IR 05000352/2022004

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Integrated Inspection Report 05000352/2022004 and 05000353/2022004
ML23041A388
Person / Time
Site: Limerick  Constellation icon.png
Issue date: 02/13/2023
From: Jon Greives
NRC/RGN-I/DORS
To: Rhoades D
Constellation Energy Generation, Constellation Nuclear
References
IR 2022004
Download: ML23041A388 (1)


Text

February 13, 2023

SUBJECT:

LIMERICK GENERATING STATION, UNITS 1 AND 2 - INTEGRATED INSPECTION REPORT 05000352/2022004 AND 05000353/2022004

Dear David Rhoades:

On December 31, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Limerick Generating Station, Units 1 and 2. On February 10, 2023, the NRC inspectors discussed the results of this inspection with Michael Gillin, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

Three findings of very low safety significance (Green) are documented in this report. One of these findings involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at Limerick Generating Station, Units 1 and 2.

If you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; and the NRC Resident Inspector at Limerick Generating Station, Units 1 and 2. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Jonathan E. Greives, Chief Projects Branch 4 Division of Operating Reactor Safety

Docket Nos. 05000352 and 05000353 License Nos. NPF-39 and NPF-85

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000352 and 05000353

License Numbers:

NPF-39 and NPF-85

Report Numbers:

05000352/2022004 and 05000353/2022004

Enterprise Identifier: I-2022-004-0035

Licensee:

Constellation Energy Generation, LLC

Facility:

Limerick Generating Station, Units 1 and 2

Location:

Sanatoga, PA 19464

Inspection Dates:

October 1, 2022 to December 31, 2022

Inspectors:

A. Ziedonis, Senior Resident Inspector

L. Grimes, Resident Inspector

M. Henrion, Health Physicist

B. Edwards, Health Physicist

Approved By:

Jonathan E. Greives, Chief

Projects Branch 4

Division of Operating Reactor Safety

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at Limerick Generating Station, Units 1

and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the

NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer

to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to use engineering controls in accordance with Radiation Work Permit (RWP)

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Occupational

Radiation Safety

Green

NCV 05000352,05000353/2022004-01

Open/Closed

[H.8] -

Procedure

Adherence

71124.03

A finding of very low safety significance (Green) and associated non-cited violation (NCV) of

Title 10 of the Code of Federal Regulations (10 CFR) 20.1701, Use of process or other

engineering controls, was self-revealed on April 9, 2022, when Constellation workers failed to

use, to the extent practical, process or other engineering controls (e.g., containment,

decontamination, or ventilation) to control the concentration of radioactive material in air meet

the requirements of 10 CFR 20.1701. Specifically, on April 9, 2022, during a refuel outage at

Limerick Generating Station, Constellation failed to use process or other engineering controls

(e.g., high-efficiency particulate air (HEPA) ventilation unit and maintain the work in a wetted

condition) prior to engaging in aggressive work activities on the main steam isolation valve

(MSIV) in the Unit 1 drywell. This resulted in airborne radioactivity in the immediate work area

and one worker received an unplanned exposure of 49 millirem committed effective dose

equivalent.

Inadequate maintenance procedure results in electrohydraulic (EHC) fluid leak from main

turbine bypass valve (BPV)

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

FIN 05000352,05000353/2022004-02

Open/Closed

None (NPP)

71152A

The inspectors determined there was a Green, self-revealing finding because maintenance

procedure MA-LG-763-473, Disassemble and Assemble Main Steam BPV Actuator/Spring

Can, Revision 0, did not include adequate steps to effectively reassemble BPV number 1

(BPV-1) actuator following the performance of preventive maintenance activities, which

resulted in an EHC fluid leak on May 14, 2022, and adversely impacted the reliability of the

main turbine bypass system.

Inadequate performance monitoring and margin management associated with MSIV local leak

rate testing (LLRT)

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Barrier Integrity

Green

FIN 05000352,05000353/2022004-03

Open/Closed

[H.6] - Design

Margins

71152A

The inspectors identified a Green finding against procedure ER-AA-2003, System

Performance Monitoring and Analysis, Revision 8, because Constellation did not perform

adequate performance monitoring and analysis of MSIV LLRT results to ensure that

degrading trends were identified prior to challenging required limits during the operating cycle.

Additional Tracking Items

Type

Issue Number

Title

Report Section

Status

URI

05000352,05000353/

2022004-04

Failure to follow

maintenance procedure

results in emergency diesel

generator (EDG) jacket

water (JW) leak

71152A

Open

PLANT STATUS

Unit 1 began the inspection period at rated thermal power (RTP). On November 26, 2022, the

unit was down-powered to approximately 75 percent thermal power for a control rod sequence

exchange. The unit was returned to full power on November 27, 2022, and remained at or near

RTP for the remainder of the inspection period.

Unit 2 began the inspection period at RTP. On November 19, 2022, the unit was down-powered

to approximately 75 percent thermal power for a control rod sequence exchange. The unit was

returned to full power on November 20, 2022, and remained at or near RTP for the remainder of

the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed activities described in IMC 2515,

Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of

IPs. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel to assess licensee performance and compliance with Commission rules

and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated readiness for seasonal extreme weather conditions prior to

the onset of seasonal cold temperatures for the following systems during the week of

December 12, 2022:

  • Unit 1 and 2 hardened vent remote operation control system batteries

Unit 1 and 2 residual heat removal (RHR) systems

Unit 1 and 2 control rod hydraulic control units and scram discharge volumes

Impending Severe Weather Sample (IP Section 03.02) (1 Sample)

(1)

The inspectors evaluated the adequacy of the overall preparations to protect risk-

significant systems from impending severe weather associated with a winter weather

advisory during the week of December 12, 2022

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1)

Unit 1 'A' drywell chiller following 'B' chiller trip on October 11, 2022

(2)

Unit common off-site power alignment during period of elevated voltage on the 20

regulating transformer on October 20, 2022

(3)

Unit 2 safeguard battery divisions 1, 2, and 4, during troubleshooting of Division 3 on

December 13, 2022

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire areas:

(1)

Unit common fire area 25, auxiliary equipment room 542 with area fire panel non-

functional due to heat detection trouble on October 28, 2022

(2)

Unit 2 fire area 16, D24 emergency 4KV switchgear room on November 10, 2022

(3)

Unit common FLEX diesel generator storage building on November 15, 2022

(4)

Unit 2 fire area 64, reactor enclosure cooling water heat exchanger area rooms 284

and 286 on December 9, 2022

(5)

Unit 1 fire area 31, 'B' and 'D' RHR heat exchanger and pump room, rooms 103 and

204 on December 16, 2022

71111.07A - Heat Exchanger/Sink Performance

Annual Review (IP Section 03.01) (1 Sample)

The inspectors evaluated readiness and performance of:

(1)

Unit common, RT-1-011-391-0, main control room chiller heat transfer performance

calculation test on December 15, 2022

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

(1)

The inspectors reviewed and evaluated the licensed operator annual requalification

results for the annual operating exams completed on November 17, 2022.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1)

The inspectors observed and evaluated licensed operator performance in the control

room during a Unit 2 planned power reduction for a rod pattern adjustment on

November 19 and 20, 2022; and during near-rated rod notching on Unit 2 on

December 11, 2022

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1)

The inspectors observed and evaluated licensed operator requalification training

scenarios in the simulator on November 8, 2022

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (3 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following

structures, systems, and components remain capable of performing their intended function:

(1)

Unit 2 'B' primary containment instrument gas subsystem on November 10, 2022

(2)

Unit 1 EDG D12 following speed switch failure on December 20 and 21, 2022

(3)

Unit 2 EDG D22 following output breaker trip on reverse power trip during the week

December 19, 2022

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed:

(1)

Unit 1 implementation of risk informed completion time with the average power range

monitor (APRM) voter number 1 inoperable on October 14, 2022

(2)

Unit 1 high-pressure coolant injection (HPCI) emergent work on October 14, 15,

and 16

(3)

Unit 2 EDG D22 emergent work following surveillance test (ST) failure on October 15

and 16, 2022

(4)

Unit 2 EDG D21 emergent work following ST failure on November 3, 2022

(5)

Unit 1 risk assessment during planned testing with select nuclear steam supply

shutoff system valves inoperable on December 19, 2022

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (6 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1)

Unit 1 APRM ST results evaluation on October 14, 2022

(2)

Unit 2 EDG D22 following ST failure on October 14, 17, and 18, 2022

(3)

Unit 1 'A' adjustable speed drive functionality with the runback feature placed in

bypass on October 31, 2022

(4)

Unit 1 EDG D12 after unexpected 'EDG running' alarms received in main control

room November 1 and 2, 2022

(5)

Unit 2 EDG D22 following receipt of motor control center shunt trip coil undervoltage

alarm during the week of November 14, 2022

(6)

Unit 1 'L' safety relief valve following step increase in tailpipe temperature on

November 28 and 29, 2022

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1)

Unit common third off-site source transfer switch on October 3 and 4, 2022

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (7 Samples)

The inspectors evaluated the following post-maintenance testing activities to verify system

operability and/or functionality:

(1)

Unit common 101 safeguard transformer load tap changer following transformer

replacement on October 4, 5, and 6, 2022

(2)

Unit 2 EDG D21 following speed switch replacement on November 4, 2022

(3)

Unit 2 reactor core isolation cooling following planned maintenance on November 16,

2022

(4)

Unit common 'A' emergency service water system following motor replacement on

November 22, 2022

(5)

Unit 1 'A' RHR following planned maintenance on November 30, 2022

(6)

Unit common 'A' RHR service water pump following planned maintenance on

December 14 and 15, 2022

(7)

Unit 2 'B' core spray system unit cooler following corrective maintenance on

December 22, 2022

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities to verify system operability

and/or functionality:

Surveillance Tests (other) (IP Section 03.01) (2 Samples)

(1)

ST-6-092-312-2, Unit 2 D22 diesel generator slow start operability test run, with

additional instrumentation, on November 7, 2022

(2)

ST-6-055-230-2, Unit 2 HPCI pump, valve, and flow test on December 21, 2022

Reactor Coolant System (RCS) Leakage Detection Testing (IP Section 03.01) (1 Sample)

(1)

ST-6-107-590-2, Unit 2 daily surveillance log with elevated RCS unidentified leakage

on December 16, 2022

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1)

An emergency preparedness training evolution on November 17, 2022

RADIATION SAFETY

71124.03 - In-Plant Airborne Radioactivity Control and Mitigation

Permanent Ventilation Systems (IP Section 03.01) (1 Sample)

The inspectors evaluated the configuration of the following permanently installed ventilation

systems:

(1)

Unit common spent fuel pool ventilation system

Temporary Ventilation Systems (IP Section 03.02) (1 Sample)

The inspectors evaluated the configuration of the following temporary ventilation system:

(1)

Walked down HEPA vacuum and unit storage locations and reviewed inventory

procedures

Use of Respiratory Protection Devices (IP Section 03.03) (1 Sample)

(1)

The inspectors evaluated the licensees use of respiratory protection devices

Self-Contained Breathing Apparatus for Emergency Use (IP Section 03.04) (1 Sample)

(1)

The inspectors evaluated the licensees use and maintenance of self-contained

breathing apparatuses

71124.04 - Occupational Dose Assessment

Source Term Characterization (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated licensee performance as it pertains to radioactive source

term characterization

External Dosimetry (IP Section 03.02) (1 Sample)

(1)

The inspectors evaluated how the licensee processes, stores, and uses external

dosimetry

Internal Dosimetry (IP Section 03.03) (2 Samples)

The inspectors evaluated the following internal dose assessments:

(1)

Reviewed Accuscan of worker with internal contamination

(2)

Reviewed Fastscan of worker with internal contamination

Special Dosimetric Situations (IP Section 03.04) (2 Samples)

The inspectors evaluated the following special dosimetric situations:

(1)

Reviewed evaluation of a declared pregnant worker

(2)

Reviewed procedure for special increased exposures

71124.07 - Radiological Environmental Monitoring Program

Environmental Monitoring Equipment and Sampling (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated environmental monitoring equipment and observed

collection of environmental samples

Radiological Environmental Monitoring Program (IP Section 03.02) (1 Sample)

(1)

The inspectors evaluated the implementation of the licensees radiological

environmental monitoring program

GPI Implementation (IP Section 03.03) (1 Sample)

(1)

The inspectors evaluated the licensees implementation of the Groundwater

Protection Initiative program to identify incomplete or discontinued program elements

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

MS10: Cooling Water Support Systems (IP Section 02.09) (2 Samples)

(1)

Unit 1 for the period of October 1, 2021, through September 30, 2022

(2)

Unit 2 for the period of October 1, 2021, through September 30, 2022

BI01: RCS Specific Activity Sample (IP Section 02.10) (2 Samples)

(1)

Unit 1 for the period of October 1, 2021, through September 30, 2022

(2)

Unit 2 for the period of October 1, 2021, through September 30, 2022

BI02: RCS Leak Rate Sample (IP Section 02.11) (2 Samples)

(1)

Unit 1 for the period of October 1, 2021, through September 30, 2022

(2)

Unit 2 for the period of October 1, 2021, through September 30, 2022

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)

(1)

December 2021 through October 2022

PR01: Radiological Effluent Technical Specifications (TSs)/Offsite Dose Calculation Manual

Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample

(IP Section 02.16) (1 Sample)

(1)

December 2021 through October 2022

71152A - Annual Follow-up Problem Identification and Resolution

Annual Follow-up of Selected Issues (Section 03.03) (3 Samples)

The inspectors reviewed the licensees implementation of its corrective action program

(CAP) related to the following issues:

(1)

Potential adverse trends associated with MSIV LLRT on November 17, 18, 21,

and 30, 2022

(2)

Evaluation and corrective actions associated with Unit 1 BPV #1 EHC fluid leakage,

and associated work group evaluation (WGE) 4499745 on November 21 and

December 12, 2022

(3)

Evaluation and corrective actions associated with Unit 2 EDG D21 jacket water

leakage, and associated WGE 4514473 on December 9, 12, and 21, 2022

71152S - Semiannual Trend Problem Identification and Resolution

Semiannual Trend Review (Section 03.02) (1 Sample)

(1)

The inspectors reviewed Constellations CAP for potential adverse trends that might

be indicative of a more significant safety issue. The inspectors determined that

Constellation was appropriately identifying, evaluating, and resolving adverse trends.

INSPECTION RESULTS

Failure to use engineering controls in accordance with RWP

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Occupational

Radiation Safety

Green

NCV 05000352,05000353/2022004-01

Open/Closed

[H.8] -

Procedure

Adherence

71124.03

A finding of very low safety significance (Green) and associated NCV of 10 CFR 20.1701,

Use of process or other engineering controls, was self-revealed on April 9, 2022, when

Constellation workers failed to use, to the extent practical, process or other engineering

controls (e.g., containment, decontamination, or ventilation) to control the concentration of

radioactive material in air meet the requirements on of 10 CFR 20.1701. Specifically, on

April 9, 2022, during a refuel outage at Limerick Generating Station, Constellation failed to

use process or other engineering controls (e.g., HEPA ventilation unit and maintain the work

in a wetted condition) prior to engaging in aggressive work activities on the MSIV in the Unit 1

drywell. This resulted in airborne radioactivity in the immediate work area and one worker

received an unplanned exposure of 49 millirem committed effective dose equivalent.

Description: On April 9, 2022, two workers entered the Unit 1 drywell under RWP (LG-0-22-

00509) to complete machining work of MSIV valves 'B' and 'D'. The individuals alarmed the

personnel contamination monitor (PM-12) at the radiologically controlled area (RCA) exit.

One worker was machining in the drywell on the B MSIV. The other individual was setting up

on the D MSIV nearby. The individual machining on the B MSIV had assumed the work

after receiving turnover from the previous crew who had set the machine in the valve. The B

MSIV did not have the required HEPA ventilation, and the valve seat was not properly

maintained wet during the evolution as required by the RWP and the as low as reasonably

achievable (ALARA) plan. The worker at the B MSIV also reported hearing a loud banging

noise above where they were working and that the pipe and valve vibrated with the banging.

The vibrations were determined to be from power tool ratcheting to loosen the main steam

relief valve (MSRV) bolts on the same line nearby. This vibration is thought to have

contributed to an airborne event in the work area from the valve. The lack of proper HEPA

ventilation and maintaining the work wet caused one worker to receive 49 millirem (mrem)

committed effective dose equivalent (internal dose).

The licensee evaluated the event and found that contributing factors which led to these

degraded conditions were as follows:

  • The workers did not understand ALARA plan requirements and were not aware of the

requirements due to only being discussed verbally well in advance of the work.

The ALARA brief was not discussed by radiation protection (RP) staff and the workers

during the radiological conditions briefing provided before the workers entered to

perform the work on the MSIVs. Workers stated that the briefing was focused on the

dose rates in the area and did not include the contamination control aspects of the

ALARA plan. In addition, the ALARA plan was not reviewed in detail as the RP

technician thought the initial ALARA brief was adequate.

Various roles and responsibilities were not made clear at the initial ALARA brief, as

RP staff assumed that the workers would set up the HEPA and the workers thought

that a HEPA vacuum in the valve was adequate.

RP did not provide adequate oversite of the work area. The RP brief should have

identified the need for the workers to contact RP to verify the engineering controls

(HEPA placement and wetting of surfaces) were adequate prior to aggressive

work. This did not occur due to the key ALARA plan requirements not being reviewed

during subsequent briefs.

Corrective Actions:

  • Performed a training performance analysis

Define which jobs will require oversight/observations to ensure RP/ALARA plan

compliance and invite corporate oversight to those activities

Identify critical jobs using the RP manpower sheet for on-line and schedule review for

outages and assign the responsible oversight Supervisor/Manager

Benchmark industry leader for education of outage supplemental workforce on basic

RP fundamentals including engineering controls and site operating experience

Implement actions from the benchmark

Review and validate the use of engineering controls

Corrective Action References: Issue Report (IR) 04491897

Performance Assessment:

Performance Deficiency: The improper use of engineering controls (HEPA unit and

maintaining work wet) was reasonably within Constellations ability to foresee and correct and

should have been prevented and therefore was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Program and Process attribute of the Occupational

Radiation Safety cornerstone and adversely affected the cornerstone objective to ensure the

adequate protection of the worker health and safety from exposure to radiation from

radioactive material during routine civilian nuclear reactor operation. In addition, it is similar to

example 6.h of IMC 0612, Appendix E. Specifically, the worker failed to use a HEPA and

keep work wet during the duration of the valve work per the RWP ALARA Plan, which

resulted in an unplanned exposure of 49 mrem committed effective dose equivalent (internal

dose).

Significance: The inspectors assessed the significance of the finding using IMC 0609,

Appendix C, Occupational Radiation Safety Significance Determination Process (SDP). The

finding was of very low safety significance (Green) because: 1) it was not ALARA finding, 2)

there was no overexposure, 3) there was no substantial potential for an overexposure, and 4)

the ability to assess dose was not compromised.

Cross-Cutting Aspect: H.8 - Procedure Adherence: Individuals follow processes, procedures,

and work instructions. The inspectors determined that this finding had a cross-cutting aspect

in the area of Human Performance, Procedure Adherence, because the individuals failed to

follow verbal and written work instructions.

Enforcement:

Violation: Title 10 of the CFR 20.1701, Use of process or other engineering controls, states

that, The licensee shall use, to the extent practical, process or other engineering controls

(e.g., containment, decontamination, or ventilation) to control the concentration of radioactive

material in air." Contrary to the above, on April 9, 2022, Constellation failed to use process or

other engineering controls (e.g., HEPA ventilation unit and maintain the work in a wetted

condition), in violation of 10 CFR 20.1701; resulting in airborne radioactivity and unplanned

dose of 49 mrem committed effective dose equivalent to one worker.

Enforcement Action: This violation is being treated as a NCV, consistent with Section 2.3.2 of

the Enforcement Policy.

Inadequate maintenance procedure results in EHC fluid leak from main turbine BPV

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

FIN 05000352,05000353/2022004-02

Open/Closed

None (NPP)

71152A

The inspectors determined there was a Green, self-revealing finding because maintenance

procedure MA-LG-763-473, Disassemble and Assemble Main Steam BPV Actuator/Spring

Can, Revision 0, did not include adequate steps to effectively reassemble BPV number 1

(BPV-1) actuator following the performance of preventive maintenance activities, which

resulted in an EHC fluid leak on May 14, 2022, and adversely impacted the reliability of the

main turbine bypass system.

Description: The main turbine steam bypass system is designed to control steam pressure

when reactor steam generation exceeds turbine requirements during unit startup, sudden

load reduction, and cooldown. It allows excess steam flow from the reactor to the condenser

without going through the turbine. The system is comprised of nine valves that have a total

bypass capacity of approximately 25 percent of the nuclear steam supply system rated steam

flow. The main turbine bypass system is designed to limit the peak pressure in the main

steam lines and maintain reactor pressure within acceptable limits during events that cause

rapid pressurization such that the safety limit minimum critical power ration is not exceeded.

Each of the nine BPVs consist of a dual-acting actuator that uses EHC fluid flow both over

and under an actuator piston to allow for precise control in both the open and close direction

of the valve. EHC fluid is directed to the top and bottom of the actuator piston using an

electronic servo. When a BPV is closed, the servo directs EHC fluid to the top of the actuator

piston at full EHC system pressure (approximately 1600 pounder per square inch) to maintain

the valve closed, with some residual amount of fluid maintained at the bottom of the piston to

support a fast opening function. For the BPV to open, the servo repositions to increase the

volume of fluid at the bottom of the actuator piston.

On May 14, 2022, during Unit 1 shutdown for a planned maintenance outage, operators

received a low-level alarm for the EHC fluid reservoir. Operators entered the abnormal

operating procedure for response to EHC leaks, and dispatched operators into the plant in an

attempt to identify the leak location. After approximately 24 minutes, operators in the main

control room decided to secure the in-service EHC pump, based on the leak location not

being identified, and the fact that Unit 1 had entered OPCON 4 (Cold Shutdown)

approximately 8 minutes prior to receipt of the alarm with shutdown cooling already placed in-

service following closure of the final BPV (BPV-1) during the plant cooldown. Trending of

plant data for EHC level estimated the leak was approximately 6.5 gallons per minute (gpm).

Subsequent operator entry into the main condenser bay identified the leak location was from

BPV-1. Upon disassembly of the BPV-1 for repairs, it was identified that there was a loose

mounting bolt and deteriorated o-ring from one of four bolts that secure the actuator assembly

to the servo mounting plate, which is referred to as the tombstone. The tombstone is

designed with internal fluid ports that direct EHC fluid flow from the servo to the actuator. The

loose mounting bolt was therefore determined to have allowed pressurized EHC fluid to leak

from the mating surface between the tombstone and the actuator following closure of BPV-1,

which is the last BPV to close during unit cooldown.

Constellation performed a WGE under IR 4499745, and determined that the loose mounting

bolt was most likely caused by an o-ring extruding through a clearance gap between the

tombstone and actuator, as a result of inadequate procedural guidance that omitted any steps

to check for clearance gaps to ensure for proper alignment between mating surfaces.

Specifically, Limerick procedure MA-LG-763-473, Disassemble and Assemble Main Steam

BPV Actuator/Spring Can, was used during the previous reassembly of the BPV-1 actuator

and tombstone following the completion of preventive maintenance activities in 2012, under

work order (WO) R1130130. Procedure step 4.6.17 specified a torque value of 95 foot-

pounds, applied over 3 torque passes, but did not include a step to check clearance gaps to

ensure proper alignment between mating surfaces.

The inspectors reviewed WGE 4499745, as well as the completed WO R1130130 from 2012,

and verified that step 4.6.17 of MA-LG-763-473 was signed off as completed with the

specified torque value of 95 foot-pounds. The inspectors also reviewed procedure MA-LG-

763-473, Revision 0, and noted that it was issued in 2012, just prior to performance of WO

R1130130. The inspectors subsequently reviewed Constellation procedure MA-AA-736-600,

Torquing and Tightening of Bolted Connections, Revision 14, issued in 2022, and noted that

Section 4.2, Connection Reassembly, included steps to remove all clearance gaps during

application of torque passes, and contained clearance gap criteria for misaligned joints. The

inspectors subsequently reviewed the equivalent Limerick maintenance procedure in effect in

2012, MA-LG-716-1017, Control of Bolting / Torquing / Tensioning, Revision 0 (issued in

2010), and noted that section 7.2.5 covered torque sequencing and contained steps to

ensure uniform surface alignment, including steps to ensure uniform gap checks for

misaligned flanges. Based on this procedure review, the inspectors determined that it was

reasonably within Limericks ability to foresee and correct the inadequate instructions for BPV

reassembly contained in maintenance procedure MA-LG-763-473 that was issued in 2012,

and the inspectors therefore determined that uneven clearance gaps between the tombstone

and actuator should have been prevented to ensure reliable BPV operation.

Corrective Actions: Constellation replaced the failed BPV-1 actuator and verified all four of

the tombstone-to-actuator mounting bolts were adequately torqued to the required values and

performed an extent of condition torque check on all the remaining BPV accessible bolts to

verify as-found values of 95 foot-pounds. Constellation assigned WGE action 4499745-14 to

add a step to procedure MA-LG-763-473 to ensure that clearance values were less than

0.0015 inches between the tombstone and the actuator. WGE action 4499745-15 was

created to scope torque checks of all remaining BPV bolts into the next refueling outages for

Unit 1 (1R20) and Unit 2 (2R17), and action 4499745-16 was created to evaluate creating a

new preventive maintenance task to perform torque checks, in between actuator inspection

preventive maintenance activities, if additional bolts are found loose under action 4499745-

15.

Corrective Action References: IRs 4499745, 4499944, 4499968, 4537024

Performance Assessment:

Performance Deficiency: The inspectors determined that Constellations inadequate

maintenance procedure instructions for BPV reassembly was reasonably within

Constellations ability to foresee and correct, and should have been prevented, and therefore

constituted a performance deficiency. Specifically, procedure MA-LG-763-473, Disassemble

and Assemble Main Steam BPV Actuator/Spring Can, Revision 0, did not contain adequate

instructions to ensure the BPV actuator and tombstone mounting surfaces were properly

aligned with consistent clearance gaps to prevent o-ring extrusion and EHC fluid leakage.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Equipment Performance attribute of the Mitigating

Systems cornerstone and adversely affected the cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. Specifically, failure to ensure properly assembly of the BPV-1

actuator resulted in a significant EHC fluid leak from the valve and challenged reliable

operation of the main turbine bypass system.

Significance: The inspectors assessed the significance of the finding using IMC 0609

Appendix A, The SDP for Findings At-Power. This finding was screened to Green using the

Mitigating Systems screening questions because it did not involve a design deficiency, did not

represent the loss of a train of TS equipment for longer than its allowed outage time, and did

not represent loss of a probabilistic risk analysis system or function.

Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to

this finding because the inspectors determined the finding did not reflect present licensee

performance. Specifically, the BPV-1 maintenance utilizing the deficient preventive

maintenance procedure was performed in 2012, and no maintenance was performed on the

actuator and tombstone of any other BPVs on either unit in the last three years using the

deficient preventive maintenance procedure.

Enforcement: Inspectors did not identify a violation of regulatory requirements associated

with this finding.

Inadequate performance monitoring and margin management associated with MSIV LLRT

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Barrier Integrity

Green

FIN 05000352,05000353/2022004-03

Open/Closed

[H.6] - Design

Margins

71152A

The inspectors identified a Green finding against procedure ER-AA-2003, System

Performance Monitoring and Analysis, Revision 8, because Constellation did not perform

adequate performance monitoring and analysis of MSIV LLRT results to ensure that

degrading trends were identified prior to challenging required limits during the operating

cycle.

Description: The inspectors performed a historical review of MSIV as-found LLRT data on

Unit 1, and noted in refueling outage 1R18 (spring of 2020) three of the eight MSIVs

exceeded the TS limit of 100 standard cubic foot per hour (scfh): specifically, outboard valves

28B, 28C and 28D. TS 3.6.1.2 requires each MSIV leak rate to be less than or equal to 100

scfh, and the total leak rate through all four main steam lines to be less than or equal to 200

scfh, in operational conditions 1, 2 and 3. Constellation determined the 200 scfh total as-

found limit through all four main steam lines was not exceeded, because the leakage values

through the A main steam line, as well as the B, C, and D inboard MSIVs, were all

sufficiently low enough to ensure the total leakage was less than 200 scfh, when considering

the performance of the redundant inboard valve in each line. Two of the MSIVs (28C and

28D) were repaired in 1R18 to restore leakage below the 100 scfh single MSIV limit. For the

third MSIV (28D), an emergency license amendment was approved (ML20098C922) to allow

for a one-time TS change from 100 scfh to 105 scfh, due to challenges related to the COVID-

19 public health emergency.

The inspectors reviewed the LLRT performance data for the 28C and 28D MSIVs and noted

progressively increasing trends from 1R15 through 1R18. As a result, inspectors determined

that further review was warranted to understand whether appropriate MSIV LLRT

performance monitoring and margin management was being performed to ensure leak rates

were maintained below required limits during plant operation.

The inspectors reviewed MSIV maintenance history, and noted MSIVs did not have regularly

scheduled in-body preventive maintenance activities to proactively limit valve seat leakage,

and further noted that no in-body maintenance was performed on the 28C or 28D during the

time period from 1R15 until 1R18, when as-found results exceeded TS limits. The inspectors

noted that MSIVs at Limerick were exempt from 10 CFR Part 50, Appendix J, Primary

Containment Leakage Testing, and were therefore not subject to overall allowable

containment leakage limits required under Appendix J. The inspectors reviewed design

analysis LM-0646, Re-analysis of loss of coolant accident (LOCA) Using Alternate Source

Terms, Revision 6, and noted the TS 3.6.1.2 total MSIV leakage limit of 200 scfh was used

as an analytical input to validate the radiological consequences of a LOCA remained below

regulatory limits. The inspectors subsequently reviewed ST-4-LLR-001-1, The Local Leak

Rate (LLR) Program an Accountability Test, Revision 18, and ST-4-LLR-03/4/5/61-001,

Main Steam Line A/B/C/D LLR STs, Revisions 16, 15, 15, and 16, respectively, and noted

the acceptance criteria were established at the TS 3.6.1.2 limits. The inspectors noted that

there was no established margin between the LLRT ST limits, the LM-0646 analysis of

record, and the TS 3.6.1.2 limits.

The inspectors reviewed Constellation procedure ER-AA-2003, System Performance

Monitoring and Analysis, Revision 8, and noted that performance monitoring plans were

required for Tier 1 systems, which included the main steam system. Step 4.1.5 requires

establishment of alert levels and action levels. An alert level is described as a parameter level

that when exceeded is indicative of equipment degradation and requires IR initiation. An

action level is described as the threshold where action is required to prevent a consequential

event, though consequential events are undefined. Attachment 2 further describes monitoring

alert level considerations, and states that monitoring bands and frequencies should be

sufficient to identify degrading trends before design, operating, or licensing requirements are

challenged. In addition, Attachment 1 lists items to consider for trending, and refers to ER-

AA-2007, Management of Design and Operating Margins, Revision 8, which discusses how

to identify and control design and analytical margins. The inspectors reviewed the main

steam performance monitoring plan, and noted MSIV LLR STs were included in the plan, but

the alert and action levels were each established at the TS limits. The inspectors further

noted the MSIV LLR STs did not establish any administrative limits. The inspectors therefore

concluded that Constellation did not adequately perform step 4.1.5 of ER-AA-2003 to conduct

performance monitoring of MSIV LLRT data, because alert levels were not established to

indicate equipment degradation, and IRs were not initiated until TS limits were exceeded.

Corrective Actions: Constellation performed industry benchmarking and captured the

performance deficiency under IR 4553559, to evaluate the issue and develop appropriate

corrective actions. There were no violations of regulatory requirements that warranted

immediate corrective action, because both C and D outboard MSIVs had been repaired in

1R18 and there were no existing MSIVs with adverse trends.

Corrective Action References: IRs 4553559, 4331517, 4331518, 4331519

Performance Assessment:

Performance Deficiency: The inspectors determined that Constellations inadequate

performance monitoring and analysis in accordance with station procedures was reasonably

within Constellations ability to foresee and correct, should have been prevented, and was

therefore determined to be a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because if left uncorrected, it would have the potential to lead to a more significant safety

concern. Specifically, the inspectors determined that if no additional actions were taken to

monitor MSIV leakage performance, then TS and analytical limits could be exceeded during

the operating cycle.

Significance: The inspectors assessed the significance of the finding using IMC 0609,

Appendix A, The SDP for Findings At-Power. The inspectors utilized IMC 0609, Appendix A,

Exhibit 3, Barrier Integrity Screening Questions, to determine this finding was of very low

safety significance (Green) because it did not represent an actual open pathway in the

reactor containment barrier, and did not involve a failure of the any one of the following: the

containment isolation system, containment pressure control equipment, containment heat

removal components, or severe accident mitigation features.

Cross-Cutting Aspect: H.6 - Design Margins: The organization operates and maintains

equipment within design margins. Margins are carefully guarded and changed only through a

systematic and rigorous process. Special attention is placed on maintaining fission product

barriers, defense-in-depth, and safety-related equipment. Specifically, Constellation did not

perform adequate performance monitoring of MSIV LLRT results to guard and maintain

design margins to the allowable limits and did not place special attention on maintaining

containment barrier margins below analyzed limits.

Enforcement: Inspectors did not identify a violation of regulatory requirements associated

with this finding.

Unresolved Item

(Open)

Failure to follow maintenance procedure results in EDG JW

leak

URI 05000352,05000353/2022004-04

71152A

Description: On August 2, 2022, during a monthly ST of D21 EDG at full load, equipment

operators discovered a JW leak from a threaded fitting connection on a 0.25-inch diameter

tubing instrument root valve connection to the five-inch JW piping header. At approximately

30 minutes into the loaded run, operators measure leakage at 0.37 ounces per minute. Just

prior to completion of the two-hour loaded run, operators measure leakage at 0.78 ounces

per minute. Operators subsequently declared D21 EDG inoperable, because leakage was

measured above the pre-determined operability limit of 0.5 ounces per minute, as calculated

in Technical Evaluation (TE) 202873-01. The inspectors noted the 0.5 ounce per minute limit

supported successful operation of the EDG over the seven-day mission time required for TS

operability, without credit for inventory make-up to the closed-loop JW sub-system. The

inspectors further noted that Updated Final Safety Analysis Report section 9.5.5.2.1, stated

that normal maintenance of system components will ensure that leakage rates will be kept

below the amount requiring tank makeup within a seven-day period. Operators determined

that D21 EDG remained available, because leakage was not expected to exceed the 24-hour

probabilistic risk assessment mission time limit of 3.5 ounces per minute, based on no visible

cracks observed in the fitting connection, and no evidence that there was a risk of complete

fitting failure. In addition, the downstream (JW outlet) side of the instrument root valve was

noted to consist of a second, leak-tight, threaded connection to a pressure switch and small

diameter hard pipe tubing, such that complete unthreading of the upstream (JW inlet)

threaded connection to the JW header was determined by Constellation to be very unlikely.

On August 3, 2022, Constellation performed corrective maintenance repairs that consisted of

tagging out D21 EDG, draining the JW system, disassembling the two fittings on either side of

the instrument root valve, replacing a reducer coupling at the threaded connection between

the instrument root valve and JW header, re-installing the threaded fittings on either side of

the instrument root valve one at a time, and performing an unloaded EDG run with no JW

leakage observed from the re-assembled threaded connections.

Following corrective maintenance, Constellation performed WGE 4514473-12, to determine

the cause of the leaking fitting that resulted in D21 EDG inoperability. Constellation

determined that the cause was attributed to inadequately tightening the instrument root valve

fitting connection to the JW header during D21 EDG planned maintenance that was

completed on June 18, 2022. The WGE further stated that the instrument root valve fitting

was re-assembled under maintenance procedure M-020-002, Fairbanks Morse Opposed

Piston Diesel Generator Major Examination and General Maintenance. In addition, while no

leakage was noted during multiple post-maintenance test runs that were conducted on

June 17 and 18, Constellation noted that IR 4508586 was generated on June 30, during

equipment operator rounds with D21 EDG in a standby condition, which documented minor

weepage at the instrument root valve threaded connection to the JW piping header. The

inspectors noted that no observations of leakage were documented during the July 5, 2022,

monthly ST. As part of the WGE, Constellation sent the reducer coupling, which was removed

during the August 3 corrective maintenance, off-site for a failure analysis. No presence of

cracks, galling, or cross-threading were noted in the reducer coupling.

The inspectors reviewed the WGE, and discussed the D21 EDG JW leak with maintenance

technicians, operators, and engineers. The inspectors agreed with Constellations causal

determination in the WGE. In addition, the inspectors noted that after the D21 EDG

instrument root valve fitting connection was not properly tightened during planned

maintenance that completed on June 18, minor leakage from the fitting was subsequently

discovered on June 30 that progressively degraded to 0.78 ounces per minute on August 2,

after accruing approximately 14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br /> of run time during post-maintenance test runs and

ST. Based on this information, the inspectors questioned Constellation as to whether the D21

EDG was inoperable for greater than the allowed outage time of 30 days, and whether it

therefore constituted a violation of TS Limiting Condition for Operation 3.8.1. At the close of

the inspection period, Constellation was re-evaluating the assumptions and inherent margin

in TE 202873-01, with respect to the allowable JW leakage over the 7-day mission time, in

response to the inspectors question.

Planned Closure Actions: The inspectors will review Constellation's re-evaluation of TE

202873-01 to understand the allowable JW leak rate in support of the 7-day mission time of

the D21 EDG, and whether the D21 EDG was inoperable from June 18 to August 2, 2021.

Licensee Actions: At the close of the inspection period, Constellation was re-evaluating the

assumptions and inherent margin in TE 202873-01, with respect to the allowable JW leakage

over the 7-day mission time, in response to the inspectors question.

Corrective Action References: IRs 4514473 and 4508586, and TE 202873

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On February 10, 2023, the inspectors presented the integrated inspection results to

Michael Gillin, Site Vice President, and other members of the licensee staff.

On December 15, 2022, the inspectors presented the IP 71124.03 and IP 71124.04

inspection results to Mike Gillin, Site Vice President, and other members of the licensee

staff.

On November 10, 2022, the inspectors presented the IP 71124.07, Radiological

Environmental Monitoring Program, inspection results to Matt Bonanno, Plant Manager,

and other members of the licensee staff.