IR 05000352/2021003
| ML21308A019 | |
| Person / Time | |
|---|---|
| Site: | Limerick |
| Issue date: | 11/04/2021 |
| From: | Jon Greives Division of Operating Reactors |
| To: | Rhoades D Exelon Generation Co LLC, Exelon Nuclear |
| Greives J | |
| References | |
| IR 2021003 | |
| Download: ML21308A019 (12) | |
Text
November 4, 2021
SUBJECT:
LIMERICK GENERATING STATION, UNITS 1 AND 2 - INTEGRATED INSPECTION REPORT 05000352/2021003 AND 05000353/2021003
Dear Mr. Rhoades:
On September 30, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Limerick Generating Station, Units 1 and 2. On October 22, 2021, the NRC inspectors discussed the results of this inspection with Mr. Frank Sturniolo, Site Vice President and other members of your staff. The results of this inspection are documented in the enclosed report.
No findings or violations of more than minor significance were identified during this inspection.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely, Jonathan E. Greives, Chief Reactor Projects Branch 4 Division of Operating Reactor Safety
Docket Nos. 05000352 and 05000353 License Nos. NPF-39 and NPF-85
Enclosure:
As stated
Inspection Report
Docket Numbers:
05000352 and 05000353
License Numbers:
Report Numbers:
05000352/2021003 and 05000353/2021003
Enterprise Identifier: I-2021-003-0022
Licensee:
Exelon Generation Company, LLC
Facility:
Limerick Generating Station, Units 1 and 2
Location:
Sanatoga, PA 19464
Inspection Dates:
July 1, 2021 through September 30, 2021
Inspectors:
A. Ziedonis, Senior Resident Inspector
S. Haney, Resident Inspector
L. Grimes, Resident Inspector
E. Garcia, Reactor Engineer
Approved By:
Jonathan E. Greives, Chief
Reactor Projects Branch 4
Division of Operating Reactor Safety
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Limerick Generating Station, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors.
Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
No findings or violations of more than minor significance were identified.
Additional Tracking Items
None.
PLANT STATUS
Unit 1 began the inspection period at rated thermal power. On September 2, 2021, the unit was down powered to approximately 86 percent, due to grid stability concerns following heavy rains and off-site sub-station flooding in the region. The unit was returned to rated thermal power later the same day. On September 17, 2021, the unit was down powered to approximately 79 percent, to perform turbine valve testing and a control rod sequence exchange. The unit was returned to full power on September 18, 2021, and remained at or near rated thermal power for the remainder of the inspection period.
Unit 2 began the inspection period at rated thermal power. On September 11, 2021, the unit was down powered to approximately 75 percent, to perform turbine valve testing and a control rod sequence exchange. The unit was returned to rated thermal power later the same day, and remained at or near rated thermal power for the remainder of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the coronavirus (COVID-19), resident and regional inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time, the resident inspectors performed periodic site visits each week, increasing the amount of time on site as local COVID-19 conditions permitted.
As part of their onsite activities, resident inspectors conducted plant status activities as described in IMC 2515, Appendix D, Plant Status, conducted routine reviews using IP 71152, Problem Identification and Resolution, observed risk significant activities; and completed on site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all or a portion of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on site. The inspections documented below met the objectives and requirements for completion of the IP.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Impending Severe Weather Sample (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated readiness for impending adverse weather conditions associated with multiple hot weather alerts during the week of August 23, 2021
External Flooding Sample (IP Section 03.03) (1 Sample)
- (1) The inspectors evaluated that flood protection barriers, mitigation plans, procedures, and equipment are consistent with the licensees design requirements and risk analysis assumptions for coping with external flooding on July 12, 2021
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Unit 1 D14 emergency diesel generator during instrumented run on August 16, 2021
- (2) Unit 2 reactor core isolation cooling system following planned testing on August 18, 2021
- (3) Unit common 'A' standby gas treatment system train during 'B' standby gas treatment system controller replacement on September 21, 2021
71111.05 - Fire Protection
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:
- (1) Fire area 33, Unit 1 reactor core isolation cooling pump and turbine room on July 7, 2021
- (2) Fire area 113, Unit common railroad access bay and generator equipment area rooms on July 7, 2021
- (3) Fire area 45, Unit 1 control rod drive equipment and neutron monitoring areas on August 19, 2021
- (4) Fire area 25, Unit common auxiliary equipment room on September 1, 2021
- (5) Fire area 32, Unit 1 'A' and 'C' residual heat removal rooms on September 1, 2021
Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated the on-site fire brigade training and performance during an unannounced fire drill on September 2, 2021
71111.06 - Flood Protection Measures
Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)
The inspectors evaluated internal flooding mitigation protections in the:
- (1) Unit 1 reactor building safeguards system access area on September 8, 2021
Cable Degradation (IP Section 03.02) (1 Sample)
The inspectors evaluated cable submergence protection in:
- (1) Review of 103W and 104W manholes inspection in March 2021 and review of cable condition monitoring program
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
- (1) The inspectors observed and evaluated licensed operator performance in the Control Room during a Unit 1 planned power reduction for turbine valve testing and a control rod sequence exchange on September 18, 2020
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
- (1) The inspectors observed and evaluated licensed operator requalification training on September 7, 2021
71111.12 - Maintenance Effectiveness
Maintenance Effectiveness (IP Section 03.01) (1 Sample)
The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components remain capable of performing their intended function:
- (1) Unit common emergency service water boundary check vale 011-0063 on August 9, 2021
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:
- (1) Unit common emergent troubleshooting and repair in response to emergency service water check valve leakage on July 20, 2021
- (2) Unit 1 emergent work associated with D14 emergency diesel generator on July 27, 2021
- (3) Unit 2 risk-informed completion time limiting condition for operation emergent extension following 'A' traversing in-core probe stuck electronic drive on August 11, 2021
- (4) Unit common fuel floor crane following emergent repairs on September 3, 2021
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 03.01) (6 Samples)
The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:
- (1) Unit common emergency service water check valve boundary leakage on July 14, 2021
- (2) Unit 1 D14 emergency diesel generator following safeguard battery alarms on July 29, 2021
- (3) Unit 2 automatic depressurization system following division 1 out of service alarm on August 23, 2021
- (4) Unit 2 thermal limits following identification of potential foreign material that could result in fuel channel flow diversion on September 1, 2021
- (5) Unit 1 controls rods during periodic channel distortion testing on September 18, 2021
- (6) Unit 1 high pressure coolant injection system flow controller functionality following emergency shutdown switch replacement on September 26, 2021
71111.18 - Plant Modifications
Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)
The inspectors evaluated the following temporary or permanent modifications:
- (1) Unit 2 low pressure coolant injection testable injection check valves (HV-051-2F041A and D) vibration monitoring instrumentation
71111.19 - Post-Maintenance Testing
Post-Maintenance Test Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated the following post-maintenance test activities to verify system operability and functionality:
- (1) Unit 2 'C' residual heat removal pump discharge pressure permissive signal to the division 1 automatic depressurization system following trip unit replacement on August 26, 2021
- (2) Unit 1 'A' residual heat removal shutdown cooling suction motor operated valve following motor starter replacement on August 27, 2021
- (3) Unit 2 reactor core isolation cooling steam supply valve stroke following back-seat configuration on September 9, 2021
- (4) Unit common 'B' main control room chiller cleaning and condenser tube inspection on September 21, 2021
- (5) Unit 1 high pressure coolant injection system following repairs on September 26, 2021
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Surveillance Tests (other) (IP Section 03.01)
- (1) ST-6-011-231-0, Unit 1 'A' loop emergency service water pump, valve and flow test on July 12, 2021
- (2) ST-6-048-230-1/2, Unit 1 and 2 standby liquid control pump surveillance alternate treatment frequency change on July 16, 2021
- (3) ST-6-092-314-1, Unit 1 D14 emergency diesel generator slow start operability test run on July 30, 2021
- (4) ST-6-049-230-2, Unit 2 reactor core isolation cooling system pump, valve and flow in-service test on August 17, 2021
71114.06 - Drill Evaluation
Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated the conduct of an emergency preparedness drill on October 7, 2021
Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated a simulator training evolution on August 3,
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01)===
- (1) Unit 1 for the period of July 1, 2020, through June 30, 2021
- (2) Unit 2 for the period of July 1, 2020, through June 30, 2021
IE04: Unplanned Scrams with Complications Sample (IP Section 02.03) (2 Samples)
- (1) Unit 1 for the period of July 1, 2020, through June 30, 2021
- (2) Unit 2 for the period of July 1, 2020, through June 30, 2021
MS09: Residual Heat Removal Systems (IP Section 02.08) (2 Samples)
- (1) Unit 1 for the period of July 1, 2020, through June 30, 2021
- (2) Unit 2 for the period of July 1, 2020, through June 30, 2021
71152 - Problem Identification and Resolution
Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
- (1) Identification, evaluation and corrective action in response to NRC-identified submerged safety-related cables in manhole 103W (IR 4440505)
71153 - Follow-Up of Events and Notices of Enforcement Discretion Event Follow-Up (IP Section 03.01)
- (1) Unit 1 high pressure coolant injection system declared inoperable on September 23, 2020 (Event Notification 55484)
INSPECTION RESULTS
Minor Performance Deficiency 71152 Minor Performance Deficiency: Exelon procedure ER-AA-300-150, Cable Condition Monitoring Program, Step 4.5.20.3, states Issue reports shall be issued to document as-found conditions of underground structures, documenting adverse conditions; and "Inspection and pumping frequencies shall be adjusted as necessary when cables are found submerged." Contrary to this, the inspectors identified that safety-related low voltage power cables were submerged in standing water inside of manhole 103-west (MH103W) during video review of Exelon's manhole inspection under Work Order 4317542, and no issue report had been generated by Exelon to document the as-found adverse condition. In addition, the inspectors identified that work order instructions directed maintenance to de-water the manhole prior to the engineering inspection of the manhole. The inspectors further noted that the manhole inspection was performed by a structural engineer in accordance with the structures monitoring program, but the cable condition monitoring program engineer was not involved with the manhole inspection. The inspectors also identified the condition existed during the previous MH103W inspection performed in 2016. In response, Exelon generated Issue Report 4440505, and added the issue to the station's priority work list to expedite manhole inspection and troubleshooting of the dewatering system pump and high-level alarm.
Screening: The inspectors determined the performance deficiency was minor. The inspectors screened this performance deficiency in accordance with IMC 0612, Appendix B, "Additional Issue Screening Guidance," effective date January 1, 2021, and determined it was minor, because there were no cable failures that adversely impacted a cornerstone objective; and because the performance deficiency did not have the potential to lead to a more significant safety concern if left uncorrected, based on satisfactory cable insulation resistance test results that did not indicate a degrading trend in cable insulation material.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On October 22, 2021, the inspectors presented the integrated inspection results to Mr. Frank Sturniolo, Site Vice President and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Corrective Action
Documents
4444518
Degraded radio communications in the U2 air compressor
room
09/03/2021
Corrective Action
Documents
Resulting from
Inspection
4433791
NRC ID: Door 205 was found opened and unattended
07/08/2021
Corrective Action
Documents
4445260
Drain backup - reactor building unit 1
09/08/2021
4445404
Unit 2 turbine building floor drain clogged
09/09/2021
71111.11Q Corrective Action
Documents
4447358
Bently Nevada VMS 'A' host computer is not functional
09/19/2021
4447419
4.0 critique for post-summer load drop
09/19/2021
Corrective Action
Documents
4434220
Check valve leaks by excessively
07/09/2021
4436263
ESW check valve 011-0063 leaks by
07/21/2021
Corrective Action
Documents
Resulting from
Inspection
4443659
RT-1-011-875-0 acceptance criteria requires updating
08/31/2021
4451105
Enhancement for leak testing in ST-6-011-231-0
10/06/2021
Corrective Action
Documents
4377721
Momentary U1 div 4 sfgd battery ground alarm
10/19/2020
25639
Div 4 sfgd battery grounds during D14 DG run
05/25/2021
4430559
Unit 1 div 4 safeguards battery ground alarm
06/21/2021
4437109
D14 D/G loss of control during surveillance testing
07/26/2021
4437110
Div 4 sfgd battery grounds during D14 DG run
07/26/2021
4437112
U1 div 4 safeguard battery charger trouble following D14 DG
trip
07/26/2021
4437519
D14 LSRA relay out of tolerance
07/28/2021
4439018
4.0 critique for D14 D/G abnormal indications
08/04/2021
4440855
D14 OCC critique
08/16/2021
Corrective Action
Documents
Resulting from
Inspection
4438504
D14 additional monitoring needed for the next run per ODM
08/02/2021
Corrective Action
Documents
4437521
FME - 'C' MSLP PM identified missing parts
07/28/2021
4438598
GNF2 flow blockage report applicability concerns
08/03/2021
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
4443530
Erroneous LGS U2 flow blockage MFLCPR penalty
08/30/2021
4444088
NF RPV lost parts improvement AR
09/01/2021
Corrective Action
Documents
4447613
WO needed to remove TCC 630223 from 2A and 2D LPCI
lines
09/20/2021
Engineering
Changes
630223
Vibration Instrumentation Installed on HV-051-2F041D and
HV-051-2F041A
Revision 1
Work Orders
4945745
Corrective Action
Documents
4442159
Gross fail on trip unit
08/23/2021
4442993
Procedure MA-AA-716-012 needs improved guidance
08/27/2021
4445747
PCRA requested to corporate maintenance procedure MA-AA-
716-012
09/10/2021
4452175
D234-D-G-19 power wires swapped at thermal o/L relay
10/11/2021
Corrective Action
Documents
Resulting from
Inspection
4443727
CAP product needed for HV-051-1F006A failed PMT
08/31/2021
4443735
Timeliness for HV-051-1F006A investigation
08/31/2021
4447960
Procedure MA-AA-716-012 needs improved guidance
09/22/2021
Work Orders
5044941
Corrective Action
Documents
4417604
Tech spec surveillance changes for 10 CFR 50.69
04/19/2020
Corrective Action
Documents
4448242
U1 HPCI unsat response during ST-6-055-230-1
09/23/2021
4448568
CCP: U1 HPCI RSP emerg S/D switch drawing error
09/25/2021
4448701
PIS-056-1N653 gross fail during ST-2-055-101-1
09/26/2021
4448719
Unit 1 HPCI - minor oil leak at PCV-056-149
09/26/2021
4449311
10C201 power supply light flickering
09/29/2021
4449379
Proactive replacement of HS-056-262
09/29/2021