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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M0721999-10-19019 October 1999 Forwards NRC Rept Number 17, Requal Tracking Rept from Operator Licensing Tracking Sys.Rept Was Used by NRC to Schedule Requalification Exam for Operators & Record Pass Dates ML20217D8361999-10-11011 October 1999 Provides NRC with Summary of Activities at TMI-2 During 3rd Quarter of 1999 ML20217F8271999-10-0707 October 1999 Forwards Pmpr 99-13, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting Period 990828- 0924.Diskette Containing Pmpr in Wordperfect 8 Is Encl. All Variances Are Expressed with Regard to Current Plans ML20212L1831999-10-0101 October 1999 Responds to Recent Ltr to Wd Travers Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Performance of Millstone to Ensure Adequate Protection to Public Health ML20212L2081999-10-0101 October 1999 Responds to Recent Ltrs to President Wj Clinton,Chairman Jackson & Commissioners & Wd Travers,Expressing Concerns Re Millstone NPPs & Continued Lack of Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance ML20212K1241999-10-0101 October 1999 Responds to Recent Ltrs to Chairman Jackson,Commissioners & Wd Travers,Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performace of Millstone to Ensure That Public Health & Safety,Adequately Protected ML20212L1971999-10-0101 October 1999 Responds to Recent Ltr to Chairman Jackson & Commissioners Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance to Ensure Public Health & Safety ML20212J9991999-10-0101 October 1999 Responds to Recent Ltr to President Clinton,H Clinton, Chairman Jackson &/Or Wd Travers Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performance of Plant to Ensure That Public Health & Safety Adequately Protected ML20212L0061999-10-0101 October 1999 Discusses GL 97-06 Issued by NRC on 971231 & Gpu Response for Three Mile Island .Staff Reviewed Response & Found No New Concerns with Condition of SG Internals or with Insp Practices Used to Detect Degradation of SG Internals ML20212L2171999-10-0101 October 1999 Responds to Recent Ltr to President Wj Clinton,Chairman Jackson & Commissioners,Wd Travers & Ferc,Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island ML20212K8771999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Three Mile Island on 990913.No Areas Identified in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Provides Historical Listing of Plant Issues & Insp Schedule ML20212K8551999-09-30030 September 1999 Informs That During 990921 Telcon Between P Bissett & F Kacinko,Arrangements Were Made for Administration of Licensing Exams at Facility During Wk of 000214.Outlines Should Be Provided to NRC by 991122 ML20216J6581999-09-28028 September 1999 Provides Info as Requested of Licensees by NRC in Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Exams ML20212J0011999-09-27027 September 1999 Forwards Insp Rept 50-289/99-07 on 990828.No Violations Noted ML20212E1971999-09-16016 September 1999 Forwards Rev 11 of Gpu Nuclear Operational QAP, Reflecting Organizational Change in Which Functions & Responsibilities of Nuclear Safety & Technical Support Div Were Assigned to Other Divisions ML20212A2101999-09-13013 September 1999 Forwards Rev 3 of Gpu Nuclear Post-Defueling Monitored Storage QAP for Three Mile Island Unit 2, Including Changes Made During 1998.Description of Changes Provided on Page 2 ML20216G4151999-09-0909 September 1999 Forwards Pmpr 99-12, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting Period 990731- 0827.All Variances Expressed with Regard to Current Operations Plans ML20211M5861999-09-0202 September 1999 Forwards non-proprietary & Proprietary Response to NRC 990708 RAI Re TS Change Request 272,reactor Coolant Sys Coolant Activity.Proprietary Encl Withheld ML20211M6591999-09-0101 September 1999 Forwards Errata Page to 990729 Suppl to TS Change Request 274,to Reflect Proposed Changes Requested by . Page Transmitted by Submitted in Error ML20211L2401999-09-0101 September 1999 Submits Response to NRC AL 99-02, Operator Reactor Licensing Action Estimates ML20211H3731999-08-27027 August 1999 Responds to NRC 990810 RAI Re TMI LAR 285 & TMI-2 LAR 77 Re Changes Reflecting Storage of TMI-1 Radioactive Matls in TMI-2 Facility.Revised License Page mark-up,incorporating Response,Encl ML20211H4001999-08-27027 August 1999 Responds to NRC 990810 RAI Re TMI-1 LAR 285 & TMI-2 LAR 77 Re Changes to Clarify Authority to Possess Radioactive Matls Without Unit Distinction.Revised License Page mark-up, Incorporating Response Encl ML20211K2391999-08-23023 August 1999 Forwards fitness-for-duty Performance Data Repts for TMI, Oyster Creek & Corporate Headquarters Located in Parsippany, Nj ML20211H5041999-08-20020 August 1999 Forwards Proprietary & non-proprietary Rept MPR-1820,rev 1, TMI Nuclear Generating Station OTSG Kinetic Expansion Insp Criteria Analysis. Affidavit Encl.Proprietary Rept Wihheld 05000289/LER-1999-007, Forwards LER 99-007-01 Re Increasing Failure Rate of ESAS Relays.Rept Supplements Preliminary Info Re Determination of Root Cause & Long Term Corrective Actions.Changes Made for Supplement Are Indicated in Bold Typeface1999-08-20020 August 1999 Forwards LER 99-007-01 Re Increasing Failure Rate of ESAS Relays.Rept Supplements Preliminary Info Re Determination of Root Cause & Long Term Corrective Actions.Changes Made for Supplement Are Indicated in Bold Typeface ML20211A4261999-08-19019 August 1999 Forwards Insp Rept 50-289/99-04 on 990606-0717.Two Severity Level 4 Violations Occurred & Being Treated as Noncited Violations ML20211H3571999-08-19019 August 1999 Forwards Itemized Response to NRC 990712 RAI Re TS Change Request 248 Re Remote Shutdown Sys,Submitted on 981019 ML20211A3931999-08-12012 August 1999 Requests NRC Concurrence with Ongoing Analytical Approach as Described in Attachment,Which Is Being Utilized by Gpu Nuclear to Support Detailed License Amend Request to Revise Design Basis for TMI-1 Pressurizer Supports ML20210R4691999-08-11011 August 1999 Forwards Update 3 to Post-Defueling Monitored Storage SAR, for TMI-2.Update 3 Revises SAR to Reflect Current Plant Configuration & Includes Minor Editorial Changes & Corrections.Revised Pages on List of Effective Pages ML20210N7601999-08-10010 August 1999 Informs That NRC Staff Reviewed Applications Dtd 990629, Which Requested Review & Approval to Allow Authority to Possess Radioactive Matl Without Unit Distinction Between Units 1 & 2.Forwards RAI Re License Amend Request 285 ML20210N7191999-08-0606 August 1999 Forwards Notice of Partial Denial of Amend to FOL & Opportunity for Hearing Re Proposed Change to TS 3.1.12.3 to Add LCO That Would Allow Continued HPI Operation ML20210L3831999-07-30030 July 1999 Responds to NRC 990617 RAI Re OTSG Kinetic Expansion Region Insp Acceptance Criteria That Was Used for Dispositioning Indications During Cycle 12 Refueling (12R) Outage ML20210K7371999-07-30030 July 1999 Forwards Rev 2 to 86-5002073-02, Summary Rept for Bwog 20% Tp LOCA, Which Corrects Evaluation Model for Mk-B9 non- Mixing Vane Grid Previously Reported in Util to Nrc,Per 10CFR50.46 ML20210L1151999-07-28028 July 1999 Confirms Two Senior Management Changes Made within Amergen Energy Co,Per Proposed License Transfer & Conforming Administrative License Amends for TMI-1 05000289/LER-1999-009, Forwards LER 99-009-00 Re 990626 Event Involving Partial Loss of Offsite Power & Subsequent Automatic Start of EDG 1A.Commitments Made by Util Are Contained in long-term Corrective Actions Section1999-07-22022 July 1999 Forwards LER 99-009-00 Re 990626 Event Involving Partial Loss of Offsite Power & Subsequent Automatic Start of EDG 1A.Commitments Made by Util Are Contained in long-term Corrective Actions Section ML20216D4001999-07-22022 July 1999 Provides Summary of Activities at TMI-2 During 2nd Quarter of 1999 ML20210B8231999-07-21021 July 1999 Forwards Exemption from Certain Requirements of 10CFR50.54(w) for Three Mile Island Nuclear Station,Unit 2 in Response to Licensee Application Dtd 990309,requesting Reduction in Amount of Insurance for Unit to Amount Listed ML20210G9471999-07-15015 July 1999 Forwards Pmpr 99-10, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting period,990605- 0702.Diskette Containing Pmpr in Wordperfect 8 Format Is Also Encl ML20209H9401999-07-15015 July 1999 Forwards Copy of Environ Assessment & Findings of No Significant Impact Re Application for Exemption Dtd 990309. Proposed Exemption Would Reduce Amount of Insurance for Onsite Property Damage Coverage as Listed ML20209G2451999-07-15015 July 1999 Advises That Suppl Info in Support of Proposed License Transfer & Conforming Adminstrative License Amends,Submitted in & Affidavit,Marked Proprietary,Will Be Withheld from Public Disclosure,Per 10CFR2.790(b)(5) ML20212K1701999-07-13013 July 1999 Submits Concerns Re Millstone & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Should Provide Adequate Emergency Planning in Case of Radiological Accident ML20216D9861999-07-12012 July 1999 Forwards RAI Re 981019 Application Request for Review & Approval of Operability & SRs for Remote Shutdown Sys. Response Requested within 30 Days of Receipt of Ltr ML20209G5861999-07-0909 July 1999 Forwards Insp Rept 50-289/99-05 on 990510-28.No Violations Noted ML20209F2571999-07-0909 July 1999 Forwards Staff Evaluation Rept of Individual Plant Exam of External Events Submittal on Three Mile Nuclear Station, Unit 1 ML20209D8451999-07-0808 July 1999 Forwards Insp Rept 50-289/99-06 on 990608-11.No Violations Noted.Overall Performance of ERO Very Good & Demonstrated, with Reasonable Assurance,That Onsite Emergency Plans Adequate & That Util Capable of Implementing Plan ML20209D6291999-07-0808 July 1999 Forwards Notice of Withdrawal & Corrected TS Pages 3-21 & 4-9 for Amend 211 & 4-5a,4-38 & 6-3 for Amend 212,which Was Issued in Error.Amends Failed to Reflect Previously Changes Granted by Amends 203 & 204 ML20209D5141999-07-0808 July 1999 Forwards RAI Re 981019 Application & Suppl ,which Requested Review & Approval of Revised Rc Allowable Dose Equivalent I-131 Activity Limit with Max Dose Equivalent Limit of 1.0 Uci/Gram.Response Requested within 30 Days 05000289/LER-1999-008, Forwards LER 99-008-00 Re Discovery of Degraded But Operable Condition of RB Emergency Cooling Sys.Condition Did Not Adversely Affect Health & Safety of Public1999-07-0202 July 1999 Forwards LER 99-008-00 Re Discovery of Degraded But Operable Condition of RB Emergency Cooling Sys.Condition Did Not Adversely Affect Health & Safety of Public ML20196J3981999-07-0101 July 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Npps. Y2K Readiness Disclosure for TMI-1 Encl ML20209C1131999-07-0101 July 1999 Forwards Signed Agreement as Proposed in NRC Requesting Gpu Nuclear Consent in Incorporate TMI-1 Thermo Lag Fire Barrier Final Corrective Action Completion Schedule Commitment of 000630 Into Co Modifying License 1999-09-09
[Table view] Category:OUTGOING CORRESPONDENCE
MONTHYEARML20217M0721999-10-19019 October 1999 Forwards NRC Rept Number 17, Requal Tracking Rept from Operator Licensing Tracking Sys.Rept Was Used by NRC to Schedule Requalification Exam for Operators & Record Pass Dates ML20212J9991999-10-0101 October 1999 Responds to Recent Ltr to President Clinton,H Clinton, Chairman Jackson &/Or Wd Travers Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performance of Plant to Ensure That Public Health & Safety Adequately Protected ML20212L0061999-10-0101 October 1999 Discusses GL 97-06 Issued by NRC on 971231 & Gpu Response for Three Mile Island .Staff Reviewed Response & Found No New Concerns with Condition of SG Internals or with Insp Practices Used to Detect Degradation of SG Internals ML20212L1831999-10-0101 October 1999 Responds to Recent Ltr to Wd Travers Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Performance of Millstone to Ensure Adequate Protection to Public Health ML20212L2081999-10-0101 October 1999 Responds to Recent Ltrs to President Wj Clinton,Chairman Jackson & Commissioners & Wd Travers,Expressing Concerns Re Millstone NPPs & Continued Lack of Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance ML20212K1241999-10-0101 October 1999 Responds to Recent Ltrs to Chairman Jackson,Commissioners & Wd Travers,Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performace of Millstone to Ensure That Public Health & Safety,Adequately Protected ML20212L2171999-10-0101 October 1999 Responds to Recent Ltr to President Wj Clinton,Chairman Jackson & Commissioners,Wd Travers & Ferc,Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island ML20212L1971999-10-0101 October 1999 Responds to Recent Ltr to Chairman Jackson & Commissioners Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance to Ensure Public Health & Safety ML20212K8771999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Three Mile Island on 990913.No Areas Identified in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Provides Historical Listing of Plant Issues & Insp Schedule ML20212K8551999-09-30030 September 1999 Informs That During 990921 Telcon Between P Bissett & F Kacinko,Arrangements Were Made for Administration of Licensing Exams at Facility During Wk of 000214.Outlines Should Be Provided to NRC by 991122 ML20212J0011999-09-27027 September 1999 Forwards Insp Rept 50-289/99-07 on 990828.No Violations Noted ML20211A4261999-08-19019 August 1999 Forwards Insp Rept 50-289/99-04 on 990606-0717.Two Severity Level 4 Violations Occurred & Being Treated as Noncited Violations ML20210N7601999-08-10010 August 1999 Informs That NRC Staff Reviewed Applications Dtd 990629, Which Requested Review & Approval to Allow Authority to Possess Radioactive Matl Without Unit Distinction Between Units 1 & 2.Forwards RAI Re License Amend Request 285 ML20210N7191999-08-0606 August 1999 Forwards Notice of Partial Denial of Amend to FOL & Opportunity for Hearing Re Proposed Change to TS 3.1.12.3 to Add LCO That Would Allow Continued HPI Operation ML20210B8231999-07-21021 July 1999 Forwards Exemption from Certain Requirements of 10CFR50.54(w) for Three Mile Island Nuclear Station,Unit 2 in Response to Licensee Application Dtd 990309,requesting Reduction in Amount of Insurance for Unit to Amount Listed ML20209H9401999-07-15015 July 1999 Forwards Copy of Environ Assessment & Findings of No Significant Impact Re Application for Exemption Dtd 990309. Proposed Exemption Would Reduce Amount of Insurance for Onsite Property Damage Coverage as Listed ML20209G2451999-07-15015 July 1999 Advises That Suppl Info in Support of Proposed License Transfer & Conforming Adminstrative License Amends,Submitted in & Affidavit,Marked Proprietary,Will Be Withheld from Public Disclosure,Per 10CFR2.790(b)(5) ML20216D9861999-07-12012 July 1999 Forwards RAI Re 981019 Application Request for Review & Approval of Operability & SRs for Remote Shutdown Sys. Response Requested within 30 Days of Receipt of Ltr ML20209F2571999-07-0909 July 1999 Forwards Staff Evaluation Rept of Individual Plant Exam of External Events Submittal on Three Mile Nuclear Station, Unit 1 ML20209G5861999-07-0909 July 1999 Forwards Insp Rept 50-289/99-05 on 990510-28.No Violations Noted ML20209D8451999-07-0808 July 1999 Forwards Insp Rept 50-289/99-06 on 990608-11.No Violations Noted.Overall Performance of ERO Very Good & Demonstrated, with Reasonable Assurance,That Onsite Emergency Plans Adequate & That Util Capable of Implementing Plan ML20209D6291999-07-0808 July 1999 Forwards Notice of Withdrawal & Corrected TS Pages 3-21 & 4-9 for Amend 211 & 4-5a,4-38 & 6-3 for Amend 212,which Was Issued in Error.Amends Failed to Reflect Previously Changes Granted by Amends 203 & 204 ML20209D5141999-07-0808 July 1999 Forwards RAI Re 981019 Application & Suppl ,which Requested Review & Approval of Revised Rc Allowable Dose Equivalent I-131 Activity Limit with Max Dose Equivalent Limit of 1.0 Uci/Gram.Response Requested within 30 Days ML20196J5631999-07-0101 July 1999 Informs That Util 981203 Joint Application with Amergen Energy Co Marked Proprietary Will Be Withheld from Public Disclosure Pursuant to 10CFR2.790(b)(5) & Section 103(b) of Atomic Energy Act of 1954,as Amended ML20196J5741999-06-30030 June 1999 Informs That as Result of Staff Review of Util Response to GL 92-01,rev 1,suppl 1,info Provided in Support of PT Limits License Amend & B&W Topical Rept,Staff Revised Info for Plant,Unit 1,in Reactor Vessel Integrity Database ML20196H6811999-06-29029 June 1999 Forwards Insp Rept 50-289/99-03 on 990425-0605.No Violations Noted.However,Adequacy of Assessment of Reactor Bldg Emergency Cooler Operability Prior to Conducting Maintenance on One Reactor Bldg Spray Sys,Questionable ML20212H8711999-06-21021 June 1999 Discusses Updated Schedule Commitment Submitted by Gpu on 990602 for Implementing Thermo-Lag 330-1 Fire Barrier C/As & Completion of Thermo-Lag Effort at TMI-1.Informs NRC Will Incorporate Commitment Into Co Modifying License ML20195K2821999-06-17017 June 1999 Forwards Request for Addl Info Re Kinetic Expansion Region Inspection Acceptance Criteria ML20212H6621999-06-0404 June 1999 Informs That NRC Office of Nuclear Reactor Regulation Reorganized Effective 990328.As Part of Reorganization,Div of Licensing Project Mgt Created.Ss Bajwa Will Be Section Chief for Three Mile Island Nuclear Station ML20207E7201999-05-27027 May 1999 Discusses Reorganization of Nrr,Effective 990328. Organization Chart Encl ML20207B6541999-05-27027 May 1999 Forwards SER Accepting Util Program to Periodically Verify design-basis Capability of safety-related MOV at TMI-1 & That Util Adequately Addressed Actions Requested in GL 96-05 ML20207C0321999-05-18018 May 1999 Forwards Fifth Rept Which Covers Month of Apr 1999. Commission Approved Transfer of TMI-1 Operating License from Gpu to Amergen & Transfer of Operating License for Pilgrim Station from Beco to Entergy Nuclear Generating Co ML20206S3411999-05-14014 May 1999 Forwards Insp Rept 50-289/99-02 on 990314-0424.Violations Occurred & Being Treated as non-cited Violations.Security Program Was Inspected During Period & Found to Be Effective ML20206N5831999-05-13013 May 1999 Requests Description of Proposed Corrective Actions for Fire Zones AB-FZ-3,AB-FZ-5,AB-FZ-7,FH-FZ-2,CB-FA-1 & FH-FZ-6. Confirmation That Corrective Actions & Commitments Made Will Be Completed by 991231,requested IR 05000298/19980091999-05-12012 May 1999 Refers to Insp Rept 50-298/98-09 Conducted Between 981227-990130.During Insp,Apparent Violation of 10CFR50.50 Identified & Being Treated as non-cited ML20206H3571999-05-0606 May 1999 Forwards RAI Re 981203 Application & Suppls & 0416,requesting Review & Approval of Revised Core Protection SL & Bases for TMI-1 to Reflect Average of 20% of Tubes Plugged Per Sg.Response Requested within 10 Days of Receipt ML20207A5401999-04-29029 April 1999 Informs That Licensee 980930 Response to GL 96-06,appears to Be Reasonable & Appropriate for Specific Design & Configuration of RB Emergency Cooling at Plant,Unit 1 & That Staff Satisfied with Licensee Resolution of Waterhammer ML20206D4001999-04-20020 April 1999 Informs of Completion of Review of Gpu Request for Exemption Submitted on 961231,970908,971230,980521,981014,981125 & 981223 from Requirements of 10CFR50,App R,Section III.G.2 for TMI Unit 1.Forwards Exemption & Safety Evaluation ML20205S6791999-04-16016 April 1999 Forwards Insp Rept 50-289/99-01 on 990131-0313.No Violations Noted.Identification by Licensee Staff of Elevated Tritium Activity in Monitoring Well Led to Investigation & Identification of Leak from Buried Radwaste Path ML20205P3391999-04-0909 April 1999 Discusses Results of Plant Performance Review for Three Mile Island Completed on 990225.Historical Listing of Plant Issues That Were Considered During PPR Encl IR 05000289/19980061999-03-26026 March 1999 Ack Receipt of 981112 & s Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-289/98-06 .Action Does Not Change NRC Determination That Change to Hpis Valve Configuration Involved URI ML20204E3911999-03-17017 March 1999 Informs That Region I Plans to Conduct Open Predecisional Enforcement Conference to Discuss Apparent Violations Re Efs Issues as Described in Insp Rept 50-289/98-09,per ML20204B6771999-03-15015 March 1999 Submits Withdrawal of Amend Request for Operating License DPR-46.Proposed Change Would Have Modified Facility TSs Pertaining to Neutron Monitoring Neutron Detectors ML20207H7391999-03-0505 March 1999 Forwards Insp Rept 50-289/98-09 on 981227-990130.Two Apparent Violations Being Considered for Enforcement Action.First Violation Deals with Failure to Follow Procedures for Control of Emergency Boration Source ML20203F4911999-02-0505 February 1999 Forwards Request for Addl Info Re Licensee 981125 Amend Application Re TS Change Request 277 for OTSG Inservice Insp During 13R for Three Mile Island,Unit 1 ML20202H6771999-02-0303 February 1999 Documents Basis for NRC Staff Generic Approval of Requests to Relocate TS Requirements from Tss.Staff Generic SER Finding Relative to Relocated TS Requirements Encl ML20196K3511999-01-22022 January 1999 Refers to Gpu Responses to Second NRC RAI Re GL 92-08 & Review of Gpu Analytical Approach for Ampacity Derating Determinations.Forwards SE & SNL Technical Ltr Rept Concluding That No Outstanding Safety Concerns Identified ML20199H6471999-01-20020 January 1999 Forwards RAI Re Gpu TS Change Request 277 OTSG Cycle 13 for Plant Unit 1.NRC Has Determined That Addl Info Needed to Complete Review ML20199G7401999-01-12012 January 1999 Forwards Insp Rept 50-289/98-08 on 981101-1226.No Violations Noted.Operator Workaround Program Found to Be Acceptable ML20206S0221999-01-0808 January 1999 Responds to Re Changes to Physical Security Plan Identified as Rev 38,submitted Under Provisions of 10CFR50.54(p).Based on NRC Determination,Changes Do Not Decrease Overall Effectiveness of Security Plan 1999-09-30
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.P &f 2 res g \ UNITED STATES g j - NUCLEAR REGULATORY COMMISSION WASHINGTON. D.C. 30006 0001 p\ *****/ March 30, 1998 [pdf7 Mr. James W. Langenbach, Vice President and Director- TMI-1 GPU Nuclear Corporaibn P.O. Box 480 Middletown, PA 17057
SUBJECT:
REVIEW OF PRELIMINARY ACCIDENT SEQUENCE PRECURSOR ANALYSIS OF OPERATIONAL EVENT AT THREE MILE ISLAND NUCLEAR STATION, UNIT NO.1
Dear Mr. Langenbach:
Enclosed for your review and comment is a copy of the preliminary Accident Sequence Precursor (ASP) analysis of an operational event which occurred at the Three Mile Island Nuclear Station, Unit 1, on June 21,1997 (Enclosure 1), and was reported in Licensee Event Report (LER) Nos.
289/97-007, -006, and -010. This analysis was prepared by our contractor at the Oak Ridge National Laboratory. The results of this preliminary analysis indicate that this event is an accident sequence precursor for 1997. In assessing operational events, an effort was made to make the ASP models as realistic as possible regarding the specific features and response of a given plant to various accident sequence initiators. We realize that licensees may have additional systems and emergency procedures, or other features at their plaints that might affect the analysis. Therefore, we are providing you an opportunity to review and comment on the technical adequacy of the preliminary ASP analysis, including the depiction of plant equipment and equipment capabilities. Upon receipt and evaluation of your comments, we will revise the conditional core damage probability calculations where necessary to consider the specific
- information you have provided. The object of the review process is to provide as realistic an analysis of the significance of the event as possible.
In order for us to incorporate your comments, perform any required reanalysis, and prepare the final report of our anaysia of this event in a timely manner, you are requested to complete your review and to provlje any comments within 30 days of receipt of this letter. We have streamlined the ASP Program with the objective of significantly improving the time after an event in which the final precursor analysis of the event is made publicly available. As soon as our final analysis of the event has been completed, we will provide to you the final precursor analysis of the event and the resolution of your comments.
We have also enclosed severalitems to facilitate your review. Enclosure 2 contains specific guidance for performing the requested review. It also identifies the criteria that we will apply to determine whether any credit should be given in the analysis for the use of licensee-identified additional equipment or specific actions in recovering from the event, and describes the specific information that you should provide to support such a claim. Enclosure 3 consists of copies of LER Nos. 289/97-007, -008, and -010, which documented the event.
h 9904010147 980330 PDR ADOCK 05000289 S PDR NRC m.E CEMIS C
7 i
.o J.' Langenbach Please contact me at (?O1) 415-1402 if you have any questione regardmg this request. This j request is covered by the existing OMB clearance number (31660-0104) for NRC staff follow up i review of events documented in LERs. Your response to this request is voluntary and does not constitute a licensing requirement.
Sincerely, Original signed by T: mothy G. Colbum, Senior Project Manager Project Directorate 1-3 Division of Reactor Projects - t/11 Office of Nuclear Reactor Regulation Docket No. 50-289
Enclosures:
- 1. ASP Analysis of Operational Event
- 2. Specific Guidance Requested Review
- 3. Licensee Eveni Reports .
cc w/encis' See next psge DISTRIBUTION g Docket File +
PUBLIC PDI-3 r/f J Zwolinski TColbum TClark OGC ACRS C. Hehl, RI DOCUMENT NAME: G:\COLBURN\TMl197ST.WPD
. To receive a copy of this document, indicate in the box: "C" = Copy without attachment / enclosure "E" = Copy with ctt chment/ enclosure "N"= No' copy OFFICE PDl-3/PM l PDI-3/LA2 , j ()- l6 PD}3/D J' '
I NAME TColbum P TClark(MO N ,
DATE 03/ 2 /98 03/JG /98" W3ffo/98 OFFICIAL RECORD COPY
Z 9
J.Langenbarh Three Mile Island Nuclear Station, Unit No.1 cc:
Michael Ross Robert B. Borsum Director, O&M, TMI B&W Nuclear Technologies GPU Nuclear Corporation Suite 525 '
P.O. Box 480 1700 Rockville Pike Middletown, PA 17057 Rockville, MD 20852 John C. Fomicola William Domsife, Acting Director -
Director, Planning and Bureau of Radiation Protection Regulatory Affairs Pennsylvania Department of GPU Nuclear Corporation Environmental Resources 100 Interpace Parkway P.O. Box 2063 Parsippany, NJ 07054 Harrisburg, PA 17120 Jack S. Wetmore Dr. Judith Johnsrud Manager, TMl Regulatory Affairs National Energy Committee GPU Nuclear Corporation Sierra Club P.O. Box 480 433 Orlando Avenue Middletown, PA 17057 State College, PA 16803 Emest L. Blake, Jr., Esquire Peter W. Eselgroth, Region i Shaw, Pittman, Potts & Trowbridge U.S. Nuclear Regulatory Commission 2300 N Street, NW. 475 Allendale Road Washington, DC 20037 King of Prussia, PA 19406 Chairman Board of County Commissioners of Dauphin County Dauphin County Courthouse Harrisburg, PA 17120 Chairman Board of Supervisors of LondonderryTownship R.D. f1, Geyers Church Road Middletown, PA 17057 Wayne L Schmidt Senior Resident inspector (TMI-1)
U.S. Nuclear Regulatory Commission P.O. Box 311 Middistown, PA 17057 Regional Administrator Region i U.S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406
~T 8
LER Nos. 289/97-007,-008 -010 LER Nos. 289/97-007,-008,-010 Event
Description:
Failure of both generator output breakers capws a LOOP Date of Event: June 21,1997 Plant: Three Mile Island, Unit 1 Event Siammary 1hree Mile Island, Unit 1 (TMI 1) was at 100% power when the plant experienced a loss of offsite power (LOOP) aAer both generator output breakers in the 230-kV substatior failed.' The LOOP resulted in an immediate trip of both the reactor and the turbine; plant computer data indicated that the trip insertion times .
were excessive for four control inds.2 Both emergency diesel generators (EDGs) started and loaded as I designed. Offsite power was restored within 90 min. 'Ihe unit was cooled by natural circulation cooling until
~offsite power was restored. It was subsequently discovered that the pressurizer power-operated relief valve g (PORV) was failed closed during this event (see Additional Event-Related Information section).Ihe aded conditional core damage probability (CCDP) for this plant-centered LOOP is 9.6 x 104 Event Description .
TMI 1 was at 100% power aAer almost 617 days of continuous operation. On June 21,1997, the B phase of the 230-kV power transformer developed a fault causing severe overheating and the subsequent ejection of the bushing and conductor from the breaker housing of output breaker GBI-02 (Fig.1). This resulted in a fault being detected on 230-kV bus 4. The parallel generator breaker, GBI 12, opened because of the detected fault on 230-kV bus 4. Breaker GBI-12 subsequently suffered a re-stnke, which damaged the B phase of this breaker, causing a fault on 230-kV bus 8. Automatic breaker action because of both faults isolated electric power to the station resulting in a LOOP.'
1he LOOP caused an immediate reactor trip and turbine trip. The plant computer captured times associated with each control rod reachmg the 25% zone reference as the reactor trip occurred. A review of the data ;
showed that four control rods exceeded the trip insertion time limit of 1.66 s for % msertion. Personnel attributed the slow insertion times to reduced clearances in the old style control rod drive thermal barriers because of the presence of deposits on the internal check valves, between the thermal barrier bushmg, and on the leadscinw. All L. ntrol rods inserted to the % insertion position within 2.2 s. The licensee determmed that there would be no aJ erse effects associated with control rod insertion times as high as 3.0 s (Ref. 2).
Both EDGs started and loaded onto their respective safeguards bus as designed. Nonvital loads, including circulating water and main condenser vacuum pumps, were not energtzed The reactor coolant pumps were also without power. Natural circulation was verified in the reactor coolant system within 19 min followmg the trip and LOOP. Decay heat removal was estat,lished using the emergency foodwater (EFW) system and the steam generator atmospheric dump valves. Offsite power was restored within 90 min aAer the breaker failures.
1 Enclosure 1
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, *l LER Nos. 289/97-007 -008. -010 AAer operators established the main %= heat sink, the reactor coolant pumps were restarted, returning i the reactor coolant system to forced circulation cooling.'
Additional Event-Related Information TMI 1 has a single PORV installed on the pressurizer that is replaced with a spare PORV during each refueling outage. The licensee discovered that during the previous refueling outage, the PORV was wired incorrectly and was subsequently inoperable for the entire operatmg cycle. 'Ihe PORV was failed in the closed position and would not have opened in response to an automatic (2,450 psig) or a manual signal.' The operating cycle -
completed with a failed PORV encompassed the LOOP event described by Refs. I and 2.
Besides the PORV, there are two safety relief valves connected to the pressurizer with a nommal relief setpoint of 2,500 psig. The shutoff head of the safety injection pumps is ~2,900 psig. Feed-and-bleed operation is possible with an inoperable PORV because the safety relief valves can be lifted with the head established by operstmg the safety injection pumps.'
TMI 1 has two dedicated EDGs (1 A and IB) to supply electric power to engineered safeguards buses ID and IE, respectively, in the event of a LOOP. Additionally, one EDG from TM12 is available as an alternate ac power source during a station blackout (SBO). The alternate EDG, which is manually started from the control room, can be aligned to either engineered safeguards bus 1D or iE within 10 min following an S BO. Operators must close two breakers and any desired loads must be manually loaded onto the bus selected to be re-energized.d Modeling Assumptions This combination of events was modeled as a plant centered LOOP. The probability of not recovering offsite power in the short term is included in the initiating event probability (IE-LOOP). Consequently, this term was set to the probability for a plant-centered LOOP assummg operators fail to recover offsite power in the short term (5.0 x 10-').
The probability of short-tenn and long-term offsite power recovery for a plant centered LOOP and the probability of an RCP seal loss-of-coolant accident (LOCA) following a postulated station blackout were developed based on data distributions contamed in NUREG-1032, Evaluation ofStation Blackout Accidents at Nuclear Power Plants.5 The RCP seal LOCA models were developed as part of the NUREG-1150 probabilistic risk assessment (PRA) effo:ts. Both models are described in RevisedLOOPRecoveryandPWR SealLOCA Models.' The probabilities for the followmg basic events are based on these models:
- 1. Initiatmg event-LOOP (IE-LOOP),
- 2. operator fails to recover offsite power within 2 h (OEP-XHE-NOREC-2H),
- 3. operator fails t-) recover offsite power within 6 h (OEP-XHE-NOREC-6H), i
- 4. operator fails to recover offsite power before battery depletion (OPE-XHE-NOREC-BD),
- 5. operator fails to recover offsite power before RCP seals fail (OPE-XHE-NOREC-SL), and '
i
.6. RCP seals fail without cooling and injection water (RCS -MDP-LK-SEALS).
1 l
l 1
'. t LER Nos. 289/97-007,-008.-010 he PRA for TMI I indicates that an SBO with a concurrent failure of EFW would lead to core damage in approximately 2 h (Ref. 7, Table B.1-11, page B.1-25). His indicates that substantial time is available for the recovery of electric power. Potential recovery actions were modeled by the #dition of a basic event (basic ever.t OEP-XHE-NOREC-SB) under the OP-SBO top event (OP-2H) on the Ih0P event tree (Fig. 2). Top event OP-SBO is substituted for the OP-2H top event whenever emergency power (EP) and EFW are failed.
The alternate EDG (from TMI 2) was added to the Integrated Reliability and Risk Analysis System (IRRAS) model for TMI 1. He probability that the alternate EDG faib to start and run (basic event EPS-DGN-FC-AAC) was set to the same value as the dedicated EDGs (4.2 x 104 ). In addition, because ,
operators must start and load the alternate EDG manually, a basic event was added to reflect the probability that the operator fails to start and load the alternate EDG (basic event EPS-XHE-XM-AAC). Basic event EPS-XHE-XM-AAC was set at 1.0 x 104 in accordance with sim4r human error probabilities already incorporated in the IRRAS model for TMI. De common-cause failure probability of the emergency power system for the base case was based on two EDGs. This was adjusted based on the availability of three EDGs and was developed based on data distributions contained in INEL-94-0064, Common-Cause Failure Data Collection and Analysis System (Ref. 8, Table 5-8: alpha factor distribution summary - fail to start, CCCG = 3, a33 = 0.0224; and Table 5-11: alpha factor distribution summary - fail to run, CCCG = 3, ag = 0.0232). Because a3 si equivalent to the p factor of the multiple Greek letter method used in the IRRAS models, the common-cause failure probability of the EDGs (basic event EPS-DGN-CF-ALL) wm adjusted from 1.6 x 10-8 based on two EDGs to 9.5 x 10" based on three EDGs.
De slow insertion of four reactor control rods was not considered in the model. De control rods inserted well within the time (3.0 s) that the licensee calculated to be limiting. Additionally, all but four control rods met the % insertion time prescribed by the Technical Specifications.
Because the PORV was inadvenently disabled during the operating cycle that encompassed the LOOP event, the probability that the PORV fails to open on demand (basic event PPR-SRV-CC-PORV) wm set to "TRUE" (i.e., will not open).' Two additional basic events were added to the IRRAS model to account for the availability of the safety reliefvalves to relieve any pressure buildup (basic events PPR-SRV-CC-1 A and PPR-SRV-CC-1B). De probability that a safety relief valve would fail to open when its setpoint was reached was set to the nommal failure rate for the PORV (see Table 1). Additionally, the operator would only need to verify the high pressure injection (HPI) pumps started in a situation that required feed-and-bleed cooling to remove decay heat; no other action regarding the PORV or the safety relief valves is required from the operators.
Therefore, the probability that the operator fails to initiate feed and-bleed cooling (basic event HPI-XHE-XM-4 HPICL) was reduced from 1.0 x 10 to 1.0 x 103 Analysis Results The CCDP for this event is 9.6 x 104. He dominant core damage sequence for this event (sequence 26 on Fig.
- 2) involves e a LOOP,
. a successful reactor trip, 3
l 1
1
c: ,
- ;t LER Nos. 289/97-007.-008.-010
. a failure of emergency power,
. . a successful initiation of emerBency feedwater,
+ no challenge to the PORV (failed) or pressurizer safety relief valves, a failure of the reactor coolant pump seals, and
- a failure to restore electric power before core damage.
This SBO sequence (sequence 26 on Fig. 2) accounts for 85% of the total contribution to the CCDP. The next most dominant sequence (sequence 41 on Fig. 2) contributes 11% to the total CCDP. This sequence involves an SBO, a failure of the EFW system, and a failure to recover any form of electrical power before the onset of core damage.
1 All of the most significant sequences involve an SBO. The nominal probability that a PORV is challenged duiing a LOOP or an SBO is 0.16 and 0.37, respectively, based on actual LOOP and SBO events. However, the PORV failure duninished those sequences where the PORV could potentially have lifted and then failed to rescat. Basic events PPR-SRV-CO-L and PPR-SRV-CO-SRO (defmed in Table 1) were set to 5.0 x 10-8and ,
5.4 x 10-', respectively (i.e., the PORV will not open, but the safety valves are challenged) based on Integrated l Plant Exammation (IPE) data. Because the safety relief valves have a higher set point than the PORV, they l may or may not have lifted in place of the PORV. However, the safety valves were assumed to lift during feed-and-bleed operation.
Defmitions anil probabilities for selected basic events are shown in Table 1. The conditional probabilities associated wid the highest probability sequences are shown m Table 2. Table 3 lists the sequence logic associated with the sequences listed in Table 2. Table 4 describes the system names associated with the dommant sequences. Minimal cut sets associated with the <tamiamat sequences are shown in Table 5.
Acronyms CCDP conditional core damage probability CDP core damage probability EDG emergency dieselgenerator EFW emergency feedwater system i HPI high-pressure injection IPE integrated plant exammation IRRAS Integrated Reliability and Risk Analysis System LOOP loss ofoffsite power MOV motor operated valve PORV power operated reliefvalve I PRA probabilistic risk assessment RCP reactor coolant pump .
SBO I staten blackout SGTR_ steam generator tube rupture SLOCA smallloss of-coolant accident TRANS transient event 4
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LER Nos. 289/97-007,-008,-010 i
References 1 LER 289/97-007, Rev. O," Generator Output Breaker Failure Resulting in a loss of Off-Site Power and Reactor Trip," July 21,1997.
1
- 2. LER 289/97-008, Rev. O, " Control Rod Trip Insertion Tunes Exceed TS Section 4.7.1.1 Limits," July 21, 1997.
l
- 3. LER 289/97-010, Rev. O, " Pilot Operated Relief Valve (PORV) Inoperability Due to Being Mis-Wired {
and Failure to Perform Post-Maintenance Test (PMT) Following Replacement During 11R Refueling Outage," November 12,1997.
- 4. Three Mile Island, FinalSafety Analysis Report (Updated Version).
- 5. Evaluation of&ation Blackout Accidents at Nuclear Power Plants, NUREG-1032.
- 6. RevisedLOOP RecoveryandPWR SealLOCA Models, ORNIJNRCILTR-89111, August 1989.
7, Three Mile Island Unit 1, Probabilistic Risk Assessment (Level 1), Dec~nber 1992.
- 8. Marshall and Rasmuson, Common-Cause Failure Data Collection andAnalysis System, INEL-94/0064, December 1995.
5
g LER Nos. 289/97-007,-008,-010
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- 4 230 kV bus _ 1B oux
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