IR 05000275/2017002: Difference between revisions

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=Text=
=Text=
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION IV 1600 E. LAMAR BLVD.
{{#Wiki_filter:UNITED STATES ust 10, 2017


ARLINGTON, TX 76011-4511 August 10, 2017 Mr. Edward Senior Vice President and Chief Nuclear Officer Pacific Gas and Electric Company Diablo Canyon Power Plant P.O. Box 56, Mail Code 104/6 Avila Beach, CA 93424 SUBJECT: DIABLO CANYON POWER PLANT
==SUBJECT:==
- NR C INTEGRATED IN SPECTION REPORT 05000275/201700 2 and 05000323/201700
DIABLO CANYON POWER PLANT - NRC INTEGRATED INSPECTION REPORT 05000275/2017002 and 05000323/2017002


==Dear Mr. Halpin:==
==Dear Mr. Halpin:==
On June 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Diablo Canyon Power Plant
On June 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Diablo Canyon Power Plant, Units 1 and 2. On July 11, 2017, the NRC inspectors discussed the results of this inspection with Mr. J. Welsch, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.
, Units 1 and 2. On July 11, 2017
, the NRC inspectors discussed the results of this inspection with Mr. J. Welsch, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.


NRC inspectors documented two finding s of very low safety significance (Green) in this report.
NRC inspectors documented two findings of very low safety significance (Green) in this report.


These finding s involved violation s of NRC requirements. Additionally, NRC inspectors documented two Severity Level IV (SL-IV) violation s with no associated finding s. The NRC is treating these violation s as non-cited violation s (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.
These findings involved violations of NRC requirements. Additionally, NRC inspectors documented two Severity Level IV (SL-IV) violations with no associated findings. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.


If you contest the violation s or significance of the se NCV s , you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S.
If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC resident inspector at the Diablo Canyon Power Plant.


Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC resident inspector at the Diablo Canyon Power Plant
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC resident inspector at the Diablo Canyon Power Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.
. If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S.
 
Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC resident inspector at the Diablo Canyon Power Plant
. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, "Public Inspections, Exemptions, Requests for Withholding.
 
"


Sincerely,
Sincerely,
/RA/
/RA/
Mark S. Haire, Branch Chief Project Branch A Division of Reactor Projects Docket Nos.
Mark S. Haire, Branch Chief Project Branch A Division of Reactor Projects Docket Nos. 05000275 and 05000323 License Nos. DPR-80 and DPR-82
 
0 50 00 275 and 05000 323 License Nos
. DPR-80 and DPR-82  


===Enclosure:===
===Enclosure:===
Inspection Report 05000 275/201700 2 and 05000 323/201700 2 w/ Attachment s: 1. Supplemental Information 2. RFI for Inservice Inspection 3. RFI for O
Inspection Report 05000275/2017002 and 05000323/2017002 w/ Attachments:
 
1. Supplemental Information 2. RFI for Inservice Inspection 3. RFI for O
REGION IV Docket: 05000275; 05000323 License: DPR-80; DPR-82 Report: 05000 275/20 17 0 0 2; 05000323/201700 2 Licensee: Pacific Gas and Electric Company Facility: Diablo Canyon Power Plant, Units 1 and 2 Location: 7 1/2 miles NW of Avila Beach Avila Beach, CA Dates: April 1 through June 3 0, 20 17 Inspectors:
C. Newport, Senior Resident Inspector J. Reynoso, Resident Inspector J. Choate, Acting Resident Inspector I. Anchondo, Reactor Inspector T. Farina, Senior Operations Engine er C. Osterholtz, Senior Operations Engineer C. Steely, Operations Engineer L. Carson II, Sr. Health Physicist J. O'Donnell, CHP, Health Physicist G. George, Senior Reactor Inspector, Engineering Branch 1
, Lead S. Makor, Reactor Inspector, Engineering Branch 2 C. Stott, Reactor Inspector, Engineering Branch 1 Approved By: Mark S. Haire Chief, Project Branch A Division of Reactor Projects


2  
REGION IV==
Docket: 05000275; 05000323 License: DPR-80; DPR-82 Report: 05000275/2017002; 05000323/2017002 Licensee: Pacific Gas and Electric Company Facility: Diablo Canyon Power Plant, Units 1 and 2 Location: 7 1/2 miles NW of Avila Beach Avila Beach, CA Dates: April 1 through June 30, 2017 Inspectors: C. Newport, Senior Resident Inspector J. Reynoso, Resident Inspector J. Choate, Acting Resident Inspector I. Anchondo, Reactor Inspector T. Farina, Senior Operations Engineer C. Osterholtz, Senior Operations Engineer C. Steely, Operations Engineer L. Carson II, Sr. Health Physicist J. ODonnell, CHP, Health Physicist G. George, Senior Reactor Inspector, Engineering Branch 1, Lead S. Makor, Reactor Inspector, Engineering Branch 2 C. Stott, Reactor Inspector, Engineering Branch 1 Approved Mark S. Haire By: Chief, Project Branch A Division of Reactor Projects 1  Enclosure


=SUMMARY=
=SUMMARY=
IR 05000275/201700 2, 05000323/201700 2; 04/01/20 17 - 06/30/20 17; Diablo Canyon Power Plant; inservice inspection activities, licensed operator requalification program and licensed operator performance, refueling and other outage activities  The inspection activities described in this report were performed between April 1 and June 30 , 2017, by the resident inspectors at Diablo Canyon Power Plant and inspectors from the NRC's Region IV office. Two findings of very low safety significance (Green) are documented in this report.
IR 05000275/2017002, 05000323/2017002; 04/01/2017 - 06/30/2017; Diablo Canyon Power


These finding s involved violation s of NRC requirements. Additionally, NRC inspectors documented two Severity Level IV violation s with no associated finding s. The significance of inspection findings is indicated by their color (i.e., Green , greater than Green, White, Yellow, or Red), determined using Inspection Manual Chapter 0609, "Significance Determination Process," dated April 29, 2015.
Plant; inservice inspection activities, licensed operator requalification program and licensed operator performance, refueling and other outage activities The inspection activities described in this report were performed between April 1 and June 30, 2017, by the resident inspectors at Diablo Canyon Power Plant and inspectors from the NRCs Region IV office. Two findings of very low safety significance (Green) are documented in this report. These findings involved violations of NRC requirements.


Their cross-cutting aspects are determined using Inspection Manual Chapter 0310, "Aspects within the Cross-Cutting Areas," dated December 4, 2014
Additionally, NRC inspectors documented two Severity Level IV violations with no associated findings. The significance of inspection findings is indicated by their color (i.e., Green, greater than Green, White, Yellow, or Red), determined using Inspection Manual Chapter 0609,
. Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy.
Significance Determination Process, dated April 29, 2015. Their cross-cutting aspects are determined using Inspection Manual Chapter 0310, Aspects within the Cross-Cutting Areas, dated December 4, 2014. Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, dated July 2016.
 
The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG
-1649, "Reactor Oversight Process
," dated July 2016.


===Cornerstone: Mitigating Systems===
===Cornerstone: Mitigating Systems===
: '''Green.'''
: '''Green.'''
The inspector s identified a non-cited violation of the licensee's risk-informed inservice inspection program (which is their alternative to portions of the ASME Code
The inspectors identified a non-cited violation of the licensees risk-informed inservice inspection program (which is their alternative to portions of the ASME Code,
, Section XI inservice inspection program approved in accordance with 10 CFR 50.55a(z)) for the failure to properly expand the scope of additional welds to inspect. Specifically, a rejectable flaw on a pipe weld in the pressurizer sp ray line was identified during refueling outage 1R19 while performing an ultrasonic examination. The licensee expanded th e inspection scope by four additional welds, but failed to select those assigned with the same degradation. For immediate corrective actions, the licensee identified and intended to inspect four additional welds assigned to the same degradation mechanism as required by the risk-informed inservice inspection program.
Section XI inservice inspection program approved in accordance with 10 CFR 50.55a(z)) for the failure to properly expand the scope of additional welds to inspect. Specifically, a rejectable flaw on a pipe weld in the pressurizer spray line was identified during refueling outage 1R19 while performing an ultrasonic examination. The licensee expanded the inspection scope by four additional welds, but failed to select those assigned with the same degradation. For immediate corrective actions, the licensee identified and intended to inspect four additional welds assigned to the same degradation mechanism as required by the risk-informed inservice inspection program. This issue was entered into the licensees corrective action program as Notification 50920222.


This issue was entered into the licensee's corrective action program as Notification 50920222. The licensee's failure to properly expand the weld examination scope as required by the risk-informed inservice inspection program was a performance deficiency. The performance deficiency was more than minor because it was associated with the equipment performance attribute of the Mitigating System Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to select additional welds that were susceptible to the same degradation mechanism as weld WIB-378 placed the plant at an increased risk due to the potential of having an active degradation mechanism that could affect additional components. Using Inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power," dated June 19, 2012, the inspector s determined the finding screened as having very low significance (Green) because: (1) it was not a design deficiency; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and (4)did not result in the loss of a high safety-significant non-technical specification train. This finding had a cross-cutting aspect in the area of human performance associated with change management because leaders failed to use a systematic process for evaluating and implementing the change to a risk-informed inservice inspection program. The implementing procedure failed to include the reference to "degradation mechanism" allowing for a misinterpretation of weld expansion requirements once a flaw was identified in a weld WIB-378 [H.3]. (Section 1R08) SL-IV. The inspectors identified a Severity Level IV , non-cited violation of 10 CFR 55.21 , "Medical Examination," for the licensee's failure to ensure that a medical examination by a physician to determine satisfaction of 10 CFR 55.33(a)(1)requirements was conducted every 2 years for two licensed senior operators. Specifically, one licensed senior operator exceeded the two-year medical examination requirement by approximately 16 months between November 27, 2015, and April 6, 2017. A second licensed senior operator exceeded the 2-year medical examination requirement by 4 months between November 19, 2016, and April 6, 2017. As a corrective action, the licensee has conducted the required medical examination for one senior operator and initiated a license termination request for the other senior operator.
The licensees failure to properly expand the weld examination scope as required by the risk-informed inservice inspection program was a performance deficiency. The performance deficiency was more than minor because it was associated with the equipment performance attribute of the Mitigating System Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to select additional welds that were susceptible to the same degradation mechanism as weld WIB-378 placed the plant at an increased risk due to the potential of having an active degradation mechanism that could affect additional components. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, the inspectors determined the finding screened as having very low significance (Green) because: (1) it was not a design deficiency; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and (4)did not result in the loss of a high safety-significant non-technical specification train. This finding had a cross-cutting aspect in the area of human performance associated with change management because leaders failed to use a systematic process for evaluating and implementing the change to a risk-informed inservice inspection program. The implementing procedure failed to include the reference to degradation mechanism allowing for a misinterpretation of weld expansion requirements once a flaw was identified in a weld WIB-378 [H.3]. (Section 1R08)
* SL-IV. The inspectors identified a Severity Level IV, non-cited violation of 10 CFR 55.21,
Medical Examination, for the licensees failure to ensure that a medical examination by a physician to determine satisfaction of 10 CFR 55.33(a)(1) requirements was conducted every 2 years for two licensed senior operators. Specifically, one licensed senior operator exceeded the two-year medical examination requirement by approximately 16 months between November 27, 2015, and April 6, 2017. A second licensed senior operator exceeded the 2-year medical examination requirement by 4 months between November 19, 2016, and April 6, 2017. As a corrective action, the licensee has conducted the required medical examination for one senior operator and initiated a license termination request for the other senior operator. This issue was entered into the licensees corrective action program as Notification 50912407.


This issue was entered into the licensee's corrective action program as Notification 50912407
The failure of the facility licensee to conduct required biennial medical examinations for two licensed senior operators was a performance deficiency. This issue was evaluated using the traditional enforcement process because it negatively impacted the NRCs ability to perform its regulatory oversight function. Specifically, the failure to comply with medical testing requirements for two operators compromised the facility licensees ability to assure conformance to medical standards, detect non-conforming medical conditions, and report non-conformances to the NRC. This performance deficiency was determined to be Severity Level IV because it fits the Severity Level IV example of Enforcement Policy Section 6.4.d.1,
. The failure of the facility licensee to conduct required biennial medical examinations for two licensed senior operators was a performance deficiency. This issue was evaluated using the traditional enforcement process because it negatively impacted the NRC's ability to perform its regulatory oversight function. Specifically, the failure to comply with medical testing requirements for two operators compromised the facility licensee's ability to assure conformance to medical standards, detect non-conforming medical conditions, and report non-conformances to the NRC. This performance deficiency was determined to be Severity Level IV because it fits the Severity Level IV example of Enforcement Policy Section 6.4.d.1, "Violation Examples: Licensed Reactor Operators.This section states, "Severity Level IV violations involve, for example -
Violation Examples: Licensed Reactor Operators. This section states, Severity Level IV violations involve, for example  (b) an individual operator who did not meet the American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.4, Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants, Section 5, Health Requirements and Disqualifying Conditions, as certified on NRC Form 396, Certification of Medical Examination by Facility Licensee, required by 10 CFR 55.23, Certification, but who did not perform the functions of a licensed operator or senior operator while having a disqualifying medical condition. No cross-cutting aspect was assigned because the violation was processed using traditional enforcement.
  (b) an individual operator who did not meet the American National Standards Institute/American Nuclear Society (ANSI/ANS)3.4," "Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants," Section 5, "Health Requirements and Disqualifying Conditions," as certified on NRC Form 396, "Certification of Medical Examination by Facility Licensee," required by 10 CFR 55.23, Certification, but who did not perform the functions of a licensed operator or senior operator while having a disqualifying medical condition.No cross-cutting aspect was assigned because the violation was processed using traditional enforcement.


(Section 1R11.3) SL-IV. The inspectors identified a Severity Level IV
  (Section 1R11.3)
, non-cited violation of 10 CFR 55.25 , "Incapacitation Because of Disability or Illness
* SL-IV. The inspectors identified a Severity Level IV, non-cited violation of 10 CFR 55.25,
," for the licensee's failure to notify the NRC within 30 days of a change to one licensed senior operator's medical condition. Specifically, the licensed senior operator developed a permanent medical condition which caused him to permanently leave the site on December 1, 2014, and transition into a long-term disability program on April 23, 2015. The licensee did not notify the NRC of this change in medical condition. As a corrective action, the licensee initiated a license termination request for the affected operator, effective April 6, 2017. This issue was entered into the licensee's corrective action program as Notification 50912407
Incapacitation Because of Disability or Illness, for the licensees failure to notify the NRC within 30 days of a change to one licensed senior operators medical condition. Specifically, the licensed senior operator developed a permanent medical condition which caused him to permanently leave the site on December 1, 2014, and transition into a long-term disability program on April 23, 2015. The licensee did not notify the NRC of this change in medical condition. As a corrective action, the licensee initiated a license termination request for the affected operator, effective April 6, 2017. This issue was entered into the licensees corrective action program as Notification 50912407.
. The failure of the facility licensee to notify the NRC within 30 days of a change in a licensed senior operator's medical condition was a performance deficiency. This issue was evaluated using the traditional enforcement process because it negatively impacted the NRC's ability to perform its regulatory oversight function. Specifically, the failure to report changes in a licensed senior operator's medical condition prevented the NRC from taking action to issue either a license amendment or termination, as appropriate. This performance deficiency was determined to be Severity Level IV because it fits the Severity Level IV example of Enforcement Policy Section 6.4.d.1, "Violation Examples: Licensed Reactor Operators."  This section states, "Severity Level IV violations involve, for example (b) an individual operator who did not meet the American National Standards Institute/American Nuclear Society (ANSI/ANS)3.4," "Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants," Section 5, "Health Requirements and Disqualifying Conditions," as certified on NRC Form 396, "Certification of Medical Examination by Facility Licensee," required by 10 CFR 55.23, Certification, but who did not perform the functions of a licensed operator or senior operator while having a disqualifying medical condition."  No cross-cutting aspect was assigned because the violation was processed using traditional enforcement.


(Section 1R11.3)
The failure of the facility licensee to notify the NRC within 30 days of a change in a licensed senior operators medical condition was a performance deficiency. This issue was evaluated using the traditional enforcement process because it negatively impacted the NRCs ability to perform its regulatory oversight function. Specifically, the failure to report changes in a licensed senior operators medical condition prevented the NRC from taking action to issue either a license amendment or termination, as appropriate. This performance deficiency was determined to be Severity Level IV because it fits the Severity Level IV example of Enforcement Policy Section 6.4.d.1, Violation Examples: Licensed Reactor Operators. This section states, Severity Level IV violations involve, for example (b) an individual operator who did not meet the American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.4, Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants, Section 5, Health Requirements and Disqualifying Conditions, as certified on NRC Form 396, Certification of Medical Examination by Facility Licensee, required by 10 CFR 55.23, Certification, but who did not perform the functions of a licensed operator or senior operator while having a disqualifying medical condition. No cross-cutting aspect was assigned because the violation was processed using traditional enforcement. (Section 1R11.3)
: '''Green.'''
: '''Green.'''
The inspectors reviewed a self-revealing , non-cited violation of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," because PG&E personnel failed to follow the requirements of AD7.ID14, "Assessment of Integrated Risk," Revision 11. Specifically, PG&E personnel failed to obtain shift manager permission, conduct a protected equipment briefing, and document shift manager approval prior to performing work on protected equipment. This resulted in a loss of flow of cooling water to one of two in-service shutdown cooling residual heat removal heat exchangers and subsequent perturbation in reactor coolant system temperature during refueling outage 1R20. The inspectors determined that PG&E's failure to follow AD7.ID14, "Assessment of Integrated Risk," Section 5.14 "Performing Work on Posted Protected Equipment," was a performance deficiency within PG&E's ability to foresee and correct. This performance deficiency was considered to be more than minor because it impacted the configuration control attribute of the Mitigating Systems cornerstone and its objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the loss of cooling flow to the RHR heat exchanger while in shutdown cooling mode resulted in a perturbation in RCS temperature of approximately degrees Fahrenheit. The finding was evaluated in accordance with IMC 0609, Appendix G, "Shutdown Operations Significance Determination Process," and determined to be of very low safety significance (Green) since it did not represent a loss of system safety function of at least a single train for greater than four hours. The finding had a cross-cutti ng aspect in the area of human performance associated with conservative bias because PG&E personnel did not use decision-making practices that emphasize prudent choices over those that are simply allowable. Specifically, despite being authorized to close component cooling water cross connect valves by the work control process, PG&E personnel did not question the impact of their actions on shutdown cooling
The inspectors reviewed a self-revealing, non-cited violation of 10 CFR 50,
[H.14]. (Section 1R20)5
Appendix B, Criterion V, Instructions, Procedures, and Drawings, because PG&E personnel failed to follow the requirements of AD7.ID14, Assessment of Integrated Risk,
Revision 11. Specifically, PG&E personnel failed to obtain shift manager permission, conduct a protected equipment briefing, and document shift manager approval prior to performing work on protected equipment. This resulted in a loss of flow of cooling water to one of two in-service shutdown cooling residual heat removal heat exchangers and subsequent perturbation in reactor coolant system temperature during refueling outage 1R20.
 
The inspectors determined that PG&Es failure to follow AD7.ID14, Assessment of Integrated Risk, Section 5.14 Performing Work on Posted Protected Equipment, was a performance deficiency within PG&Es ability to foresee and correct. This performance deficiency was considered to be more than minor because it impacted the configuration control attribute of the Mitigating Systems cornerstone and its objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the loss of cooling flow to the RHR heat exchanger while in shutdown cooling mode resulted in a perturbation in RCS temperature of approximately 8 degrees Fahrenheit. The finding was evaluated in accordance with IMC 0609, Appendix G, Shutdown Operations Significance Determination Process, and determined to be of very low safety significance (Green) since it did not represent a loss of system safety function of at least a single train for greater than four hours. The finding had a cross-cutting aspect in the area of human performance associated with conservative bias because PG&E personnel did not use decision-making practices that emphasize prudent choices over those that are simply allowable. Specifically, despite being authorized to close component cooling water cross connect valves by the work control process, PG&E personnel did not question the impact of their actions on shutdown cooling [H.14].
  (Section 1R20)


=PLANT STATUS=
=PLANT STATUS=
Line 95: Line 82:
Units 1 and 2 began the inspection period at full power.
Units 1 and 2 began the inspection period at full power.


On April 23, 2017, Unit 1 was shut down for a planned refueling outage. On June 21, 2017, Unit 1 returned to operation and began a controlled power ascension; it returned to full power on June 27, 2017. Units 1 and 2 operated at or near full power for the remainder of the inspection period.
On April 23, 2017, Unit 1 was shut down for a planned refueling outage. On June 21, 2017, Unit 1 returned to operation and began a controlled power ascension; it returned to full power on June 27, 2017.
 
Units 1 and 2 operated at or near full power for the remainder of the inspection period.


REPORT DETAILS
REPORT DETAILS


===1. ===
==REACTOR SAFETY==
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness 1 R 01 Adverse Weather Protection (71111.01Summer Readiness for Offsite and Alternate AC Power Systems
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness
{{a|1R01}}
==1R01 Adverse Weather Protection==
{{IP sample|IP=IP 71111.01}}
Summer Readiness for Offsite and Alternate AC Power Systems


====a. Inspection Scope====
====a. Inspection Scope====
On June 23, 2017, the inspectors completed an inspection of the station's off
On June 23, 2017, the inspectors completed an inspection of the stations off-site and alternate-ac power systems. The inspectors inspected the material condition of these systems, including transformers and other switchyard equipment to verify that plant features and procedures were appropriate for operation and continued availability of off-site and alternate-ac power systems. The inspectors reviewed outstanding work orders and open condition reports for these systems. The inspectors walked down the switchyard to observe the material condition of equipment providing off-site power sources. The inspectors assessed corrective actions for identified degraded conditions and verified that the licensee had considered the degraded conditions in its risk evaluations and had established appropriate compensatory measures.
-site and alternate-ac power systems.


The inspectors inspected the material condition of these systems, including transformers and other switchyard equipment to verify that plant features and procedures were appropriate for operation and continued availability of off-site and alternate
The inspectors verified that the licensees procedures included appropriate measures to monitor and maintain availability and reliability of the off-site and alternate-ac power systems.
-ac power systems. The inspectors reviewed outstanding work orders and open condition reports for these systems
. The inspectors walked down the switchyard to observe the material condition of equipment providing off-site power sources. The inspectors assessed corrective actions for identified degraded conditions and verified that the licensee had considered the degraded conditions in its risk evaluations and had established appropriate compensatory measures.


The inspectors verified that the licensee's procedures included appropriate measures to monitor and maintain availability and reliability of the off
These activities constituted one sample of summer readiness of off-site and alternate-ac power systems, as defined in Inspection Procedure 71111.01.
-site and alternate-ac power systems. These activities constitute d one sample of summer readiness of off-site and alternate
-ac power systems , as defined in Inspection Procedure 71111.01.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
 
{{a|1R04}}
1 R 04 Equipment Alignment (71111.04)
==1R04 Equipment Alignment==
 
{{IP sample|IP=IP 71111.04}}
===.1 Partial Walk-Down===
===.1 Partial Walk-Down===


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed partial system walk
The inspectors performed partial system walk-downs of the following risk-significant systems:
-downs of the following risk
* April 6, 2017, Unit 2, safety injection system
-significant systems: April 6, 2017, Unit 2, safety injection system April 24, 2017, Unit 1, residual heat removal system May 1, 2017, Unit 1, reactor vessel refueling level indication system June 14-15, 2017, Unit 1, containment ventilation and air system June 21, 2017, Unit 2, containment spray system The inspectors reviewed the licensee's procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration
* April 24, 2017, Unit 1, residual heat removal system
. These activities constitute d five partial system walk
* May 1, 2017, Unit 1, reactor vessel refueling level indication system
-down sample s as defined i n Inspection Procedure 71111.04.
* June 14-15, 2017, Unit 1, containment ventilation and air system
* June 21, 2017, Unit 2, containment spray system The inspectors reviewed the licensees procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration.
 
These activities constituted five partial system walk-down samples as defined in Inspection Procedure 71111.04.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


===.2 Complete Walk===
===.2 Complete Walk-Down===
 
-Down


====a. Inspection Scope====
====a. Inspection Scope====
On June 29, 2017, the inspectors performed a complete system walk-down inspection of the Unit 1, containment fan cooling unit system. The inspectors reviewed the licensee's procedures and system design information to determine the correct system lineup for the existing plant configuration. The inspectors also reviewed outstanding work orders, open condition reports, in
On June 29, 2017, the inspectors performed a complete system walk-down inspection of the Unit 1, containment fan cooling unit system. The inspectors reviewed the licensees procedures and system design information to determine the correct system lineup for the existing plant configuration. The inspectors also reviewed outstanding work orders, open condition reports, in-process design changes, temporary modifications, and other open items tracked by the licensees operations and engineering departments. The inspectors then visually verified that the system was correctly aligned for the existing plant configuration.
-process design changes, temporary modifications, and other open items tracked by the licensee's operations and engineering departments.
 
The inspectors then visually verified that the system was correctly aligned for the existing plant configuration.


These activities constitute d one complete system wal k-down sample , as defined in Inspection Procedure 71111.04.
These activities constituted one complete system walk-down sample, as defined in Inspection Procedure 71111.04.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
 
{{a|1R05}}
1 R 05 Fire Protection (71111.05Quarterly Inspection
==1R05 Fire Protection==
{{IP sample|IP=IP 71111.05}}
Quarterly Inspection


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated the licensee's fire protection program for operational status and material condition. The inspectors focused their inspection on five plant areas important to safety
The inspectors evaluated the licensees fire protection program for operational status and material condition. The inspectors focused their inspection on five plant areas important to safety:
April 20, 2017, Units 1 and 2, auxiliary building fire areas located on the 64 foot elevation April 25, 2017, Unit 1 , containment building fire areas located on the 140 foot elevation April 2 5, 2017, Unit 1, containment building fire areas located on the 91 f oo t elevation May 4, 2017, Unit 1 , containment building fire areas located on the 117 foot elevation   June 28, 2017, Units 1 and 2, auxiliary building fire areas located at the 73 foot elevation For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensee's fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.
* April 20, 2017, Units 1 and 2, auxiliary building fire areas located on the 64 foot elevation
* April 25, 2017, Unit 1, containment building fire areas located on the 140 foot elevation
* April 25, 2017, Unit 1, containment building fire areas located on the 91 foot elevation
* May 4, 2017, Unit 1, containment building fire areas located on the 117 foot elevation
* June 28, 2017, Units 1 and 2, auxiliary building fire areas located at the 73 foot elevation For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensees fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.


These activities constitute d five quarterly inspection sample s , as defined in Inspection Procedure 71111.05.
These activities constituted five quarterly inspection samples, as defined in Inspection Procedure 71111.05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
 
{{a|1R06}}
1 R 06 Flood Protection Measures (71111.06)
==1R06 Flood Protection Measures==
{{IP sample|IP=IP 71111.06}}


====a. Inspection Scope====
====a. Inspection Scope====
O n April 27, 2017, the inspectors completed an inspection of underground bunkers susceptible to flooding. The inspectors selected underground vaults that contained risk-significant or multiple
On April 27, 2017, the inspectors completed an inspection of underground bunkers susceptible to flooding. The inspectors selected underground vaults that contained risk-significant or multiple-train cables whose failure could disable risk-significant equipment:
-train cables whose failure could disable risk
* April 27, 2017, Units 1 and 2, auxiliary salt water vault BPO44 The inspectors observed the material condition of the cables and splices and looked for evidence of cable degradation due to water intrusion. The inspectors verified that the cables and vaults met design requirements.
-significant equipment: April 27, 20 17 , Unit s 1 and 2 , auxiliary salt water vault BPO44 The inspectors observed the material condition of the cables and splices and looked for evidence of cable degradation due to water intrusion.
 
The inspectors verified that the cables and vaults met design requirements.


These activities constitute d completion of one bunker/manhole sample, as defined in Inspection Procedure 71111.06.
These activities constituted completion of one bunker/manhole sample, as defined in Inspection Procedure 71111.06.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
 
{{a|1R07}}
1 R 07 Heat Sink Performance (71111.07)
==1R07 Heat Sink Performance==
{{IP sample|IP=IP 71111.07}}


====a. Inspection Scope====
====a. Inspection Scope====
On June 26, 2017 , the inspectors completed an inspection of the readiness and availability of risk
On June 26, 2017, the inspectors completed an inspection of the readiness and availability of risk-significant heat exchangers. The inspectors reviewed the data from performance tests for the Unit 1 component cooling water heat exchangers. Additionally, the inspectors walked down the heat exchangers to observe their performance and material condition.
-significant heat exchangers. The inspectors reviewed the data from performance test s for the Unit 1 component cooling water heat exchangers
. Additionally, the inspectors walked down the heat exchangers to observe their performance and material condition.


These activities constitute d completion of one heat sink performance annual review sample , as defined in Inspection Procedure 71111.07.
These activities constituted completion of one heat sink performance annual review sample, as defined in Inspection Procedure 71111.07.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
 
{{a|1R08}}
1 R 08 Inservice Inspection Activities (71111.08)
==1R08 Inservice Inspection Activities==
{{IP sample|IP=IP 71111.08}}
The activities described in subsections 1 through 4 below constitute completion of one inservice inspection (ISI) sample, as defined in Inspection Procedure 71111.08.
The activities described in subsections 1 through 4 below constitute completion of one inservice inspection (ISI) sample, as defined in Inspection Procedure 71111.08.


Line 190: Line 181:
====a. Inspection Scope====
====a. Inspection Scope====
The inspector directly observed the following nondestructive examinations:
The inspector directly observed the following nondestructive examinations:
SYSTEM WELD/COMPONENT IDENTIFICATION EXAMINATION TYPE Residual Heat Removal Line 109 (Weld WIB-228) Ultrasonic Reactor Vessel Inlet Nozzle to DM Weld @
EXAMINATION SYSTEM             WELD/COMPONENT IDENTIFICATION TYPE Residual           Line 109 (Weld WIB-228)                       Ultrasonic Heat Removal Reactor Vessel Inlet Nozzle to DM Weld @ 67º                     Ultrasonic (Weld WIB-RC-2-20-SE)
67º (Weld WIB-RC-2-20-SE) Ultrasonic Reactor Vessel Inlet Nozzle to DM Weld @ 113º (Weld WIB-RC-3-18-SE) Ultrasonic The inspector reviewed records for the following nondestructive examinations:
Reactor Vessel Inlet Nozzle to DM Weld @ 113º                     Ultrasonic (Weld WIB-RC-3-18-SE)
SYSTEM WELD/COMPONENT IDENTIFICATION EXAMINATION TYPE Pressurizer Spray Line 15-4 (Weld WIB-378) Ultrasonic SYSTEM WELD/COMPONENT IDENTIFICATION EXAMINATION TYPE Residual Hea t Removal Line 109 (Weld WIB-228) Ultrasonic Reactor Vessel Inlet Nozzle to DM Weld @
The inspector reviewed records for the following nondestructive examinations:
293º (Weld WIB-RC-1-18-SE) Ultrasonic Reactor Vessel Inlet Nozzle to DM Weld @
EXAMINATION SYSTEM             WELD/COMPONENT IDENTIFICATION TYPE Pressurizer         Spray Line 15-4 (Weld WIB-378)               Ultrasonic EXAMINATION SYSTEM             WELD/COMPONENT IDENTIFICATION TYPE Residual Heat      Line 109 (Weld WIB-228)                       Ultrasonic Removal Reactor Vessel Inlet Nozzle to DM Weld @ 293º                   Ultrasonic (Weld WIB-RC-1-18-SE)
247º (Weld WIB-RC-4-18-SE) Ultrasonic Various Various (ASME Class 1 boundary)
Reactor Vessel Inlet Nozzle to DM Weld @ 247º                   Ultrasonic (Weld WIB-RC-4-18-SE)
Visual (V T-2) Various Test #8 (ASME Class 2 boundary) Visual (VT
Various           Various (ASME Class 1 boundary)               Visual (VT-2)
-2) During the review and observation of each examination, the inspector observed whether activities were performed in accordance with the ASME Code requirements and applicable procedures. The inspector reviewed two indications that were previously examined, and observed whether the licensee evaluated and accepted the indications in accordance with the ASME Code. The inspector also reviewed the qualifications of all nondestructive examination technicians performing the inspections to determine whether they were current.
Various           Test #8 (ASME Class 2 boundary)               Visual (VT-2)
During the review and observation of each examination, the inspector observed whether activities were performed in accordance with the ASME Code requirements and applicable procedures. The inspector reviewed two indications that were previously examined, and observed whether the licensee evaluated and accepted the indications in accordance with the ASME Code. The inspector also reviewed the qualifications of all nondestructive examination technicians performing the inspections to determine whether they were current.


The inspector directly observed a portion of the following welding activities:
The inspector directly observed a portion of the following welding activities:
SYSTEM WELD IDENTIFICATION EXAMINATION TYPE Containment Fan Cooling Unit Weld No. 38 & 40 Gas Tungsten Arc Welding The inspector reviewed whether the welding procedure specifications and the welders had been properly qualified in accordance with ASME Code
SYSTEM               WELD IDENTIFICATION                 EXAMINATION TYPE Containment Fan Weld No. 38 & 40                         Gas Tungsten Arc Cooling Unit                                            Welding The inspector reviewed whether the welding procedure specifications and the welders had been properly qualified in accordance with ASME Code, Section IX requirements.
, Section IX requirements. The inspector also determined that essential variables were identified, recorded in the procedure qualification record, and formed the bases for qualification of the welding procedure specifications.
 
The inspector also determined that essential variables were identified, recorded in the procedure qualification record, and formed the bases for qualification of the welding procedure specifications.


====b. Findings====
====b. Findings====
Green. The inspector identified a non-cited violation of the licensee's risk
Green. The inspector identified a non-cited violation of the licensees risk-informed inservice inspection program (which is their alternative to portions of the ASME Code, Section XI inservice inspection program approved in accordance with 10 CFR 50.55a(z))
-informed inservice inspection program (which is their alternative to portions of the ASME Code
for the failure to properly expand the scope of additional welds to inspect. Specifically, a rejectable flaw on a pipe weld in the pressurizer spray line was identified during refueling outage 1R19 while performing an ultrasonic examination. The licensee expanded the inspection scope by four additional welds but failed to select those assigned with the same degradation mechanism.
, Section XI inservice inspection program approved in accordance with 10 CFR 50.55a(z)) for the failure to properly expand the scope of additional welds to inspect. Specifically, a rejectable flaw on a pipe weld in the pressurizer sp ray line was identified during refueling outage 1R19 while performing an ultrasonic examination. The licensee expanded the inspection scope by four additional welds but failed to select those assigned with the same degradation mechanism
.


=====Description.=====
=====Description.=====
On November 8, 2001, the licensee received NRC approval to implement a risk-informed inservice inspection program for ASME Code
On November 8, 2001, the licensee received NRC approval to implement a risk-informed inservice inspection program for ASME Code, Class 1 and 2 piping welds.
, Class 1 and 2 piping welds. The risk-informed inservice inspection program was developed in accordance with Electric Power Research Institute (EPRI) Topical Report TR
-112657, "Revised Risk-Informed Inservice Inspection Evaluation," Revision B
-A. During refueling outage 1R19, the licensee was completing the remaining inspections for the third 10
-year ISI interval as required by ASME Code, Section XI. During an ultrasonic examination, a rejectable flaw was identified in the pressurizer spray line, weld WIB
-378. The results and corrective actions were documented in Notification 50809162. The risk-informed inservice inspection program assigns a risk profile of each Class 1 and 2 piping weld based on risk significance, consequence of failure, and failure potential. The purpose of assigning a failure potential is to differentiate welds that are affected by a specific degradation mechanism. Topical Report TR
-112657 provides the guidance to assign a degradation mechanism. Welds that do not meet the specific criteria are assigned to a failure potential without a degradation mechanism. When a flaw is identified, additional examinations are required to be performed to determine if an active degradation mechanism exist.


Procedure ISI ADD SUCCESS, "Additional, Supplemental
The risk-informed inservice inspection program was developed in accordance with Electric Power Research Institute (EPRI) Topical Report TR-112657, Revised Risk-Informed Inservice Inspection Evaluation, Revision B-A. During refueling outage
, and Successive Inspections," Revision 6, implements the guidance of additional inspections per Topical Report TR-112657. Section 4.2.6, states the following
: "All other examination s performed on piping welds per the ri sk-informed ISI Program Plan that detect flaws or relevant conditions require additional examinations on elements in segments subject to the same root cause conditions. The number of additional examinations shall be equivalent to the number examined initially for the current refueling outage, and shall include high risk-significant as well as medium risk
-significant elements (if needed) to reach the required number of additional elements
." The inspector noted that the term "elements" referred to selected welds per EPRI guidance. The inspector also noted that this procedural requirement was missing the reference to "degradation mechanism" in addition to "root cause conditions" as provided by Topical Report TR
-112657. Notification 50809162 documents that a flaw was identified in weld WIB
-378. Per the risk-informed inservice inspection program, this weld has a failure potential assigned to the degradation mechanism of Thermal Stratification, Cycling, and Striping (TASCS).


The licensee expanded the inspection scope to four additional examinations as required by Section 4.2.6 of Procedure ISI ADD SUCCESS. The inspector checked whether the selected welds had the same degradation mechanism as Weld WIB
{{a|1R19}}
-378 and identified that none of them had been assigned with TASCS as a degradation mechanism per their failure potential designation. The inspector concluded that although the licensee had correctly expanded the number of weld examinations it had failed to select those susceptible to TASCS.
==1R19 , the licensee was completing the remaining inspections for the third 10-year ISI==
 
interval as required by ASME Code, Section XI. During an ultrasonic examination, a rejectable flaw was identified in the pressurizer spray line, weld WIB-378. The results and corrective actions were documented in Notification 50809162.
 
The risk-informed inservice inspection program assigns a risk profile of each Class 1 and 2 piping weld based on risk significance, consequence of failure, and failure potential. The purpose of assigning a failure potential is to differentiate welds that are affected by a specific degradation mechanism. Topical Report TR-112657 provides the guidance to assign a degradation mechanism. Welds that do not meet the specific criteria are assigned to a failure potential without a degradation mechanism. When a flaw is identified, additional examinations are required to be performed to determine if an active degradation mechanism exist.
 
Procedure ISI ADD SUCCESS, Additional, Supplemental, and Successive Inspections, Revision 6, implements the guidance of additional inspections per Topical Report TR-112657. Section 4.2.6, states the following:
All other examinations performed on piping welds per the risk-informed ISI Program Plan that detect flaws or relevant conditions require additional examinations on elements in segments subject to the same root cause conditions. The number of additional examinations shall be equivalent to the number examined initially for the current refueling outage, and shall include high risk-significant as well as medium risk-significant elements (if needed) to reach the required number of additional elements.
 
The inspector noted that the term elements referred to selected welds per EPRI guidance. The inspector also noted that this procedural requirement was missing the reference to degradation mechanism in addition to root cause conditions as provided by Topical Report TR-112657.
 
Notification 50809162 documents that a flaw was identified in weld WIB-378. Per the risk-informed inservice inspection program, this weld has a failure potential assigned to the degradation mechanism of Thermal Stratification, Cycling, and Striping (TASCS).
 
The licensee expanded the inspection scope to four additional examinations as required by Section 4.2.6 of Procedure ISI ADD SUCCESS. The inspector checked whether the selected welds had the same degradation mechanism as Weld WIB-378 and identified that none of them had been assigned with TASCS as a degradation mechanism per their failure potential designation. The inspector concluded that although the licensee had correctly expanded the number of weld examinations it had failed to select those susceptible to TASCS.


=====Analysis.=====
=====Analysis.=====
The licensee's failure to properly expand the weld examination scope as required by the risk
The licensees failure to properly expand the weld examination scope as required by the risk-informed inservice inspection program was a performance deficiency. The performance deficiency was more than minor because it was associated with the equipment performance attribute of the Mitigating System Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to select additional welds that were susceptible to the same degradation mechanism as weld WIB-378 placed the plant at an increased risk due to the potential of having an active degradation mechanism that could affect additional components. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, the inspector determined the finding screened as having very low significance (Green)because: it was not a design deficiency; did not represent a loss of system and/or function; did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and did not result in the loss of a high safety-significant, non-technical specification train. This finding had a cross-cutting aspect in the area of Human Performance associated with Change Management because leaders failed to use a systematic process for evaluating and implementing the change to a risk-informed inservice inspection program. The implementing procedure failed to include the reference to degradation mechanism allowing for a misinterpretation of weld expansion requirements once a flaw was identified in weld WIB-378 [H.3].
-informed inservice inspection program was a performance deficiency. The performance deficiency was more than minor because it was associated with the equipment performance attribute of the Mitigating System Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to select additional welds that were susceptible to the same degradation mechanism as weld WIB
-378 placed the plant at an increased risk due to the potential of having an active degradation mechanism that could affect additional components. Using Inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At
-Power," dated June 19, 2012, the inspector determined the finding screened as having very low significance (Green) because: it was not a design deficiency; did not represent a loss of system and/or function; did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and did not result in the loss of a high safety
-significant
, non-technical specification train. This finding had a cross-cutting aspect in the area of Human Performance associated with Change Management because leaders failed to use a systematic process for evaluating and implementing the change to a risk
-informed inservice inspection program. The implementing procedure failed to include the reference to "degradation mechanism" allowing for a misinterpretation of weld expansion requirements once a flaw was identified in weld WIB-378 [H.3].  


=====Enforcement.=====
=====Enforcement.=====
Title 10 CFR 50.55a(z), states in part, that alternatives to the requirements of this section must be submitted and authorized prior to implementation.
Title 10 CFR 50.55a(z), states in part, that alternatives to the requirements of this section must be submitted and authorized prior to implementation.


The licensee received prior approval to implement a risk
The licensee received prior approval to implement a risk-informed inservice inspection process developed based on the EPRI Topical Report TR-112657, Revision B-A, as an alternative to applicable requirements of Section XI of the ASME Code. The risk-informed inservice inspection process requires that when flaws or relevant conditions are detected, additional examinations on elements in segments subject to the same root cause conditions or degradation mechanism are required. Contrary to the above, from November 1, 2015, until May 17, 2017, the licensee failed to conduct the required additional examinations on elements in segments subject to the same root cause conditions or degradation mechanism after flaws or relevant conditions were detected. Specifically, the licensee completed ultrasonic examinations of four additional pipe welds, but failed to select those that were assigned the same degradation mechanism as pipe weld WIB-378. As part of their corrective actions, the licensee, at the time of the inspection, identified and intended to inspect four additional welds assigned to the same degradation mechanism as required by the risk-informed inservice inspection program. Because the violation was of very low safety significance and it was entered into the corrective action program as Notification 50920222, this violation is being treated as a non-cited violation consistent with Section 2.3.2a of the NRC Enforcement Policy. NCV 05000275/2017002-01, Inadequate Expansion Scope of Risk-Informed Welds
-informed inservice inspection process developed based on the EPRI Topical Report TR
-112657, Revision B
-A, as an alternative to applicable requirements of Section XI of the ASME Code. The risk-informed inservice inspection process requires that when flaws or relevant conditions are detected, additional examinations on elements in segments subject to the same root cause conditions or degradation mechanism are required. Contrary to t he above, from November 1, 2015, until May 17, 2017, the licensee failed to conduct the required additional examinations on elements in segments subject to the same root cause conditions or degradation mechanism after flaws or relevant conditions were detected. Specifically, the licensee completed ultrasonic examinations of four additional pipe welds, but failed to select those that were assigned the same degradation mechanism as pipe weld WIB
-378. As part of their corrective actions, the licensee, at the time of the inspection, identified and intended to inspect four additional welds assigned to the same degradation mechanism as required by the risk
-informed inservice inspection program.
 
Because the violation was of very low safety significance and it wa s entered into the corrective action program as Notification 50920222, this violation is being treated as a non-cited violation consistent with Section 2.3.
 
2 a of the NRC Enforcement Policy.
 
NCV 05000275/2017002
-01 , "Inadequate Expansion Scope of Risk-Informed Welds"


===.2 Vessel Upper Head Penetration Inspection Activities===
===.2 Vessel Upper Head Penetration Inspection Activities===
Line 265: Line 239:


====a. Inspection Scope====
====a. Inspection Scope====
The inspector reviewed the licensee's implementation of its boric acid corrosion control program for monitoring degradation of those systems that could be adversely affected by boric acid corrosion. The inspector s reviewed the documentation associated with the licensee's boric acid corrosion control walk
The inspector reviewed the licensees implementation of its boric acid corrosion control program for monitoring degradation of those systems that could be adversely affected by boric acid corrosion. The inspectors reviewed the documentation associated with the licensees boric acid corrosion control walk-down as specified in Procedure ER1.ID2, Boric Acid Corrosion Control Program, Revision 7. The inspector determined that the visual inspections emphasized locations where boric acid leaks could cause degradation of safety-significant components, and that engineering evaluations used corrosion rates applicable to the affected components and properly assessed the effects of corrosion induced wastage on structural or pressure boundary integrity. The inspector observed that corrective actions taken were consistent with the ASME Code, and 10 CFR 50, Appendix B requirements.
-down as specified in Procedure ER1.ID2, "Boric Acid Corrosion Control Program," Revision 7. The inspector determined that the visual inspections emphasized locations where boric acid leaks could cause degradation of safety-significant components, and that engineering evaluation s used corrosion rates applicable to the affected components and properly assessed the effects of corrosion induced wastage on structural or pressure boundary integrity. The inspector observed that corrective actions taken were consistent with the ASME Code, and 10 CFR 50, Appendix B requirements.


====b. Findings====
====b. Findings====
Line 274: Line 247:


====a. Inspection Scope====
====a. Inspection Scope====
No steam generator tube inspection activities were scheduled for Diablo Canyon Power Plant, Unit 1, during Outage 1 R 20.
No steam generator tube inspection activities were scheduled for Diablo Canyon Power Plant, Unit 1, during Outage 1R20.


====b. Findings====
====b. Findings====
Line 282: Line 255:


====a. Inspection Scope====
====a. Inspection Scope====
The inspector reviewed 13 condition reports which dealt with inservice inspection activities and found the corrective actions for inservice inspection issues were appropriate. From this review the inspector concluded that the licensee has an appropriate threshold for entering inservice inspection issues into the corrective action program and has procedures that direct a root cause evaluation when necessary. The licensee also has an effective program for applying industry inservice inspecti on operating experience.
The inspector reviewed 13 condition reports which dealt with inservice inspection activities and found the corrective actions for inservice inspection issues were appropriate. From this review the inspector concluded that the licensee has an appropriate threshold for entering inservice inspection issues into the corrective action program and has procedures that direct a root cause evaluation when necessary. The licensee also has an effective program for applying industry inservice inspection operating experience.


The inspector also performed a review of licensee evaluations and corrective actions related to recent operating experience with degraded reactor vessel internal baffle-former bolts. Specifically, Diablo Canyon Power Plant, Unit 1, is a Tier 1a plant as identified in Nuclear Safety Advisory Letter (NSAL)1 "Baffle-Former Bolts.For a Tier 1a plant, the following actions were recommended:
The inspector also performed a review of licensee evaluations and corrective actions related to recent operating experience with degraded reactor vessel internal baffle-former bolts. Specifically, Diablo Canyon Power Plant, Unit 1, is a Tier 1a plant as identified in Nuclear Safety Advisory Letter (NSAL)-16-1 Baffle-Former Bolts. For a Tier 1a plant, the following actions were recommended:
Complete ultrasonic inspection of the baffle
* Complete ultrasonic inspection of the baffle-former bolts at the next schedule outage (1R20).
-former bolts at the next schedule outage (1R20). Consider developing an acceptable bolting pattern analysis.
* Consider developing an acceptable bolting pattern analysis.
* Replace any baffle-former bolts with visible damage or ultrasonic indications prior to starting up.


Replace any baffle
The inspector reviewed the licensees evaluations and corrective action to determine if they were consistent with recommendations identified in NSAL-16-1 and other applicable industry operating experience related to degraded baffle-former bolts. The inspectors observed portions of the ultrasonic examinations and baffle-former bolt inspection activities. Specific documents reviewed during this inspection are listed in the attachment.
-former bolts with visible damage or ultrasonic indications prior to starting up.
 
The inspector reviewed the licensee's evaluations and corrective action to determine if they were consistent with recommendations identified in NSAL 1 and other applicable industry operating experience related to degraded baffle
-former bolts. The inspectors observed portions of the ultrasonic examinations and baffle
-former bolt inspection activities. Specific documents reviewed during this inspection are listed in the attachment.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
{{a|1R11}}
==1R11 Licensed Operator Requalification Program and Licensed Operator Performance==


1 R 11 Licensed Operator Requalification Program and Licensed Operator Performance (71111.11)
      (71111.11)


===.1 Review of Licensed Operator===
===.1 Review of Licensed Operator Requalification===


Requalification
====a. Inspection Scope====
On June 27, 2017, the inspectors observed simulator scenarios for an operating crew.


====a. Inspection Scope====
The inspectors assessed the performance of the operators and the evaluators critique of their performance. The inspectors also assessed the modeling and performance of the simulator during the simulator training scenario.
On June 27, 2017, the inspectors observed simulator scenarios for an operating crew. The inspectors assessed the performance of the operators and the evaluators' critique of their performance. The inspectors also assessed the modeling and performance of the simulator during the simulator training scenario
 
. These activities constitute d completion of one quarterly licensed operator requalification program sample , as defined in Inspection Procedure 71111.11.
These activities constituted completion of one quarterly licensed operator requalification program sample, as defined in Inspection Procedure 71111.11.


====b. Findings====
====b. Findings====
Line 314: Line 286:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed the performance of on
The inspectors observed the performance of on-shift licensed operators in the plants main control room. At the time of the observations, the plant was in a period of heightened activity. The inspectors observed the operators performance of the following activities:
-shift licensed operators in the plant's main control room. At the time of the observations, the plant was in a period of heightened activity.
* April 23, 2017, Unit 1, reactor shutdown for refueling outage 1R20
* May 1, 2017, Unit 1, reactor coolant system drain down for reactor head removal
* June 12, 2017, Unit 1, reduced inventory operations for vacuum refill of the reactor coolant system In addition, the inspectors assessed the operators adherence to plant procedures, including conduct of operations procedure and other operations department policies.


The inspectors observed the operators' performance of the following activities:
These activities constituted completion of one quarterly licensed operator performance sample, as defined in Inspection Procedure 71111.11.
April 23, 2017, Unit 1, reactor shutdown for refueling outage 1R20 May 1, 2017, Unit 1, reactor coolant system drain down for reactor head removal June 12, 2017, Unit 1, reduced inventory operations for vacuum refill of the reactor coolant system In addition, the inspectors assessed the operators' adherence to plant procedures, including conduct of operations procedure and other operations department policies.
 
These activities constitute d completion of one quarterly licensed operator performance sample , a s defined in Inspection Procedure 71111.11.


====b. Findings====
====b. Findings====
Line 329: Line 300:
Every year, either an annual review or a biennial review is performed on the licensed operator requalification program. For 2017, the biennial review was completed and the annual review was performed as part of this review.
Every year, either an annual review or a biennial review is performed on the licensed operator requalification program. For 2017, the biennial review was completed and the annual review was performed as part of this review.


The licensed operator requalification program involves two training cycles that are conducted over a 2
The licensed operator requalification program involves two training cycles that are conducted over a 2-year period. In the first cycle, the annual cycle, the operators are administered an operating test consisting of job performance measures and simulator scenarios. In the second part of the training cycle, the biennial cycle, operators are administered an operating test and a comprehensive written examination.
-year period. In the first cycle, the annual cycle, the operators are administered an operating test consisting of job performance measures and simulator scenarios. In the second part of the training cycle, the biennial cycle, operators are administered an operating test and a comprehensive written examination.


====a. Inspection Scope====
====a. Inspection Scope====
To assess the performance effectiveness of the licensed operator requalification program, the inspectors reviewed both the written examination and operating test quality and observed licensee administration of an annual requalification test while on
To assess the performance effectiveness of the licensed operator requalification program, the inspectors reviewed both the written examination and operating test quality and observed licensee administration of an annual requalification test while on-site. The operating tests observed included multiple administrations of four job performance measures and two scenarios that were used in the current biennial requalification cycle.
-site. The operating tests observed included multiple administrations of four job performance measures and two scenarios that were used in the current biennial requalification cycle. These observations allowed the inspectors to assess the licensee's effectiveness in conducting the operating test to ensure operator mastery of the training program content and to determine if feedback of performance analyses into the requalification training program was being accomplished.


On April 20, 2017, the licensee informed the inspectors of the completed cycle results for Diablo Canyon Power Plant for both the written examinations and the operating tests:  16 of 17 crews passed the simulator portion of the operating test 84 of 91 licensed operators passed the simulator portion of the operating test 90 of 91 licensed operators passed the job performance measure portion of the operating test 87 of 91 licensed operators passed the written examination The individuals that failed a portion of the examination were remediated, retested, and passed their retake examinations.
These observations allowed the inspectors to assess the licensee's effectiveness in conducting the operating test to ensure operator mastery of the training program content and to determine if feedback of performance analyses into the requalification training program was being accomplished.


The inspectors observed examination security measures in place during administration of the exams (including controls and content overlap) and reviewed remedial training and re-examinations, as available. The inspectors also reviewed medical records of 10 licensed operators for conformance to license conditions and the licensee's system for tracking qualifications and records of license reactivation for 11 operators.
On April 20, 2017, the licensee informed the inspectors of the completed cycle results for Diablo Canyon Power Plant for both the written examinations and the operating tests:
* 16 of 17 crews passed the simulator portion of the operating test
* 84 of 91 licensed operators passed the simulator portion of the operating test
* 90 of 91 licensed operators passed the job performance measure portion of the operating test
* 87 of 91 licensed operators passed the written examination The individuals that failed a portion of the examination were remediated, retested, and passed their retake examinations.
 
The inspectors observed examination security measures in place during administration of the exams (including controls and content overlap) and reviewed remedial training and re-examinations, as available. The inspectors also reviewed medical records of 10 licensed operators for conformance to license conditions and the licensees system for tracking qualifications and records of license reactivation for 11 operators.


The inspectors reviewed simulator performance for fidelity with the actual plant and the overall simulator program of maintenance, testing, and discrepancy correction.
The inspectors reviewed simulator performance for fidelity with the actual plant and the overall simulator program of maintenance, testing, and discrepancy correction.
Line 348: Line 323:


=====Introduction.=====
=====Introduction.=====
The inspector s identified a Severity Level IV (SL-IV) non-cited violation (NCV) of 10 CFR 55.21, "Medical Examination," for the licensee's failure to ensure that a medical examination by a physician to determine satisfaction of 10 CFR 55.33(a)(1) requirements was conducted every two years for two licensed senior operators.
The inspectors identified a Severity Level IV (SL-IV) non-cited violation (NCV) of 10 CFR 55.21, Medical Examination, for the licensees failure to ensure that a medical examination by a physician to determine satisfaction of 10 CFR 55.33(a)(1)requirements was conducted every two years for two licensed senior operators.


=====Description.=====
=====Description.=====
On April 5, 2017, an NRC inspector identified that a currently licensed senior operator last had a 10 CFR 55.21 required medical examination on Novemb er 27, 2013, a span of 40 months. On March 12, 2014, the facility licensee informed the NRC by letter that this operator had developed a "temporary medical condition," and had been administratively removed from engaging in licensed activities. On December 1, 2014, the individual left the site permanently, ultimately transitioning into the licensee's long
On April 5, 2017, an NRC inspector identified that a currently licensed senior operator last had a 10 CFR 55.21 required medical examination on November 27, 2013, a span of 40 months.
-term disability program on April 23, 2015. Following the notification of March 12, 2014, no further communication was submitted to the NRC regarding this operator's status until the date of this inspection, and his license remained active. Following NRC identification, the licensee issued Notification 50911467 on April 6, 2017, to initiate termination of the operator's license. No licensed duties were performed by the operator subsequent to the expiration of his 2-year medical examination on November 26, 2015.


On April 13, 2017, the facility licensee informed the inspectors that during an Extent of Condition review, a second licensed senior operator was identified who had exceeded two years between 10 CFR 55.21 required medical examinations. The individual received a medical examination on November 19, 2014, but did not receive a subsequent biennial medical examination until April 6, 2017, a period of two years and four months. During this time
On March 12, 2014, the facility licensee informed the NRC by letter that this operator had developed a temporary medical condition, and had been administratively removed from engaging in licensed activities. On December 1, 2014, the individual left the site permanently, ultimately transitioning into the licensees long-term disability program on April 23, 2015. Following the notification of March 12, 2014, no further communication was submitted to the NRC regarding this operators status until the date of this inspection, and his license remained active. Following NRC identification, the licensee issued Notification 50911467 on April 6, 2017, to initiate termination of the operators license. No licensed duties were performed by the operator subsequent to the expiration of his 2-year medical examination on November 26, 2015.
, the operator was periodically evaluated for a medical condition which approached, but did not yet exceed
 
, the threshold for a disqualifying condition under ANSI/ANS
On April 13, 2017, the facility licensee informed the inspectors that during an Extent of Condition review, a second licensed senior operator was identified who had exceeded two years between 10 CFR 55.21 required medical examinations. The individual received a medical examination on November 19, 2014, but did not receive a subsequent biennial medical examination until April 6, 2017, a period of two years and four months. During this time, the operator was periodically evaluated for a medical condition which approached, but did not yet exceed, the threshold for a disqualifying condition under ANSI/ANS-3.4/2013, Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants, to which the facility licensee is committed to follow. When subsequently evaluated on April 6, 2017, the facility licensee determined that a license amendment was necessary for the previously conforming medical condition. The operator was administratively suspended from engaging in licensed activities on July 13, 2016, and remained so as of the date of the on-site inspection. No licensed duties were performed by the operator subsequent to the expiration of his 2-year medical examination on November 19, 2016.
-3.4/2013, "Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants," to which the facility licensee is committed to follow. When subsequently evaluated on April 6, 2017, the facility licensee determined that a license amendment was necessary for the previously conforming medical condition. The operator was administratively suspended from engaging in licensed activities on July 13, 2016, and remained so as of the date of the on
-site inspection. No licensed duties were performed by the operator subsequent to the expiration of his 2-year medical examination on November 19, 2016.


=====Analysis.=====
=====Analysis.=====
The failure of the licensee to conduct required biennial medical examinations for two licensed senior operators was a performance deficiency that was reasonably within the licensee's ability to foresee and prevent. This issue was evaluated using the traditional enforcement process because it negatively impacted the NRC's ability to perform its regulatory oversight function. Specifically, the failure to comply with medical testing requirements for two licensed senior operators compromised the facility licensee's ability to assure conformance to medical standards, detect non-conforming medical conditions, and report non
The failure of the licensee to conduct required biennial medical examinations for two licensed senior operators was a performance deficiency that was reasonably within the licensees ability to foresee and prevent. This issue was evaluated using the traditional enforcement process because it negatively impacted the NRCs ability to perform its regulatory oversight function. Specifically, the failure to comply with medical testing requirements for two licensed senior operators compromised the facility licensees ability to assure conformance to medical standards, detect non-conforming medical conditions, and report non-conformances to the NRC. In the case of one senior operator, it prevented the facility licensee from documenting and reporting an adverse medical condition which had transitioned from temporary to permanent in nature, thereby requiring either a license amendment or termination. In the case of the other senior operator, it prevented the facility licensee from evaluating the need for a license amendment for a medical condition which had previously approached, but not yet exceeded, the threshold for a disqualifying condition under ANSI/ANS-3.4/2013. This performance deficiency was determined to be SL-IV because it fits the SL-IV example of Enforcement Policy Section 6.4.d.1, Violation Examples: Licensed Reactor Operators.
-conformances to the NRC. In the case of one senior operator, it prevented the facility licensee from documenting and reporting an adverse medical condition which had transitioned from temporary to permanent in nature, thereby requiring either a license amendment or termination. In the case of the other senior operator, it prevented the facility licensee from evaluating the need for a license amendment for a medical condition which had previously approache d , but not yet exceeded , the threshold for a disqualifying condition under ANSI/ANS-3.4/2013. This performance deficiency was determined to be SL
 
-IV because it fits the SL
This section states the following:
-IV example of Enforcement Policy Section 6.4.d.1, "Violation Examples: Licensed Reactor Operators.This section states the following
Severity Level IV violations involve : A non-willful compromise of an application, test, or examination required by 10 CFR Part 55. For example
:  "Severity Level IV violations involve - : A non
: (b) an individual operator who did not meet the American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.4, Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants, Section 5, Health Requirements and Disqualifying Conditions, as certified on NRC Form 396, Certification of Medical Examination by Facility Licensee, required by 10 CFR 55.23, Certification, but who did not perform the functions of a licensed operator or senior operator while having a disqualifying medical condition.
-willful compromise - of an application, test, or examination required by 10 CFR Part 55. For example -
 
: (b) an individual operator who did not meet the American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.4, "Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants," Section 5, "Health Requirements and Disqualifying Conditions," as certified on NRC Form 396, "Certification of Medical Examination by Facility Licensee," required by 10 CFR 55.23, Certification, but who did not perform the functions of a licensed operator or senior operator while having a disqualifying medical condition.This example fits the first identified non
This example fits the first identified non-conforming senior operator, for whom a subsequent medical examination would have required documentation of a new permanent medical condition, submittal of a new NRC Form 396, and issuance of a license amendment or termination. The second identified non-conforming senior operator is also similar to this example, except that he was periodically assessed for a medical condition which approached, but did not yet exceed the threshold for a disqualifying condition under ANSI/ANS-3.4/2013. When subsequently evaluated on April 6, 2017, the facility licensee determined that a license amendment was necessary for the previously conforming medical condition.
-conforming senior operator, for whom a subsequent medical examination would have required documentation of a new permanent medical condition, submittal of a new NRC Form 396, and issuance of a license amendment or termination. The second identified non
-conforming senior operator is also similar to this example, except that he was periodically assessed for a medical condition which approached, but did not yet exceed the threshold for a disqualifying condition under ANSI/ANS-3.4/2013. When subsequently evaluated on April 6, 2017, the facility licensee determined that a license amendment was necessary for the previously conforming medical condition.


This finding is being treated as a NCV because:
This finding is being treated as a NCV because:
: (1) the facility licensee placed the violation into the corrective action program as Notification 50912407; (2)the facility licensee restored compliance within a reasonable period of time by requesting termination of one license, and re
: (1) the facility licensee placed the violation into the corrective action program as Notification 50912407;
-examining the holder of another license;
: (2) the facility licensee restored compliance within a reasonable period of time by requesting termination of one license, and re-examining the holder of another license;
: (3) the violation was non
: (3) the violation was non-repetitive as determined by a search on NRC databases for prior violations issued to the facility licensee; and
-repetitive as determined by a search on NRC databases for prior violations issued to the facility licensee; and (4)the violation did not involve willfulness. There is no cross
: (4) the violation did not involve willfulness.
-cutting aspect associated with this violation because it was processed using traditional enforcement.


In accordance with Inspection Manual Chapter 0612, Appendix B, "Issue Screening," the performance deficiency was also evaluated for significance under the Reactor Oversight Process. Licensed operators are treated as Mitigating Systems under the Reactor Oversight Process regulatory framework. Since the facility licensee administratively suspended both operators' qualifications prior to expiration of their biennial medical examination periods, neither operator was able to perform licensed duties while either diagnosed as medically unfit or after expiration of the medical exam. As a result, there was no adverse effect on the Mitigating Systems Cornerstone objective of the Reactor Oversight Process, and therefore no more
There is no cross-cutting aspect associated with this violation because it was processed using traditional enforcement.
-than-minor Reactor Oversight Process violation existed.


Enforcement
In accordance with Inspection Manual Chapter 0612, Appendix B, Issue Screening, the performance deficiency was also evaluated for significance under the Reactor Oversight Process. Licensed operators are treated as Mitigating Systems under the Reactor Oversight Process regulatory framework. Since the facility licensee administratively suspended both operators qualifications prior to expiration of their biennial medical examination periods, neither operator was able to perform licensed duties while either diagnosed as medically unfit or after expiration of the medical exam. As a result, there was no adverse effect on the Mitigating Systems Cornerstone objective of the Reactor Oversight Process, and therefore no more-than-minor Reactor Oversight Process violation existed.
. Title 10 CFR 55.21 requires, in part, that, a licensee (licensed senior operator) shall have a medical examination by a physician every two years to determine that the licensed senior operator meets the requirements of 10 CFR 55.33(a)(1). Contrary to the above, between November 27, 2015, and April 6, 2017, licensed senior operators failed to have a medical examination by a physician every two years to determine that the licensed senior operator met the requirements of 10 CFR 55.33(a)(1), as evidenced by two examples.


Specifically, one licensed senior operator exceeded the 2-year medical examination requirement by approximately 16 months between November 27, 2015, and April 6, 2017.
=====Enforcement.=====
 
Title 10 CFR 55.21 requires, in part, that, a licensee (licensed senior operator) shall have a medical examination by a physician every two years to determine that the licensed senior operator meets the requirements of 10 CFR 55.33(a)(1).
The facility licensee subsequently initiated action to terminate the operator's license.


The second licensed senior operator exceeded the 2-year medical examination requirement by four months, between November 19, 2016, and April 6, 2017, before the licensed senior operator was re-examined. Because this finding is of very low safety significance and was entered into the corrective action program as Notification 50912407, this violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the NRC Enforcement Policy. NCV 05000275/2017002
Contrary to the above, between November 27, 2015, and April 6, 2017, licensed senior operators failed to have a medical examination by a physician every two years to determine that the licensed senior operator met the requirements of 10 CFR 55.33(a)(1),
-02; 05000323/2017002
as evidenced by two examples. Specifically, one licensed senior operator exceeded the 2-year medical examination requirement by approximately 16 months between November 27, 2015, and April 6, 2017. The facility licensee subsequently initiated action to terminate the operators license. The second licensed senior operator exceeded the 2-year medical examination requirement by four months, between November 19, 2016, and April 6, 2017, before the licensed senior operator was re-examined. Because this finding is of very low safety significance and was entered into the corrective action program as Notification 50912407, this violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the NRC Enforcement Policy. NCV 05000275/2017002-02; 05000323/2017002-02, Failure to Conduct Required Biennial Medical Examinations Within Two Years (2)
-02, "Failure to Conduct Required Biennial Medical Examinations Within Two Years
" (2)


=====Introduction.=====
=====Introduction.=====
The inspectors identified a Severity Level IV non-cited violation of 10 CFR 55.25, "Incapacitation Because of Disability or Illness," for the facility licensee's failure to notify the NRC within 30 days of changes to one licensed senior operator's medical condition.
The inspectors identified a Severity Level IV non-cited violation of 10 CFR 55.25, Incapacitation Because of Disability or Illness, for the facility licensees failure to notify the NRC within 30 days of changes to one licensed senior operators medical condition.


=====Description.=====
=====Description.=====
On April 5, 2017, an NRC inspector identified that the facility licensee failed to inform the NRC within 30 days that a currently licensed senior operator had developed a permanent medical condition which had prevented the senior operator from engaging in licensed activities since March 12, 2014. On March 12, 2014, the facility licensee informed the NRC by letter that this senior operator had developed a "temporary medical condition," and had been administratively removed from engaging in licensed activities. On December 1, 2014, the senior operator left the site permanently, ultimately transitioning into the facility licensee's long
On April 5, 2017, an NRC inspector identified that the facility licensee failed to inform the NRC within 30 days that a currently licensed senior operator had developed a permanent medical condition which had prevented the senior operator from engaging in licensed activities since March 12, 2014. On March 12, 2014, the facility licensee informed the NRC by letter that this senior operator had developed a temporary medical condition, and had been administratively removed from engaging in licensed activities. On December 1, 2014, the senior operator left the site permanently, ultimately transitioning into the facility licensees long-term disability program on April 23, 2015. Following the letter of March 12, 2014, no further communication was submitted to the NRC regarding this senior operators status until the date of this inspection, and his license remained active. Following NRC identification, the facility licensee issued Notification 50911467 on April 6, 2017, to initiate termination of the senior operators license. No licensed activities were performed by the senior operator subsequent to the facility licensees initial diagnosis of a temporary medical condition on March 12, 2014.
-term disability program on April 23, 2015. Following the letter of March 12, 2014, no further communication was submitted to the NRC regarding this senior operator's status until the date of this inspection, and his license remained active. Following NRC identification, the facility licensee issued Notification 50911467 on April 6, 2017, to initiate termination of the senior operator's license. No licensed activities were performed by the senior operator subsequent to the facility licensee's initial diagnosis of a temporary medical condition on March 12, 2014.
 
The facility licensee endorsed ANSI/ANS-3.4-2013, medical certification and monitoring of personnel requiring operator licenses for nuclear power plants, on March 26, 2015.


The facility licensee endorsed ANSI/ANS
ANSI/ANS-3.4-2013 defines a temporary medical condition as follows:
-3.4-2013, "medical certification and monitoring of personnel requiring operator licenses for nuclear power plants," on March 26, 2015.
When an operator does not meet the specific minimum requirements in this standard but is expected to meet those requirements (without exception) again in the future, the operators condition/disability is considered temporary and does not need to be reported to the NRC. The facility licensee is expected to administratively restrict the operators activities, as appropriate, during the term of the condition/disability. It is up to the licensees examining physician to evaluate each operators situation and assess whether the operator will be capable of meeting the requirements within 90 days.


ANSI/ANS-3.4-2013 defines a "temporary medical condition" as follows:  
ANSI/ANS-3.4-2013 defines a permanent medical condition as follows:
"When an operator does not meet the specific minimum requirements in this standard but is expected to meet those requirements (without exception) again in the future, the operator's condition/disability is considered temporary and does not need to be reported to the NRC. The facility licensee is expected to administratively restrict the operator's activities, as appropriate, during the term of the condition/disability. It is up to the licensee's examining physician to evaluate each operator's situation and assess whether the operator will be capable of meeting the requirements within 90 days."
An injury or condition that impairs the physical and/or mental ability of an operator to meet the specific minimum requirements in this standard and is, as evaluated by the examining physician, expected to extend beyond 90 days.


ANSI/ANS-3.4-2013 defines a "permanent medical condition" as follows:
Based on the above definitions, the facility licensee was expected to recognize that the operators medical condition had become permanent in nature, by extending well beyond 90 days such that the operator was required to leave the site permanently and transition into a long-term disability program.
"An injury or condition that impairs the physical and/or mental ability of an operator to meet the specific minimum requirements in this standard and is, as evaluated by the examining physician, expected to extend beyond 90 days." Based on the above definitions, the facility licensee was expected to recognize that the operator's medical condition had become permanent in nature, by extending well beyond 90 days such that the operator was required to leave the site permanently and transition into a long
-term disability program.


=====Analysis.=====
=====Analysis.=====
The failure of the facility licensee to notify the NRC within 30 days of changes in a licensed senior operator's medical condition was a performance deficiency that was reasonably within the facility licensee's ability to foresee and prevent. This issue was evaluated using the traditional enforcement process because it negatively impacted the NRC's ability to perform its regulatory oversight function. Specifically, the failure t o report changes in a licensed senior operator's medical condition prevented the NRC from taking action to issue either a license amendment or termination, as appropriate. This performance deficiency was determined to be SL
The failure of the facility licensee to notify the NRC within 30 days of changes in a licensed senior operators medical condition was a performance deficiency that was reasonably within the facility licensees ability to foresee and prevent. This issue was evaluated using the traditional enforcement process because it negatively impacted the NRCs ability to perform its regulatory oversight function. Specifically, the failure to report changes in a licensed senior operators medical condition prevented the NRC from taking action to issue either a license amendment or termination, as appropriate.
-IV because it fits the SL
 
-IV example of Enforcement Policy Section 6.4.d.1, "Violation Examples: Licensed Reactor Operators.This section states the following
This performance deficiency was determined to be SL-IV because it fits the SL-IV example of Enforcement Policy Section 6.4.d.1, Violation Examples: Licensed Reactor Operators. This section states the following:
:  "Severity Level IV violations involve - : A non
Severity Level IV violations involve : A non-willful compromise of an application, test, or examination required by 10 CFR Part 55. For example
-willful compromise - of an application, test, or examination required by 10 CFR Part 55. For example -
: (b) an individual operator who did not meet the American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.4, Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants, Section 5, Health Requirements and Disqualifying Conditions, as certified on NRC Form 396, Certification of Medical Examination by Facility Licensee, required by 10 CFR 55.23, Certification, but who did not perform the functions of a licensed operator or senior operator while having a disqualifying medical condition.
: (b) an individual operator who did not meet the American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.4, "Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants," Section 5, "Health Requirements and Disqualifying Conditions," as certified on NRC Form 396, "Certification of Medical Examination by Facility Licensee," required by 10 CFR 55.23, Certification, but who did not perform the functions of a licensed operator or senior operator while having a disqualifying medical condition.This example fits the non
 
-conforming senior operator, who would have required either a license amendment or termination for the unreported permanent medical condition, but who did not engage in licensed activities from the time that a license amendment or termination was required.
This example fits the non-conforming senior operator, who would have required either a license amendment or termination for the unreported permanent medical condition, but who did not engage in licensed activities from the time that a license amendment or termination was required.


This finding is being treated as a NCV because:
This finding is being treated as a NCV because:
: (1) the facility licensee placed the violation into the corrective action program as Notification 50912407,
: (1) the facility licensee placed the violation into the corrective action program as Notification 50912407,
: (2) the facility licensee restored compliance within a reasonable period of time by requesting termination of the license, (3)the violation was non
: (2) the facility licensee restored compliance within a reasonable period of time by requesting termination of the license,
-repetitive as determined by a search on NRC databases for prior violations issued to the facility licensee, and (4)the violation did not involve willfulness. There is no cross
: (3) the violation was non-repetitive as determined by a search on NRC databases for prior violations issued to the facility licensee, and
-cutting aspect associated with this violation because it was processed using traditional enforcement.
: (4) the violation did not involve willfulness. There is no cross-cutting aspect associated with this violation because it was processed using traditional enforcement.


In accordance with Inspection Manual Chapter 0612, Appendix B, "Issue Screening," the performance deficiency was also evaluated for significance under the Reactor Oversight Process. Licensed operators are treated as mitigating systems under the Reactor Oversight Process regulatory framework. Since the facility licensee administratively suspended the senior operator's qualifications prior to the need for a license amendment or termination, the operator was unable to perform licensed duties while diagnosed as medically unfit. As a result, there was no adverse effect on the Mitigating Systems Cornerstone objective of the Reactor Oversight Process and, therefore, no more-than-minor Reactor Oversight Process violation exists.
In accordance with Inspection Manual Chapter 0612, Appendix B, Issue Screening, the performance deficiency was also evaluated for significance under the Reactor Oversight Process. Licensed operators are treated as mitigating systems under the Reactor Oversight Process regulatory framework. Since the facility licensee administratively suspended the senior operators qualifications prior to the need for a license amendment or termination, the operator was unable to perform licensed duties while diagnosed as medically unfit. As a result, there was no adverse effect on the Mitigating Systems Cornerstone objective of the Reactor Oversight Process and, therefore, no more-than-minor Reactor Oversight Process violation exists.


=====Enforcement.=====
=====Enforcement.=====
Title 10 CFR 55.25 requires, in part, that, if the licensee (licensed senior operator) develops a permanent physical condition that causes the licensed senior operator to fail to meet the requirements of 10 CFR 55.21, the facility licensee shall notify the Commission, within 30 days of learning of the diagnosis, in accordance with 10 CFR 50.74(c).
Title 10 CFR 55.25 requires, in part, that, if the licensee (licensed senior operator) develops a permanent physical condition that causes the licensed senior operator to fail to meet the requirements of 10 CFR 55.21, the facility licensee shall notify the Commission, within 30 days of learning of the diagnosis, in accordance with 10 CFR 50.74(c). Contrary to the above, from May 23, 2015, to April 6, 2017, the facility licensee failed to notify the Commission, within 30 days of learning of the diagnosis, in accordance with 10 CFR 50.74(c), that a licensed senior operator developed a permanent physical condition that caused the licensed senior operator to fail to meet the requirements of 10 CFR 55.21. Specifically, a licensed senior operator permanently left the site on December 1, 2014, and transitioned into a long-term disability program on April 23, 2015. The facility licensee subsequently initiated action to terminate the senior operators license, effective April 6, 2017. Because this finding is of very low safety significance and was entered into the CAP as Notification 50912407, this violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the NRC Enforcement Policy. NCV 05000275/2017002-03; 05000323/2017002-03, Failure to Report a Permanent Medical Condition Within 30 Days
 
{{a|1R12}}
Contrary to the above, from May 23, 2015, to April 6, 2017, the facility licensee failed to notify the Commission, within 30 days of learning of the diagnosis, in accordance with 10 CFR 50.74(c), that a licensed senior operator developed a permanent physical condition that caused the licensed senior operator to fail to meet the requirements of 10 CFR 55.21.
==1R12 Maintenance Effectiveness==
 
{{IP sample|IP=IP 71111.12}}
Specifically, a licensed senior operator permanently left the site on December 1, 2014, and transitioned into a long
-term disability program on April 23, 2015. The facility licensee subsequently initiated action to terminate the senior operator's license, effective April 6, 2017. Because this finding is of very low safety significance and was entered into the CAP as Notification 50912407, this violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the NRC Enforcement Policy
. NCV 05000275/2017002
-03; 05000323/2017002
-03 , "Failure to Report a Permanent Medical Condition Within 30 Days" 1 R 12 Maintenance Effectiveness (71111.
 
12)


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed two instance s of degraded performance or condition of safety-significant structures, systems, and components (SSCs):
The inspectors reviewed two instances of degraded performance or condition of safety-significant structures, systems, and components (SSCs):
J une 16, 2017, Units 1 and 2, emergency diesel generator fuel injection shaft spalling June 21, 2017, Unit s 1 and 2, containment fan cooling units The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensee's corrective actions. The inspectors reviewed the licensee's work practices to evaluate whether these may have played a role in the degradation of the SSCs. The inspectors assessed the licensee's characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.
* June 16, 2017, Units 1 and 2, emergency diesel generator fuel injection shaft spalling
* June 21, 2017, Units 1 and 2, containment fan cooling units The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensees corrective actions. The inspectors reviewed the licensees work practices to evaluate whether these may have played a role in the degradation of the SSCs. The inspectors assessed the licensees characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.


These activities constituted completion of two maintenance effectiveness sample s, as defined in Inspection Procedure 71111.12.
These activities constituted completion of two maintenance effectiveness samples, as defined in Inspection Procedure 71111.12.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
 
{{a|1R13}}
1 R 13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed four risk assessments performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk:
The inspectors reviewed four risk assessments performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk:
April 10, 2017, Unit 1, vital battery charger 132, maintenance outage April 26, 2017, Unit 1, vital bus F, maintenance outage May 30 - June 1, 2017, Units 1 and 2, single source of off
* April 10, 2017, Unit 1, vital battery charger 132, maintenance outage
-site power for planned switchyard outage June 12, 2017, Unit 1, reactor coolant system mid loop operations for vacuum fill The inspectors verified that these risk assessment s were performed in a timely manner and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant procedures. The inspectors reviewed the accuracy and completeness of the licensee's risk assessment s and verified that the licensee implemented appropriate risk management actions based on the result of the assessment s. Additionally, on May 2, 2017, the inspectors observed portions of one emergent work activity, Unit 1
* April 26, 2017, Unit 1, vital bus F, maintenance outage
, residual heat removal pump 1-2 , troubleshooting and repair of a failed lower bearing thermocouple, that had the potential to affect the functional capability of mitigating systems. The inspectors verified that the licensee appropriately developed and followed a work plan for this activity. The inspectors verified that the licensee took precautions to minimize the impact of the work activity on unaffected SSCs. These activities constitute d completion of five maintenance risk assessments and emergent work control inspection sample s , as defined in Inspection Procedure 71111.13.
* May 30 - June 1, 2017, Units 1 and 2, single source of off-site power for planned switchyard outage
* June 12, 2017, Unit 1, reactor coolant system mid loop operations for vacuum fill The inspectors verified that these risk assessments were performed in a timely manner and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant procedures. The inspectors reviewed the accuracy and completeness of the licensees risk assessments and verified that the licensee implemented appropriate risk management actions based on the result of the assessments.
 
Additionally, on May 2, 2017, the inspectors observed portions of one emergent work activity, Unit 1, residual heat removal pump 1-2, troubleshooting and repair of a failed lower bearing thermocouple, that had the potential to affect the functional capability of mitigating systems. The inspectors verified that the licensee appropriately developed and followed a work plan for this activity. The inspectors verified that the licensee took precautions to minimize the impact of the work activity on unaffected SSCs.
 
These activities constituted completion of five maintenance risk assessments and emergent work control inspection samples, as defined in Inspection Procedure 71111.13.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
 
{{a|1R15}}
1 R 15 Operability Determinations and Functionality Assessmen ts (71111.15)
==1R15 Operability Determinations and Functionality Assessments==
{{IP sample|IP=IP 71111.15}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed five operability determinations that the licensee performed for degraded or nonconforming SSCs:
The inspectors reviewed five operability determinations that the licensee performed for degraded or nonconforming SSCs:
April 27, 2017, Unit 1, volume control tank outlet isolation valve LCV
* April 27, 2017, Unit 1, volume control tank outlet isolation valve LCV-112B, failure to open following integrated safeguards test
-112B, failure to open following integrated safeguards test April 28, 2017, operability determination of Unit 1, Loop 4
* April 28, 2017, operability determination of Unit 1, Loop 4, residual heat removal suction line weld WIB-228 indication
, residual heat removal suction line weld WIB
* May 17-18, 2017, operability determination of Unit 1, safety injection valves SI-1-8923A and SI-1- 8802B anomalous behavior
-228 indication May 17-18, 2017, operability determination of Unit 1, safety injection valves SI-1-8923A and SI 8802B anomalous behavior May 25, 2017, operability determination of Unit 1, baffle
* May 25, 2017, operability determination of Unit 1, baffle-former bolt replacement
-former bolt replacement June 15-16, 2017, operability determination of Unit 1, emergency diesel generator 1
* June 15-16, 2017, operability determination of Unit 1, emergency diesel generator 1-3, radiator leak following maintenance The inspectors reviewed the timeliness and technical adequacy of the licensees evaluations. Where the licensee determined the degraded SSC to be operable, the inspectors verified that the licensees compensatory measures were appropriate to provide reasonable assurance of operability. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability of the degraded SSC.
-3 , radiator leak following maintenance The inspectors reviewed the timeliness and technical adequacy of the licensee's evaluations. Where the licensee determined the degraded SSC to be operable, t he inspectors verified that the licensee's compensatory measures were appropriate to provide reasonable assurance of operability. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability of the degraded SSC
 
. These activities constitute d completion of five operability and functionality review sample s, as defined in Inspection Procedure 71111.15.
These activities constituted completion of five operability and functionality review samples, as defined in Inspection Procedure 71111.15.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
 
{{a|1R17}}
1 R 17 Evaluations of Changes, Tests, and Experiments (71111.17 T)  Evaluations of Changes, Tests, and Experiments
==1R17 Evaluations of Changes, Tests, and Experiments==
{{IP sample|IP=IP 71111.17T}}
Evaluations of Changes, Tests, and Experiments


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed 7 evaluations performed pursuant to 10 CFR 50.59, to determine whether the evaluations were adequate and that prior NRC approval was obtained as appropriate.
The inspectors reviewed 7 evaluations performed pursuant to 10 CFR 50.59, to determine whether the evaluations were adequate and that prior NRC approval was obtained as appropriate. The inspectors also reviewed 12 screenings and/or applicability determinations, where licensee personnel had determined that a 10 CFR 50.59 evaluation was not necessary. The inspectors reviewed these documents to:
* verify that evaluations were performed in accordance with 10 CFR 50.59 when changes, tests, or experiments were made;
* verify that the licensee has appropriately concluded that the change, test or experiment can be accomplished without obtaining a license amendment;
* verify that safety issues related to the changes, tests, or experiments have been resolved; and
* verify that the licensees conclusions were correct and consistent with 10 CFR 50.59 for the changes, tests, or experiments that the licensee determined that evaluations were not required The inspectors used, in part, Nuclear Energy Institute (NEI) 96-07, Guidelines for 10 CFR 50.59 Implementation, Revision 1, to determine acceptability of the completed evaluations and screenings. The NEI document was endorsed by the NRC in Regulatory Guide 1.187, Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments, dated November 2000. The list of evaluations, screenings, and/or applicability determinations reviewed by the inspectors is included as an attachment to this report.


The inspectors also reviewed 12 screenings and/or applicability determinations, where licensee personnel had determined that a 10 CFR 50.59 evaluation was not necessary.
These activities constituted 19 reviews of evaluations, screenings, and/or applicability determinations as defined in Inspection Procedure 71111.17T.
 
The inspectors reviewed these documents to:  verify that evaluations were performed in accordance with 10 CFR 50.59 when changes, tests, or experiments were made
;  verify that the licensee has appropriately concluded that the change, test or experiment can be accomplished without obtaining a license amendment; verify that safety issues related to the changes, tests, or experiments have been resolved; and verify that the licensee's conclusions were correct and consistent with 10 CFR 50.59 for the changes, tests, or experiments that the licensee determined that evaluations were not required The inspectors used, in part, Nuclear Energy Institute (NEI) 96
-07, "Guidelines for 10 CF R 50.59 Implementation," Revision 1, to determine acceptability of the completed evaluations and screenings.
 
The NEI document was endorsed by the NRC in Regulatory Guide 1.187, "Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments," dated November 2000.
 
The list of evaluations, screenings , and/or applicability determinations reviewed by the inspectors is included as an attachment to this report.
 
These activities constituted 19 reviews of evaluations , screenings
, and/or applicability determinations as defined in Inspection Procedure 71111.17 T.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
{{a|1R18}}
==1R18 Plant Modifications==
{{IP sample|IP=IP 71111.18}}


1 R 18 Plant Modifications (71111.18)
====a. Inspection Scope====
On May 3-17, 2017, the inspectors reviewed a permanent modification to the Units 1 and 2, NFPA 805 fire detection SSCs, Work Order 68041843. The inspectors reviewed the design and implementation of the modification. The inspectors verified that work activities involved in implementing the modification did not adversely impact operator actions that may be required in response to an emergency or other unplanned event.


====a. Inspection Scope====
The inspectors verified that post-modification testing was adequate to establish the operability of the SSC as modified.
On May 3-17, 2017, the inspectors reviewed a permanent modification to the Units 1 and 2 , NFPA 805 fire detection SSCs, Work Order 68041843. The inspectors reviewed the design and implementation of the modification. The inspectors verified that work activities involved in implementing the modification did not adversely impact operator actions that may be required in response to an emergency or other unplanned event. The inspectors verified that post
-modification testing was adequate to establish the operability of the SSC as modified.


These activities constitute d completion of one sample of permanent modifications , a s defined in Inspection Procedure 71111.18.
These activities constituted completion of one sample of permanent modifications, as defined in Inspection Procedure 71111.18.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
 
{{a|1R19}}
1 R 19 Post-Maintenance Testing (71111.19)
==1R19 Post-Maintenance Testing==
{{IP sample|IP=IP 71111.19}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed s i x post-maintenance testing activities that affected risk-significant SSCs:
The inspectors reviewed six post-maintenance testing activities that affected risk-significant SSCs:
April 5, 2017, Unit 2, safety injection pump 2-1 oil change, clean, and inspect, post maintenance testing
* April 5, 2017, Unit 2, safety injection pump 2-1 oil change, clean, and inspect, post maintenance testing, Work Order 64114156
, Work Order 64114156 April 18, 2017, Unit 1, residual heat removal pump 1
* April 18, 2017, Unit 1, residual heat removal pump 1-2, 4 kV breaker 52HH11, post maintenance testing, Work Order 60093452
-2, 4 kV breaker 52HH11 , post maintenance testing, Work Order 60093452 May 2, 2017, Unit 1, residual heat removal pump 1
* May 2, 2017, Unit 1, residual heat removal pump 1-2, repairs to lower thermocouple, post maintenance testing, Work Order 60100221
-2, repairs to lower thermocouple
* May 10, 2017, Unit 2, turbine driven auxiliary feedwater pump, post maintenance testing, Work Order 64170321
, post maintenance testing, Work Order 60100221 May 10, 2017, Unit 2, turbine driven auxiliary feedwater pump, post maintenance testing, Work Order 64170321 June 16, 2017, Unit 1, emergency diesel generator 1
* June 16, 2017, Unit 1, emergency diesel generator 1-3, piston liner inspection, post maintenance testing, Work Order 64180314
-3, piston liner inspection, post maintenance testing, Work Order 64180314 June 22-23, 2017, Unit 1, containment fan cooling unit 1
* June 22-23, 2017, Unit 1, containment fan cooling unit 1-5 replacement, post maintenance testing, Work Order 68034821 The inspectors reviewed licensing- and design-basis documents for the SSCs and the maintenance and post-maintenance test procedures. The inspectors observed the performance of the post-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs.
-5 replacement, post maintenance testing, Work Order 68034821 The inspectors reviewed licensing- and design
-basis documents for the SSCs and the maintenance and post-maintenance test procedures.


The inspectors observed the performance of the post
These activities constituted completion of six post-maintenance testing inspection samples, as defined in Inspection Procedure 71111.19.
-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs.
 
These activities constitute d completion of s i x post-maintenance testing inspection sample s , as defined in Inspection Procedure 71111.19.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
 
{{a|1R20}}
1 R 20 Refueling and Other Outage Activities (71111.20)
==1R20 Refueling and Other Outage Activities==
{{IP sample|IP=IP 71111.20}}


====a. Inspection Scope====
====a. Inspection Scope====
During the station's Unit 1 refueling outage (1R20) that concluded on June 2 1, 2017, the inspectors evaluated the licensee's outage activities. The inspectors verified that the licensee considered risk in developing and implementing the outage plan, appropriately managed personnel fatigue, and developed mitigation strategies for losses of key safety functions. This verification included the following:
During the stations Unit 1 refueling outage (1R20) that concluded on June 21, 2017, the inspectors evaluated the licensees outage activities. The inspectors verified that the licensee considered risk in developing and implementing the outage plan, appropriately managed personnel fatigue, and developed mitigation strategies for losses of key safety functions. This verification included the following:
Review of the licensee's outage plan prior to the outage Review and verification of the licensee's fatigue management activities Monitoring of shut
* Review of the licensees outage plan prior to the outage
-down and cool
* Review and verification of the licensees fatigue management activities
-down activities Verification that the licensee maintained defense
* Monitoring of shut-down and cool-down activities
-in-depth during outage activities Observation and review of reduced
* Verification that the licensee maintained defense-in-depth during outage activities
-inventory and mid-loop activities Observation and review of fuel handling activities Monitoring of heat
* Observation and review of reduced-inventory and mid-loop activities
-up and startup activities These activities constitute d completion of one refueling outage sample , as defined in Inspection Procedure 71111.20.
* Observation and review of fuel handling activities
* Monitoring of heat-up and startup activities These activities constituted completion of one refueling outage sample, as defined in Inspection Procedure 71111.20.


====b. Findings====
====b. Findings====


=====Introduction.=====
=====Introduction.=====
The inspectors identified a Gre en , self-revealing , non-cited violation of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," because PG&E personnel failed to follow the requirements of AD7.ID14, "Assessment of Integrated Risk," Revision 11. Specifically, PG&E personnel failed to obtain shift manager permission, conduct a protected equipment briefing, and document shift manager approval prior to performing work on protected equipment. This resulted in a loss of flow of cooling water to one of two in service shutdown cooling residual heat removal (RHR) heat exchangers and subsequent perturbation in reactor coolant system (RCS) temperature during refueling outage 1R20.
The inspectors identified a Green, self-revealing, non-cited violation of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, because PG&E personnel failed to follow the requirements of AD7.ID14, Assessment of Integrated Risk, Revision 11. Specifically, PG&E personnel failed to obtain shift manager permission, conduct a protected equipment briefing, and document shift manager approval prior to performing work on protected equipment. This resulted in a loss of flow of cooling water to one of two in service shutdown cooling residual heat removal (RHR) heat exchangers and subsequent perturbation in reactor coolant system (RCS) temperature during refueling outage 1R20.


=====Description.=====
=====Description.=====
During plant shutdown conditions, both t rain A and train B of the RHR system are used in the shutdown cooling mode to remove decay heat generated from the nuclear fuel. The component cooling water (CCW) system is used to provide cooling flow to the RHR heat exchangers which are used as part of the shutdown cooling system. As part of the normal shutdown cooling system alignment, CCW header A provides cooling water flow to the train A , RHR heat exchanger and CCW header B provides cooling water flow to the train B, RHR heat exchanger. CCW header C is not normally aligned to provide cooling flow to a RHR heat exchanger. While preparing for maintenance on the Unit 1
During plant shutdown conditions, both train A and train B of the RHR system are used in the shutdown cooling mode to remove decay heat generated from the nuclear fuel. The component cooling water (CCW) system is used to provide cooling flow to the RHR heat exchangers which are used as part of the shutdown cooling system. As part of the normal shutdown cooling system alignment, CCW header A provides cooling water flow to the train A, RHR heat exchanger and CCW header B provides cooling water flow to the train B, RHR heat exchanger. CCW header C is not normally aligned to provide cooling flow to a RHR heat exchanger. While preparing for maintenance on the Unit 1, CCW header C, motor-operated flow control valve FCV-355, PG&E operations personnel closed CCW cross tie valves CCW-23 and CCW-24. At the time of the cross tie valve closures, CCW heat exchanger 1-1 was removed from service for maintenance. Flow to CCW header A was being supplied from CCW header B via valves CCW-23 and CCW-24. The closure of the cross tie valves removed CCW cooling flow from CCW header A and accordingly to one of the two operating trains of RHR shutdown cooling. Due to the subsequent imbalance of flowrates through the CCW headers, RCS temperature fluctuated by approximately 8 degrees Fahrenheit prior to the CCW normal lineup being restored approximately 10 minutes later. Train B of RHR shutdown cooling remained in service throughout the event and was sufficient to prevent an uncontrollable increase in RCS temperature and the onset of core boiling. Time to boil in the RCS during the event was 154 minutes. PG&E determined that the causes of the loss of flow of CCW to the RHR heat exchanger included failure to follow protected equipment postings, improper operations turnover, inadequate situational awareness, and improper outage work planning logic. PG&E entered the event into their corrective action program and conducted a barrier analysis to determine the causes of the event and to identify corrective actions. PG&E initiated actions to prevent future recurrence including evaluating changes to training and work practices. The inspectors reviewed PG&Es actions to identify and correct the cause of the event.
, CCW header C, mot or-operated flow control valve FCV-355, PG&E operations personnel closed CCW cross tie valves CCW
-23 and CCW
-24. At the time of the cross tie valve closures, CCW heat exchanger 1-1 was removed from service for maintenance. Flow to CCW header A was being supplied from CCW header B via valves CCW
-23 and CCW-24. The closure of the cross tie valves removed CCW cooling flow from CCW header A and accordingly to one of the two operating trains of RHR shutdown cooling. Due to the subsequent imbalance of flowrates through the CCW headers, RCS temperature fluctuated by approximately 8 degrees Fahrenheit prior to the CCW normal lineup being restored approximately 10 minutes later. Train B of RHR shutdown cooling remained in service throughout the event and was sufficient to prevent an uncontrollable increase in RCS temperature and the onset of core boiling. Time to boil in the RCS during the event was 154 minutes. PG&E determined that the causes of the loss of flow of CCW to the RHR heat exchanger included failure to follow protected equipment postings, improper operations turnover, inadequate situational awareness, and improper outage work planning logic. PG&E entered the event into their corrective action program and conducted a barrier analysis to determine the causes of the event and to identify corrective actions. PG&E initiated actions to prevent future recurrence including evaluating changes to training and work practices. The inspectors reviewed PG&E's actions to identify and correct the cause of the event.


=====Analysis.=====
=====Analysis.=====
The inspectors determined that PG&E's failure to follow AD7.ID14, "Assessment of Integrated Risk," Section 5.14 "Performing Work on Posted Protected Equipment,"
The inspectors determined that PG&Es failure to follow AD7.ID14, Assessment of Integrated Risk, Section 5.14 Performing Work on Posted Protected Equipment, was a performance deficiency within PG&Es ability to foresee and correct.
was a performance deficiency within PG&E's ability to foresee and correct. This performance deficiency was considered to be more than minor because it impacted the configuration control attribute of the Mitigating Systems cornerstone and its objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the loss of cooling flow to the RHR heat exchanger while in shutdown cooling mode resulted in a perturbation in RCS temperature of approximately 8 degrees Fahrenheit. The finding was evaluated in accordance with IMC 0609, Appendix G, "Shutdown Operations Significance Determination Process,"
 
and determined to be of very low safety significance (Green) since it did not represent a loss of system safety function of at least a single train for greater than four hours. The finding had a cross
This performance deficiency was considered to be more than minor because it impacted the configuration control attribute of the Mitigating Systems cornerstone and its objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the loss of cooling flow to the RHR heat exchanger while in shutdown cooling mode resulted in a perturbation in RCS temperature of approximately 8 degrees Fahrenheit. The finding was evaluated in accordance with IMC 0609, Appendix G, Shutdown Operations Significance Determination Process, and determined to be of very low safety significance (Green)since it did not represent a loss of system safety function of at least a single train for greater than four hours. The finding had a cross-cutting aspect in the area of human performance associated with conservative bias because PG&E personnel did not use decision-making practices that emphasize prudent choices over those that are simply allowable. Specifically, despite being authorized to close CCW cross connect valves by the work control process, PG&E personnel did not question the impact of their actions on shutdown cooling [H.14].
-cutting aspect in the area of human performance associated with conservative bias because PG&E personnel did not use decision-making practices that emphasize prudent choices over those that are simply allowable. Specifically, despite being authorized to close CCW cross connect valves by the work control process, PG&E personnel did not question the impact of their actions on shutdown cooling
[H.14].


=====Enforcement.=====
=====Enforcement.=====
Title 10 CFR Part 50, Appendix B, Criterion V requires, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. PG&E procedure AD7.ID14, "Assessment of Integrated Risk,"
Title 10 CFR Part 50, Appendix B, Criterion V requires, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. PG&E procedure AD7.ID14, Assessment of Integrated Risk, Revision 11, Section 5.14 requires that personnel obtain shift manager permission, conduct a protected equipment briefing, and document shift manager approval prior to performing work on protected equipment.
Revision 11, Section 5.14 requires that personnel obtain shift manager permission, conduct a protected equipment briefing, and document shift manager approval prior to performing work on protected equipment. Contrary to the above, PG&E maintenance and operations personnel conducted work on the Unit 1
 
, CCW system without obtaining shift manager permission, conducting a protected equipment briefing, and documenting shift manager permission  
Contrary to the above, PG&E maintenance and operations personnel conducted work on the Unit 1, CCW system without obtaining shift manager permission, conducting a protected equipment briefing, and documenting shift manager permission - actions designed to prevent unnecessary protected system equipment impacts. These actions resulted in a loss of flow of cooling water to one of two in service shutdown cooling RHR heat exchangers and subsequent perturbation in RCS temperature during refueling outage 1R20. After the issue was identified, PG&E entered the issue into their corrective action program as Notification 50915907 and initiated a barrier review. Additionally, PG&E initiated actions to prevent future recurrence including evaluating changes to training and work practices. Because this violation is of very low safety significance (Green) and PG&E entered the issue into their corrective action program, this violation is being treated as a NCV consistent with the NRC Enforcement Policy. NCV 05000275/2017002-04, Failure to Follow Procedures Results in Partial Loss of Cooling Flow to Shutdown Cooling
- actions designed to prevent unnecessary protected system equipment impacts. These actions resulted in a loss of flow of cooling water to one of two in service shutdown cooling RHR heat exchangers and subsequent perturbation in RCS temperature during refueling outage 1R20. After the issue was identified, PG&E entered the issue into their corrective action program as Notification 50915907 and initiated a barrier review. Additionally, PG&E initiated actions to prevent future recurrence including evaluating changes to training and work practices. Because this violation is of very low safety significance (Green) and PG&E entered the issue into their corrective action program, this violation is being treated as a NCV consistent with the NRC Enforcement Policy. NCV 05000275/2017002
{{a|1R22}}
-04, "Failure to Follow Procedures Results in Partial Loss of Cooling Flow to Shutdown Cooling" 1 R 22 Surveillance Testing (71111.22)
==1R22 Surveillance Testing==
{{IP sample|IP=IP 71111.22}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed six risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the SSCs were capable of performing their safety functions: In-service test s: April 18, 2017, Unit 1, main steam safety valve testing of RV
The inspectors observed six risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the SSCs were capable of performing their safety functions:
-4, per procedure STP M-77 Containment isolation valve surveillance tests: May 11, 2017, Unit 1, containment isolation valve testing of penetration 54 associated with instrument air valves
In-service tests:
, per procedure STP V
* April 18, 2017, Unit 1, main steam safety valve testing of RV-4, per procedure STP M-77 Containment isolation valve surveillance tests:
-654 May 24, 2017, Unit 1, containment isolation valve testing of penetration 59C associated with safety injection accumulator instrument line
* May 11, 2017, Unit 1, containment isolation valve testing of penetration 54 associated with instrument air valves, per procedure STP V-654
, per procedure STP V-659C Other surveillance tests:
* May 24, 2017, Unit 1, containment isolation valve testing of penetration 59C associated with safety injection accumulator instrument line, per procedure STP V-659C Other surveillance tests:
April 6, 2017, Unit 1, reactor coolant system, loop 3, flow channel FT
* April 6, 2017, Unit 1, reactor coolant system, loop 3, flow channel FT-434 calibration, per procedure STP I-7-F434
-434 calibration, per procedure STP I F434 April 24, 2017, Unit 1, 4 kV bus H non
* April 24, 2017, Unit 1, 4 kV bus H non-SI auto transfer test, per procedure STP M-13H
-SI auto transfer test, per procedure STP M-13H May 10-11, 2017, Unit 1, leakage testing of systems outside containment, pe r  procedure STP M
* May 10-11, 2017, Unit 1, leakage testing of systems outside containment, per procedure STP M-86G The inspectors verified that these tests met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the test satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected SSCs following testing.
-86G The inspectors verified that these test s met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the test satisfied appropriate acceptance criteria.


The inspectors verified that the licensee restored the operability of the affected SSCs following testing.
These activities constituted completion of six surveillance testing inspection samples, as defined in Inspection Procedure 71111.22.
 
These activities constitute d completion of s i x surveillance testing inspection sample s , a s defined in Inspection Procedure 71111.22.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


===2. ===
==RADIATION SAFETY==
==RADIATION SAFETY==
Cornerstones:
Cornerstones: Public Radiation Safety and Occupational Radiation Safety
Public Radiation Safety and Occupational Radiation Safety 2 RS 1 Radiological Hazard Assessment and Exposure Controls (71124.01)
{{a|2RS1}}
==2RS1 Radiological Hazard Assessment and Exposure Controls==
{{IP sample|IP=IP 71124.01}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated the licensee's performance in assessing the radiological hazards in the workplace associated with licensed activities. The inspectors assessed the licensee's implementation of appropriate radiation monitoring and exposure control measures for both individual and collective exposures. During the inspection, the inspectors interviewed licensee personnel, walked down various areas in the plant, performed independent radiation dose rate measurements, and observed postings and physical controls. The inspectors reviewed licensee performance in the following areas:
The inspectors evaluated the licensees performance in assessing the radiological hazards in the workplace associated with licensed activities. The inspectors assessed the licensees implementation of appropriate radiation monitoring and exposure control measures for both individual and collective exposures. During the inspection, the inspectors interviewed licensee personnel, walked down various areas in the plant, performed independent radiation dose rate measurements, and observed postings and physical controls. The inspectors reviewed licensee performance in the following areas:
Radiological hazard assessment, including a review of the plant's radiological source terms and associated radiological hazards. The inspectors also reviewed the licensee's radiological survey program to determine wheth er radiological hazards were properly identified for routine and non
* Radiological hazard assessment, including a review of the plants radiological source terms and associated radiological hazards. The inspectors also reviewed the licensees radiological survey program to determine whether radiological hazards were properly identified for routine and non-routine activities and assessed for changes in plant operations.
-routine activities and assessed for changes in plant operations
* Instructions to workers, including radiation work permit requirements and restrictions, actions for electronic dosimeter alarms, changing radiological condition, and radioactive material container labeling.
. Instructions to workers
* Contamination and radioactive material control, including release of potentially contaminated material from the radiologically controlled area, radiological survey performance, radiation instrument sensitivities, material control and release criteria, and control and accountability of sealed radioactive sources.
, including radiation work permit requirements and restrictions, actions for electronic dosimeter alarms , changing radiological condition, and radioactive material container labeling. Contamination and radioactive material control
* Radiological hazards control and work coverage. During walk downs of the facility and job performance observations, the inspectors evaluated ambient radiological conditions, radiological postings, adequacy of radiological controls, radiation protection job coverage, and contamination controls. The inspectors also evaluated dosimetry selection and placement as well as the use of dosimetry in areas with significant dose rate gradients. The inspectors examined the licensees controls for items stored in the spent fuel pool and evaluated airborne radioactivity controls and monitoring.
, including release of potentially contaminated material from the radiologically controlled area, radiological survey performance, radiation instrument sensitivities, material control and release criteria, and control and accountability of sealed radioactive sources.
* High radiation area and very high radiation area controls. During plant walk downs, the inspectors verified the adequacy of posting and physical controls, including areas of the plant with the potential to become risk-significant high radiation areas.
 
* Radiation worker performance and radiation protection technician proficiency with respect to radiation protection work requirements. The inspectors determined if workers were aware of significant radiological conditions in their workplace, radiation work permit controls/limits in place, and electronic dosimeter dose and dose rate set points. The inspectors observed radiation protection technician job performance, including the performance of radiation surveys.
Radiological hazards control and work coverage. During walk downs of the facility and job performance observations, the inspectors evaluated ambient radiological conditions, radiological postings, adequacy of radiological controls, radiation protection job coverage, and contamination controls. The inspectors also evaluated dosimetry selection and placement as well as the use of dosimetry in areas with significant dose rate gradients. The inspectors examined the licensee's controls for items stored in the spent fuel pool and evaluated airborne radioactivity controls and monitoring.
* Problem identification and resolution for radiological hazard assessment and exposure controls. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.
 
High radiation area and very high radiation area controls. During plant walk downs, the inspectors verified the adequacy of posting and physical controls, including areas of the plant with the potential to become risk
-significant high radiation areas.
 
Radiation worker performance and radiation protection technician proficiency with respect to radiation protection work requirements. The inspectors determined if workers were aware of significant radiological conditions in their workplace, radiation work permit controls/limits in place, and electronic dosimeter dose and dose rate set points. The inspectors observed radiation protection technician job performance, including the performance of radiation surveys.
 
Problem identification and resolution for radiological hazard assessment and exposure controls. The inspectors reviewed audits, self
-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.


These activities constitute completion of the seven required samples of radiological hazard assessment and exposure control program, as defined in Inspection Procedure 71124.01.
These activities constitute completion of the seven required samples of radiological hazard assessment and exposure control program, as defined in Inspection Procedure 71124.01.
Line 609: Line 555:
====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
 
{{a|2RS3}}
2 RS 3 In-Plant Airborne Radioactivity Control and Mitigation (71124.03)
==2RS3 In-Plant Airborne Radioactivity Control and Mitigation==
{{IP sample|IP=IP 71124.03}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated whether the licensee controlled in
The inspectors evaluated whether the licensee controlled in-plant airborne radioactivity concentrations consistent with ALARA principles and that the use of respiratory protection devices did not pose an undue risk to the wearer. During the inspection, the inspectors interviewed licensee personnel, walked down various areas in the plant, and reviewed licensee performance in the following areas:
-plant airborne radioactivity concentrations consistent with ALARA principles and that the use of respiratory protection devices did not pose an undue risk to the wearer. During the inspection, the inspectors interviewed licensee personnel, walked down various areas in the plant, and reviewed licensee performance in the following areas:
* Engineering controls, including the use of permanent and temporary ventilation systems to control airborne radioactivity. The inspectors evaluated installed ventilation systems, including review of procedural guidance, verification the systems were used during high-risk activities, and verification of airflow capacity, flow path, and filter/charcoal unit efficiencies. The inspectors also reviewed the use of temporary ventilation systems used to support work in contaminated areas such as high-efficiency particulate air (HEPA)/charcoal negative pressure units.
Engineering controls, including the use of permanent and temporary ventilation systems to control airborne radioactivity. The inspectors evaluated installed ventilation systems, including review of procedural guidance, verification the systems were used during high
-risk activities, and verification of airflow capacity , flow path, and filter/charcoal unit efficiencies. The inspectors also reviewed the use of temporary ventilation systems used to support work in contaminated areas such as high
-efficiency particulate air (HEPA)/charcoal negative pressure units. Additionally, the inspectors evaluated the licensee's airborne monitoring
 
protocols, including verification that alarms and set points were appropriate.


Use of respiratory protection devices, including an evaluation of the licensee's respiratory protection program for use , storage, maintenance, and quality assurance of National Institute for Occupational Safety and Health (NIOSH) certified equipment , air quality and quantity for supplied-air devices and self-contained breathing apparatus (SCBA) bottles, qualification and training of personnel, and user performance
Additionally, the inspectors evaluated the licensees airborne monitoring protocols, including verification that alarms and set points were appropriate.
. Self-contained breathing apparatus for emergency use
* Use of respiratory protection devices, including an evaluation of the licensees respiratory protection program for use, storage, maintenance, and quality assurance of National Institute for Occupational Safety and Health (NIOSH)certified equipment, air quality and quantity for supplied-air devices and self-contained breathing apparatus (SCBA) bottles, qualification and training of personnel, and user performance.
, including the licensee's capability for refilling and transporting SCBA air bottles to and from the control room and operations support center during emergency conditions, hydrostatic testing of SCBA bottles, status of SCBA staged and ready for use in the plant including vision correction, mask sizes, etc., SCBA surveillance and maintenance records, and personnel qualification, training, and readiness.
* Self-contained breathing apparatus for emergency use, including the licensees capability for refilling and transporting SCBA air bottles to and from the control room and operations support center during emergency conditions, hydrostatic testing of SCBA bottles, status of SCBA staged and ready for use in the plant including vision correction, mask sizes, etc., SCBA surveillance and maintenance records, and personnel qualification, training, and readiness.
 
* Problem identification and resolution for airborne radioactivity control and mitigation. The inspectors reviewed audits, self-assessments, and corrective action documents to verify problems were being identified and properly addressed for resolution.
Problem identification and resolution for airborne radioactivity control and mitigation. The inspectors reviewed audits, self
-assessments, and corrective action documents to verify problems were being identified and properly addressed for resolution.


These activities constitute completion of the four required samples of in-plant airborne radioactivity control and mitigation program, as defined in Inspection Procedure 71124.03.
These activities constitute completion of the four required samples of in-plant airborne radioactivity control and mitigation program, as defined in Inspection Procedure 71124.03.
Line 633: Line 573:
No findings were identified.
No findings were identified.


===4. ===
==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security 4OA 1 Performance Indicator Verification (71151)
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security
 
{{a|4OA1}}
==4OA1 Performance Indicator Verification==
{{IP sample|IP=IP 71151}}
===.1 Safety System Functional Failures (MS05)===
===.1 Safety System Functional Failures (MS05)===


====a. Inspection Scope====
====a. Inspection Scope====
For the period of April 1, 2016 through March 31, 2017, the inspectors reviewed licensee event reports (LERs), maintenance rule evaluations, and other records that could indicate whether safety system functional failures had occurred. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, and NUREG-1022, "Event Reporting Guidelines: 10 CFR 50.72 and 50.73," Revisio n 3, to determine the accuracy of the data reported.
For the period of April 1, 2016 through March 31, 2017, the inspectors reviewed licensee event reports (LERs), maintenance rule evaluations, and other records that could indicate whether safety system functional failures had occurred. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, and NUREG-1022, Event Reporting Guidelines: 10 CFR 50.72 and 50.73, Revision 3, to determine the accuracy of the data reported.


These activities constituted verification of the safety system functional failures performance indicator for Units 1 and 2, as defined in Inspection Procedure 71151.
These activities constituted verification of the safety system functional failures performance indicator for Units 1 and 2, as defined in Inspection Procedure 71151.
Line 646: Line 589:
No findings were identified.
No findings were identified.


===.2 Mitigating Systems Performance Index:===
===.2 Mitigating Systems Performance Index: Emergency AC Power Systems (MS06)===


Emergency AC Power System s (MS06)
====a. Inspection Scope====
The inspectors reviewed the licensees mitigating system performance index data for the period of April 1, 2016 through March 31, 2017, to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.


====a. Inspection Scope====
These activities constituted verification of the mitigating system performance index for emergency ac power systems for Units 1 and 2, as defined in Inspection Procedure 71151.
The inspectors reviewed the licensee's mitigating system performance index data for the period of April 1, 2016 through March 31, 2017, to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the reported data. These activities constituted verification of the mitigating system performance index for emergency ac power systems for Units 1 and 2, as defined in Inspection Procedure 71151.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


===.3 Mitigating Systems Performance Index===
===.3 Mitigating Systems Performance Index: High Pressure Injection Systems (MS07)===
: High Pressure Injection Systems (MS07)


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the licensee's mitigating system performance index data for the period of April 1, 2016 through March 31, 2017, to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the reported data.
The inspectors reviewed the licensees mitigating system performance index data for the period of April 1, 2016 through March 31, 2017, to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.


These activities constituted verification of the mitigating system performance index for high pressure injection systems for Units 1 and 2, as defined in Inspection Procedure 71151.
These activities constituted verification of the mitigating system performance index for high pressure injection systems for Units 1 and 2, as defined in Inspection Procedure 71151.
Line 670: Line 612:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors verified that there were no unplanned exposures or losses of radiological control over locked high radiation areas and very high radiation areas during the period of June 1, 2016, to April 30, 2017
The inspectors verified that there were no unplanned exposures or losses of radiological control over locked high radiation areas and very high radiation areas during the period of June 1, 2016, to April 30, 2017. The inspectors reviewed a sample of radiologically controlled area exit transactions showing exposures greater than 100 mrem. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.
. The inspectors reviewed a sample of radiologically controlled area exit transactions showing exposures greater than 100 mrem. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7 , to determine the accuracy of the reported data.


These activities constituted verification of the occupational exposure control effectiveness performance indicator as defined in Inspection Procedure 71151.
These activities constituted verification of the occupational exposure control effectiveness performance indicator as defined in Inspection Procedure 71151.
Line 678: Line 619:
No findings were identified.
No findings were identified.


===.5 Radiological Effluent Technical Specifications (RETS)/Offsite Dose Calculation Manual (ODCM) Radiological Effluent Occurrences (PR01)===
===.5 Radiological Effluent Technical Specifications (RETS)/Offsite Dose Calculation Manual===
 
      (ODCM) Radiological Effluent Occurrences (PR01)


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed corrective action program records for liquid or gaseous effluent releases that occurred during the period of June 1, 2016, to April 30, 2017, and were reported to the NRC to verify the performance indicator data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the reported data.
The inspectors reviewed corrective action program records for liquid or gaseous effluent releases that occurred during the period of June 1, 2016, to April 30, 2017, and were reported to the NRC to verify the performance indicator data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.


These activities constituted verification of the RETS/ODCM radiological effluent occurrences performance indicator as defined in Inspection Procedure 71151.
These activities constituted verification of the RETS/ODCM radiological effluent occurrences performance indicator as defined in Inspection Procedure 71151.
Line 687: Line 630:
====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
 
{{a|4OA2}}
4OA 2 Problem Identification and Resolution (71152)
==4OA2 Problem Identification and Resolution==
 
{{IP sample|IP=IP 71152}}
===.1 Routine Review===
===.1 Routine Review===


====a. Inspection Scope====
====a. Inspection Scope====
Throughout the inspection period, the inspectors performed daily reviews of items entered into the licensee's corrective action program and periodically attended the licensee's condition report screening meetings. The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the corrective action program for resolution. The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified.
Throughout the inspection period, the inspectors performed daily reviews of items entered into the licensees corrective action program and periodically attended the licensees condition report screening meetings. The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the corrective action program for resolution. The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified. The inspectors also reviewed the licensees problem identification and resolution activities during the performance of the other inspection activities documented in this report.


The inspectors also reviewed the licensee's problem identification and resolution activities during the performance of the other inspection activities documented in this report.
====b. Findings====
No findings were identified.


b. Finding s No findings were identified.
===.2 Annual Follow-up of Selected Issues===
 
===.2 Annual Follow===
 
-up of Selected Issues


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors selected two issues for an in
The inspectors selected two issues for an in-depth follow-up:
-depth follow
* On May 19, 2017, Anchor-Darling double disc gate valve wedge pin failure operating experience.
-up: On May 19, 2017, Anchor
-Darling double disc gate valve wedge pin failure operating experience.
 
The inspectors reviewed the status of PG&Es efforts to address operating experience (OE) concerning Anchor-Darling double disc gate valve wedge pin failure s. As part of the inspection, the inspectors assessed PG&E's response to industry OE including reviewing extent of condition evaluations, valve diagnostic traces, observing valve inspection activities, and interviewing PG&E engineering and maintenance personnel.
 
On June 30, 2017, Units 1 and 2
, NFPA fire impairments.


The inspectors conducted an in
The inspectors reviewed the status of PG&Es efforts to address operating experience (OE) concerning Anchor-Darling double disc gate valve wedge pin failures. As part of the inspection, the inspectors assessed PG&Es response to industry OE including reviewing extent of condition evaluations, valve diagnostic traces, observing valve inspection activities, and interviewing PG&E engineering and maintenance personnel.
-depth review of the licensee
* On June 30, 2017, Units 1 and 2, NFPA fire impairments.
's fire transient combustible permit program and change management issues related to transiting to new NFPA 805 program requirements. Specifically, the inspectors reviewed the training, planning, and requirements associated with the licensee NFPA 0805 implementation related to transient combustible permit program.


The inspectors assessed the licensee's problem identification threshold, interim, and compensatory actions. The inspectors verified that the licensee appropriately prioritized the corrective actions and these actions were adequate to correct the conditions associated with transient combustible permit process.
The inspectors conducted an in-depth review of the licensees fire transient combustible permit program and change management issues related to transiting to new NFPA 805 program requirements. Specifically, the inspectors reviewed the training, planning, and requirements associated with the licensee NFPA 0805 implementation related to transient combustible permit program. The inspectors assessed the licensees problem identification threshold, interim, and compensatory actions. The inspectors verified that the licensee appropriately prioritized the corrective actions and these actions were adequate to correct the conditions associated with transient combustible permit process.


These activities constitute d completion of two annual follow
These activities constituted completion of two annual follow-up samples as defined in Inspection Procedure 71152.
-up sample s as defined i n Inspection Procedure 71152.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


4OA 6 Meetings, Including Exit
{{a|4OA6}}
==4OA6 Meetings, Including Exit==


===Exit Meeting Summary===
===Exit Meeting Summary===


On May 12, 2017, the inspectors presented the radiation safety inspection results (Sections 2RS1, 2RS3, 4OA1.4, and 4OA1.5)to Ms. P. Gerfen , Senior Director Plant Manager, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
On May 12, 2017, the inspectors presented the radiation safety inspection results (Sections 2RS1, 2RS3, 4OA1.4, and 4OA1.5) to Ms. P. Gerfen, Senior Director Plant Manager, and other members of the licensee staff. The licensee acknowledged the issues presented.


On May 17, 2017, the inspector s presented the ISI inspection results (Section 1R08)to Mr. J. Welsch, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspector s had been returned or destroyed.
The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
 
On May 17, 2017, the inspectors presented the ISI inspection results (Section 1R08) to Mr. J. Welsch, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.


On May 17, 2017, the inspectors presented the results of the licensed operator requalification program inspection (Section 1R11.3) to Ms. P. Gerfen, Senior Director Plant Manager, and other members of the licensee's staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
On May 17, 2017, the inspectors presented the results of the licensed operator requalification program inspection (Section 1R11.3) to Ms. P. Gerfen, Senior Director Plant Manager, and other members of the licensee's staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.


On June 23, 2017, the inspectors presented the evaluations of changes, tests and experiments inspection results (Section 1R17)to J. Welsch, Site Vice President, and other members of the licensee staff.
On June 23, 2017, the inspectors presented the evaluations of changes, tests and experiments inspection results (Section 1R17) to J. Welsch, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.


The licensee acknowledged the issues presented.
On July 11, 2017, the resident inspectors presented the quarterly inspection results to J.
 
The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.


On July 11, 2017, the resident inspectors presented the quarterly inspection results to J. Welsch, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
Welsch, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.


=SUPPLEMENTAL INFORMATION=
=SUPPLEMENTAL INFORMATION=
Line 751: Line 683:
: [[contact::T. Baldwin]], Director, Nuclear Site Services
: [[contact::T. Baldwin]], Director, Nuclear Site Services
: [[contact::K. Bych]], Manager, Engineering
: [[contact::K. Bych]], Manager, Engineering
: [[contact::D. Cortina]], Manager, Chemist
: [[contact::D. Cortina]], Manager, Chemistry
ry
: [[contact::D. Evans]], Director, Security & Emergency Services
: [[contact::D. Evans]], Director, Security & Emergency Services
: [[contact::R. Fortier]], Lead Exam Writer
: [[contact::R. Fortier]], Lead Exam Writer
Line 770: Line 701:
: [[contact::T. Irving]], Manager, Radiation Protection
: [[contact::T. Irving]], Manager, Radiation Protection
: [[contact::K. Johnston]], Director of Operations
: [[contact::K. Johnston]], Director of Operations
: [[contact::K. Kaminski]], Supervisor, Operations  
: [[contact::K. Kaminski]], Supervisor, Operations
: [[contact::R. Kelley]], Supervisor, Radiation Protection  
: [[contact::R. Kelley]], Supervisor, Radiation Protection
: [[contact::B. Lopez]], Engineer, Regulatory Services
: [[contact::B. Lopez]], Engineer, Regulatory Services
: [[contact::D. Madsen]], NRC Interface, Regulatory Services
: [[contact::D. Madsen]], NRC Interface, Regulatory Services
Line 793: Line 724:
: [[contact::P. Vobork]], Manager, Outage Work Week
: [[contact::P. Vobork]], Manager, Outage Work Week
: [[contact::R. Waltos]], Assistant Director, Engineering
: [[contact::R. Waltos]], Assistant Director, Engineering
: [[contact::A. Warwick]], Supervisor, Emergency Planning  
: [[contact::A. Warwick]], Supervisor, Emergency Planning
: [[contact::J. Welsch]], Site Vice President
: [[contact::J. Welsch]], Site Vice President
: [[contact::D. Williams]], Operations
: [[contact::D. Williams]], Operations
Attachment 1


==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==


===Opened and Closed===
===Opened and Closed===
: 05000275/2017002-01 NCV Inadequate Expansion Scope of Risk
: 05000275/2017002-01     NCV   Inadequate Expansion Scope of Risk-Informed Welds
-Informed Welds  
                                (Section 1R08)
(Section 1R08)
: 05000275/2017002-02     NCV   Failure to Conduct Required Biennial Medical Examinations
: 05000275/2017002
: 05000323/2017002-02            Within Two Years (Section 1R11.3)
-02
: 05000275/2017002-03     NCV   Failure to Report a Permanent Medical Condition Within
: 05000323/2017002
: 05000323/2017002-03            30 Days (Section 1R11.3)
-02 NCV Failure to Conduct Required Biennial Medical Examinations Within Two Years (Section
: 05000275/2017002-04     NCV   Failure to Follow Procedures Results in Partial Loss of Cooling
R11.3)  
Flow to Shutdown Cooling (Section 1R20)
: 05000275/2017002
-03
: 05000323/2017002
-03 NCV Failure to Report a Permanent Medical Condition Within
Days (Section
R11.3)  
: 05000275/2017002
-04 NCV Failure to Follow Procedures Results in Partial Loss of Cooling Flow to Shutdown Cooling (Section 1R20)


==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==


}}
}}

Revision as of 22:03, 29 October 2019

NRC Integrated Inspection Report 05000275/2017002 and 05000323/2017002
ML17223A120
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 08/10/2017
From: Mark Haire
NRC/RGN-IV/DRP/RPB-A
To: Halpin E
Pacific Gas & Electric Co
Mark Haire
References
IR 2017002
Download: ML17223A120 (69)


Text

UNITED STATES ust 10, 2017

SUBJECT:

DIABLO CANYON POWER PLANT - NRC INTEGRATED INSPECTION REPORT 05000275/2017002 and 05000323/2017002

Dear Mr. Halpin:

On June 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Diablo Canyon Power Plant, Units 1 and 2. On July 11, 2017, the NRC inspectors discussed the results of this inspection with Mr. J. Welsch, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented two findings of very low safety significance (Green) in this report.

These findings involved violations of NRC requirements. Additionally, NRC inspectors documented two Severity Level IV (SL-IV) violations with no associated findings. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC resident inspector at the Diablo Canyon Power Plant.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the NRC resident inspector at the Diablo Canyon Power Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Mark S. Haire, Branch Chief Project Branch A Division of Reactor Projects Docket Nos. 05000275 and 05000323 License Nos. DPR-80 and DPR-82

Enclosure:

Inspection Report 05000275/2017002 and 05000323/2017002 w/ Attachments:

1. Supplemental Information 2. RFI for Inservice Inspection 3. RFI for O

REGION IV==

Docket: 05000275; 05000323 License: DPR-80; DPR-82 Report: 05000275/2017002; 05000323/2017002 Licensee: Pacific Gas and Electric Company Facility: Diablo Canyon Power Plant, Units 1 and 2 Location: 7 1/2 miles NW of Avila Beach Avila Beach, CA Dates: April 1 through June 30, 2017 Inspectors: C. Newport, Senior Resident Inspector J. Reynoso, Resident Inspector J. Choate, Acting Resident Inspector I. Anchondo, Reactor Inspector T. Farina, Senior Operations Engineer C. Osterholtz, Senior Operations Engineer C. Steely, Operations Engineer L. Carson II, Sr. Health Physicist J. ODonnell, CHP, Health Physicist G. George, Senior Reactor Inspector, Engineering Branch 1, Lead S. Makor, Reactor Inspector, Engineering Branch 2 C. Stott, Reactor Inspector, Engineering Branch 1 Approved Mark S. Haire By: Chief, Project Branch A Division of Reactor Projects 1 Enclosure

SUMMARY

IR 05000275/2017002, 05000323/2017002; 04/01/2017 - 06/30/2017; Diablo Canyon Power

Plant; inservice inspection activities, licensed operator requalification program and licensed operator performance, refueling and other outage activities The inspection activities described in this report were performed between April 1 and June 30, 2017, by the resident inspectors at Diablo Canyon Power Plant and inspectors from the NRCs Region IV office. Two findings of very low safety significance (Green) are documented in this report. These findings involved violations of NRC requirements.

Additionally, NRC inspectors documented two Severity Level IV violations with no associated findings. The significance of inspection findings is indicated by their color (i.e., Green, greater than Green, White, Yellow, or Red), determined using Inspection Manual Chapter 0609,

Significance Determination Process, dated April 29, 2015. Their cross-cutting aspects are determined using Inspection Manual Chapter 0310, Aspects within the Cross-Cutting Areas, dated December 4, 2014. Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, dated July 2016.

Cornerstone: Mitigating Systems

Green.

The inspectors identified a non-cited violation of the licensees risk-informed inservice inspection program (which is their alternative to portions of the ASME Code,

Section XI inservice inspection program approved in accordance with 10 CFR 50.55a(z)) for the failure to properly expand the scope of additional welds to inspect. Specifically, a rejectable flaw on a pipe weld in the pressurizer spray line was identified during refueling outage 1R19 while performing an ultrasonic examination. The licensee expanded the inspection scope by four additional welds, but failed to select those assigned with the same degradation. For immediate corrective actions, the licensee identified and intended to inspect four additional welds assigned to the same degradation mechanism as required by the risk-informed inservice inspection program. This issue was entered into the licensees corrective action program as Notification 50920222.

The licensees failure to properly expand the weld examination scope as required by the risk-informed inservice inspection program was a performance deficiency. The performance deficiency was more than minor because it was associated with the equipment performance attribute of the Mitigating System Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to select additional welds that were susceptible to the same degradation mechanism as weld WIB-378 placed the plant at an increased risk due to the potential of having an active degradation mechanism that could affect additional components. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, the inspectors determined the finding screened as having very low significance (Green) because: (1) it was not a design deficiency; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and (4)did not result in the loss of a high safety-significant non-technical specification train. This finding had a cross-cutting aspect in the area of human performance associated with change management because leaders failed to use a systematic process for evaluating and implementing the change to a risk-informed inservice inspection program. The implementing procedure failed to include the reference to degradation mechanism allowing for a misinterpretation of weld expansion requirements once a flaw was identified in a weld WIB-378 [H.3]. (Section 1R08)

Medical Examination, for the licensees failure to ensure that a medical examination by a physician to determine satisfaction of 10 CFR 55.33(a)(1) requirements was conducted every 2 years for two licensed senior operators. Specifically, one licensed senior operator exceeded the two-year medical examination requirement by approximately 16 months between November 27, 2015, and April 6, 2017. A second licensed senior operator exceeded the 2-year medical examination requirement by 4 months between November 19, 2016, and April 6, 2017. As a corrective action, the licensee has conducted the required medical examination for one senior operator and initiated a license termination request for the other senior operator. This issue was entered into the licensees corrective action program as Notification 50912407.

The failure of the facility licensee to conduct required biennial medical examinations for two licensed senior operators was a performance deficiency. This issue was evaluated using the traditional enforcement process because it negatively impacted the NRCs ability to perform its regulatory oversight function. Specifically, the failure to comply with medical testing requirements for two operators compromised the facility licensees ability to assure conformance to medical standards, detect non-conforming medical conditions, and report non-conformances to the NRC. This performance deficiency was determined to be Severity Level IV because it fits the Severity Level IV example of Enforcement Policy Section 6.4.d.1,

Violation Examples: Licensed Reactor Operators. This section states, Severity Level IV violations involve, for example (b) an individual operator who did not meet the American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.4, Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants, Section 5, Health Requirements and Disqualifying Conditions, as certified on NRC Form 396, Certification of Medical Examination by Facility Licensee, required by 10 CFR 55.23, Certification, but who did not perform the functions of a licensed operator or senior operator while having a disqualifying medical condition. No cross-cutting aspect was assigned because the violation was processed using traditional enforcement.

(Section 1R11.3)

Incapacitation Because of Disability or Illness, for the licensees failure to notify the NRC within 30 days of a change to one licensed senior operators medical condition. Specifically, the licensed senior operator developed a permanent medical condition which caused him to permanently leave the site on December 1, 2014, and transition into a long-term disability program on April 23, 2015. The licensee did not notify the NRC of this change in medical condition. As a corrective action, the licensee initiated a license termination request for the affected operator, effective April 6, 2017. This issue was entered into the licensees corrective action program as Notification 50912407.

The failure of the facility licensee to notify the NRC within 30 days of a change in a licensed senior operators medical condition was a performance deficiency. This issue was evaluated using the traditional enforcement process because it negatively impacted the NRCs ability to perform its regulatory oversight function. Specifically, the failure to report changes in a licensed senior operators medical condition prevented the NRC from taking action to issue either a license amendment or termination, as appropriate. This performance deficiency was determined to be Severity Level IV because it fits the Severity Level IV example of Enforcement Policy Section 6.4.d.1, Violation Examples: Licensed Reactor Operators. This section states, Severity Level IV violations involve, for example (b) an individual operator who did not meet the American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.4, Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants, Section 5, Health Requirements and Disqualifying Conditions, as certified on NRC Form 396, Certification of Medical Examination by Facility Licensee, required by 10 CFR 55.23, Certification, but who did not perform the functions of a licensed operator or senior operator while having a disqualifying medical condition. No cross-cutting aspect was assigned because the violation was processed using traditional enforcement. (Section 1R11.3)

Green.

The inspectors reviewed a self-revealing, non-cited violation of 10 CFR 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, because PG&E personnel failed to follow the requirements of AD7.ID14, Assessment of Integrated Risk,

Revision 11. Specifically, PG&E personnel failed to obtain shift manager permission, conduct a protected equipment briefing, and document shift manager approval prior to performing work on protected equipment. This resulted in a loss of flow of cooling water to one of two in-service shutdown cooling residual heat removal heat exchangers and subsequent perturbation in reactor coolant system temperature during refueling outage 1R20.

The inspectors determined that PG&Es failure to follow AD7.ID14, Assessment of Integrated Risk, Section 5.14 Performing Work on Posted Protected Equipment, was a performance deficiency within PG&Es ability to foresee and correct. This performance deficiency was considered to be more than minor because it impacted the configuration control attribute of the Mitigating Systems cornerstone and its objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the loss of cooling flow to the RHR heat exchanger while in shutdown cooling mode resulted in a perturbation in RCS temperature of approximately 8 degrees Fahrenheit. The finding was evaluated in accordance with IMC 0609, Appendix G, Shutdown Operations Significance Determination Process, and determined to be of very low safety significance (Green) since it did not represent a loss of system safety function of at least a single train for greater than four hours. The finding had a cross-cutting aspect in the area of human performance associated with conservative bias because PG&E personnel did not use decision-making practices that emphasize prudent choices over those that are simply allowable. Specifically, despite being authorized to close component cooling water cross connect valves by the work control process, PG&E personnel did not question the impact of their actions on shutdown cooling [H.14].

(Section 1R20)

PLANT STATUS

Units 1 and 2 began the inspection period at full power.

On April 23, 2017, Unit 1 was shut down for a planned refueling outage. On June 21, 2017, Unit 1 returned to operation and began a controlled power ascension; it returned to full power on June 27, 2017.

Units 1 and 2 operated at or near full power for the remainder of the inspection period.

REPORT DETAILS

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness

1R01 Adverse Weather Protection

Summer Readiness for Offsite and Alternate AC Power Systems

a. Inspection Scope

On June 23, 2017, the inspectors completed an inspection of the stations off-site and alternate-ac power systems. The inspectors inspected the material condition of these systems, including transformers and other switchyard equipment to verify that plant features and procedures were appropriate for operation and continued availability of off-site and alternate-ac power systems. The inspectors reviewed outstanding work orders and open condition reports for these systems. The inspectors walked down the switchyard to observe the material condition of equipment providing off-site power sources. The inspectors assessed corrective actions for identified degraded conditions and verified that the licensee had considered the degraded conditions in its risk evaluations and had established appropriate compensatory measures.

The inspectors verified that the licensees procedures included appropriate measures to monitor and maintain availability and reliability of the off-site and alternate-ac power systems.

These activities constituted one sample of summer readiness of off-site and alternate-ac power systems, as defined in Inspection Procedure 71111.01.

b. Findings

No findings were identified.

1R04 Equipment Alignment

.1 Partial Walk-Down

a. Inspection Scope

The inspectors performed partial system walk-downs of the following risk-significant systems:

  • April 6, 2017, Unit 2, safety injection system
  • May 1, 2017, Unit 1, reactor vessel refueling level indication system
  • June 14-15, 2017, Unit 1, containment ventilation and air system
  • June 21, 2017, Unit 2, containment spray system The inspectors reviewed the licensees procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration.

These activities constituted five partial system walk-down samples as defined in Inspection Procedure 71111.04.

b. Findings

No findings were identified.

.2 Complete Walk-Down

a. Inspection Scope

On June 29, 2017, the inspectors performed a complete system walk-down inspection of the Unit 1, containment fan cooling unit system. The inspectors reviewed the licensees procedures and system design information to determine the correct system lineup for the existing plant configuration. The inspectors also reviewed outstanding work orders, open condition reports, in-process design changes, temporary modifications, and other open items tracked by the licensees operations and engineering departments. The inspectors then visually verified that the system was correctly aligned for the existing plant configuration.

These activities constituted one complete system walk-down sample, as defined in Inspection Procedure 71111.04.

b. Findings

No findings were identified.

1R05 Fire Protection

Quarterly Inspection

a. Inspection Scope

The inspectors evaluated the licensees fire protection program for operational status and material condition. The inspectors focused their inspection on five plant areas important to safety:

  • April 20, 2017, Units 1 and 2, auxiliary building fire areas located on the 64 foot elevation
  • April 25, 2017, Unit 1, containment building fire areas located on the 140 foot elevation
  • April 25, 2017, Unit 1, containment building fire areas located on the 91 foot elevation
  • May 4, 2017, Unit 1, containment building fire areas located on the 117 foot elevation
  • June 28, 2017, Units 1 and 2, auxiliary building fire areas located at the 73 foot elevation For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensees fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.

These activities constituted five quarterly inspection samples, as defined in Inspection Procedure 71111.05.

b. Findings

No findings were identified.

1R06 Flood Protection Measures

a. Inspection Scope

On April 27, 2017, the inspectors completed an inspection of underground bunkers susceptible to flooding. The inspectors selected underground vaults that contained risk-significant or multiple-train cables whose failure could disable risk-significant equipment:

  • April 27, 2017, Units 1 and 2, auxiliary salt water vault BPO44 The inspectors observed the material condition of the cables and splices and looked for evidence of cable degradation due to water intrusion. The inspectors verified that the cables and vaults met design requirements.

These activities constituted completion of one bunker/manhole sample, as defined in Inspection Procedure 71111.06.

b. Findings

No findings were identified.

1R07 Heat Sink Performance

a. Inspection Scope

On June 26, 2017, the inspectors completed an inspection of the readiness and availability of risk-significant heat exchangers. The inspectors reviewed the data from performance tests for the Unit 1 component cooling water heat exchangers. Additionally, the inspectors walked down the heat exchangers to observe their performance and material condition.

These activities constituted completion of one heat sink performance annual review sample, as defined in Inspection Procedure 71111.07.

b. Findings

No findings were identified.

1R08 Inservice Inspection Activities

The activities described in subsections 1 through 4 below constitute completion of one inservice inspection (ISI) sample, as defined in Inspection Procedure 71111.08.

.1 Non-destructive Examination Activities and Welding Activities

a. Inspection Scope

The inspector directly observed the following nondestructive examinations:

EXAMINATION SYSTEM WELD/COMPONENT IDENTIFICATION TYPE Residual Line 109 (Weld WIB-228) Ultrasonic Heat Removal Reactor Vessel Inlet Nozzle to DM Weld @ 67º Ultrasonic (Weld WIB-RC-2-20-SE)

Reactor Vessel Inlet Nozzle to DM Weld @ 113º Ultrasonic (Weld WIB-RC-3-18-SE)

The inspector reviewed records for the following nondestructive examinations:

EXAMINATION SYSTEM WELD/COMPONENT IDENTIFICATION TYPE Pressurizer Spray Line 15-4 (Weld WIB-378) Ultrasonic EXAMINATION SYSTEM WELD/COMPONENT IDENTIFICATION TYPE Residual Heat Line 109 (Weld WIB-228) Ultrasonic Removal Reactor Vessel Inlet Nozzle to DM Weld @ 293º Ultrasonic (Weld WIB-RC-1-18-SE)

Reactor Vessel Inlet Nozzle to DM Weld @ 247º Ultrasonic (Weld WIB-RC-4-18-SE)

Various Various (ASME Class 1 boundary) Visual (VT-2)

Various Test #8 (ASME Class 2 boundary) Visual (VT-2)

During the review and observation of each examination, the inspector observed whether activities were performed in accordance with the ASME Code requirements and applicable procedures. The inspector reviewed two indications that were previously examined, and observed whether the licensee evaluated and accepted the indications in accordance with the ASME Code. The inspector also reviewed the qualifications of all nondestructive examination technicians performing the inspections to determine whether they were current.

The inspector directly observed a portion of the following welding activities:

SYSTEM WELD IDENTIFICATION EXAMINATION TYPE Containment Fan Weld No. 38 & 40 Gas Tungsten Arc Cooling Unit Welding The inspector reviewed whether the welding procedure specifications and the welders had been properly qualified in accordance with ASME Code,Section IX requirements.

The inspector also determined that essential variables were identified, recorded in the procedure qualification record, and formed the bases for qualification of the welding procedure specifications.

b. Findings

Green. The inspector identified a non-cited violation of the licensees risk-informed inservice inspection program (which is their alternative to portions of the ASME Code,Section XI inservice inspection program approved in accordance with 10 CFR 50.55a(z))

for the failure to properly expand the scope of additional welds to inspect. Specifically, a rejectable flaw on a pipe weld in the pressurizer spray line was identified during refueling outage 1R19 while performing an ultrasonic examination. The licensee expanded the inspection scope by four additional welds but failed to select those assigned with the same degradation mechanism.

Description.

On November 8, 2001, the licensee received NRC approval to implement a risk-informed inservice inspection program for ASME Code, Class 1 and 2 piping welds.

The risk-informed inservice inspection program was developed in accordance with Electric Power Research Institute (EPRI) Topical Report TR-112657, Revised Risk-Informed Inservice Inspection Evaluation, Revision B-A. During refueling outage

1R19 , the licensee was completing the remaining inspections for the third 10-year ISI

interval as required by ASME Code,Section XI. During an ultrasonic examination, a rejectable flaw was identified in the pressurizer spray line, weld WIB-378. The results and corrective actions were documented in Notification 50809162.

The risk-informed inservice inspection program assigns a risk profile of each Class 1 and 2 piping weld based on risk significance, consequence of failure, and failure potential. The purpose of assigning a failure potential is to differentiate welds that are affected by a specific degradation mechanism. Topical Report TR-112657 provides the guidance to assign a degradation mechanism. Welds that do not meet the specific criteria are assigned to a failure potential without a degradation mechanism. When a flaw is identified, additional examinations are required to be performed to determine if an active degradation mechanism exist.

Procedure ISI ADD SUCCESS, Additional, Supplemental, and Successive Inspections, Revision 6, implements the guidance of additional inspections per Topical Report TR-112657. Section 4.2.6, states the following:

All other examinations performed on piping welds per the risk-informed ISI Program Plan that detect flaws or relevant conditions require additional examinations on elements in segments subject to the same root cause conditions. The number of additional examinations shall be equivalent to the number examined initially for the current refueling outage, and shall include high risk-significant as well as medium risk-significant elements (if needed) to reach the required number of additional elements.

The inspector noted that the term elements referred to selected welds per EPRI guidance. The inspector also noted that this procedural requirement was missing the reference to degradation mechanism in addition to root cause conditions as provided by Topical Report TR-112657.

Notification 50809162 documents that a flaw was identified in weld WIB-378. Per the risk-informed inservice inspection program, this weld has a failure potential assigned to the degradation mechanism of Thermal Stratification, Cycling, and Striping (TASCS).

The licensee expanded the inspection scope to four additional examinations as required by Section 4.2.6 of Procedure ISI ADD SUCCESS. The inspector checked whether the selected welds had the same degradation mechanism as Weld WIB-378 and identified that none of them had been assigned with TASCS as a degradation mechanism per their failure potential designation. The inspector concluded that although the licensee had correctly expanded the number of weld examinations it had failed to select those susceptible to TASCS.

Analysis.

The licensees failure to properly expand the weld examination scope as required by the risk-informed inservice inspection program was a performance deficiency. The performance deficiency was more than minor because it was associated with the equipment performance attribute of the Mitigating System Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to select additional welds that were susceptible to the same degradation mechanism as weld WIB-378 placed the plant at an increased risk due to the potential of having an active degradation mechanism that could affect additional components. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, the inspector determined the finding screened as having very low significance (Green)because: it was not a design deficiency; did not represent a loss of system and/or function; did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and did not result in the loss of a high safety-significant, non-technical specification train. This finding had a cross-cutting aspect in the area of Human Performance associated with Change Management because leaders failed to use a systematic process for evaluating and implementing the change to a risk-informed inservice inspection program. The implementing procedure failed to include the reference to degradation mechanism allowing for a misinterpretation of weld expansion requirements once a flaw was identified in weld WIB-378 [H.3].

Enforcement.

Title 10 CFR 50.55a(z), states in part, that alternatives to the requirements of this section must be submitted and authorized prior to implementation.

The licensee received prior approval to implement a risk-informed inservice inspection process developed based on the EPRI Topical Report TR-112657, Revision B-A, as an alternative to applicable requirements of Section XI of the ASME Code. The risk-informed inservice inspection process requires that when flaws or relevant conditions are detected, additional examinations on elements in segments subject to the same root cause conditions or degradation mechanism are required. Contrary to the above, from November 1, 2015, until May 17, 2017, the licensee failed to conduct the required additional examinations on elements in segments subject to the same root cause conditions or degradation mechanism after flaws or relevant conditions were detected. Specifically, the licensee completed ultrasonic examinations of four additional pipe welds, but failed to select those that were assigned the same degradation mechanism as pipe weld WIB-378. As part of their corrective actions, the licensee, at the time of the inspection, identified and intended to inspect four additional welds assigned to the same degradation mechanism as required by the risk-informed inservice inspection program. Because the violation was of very low safety significance and it was entered into the corrective action program as Notification 50920222, this violation is being treated as a non-cited violation consistent with Section 2.3.2a of the NRC Enforcement Policy. NCV 05000275/2017002-01, Inadequate Expansion Scope of Risk-Informed Welds

.2 Vessel Upper Head Penetration Inspection Activities

a. Inspection Scope

No vessel upper head penetration inspection activities were scheduled for Diablo Canyon Power Plant, Unit 1, during Outage 1R20.

b. Findings

No findings were identified.

.3 Boric Acid Corrosion Control Inspection Activities

a. Inspection Scope

The inspector reviewed the licensees implementation of its boric acid corrosion control program for monitoring degradation of those systems that could be adversely affected by boric acid corrosion. The inspectors reviewed the documentation associated with the licensees boric acid corrosion control walk-down as specified in Procedure ER1.ID2, Boric Acid Corrosion Control Program, Revision 7. The inspector determined that the visual inspections emphasized locations where boric acid leaks could cause degradation of safety-significant components, and that engineering evaluations used corrosion rates applicable to the affected components and properly assessed the effects of corrosion induced wastage on structural or pressure boundary integrity. The inspector observed that corrective actions taken were consistent with the ASME Code, and 10 CFR 50, Appendix B requirements.

b. Findings

No findings were identified.

.4 Steam Generator Tube Inspection Activities

a. Inspection Scope

No steam generator tube inspection activities were scheduled for Diablo Canyon Power Plant, Unit 1, during Outage 1R20.

b. Findings

No findings were identified.

.5 Identification and Resolution of Problems

a. Inspection Scope

The inspector reviewed 13 condition reports which dealt with inservice inspection activities and found the corrective actions for inservice inspection issues were appropriate. From this review the inspector concluded that the licensee has an appropriate threshold for entering inservice inspection issues into the corrective action program and has procedures that direct a root cause evaluation when necessary. The licensee also has an effective program for applying industry inservice inspection operating experience.

The inspector also performed a review of licensee evaluations and corrective actions related to recent operating experience with degraded reactor vessel internal baffle-former bolts. Specifically, Diablo Canyon Power Plant, Unit 1, is a Tier 1a plant as identified in Nuclear Safety Advisory Letter (NSAL)-16-1 Baffle-Former Bolts. For a Tier 1a plant, the following actions were recommended:

  • Complete ultrasonic inspection of the baffle-former bolts at the next schedule outage (1R20).
  • Consider developing an acceptable bolting pattern analysis.
  • Replace any baffle-former bolts with visible damage or ultrasonic indications prior to starting up.

The inspector reviewed the licensees evaluations and corrective action to determine if they were consistent with recommendations identified in NSAL-16-1 and other applicable industry operating experience related to degraded baffle-former bolts. The inspectors observed portions of the ultrasonic examinations and baffle-former bolt inspection activities. Specific documents reviewed during this inspection are listed in the attachment.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

(71111.11)

.1 Review of Licensed Operator Requalification

a. Inspection Scope

On June 27, 2017, the inspectors observed simulator scenarios for an operating crew.

The inspectors assessed the performance of the operators and the evaluators critique of their performance. The inspectors also assessed the modeling and performance of the simulator during the simulator training scenario.

These activities constituted completion of one quarterly licensed operator requalification program sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

.2 Review of Licensed Operator Performance

a. Inspection Scope

The inspectors observed the performance of on-shift licensed operators in the plants main control room. At the time of the observations, the plant was in a period of heightened activity. The inspectors observed the operators performance of the following activities:

  • April 23, 2017, Unit 1, reactor shutdown for refueling outage 1R20
  • June 12, 2017, Unit 1, reduced inventory operations for vacuum refill of the reactor coolant system In addition, the inspectors assessed the operators adherence to plant procedures, including conduct of operations procedure and other operations department policies.

These activities constituted completion of one quarterly licensed operator performance sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

.3 Biennial Review of Requalification Program

Every year, either an annual review or a biennial review is performed on the licensed operator requalification program. For 2017, the biennial review was completed and the annual review was performed as part of this review.

The licensed operator requalification program involves two training cycles that are conducted over a 2-year period. In the first cycle, the annual cycle, the operators are administered an operating test consisting of job performance measures and simulator scenarios. In the second part of the training cycle, the biennial cycle, operators are administered an operating test and a comprehensive written examination.

a. Inspection Scope

To assess the performance effectiveness of the licensed operator requalification program, the inspectors reviewed both the written examination and operating test quality and observed licensee administration of an annual requalification test while on-site. The operating tests observed included multiple administrations of four job performance measures and two scenarios that were used in the current biennial requalification cycle.

These observations allowed the inspectors to assess the licensee's effectiveness in conducting the operating test to ensure operator mastery of the training program content and to determine if feedback of performance analyses into the requalification training program was being accomplished.

On April 20, 2017, the licensee informed the inspectors of the completed cycle results for Diablo Canyon Power Plant for both the written examinations and the operating tests:

  • 16 of 17 crews passed the simulator portion of the operating test
  • 84 of 91 licensed operators passed the simulator portion of the operating test
  • 87 of 91 licensed operators passed the written examination The individuals that failed a portion of the examination were remediated, retested, and passed their retake examinations.

The inspectors observed examination security measures in place during administration of the exams (including controls and content overlap) and reviewed remedial training and re-examinations, as available. The inspectors also reviewed medical records of 10 licensed operators for conformance to license conditions and the licensees system for tracking qualifications and records of license reactivation for 11 operators.

The inspectors reviewed simulator performance for fidelity with the actual plant and the overall simulator program of maintenance, testing, and discrepancy correction.

The inspectors completed one inspection sample of the biennial licensed operator requalification program.

b. Findings

(1)

Introduction.

The inspectors identified a Severity Level IV (SL-IV) non-cited violation (NCV) of 10 CFR 55.21, Medical Examination, for the licensees failure to ensure that a medical examination by a physician to determine satisfaction of 10 CFR 55.33(a)(1)requirements was conducted every two years for two licensed senior operators.

Description.

On April 5, 2017, an NRC inspector identified that a currently licensed senior operator last had a 10 CFR 55.21 required medical examination on November 27, 2013, a span of 40 months.

On March 12, 2014, the facility licensee informed the NRC by letter that this operator had developed a temporary medical condition, and had been administratively removed from engaging in licensed activities. On December 1, 2014, the individual left the site permanently, ultimately transitioning into the licensees long-term disability program on April 23, 2015. Following the notification of March 12, 2014, no further communication was submitted to the NRC regarding this operators status until the date of this inspection, and his license remained active. Following NRC identification, the licensee issued Notification 50911467 on April 6, 2017, to initiate termination of the operators license. No licensed duties were performed by the operator subsequent to the expiration of his 2-year medical examination on November 26, 2015.

On April 13, 2017, the facility licensee informed the inspectors that during an Extent of Condition review, a second licensed senior operator was identified who had exceeded two years between 10 CFR 55.21 required medical examinations. The individual received a medical examination on November 19, 2014, but did not receive a subsequent biennial medical examination until April 6, 2017, a period of two years and four months. During this time, the operator was periodically evaluated for a medical condition which approached, but did not yet exceed, the threshold for a disqualifying condition under ANSI/ANS-3.4/2013, Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants, to which the facility licensee is committed to follow. When subsequently evaluated on April 6, 2017, the facility licensee determined that a license amendment was necessary for the previously conforming medical condition. The operator was administratively suspended from engaging in licensed activities on July 13, 2016, and remained so as of the date of the on-site inspection. No licensed duties were performed by the operator subsequent to the expiration of his 2-year medical examination on November 19, 2016.

Analysis.

The failure of the licensee to conduct required biennial medical examinations for two licensed senior operators was a performance deficiency that was reasonably within the licensees ability to foresee and prevent. This issue was evaluated using the traditional enforcement process because it negatively impacted the NRCs ability to perform its regulatory oversight function. Specifically, the failure to comply with medical testing requirements for two licensed senior operators compromised the facility licensees ability to assure conformance to medical standards, detect non-conforming medical conditions, and report non-conformances to the NRC. In the case of one senior operator, it prevented the facility licensee from documenting and reporting an adverse medical condition which had transitioned from temporary to permanent in nature, thereby requiring either a license amendment or termination. In the case of the other senior operator, it prevented the facility licensee from evaluating the need for a license amendment for a medical condition which had previously approached, but not yet exceeded, the threshold for a disqualifying condition under ANSI/ANS-3.4/2013. This performance deficiency was determined to be SL-IV because it fits the SL-IV example of Enforcement Policy Section 6.4.d.1, Violation Examples: Licensed Reactor Operators.

This section states the following:

Severity Level IV violations involve  : A non-willful compromise of an application, test, or examination required by 10 CFR Part 55. For example

(b) an individual operator who did not meet the American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.4, Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants, Section 5, Health Requirements and Disqualifying Conditions, as certified on NRC Form 396, Certification of Medical Examination by Facility Licensee, required by 10 CFR 55.23, Certification, but who did not perform the functions of a licensed operator or senior operator while having a disqualifying medical condition.

This example fits the first identified non-conforming senior operator, for whom a subsequent medical examination would have required documentation of a new permanent medical condition, submittal of a new NRC Form 396, and issuance of a license amendment or termination. The second identified non-conforming senior operator is also similar to this example, except that he was periodically assessed for a medical condition which approached, but did not yet exceed the threshold for a disqualifying condition under ANSI/ANS-3.4/2013. When subsequently evaluated on April 6, 2017, the facility licensee determined that a license amendment was necessary for the previously conforming medical condition.

This finding is being treated as a NCV because:

(1) the facility licensee placed the violation into the corrective action program as Notification 50912407;
(2) the facility licensee restored compliance within a reasonable period of time by requesting termination of one license, and re-examining the holder of another license;
(3) the violation was non-repetitive as determined by a search on NRC databases for prior violations issued to the facility licensee; and
(4) the violation did not involve willfulness.

There is no cross-cutting aspect associated with this violation because it was processed using traditional enforcement.

In accordance with Inspection Manual Chapter 0612, Appendix B, Issue Screening, the performance deficiency was also evaluated for significance under the Reactor Oversight Process. Licensed operators are treated as Mitigating Systems under the Reactor Oversight Process regulatory framework. Since the facility licensee administratively suspended both operators qualifications prior to expiration of their biennial medical examination periods, neither operator was able to perform licensed duties while either diagnosed as medically unfit or after expiration of the medical exam. As a result, there was no adverse effect on the Mitigating Systems Cornerstone objective of the Reactor Oversight Process, and therefore no more-than-minor Reactor Oversight Process violation existed.

Enforcement.

Title 10 CFR 55.21 requires, in part, that, a licensee (licensed senior operator) shall have a medical examination by a physician every two years to determine that the licensed senior operator meets the requirements of 10 CFR 55.33(a)(1).

Contrary to the above, between November 27, 2015, and April 6, 2017, licensed senior operators failed to have a medical examination by a physician every two years to determine that the licensed senior operator met the requirements of 10 CFR 55.33(a)(1),

as evidenced by two examples. Specifically, one licensed senior operator exceeded the 2-year medical examination requirement by approximately 16 months between November 27, 2015, and April 6, 2017. The facility licensee subsequently initiated action to terminate the operators license. The second licensed senior operator exceeded the 2-year medical examination requirement by four months, between November 19, 2016, and April 6, 2017, before the licensed senior operator was re-examined. Because this finding is of very low safety significance and was entered into the corrective action program as Notification 50912407, this violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the NRC Enforcement Policy. NCV 05000275/2017002-02; 05000323/2017002-02, Failure to Conduct Required Biennial Medical Examinations Within Two Years (2)

Introduction.

The inspectors identified a Severity Level IV non-cited violation of 10 CFR 55.25, Incapacitation Because of Disability or Illness, for the facility licensees failure to notify the NRC within 30 days of changes to one licensed senior operators medical condition.

Description.

On April 5, 2017, an NRC inspector identified that the facility licensee failed to inform the NRC within 30 days that a currently licensed senior operator had developed a permanent medical condition which had prevented the senior operator from engaging in licensed activities since March 12, 2014. On March 12, 2014, the facility licensee informed the NRC by letter that this senior operator had developed a temporary medical condition, and had been administratively removed from engaging in licensed activities. On December 1, 2014, the senior operator left the site permanently, ultimately transitioning into the facility licensees long-term disability program on April 23, 2015. Following the letter of March 12, 2014, no further communication was submitted to the NRC regarding this senior operators status until the date of this inspection, and his license remained active. Following NRC identification, the facility licensee issued Notification 50911467 on April 6, 2017, to initiate termination of the senior operators license. No licensed activities were performed by the senior operator subsequent to the facility licensees initial diagnosis of a temporary medical condition on March 12, 2014.

The facility licensee endorsed ANSI/ANS-3.4-2013, medical certification and monitoring of personnel requiring operator licenses for nuclear power plants, on March 26, 2015.

ANSI/ANS-3.4-2013 defines a temporary medical condition as follows:

When an operator does not meet the specific minimum requirements in this standard but is expected to meet those requirements (without exception) again in the future, the operators condition/disability is considered temporary and does not need to be reported to the NRC. The facility licensee is expected to administratively restrict the operators activities, as appropriate, during the term of the condition/disability. It is up to the licensees examining physician to evaluate each operators situation and assess whether the operator will be capable of meeting the requirements within 90 days.

ANSI/ANS-3.4-2013 defines a permanent medical condition as follows:

An injury or condition that impairs the physical and/or mental ability of an operator to meet the specific minimum requirements in this standard and is, as evaluated by the examining physician, expected to extend beyond 90 days.

Based on the above definitions, the facility licensee was expected to recognize that the operators medical condition had become permanent in nature, by extending well beyond 90 days such that the operator was required to leave the site permanently and transition into a long-term disability program.

Analysis.

The failure of the facility licensee to notify the NRC within 30 days of changes in a licensed senior operators medical condition was a performance deficiency that was reasonably within the facility licensees ability to foresee and prevent. This issue was evaluated using the traditional enforcement process because it negatively impacted the NRCs ability to perform its regulatory oversight function. Specifically, the failure to report changes in a licensed senior operators medical condition prevented the NRC from taking action to issue either a license amendment or termination, as appropriate.

This performance deficiency was determined to be SL-IV because it fits the SL-IV example of Enforcement Policy Section 6.4.d.1, Violation Examples: Licensed Reactor Operators. This section states the following:

Severity Level IV violations involve  : A non-willful compromise of an application, test, or examination required by 10 CFR Part 55. For example

(b) an individual operator who did not meet the American National Standards Institute/American Nuclear Society (ANSI/ANS) 3.4, Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants, Section 5, Health Requirements and Disqualifying Conditions, as certified on NRC Form 396, Certification of Medical Examination by Facility Licensee, required by 10 CFR 55.23, Certification, but who did not perform the functions of a licensed operator or senior operator while having a disqualifying medical condition.

This example fits the non-conforming senior operator, who would have required either a license amendment or termination for the unreported permanent medical condition, but who did not engage in licensed activities from the time that a license amendment or termination was required.

This finding is being treated as a NCV because:

(1) the facility licensee placed the violation into the corrective action program as Notification 50912407,
(2) the facility licensee restored compliance within a reasonable period of time by requesting termination of the license,
(3) the violation was non-repetitive as determined by a search on NRC databases for prior violations issued to the facility licensee, and
(4) the violation did not involve willfulness. There is no cross-cutting aspect associated with this violation because it was processed using traditional enforcement.

In accordance with Inspection Manual Chapter 0612, Appendix B, Issue Screening, the performance deficiency was also evaluated for significance under the Reactor Oversight Process. Licensed operators are treated as mitigating systems under the Reactor Oversight Process regulatory framework. Since the facility licensee administratively suspended the senior operators qualifications prior to the need for a license amendment or termination, the operator was unable to perform licensed duties while diagnosed as medically unfit. As a result, there was no adverse effect on the Mitigating Systems Cornerstone objective of the Reactor Oversight Process and, therefore, no more-than-minor Reactor Oversight Process violation exists.

Enforcement.

Title 10 CFR 55.25 requires, in part, that, if the licensee (licensed senior operator) develops a permanent physical condition that causes the licensed senior operator to fail to meet the requirements of 10 CFR 55.21, the facility licensee shall notify the Commission, within 30 days of learning of the diagnosis, in accordance with 10 CFR 50.74(c). Contrary to the above, from May 23, 2015, to April 6, 2017, the facility licensee failed to notify the Commission, within 30 days of learning of the diagnosis, in accordance with 10 CFR 50.74(c), that a licensed senior operator developed a permanent physical condition that caused the licensed senior operator to fail to meet the requirements of 10 CFR 55.21. Specifically, a licensed senior operator permanently left the site on December 1, 2014, and transitioned into a long-term disability program on April 23, 2015. The facility licensee subsequently initiated action to terminate the senior operators license, effective April 6, 2017. Because this finding is of very low safety significance and was entered into the CAP as Notification 50912407, this violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the NRC Enforcement Policy. NCV 05000275/2017002-03; 05000323/2017002-03, Failure to Report a Permanent Medical Condition Within 30 Days

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed two instances of degraded performance or condition of safety-significant structures, systems, and components (SSCs):

  • June 21, 2017, Units 1 and 2, containment fan cooling units The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensees corrective actions. The inspectors reviewed the licensees work practices to evaluate whether these may have played a role in the degradation of the SSCs. The inspectors assessed the licensees characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.

These activities constituted completion of two maintenance effectiveness samples, as defined in Inspection Procedure 71111.12.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed four risk assessments performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk:

  • April 10, 2017, Unit 1, vital battery charger 132, maintenance outage
  • April 26, 2017, Unit 1, vital bus F, maintenance outage
  • May 30 - June 1, 2017, Units 1 and 2, single source of off-site power for planned switchyard outage
  • June 12, 2017, Unit 1, reactor coolant system mid loop operations for vacuum fill The inspectors verified that these risk assessments were performed in a timely manner and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant procedures. The inspectors reviewed the accuracy and completeness of the licensees risk assessments and verified that the licensee implemented appropriate risk management actions based on the result of the assessments.

Additionally, on May 2, 2017, the inspectors observed portions of one emergent work activity, Unit 1, residual heat removal pump 1-2, troubleshooting and repair of a failed lower bearing thermocouple, that had the potential to affect the functional capability of mitigating systems. The inspectors verified that the licensee appropriately developed and followed a work plan for this activity. The inspectors verified that the licensee took precautions to minimize the impact of the work activity on unaffected SSCs.

These activities constituted completion of five maintenance risk assessments and emergent work control inspection samples, as defined in Inspection Procedure 71111.13.

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

The inspectors reviewed five operability determinations that the licensee performed for degraded or nonconforming SSCs:

  • April 27, 2017, Unit 1, volume control tank outlet isolation valve LCV-112B, failure to open following integrated safeguards test
  • June 15-16, 2017, operability determination of Unit 1, emergency diesel generator 1-3, radiator leak following maintenance The inspectors reviewed the timeliness and technical adequacy of the licensees evaluations. Where the licensee determined the degraded SSC to be operable, the inspectors verified that the licensees compensatory measures were appropriate to provide reasonable assurance of operability. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability of the degraded SSC.

These activities constituted completion of five operability and functionality review samples, as defined in Inspection Procedure 71111.15.

b. Findings

No findings were identified.

1R17 Evaluations of Changes, Tests, and Experiments

Evaluations of Changes, Tests, and Experiments

a. Inspection Scope

The inspectors reviewed 7 evaluations performed pursuant to 10 CFR 50.59, to determine whether the evaluations were adequate and that prior NRC approval was obtained as appropriate. The inspectors also reviewed 12 screenings and/or applicability determinations, where licensee personnel had determined that a 10 CFR 50.59 evaluation was not necessary. The inspectors reviewed these documents to:

  • verify that evaluations were performed in accordance with 10 CFR 50.59 when changes, tests, or experiments were made;
  • verify that the licensee has appropriately concluded that the change, test or experiment can be accomplished without obtaining a license amendment;
  • verify that safety issues related to the changes, tests, or experiments have been resolved; and
  • verify that the licensees conclusions were correct and consistent with 10 CFR 50.59 for the changes, tests, or experiments that the licensee determined that evaluations were not required The inspectors used, in part, Nuclear Energy Institute (NEI) 96-07, Guidelines for 10 CFR 50.59 Implementation, Revision 1, to determine acceptability of the completed evaluations and screenings. The NEI document was endorsed by the NRC in Regulatory Guide 1.187, Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments, dated November 2000. The list of evaluations, screenings, and/or applicability determinations reviewed by the inspectors is included as an attachment to this report.

These activities constituted 19 reviews of evaluations, screenings, and/or applicability determinations as defined in Inspection Procedure 71111.17T.

b. Findings

No findings were identified.

1R18 Plant Modifications

a. Inspection Scope

On May 3-17, 2017, the inspectors reviewed a permanent modification to the Units 1 and 2, NFPA 805 fire detection SSCs, Work Order 68041843. The inspectors reviewed the design and implementation of the modification. The inspectors verified that work activities involved in implementing the modification did not adversely impact operator actions that may be required in response to an emergency or other unplanned event.

The inspectors verified that post-modification testing was adequate to establish the operability of the SSC as modified.

These activities constituted completion of one sample of permanent modifications, as defined in Inspection Procedure 71111.18.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed six post-maintenance testing activities that affected risk-significant SSCs:

  • April 5, 2017, Unit 2, safety injection pump 2-1 oil change, clean, and inspect, post maintenance testing, Work Order 64114156
  • June 22-23, 2017, Unit 1, containment fan cooling unit 1-5 replacement, post maintenance testing, Work Order 68034821 The inspectors reviewed licensing- and design-basis documents for the SSCs and the maintenance and post-maintenance test procedures. The inspectors observed the performance of the post-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs.

These activities constituted completion of six post-maintenance testing inspection samples, as defined in Inspection Procedure 71111.19.

b. Findings

No findings were identified.

1R20 Refueling and Other Outage Activities

a. Inspection Scope

During the stations Unit 1 refueling outage (1R20) that concluded on June 21, 2017, the inspectors evaluated the licensees outage activities. The inspectors verified that the licensee considered risk in developing and implementing the outage plan, appropriately managed personnel fatigue, and developed mitigation strategies for losses of key safety functions. This verification included the following:

  • Review of the licensees outage plan prior to the outage
  • Review and verification of the licensees fatigue management activities
  • Monitoring of shut-down and cool-down activities
  • Verification that the licensee maintained defense-in-depth during outage activities
  • Observation and review of reduced-inventory and mid-loop activities
  • Observation and review of fuel handling activities
  • Monitoring of heat-up and startup activities These activities constituted completion of one refueling outage sample, as defined in Inspection Procedure 71111.20.

b. Findings

Introduction.

The inspectors identified a Green, self-revealing, non-cited violation of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, because PG&E personnel failed to follow the requirements of AD7.ID14, Assessment of Integrated Risk, Revision 11. Specifically, PG&E personnel failed to obtain shift manager permission, conduct a protected equipment briefing, and document shift manager approval prior to performing work on protected equipment. This resulted in a loss of flow of cooling water to one of two in service shutdown cooling residual heat removal (RHR) heat exchangers and subsequent perturbation in reactor coolant system (RCS) temperature during refueling outage 1R20.

Description.

During plant shutdown conditions, both train A and train B of the RHR system are used in the shutdown cooling mode to remove decay heat generated from the nuclear fuel. The component cooling water (CCW) system is used to provide cooling flow to the RHR heat exchangers which are used as part of the shutdown cooling system. As part of the normal shutdown cooling system alignment, CCW header A provides cooling water flow to the train A, RHR heat exchanger and CCW header B provides cooling water flow to the train B, RHR heat exchanger. CCW header C is not normally aligned to provide cooling flow to a RHR heat exchanger. While preparing for maintenance on the Unit 1, CCW header C, motor-operated flow control valve FCV-355, PG&E operations personnel closed CCW cross tie valves CCW-23 and CCW-24. At the time of the cross tie valve closures, CCW heat exchanger 1-1 was removed from service for maintenance. Flow to CCW header A was being supplied from CCW header B via valves CCW-23 and CCW-24. The closure of the cross tie valves removed CCW cooling flow from CCW header A and accordingly to one of the two operating trains of RHR shutdown cooling. Due to the subsequent imbalance of flowrates through the CCW headers, RCS temperature fluctuated by approximately 8 degrees Fahrenheit prior to the CCW normal lineup being restored approximately 10 minutes later. Train B of RHR shutdown cooling remained in service throughout the event and was sufficient to prevent an uncontrollable increase in RCS temperature and the onset of core boiling. Time to boil in the RCS during the event was 154 minutes. PG&E determined that the causes of the loss of flow of CCW to the RHR heat exchanger included failure to follow protected equipment postings, improper operations turnover, inadequate situational awareness, and improper outage work planning logic. PG&E entered the event into their corrective action program and conducted a barrier analysis to determine the causes of the event and to identify corrective actions. PG&E initiated actions to prevent future recurrence including evaluating changes to training and work practices. The inspectors reviewed PG&Es actions to identify and correct the cause of the event.

Analysis.

The inspectors determined that PG&Es failure to follow AD7.ID14, Assessment of Integrated Risk, Section 5.14 Performing Work on Posted Protected Equipment, was a performance deficiency within PG&Es ability to foresee and correct.

This performance deficiency was considered to be more than minor because it impacted the configuration control attribute of the Mitigating Systems cornerstone and its objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the loss of cooling flow to the RHR heat exchanger while in shutdown cooling mode resulted in a perturbation in RCS temperature of approximately 8 degrees Fahrenheit. The finding was evaluated in accordance with IMC 0609, Appendix G, Shutdown Operations Significance Determination Process, and determined to be of very low safety significance (Green)since it did not represent a loss of system safety function of at least a single train for greater than four hours. The finding had a cross-cutting aspect in the area of human performance associated with conservative bias because PG&E personnel did not use decision-making practices that emphasize prudent choices over those that are simply allowable. Specifically, despite being authorized to close CCW cross connect valves by the work control process, PG&E personnel did not question the impact of their actions on shutdown cooling [H.14].

Enforcement.

Title 10 CFR Part 50, Appendix B, Criterion V requires, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. PG&E procedure AD7.ID14, Assessment of Integrated Risk, Revision 11, Section 5.14 requires that personnel obtain shift manager permission, conduct a protected equipment briefing, and document shift manager approval prior to performing work on protected equipment.

Contrary to the above, PG&E maintenance and operations personnel conducted work on the Unit 1, CCW system without obtaining shift manager permission, conducting a protected equipment briefing, and documenting shift manager permission - actions designed to prevent unnecessary protected system equipment impacts. These actions resulted in a loss of flow of cooling water to one of two in service shutdown cooling RHR heat exchangers and subsequent perturbation in RCS temperature during refueling outage 1R20. After the issue was identified, PG&E entered the issue into their corrective action program as Notification 50915907 and initiated a barrier review. Additionally, PG&E initiated actions to prevent future recurrence including evaluating changes to training and work practices. Because this violation is of very low safety significance (Green) and PG&E entered the issue into their corrective action program, this violation is being treated as a NCV consistent with the NRC Enforcement Policy. NCV 05000275/2017002-04, Failure to Follow Procedures Results in Partial Loss of Cooling Flow to Shutdown Cooling

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed six risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the SSCs were capable of performing their safety functions:

In-service tests:

  • April 18, 2017, Unit 1, main steam safety valve testing of RV-4, per procedure STP M-77 Containment isolation valve surveillance tests:
  • May 11, 2017, Unit 1, containment isolation valve testing of penetration 54 associated with instrument air valves, per procedure STP V-654
  • May 24, 2017, Unit 1, containment isolation valve testing of penetration 59C associated with safety injection accumulator instrument line, per procedure STP V-659C Other surveillance tests:
  • April 24, 2017, Unit 1, 4 kV bus H non-SI auto transfer test, per procedure STP M-13H
  • May 10-11, 2017, Unit 1, leakage testing of systems outside containment, per procedure STP M-86G The inspectors verified that these tests met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the test satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected SSCs following testing.

These activities constituted completion of six surveillance testing inspection samples, as defined in Inspection Procedure 71111.22.

b. Findings

No findings were identified.

2.

RADIATION SAFETY

Cornerstones: Public Radiation Safety and Occupational Radiation Safety

2RS1 Radiological Hazard Assessment and Exposure Controls

a. Inspection Scope

The inspectors evaluated the licensees performance in assessing the radiological hazards in the workplace associated with licensed activities. The inspectors assessed the licensees implementation of appropriate radiation monitoring and exposure control measures for both individual and collective exposures. During the inspection, the inspectors interviewed licensee personnel, walked down various areas in the plant, performed independent radiation dose rate measurements, and observed postings and physical controls. The inspectors reviewed licensee performance in the following areas:

  • Radiological hazard assessment, including a review of the plants radiological source terms and associated radiological hazards. The inspectors also reviewed the licensees radiological survey program to determine whether radiological hazards were properly identified for routine and non-routine activities and assessed for changes in plant operations.
  • Instructions to workers, including radiation work permit requirements and restrictions, actions for electronic dosimeter alarms, changing radiological condition, and radioactive material container labeling.
  • Contamination and radioactive material control, including release of potentially contaminated material from the radiologically controlled area, radiological survey performance, radiation instrument sensitivities, material control and release criteria, and control and accountability of sealed radioactive sources.
  • Radiological hazards control and work coverage. During walk downs of the facility and job performance observations, the inspectors evaluated ambient radiological conditions, radiological postings, adequacy of radiological controls, radiation protection job coverage, and contamination controls. The inspectors also evaluated dosimetry selection and placement as well as the use of dosimetry in areas with significant dose rate gradients. The inspectors examined the licensees controls for items stored in the spent fuel pool and evaluated airborne radioactivity controls and monitoring.
  • Radiation worker performance and radiation protection technician proficiency with respect to radiation protection work requirements. The inspectors determined if workers were aware of significant radiological conditions in their workplace, radiation work permit controls/limits in place, and electronic dosimeter dose and dose rate set points. The inspectors observed radiation protection technician job performance, including the performance of radiation surveys.
  • Problem identification and resolution for radiological hazard assessment and exposure controls. The inspectors reviewed audits, self-assessments, and corrective action program documents to verify problems were being identified and properly addressed for resolution.

These activities constitute completion of the seven required samples of radiological hazard assessment and exposure control program, as defined in Inspection Procedure 71124.01.

b. Findings

No findings were identified.

2RS3 In-Plant Airborne Radioactivity Control and Mitigation

a. Inspection Scope

The inspectors evaluated whether the licensee controlled in-plant airborne radioactivity concentrations consistent with ALARA principles and that the use of respiratory protection devices did not pose an undue risk to the wearer. During the inspection, the inspectors interviewed licensee personnel, walked down various areas in the plant, and reviewed licensee performance in the following areas:

  • Engineering controls, including the use of permanent and temporary ventilation systems to control airborne radioactivity. The inspectors evaluated installed ventilation systems, including review of procedural guidance, verification the systems were used during high-risk activities, and verification of airflow capacity, flow path, and filter/charcoal unit efficiencies. The inspectors also reviewed the use of temporary ventilation systems used to support work in contaminated areas such as high-efficiency particulate air (HEPA)/charcoal negative pressure units.

Additionally, the inspectors evaluated the licensees airborne monitoring protocols, including verification that alarms and set points were appropriate.

  • Use of respiratory protection devices, including an evaluation of the licensees respiratory protection program for use, storage, maintenance, and quality assurance of National Institute for Occupational Safety and Health (NIOSH)certified equipment, air quality and quantity for supplied-air devices and self-contained breathing apparatus (SCBA) bottles, qualification and training of personnel, and user performance.
  • Self-contained breathing apparatus for emergency use, including the licensees capability for refilling and transporting SCBA air bottles to and from the control room and operations support center during emergency conditions, hydrostatic testing of SCBA bottles, status of SCBA staged and ready for use in the plant including vision correction, mask sizes, etc., SCBA surveillance and maintenance records, and personnel qualification, training, and readiness.
  • Problem identification and resolution for airborne radioactivity control and mitigation. The inspectors reviewed audits, self-assessments, and corrective action documents to verify problems were being identified and properly addressed for resolution.

These activities constitute completion of the four required samples of in-plant airborne radioactivity control and mitigation program, as defined in Inspection Procedure 71124.03.

b. Findings

No findings were identified.

4.

OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security

4OA1 Performance Indicator Verification

.1 Safety System Functional Failures (MS05)

a. Inspection Scope

For the period of April 1, 2016 through March 31, 2017, the inspectors reviewed licensee event reports (LERs), maintenance rule evaluations, and other records that could indicate whether safety system functional failures had occurred. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, and NUREG-1022, Event Reporting Guidelines: 10 CFR 50.72 and 50.73, Revision 3, to determine the accuracy of the data reported.

These activities constituted verification of the safety system functional failures performance indicator for Units 1 and 2, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

.2 Mitigating Systems Performance Index: Emergency AC Power Systems (MS06)

a. Inspection Scope

The inspectors reviewed the licensees mitigating system performance index data for the period of April 1, 2016 through March 31, 2017, to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constituted verification of the mitigating system performance index for emergency ac power systems for Units 1 and 2, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

.3 Mitigating Systems Performance Index: High Pressure Injection Systems (MS07)

a. Inspection Scope

The inspectors reviewed the licensees mitigating system performance index data for the period of April 1, 2016 through March 31, 2017, to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constituted verification of the mitigating system performance index for high pressure injection systems for Units 1 and 2, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

.4 Occupational Exposure Control Effectiveness (OR01)

a. Inspection Scope

The inspectors verified that there were no unplanned exposures or losses of radiological control over locked high radiation areas and very high radiation areas during the period of June 1, 2016, to April 30, 2017. The inspectors reviewed a sample of radiologically controlled area exit transactions showing exposures greater than 100 mrem. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constituted verification of the occupational exposure control effectiveness performance indicator as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

.5 Radiological Effluent Technical Specifications (RETS)/Offsite Dose Calculation Manual

(ODCM) Radiological Effluent Occurrences (PR01)

a. Inspection Scope

The inspectors reviewed corrective action program records for liquid or gaseous effluent releases that occurred during the period of June 1, 2016, to April 30, 2017, and were reported to the NRC to verify the performance indicator data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the reported data.

These activities constituted verification of the RETS/ODCM radiological effluent occurrences performance indicator as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review

a. Inspection Scope

Throughout the inspection period, the inspectors performed daily reviews of items entered into the licensees corrective action program and periodically attended the licensees condition report screening meetings. The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the corrective action program for resolution. The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified. The inspectors also reviewed the licensees problem identification and resolution activities during the performance of the other inspection activities documented in this report.

b. Findings

No findings were identified.

.2 Annual Follow-up of Selected Issues

a. Inspection Scope

The inspectors selected two issues for an in-depth follow-up:

  • On May 19, 2017, Anchor-Darling double disc gate valve wedge pin failure operating experience.

The inspectors reviewed the status of PG&Es efforts to address operating experience (OE) concerning Anchor-Darling double disc gate valve wedge pin failures. As part of the inspection, the inspectors assessed PG&Es response to industry OE including reviewing extent of condition evaluations, valve diagnostic traces, observing valve inspection activities, and interviewing PG&E engineering and maintenance personnel.

The inspectors conducted an in-depth review of the licensees fire transient combustible permit program and change management issues related to transiting to new NFPA 805 program requirements. Specifically, the inspectors reviewed the training, planning, and requirements associated with the licensee NFPA 0805 implementation related to transient combustible permit program. The inspectors assessed the licensees problem identification threshold, interim, and compensatory actions. The inspectors verified that the licensee appropriately prioritized the corrective actions and these actions were adequate to correct the conditions associated with transient combustible permit process.

These activities constituted completion of two annual follow-up samples as defined in Inspection Procedure 71152.

b. Findings

No findings were identified.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On May 12, 2017, the inspectors presented the radiation safety inspection results (Sections 2RS1, 2RS3, 4OA1.4, and 4OA1.5) to Ms. P. Gerfen, Senior Director Plant Manager, and other members of the licensee staff. The licensee acknowledged the issues presented.

The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

On May 17, 2017, the inspectors presented the ISI inspection results (Section 1R08) to Mr. J. Welsch, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

On May 17, 2017, the inspectors presented the results of the licensed operator requalification program inspection (Section 1R11.3) to Ms. P. Gerfen, Senior Director Plant Manager, and other members of the licensee's staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

On June 23, 2017, the inspectors presented the evaluations of changes, tests and experiments inspection results (Section 1R17) to J. Welsch, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

On July 11, 2017, the resident inspectors presented the quarterly inspection results to J.

Welsch, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

T. Baldwin, Director, Nuclear Site Services
K. Bych, Manager, Engineering
D. Cortina, Manager, Chemistry
D. Evans, Director, Security & Emergency Services
R. Fortier, Lead Exam Writer
R. Gagne, Supervisor, Hazardous Waste
P. Gerfen, Senior Director Plant Manager
M. Ginn, Manager, Emergency Planning
D. Gonzalez, Supervisor, Inservice Inspection
S. Guess, Manager, Operations
E. Halpin, Sr. Vice President, Chief Nuclear Officer Generation
H. Hamzehee, Manager, Regulatory Services
M. Hayes, Supervisor, Radiation Protection
A. Heffner, NRC Interface, Regulatory Services
J. Hill, Engineer
J. Hinds, Director, Quality Verification
K. Hinrichsen, Supervisor, Radiation Protection
L. Hopson, Director Maintenance Services
T. Irving, Manager, Radiation Protection
K. Johnston, Director of Operations
K. Kaminski, Supervisor, Operations
R. Kelley, Supervisor, Radiation Protection
B. Lopez, Engineer, Regulatory Services
D. Madsen, NRC Interface, Regulatory Services
M. McCoy, NRC Interface, Regulatory Services
J. Morris, Senior Advising Engineer
C. Murry, Director Nuclear Work Management
C. Neary, Welding Engineer
E. Nelson, Director, Regulatory Projects
J. Nimick, Senior Director Nuclear Services
P. Nugent, Director, Quality Verification
L. Parker, Supervisor, STARS
A. Peck, Director, Nuclear Engineering
D. Peterson, Director, Learning Services
M. Sarantos, Supervisor, Radiation Protection
B. Sawyer, Simulator Support
L. Sewell, Principal Health Physicist, Radiation Protection
M. Sharp, Manager, Design Engineering
B. Simpson, Manager (Acting), Operations Training
J. Skov, Senior Advisor, Regulatory Services
C. Sutton, Supervisor, Radiation Protection
P. Vobork, Manager, Outage Work Week
R. Waltos, Assistant Director, Engineering
A. Warwick, Supervisor, Emergency Planning
J. Welsch, Site Vice President
D. Williams, Operations

Attachment 1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000275/2017002-01 NCV Inadequate Expansion Scope of Risk-Informed Welds

(Section 1R08)

05000275/2017002-02 NCV Failure to Conduct Required Biennial Medical Examinations
05000323/2017002-02 Within Two Years (Section 1R11.3)
05000275/2017002-03 NCV Failure to Report a Permanent Medical Condition Within
05000323/2017002-03 30 Days (Section 1R11.3)
05000275/2017002-04 NCV Failure to Follow Procedures Results in Partial Loss of Cooling

Flow to Shutdown Cooling (Section 1R20)

LIST OF DOCUMENTS REVIEWED