examinations and observing control point activities. Through interviews and task observations, the inspector evaluated job preparations, the degree of technician coverage for work performed in LHRAs, and the knowledge level of the technicians for specific tasks.


14EnclosureKeys to Unit 1 and Unit 2 locked high radiation areas (LHRA) and very high radiationareas (designated A and B keys) were inventoried and 172 LHRAs were verified to be properly secured and posted during plant tours. In addition, selected Unit 1 LHRAs were verified to be properly secured and posted during plant tours during 1R11.Radiation Worker/Radiation Protection Technician PerformanceDuring both inspection periods, the inspector assessed radiation worker and radiationprotection technician performance by attending a pre-job briefing for radiographic examinations and observing control point activities. Through interviews and task observations, the inspector evaluated job preparations, the degree of technician coverage for work performed in LHRAs, and the knowledge level of the technicians for specific tasks.The inspector also reviewed issue reports related to radiation worker and radiationprotection technician errors to determine if an observable pattern traceable to a similar cause was evident.
The inspector also reviewed issue reports related to radiation worker and radiation protection technician errors to determine if an observable pattern traceable to a similar cause was evident.


====b. Findings====
====b. Findings====
No findings of significance were identified.2OS2ALARA Planning and Controls (71121.02 - 6 samples)
No findings of significance were identified.
 
2OS2 ALARA Planning and Controls (71121.02 - 6 samples)


====a. Inspection Scope====
====a. Inspection Scope====
During the period March 13 - 17, 2006, the inspector conducted the following activitiesto verify that Exelon properly implemented operational, engineering, and administrative controls to maintain personnel exposure as low as is reasonably achievable (ALARA) for
During the period March 13 - 17, 2006, the inspector conducted the following activities to verify that Exelon properly implemented operational, engineering, and administrative controls to maintain personnel exposure as low as is reasonably achievable (ALARA) for tasks conducted during the Unit 1 refueling outage (1R11), and during the Unit 2 maintenance outage (2M36), which occurred February 23 - 26, 2006.
 
This inspection represents the completion of six
: (6) samples for IP 71121.02, partially completing the biennial inspection requirement of fifteen
: (15) samples.
 
Radiological Work Planning The inspector reviewed pertinent information regarding cumulative exposure history, current exposure trends, and ongoing activities to assess current performance and outage exposure challenges. The inspector determined the sites three-year rolling collective average exposure.
 
The inspector reviewed the Unit 1 refueling outage work scheduled during the inspection period and the associated work activity dose estimates. Scheduled work reviewed included regenerative heat exchanger repairs, installation of permanent shielding in the drywell, and removal/transfer of spent suppression pool filters.
 
The inspector reviewed procedures associated with maintaining worker dose ALARA and with estimating and tracking work activity specific exposures. The inspector reviewed the assumptions used in estimating outage dose, and radiation protection management briefed the inspector on recent upgrades to the access control program, in which work orders will be electronically tracked with RWPs to improve dose forecasting.
 
The inspector compared the person-hour estimates provided by maintenance planning and other work groups with actual work activity time requirements and evaluated the accuracy of these estimates. Specific jobs reviewed included installation and removal of scaffolding and shielding in the drywell, regenerative heat exchanger repairs, and main steam relief valve removal/installation.
 
The inspector reviewed the dose summary reports, detailing worker estimated and actual exposures, through March 16, 2006, for jobs performed during the 1R11 refueling outage and for the Unit 2 maintenance outage (2M36).
 
The inspector evaluated the exposure mitigation requirements specified in RWPs and ALARA Plans (AP), and compared actual worker cumulative exposure to estimated dose for tasks associated with these activities. The inspector reviewed in detail those work activities whose actual cumulative exposure approached the estimated dose, which resulted in a subsequent Work-In-Progress ALARA Review. Jobs reviewed included Install/Remove Drywell Shielding in support of 1R11, Install/Remove Drywell Scaffolding in support of 1R11, and Install/Remove Main Steam Relief Valves (MSRV) for 1R11.
 
The inspector evaluated the departmental interfaces between radiation protection, engineering, maintenance crafts, and operations to identify missing ALARA program elements and interface problems. The inspector accomplished the evaluation by interviewing the Radiological Engineering Manager and Radiation Protection Manager, reviewing station ALARA Committee meeting minutes, and attending pre-job briefings for jobs-in-progress (suppression pool spent filter removal and regenerative heat exchanger repairs).
 
The inspector determined if work activity planning included the use of temporary shielding, system flushes, hydrolazing of piping, and operational considerations to further to minimize worker exposure. The inspector examined the effectiveness of temporary and permanent shielding installed in the drywell, and pre/post dose rate data for the reactor vessel nozzle flushes.
 
Verification of Dose Estimates and Exposure Tracking Systems The inspector reviewed the assumptions and basis for the annual site collective exposure estimate and the Unit 1 refueling outage dose projection. The inspector reviewed personnel contamination reports and evaluated the need for internal dose assessments.
 
The inspector reviewed Exelons method for adjusting exposure estimates, and re-planning work, when emergent work was encountered. The inspector reviewed the Work-In-Progress ALARA reviews, ALARA Plans, and actions of the station ALARA Committee in monitoring and controlling dose allocations.
 
The inspector reviewed Exelons exposure tracking system to determine whether the level of detail, exposure report timeliness and dissemination was sufficient to support the control of collective exposures. The inspector included departmental dose compilations, highest personnel exposures to date, and individual exposure records in this review.
 
Job Site Inspection and ALARA Control The inspector observed the maintenance and operational activities being performed for drywell demobilization, regenerative heat exchanger repair, and removal of spent suppression pool filters to verify that Exelon implemented radiological controls, such as required surveys, job coverage, and contamination controls; personnel dosimetry was properly worn; and that workers were knowledgeable of work area radiological conditions.


tasks conducted during the Unit 1 refueling outage (1R11), and during the Unit 2maintenance outage (2M36), which occurred February 23 - 26, 2006.This inspection represents the completion of six
The inspector reviewed the exposure of individuals in selected work groups, including mechanical maintenance, radiation protection, and outage services to determine if supervisors were making efforts to equalize doses among the workers.
: (6) samples for IP 71121.02, partiallycompleting the biennial inspection requirement of fifteen
: (15) samples.Radiological Work PlanningThe inspector reviewed pertinent information regarding cumulative exposure history,current exposure trends, and ongoing activities to assess current performance and outage exposure challenges. The inspector determined the site's three-year rollingcollective average exposure. The inspector reviewed the Unit 1 refueling outage work scheduled during the inspectionperiod and the associated work activity dose estimates. Scheduled work reviewed included regenerative heat exchanger repairs, installation of permanent shielding in the drywell, and removal/transfer of spent suppression pool filters.


15EnclosureThe inspector reviewed procedures associated with maintaining worker dose ALARAand with estimating and tracking work activity specific exposures. The inspector reviewed the assumptions used in estimating outage dose, and radiation protection management briefed the inspector on recent upgrades to the access control program, in which work orders will be electronically tracked with RWPs to improve dose forecasting.
Source Term Reduction and Control Through data review and telephone discussions held on March 28, 2006, with the Radiation Protection Manager, the inspector evaluated the status and historical trends for the Unit 1 source term.


The inspector compared the person-hour estimates provided by maintenance planning and other work groups with actual work activity time requirements and evaluated the accuracy of these estimates. Specific jobs reviewed included installation and removal of scaffolding and shielding in the drywell, regenerative heat exchanger repairs, and main steam relief valve removal/installation. The inspector reviewed the dose summary reports, detailing worker estimated andactual exposures, through March 16, 2006, for jobs performed during the 1R11 refueling outage and for the Unit 2 maintenance outage (2M36). The inspector evaluated the exposure mitigation requirements specified in RWPs andALARA Plans (AP), and compared actual worker cumulative exposure to estimated dose for tasks associated with these activities. The inspector reviewed in detail those workactivities whose actual cumulative exposure approached the estimated dose, which resulted in a subsequent Work-In-Progress ALARA Review. Jobs reviewed included Install/Remove Drywell Shielding in support of 1R11, Install/Remove Drywell Scaffolding in support of 1R11, and Install/Remove Main Steam Relief Valves (MSRV) for 1R11.The inspector evaluated the departmental interfaces between radiation protection,engineering, maintenance crafts, and operations to identify missing ALARA program elements and interface problems. The inspector accomplished the evaluation by interviewing the Radiological Engineering Manager and Radiation Protection Manager, reviewing station ALARA Committee meeting minutes, and attending pre-job briefings for jobs-in-progress (suppression pool spent filter removal and regenerative heat exchanger repairs).The inspector determined if work activity planning included the use of temporaryshielding, system flushes, hydrolazing of piping, and operational considerations tofurther to minimize worker exposure. The inspector examined the effectiveness of temporary and permanent shielding installed in the drywell, and pre/post dose rate data for the reactor vessel nozzle flushes.Verification of Dose Estimates and Exposure Tracking SystemsThe inspector reviewed the assumptions and basis for the annual site collectiveexposure estimate and the Unit 1 refueling outage dose projection. The inspector reviewed personnel contamination reports and evaluated the need for internal dose assessments.The inspector reviewed Exelon's method for adjusting exposure estimates, andre-planning work, when emergent work was encountered. The inspector reviewed the 16EnclosureWork-In-Progress ALARA reviews, ALARA Plans, and actions of the station ALARACommittee in monitoring and controlling dose allocations. The inspector reviewed Exelon's exposure tracking system to determine whether thelevel of detail, exposure report timeliness and dissemination was sufficient to support the control of collective exposures. The inspector included departmental dose compilations, highest personnel exposures to date, and individual exposure records in this review. Job Site Inspection and ALARA ControlThe inspector observed the maintenance and operational activities being performed fordrywell demobilization, regenerative heat exchanger repair, and removal of spentsuppression pool filters to verify that Exelon implemented radiological controls, such as required surveys, job coverage, and contamination controls; personnel dosimetry was properly worn; and that workers were knowledgeable of work area radiological conditions.The inspector reviewed the exposure of individuals in selected work groups, includingmechanical maintenance, radiation protection, and outage services to determine if supervisors were making efforts to equalize doses among the workers. Source Term Reduction and ControlThrough data review and telephone discussions held on March 28, 2006, with theRadiation Protection Manager, the inspector evaluated the status and historical trends for the Unit 1 source term.Declared Pregnant WorkersThe inspector reviewed the radiological controls and dosimetry records for four declaredpregnant workers performing outage related tasks to determine if Exelon met regulatoryrequirements in controlling their exposure.Identification and Resolution of ProblemsThe inspector reviewed elements of Exelon's corrective action program related toimplementing radiological controls to determine if station personnel were entering problems into the program for resolution. Details of this review are contained in section
Declared Pregnant Workers The inspector reviewed the radiological controls and dosimetry records for four declared pregnant workers performing outage related tasks to determine if Exelon met regulatory requirements in controlling their exposure.
{{a|4OA2}}
 
==4OA2 of this report.==
Identification and Resolution of Problems The inspector reviewed elements of Exelons corrective action program related to implementing radiological controls to determine if station personnel were entering problems into the program for resolution. Details of this review are contained in section 4OA2 of this report.


====b. Findings====
====b. Findings====
No findings of significance were identified.
No findings of significance were identified.


17Enclosure4.OTHER ACTIVITIES
==OTHER ACTIVITIES==
{{a|4OA2}}
{{a|4OA2}}
==4OA2 Identification and Resolution of Problems==
==4OA2 Identification and Resolution of Problems==
{{IP sample|IP=IP 71152}}
{{IP sample|IP=IP 71152}}
.1Review of Items Entered into the Corrective Action ProgramAs required by inspection procedure 71152, "Identification and Resolution of Problems,"and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a screening of all items entered into Exelon's corrective action program. Inspectors assessed each new issue report to verify whether Exelon adequately identified the full extent of various issues, performed appropriate evaluations, and identified reasonable corrective actions..2Annual Sample: Review of Unit 2 Residual Heat Removal (RHR) Discharge HighPressure Alarms (71152 - 1 sample)
===.1 Review of Items Entered into the Corrective Action Program===
 
As required by inspection procedure 71152, Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a screening of all items entered into Exelons corrective action program. Inspectors assessed each new issue report to verify whether Exelon adequately identified the full extent of various issues, performed appropriate evaluations, and identified reasonable corrective actions.
 
===.2 Annual Sample: Review of Unit 2 Residual Heat Removal (RHR) Discharge High===
 
Pressure Alarms (71152 - 1 sample)


====a. Inspection Scope====
====a. Inspection Scope====
In January 2006, the inspectors reviewed station actions in response to multipleoccurrences of higher than normal pressure in the Unit 2 RHR system discharge pipingin 2005 and 2006. The inspectors reviewed various issue reports, operator logs, action requests, and procedures as well as performed walkdowns and interviews to determine if Exelon adequately resolved the issue. The inspectors evaluated Exelon's actions against the requirements of the corrective action program.
In January 2006, the inspectors reviewed station actions in response to multiple occurrences of higher than normal pressure in the Unit 2 RHR system discharge piping in 2005 and 2006. The inspectors reviewed various issue reports, operator logs, action requests, and procedures as well as performed walkdowns and interviews to determine if Exelon adequately resolved the issue. The inspectors evaluated Exelons actions against the requirements of the corrective action program.


====b. Findings and Observations====
====b. Findings and Observations====
No findings of significance were identified.
No findings of significance were identified.


Exelon evaluated the potential leak-by past the Low Pressure Coolant Injection (LPCI)valve (2F017), and, based on rate of pressurization, procedural guidance, and evaluation of design basis documents, correctly determined that the leak-by did notaffect the ability of the LPCI system to perform its design function, and did not exceedthe requirements for leakage past a primary containment isolation valve.In response to each of these high pressure events, operators depressurized the RHRsystem in accordance with procedure S51.4.A, "Manual Depressurization of RHR."  Thenormal RHR discharge pressure is 150 psig. The procedure directs depressurization ofthe system anytime the affected RHR loop is not in operation and loop pressure isgreater than a nominal 275 psig. At the time, this procedure directed cracking open and then closing the 18-inch RHR full-flow test motor operated valve to depressurize theRHR system. Though depressurization of this system through the full-flow test valvecan be accomplished from the control room, this may not be the most optimal method. Using a large valve to depressurize the system could result in a rapid drop in systempressure which could cause low pressure alarms and challenge the keep-fill systems. Additionally, if the valve were to fail open for any reason during depressurization, the 18Enclosurepotential exists for the affected loop to be drained to the suppression pool. This wouldresult in a loss of the LPCI function.Alternate means, which included procedures that already existed, were available todepressurize the RHR system through smaller lines, such as the one inch high pointvent valves and RHR heat exchanger sample lines. On February 23, 2006, stationpersonnel developed a temporary procedure change to S51.4.A to direct depressurization using the smaller manual valves. Exelon authorized and implemented this temporary procedure change on April 2, 2006.The inspectors reviewed the changes that Exelon made to procedure S51.4.A and foundthe changes to be acceptable..3Access Control to Radiologically Significant Areas (71121.01)
Exelon evaluated the potential leak-by past the Low Pressure Coolant Injection (LPCI)valve (2F017), and, based on rate of pressurization, procedural guidance, and evaluation of design basis documents, correctly determined that the leak-by did not affect the ability of the LPCI system to perform its design function, and did not exceed the requirements for leakage past a primary containment isolation valve.
 
In response to each of these high pressure events, operators depressurized the RHR system in accordance with procedure S51.4.A, Manual Depressurization of RHR. The normal RHR discharge pressure is 150 psig. The procedure directs depressurization of the system anytime the affected RHR loop is not in operation and loop pressure is greater than a nominal 275 psig. At the time, this procedure directed cracking open and then closing the 18-inch RHR full-flow test motor operated valve to depressurize the RHR system. Though depressurization of this system through the full-flow test valve can be accomplished from the control room, this may not be the most optimal method.
 
Using a large valve to depressurize the system could result in a rapid drop in system pressure which could cause low pressure alarms and challenge the keep-fill systems.
 
Additionally, if the valve were to fail open for any reason during depressurization, the potential exists for the affected loop to be drained to the suppression pool. This would result in a loss of the LPCI function.
 
Alternate means, which included procedures that already existed, were available to depressurize the RHR system through smaller lines, such as the one inch high point vent valves and RHR heat exchanger sample lines. On February 23, 2006, station personnel developed a temporary procedure change to S51.4.A to direct depressurization using the smaller manual valves. Exelon authorized and implemented this temporary procedure change on April 2, 2006.
 
The inspectors reviewed the changes that Exelon made to procedure S51.4.A and found the changes to be acceptable.
 
===.3 Access Control to Radiologically Significant Areas===
{{IP sample|IP=IP 71121.01}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspector reviewed 20 issue reports, recent Station ALARA Committee meetingminutes, eight Nuclear Oversight Objective Evidence Reports, and eight Nuclear Oversight Field Observation summaries, relating to controlling work activities in Unit 1 radiologically controlled areas, to evaluate Exelon's threshold for identifying, evaluating, and resolving occupational radiation safety problems. The review included a check of possible repetitive issues such as radiation worker and radiation protection technician errors.The review was conducted against the criteria contained in 10 CFR 20, TechnicalSpecifications, and Exelon procedures.
The inspector reviewed 20 issue reports, recent Station ALARA Committee meeting minutes, eight Nuclear Oversight Objective Evidence Reports, and eight Nuclear Oversight Field Observation summaries, relating to controlling work activities in Unit 1 radiologically controlled areas, to evaluate Exelons threshold for identifying, evaluating, and resolving occupational radiation safety problems. The review included a check of possible repetitive issues such as radiation worker and radiation protection technician errors.
 
The review was conducted against the criteria contained in 10 CFR 20, Technical Specifications, and Exelon procedures.


====b. Findings and Observations====
====b. Findings and Observations====
No findings of significance were identified..4ISI Finding Dispositions (71111.08)
No findings of significance were identified.
 
===.4 ISI Finding Dispositions===
{{IP sample|IP=IP 71111.08}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspector reviewed a sample of ISI related issues to verify that Exelon identified theissues at the appropriate threshold and entered them into the corrective action program.
The inspector reviewed a sample of ISI related issues to verify that Exelon identified the issues at the appropriate threshold and entered them into the corrective action program.


The inspector conducted interviews with plant personnel and reviewed issue reports and GE notification reports generated from IVVI and the core shroud inspection. The inspector verified that Exelon entered deficiencies into the corrective action program and evaluated and appropriately resolved these deficiencies within the corrective action program.
The inspector conducted interviews with plant personnel and reviewed issue reports and GE notification reports generated from IVVI and the core shroud inspection. The inspector verified that Exelon entered deficiencies into the corrective action program and evaluated and appropriately resolved these deficiencies within the corrective action program.
Line 290: Line 480:
No findings of significance were identified.
No findings of significance were identified.


19Enclosure4OA3Event Followup (71153 - 3 samples).1(Closed) LER 05000353/02-05-001, Core Alterations Performed With Source RangeMonitor Alarm Horn InoperableOn March 12, 2005, Unit 2 source range monitors (SRMs) became inoperable due to aloss of the SRM audible alarm function which resulted from an equipment problem that caused a continuous audible alarm in the main control room. Operators removed power fuses to silence the horn which in turn removed audible annunciator indication on 13 alarm panels. Exelon assigned a dedicated individual to monitor the alarm panels and alert the duty reactor operator in the event of a visual alarm on the affected panels. Core alterations were in progress during this event. Operators did not recognize that Technical Specifications (TS) requires the SRM audible alarm function to be operable anytime core alterations are in progress, resulting in operation in a condition prohibited by TS. The NRC is issuing a green non-cited violation regarding this issue in this report(Section 1R14). The inspectors did not identify any additional findings associated with this LER. Exelon documented this issue, along with completed and planned corrective actions, in IR 312046. This LER is closed..2(Closed) LER 05000352/01-05-004, Minimum Critical Power Ratio Limiting Condition forOperation Non-complianceOn September 20, 2005, a General Electric Part 21 report determined that LimerickUnit 1 exceeded the Technical Specification (TS) 3.2.3, "Minimum Critical Power Ratio,"
{{a|4OA3}}
(MCPR) limit on May 29, 2004, and on September 11, 2004. On May 29, 2004, theMCPR TS limit of 1.0 was exceeded for six hours and reached a maximum value of 1.03. On September 11, 2004, the MCPR limit was exceeded for seven hours and reached a maximum value of 1.002. There was no impact on the reactor fuel because no plant transients occurred during the periods when the MCPR ratio exceeded the TS limit of 1.0. The non-compliance was due to an error in GE's fuel test performance and final data. Exelon corrective actions included a review of Limerick Units 1 and 2 during the past two year operating cycle to determine the extent of condition and theinstallation of a new computer data bank on the core process computer for both units.
==4OA3 Event Followup==
{{IP sample|IP=IP 71153|count=3}}
 
===.1 (Closed) LER 05000353/02-05-001, Core Alterations Performed With Source Range===
 
Monitor Alarm Horn Inoperable On March 12, 2005, Unit 2 source range monitors (SRMs) became inoperable due to a loss of the SRM audible alarm function which resulted from an equipment problem that caused a continuous audible alarm in the main control room. Operators removed power fuses to silence the horn which in turn removed audible annunciator indication on 13 alarm panels. Exelon assigned a dedicated individual to monitor the alarm panels and alert the duty reactor operator in the event of a visual alarm on the affected panels.
 
Core alterations were in progress during this event. Operators did not recognize that Technical Specifications (TS) requires the SRM audible alarm function to be operable anytime core alterations are in progress, resulting in operation in a condition prohibited by TS. The NRC is issuing a green non-cited violation regarding this issue in this report (Section 1R14). The inspectors did not identify any additional findings associated with this LER. Exelon documented this issue, along with completed and planned corrective actions, in IR 312046. This LER is closed.
 
===.2 (Closed) LER 05000352/01-05-004, Minimum Critical Power Ratio Limiting Condition for===
 
Operation Non-compliance On September 20, 2005, a General Electric Part 21 report determined that Limerick Unit 1 exceeded the Technical Specification (TS) 3.2.3, Minimum Critical Power Ratio, (MCPR) limit on May 29, 2004, and on September 11, 2004. On May 29, 2004, the MCPR TS limit of 1.0 was exceeded for six hours and reached a maximum value of 1.03. On September 11, 2004, the MCPR limit was exceeded for seven hours and reached a maximum value of 1.002. There was no impact on the reactor fuel because no plant transients occurred during the periods when the MCPR ratio exceeded the TS limit of 1.0. The non-compliance was due to an error in GEs fuel test performance and final data. Exelon corrective actions included a review of Limerick Units 1 and 2 during the past two year operating cycle to determine the extent of condition and the installation of a new computer data bank on the core process computer for both units.
 
The new computer data bank has been installed at Unit 1 and will be installed at Unit 2 prior to reaching a condition where the MCPR limit would present a concern.
 
This finding is more than minor because it had a credible impact on safety, in that a minimum critical power ratio (MCPR) value greater than the TS limit could result in fuel cladding degradation. The finding affects the Barrier Integrity Cornerstone and was considered to have very low safety significance (Green) using Appendix A of the Significance Determination Process (SDP) because no plant transients occurred during the periods when the MCPR ratio exceeded the TS limit and there was no fuel degradation. This licensee-identified finding involved a violation of TS 3.2.3, Minimum Critical Power Ratio. The enforcement aspects of the violation are discussed in Section 4OA7. This LER is closed.
 
===.3 (Closed) LER 05000353/02-05-004, Reactor Scram Due to EHC Malfunction===
 
On October 12, 2005, Unit 2 reactor scrammed from 100% reactor power due to problems with the main turbine electrohydraulic control (EHC) system. The plant responded as designed with the exception of the main turbine EHC malfunction. The EHC failure was due to faulty electrical circuit cards. Exelon replaced four EHC circuit cards and tested the cards satisfactorily. The inspectors reviewed this LER and identified no findings of significance and no violation of NRC requirements. Exelon documented this issue, along with completed and planned corrective actions, in IR 385399. This LER is closed.
 
{{a|4OA6}}
==4OA6 Meetings, Including Exit==
 
Exit Meetings On April 11, 2006, the resident inspectors presented the inspection results to Mr. DeGregorio and other members of his staff, who acknowledged the findings.
 
The inspectors confirmed that proprietary information was not provided or examined during the inspection.


The new computer data bank has been installed at Unit 1 and will be installed at Unit 2prior to reaching a condition where the MCPR limit would present a concern.This finding is more than minor because it had a credible impact on safety, in that aminimum critical power ratio (MCPR) value greater than the TS limit could result in fuel cladding degradation. The finding affects the Barrier Integrity Cornerstone and was considered to have very low safety significance (Green) using Appendix A of the Significance Determination Process (SDP) because no plant transients occurred during the periods when the MCPR ratio exceeded the TS limit and there was no fuel degradation. This licensee-identified finding involved a violation of TS 3.2.3, "MinimumCritical Power Ratio". The enforcement aspects of the violation are discussed in Section 4OA7. This LER is closed.
{{a|4OA7}}
==4OA7 Licensee-Identified Violations==


20Enclosure.3(Closed) LER  05000353/02-05-004, Reactor Scram Due to EHC MalfunctionOn October 12, 2005, Unit 2 reactor scrammed from 100% reactor power due toproblems with the main turbine electrohydraulic control (EHC) system. The plant responded as designed with the exception of the main turbine EHC malfunction. The EHC failure was due to faulty electrical circuit cards. Exelon replaced four EHC circuit cards and tested the cards satisfactorily. The inspectors reviewed this LER and identified no findings of significance and no violation of NRC requirements. Exelondocumented this issue, along with completed and planned corrective actions, in IR 385399. This LER is closed.4OA6Meetings, Including ExitExit MeetingsOn April 11, 2006, the resident inspectors presented the inspection results toMr. DeGregorio and other members of his staff, who acknowledged the findings.
The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.
* Technical Specification (TS) 3.2.3, Minimum Critical Power Ratio (MCPR) requires that the MCPR value remain less than one. Contrary to this, Limerick Unit 1 exceeded the MCPR limit on May 29, 2004, and on September 11, 2004. On May 29, 2004, the MCPR TS limit of 1.0 was exceeded for six hours and reached a maximum value of 1.03. On September 11, 2004, the MCPR limit was exceeded for seven hours and reached a maximum value of 1.002. This finding is of very low safety significance because no plant transients occurred during the periods when the MCPR ratio exceeded the TS limit and there was no fuel degradation. Exelon documented this issue, along with completed and planned corrective actions, in IR 352899.


The inspectors confirmed that proprietary information was not provided or examined during the inspection. 4OA7Licensee-Identified ViolationsThe following violation of very low safety significance (Green) was identified by thelicensee and is a violation of NRC requirements which meet the criteria of Section VI ofthe NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.*Technical Specification (TS) 3.2.3, "Minimum Critical Power Ratio" (MCPR) requiresthat the MCPR value remain less than one. Contrary to this, Limerick Unit 1 exceeded the MCPR limit on May 29, 2004, and on September 11, 2004. On May 29, 2004, the MCPR TS limit of 1.0 was exceeded for six hours and reached a maximum value of 1.03. On September 11, 2004, the MCPR limit was exceeded for seven hours and reached a maximum value of 1.002. This finding is of very low safety significance because no plant transients occurred during the periods when the MCPR ratio exceeded the TS limit and there was no fuel degradation. Exelon documented this issue, along with completed and planned corrective actions, in IR 352899.ATTACHMENT:  
ATTACHMENT:  


=SUPPLEMENTAL INFORMATION=
=SUPPLEMENTAL INFORMATION=


==KEY POINTS OF CONTACT==
==KEY POINTS OF CONTACT==
Exelon Generation Company
Exelon Generation Company
: [[contact::R. DeGregorio]], Site Vice President
: [[contact::R. DeGregorio]], Site Vice President
Line 309: Line 528:
: [[contact::E. Kelly]], Engineering Programs Manager
: [[contact::E. Kelly]], Engineering Programs Manager
: [[contact::W. Astbury]], ESW System Manager
: [[contact::W. Astbury]], ESW System Manager
: [[contact::J. George]], RHR System M
: [[contact::J. George]], RHR System Manager
anager
: [[contact::W. Tracey]], SRV System Manager
: [[contact::W. Tracey]], SRV System Manager
: [[contact::F. Burzynski]], Station Fire Marshall
: [[contact::F. Burzynski]], Station Fire Marshall
: [[contact::M. Kowalski]], Maintenance Rule Coordinator
: [[contact::M. Kowalski]], Maintenance Rule Coordinator
: [[contact::P. Tarpinian]], PRA Engineer
: [[contact::P. Tarpinian]], PRA Engineer
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
Opened and  
 
===Opened and Closed===
: 05000353/2006002-01          NCV          Unit 2 Core Alterations Without Audible Source Range Monitor Alarms
 
===Closed===
===Closed===
05000353/2006002-01NCVUnit 2 Core Alterations Without Audible SourceRange Monitor AlarmsClosed05000353/02-05-001LERCore Alterations Performed With Source RangeMonitor Alarm Horn Inoperable05000352/01-05-004LERMinimum Critical Power Ratio Limiting Condition forOperation Non-compliance05000353/02-05-004LERReactor Scram Due to EHC Malfunction
: 05000353/02-05-001          LER          Core Alterations Performed With Source Range Monitor Alarm Horn Inoperable
: 05000352/01-05-004          LER          Minimum Critical Power Ratio Limiting Condition for Operation Non-compliance
: 05000353/02-05-004          LER          Reactor Scram Due to EHC Malfunction
 
==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
Section 1R01: Adverse Weather ProtectionIssue Reports and Action RequestsIR
 
: 431810, "Heat Trace Alarm"IR
: 432034, "10-C183 Heat Trace Panel Trouble"
}}
}}

Revision as of 19:17, 23 November 2019

IR 05000352-06-002 and 05000353-06-002; 01/01/2006 - 03/31/2006; Limerick Generating Station, Units 1 and 2; Operator Performance During Non-Routine Plant Evolutions and Events
ML061220007
Person / Time
Site: Limerick  Constellation icon.png
Issue date: 05/01/2006
From: James Trapp
Reactor Projects Region 1 Branch 4
To: Crane C
Exelon Generation Co, Exelon Nuclear
References
IR-06-002
Download: ML061220007 (37)


Text

SUBJECT:

LIMERICK GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000352/2006002 AND 05000353/2006002

Dear Mr. Crane:

On March 31, 2006, the United States Nuclear Regulatory Commission (NRC) completed an inspection at your Limerick Generating Station Units 1 and 2. The enclosed integrated report documents the inspection results which were discussed on April 11, 2006, with Mr. R. DeGregorio and other members of your staff.

This inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

This report documents one self-revealing finding of very low safety significance (Green). This finding was determined to involve a violation of an NRC requirement. Additionally, a licensee-identified violation which was determined to be of very low safety significance is listed in this report. However, because of the very low safety significance, and because it is entered into your corrective action program, the NRC is treating this finding as a non-cited violations (NCV),

in accordance with Section VI.A.1 of the NRCs Enforcement Policy. If you contest the NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001; with copies to the Regional Administrator Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Limerick facility.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

James M. Trapp, Chief Projects Branch 4 Division of Reactor Projects Docket Nos: 50-352; 50-353 License Nos: NPF-39; NPF-85 Enclosure: Inspection Report 05000352/2006002 and 05000353/2006002 w/Attachment: Supplemental Information cc w/encl:

Chief Operating Officer, Exelon Generation Company, LLC Site Vice President - Limerick Generating Station Plant Manager, Limerick Generating Station Regulatory Assurance Manager - Limerick Senior Vice President - Nuclear Services Vice President - Mid-Atlantic Operations Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Director - Licensing and Regulatory Affairs, Exelon Generation Company, LLC Manager, Licensing - Limerick Generating Station Vice President, General Counsel and Secretary Associate General Counsel, Exelon Generation Company Correspondence Control Desk J. Johnsrud, National Energy Committee Chairman, Board of Supervisors of Limerick Township R. Janati, Chief, Division of Nuclear Safety, Pennsylvania Bureau of Radiation Protection J. Bradley Fewell, Assistant General Counsel, Exelon Nuclear D. Allard, Director, Dept. of Environmental Protection, Bureau of Radiation Protection (SLO)

SUMMARY OF FINDINGS

IR 05000352/2006-002, 05000353/2006-002; 01/01/2006 - 03/31/2006; Limerick Generating

Station, Units 1 and 2; Operator Performance During Non-Routine Plant Evolutions and Events.

The report covered a 3-month period of inspection by resident inspectors and announced inspections by a regional health physicist inspector and a reactor inspector. The inspectors identified one Green non-cited violation (NCV). The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649,

Reactor Oversight Process, Revision 3, dated July 2000.

Reactor Safety

NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

Green.

A self-revealing NCV was identified for the licensees failure to comply with Technical Specification (TS) 3.9.2, Instrumentation. Plant operations staff inappropriately started core alterations after the loss of all Unit 2 source range monitor audible alarms. Core alterations were stopped when Exelon management was informed of the problem. The source range monitor audible alarm was fixed prior to moving fuel in the reactor and this issue was entered into Exelon's corrective action program.

This finding is greater than minor because it affected the Initiating Events cornerstone objective of limiting the likelihood of those events that challenge critical safety functions during shutdown conditions. This finding is of very low safety significance because it did not increase the likelihood of a loss of reactor coolant system inventory, it did not degrade the ability to terminate a leak or add inventory to the reactor coolant system, and it did not degrade the ability to recover decay heat removal capability if lost.

(Section 1R14)

Licensee-Identified Violations

Violations of very low safety significance, which were identified by the licensee have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. One licensee identified violation and associated corrective actions are listed in Section 4OA7 of this report.

iii

REPORT DETAILS

Summary of Plant Status

Unit 1 began this inspection period at full rated thermal power and operated at full power until January 13, 2006, when operators decreased power to approximately 70 percent for power suppression testing. Unit 1 returned to full power on January 17. On February 7, 2006, Unit 1 entered reactor power end-of-cycle coastdown. On March 6, operators shutdown Unit 1 for a planned refueling and maintenance outage (1R11). The reactor achieved criticality on March 23, and following repairs to the 1C reactor feed pump, Unit 1 returned to full rated thermal power on March 28, 2006.

Unit 2 began this inspection period at full rated thermal power. Unit 2 shut down on February 23, 2006 for a planned maintenance outage to replace three safety relief valves (SRVs.) Unit 2 returned to full rated thermal power on February 26, 2006 and operated at or near full rated thermal power for the rest of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

a. Inspection Scope

Since snow storms were forecasted in the vicinity of the facility for early February 2006, the inspectors reviewed Exelons overall preparations and protection for the expected weather conditions. The inspectors walked down portions of procedure SE-14, Snow, including applicable portions of the emergency diesel generators and the condensate storage tank system. The inspectors also reviewed various related issue reports (IRs)and action requests (ARs). This inspection satisfied one inspection sample for overall preparations and protection for expected adverse weather conditions. Documents reviewed for each applicable section of this report are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

.1 Partial Walkdown

a. Inspection Scope

The inspectors performed a partial walkdown of the following three systems to verify the operability of redundant or diverse trains and components when safety equipment was inoperable. The inspectors attempted to identify any discrepancies that could impact the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, walked down control systems components, and verified that selected breakers, valves, and support equipment were in the correct position to support system operation. The inspectors also verified that Exelon had properly identified and resolved equipment mitigation problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program.

  • Unit 1 Reactor Recirculation System Following Refueling Outage

.2 Complete System Walkdown

a. Inspection Scope

The inspectors conducted one complete walkdown of the Unit 2 residual heat removal (RHR) system to verify the functional capability of the system. The inspectors used Exelon procedures and other documents listed in the Attachment to verify proper system alignment. The inspectors also verified electrical power requirements, operator workarounds, hangers and support installation, and associated support systems status.

The walkdown also included evaluation of the system piping and supports against the following considerations:

  • Oil reservoirs appeared normal
  • Snubbers did not appear to be leaking hydraulic fluid
  • Hangers were functional
  • Component foundations were not degraded The inspectors performed a review of outstanding issue reports, action requests, and work orders to ensure that the deficiencies did not affect RHR design function and to verify that Exelon was appropriately identifying and resolving any equipment alignment problems.

c. Findings

No findings of significance were identified.

1R05 Fire Protection

.1 Fire Protection - Tours

a. Inspection Scope

The inspectors conducted a tour of the areas listed below to assess the material condition and operational status of fire protection features. The inspectors verified that combustibles and ignition sources were controlled in accordance with Exelons administrative procedures, fire detection and suppression equipment was available for use, and that passive fire barriers were maintained in good material condition. The inspectors also verified that station personnel implemented compensatory measures for out-of-service, degraded, or inoperable fire protection equipment in accordance with Exelons fire plan.

  • Unit 1 Refuel Floor During New Reactor Fuel Inspections
  • Unit 1 Elevation 253' During Refuel Outage Preparations
  • D11 EDG Room During Maintenance Overhaul
  • Unit 1 Elevation 269' During Refuel Outage Preparations
  • Unit 2 Elevation 269' During Unit 1 Refuel Outage Preparations
  • Unit 1 Refuel Floor During Reactor Vessel Head Removal
  • Unit 2 Elevations 177' and 201' During Unit 1 Refuel Outage
  • Unit 2 Elevations 217' and 253' During Unit 1 Refuel Outage

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance

a. Inspection Scope

The inspectors observed portions of Exelons 1A residual heat removal (RHR) heat exchanger transfer test to ensure the heat exchanger could perform its design function.

The inspectors observed the heat transfer test from the main control room and locally in the Reactor Building. The inspectors reviewed Exelons final heat exchanger test data to ensure the as-found heat transfer values were within design limits. The inspectors also walked down the 1A RHR heat exchanger to assess its material condition.

b. Findings

No findings of significance were identified.

1R08 Inservice Inspection Activities

a. Inspection Scope

Inspectors selected a sample of non-destructive examination (NDE) activities for review from the Unit 1 refueling outage (RFO) 11 examination plan to assess the effectiveness of the inservice inspection (ISI) program for monitoring degradation of containment, the reactor coolant system (RCS), and risk-significant piping system pressure boundaries.

The inspection consisted of interviews with plant personnel, observations of nondestructive examinations and calibrations of nondestructive equipment, and review of procedures, examination results, calibration documentation, and qualification certifications. The inspector verified that Exelon performed these activities in accordance with the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code requirements.

The inspector reviewed the modification package for the replacement of the 16 inch B loop RHR containment spray outboard isolation valve to verify that the design basis and performance of the valve was not degraded as a result of the modification. The inspector verified that Exelon performed the radiography of the pipe to elbow weld FW 1301, the pipe to valve weld FW 5, and the pipe to valve weld SW 6 in accordance with the ASME Boiler and Pressure Vessel Code and that the welds met the ASME Code acceptance criteria. The inspector verified the welding procedure and the welder qualifications met the requirements of the ASME Code.

The inspector observed and reviewed several visual examinations associated with the in-vessel visual inspection (IVVI) including jet pump set screw tack welds, wedge wear, restrainer bracket adjustment screw gap measurement, riser pipe to riser brace circumferential weld, and core spray A loop shroud pipe to collar weld, P8aC. The inspector verified the camera calibration and examination met the ASME requirements for VT-1 visual examinations.

The inspector observed portions of the magnetic particle inspection of the reactor vessel skirt weld in order to evaluate examiner skill and examination technique. The inspector verified the calibration of the AC electromagnetic yoke, that the examiner was properly qualified, and that the examination procedure was followed. Examination results were reviewed for recordable indications.

The inspector observed a portion of the ultrasonic examination of 4 inch RCIC welds DBA-107-1FW54 (RC012) and DBA-107-1FW4 (RC013) in order to evaluate examiner skill, test equipment performance, and examination environment (condition of weld surface). The inspector verified the calibration and examination were performed in accordance with approved procedures and that the examiners were properly qualified.

The inspector reviewed the exam reports for recordable indications.

The inspector verified the scope of the ultrasonic examination of the core shroud welds was in accordance with the guidance from the Electric Power Research Institute (EPRI)

Boiling Water Reactor Vessel Inspection Program 76 (BWRVIP-76). The data from the ultrasonic examination of the horizontal welds H-3, H-4, H-5 and vertical welds V-15, V-16, V-17, and V-18 of the core shroud was reviewed for recordable indications.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

Resident Inspector Quarterly Review

a. Inspection Scope

On January 30, 2006, the inspectors observed a medium pipe break loss of coolant accident (LOCA) simulator scenario to assess licensed operator performance and the evaluators critique. The simulator evaluation was performed during the licensed operator annual examination. The inspectors discussed the results with operators, operations management, and training instructors.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed the two samples listed below for items such as:

(1) appropriate work practices;
(2) identifying and addressing common cause failures;
(3) scoping in accordance with 10 CFR 50.65(b) of the maintenance rule (MR);
(4) characterizing reliability issues for performance;
(5) trending key parameters for condition monitoring;
(6) charging unavailability for performance;
(7) classification and reclassification in accordance with 10 CFR 50.65 (a)(1) or (a)(2); and
(8) appropriateness of performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2)and/or appropriateness and adequacy of goals and corrective actions for SSCs/functions classified as (a)(1). Items reviewed included the following:

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the following seven activities to verify that Exelon performed the appropriate risk assessments prior to removing equipment for work. The inspectors verified that Exelon performed accurate and complete risk assessments as required by 10 CFR 50.65 (a)(4). When the station performed emergent work, the inspectors verified that the plant risk was promptly reassessed and managed in accordance with Exelons risk assessment tool and risk categories.

  • 101 Transformer Tap Changer Failed to Tap Following Modification
  • Unit 1 Risk During D11 EDG Planned Maintenance Concurrent with Maintenance on HPCI/RCIC Full-Flow Test Valve
  • Unit 1 RCIC Turbine Oil Contained Bearing Material (IR 463640)
  • HV-049-1F007 Failed to Close (A1554514)
  • High Unit 1 Reactor Conductivity and Chlorides During Start-Up from 1R11 Refueling Outage

b. Findings

No findings of significance were identified.

1R14 Operator Performance During Non-Routine Evolutions and Events (71111.14 -

2 samples)

a. Inspection Scope

For the non-routine events described below, the inspectors reviewed operator logs, plant computer data, and other documentation to determine what occurred and how the operators responded, and to determine if the response was in accordance with plant procedures.

  • On March 12, 2005, the inspectors reviewed operator and station response to the loss of an alarm horn supplying audible indication for a number of Unit 2 main control room (MCR) alarms. The inspectors reviewed the applicable Technical Specification (TS) requirements, off-normal operating procedures, and Limericks Emergency Plan. The inspectors also conducted interviews with operators and supervisors. An NRC followup review of this issue was performed prior to final documentation.
  • On February 22, 2006, the inspectors observed a reactor shutdown on Unit 2 in preparation for a short-duration maintenance outage to replace three leaking safety relief valves (SRVs). The inspectors observed operator actions in the control room, reviewed logs and outage work schedules, and monitored portions of the subsequent start-up and return to full power.

b. Findings

Introduction.

A Green self-revealing non-cited violation (NCV) was identified of TS 3.9.2, Instrumentation, because Limerick started core alterations after the loss of all Unit 2 source range monitor (SRM) audible alarms.

Description.

On the morning of March 12, 2005, while performing an annunciator check in the MCR, the horn for several MCR panels sounded continuously and could not be reset. At the time, Limerick Unit 2 was shutdown for a planned refueling outage. The control room operators entered procedure ON-122, Loss of Main Control Room Annunciators, and removed power to the alarming horn. The disabled horn provided the audible alarms for the SRMs, among others. As a compensatory measure, a dedicated operator was stationed in the MCR to monitor the panels without audible alarms.

Limerick TS 3.9.2 requires that at least two SRM channels be operable and inserted to the normal operating level with audible alarm indication available for at least one SRM.

If these conditions are not met, TS 3.9.2 requires that core alterations be suspended.

At the time the alarm function of the SRMs was lost, fuel bundle movement in the reactor core was not in progress at Unit 2. However, at 12:11 p.m. on March 12, following consultation with the Outage Control Center (OCC), Limerick shift management authorized fuel movements to commence. While corrective actions for the failed alarm function were being planned, the horn was still inoperable at that time.

Fuel movement continued until 8:58 p.m., when a supervisor on the night shift recognized that a violation of TS 3.9.2 may have occurred. The Shift Manager ordered fuel movements to be suspended and informed the OCC and Limerick senior management. The Shift Manager, Shift Operations Superintendent, and Control Room Supervisor then made the decision that the compensatory measures in place for the inoperable horn were adequate to meet the intent of the TS, and at 9:11 p.m., the station recommenced fuel movement. Operations did not coordinate this decision through the OCC. When the OCC learned that fuel movement had been resumed without the audible SRM alarm function, they notified the Operations Director, and he ordered fuel movements stopped at 9:39 p.m. Station personnel repaired the SRM audible alarm prior to moving additional fuel bundles.

Analysis.

The inspectors determined that Exelons non-compliance with the requirements of TS 3.9.2 is a performance deficiency. Additionally, once the non-compliance was identified, Limerick operations staff incorrectly determined that compensatory measures could be used to meet the TS 3.9.2 requirements, and subsequently recommenced fuel moves. Traditional enforcement does not apply because the issue did not have any actual safety consequences or potential for impacting the NRCs regulatory function, and was not the result of any willful violation of NRC requirements or Exelon procedures.

This finding is greater than minor because it was associated with the Configuration Control attribute of shutdown equipment alignment, and affected the Initiating Events Cornerstone objective of limiting the likelihood of events challenging critical safety functions during shutdown operations. Inspectors assessed this finding using Phase 1 of the Shutdown Operations Significance Determination Process. Inspectors determined this finding to be of very low safety significance (Green), because while the finding represented a non-compliance with a core alteration TS, it did not increase the likelihood of a loss of reactor coolant system (RCS) inventory, it did not degrade the ability to terminate a leak or add inventory to the RCS, and it did not degrade the ability to recover decay heat removal capability if lost.

Enforcement.

TS 3.9.2, Instrumentation, requires that at least two SRM channels be operable and that at least one has an audible indication in the MCR. If this condition is not met, TS 3.9.2 requires that core alterations be immediately suspended. Contrary to the above, on March 12, 2005, Limerick Unit 2 operators continued to perform core alterations for over nine hours following the loss of all Unit 2 SRM audible annunciators.

Because this issue is of very low safety significance and has been entered into Exelons corrective action program (IR 312046), this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000353/2006002-01, Unit 2 Core Alterations Without Audible Source Range Monitor Alarms.

1R15 Operability Evaluations

a. Inspection Scope

For the six operability evaluations listed below, the inspectors evaluated the technical adequacy of the evaluations to ensure that Exelon properly justified Technical Specification operability and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR) to verify that the system or component remained available to perform its intended function. In addition, the inspectors reviewed compensatory measures implemented to verify that the compensatory measures worked as stated and that Exelon adequately controlled these measures. The inspectors also reviewed a sampling of issue reports to verify that Exelon identified and corrected any deficiencies associated with operability evaluations.

  • Unit 1 RCIC High Turbine Oil Level (IR 436635)
  • HV-51-148B (RHR Heat Exchanger Bypass) Did Not Close (IR 437503)
  • Unit 1 RCIC Steam Admission Valve (HV-50-1F045) Operability due to Wiring Issue (IR 442831)
  • TE-041-213B Fluctuating (2B SRV) (IR 439845)
  • 20 Station Auxiliary Bus Voltage Outside Normal Band (IR 450906)

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications

a. Inspection Scope

The inspectors reviewed the engineering documentation for the Unit 1 residual heat removal (RHR) shutdown cooling check valve modification. In addition, the inspectors performed a walkdown of the modification in the drywell during initial component installation and after station personnel completed the pipe and valve work. Exelon performed the modification to eliminate intermittent check valve motion with the plant at full power operation. The check valve motion has led to valve damage and degraded internal leakage in the past.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the post-maintenance tests listed below to verify that procedures and test activities ensured system operability and functional capability. The inspectors reviewed Exelons test procedures to verify that the procedures adequately tested the safety function(s) that may have been affected by the maintenance activity, that the acceptance criteria in the procedure were consistent with information in the applicable licensing basis and/or design basis documents, and that the procedure had been properly reviewed and approved. The inspectors also witnessed the test or reviewed the test data to verify that the results adequately demonstrated restoration of the affected safety function(s).

  • D11 EDG Initial Start and Parallel to the Electrical Grid After a Major Overhaul, RT-6-092-315-1
  • Diesel Driven Fire Pump Flow Test, ST-6-022-252-0, after Control Switch Replacement
  • ADS Drywell Pressure Bypass Timer Calibration/Functional Test, ST-2-042-661, Following Relay Replacement
  • D13 Diesel Generator 4KV Safeguard Loss of Power and Outage Test after Bus Work, ST-6-092-117-1

b. Findings

No findings of significance were identified.

1R20 Refueling and Other Outage Activities

a. Inspection Scope

The inspectors reviewed the outage plan for the Unit 1 refueling outage (1R11),conducted March 6 - 24, 2006, to confirm that Exelon had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured maintenance of defense-in-depth. During the refueling outage, the inspectors observed portions of the shutdown and cooldown processes and monitored licensee controls over the outage activities listed below.

  • Configuration management, including maintenance of defense-in-depth commensurate with the outage plan for key safety functions and compliance with the applicable Technical Specifications when taking equipment out-of-service.
  • Implementation of clearance activities and confirmation that tags were properly hung and equipment appropriately configured to safely support the work or testing.
  • Installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication and instrument error accounting.
  • Controls over the status and configuration of electrical systems and switchyard activities to ensure that Technical Specifications were met.
  • Controls to ensure that outage work was not impacting the ability of the operators to operate the spent fuel pool cooling system.
  • Reactor water inventory controls, including flow paths, configurations, alternative means for inventory addition, and controls to prevent inventory loss.
  • Controls over activities that could affect reactivity.
  • Refueling activities, including fuel handling and sipping to detect fuel assembly leakage.
  • Identification and resolution of problems related to refueling outage activities.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors witnessed six surveillance tests and/or reviewed test data of selected risk significant structures, systems, or components (SSCs) to assess, as appropriate, whether the SSCs met the requirements of the Technical Specifications and the UFSAR. The inspectors also determined whether the testing effectively demonstrated that the SSCs were operationally ready and capable of performing their intended safety functions.

  • ST-2-042-933-2, RPS and NSSSS Rx Vessel Water Level Low, Level 3, Channel B Response Time Test

Functional Test

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed the temporary modification listed below, the associated 10 CFR 50.59 screening, and compared each against the UFSAR and Technical Specifications to verify that the modification did not affect operability or availability of the affected system. The inspectors ensured that each modification was in accordance with the modification documents and reviewed post-installation and removal testing to verify that Exelon adequately verified the actual impact on permanent systems by the tests.

b. Findings

No findings of significance were identified.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01 - 21 samples)

a. Scope

During the periods of January 9 - 13, 2006, and March 13 - 17, 2006, the inspector conducted the following activities to verify that Exelon implemented physical, administrative, and engineering controls for access to locked high radiation areas and other radiologically controlled areas, and that workers were adhering to these controls when working in these areas during power operations and during the Unit 1 refueling outage (1R11). The inspector reviewed implementation of these controls against the criteria contained in 10 CFR 20, applicable industry standards, and Exelon procedures.

Completion of ten samples during the January 9 - 13 inspection period and 11 samples during the March 13 - 17 inspection period completes the annual inspection requirement of 21 samples for inspection procedure 71121.01.

Plant Walkdowns and Radiation Work Permit (RWP) Reviews The inspector identified exposure significant work areas in Units 1 and 2, including areas of the Reactor Buildings, Control Structure, Radwaste Building, and Turbine Building. The inspector reviewed survey maps and RWPs for these areas to determine if the associated controls were acceptable.

The inspector toured accessible radiological controlled areas in both Units, and with the assistance of a radiation protection technician performed independent radiation surveys of selected areas to confirm the accuracy of survey maps and the adequacy of postings.

In evaluating the RWPs, the inspector reviewed electronic dosimeter (ED) dose/dose rate alarm set points to determine if the set points were consistent with the survey indications and plant policy. The inspector verified that workers were knowledgeable of the actions to be taken when the ED alarms or malfunctions for tasks being conducted under selected RWPs. Work activities reviewed included radiographic examinations performed in the Unit 1 reactor building, Unit 2 reactor feed pump turbine exhaust expansion joint inspections, control room chiller maintenance, and preparing/repairing control rod drive equipment in the Unit 2 control rod drive rebuild room. Work activities reviewed during 1R11 included removal of spent filters from the suppression pool, repair of the regenerative heat exchanger end bell, installation of permanent drywell shielding, and installation of the RHR shutdown cooling check valve differential pressure modification. Additionally, the inspector reviewed dose and dose rate alarm reports to determine if the set points were appropriate for the radiological conditions experienced by the worker, and that Exelon entered the alarms into their corrective action program for further evaluation.

The inspector examined the airborne monitoring instrumentation, air sampling results, respiratory protection evaluations, and engineering controls for potential airborne radioactivity areas. Through review of relevant documentation, the inspector confirmed that no worker received an internal dose in excess of 50 mrem due to airborne radioactivity for 2005, including during the Unit 1 refueling outage and the Unit 2 maintenance (2M36) outage.

The inspector examined the physical and programmatic controls for highly activated/contaminated components stored in the spent fuel pools. The inspector verified that stored materials were properly secured.

Identification and Resolution of Problems The inspector reviewed elements of Exelons corrective action program related to controlling access to radiologically controlled areas and evaluating dose and dose rate alarms, completed since the last inspection of this area, to determine if problems were being entered into the program for resolution. Details of this review are contained in Section 4OA2 of this report.

Jobs-In-Progress Review The inspector observed aspects of various maintenance activities being performed during the inspection periods to verify that radiological controls, such as required surveys, area postings, job coverage, locked high radiation area controls, and pre-job RWP briefings were implemented; personnel dosimetry was properly worn; and that workers were knowledgeable of work area radiological conditions. Tasks observed included control room chiller maintenance and radiographic examinations. Tasks observed during 1R11 included regenerative heat exchanger repairs, removal of suppression pool cleanup filters, and installation of permanent drywell shielding.

During the January 9 - 13 inspection period, the inspector attended pre-job briefings for radiographic examinations that station personnel performed on various components located in the Unit 1 reactor building, and a Chemistry Department planning meeting regarding preparations for conducting power suppression testing. During 1R11, the inspector attended pre-job briefings for regenerative heat exchanger repairs and for removal of suppression pool filters. The inspector assessed the adequacy of information presented during these briefings and the interdepartmental coordination required in completing these tasks.

High Risk Significant, High Dose Rate HRA, and VHRA Controls The inspector and the Radiation Protection Supervisor discussed High Dose Rate (HDR) areas and Very High Radiation Area (VHRA) controls and procedures. The inspector verified that any changes made to relevant Exelon procedures did not substantially reduce the effectiveness and level of worker protection. Controls of significant high risk areas reviewed during the inspection periods included the Unit 1 and Unit 2 drywells and Traversing Incore Probe (TIP) rooms.

Keys to Unit 1 and Unit 2 locked high radiation areas (LHRA) and very high radiation areas (designated A and B keys) were inventoried and 172 LHRAs were verified to be properly secured and posted during plant tours. In addition, selected Unit 1 LHRAs were verified to be properly secured and posted during plant tours during 1R11.

Radiation Worker/Radiation Protection Technician Performance During both inspection periods, the inspector assessed radiation worker and radiation protection technician performance by attending a pre-job briefing for radiographic examinations and observing control point activities. Through interviews and task observations, the inspector evaluated job preparations, the degree of technician coverage for work performed in LHRAs, and the knowledge level of the technicians for specific tasks.

The inspector also reviewed issue reports related to radiation worker and radiation protection technician errors to determine if an observable pattern traceable to a similar cause was evident.

b. Findings

No findings of significance were identified.

2OS2 ALARA Planning and Controls (71121.02 - 6 samples)

a. Inspection Scope

During the period March 13 - 17, 2006, the inspector conducted the following activities to verify that Exelon properly implemented operational, engineering, and administrative controls to maintain personnel exposure as low as is reasonably achievable (ALARA) for tasks conducted during the Unit 1 refueling outage (1R11), and during the Unit 2 maintenance outage (2M36), which occurred February 23 - 26, 2006.

This inspection represents the completion of six

(6) samples for IP 71121.02, partially completing the biennial inspection requirement of fifteen
(15) samples.

Radiological Work Planning The inspector reviewed pertinent information regarding cumulative exposure history, current exposure trends, and ongoing activities to assess current performance and outage exposure challenges. The inspector determined the sites three-year rolling collective average exposure.

The inspector reviewed the Unit 1 refueling outage work scheduled during the inspection period and the associated work activity dose estimates. Scheduled work reviewed included regenerative heat exchanger repairs, installation of permanent shielding in the drywell, and removal/transfer of spent suppression pool filters.

The inspector reviewed procedures associated with maintaining worker dose ALARA and with estimating and tracking work activity specific exposures. The inspector reviewed the assumptions used in estimating outage dose, and radiation protection management briefed the inspector on recent upgrades to the access control program, in which work orders will be electronically tracked with RWPs to improve dose forecasting.

The inspector compared the person-hour estimates provided by maintenance planning and other work groups with actual work activity time requirements and evaluated the accuracy of these estimates. Specific jobs reviewed included installation and removal of scaffolding and shielding in the drywell, regenerative heat exchanger repairs, and main steam relief valve removal/installation.

The inspector reviewed the dose summary reports, detailing worker estimated and actual exposures, through March 16, 2006, for jobs performed during the 1R11 refueling outage and for the Unit 2 maintenance outage (2M36).

The inspector evaluated the exposure mitigation requirements specified in RWPs and ALARA Plans (AP), and compared actual worker cumulative exposure to estimated dose for tasks associated with these activities. The inspector reviewed in detail those work activities whose actual cumulative exposure approached the estimated dose, which resulted in a subsequent Work-In-Progress ALARA Review. Jobs reviewed included Install/Remove Drywell Shielding in support of 1R11, Install/Remove Drywell Scaffolding in support of 1R11, and Install/Remove Main Steam Relief Valves (MSRV) for 1R11.

The inspector evaluated the departmental interfaces between radiation protection, engineering, maintenance crafts, and operations to identify missing ALARA program elements and interface problems. The inspector accomplished the evaluation by interviewing the Radiological Engineering Manager and Radiation Protection Manager, reviewing station ALARA Committee meeting minutes, and attending pre-job briefings for jobs-in-progress (suppression pool spent filter removal and regenerative heat exchanger repairs).

The inspector determined if work activity planning included the use of temporary shielding, system flushes, hydrolazing of piping, and operational considerations to further to minimize worker exposure. The inspector examined the effectiveness of temporary and permanent shielding installed in the drywell, and pre/post dose rate data for the reactor vessel nozzle flushes.

Verification of Dose Estimates and Exposure Tracking Systems The inspector reviewed the assumptions and basis for the annual site collective exposure estimate and the Unit 1 refueling outage dose projection. The inspector reviewed personnel contamination reports and evaluated the need for internal dose assessments.

The inspector reviewed Exelons method for adjusting exposure estimates, and re-planning work, when emergent work was encountered. The inspector reviewed the Work-In-Progress ALARA reviews, ALARA Plans, and actions of the station ALARA Committee in monitoring and controlling dose allocations.

The inspector reviewed Exelons exposure tracking system to determine whether the level of detail, exposure report timeliness and dissemination was sufficient to support the control of collective exposures. The inspector included departmental dose compilations, highest personnel exposures to date, and individual exposure records in this review.

Job Site Inspection and ALARA Control The inspector observed the maintenance and operational activities being performed for drywell demobilization, regenerative heat exchanger repair, and removal of spent suppression pool filters to verify that Exelon implemented radiological controls, such as required surveys, job coverage, and contamination controls; personnel dosimetry was properly worn; and that workers were knowledgeable of work area radiological conditions.

The inspector reviewed the exposure of individuals in selected work groups, including mechanical maintenance, radiation protection, and outage services to determine if supervisors were making efforts to equalize doses among the workers.

Source Term Reduction and Control Through data review and telephone discussions held on March 28, 2006, with the Radiation Protection Manager, the inspector evaluated the status and historical trends for the Unit 1 source term.

Declared Pregnant Workers The inspector reviewed the radiological controls and dosimetry records for four declared pregnant workers performing outage related tasks to determine if Exelon met regulatory requirements in controlling their exposure.

Identification and Resolution of Problems The inspector reviewed elements of Exelons corrective action program related to implementing radiological controls to determine if station personnel were entering problems into the program for resolution. Details of this review are contained in section 4OA2 of this report.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA2 Identification and Resolution of Problems

.1 Review of Items Entered into the Corrective Action Program

As required by inspection procedure 71152, Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a screening of all items entered into Exelons corrective action program. Inspectors assessed each new issue report to verify whether Exelon adequately identified the full extent of various issues, performed appropriate evaluations, and identified reasonable corrective actions.

.2 Annual Sample: Review of Unit 2 Residual Heat Removal (RHR) Discharge High

Pressure Alarms (71152 - 1 sample)

a. Inspection Scope

In January 2006, the inspectors reviewed station actions in response to multiple occurrences of higher than normal pressure in the Unit 2 RHR system discharge piping in 2005 and 2006. The inspectors reviewed various issue reports, operator logs, action requests, and procedures as well as performed walkdowns and interviews to determine if Exelon adequately resolved the issue. The inspectors evaluated Exelons actions against the requirements of the corrective action program.

b. Findings and Observations

No findings of significance were identified.

Exelon evaluated the potential leak-by past the Low Pressure Coolant Injection (LPCI)valve (2F017), and, based on rate of pressurization, procedural guidance, and evaluation of design basis documents, correctly determined that the leak-by did not affect the ability of the LPCI system to perform its design function, and did not exceed the requirements for leakage past a primary containment isolation valve.

In response to each of these high pressure events, operators depressurized the RHR system in accordance with procedure S51.4.A, Manual Depressurization of RHR. The normal RHR discharge pressure is 150 psig. The procedure directs depressurization of the system anytime the affected RHR loop is not in operation and loop pressure is greater than a nominal 275 psig. At the time, this procedure directed cracking open and then closing the 18-inch RHR full-flow test motor operated valve to depressurize the RHR system. Though depressurization of this system through the full-flow test valve can be accomplished from the control room, this may not be the most optimal method.

Using a large valve to depressurize the system could result in a rapid drop in system pressure which could cause low pressure alarms and challenge the keep-fill systems.

Additionally, if the valve were to fail open for any reason during depressurization, the potential exists for the affected loop to be drained to the suppression pool. This would result in a loss of the LPCI function.

Alternate means, which included procedures that already existed, were available to depressurize the RHR system through smaller lines, such as the one inch high point vent valves and RHR heat exchanger sample lines. On February 23, 2006, station personnel developed a temporary procedure change to S51.4.A to direct depressurization using the smaller manual valves. Exelon authorized and implemented this temporary procedure change on April 2, 2006.

The inspectors reviewed the changes that Exelon made to procedure S51.4.A and found the changes to be acceptable.

.3 Access Control to Radiologically Significant Areas

a. Inspection Scope

The inspector reviewed 20 issue reports, recent Station ALARA Committee meeting minutes, eight Nuclear Oversight Objective Evidence Reports, and eight Nuclear Oversight Field Observation summaries, relating to controlling work activities in Unit 1 radiologically controlled areas, to evaluate Exelons threshold for identifying, evaluating, and resolving occupational radiation safety problems. The review included a check of possible repetitive issues such as radiation worker and radiation protection technician errors.

The review was conducted against the criteria contained in 10 CFR 20, Technical Specifications, and Exelon procedures.

b. Findings and Observations

No findings of significance were identified.

.4 ISI Finding Dispositions

a. Inspection Scope

The inspector reviewed a sample of ISI related issues to verify that Exelon identified the issues at the appropriate threshold and entered them into the corrective action program.

The inspector conducted interviews with plant personnel and reviewed issue reports and GE notification reports generated from IVVI and the core shroud inspection. The inspector verified that Exelon entered deficiencies into the corrective action program and evaluated and appropriately resolved these deficiencies within the corrective action program.

b. Findings and Observations

No findings of significance were identified.

4OA3 Event Followup

.1 (Closed) LER 05000353/02-05-001, Core Alterations Performed With Source Range

Monitor Alarm Horn Inoperable On March 12, 2005, Unit 2 source range monitors (SRMs) became inoperable due to a loss of the SRM audible alarm function which resulted from an equipment problem that caused a continuous audible alarm in the main control room. Operators removed power fuses to silence the horn which in turn removed audible annunciator indication on 13 alarm panels. Exelon assigned a dedicated individual to monitor the alarm panels and alert the duty reactor operator in the event of a visual alarm on the affected panels.

Core alterations were in progress during this event. Operators did not recognize that Technical Specifications (TS) requires the SRM audible alarm function to be operable anytime core alterations are in progress, resulting in operation in a condition prohibited by TS. The NRC is issuing a green non-cited violation regarding this issue in this report (Section 1R14). The inspectors did not identify any additional findings associated with this LER. Exelon documented this issue, along with completed and planned corrective actions, in IR 312046. This LER is closed.

.2 (Closed) LER 05000352/01-05-004, Minimum Critical Power Ratio Limiting Condition for

Operation Non-compliance On September 20, 2005, a General Electric Part 21 report determined that Limerick Unit 1 exceeded the Technical Specification (TS) 3.2.3, Minimum Critical Power Ratio, (MCPR) limit on May 29, 2004, and on September 11, 2004. On May 29, 2004, the MCPR TS limit of 1.0 was exceeded for six hours and reached a maximum value of 1.03. On September 11, 2004, the MCPR limit was exceeded for seven hours and reached a maximum value of 1.002. There was no impact on the reactor fuel because no plant transients occurred during the periods when the MCPR ratio exceeded the TS limit of 1.0. The non-compliance was due to an error in GEs fuel test performance and final data. Exelon corrective actions included a review of Limerick Units 1 and 2 during the past two year operating cycle to determine the extent of condition and the installation of a new computer data bank on the core process computer for both units.

The new computer data bank has been installed at Unit 1 and will be installed at Unit 2 prior to reaching a condition where the MCPR limit would present a concern.

This finding is more than minor because it had a credible impact on safety, in that a minimum critical power ratio (MCPR) value greater than the TS limit could result in fuel cladding degradation. The finding affects the Barrier Integrity Cornerstone and was considered to have very low safety significance (Green) using Appendix A of the Significance Determination Process (SDP) because no plant transients occurred during the periods when the MCPR ratio exceeded the TS limit and there was no fuel degradation. This licensee-identified finding involved a violation of TS 3.2.3, Minimum Critical Power Ratio. The enforcement aspects of the violation are discussed in Section 4OA7. This LER is closed.

.3 (Closed) LER 05000353/02-05-004, Reactor Scram Due to EHC Malfunction

On October 12, 2005, Unit 2 reactor scrammed from 100% reactor power due to problems with the main turbine electrohydraulic control (EHC) system. The plant responded as designed with the exception of the main turbine EHC malfunction. The EHC failure was due to faulty electrical circuit cards. Exelon replaced four EHC circuit cards and tested the cards satisfactorily. The inspectors reviewed this LER and identified no findings of significance and no violation of NRC requirements. Exelon documented this issue, along with completed and planned corrective actions, in IR 385399. This LER is closed.

4OA6 Meetings, Including Exit

Exit Meetings On April 11, 2006, the resident inspectors presented the inspection results to Mr. DeGregorio and other members of his staff, who acknowledged the findings.

The inspectors confirmed that proprietary information was not provided or examined during the inspection.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

  • Technical Specification (TS) 3.2.3, Minimum Critical Power Ratio (MCPR) requires that the MCPR value remain less than one. Contrary to this, Limerick Unit 1 exceeded the MCPR limit on May 29, 2004, and on September 11, 2004. On May 29, 2004, the MCPR TS limit of 1.0 was exceeded for six hours and reached a maximum value of 1.03. On September 11, 2004, the MCPR limit was exceeded for seven hours and reached a maximum value of 1.002. This finding is of very low safety significance because no plant transients occurred during the periods when the MCPR ratio exceeded the TS limit and there was no fuel degradation. Exelon documented this issue, along with completed and planned corrective actions, in IR 352899.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Exelon Generation Company

R. DeGregorio, Site Vice President
C. Mudrick, Plant Manager
P. Orphanos, Director, Operations
P. Chase, Shift Operations Superintendent
E. Kelly, Engineering Programs Manager
W. Astbury, ESW System Manager
J. George, RHR System Manager
W. Tracey, SRV System Manager
F. Burzynski, Station Fire Marshall
M. Kowalski, Maintenance Rule Coordinator
P. Tarpinian, PRA Engineer

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000353/2006002-01 NCV Unit 2 Core Alterations Without Audible Source Range Monitor Alarms

Closed

05000353/02-05-001 LER Core Alterations Performed With Source Range Monitor Alarm Horn Inoperable
05000352/01-05-004 LER Minimum Critical Power Ratio Limiting Condition for Operation Non-compliance
05000353/02-05-004 LER Reactor Scram Due to EHC Malfunction

LIST OF DOCUMENTS REVIEWED