ML20216E762

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Insp Rept 50-382/97-25 on 971201-980205.Violations Noted. Major Areas Inspected:Maint & Engineering
ML20216E762
Person / Time
Site: Waterford Entergy icon.png
Issue date: 03/12/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20216E728 List:
References
50-382-97-25, NUDOCS 9803180143
Download: ML20216E762 (59)


See also: IR 05000382/1997025

Text

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ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGIOiiIV

Docket No.: 50-382

License No.: NPF-38

Report No.: 50-382/97-25

Licensee: Entergy Operations, Inc.

Facility: Waterford Steam Electric Station, Unit 3

Location: Hwy.18

Killona, Louisiana

Dates: December 1,1997, through February 5,1998

Team Leader. L. Smith, Senior Reactor Inspector, Engineering Branch

Inspectors: C. Patel, Project Manager, PDIV-1

M. Runyan, Senior Reactor inspector, Engineering Branch

P. Goldberg, Reactor Inspector, Engineering Branch

D. Pereria, Reactor Inspector, Engineering Branch

R. Bywater, Reactor inspector, Engineering Branch

,- Contractors: D. Tondi

H. Anderson

Approved By: Thomas F. Stetka, Acting Chief, Engineering Branch

Division of Reactor Safety

ATTACHMENT: Supplemental Information

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9803180143 980319

PDR

G ADOCK 05000582

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TABLE OF CONTENTS

EXECUTIVE SUMMARY . . ... . .... ... . ... . .. .... .. . . . . iii

11. Maintenance . .. . . .. . . . . . ..... . .. . .. . .1

M2 Maintenance and Material Condition of Facilities and Equipment .. . . 1

M2.1 Control of Grounds on the Direct Current Distribution System . . 1

Ill. Engineering . . . ... . . . ... .. . ... .. . .. .. . .. 2

E1 Conduct of Engineering . . . . ... ... .. ... .. .2

E1.1 Safety injection System Design Basis Calculations . . .. ... .. 2

E1.2 Air-Operated and Hydraulic-Operated Valve Calculations . . . . . . . .6

E1.3 Hydrogen Generation Calculations . . . . . . ... ... . .. . . 11

E1.4 Low DC Voltage to Emergency Feedwater Pump Turbine Steam

Admission Valves . . . .... . .. ...... . ... . . 12

E2 Engineering Support of Facilities and Equipment . . . ... . . . . . 14

E2.1 Implementation of Emergency Core Cooling System Surveillance

Requirements . . . . .. . .. . . .. . 14

E2.2 High Pressure Safety injection Flow Control Valve Replacements 15

E2.3 10 CFR 50.59 Implementation . . . . .. . .. , 23

E3 Engineering Procedures and Documentation ... . .... ... . 30

E3.1 Engineering Request Process . . .. . 30

E3.2 Design Bases Documentation - 125V DC Distribution System. . . . 31

E3.3 Seismic Qualification Documentation - 125V DC Station Batteries . . 31

E3.4 Environmental Qualification of the Static Uninterruptible Power Supply

(SUPS) . . .. .. . . .. . .. .... .32

E4 Engineering Staff Knowledge and Performance . . . . .. 33

E4.1 Interview of Staff Personnel . . . . . .. , 33

E6 Engineering Organization and Administration . . . . ... 34

E6.1 Engineering Backlegs . . .. .. . . 34

E7 Quality Assurance in Engineering Activities .. ...... . 35

E7.1 Condition Report Review .. . ... . 35

E8 Miscellaneous Engineering issues . .. . .. . . . 37

E8.1 (Closed) Inspection Followup Item 50-382/96202-01. . .. .. 37

E8.2 (Open) Inspection Followup item 50-382/9708-01 .... ... 39

E8.3 (Closed) Licensee Event Report 50-382/97-007. . .. . 39

E8.4 (Closed) Licensee Event Report 50-382/97-015. . . 39

E8.5 (Closed) Violation 50-382/9714-01 . . .. ... . . . 39

V. Management Meetings . . . .. . .40

X1 Exit Meeting Summary . . . .40

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EXECUTIVE SUMMARY

Waterford Steam Electric Station, Unit 3

NRC Inspection Report 50-382/97-25

During the weeks of December 1 and December 14,1997, six NRC personnel and two

consultants conducted an engineering team inspection. Additionalinoffice inspection was

conducted through February 5,1998. A safety system engineering inspection was performed for

the high pressure safety injection system (HPSI). In addition, the team reviewed the design

basis for the 125V electrical distribution system and for safety-related hydraulic and air-operated

valves. The team also reviewed the status of various upgrade programs, which were planned or

in progress.

Although some unresolved issues existed at the conclusion of the inspection, the team did not

identify any inoperable equipment or systems. The team did identify six apparent violations that

focused on two major subject areas: the capability of the HPSI system to provide adequate

emergency core cooling and the licensee's interpretation and implementation of 10 CFR 50.59.

The HPSI issue was of concern because the facility was operated from July 28 through

December 17,1997, in a condition that would have been prohibited, as determined by the

licensed emergency core cooling system analysis. This issue also involved several related

concerns about prioritization of corrective action activities, the effectiveness >f some corrective

actions, and test control. The 10 CFR 50.59 issue was of concern because the licensee had

apparently failed to perform a written safety evaluation in two instances and had apparently

authorized three changes to the facility, which involved unreviewed safety questions, prior to

obtaining NRC approval. In addition, one other violation was cited that involved the licensee's

failure to appropriately assess the implications of industry information and take appropriate

corrective action. The licensee did not identify the need to reanalyze the capability of Anchor-

Darling air- and hydraulic-operated gate valves when they realized that the assumed valve

factors were not conservative.

Strong points were also identified during the inspection. The licensee had previously identified

many of the issues, which were discovered by the team during the course of the inspection. The

discovery phase of the licensee's design basis review and calculation upgrade program was

effective for the safety injection system. Despite recent turnover, in general, the team found

licensee personnel to be knowledgeable of their equipment and systems. Material condition, as

it related to the operation of the 125Vdc system, was good.

higintenanc_e

- The licensee effectively resolved long-term problems with electrical grounds by modifying

junction box seals to prevent water intrusion. In addition, the licensee promptly corrected

electrical grounds as they occurred, resulting in good material condition (Section M2.1).

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Enaineerina

The discovery phase of the licensee's design basis review and calculation upgrade

program was effective for the safety injection system. The licensee had previously

identified issues that were independently identified by the team (Section E1.1).

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The licensee took appropriate actions to establish and improve calculations for

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air-operated valves, but did not include safety-related hydraulic-operated valves in the

scope of the calculation upgrade program (Section E1.2).

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The licensee's evaluation of the applicability of NRC Information Notice 96-48,

" Motor-Operated Valve Performance issues," was inadequate. The licensee did

not promptly initiate a condition report when they identified that main feedwater

isolation valve performance did not conform with the initial sizing calculation

assumptions for the valve. The failure to initiate a condition report was identified as

a violation of 10 CFR Part 50, Appendix B, Criterion V, " Instructions, Procedures and

Drawings" (Section E1.2).

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While the emergency feedwater pump turbine steam admission valves received low

direct current voltage, the team agreed with the licensee that the valves were operable

(Section E1.4).

The team concluded that the emergency core cooling system surveillance procedures

were scheduled and implemented in accordance with the technical specification

requirements. The team noted that the schedules were in accordance with the

surveillance frequency requirements and that the acceptance limits of the technical

specification surveillance requirements were included in their respective surveillance

procedures. However, the team noted that uncertainties were not always being factored

into surveillance requirements (Sections E2.1, E2.2, and E8.1).

- One apparent violation of 10 CFR Part 50, Appendix B, Criterion XI, " Test Control," was

identified for the HPSI flow balance test related to the specification of test instrumentation

and the inclusion of valve position variability in the test acceptance limits. An additional

example was identified for the auxiliary component cooling water flow balance test

related to the inclusion of measurement uncertainty in the test acceptance limits

(Sections E2.2 and E8.1).

- Two apparent violations of 10 CFR 50.46, " Acceptance Criteria for Emergency Core

Cooling Systems for Light Water Nuclear Power Reactors," were identified. The first

involved the failure to assess the impact of the lower HPSI flow on peak fuel clad -

temperature. The second involved the failure to report operation outside the design

basis of the facility and the subsequent failure to submit the schedule for revising the

emergency core cooling system analysis within 30 days (Section E2.2).

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One apparent violation of 10 CFR Part 50, Appendix B, Criterion XVI, " Corrective Action,"

'was identified related to a failure to promptly correct the HPSI flow balance test

acceptance limit deficiency, following ident!fication of the issue in a self assessment

(Section E2.2).

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Two apparent violations of 10 CFR 50.59, " Changes, Tests, and Experiments," were I

identified. The first involved an apparent failure to perform a written safety evaluation. ;

The second involved approving three changes to the facility, which apparently involved  ;

unreviewed safety questions, prior to obtaining NRC approval (Section E2.3).

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The team found that the licensee had not completed the transition to the new  ;

engineering request process. The licensee satisfactorily resolved concerns identified by j

the team related to a review of 25 engineering requests (Section E3.1). j

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The current seismic qualification of the Waterford 3 safety-related station batteries was

acceptable. Seismic qualification from 15- to 20-years qualified life was not clearly ,

established. The licensee initiated an engineering request to further evaluate the {

qualification of the batteries during this period (Section E3.3). i

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The team noted an increasing backlog for the portions of the engineering request

process that had been implemented However, the licensee had good control of the j

condition report backlog. Since May 1997, the condition report backlog has decreased I

(Section E6.1). l

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Reoort Details

insoection Obiectives

This inspection was performed to implement the core inspection program requirements, using

the Safety System Engineering inspection Procedure to review the high pressure safety

injection (HPSI) system. This system was selected because NRC had not recently reviewed the

system and because the licensee had conducted self-assessments on the system. In addition,

the team reviewed the design basis for the 125V electrical distribution system and for safety-

related hydraulic and air-operated valves. These support systems were selected because of

their risk significance. The inspection also included an evaluation of the licensee's control of

changes to the facility pursuant to 10 CFR 50.59, " Changes, Tests and Experiments." The team

also reviewed the status of various upgrade programs, which were planned or in progress.

This inspection also included regional ;nitiative inspection focused on naluating the licensee's

plans for upgrading the design and license bases for the facility. Prior to the inspection the

NRC performed an internal review of the licensee's response, dated February 6,1997, to the

NRC's 10 CFR 50.54(f) letter of October 9,1996. The NRC 50.54(f) letter requested currently

licensed nuclear generating facilities to submit specific information pertaining to their programs

and processes for ensuring operation in accordance with design, the availability and adequacy

of design basis information, and the effectiveness of such programs or processes for

maintaining operation within design. The licensee's response was reviewed by both regional

and program office personnel. The results of this review were presented to and discussed with

regional management, inspection specialists, and program office representatives who were

knowledgeable of the facility's regulatory performance and history as it relates to the availability

and use of design basis information. The followup recommended by this review was performed

during this inspection, as documented in Sections E1.1, E1.2, E1.3, E2.2, E2.3, E3.2, E3.3,

E3.4, E7.1, and E8.1.

II. Maintenance

M2 Maintenance and Material Condition of Facilities and Equipment

M2.1 Control of Grounds on the Direct Current Distribution System

a. Insoection Scoce ( 93809)

The team conducted a walkdown of the battery rooms, the battery chargers, the direct

current distribution panels, and the 120Vac inverters. The team also reviewed Condition

Report 96-0516, " Recurring Electrical Grounds During Heavy Rainfalls."

b. Observations and Findinos

During the walkdown, the team noted that the direct current electrical system was

operating free of any grounded circuits. The licensee stated that ground alarms were

given immediate attention. The licensee provided Condition Report 96-0516, which

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described corrective actions taken by the licensee to minimize the number of grounds.

The licensee had determined that most electrical ground-related failures occurred after

heavy rains. To address this issue, the licensee implemented a corrective action

program to replace junction box gaskets. The licensee stated that this program had

significantly reduced the number of grounding problems. The team considered the

operational philosophy of operating free of electrical grounds to be an example of

maintaining good material condition of the electrical system.

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c. Conclusions _

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The licensee effectively resolved long-term problems with electrical grounds by modifying i

junction box seals to prevent water intrusion. In addition, on a continuing basis, the

licensee promptly corrected electrical grounds as they occurred, resulting in good  ;

material condition.

Ill. Enaineerina  ;

E1 Conduct of Engineering

E1.1 Safety Iniection System Desian Basis Calculations l

a. Insoection Scoce (37550. 93809)

The team reviewed six design basis calculations related to the safety injection system.

The team assessed technical adequacy, consistency with license basis commitments,

and administrative completeness. In addition, the team evaluated the design upgrade

project as it related to the upgrade of these calculations.

b. Observations and Findinos

Design Bases Upgrade

The licensee was conducting a design basis review and calculation upgrade program,

which included review of the safety injection system. Phare 1, " Discovery," involved

identification of design basis open items for conflicting or incorrect design basis

information. The licensee had completed the discovery phase for the high and low

pressure portions of the safety injection system. Phase 2," Corrective Action," involved

completion of the necessary design document revisions to develop a comprehensive

consistent design basis for the system. The licensee planned to complete Phase 2,

" Corrective Action," for these systems in 1998.

During the discovery phase, Phase 1, a senior engineering review team:

1. Determined if the specific calculation fully supports the design basis

2. Identified open items (inadequacies, errors, inconsistencies, etc.)

3. Recommended disposition of open items

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The licensee tracked open items in the program's internal open item tracking system.

The team questioned the basis for input assumptions and consistency of calculation

assumptions with the license basis. The team reviewed the licensee's entries in the

open item tracking system related to the safety injection system and found that the

licensee previously had identified the same unjustified input assumptions and license

basis inconsistencies in the design basis review / calculation upgrade program and in

Condition Report 97-806. The examples include: 1) hput assumptions for the

containment water level calculation; 2) input assumptions for the HPSI and containment

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spray net-positive; suction head calculation; and 3) the failure to include the flow control j

valve pressure drop in the HPSI flow path pressure drop calculation. The team i

determined that the licensee's discovery phase was effective and that the first two issues

required further.eview. For the third issue, the team reviewed a draft calculation and

determined that no further review was needed because the change in pressure drop was i

small and the licensee had acceptable plans to correct the deficiency.

Net-Positive Suction Head Margins Not Accurately Stated

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The licensee identified that pump run out flows were not consistently defined in various

calculations resulting in conflicting net-positive suction head (NPSH) determinations.

The licensee also identified that the safety injection sump level design calculations did

not have consistent conclusions regarding the minimum sump water level during  :

recirco'ation, which affects the available NPSH. In addition, calculation results were not

alw.sys consistent with the Updated Final Safety Analysis Report. For example,

Calculation MN(Q)-6-27, "NPSH Calculation (HPSI & CS (containment spray] Pumps),"

Revision 2 and Updated Final Safety Analysis Report (UFSAR), Section 6.3.2.2.2.3, j

specified different values for required NPSH for these pumps. Specifically:

Calculation MN(Q)-6-27 UFSAR

Revision 2 Section 6.3.2.2.2.3

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HPSI Required 20 feet 18 feet

NPSH (which matches NPSH (which matches the

available at 985 gpm per pump data sheet -

pump curve - near required for runout flow)  :

runout)

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HPSINPSH 25.35 feet 25.35 feet

Available

HPSI NPSH Margin 26.75% 40.8%

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Calculation MN(Q)-6-27 UFSAR

Revision 2 Section 6.3.2.2.2.3

CS Required NPSH 18 feet 14 feet

(which matches NPSH (which matches the

available at 2250 gpm pump data sheet-

per pump curve - near required for runout flow) i

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runout)

CS NPSH Available 27.27 feet 25.35 feet

CS NPSH Margin 51.5 % 94.8 %

As a result, the pump design margins stated in the Updated Final Safety Analysis

Report were not achievable at actual pump runout. The licensee planned to correct

Calculation MN(Q)-6-27, "NPSH Calculation for HPSI and CS ? umps," Revision 2, and

delete the margin requirements from the UFSAR. While the committed margins were not

maintained, the existing ca!culations demonstrated sufficient NPSH was available to

maintain system operability.

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In a related effort, the licensee identified inconsistencies in containment water level '

predictions and the associated inputs to NPSH calculations. The licensee planned to

revise Calculation MN(Q)-6-4, " Water Level inside Containment," Revision 0, to

comprehensively determine water level in containment for both the loss-of-coolant

accident and a main steam line break. Minimum containment water level was used to ,

determine available NPSH, during the recirculation mode. The NRC plans additional i

review of the completed HPSI calculations to determine the significance of the  !

inconsistencies and to confirm adequate resolution of the inconsistencies. Additionally, !

the NRC will review the final UFSAR revision and the associated written safety

evaluation to determine compliance with 10 CFR 50.59. This issue will be tracked as an l

unresolved item (50-382/9725-01) pending NRC review of completed

Calculations MN(Q)-6-27 and MN(Q)-6-4, and the approved written safety evaluation of

the planned change to the UFSAR.

Impact of increased Containment Flooding

Maximum predicted containment water level was used to identify equipment, which

would be adversely impacted by containment flooding. In Condition Report 97-1287

and Engineering Request ER-W3-97-0263, the licensee identified that its post

loss-of-coolant accident containment flooding analysis resulted in an unacceptable

maximum flood level. When increased instrumentation uncertainties, addition of

trisodium phosphate dodecahydrate baskets in containment, and a refueling water

storage pool (RWSP) volume versus level error were considered, the licensee predicted

partial flooding of the cooling coils for Containment Fan Cooler AH-14B-SB and

submergence of instruments, which were not qualified for submergence. Specifically, the

following instruments would be submerged:

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SG ILT 1115 A&B and Steam Generator Wide Range Level Used in

1125A Emergency Feedwater Flow Control l

RC IPT 0106 A&B Hot Leg Prt;ssure Used in Subcooled Margin

Calculation

St ILT 7145 A&B Safety injection Sump Level

The licensee determined it was necessary to administratively impose a 90 percent upper

limit on maximum RWSP inventory to prevent partial flooding of the containment fan

cooler cooling coils and flooding of the nonqualified instruments.

With respect to the containment fan cooler cov,,ng coils, the licensee evaluated the effect

of coil submergence on peak containment pressure. The licensee concluded that with

20 percent coil submergence, peak containment pressure only increased by 0.15 psig,

which they stated was within the acceptance criterion for post-accident peak containment

pressure. With respect to the instrumentation, the licensee concluded that the sump

level instrumentation would be available as the accident progressed until it was no longer l

necessary and loss of the remaining instrumentation could be compensated by the i

operators by using other backup instruments. The licensee concluded that a technical l

specification amendment was not required and that the RWSP maximum limit could be '

administratively controlled. I

As stated above, the licensee planned to revise Calculation MN(Q)-6-4, " Water Level '

inside Containment," Revision 0, to comprehensively determine water level in

containment for both the loss-of-coolant accident and a main steam line break. The

licensee deferred their past operability and their reportabilitiy determination until after this

calculation is complete.

NRC Regulatory Guide 1.97, " Instrumentation ior Light-Water-Cooled Nuclear Power

Plants to Assass Plant and Environs Conditions During and Following an Accident,"

Revision 2, identified types of variables to be monitored during post-accident conditions.

This equipment must be provided with assurance that it is environmentally qualified as

required by 10 CFR 50.49, " Environmental Qualification of Electric Equipment important

to Safety for Nuclear Power Plants."

This issue is unresolved (50-382/9725-02), pending NRC review of the completed

calculation and past operability determination to determine: 1) past compliance with the

technicsi specification, and 2) past compliance with environmental quclification

requirements for instrumentation that could become submerged following an accident.

The NRC also plans to review the written safety evaluation associated with the updated

calculations to confirm compliance with 10 CFR 50.59.

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c. Conclusions

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The discovery phase of the licensee's design basis' review and calculation upgrade

program was effective for the safety injection system. The licensee had previously

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l E1.2 Air-Ooerated and Hydraulic-Ooerated Valve Calculations

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l a. Insoection Scooe (37550)

In Generic Letter 89-10. " Safety-Related Motor-Operated Valve Testing and

Surveillance," the NRC made recommendations related to the testing, inspection, and

maintenance of motor-operated valves to provide the necessary assurance that they

would function when subjected to the design-basis conditions. The testing performed to

address the recommendations in Generic Letter 89-10 provided information about the

motcr-operated valve actuator performance and about valve performance. The valve

performance information was also applicable when other types of actuators were used,

such as: air-operated or hydraulic-operated actuators. Based on insights gained during

review of Generic Letter 89-10 testing programs, the team reviewed four air and

hydraulic-operated valve sizing calculations and discussed the documents with licensee

engineers.

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b. Observations and Findings

Through review of this material and discussions with licensee engineers, the team j

determined that the calculations adequately demonstrated the operability of the subject l

valves. However, one calculation, Calculation EC-M91-076, contained discrepancies i

that required correction.

Calculation EC-M91-076

The team identified the following four discrepancies within Calcu'at;on EC-M91-076,

"SI-405A(B) Actuator Thrust Calculation," Revision 2, dated September 14,1995:

- A valve factor of 0.5 was assumed, although this was not consistent with motor-

operated valve test results of similar valves (flex-wedge gate valves). After

review of motor-operated valve tests of similar valves, the licensee agreed to

increase the valve factor to 0.6. The team considered the revised valve factor to

be appropriate for this valve.

- The calculation to determine the minimum force necessary to keep the valve

open did not include a term to account for the weight of the valve disc and stem,

which together weighed approximately 250 pounds.

- Unseating thrusts were based on tests performed under static conditions and,

therefore, did not account for extra unwedging loads resulting from dynamic

pressures applied across the valve disc.

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in Section 8.7.2 of the calculation, packing drag forces were applied )

inconsistently because they were included for some stoke analyses, but not for

others.

The licensee agreed to correct these discrepancies and stated that the changes would

not affect the operability status of Valves SI-405A(B). The team agreed with this

assessment.

Use ofisothermal Assumptions

The team identified one general deficiency involving the lack of justification for an

assumption that most airmperated valves exhibit isothermal behavior during operation.

The team observed that numerous applications within the calculations reviewed, the

licensee used a formula of the form P / V = P / V. This formula stated that the pressure

divided by the volume in an earlier state equaled the pressure divided by the volume in

a later state. Using ideal gas laws, this implied that the temperature was constant

from the initial to the final state, which would be nonconservative for some applications of

air-operated valves.  ;

The licensee noted that isothermal conditions were not assumed for valves that had

multiple actuations during an accident scenario. Also, the licensee performed a

calculation to verify isothermal assumptions for a special case involving air leakage

during long-term holding of a valve disk in either an open or closed position against

spring pressure.

The team determined the licensee had not developed a bounding calculation, which

addressed marginal thrust-limited valves, where the nitrogen or air volume expands

during the stoke. The team noted that the expansion would cause a decrease in

temperature and a further drop in pressure t. y'nd that calculated by an isothermal

analysis. The increased pressure drop would result in less thrust being available to

stroke the valve. Eventually, the temperature in the air chamber would equalize to the

ambient, which would cause pressure to be restored to the calculated value. However, if

the valve were tn hang up in mid stroke, it would then have to overcome static friction to

resume the stroke. The static frictional forces would be greater than the sliding frictional

forces assumed in the analysis, and could potentially prevent a resumption of the valve

stroke. However, the team did not identify any valves that fit the postulated

circumstances. The team concluded that the licensee's isothermal assumpon was not

well justified and was a weakness in the licensee's air-operated valve program.

Licensee Program to Upgrade Performance Calculations for Air-Operated and

Hy:fraulic-Operated Valves

The team noted that many air and hydraulic-operated valves did not have calculations

demonstrating the capability of the valves to perform their safety functions. The licensee

previously identified this deficiency, for air-operated valves only, and hired a consultant

to generate new or improve existing calculations for approximately 120 air-operated

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valves. Selection of the valves to be analyzed by the consultant was based on l

outstanding condition reports (problematic valves), probabilistic risk assessment

rankings, and valves with active safety functions. Safety-related air-operated valves not

selected in the original contract were to be included in a second contract following

completion ef the first, and consisted of approximately 45 valves, mostly in ventilation

systems.

The team considered the licensee's selection of valves to be appropriate with one

exception. The scope did not include the plant's six safety-related hydraulic-operated

valves. These valves were:

SI-405M Component Cooling Water to Shutdown Cooling

Heat Exchanger Isolations

FW-184A/B Main Feedwater isolation Valves

MS-124A/B Main Steam isolation Valves

in response to the team' questions concerning the operability of the main feedwater

isolation valves (discussed below) the licensee decided to add the safety-related

hydraulic-operated valves to the scope of the contract. Therefore, new calculations will

be performed for each of these valves.

Valve Factor Estimate for Main Feedwater Isolation Valve (Hydraulic-Operated) i

7 team requested the calculation that demonstrated the capability of the main i

feedwater isolation valves to perform their safety functions. The licensee stated that this

calculation did not exist, but that the valves were sized during initial design in accordance ;

with the manufacturers specifications. The team was concerned that this initial sizing

may have been based on assumed valve factors that have since been proven to be

nonconservative as a result of motor-operated valve testing performed under Generic l

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Letter 89-10.

The main feedwater isolation valves are 20-inch Anchor-Darling double disk gate valves.

Though previously assumed to have 0.2 valve factors, these valves exhibited valve

factors as high as 0.4 during Generic Letter 89-10 tests. The licensee confirmed that the

initial sizing of the main feedwater isolation valves was based on a 0.2 valve factor.

During the inspection, the licensee performed a draft calculation, which determined that

the available valve factor (highest valve factor, which would yield a successful stroke by

calculation) was 0.31.

The licensee periormed a review of test results of Anchor-Darling double disk gate

valves and found valve factors ranging from 0.31 to 0.35. These test results were for

6-inch valves and the licensee stated that motor-operated valve testing had shown that

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valve factors tend to decreme with increasing valve size. The licensee determined that

the main feedwater isola valves were operable pending further analysis based on the

proximity of the availabh ive factor to the test results and based on previous

occurrences where feedwater isolations had occurred and the main feedwater isolation

valves successfully closed.

This matter was discussed with the licensee during a conference call on January 8,

1998, which included the NRC program office. The NRC observed that the 0.31 valve

factor was not conservative with respect to test results from the Electric Power Research  !

institute and testing performed by Commonwealth Edison. These test results would

suggest a more appropriate valve factor of 0.4 or greater. However, the licensee stated I

that the main feedwater isolation valves had automatically closed in response to a

feedwater isolation signal on at least five previous occasions. Each of these closures

was a complete stroke to the closed position. Some of these cycles occurred under

conditions approximating design basis conditions. There were no occurrences known to

the licensee where the main feedwater isolation valves failed to stroke properly. Based

on this historical record, the team agreed with the licensee's conclusion that, for

immediate purposes, the main feedwater isolation valves could be considered operable.

As stated above, the licensee planned to prepare actuator performance sizing

calculations for these valves. The licensee stated this effort would include a review of

design basis information to ensure the bounding design basis conditions were identified.

Based on uncertainties in the valve factor analysis, the fact that the licensee had not fully

defined the design basis conditions of the valves, and the fact that the main feedwater

isolation valves had never performed a closure under full blow down conditions, the team

considered the matter of the main feedwater isolation valve operability to be unresolved.

This issue will be tracked as an unresolved item (50-382/9725-03), pending additional

NRC review of the completed actuator performance sizing calculations and the finalized

design basis conditions.

The licensee stated that its contractor was in the process of preparing a complete

calculation for the main feedwater isolation valves on an expedited basis, with

compleijon in approximately mid-February. Depending on the results of this review,

additional compensatory actions may be necessary to ensure the continued operability of

these valves.

Failure to identify a Condition Adverse to Quality

The team considered the licensee's failure to translate information from the

Generic Letter 89-10 testing to the design of the main feedwater isolation and other

Anchor-Darling gate valves to be a significant oversight. Additional review was

performed to determine whether the licensee should have recognized this condition

adverse to quality.

NRC issued Information Notice 96-48, " Motor-Operated Valve Performance issues," on

August 21,1996. This notice alerted licensees to lessons learned from the Electric

Power Research Institute (EPRI) motor-operated valve test program. This program

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indicated that many of the previous assumptions used in motor-operated valve

calculations were not accurate and that their use resulted in the over prediction of motor-

operated valve capabilities. Within this program, testing of Anchor-Darling gate valves

indicated that a valve factor of approximately 0.4 was applied to these valves, depending

on service conditions. Based on interviews, the team determined that the licensee's j

engineers understood that this valve factor was applicable to any Anchor-Darling gate

valve, regardless of the type of operator, and also understood that the use of the

0.4 valve factor would result in a considerable increase in predicted thrust requirements

above those calculated using the previous industry-wide assumed 0.2 valve factor.

On March 7,1997, the licensee's operatioaal experience engineering evaluation (OEEE)

for Information Notice 96-48 was approvec. Issue 1 of the OEEE stated that the EPRI

program for motor-operated valves provided important information, applicable to gate,

globe and butterfly valves, regardless of type of actuator operating the valve. However,

in the October 29,1997, draft response, the component engineering group relied on the

motor-operated valve closeout report and did not address valves operated by hydraulic

or air operators. The licensee stated the draft was essentially complete except for

agreement on scheduled completion dates.

10 CFR Part 50, Appendix B, Criterion V, requires that activities affecting quality shall be

prescribed by procedures appropriate to the circumstances and shall be accomplished in ,

accordance with these procedures. l

Procedure W2.501, " Corrective Actions," Revision 6, Section 4.1, required that condition

reports be generated when an adverse condition was identified. Section 3.1 of the _

procedure defined an adverse condition as "an event, defect, characteristic, state or l

activity, which prohibits or detracts from the safe, efficient operation of Waterford 3." The

adverse condition was further defined to include nonconforming conditions.

The team determined that a condition report should have been initiated shortly after

March 7,1997, and before October 29,1997, to identify that Anchor-Darling gate valve

performance did not conform with the initial sizing calculation assumptions. The use of

a condition report to resolve this concern would have resulted in a timely operability

determination for this nonconformance and identification of the need for reanalysis.

The discovery of higher than previously assumed valve factors for Anchor-Darling

double-disk gate valves was an adverse condition with respect to the operability of

the main feedwater isolation valves. The licensee's failure to identify the need to

reanalyze the capability of the Anchor-Darling air- and hydraulic-operated gate valves

in light of this information is a violation of 10 CFR Part 50, Appendix B, Criterion V

(50-382/9725-04).

c. Conclusions

Some minor errors, which did not affect operability, were identified with

Calculation EC-M91-076, 'SI-405A(B) Actuator Thrust Calculttion, Revision 2,

dated September 14,1995. The licensee had taken appropriate actions to establish

and improve calculations for air-operated valves, but had not included hydraulic-operated

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valves in the scope of the calculation upgrade program. The licensee's evaluation of the

applicability of NRC Information Notice 96-48, was inadequate because they did not

promptly initiate a condition report when they identified that the Anchor-Darling gate

valve performance did not conform with the initial sizing calculation assumptions. The

failure to initiate a condition report was identified as a violation of 10 CFR Part 50,

Appendix B, Criterion V. The question of the operability of the main feedwater isolation

valves was identified as an unresolved item, although the team agreed with the licensee

that valves could be considered operable pending the results of further evaluation.

E1.3 Hydroaen Generation Calculations

a. Insoection Scooe (37550)

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The team reviewed Calculation HVAC-70, " Hydrogen Generation By Station Batteries,"

Revision 1, and Calculation HVAC-059, " Battery Room Air Flow Required to Limit j

Hydrogen Concentration to 1%," Revison 1, to evaluate the capability of the ventilation

system to adeouately sweep hydrogen from the battery rooms. ,

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b. Observations and Findinos

During the inspection, the team toured the battery rooms and noted in Battery Room A

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that the supply and exhcast duct were located within a few feet of each other. The team '

questioned the capability of the ventilation system to adequately sweep pockets of j

hydrogen from the far end of the battery room and to maintain the hydrogen

concentration in the room below the 1 percent limit.

The team found that Calculation HVAC-70 included a nonconservative assurnption.

Specifically, the calculation was based on nominal room temperature, rather than )

worst-case temperature. The team noted that worst-case room temperature should be I

used because hydrogen generation increases with temperature. The licensee agreed  ;

that the calculation should be corrected.

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In Calculation HVAC-59, the licensee used the hydrogen generation rate, determined in

Calculation HVAC-70, to determine the minimum required air flow to ensure hydrogen

concentration remains at less than 1 percent. The team found that Calculation HVAC-59

included an unverified assumption. Specifically, in the minimum required air flow portion

of the calculation, the licensee assumed a 25 percent mixing efficiency, which had not

been verified as achievable by a quantified test. During the inspection, the licensee

qualitatively assessed the room ventilation via a smoke test. The licensee discharged

small puffs of chemical smoke at the end of the room, which was remote from the

ventilation supply and exhaust duct. The licensee observed the smoke patterns and

concluded that some circulation was occurring at the end of the room, which was remote

from the supply and exhaust doct. The team did not agree that this test substantiated a

25 percent mixing rate.

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However, the results of the minimum required vent!'ation rate calculation were

conservative with respect to the design of the installed equipment. A much smaller-

mixing efficiency and a much larger hydrogen generation rate could have been assumed

with satisfactory results. The team concluded these errors were not signincant.

Calculation HVAC-59 also included a calculation of the minimum time to reach tne

hydrogen limit of 1 percent with the ventilation secured, which was 19 hours2.199074e-4 days <br />0.00528 hours <br />3.141534e-5 weeks <br />7.2295e-6 months <br />. The

licensee provided a design guide, which specified that a 25 percent mixing rate is

normally assumed for explosive contaminates in well vent! lated rooms. The design guide

suggested that, for improperly ventilated areas, a lower mixing rate assumption may be

necessary. The team noted that the doors to the battery rooms are typically closed.

Diffusion and thermal convection would provide the only mechanism for air mixing in this  ;

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case. The team determined that the licensee had not adequately justified the use of a 25 l

percent mixing assumption in the minimum time portion of Calculation HVAC-59. The l

licensee agreed and planned to revise or delete this partion of the calculation.  !

l

Since the licensee no longer had a valid estimate of the time to reach the hydrogen  !

concentration limit, the team discussed related operating instructions with the licerme to f

confirm hydrogen accumulatier, was being acceptab(y controlled. The licensee noted j

that the system operating procedures required that the ventilation system be in service

during battery charging. However, they also stated that the alarm response procedure

for a battery room ventilation failure did not provide direction to the operators to secure

the battery charger to prevent hydrogen accumulation. Given the iack of basis for the j

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time to reach the hydrogen limit, the tearr, considered this to be an alarm response

procedure weakness.

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c. Conclusions

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The team determined that Calculations HVAC-70 and HVAC-59 contained

nonconservative assumptions, which did not effect the conclusion that the battery room

exhaust ventilation system was capable with respect to removal of hydrogen. The team

also found that the licensee's calculation of the mirimum time to reach a 1 percent

concentration of hydrogen was not well justified, resulting in a procedure weakness.  ;

E1.4 Low DC Voltaae to Emeraencv Feedwale.dy.mo Turbine Steam Admission ValyLs 1

a. Insoection Scone (93809)

The team reviewed the voltage conditions available to the plant's only de motor-operated i

valves, MS-401 A(B) - emergency feedwater pump turbine steam admission valves.

b. Observations and Findinas

Valves MS-401 A(B) are normally closed and muct open to initiate steam flow to the I

emergency feedwater pump turbine. The valves were designed to utilize de power to

enable operation in the event that all alternating current sources are lost. The licensee

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had calculated that the minimum voltage available at the motor term.inals was 80Vde,

which was 64 percent of the rated voitage of 125Vdc.

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Tne team identified two concerns related to these voltage conditions:

The licencee used a standard formula for computing the torque capability of the

motor-actuator, using a linear relationship of voltage to output torque. The

actuator manufacturer, Limitorque, has stated that this linear relationship is valid i

only at levels of 70 percent rated voltage or greater. Below 70 percent rated I

voltage,'the voltage-torque relationship could potentially become exponential,

such that the percentage of output torque would decrease faster than the voltage. J

The licensee's use of a linear relationship appeared essentialin its calculation of )

valve operability. In consultation with the NRC program office, the team learned i

that the Idaho National Engineering Laboratory, under contract with the NRC,

was in the process of performing de motor testing. Preliminary results indicated

an exponent of 1.3 (1.0 is linear) should be applied to degraded voltage torque l

output. An exponent greater than 1.0 indicated that torque output would j

decrease at a greater rate than the voltage would decrease from the rated value.

Limitorque, during the most recent motor-operated valve users' group meeting,

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also indicated that additional testing would be performed leading to the issuance l

of new guidance conceming the sizing of de motor-operated valves.

Low voltage levels could prevent pickup of the de contactors and prevent valve

operability even if sut0cient voltage existed to operate the valve.

In response to the first concern, the licensee agreed that Limitorque did not endorse use i

of the linear voltage-to-torque relationship below 70 percent rated voltage. However, the  !

licensee researched testing performed by another licensee, Commonwealth Edison, of

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eight de moto. t The results indicated that the relationship of voltage to output torque

was linear to voltages as low as 10 percant of rated nameplate voltage. At least one of

the motors tested by Commonwealth Edison was the same size and manufacturer as the

motors used in the emergency feedwater steam admission valves. Based on this testing,

the team considered the licensee's use of the Inear equation for their valves to be

appropriate while additional industry testing is ongoing.

In response to the second concern, the licensee teferred to IEEE Standard 323-1974,

" Qualification and Test Summary Report for Class 1E Starter Control Station,"

CC 74-256, Revision 0, prepared by Gould, Inc. This report stated that the pickup

voltage for Size 1 (applicable to the licensee's valves) de contactors was 60 percent of

rated voltage. Based on this document, the licensee considered Valves MS-401A(B)

operabic. The team consulted the NRC program office and concluded that the licensee's

use of the 60 percent threshold for contactor operability was acceptable.

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c. Conclusions

The licensee adequately supported immediate operability of the turbine-driven

emergeacy feedwater steam admission valves with respect to the potential low voltage

condition. la the near future, new information concerning dc motors could affect the l

licensee's analysis. j

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E2 Engineering Support of Facilities and Equipment

E2.1 Imolementation of Emergepcv Core Coolino System Surveillance Recqirements

a. Ingstion Scoce (37550)

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The team reviewed the emergency core cooling systems (ECCS) technical specification

surveillance requirements and the associated surveillance procedures to confirm the

acceptance limits contained in the technical specification surveillance requirements were

included in the associated surveillance procedures and that the surveillances were being

tracked and properly scheduled. In this portion of the inspection, the team did not

evaluate the basis for the technical specification surveillance requirement acceptance

limits,

b. .Q)servations and Findings

The team noted that all the ECCS technical specification surveillances were being {

tracked, scheduled, and implemented during the applicable modes of operation. The

technical specification surveillance frequency requirements were met and, in fact,

surveillances were often conducted more frequently than required.

Except as described in Section E2.2, the team found that acceptance limits from the

technical specifications were correctly included in surveillance procedures. The team I

noted that the surveillance procedures detailed the acceptance, alert, and required action ,

values in their respective attachments. In addition, the team noted that each procedure l

required returning the component back to service and removing any test equipment

installed following the conclusion of the surveillance test.

c. CQDClW.SiO.D

The team concluded that the ECCS surveillance procedures were scheduled and

implemented in accordance with the technical specificat;on requirements. The team

noted that the schedules were in accordance with the surveillance frequency

requirements, and that the acceptance lirr.its of the technical specification surveillance

requirements were included in their respective surveillance procedures. However, in

Sections E2.2 and E8.1 of this report, the team noted that uncertainties were not always

being appropriately factored into surveillance requirements.

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E2.2 Hioh Pressure Safety iniection Flow Control Valve Reo!acements

a. Insoection Scope (37001.37550. 93809)

The team reviewed the documentation for Design Change 3440, "HPSI Flow Control

Valve Replacement," Revision 0, to verify that the design basis of the HPSI system had

been appropriately maintained following the installation of new valves. The team also -

reviewed the post-modification testing results.

b. Observations and Findinas

The licensee replaced the eight HPSI (HPSI) flow control valves during the 1997

refueling outage because of problems with cracks in the valve seats and valve seat

leakage problems. The team found that the valve replacements were essentially like-for-

like replacements. The flow control valves were designed to open to a throttled position

on a safety injection actuation signal. The throttled position was controlled by the limit

switch setting of the valve actuator and was determined during flow balance testing The

flow control valves were required to open sufficiently to provide enough HPSI flow to the

reactor to limit peak clad temperature without opening too far to allow the HPSI pumps to

operate in a run out condition. The team determined these valves were capable of

meeting HPSI design basis requirements. However, the team noted that during post-

modification testing, appropriate flow balancing was not performed.

Post-Modification Testing

The post-modification testing of the new valves included the HPSI flow balance test in

accordance with Technical Specification 4.5.2.h, which required the adjustment of the

actuator limit switches to the correct setting. The testing was completed on May 23-24,

1997, in accordance with Surveillance Procedure OP-903-108, "Si Flow Balance Test,"

Revision 3, Change 1, dated April 10,1994. The acceptance limit of the procedure

stated that the sum of HPSI injection header line flow rates, excluding the highest flow

rate, shall be greater than or equal to 675 gpm. This was consistent with the requirement

of Technical Specification 4.5.2.h. The resulting sum of measured HPSI injection header

line flow rates were 675 gpm (A pump /A headers), 718 gpm (AB pump /A headers),

712 gpm (8 pump /B headers), and 690 gpin (AB pump /B headers).

The new valvec were installed with the open limit switch setting for the valve actuators

set at the same setting as the original valves prior to their removal to serve as a

reasonable starting point for the flow bclance testing. The test results met the ,,

acceptance limit of the procedure; therefore, no limit switch adjustments were made.

The licensee considered the results of the tests acceptable and declared the HPSI

system operable.

The bases section for Technical Specification 3/4.5.2 states that the surveillance

requirements ensure that, at a minimum, the assumptions used in the safety analysis are

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met. The team questioned the acceptability of the test results, particularly for the A train

pump, which just met the minimum acceptance limit. The team questioned whether the ,

surveillance procedure acceptance limit properly included margin for flow measurement

uncertainty and for flow control valve position variability.

After discussions with the team, the licensee identified that not all of the flow instrument

uncertainty had been accounted for. The licensee stated that the 675 gpm acceptance j

criterion from Technical Specification Surveillance Requirement 4.5.2.h included an '

allowance of 5 gpm/ leg, to account for flow instrument measurement uncertainty.

However, Surveillance Procedure OP-903-108 directed personnel to use flow

instruments, which had a flow measurement uncertainty of approximately 18 gpm/ leg.

The licensee initiated Condition Report 97-2695 on December 5,1997, to document this

condition.

10 CFR Part 50, Appendix B, Criterion XI, requires, in part, that test procedures shall

include provisions for assuring that adequate test instrumentation is used. As of

December 18,1997, the licensee had not corrected Surveillance Procedure OP-903-108

to include provisions for assuring that adequate test instrumentation was used. The test

procedure specified instrumentation, which had an uncertainty that was greater than that ,

assumed in the basis for Technical Specification Surveillance Requirement 4.5.2.h. The  ;

failure to specify sufficiently accurate test instrumentation is the first example of an

apparent violation of 10 CFR Part 50, Anpendix B, Criterion XI (50-382/9725-05).

Technical Specification 4.5.2.g required the licensee to verify the correct position of each

electrical and/or mechanical position stop for the ECCS throttle valves each tirne the

valve was cycled. Surveillance Procedure OP-903-010, "ECCS Throttle Valves Position  ;

Verification," Revision 3, implemented this technical specification requirement and I

allowed a +/- 2 percent tolerance band for the as-found flow control valve position from

its set point value. The team questioned what impact this acceptance limit had on HPSI

flow and whether this variability was incorporated into the technical specification flow

rate acceptance limit it appeared that one or more flow control valves could open some

amount less than set point, still be within the 2 percent acceptance limit, and yet cause l

HPSI flow to the reactor to be less than 675 gpm. Likewise, one or more flow control

valves md open some amount greater than set point, still be within the 2 percent

accepta ' e limit, but cause the HPSI pump to operate closer to a run out condition.

The licensee determined that valve position variability had not been included in the

development of Technical Specification Surveillance Requirement 4.5.2.h and that after

consideration of valve position variability, the surveillance requirement would not assure I

that the assumptions used in the safety analysis were met. The team concluded that an j

additional allowance should have been included in the acceptance limit of Surveillance i

Procedure OP-903-108 to account for valve position variability. i

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10 CFR Pait 50, Appendix B, Criterion XI, requires, in part, that all testing required to l

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demonstrate that structures, systems, and components will perform satisfactorily in

service, is performed in accordance with written test procedures that incorporate the

requirements and acceptance limits contained in applicable design documents.

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As of December 18,1997, the licensee had not corrected Surveillance {

Procedure OP-903-108 to incorporate an acceptance limit allowance for valve )

position variability, which was necessary to ensure that the flow assumptions used in I

the safety analysis were met. The failure to include an appropriate acceptance limit in

Surveillance Procedure OP-903-108 is the second example of an apparent violation of ,

10 CFR Part 50, Appendix B, Criterion XI (50-382/9725-05). I

Emergency Core Cooling System Evaluation l

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The original HPSI flow limit calculation performed by the nuclear steam suMy system I

vendor was provided to the !icensee on September 9,1997, as part of a design

basis information transfer project. This calculation used an instrument uncertainty of

5 gpm/ injection leg (8.7 gpm total for combined legs). Calculation EC-195-011,

"SI-HPSI Flow Instrumentation Loop Uncertainty Calculation," Revision 1, determined

that the instrumentation uncertainty was actually approximately 18 gpm/ injection leg

(31.2 gpm total when statistically combined). Therefore, an additional 22.5 gpm of

combined flow measurement uncertainty needed to be considered. As discussed above,

on December 5,1997, after consideration of these instrument uncertainties and other

uncertainties, the licensee determined that the technical specification limit of 675 gpm

did not p,ntect the analytic value of 621.8 gpm in the small-break loss-of-coolant accident ,

(SBLOCA; safety analysis. l

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The licensee's SDLOCA safety analysis assumed a HPSI flow rate of 621.8 gpm and a

charging pump flow rate of 18 gpm. Thc analysis was performed for the licensee by its  ;

nuclear steam supply system vendor using a SBLOCA evaluation mocel previously '

reviewed by the NRC and found acceptable. The resultant peak clad temperature (PCT)

was 1879'F, which was within the 10 CFR 50.46 emergency core cooling acceptance

criterion of 2200*F.

The licensee determined that if the correct instrumentation error was accounted for,

the analytic value for HPSI flow would have to be reduced to 599.3 gpm .(621.8 gpm -

22.5 gpm). Alternatively, a hi 0her technical specification limit of 697.5 gpm (675 gpm

+ 22.5 gpm) could be used to ensure exceeding the analytic value, but this measured

flow rate wac unachievable for all HPSI pump and injection path combinations. In their

December 5,1997, operability determination, the licensee estimated the available flow at

590 gpm to account for valve position variability and other uncertainties, which were not

previously considered.

10 CFR 50.46 (a)(3)(i) requires, in part, that each holder of an operating license shall

estimate the effect of any change to, or error in, an acceptable ECCS evaluation model

or in the application of a model to determine if the change, or error, is significant. For this

purpose, a significant change or error is one that results in a calculated peak fuel

cladding temperature different by more than 50 F from the temperature calculated for the

limiting transient using the latest acceptable ECCS model, or is a cumulation of changes

and error that the sum of the absolute magnitudes of the respective temperature

changes is greater than 50 F.

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On December 5,1997, the licensee identified that the licensing basis safety analysis was

in error, in that available HPSI system flow (an ECCS system) was less than assumed.

However, the licensee failed to estimate the effect of this error on peak fuel cladding

temperature. The failure to estimate the effect of this error on peak clad temperature is

an apparent violation of 10 CFR 50.46 (a)(3)(i) (50-382/9725-06).

When asked by the team on December 18,1997, to assess the impact of lowered HPSI

flow on the calculation of PCT to account for the additional uncertainty, the licensee

determined that a HPSI flow value of 599.3 gpm as input into the SBLOCA analysis

using the original evaluation model would result in a PCT greater than 2200'F.

If the additional uncertainty for flow control valve position was accounted for

(approximately 11 gpm), the analytic value would have to be reduced further to account I

for this additional random e Tor term. This would aiso result in exceeding a PCT of l

2200'F for a SBLOCA using the original evaluation model.

10 CFR 50.46 (a)(3)(ii) requires, "Any change or error correction that results in a

calculated ECCS performance that does not conform to the criteria set forth in

paragraph (b) of thic Section is a reportable event as described in . 10 CFR 50.72 and

10 CFR 50.73." 10 CFR 50.46 (b)(1) requires, "The calculated maximum fuel elemen(

cladding temperature shall not exceed 2200'F.10 CFR 50.72 (b)(ii)(B) requires, in Part,

". . the licensee shall notify the NRC as soon as practical nnd in all cases within

one hour of the occurrence of any of the following: . (ii) Any event or condition during

operation that results in . . . the nuclear power plant being: . . (B)In a condition that is

outside the design basis of the plant."

]

On December 5,1997, the licensee identified and did not report within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> an error

correction, which would have resulted in a calculated ECCS performance that did not

conform to the criteria set forth in paragraph (b) of 10 CFR 50.46. Specifically, the

licensee identified that availab!e HPSI flow was tens than that stated in the safety

'

analysis. Using the licensing basis analysis and the available HPSI flow, the licensee

estimated that peak fuel cladding temperature would have exceeded 2200V, a condition

outside the design basis of the plant. The condition was not reported until De.nember 18,

1997. The failure to report an ert. correction that would result in a peak clad

temperature that exceedeo 22006, :., the first example of an apparent violation of

10 CFR Part 50.46 (a)(3)(ii) (50-382/9725-07).

10 CFR 50.46 (a)(3)(ii) also requires, "For each change to or error discovered in an

acceptable ECCS evaluation model or in the application of such a model that affects the

temperature calculation, the applicant shall report the nature of the change or error and

its estir...ted effect on the limiting ECCS analysis to the Commission at least annually .

as specified in 10 CFR 50.4. If the change or error is significant, the applicant shall I

provide this report withia 30 days and include with the report a proposed schedule

for providing a reanalysis or taking other action as may be needed to show compliance

with 10 CFR 50.46." The licensee reported the issue to the NRC in a 10 CFR 50.72

notification on December 18,1997, and in a licensee event report in accordance with the

requirements of 10 CFR 50.46 and 10 CFR 50.73 on January 5,1998.

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As of January 22,1998, the licensee had not provided a proposed schedule for providing l

a limiting ECCS reanalysis, which corrected the significant HPSI system flow error or for {

taking other action as may be needed to show compliance with 10 CFR 50.46. The

failure to provide a schedule for the reanalysis within 30 days of discovery is the second

example of an apparent violation of 10 CFR 50.4t (a)(3)(ii)(50-382/9725-07).

System Operability

The !icensee concluded that the HPSI system remained operabie because a new

SBLOCA evaluation model had been developed by its nuclear steam supply system  !

vendor and was nearing fermal approval by the NRC. The new evaluation model

implementsc' improvements in core heat transfer modeling, which included steam 3

cooling. A gencaic olant analysis using the original roodel and an assumed injection flow  !

of 695 cpm from H,TI rJone resulted in a PCT of 1732*F. Application of the new I

evaluatiori mode; to a generic plant SBLOCA ardalysis with no change in ECCS j

performance resulted in a 336*C reduction in PCT, from 1732 to 1396'F. The licensee 1

concluded that a similar reouction in PCT was expected when the new evaluation model l

was applieel to its plant-specific data. The analysis had not been completed at the

conclusion of the inspection. The licensee reasoned that this reduction in PCT using the l

new evaluation model could be used to reduce recuired HPSI flow rate and still achieve {

sn acceptable PCT. The NRC formally epproved the new SBLOCA methodology on j

December 17,1997. i

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The licensee stated that it had performed an informal calculation to evaluate HPSI

system performance at 108 percent power to support a possible power uprate request l

An acceptable PCT was obtained using the new model and a HPSI flow of 621.8 gpm. l

The licensee reasoned that if 621.8 gpm flow was acceptable for the 108 percent power l

case, then a reduction in HPSI flow accounting for additional uncertainties, which j

amounted to about 5 percent (588.2 gpm), was acceptable. i

On January 9,1998, the licensee initiated Condition Report 98-0046, which identified

that additional sources of instrumentation uncertainty needed consideration for the

<

operability evaluation of Condition Report CR-97-2695. They included a scaling

difference between the instruments (one of the instruments was not calibrated for the

assumed temperature) and that portioris of Procedure OP-93-108, "Si Flow Balance

Test," Revision 3, Change 1, dated April 10,1994, used the less accurate control board

instruments instead of the qualified safety parameter display system (QSPDS).

By removing from conservatisms that were in Instrument Loop Uncertainty l

Calculation EC-195-011, the licensee concluded that the HPSI system remained  ;

operable. l

Previous Opportunities to identify and Correct Condition

The team noted that the licensee had several previous opportunities to identify this  ;

condition.

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1994 Flow Anomajlims

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In 1994, the licensee noted unexpected flow anomalies, which they attributed to test '

instrumentation uncertainty. In Condition Identification 290132, the licensee noted that

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' the QSPDS flow indicators were about twice as accurate as the control board analog

{

indicators. To improve test accuracy, the licensee issued Procedure OP-903-108, l

"Si Flow Balance Test /' Revision 3, Change 1, dated April 10,1994, which changed the

flow readout device to the more accurate QSPDS indicators for portions of the test.

Licensee personnel sf.ated that the procedure was not revised to require that all of the .

test data be collected using the more accurate display because operations management

was concerned that too much dependence on QSPDS would cause the operators to lose

their control board skills. The team also noted that it appeared that the licensee did not

fully research the design basis for the test requirements at this time.

Technical Onecification Instrument Uncertaintv Proie.c.t

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Condition Report CR-96-0382 was initiated on March 15,1996, when it was identified

{

that instrumentation loop uncertainties were not accounted for in emergency feedwater '

pump acceptance criteria. An action plan was developed to perform a review of

u technical specifications to evaluate the generic issue of instrument error and surveillance

testing acceptance criteria. The action plan included an open item to evaluate the effect

of instrument error on the HPSI flow balance surveillance requirement, but the action had

not been completed at the time of the inspection.

1

During discussions with the team, the licensee stated that they considered evaluating the

impact of the flow instrument uncertainty on the surveillance testing requirements.

However, the need to perform a detailed evaluation was given a low priority because the

licensee four.d a December 1,1989, document from the nuclear steam supply system i

vendor, which stated instrument uncertainties were accounted for in determining the 1

HPSI flow balance surveillance requirement. The actual value was not provided to the

licensee in that document.

1MS_}liatdressurg_ Safety Iniection System Self Assessment

A HPSI self ascessment, completed by the licensee July 16,1996, stated:  ;

"A design engineer and a design engineering supervisor were interviewed l

concerning the generic issue of incorporating instrument error in a surveillance

'

test [s] [in] compliance with technical specification requirements. Technical

Specification Action 4.5.2.h requires the sum of the three smallest HPSI injection

flows to be greater than 675 gpm as does the acceptance criteria of surveillance

procedure OP-903-108. Both use 675 gpm but neither includes instrument error. ,

CR 96-0382 documents the instrument error question generically in action item 4 l

and will be addressed later this year."

l

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The licensee did not initially generate a separate condition report, evaluate the

operability of the HPSI system, or correct the surveillance procedure, instead they relied j

on the action plan for Condition Report 96-0382, described above. The licensee stated i

that an informal operability evaluation was perfonned on approximately August 1996,

which found the system operable based on past surveillance test data. In part, because  !

the licensee did not correct the surveillance procedure, this informal operability )

determination became invalid after the flow balance was performed in May 1997, The i

licensee did not evaluate system operability until December 5,1997, and as of i

December 18,1997, the condition was not promptly corrected. l

I

10 CFR Part 50. Appendix B, Criterion XVI, " Corrective Action," requires that measures

shall be established to ensure that conditions adverse to quality, such as failures,

malfunctions, deficiencies, deviations, defective material and equipment, and

nonconformances are promptly identified and corrected. The failure to take ,

prompt corrective action when the licensee identified that neither Surveillance I

Procedure OP-903-108,"SI Flow Balance Test," Revision 3, Change 1 nor

Technical Specification Surveillance Requirement 4.5.2.h included an adequate

allowance for test instrument uncertainty is an apparent violation of 10 CFR Part 50,

Appendix B, Criterion XVI (50-382/9725-08).  !

Eailure to ootirnally Adiust thejioh PressuleEafgly Iniection System

The team noted that during the May 1997 flow balance test, the licensee did not take

time to adjust the flow control valve positions to optimize system performance. The

A train /A pump configuration met the flow criteria exactly with no test margin. The

licensee originally planned additiona! limit switch adjustmems, but canceled these

add;tional adjustments when the acceptance limits were met. The team noted that it

would have been possible for the licensee to adjust the flow control valve limit switches

to obtain more margin, but the licensee did not take the time to make the additional

adjustments.

LR9n_Unsellaioly&alradation Update

A HPSI instrumentation loop uncertainty calculation. Calculation EC-195-011, "SI-HPSI

Flow instrumentation Loop Uncertainty Calculation," Revision 0, was performed in 1995

as part of a site-generic effort to update instrument loop uncertainty calculations, and it

was revised on September 18,1996, to implement a revised transmitter calibration

temperature. The team noted that the results of this calculation were not evaluated for

impact on surveillance testing acceptance criteria.

Rssian Bas.ijitung_radeftoiect

As stated above, the original calculation performed by the nuclear steam supply system

vendor to determine an acceptable HPSI flow technical speci5 cation acceptance

criterion was provided to the licensee in September 1997 as part of a design basis

information transfer project. For the first time, this calce!ation quantitatively provided the

licensee with the instrument uncertainty assumption used in the development of the

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technical specification surveillance requirement. The licensee had an open item in the

design basis upgrade project to compare this instrument uncertainty value with the

uncertainty estimate in Calculation EC-195-011, "SI-HPSI Flow instrumentation Loop

Uncertainty Calculation," Revision 1, but the action had not been completed at the time

of theinspection. '

Similar Low Pressure Safety Iniection System (LPSI) Dgficiency

in Cor,dition Report 97-0649, dated March 19,1997, the licensee determined that an

uncertainty of 725 gpm calculated in Revision 0 of Calculation EC-191-05.2, "LPSI Flow  ;

instrumentation Loop Uncertainty Calculation," exceeded the uncertainty assumed in the j

development of the corresponding surveillance requirement for the LPSI system portion i

of Technical Specification 3/4.5.2.h.

The surveillance requirement specified an acceptance limit of 4810 gpm, which provided

adequate allowance for the LPSI flow instrument uncertainty specified in their interface

document with the nuclear steam supply vendor However, the surveillance requirement

was not high enough to provide an adequate allowance for a 725 gpm uncertainty. In an

operability evaluation, the licensee noted that the as-tested flows exceeded the

surveillance requirement acceptance limit. As a result, the licensee determined that the

as-tested flows were sufficient to allow for the larger calculated uncertainty.

The licensee evaluated whether or not the surveillance requirement required revision.  :

'

They contacted the nuclear steam supply vendor and determired that they could lower

the amount of LPSI flow assumed in the emergency core cooling system analysis. As a

result, the licensee concluded, that even after considering the 725 gpm of uncertainty,

the surveillance requirement,4810 gpm, was acceptable.

In Condition Report CR 97-0649, the licensee documented that there were no stated  !

requirements to perform 50.59 reviews of calculations and that the interrelationship

between instrument uncertainties and testing to satisfy technical specification limiting

conditions for operation and the use of analytic values was often neither clearly apparent l

nor widely understood.

Corrective actions included ensuring that all instrument uncertainty calculations were

evaluated in accordance with 10 CFR 50.59 and reviewing the bases for all technical

specifications to determine whether associated instrument uncertainty was properly

considered. The condition report stated that these efforts were being addressed as

corrective actions for Condition Reports 95-1242 and 96-0382.

The team considered this planned corrective action to prevent recurrence to be

ineffective. On December 11,1997, the licensee evaluated the most recent revision of

the HPSI flow uncertainty calculation and determined that a full written safety evaluation

in accordance with 10 CFR 50.59 was not required. This corrective action should have

resulted in a written safety evaluation for the HPSI flow uncertainty calculation. This

failure to perform a written safety evaluation is discussed in more detailin Section E2.3.

22

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c. Conclusions

The team identified two apparent violations of 10 CFR Part 50, Appendix B, Criterion XI,

related to test control in the HPSI flow baiance test. The licensee had not specified test

instrumentation, which had an accuracy commensurate with the assumptions in 'ho

development of the surveillance requirement. The licensee also had not adequateiy

considered valve position variability when the acceptance limits were established for the

survei!!ance procedure.

.

The team identified two apparent violations of 10 CFR 50. 46. When the licensee

determined that HPSI flow was less than assumed in the emergency core cooling system

analysis, the licensee did not assess the impact of the flow deficiency on peak fuel clad

temperature, They also did not report operation outside of tne design basis or submit a

schedule for the performance of a revised emergency cure cooling system analysis.

The team identified one apparent violation of 10 CFR Part 50, Appendix B, Criterion XVI. I

In July 1996, the licensee identified the HPS) test instrumentation uncertainty issue

described above, but did not initiate a separate condition report, perform a documented

operability determination, or correct the surveillance procedure prior to the next test

performance, in addition, the team identified several prior opportunities to correct the

HPSI system flow deficiencies.

E2.3 10 CFR 53,.59 Imolementat on

a. laspection Scoce (37001)

The team reviewed 4 prescreenings,7 screenings, and 12 safety evaluations involving

permanant modifications, component replacements, engineering calculation changes,

technical specification base changes, and procedure changes.

b. Qbservations a.D.d Findinas

With the exceptions described below, the team found that the 10 CFR 50.59 written

safety evaluations were generally logical and of acceptable quality, Most of the safety

evaluations addressed the change being evaluated in adequate detail and most provided

the justifications for concluding that there were no unreviewed safety questions.

Appropriate references were provided in many safety evaluations. However, some

safety evaluations did not reference important documents like safety evaluation reports

issued by NRC during the operating license review process, standard review plans, or

appropriate sections in UFSAR.

These documentation deficiencies were discussed with the licensee. The team found

that the licensee had identified similar documentation deficiencies in their intemal

assessment, which was perfc med by quality assurance. The team found that the

licensee had appropriately initiated condition reports for the findings.

23

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The team identified two instanct s in which a written safety evaluation was not performed

and apparently should have been The team also identified three apparent unreviewed

safety questions that involved changes that were implemented without prior NRC

approval.

Securing Charging During a Loss-of-Coolant Accident (LOCA)

r The team identified a failure to perform a written safety evaluation for Change 2,

Revision 7, of Procedure OP-902-002, " Loss of Coolant Accident Recovery Procedure." ~

This procedure was the general emergency response procedure for all types of loss-of-

coolant accidents. The change directed operators to secure the charging pumps after a

recirculation actuation signal (RAS) had occurred. As discussed in Section E1.1, the

licencee identified that its post-LOCA containment flooding analysis resulted in an

unacceptable maximum flood level when appropriate uncertainties were considered. To

prevent the instrumentation from becoming submerged, the licensee imposed an

administrative limit of 90 percent maximum RWSP level. In order to provide additional

operating margin for RWSP level, the licensee evaluated the sources of water to

containment following a LOCA and determined that charging pump operation could be

stopped following a RAS.

!- The team noted that the 10 CFR 50.59 screening for this change stated that, "This

change is purely procedural and does not alter any components in the facility as

described in the Licensing Basis Documents." Therefore, the licensee determined

that a safety evaluation in accordance with 10 CFR 50.59 was not required. The team

identified that Section 6.3.3.3.1 of the UFSAR stated, "In addition to the SIS [high and

low pressure safety injection system] flows, injection from the charging pumps is credited

in the small break analysis for Waterford 3."  !

l

The team discussed this issue further w;th the licensee to determine if an immediate

safety concern existed with the change in Procedure OP-902-002 to terminate charging

pump flow, which was credited in the ECCS analysis. The licensee stated that charging

pumps were only credited for a small-break loss-of-coolant accident and that the time

when the charging pumps were secured (RAS actuation) was long after the maximum

peak clad temperature had occurred. Therefore, charging pump operation was not

required '

The team noted that Procedure OP902-002 was the general loss-of-coolant accident

recovery procedure, which also included responses to large-break loss-of-coolant l

accidents. The team determined that securing a source of coolant credited in the safety _ i

analysis required a written safety evaluation.

24

e

.

10 CFR 50.59 (b)(1) states, in part, that the licensee shall maintain records of changes in

procedures made pursuant to this section to the extent that these . changes constitute

changes in procedures as described in the safety analysis report. These records must

include a written safety evaluation, which provides the bases for the determination

that the change does not involve an unreviewed safety question. The failure of

the licensee to perform a safety evaluation for this change is an apprrent violation of

10 CFR 50.59 (b)(1) (50-382/9725-09).

10 CFR 50.59 Screening Review for Calculation EC-195-011

On December 18,1997, the team requested the 10 CFR 50.59 safety evaluation for the

most recent revision of Calculation EC-195-011. "SI-HPSI Flow instrumentation Loop

Uncertainty Calculation," Revision 1, dated September 18,1996. The team found that as

of December 18,1997, the licensee had not performed a written safety evaluation for this

calculation.

The licensee performed a screening review of the calculation on December 11,1997,

and incorrectly concluded that the instrument loop uncertainty calculation did not have

the potential to alter the information described in license basis documents. The team

found that the calculation did have the potential to alter the information described in l

license basis documents. For example, UFSAR, Section 6.3.3.1, " Emergency Core 1

Cooling System Performance Evaluation," stated that the results of the ECCS

performance analysis show that the plant meets the 10 CFR 50.46 acceptance criteria. f

j

The team noted that, when the results of Calculation EC-195-011 were applied to the i

NRC approved model, it resulted in exceeding the 10 CFR 50.46 ECCS acceptance

criteria, which changed the facility as described in UFSAR, Section 6.3.3.1. ,

The team determined that failure to perform a written safety evaluation apparently

resulted in operation with an unreviewed safety question, without prior NRC approval.

The results of Revision 1 to Calculation EC-195-011 effectively made a change to the

facility described in the safety analysis report, which reduced the margin of safety

defined in the basis for a technical specification. Specifically, UFSAR, Table 6.3-7,  !

"HPSI Pump Minimum Delivered Flow to Reactor Coolant System for The 0.04 FT' Break

Analysis," stated that 207.25 gpm is 25 percent of the delivered flow from one high  !

pressure pump at .0 psig (or the flow in one injection path). The safety analysis assumed i

that flow is delivered from three out of four of the injection paths or a total of 621.8 gpm.

Technical Specification Bases 3/4.5.2 stated that the surveillance requirements ensure

that, at a minimum, the assumptions used in the safety analysis are met. The bases j

'

section further stated that maintenance of proper flow resistance and pressure drop in

the piping system to each injection point is necessary to provide an acceptable level of 4

total ECCS flow to all injection points equal to or above that assumed in the ECCS LOCA i

analyses. )

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However, after consideration of instrument uncertainty as calculated in Revidon 1 of

Calculation EC-195-011, the licensee estimated that Technical Specification 4.5.2.h did

not assure HPSI flow greater than the assumptions in the ECCS LOCA analyses.

Twenty-five percent of the surveillance acceptance limit less uncertainties was 197 gpm,

which was less than 207.25 gpm specified in UFSAR, Table 6.3-7. As a result, this

revision reduced the margin of safety defined in Technical Spccification Bases 3/4.5.2,

because the surveillance no longer provided an acceptable level of flow to all points

equal to or above that assumed in the currently licensed ECCS-LOCA analyses.

10 CFR 50.59 (a)(1) states, in part, that a licer,see may make changes in the facility as '

.

described in the safety analysis report without prior Commission approval unless the

proposed change involves a change in the technical specifications incorporated in the

license or an unreviewed safety question.10 CFR 50.59 (a)(2) states that a proposed

change, test, or experiment shall be deemed to involve an unreviewed safety question if

the margin of safety as defined in the basis for any technical specification is reduced.

The reduction in the margin of safety as defined in the basis for a technical specifir?;cn

was considered to be an unreviewed safety question and the first example of appant

violation of 10 CFR 50.59(a)(1) (50-382/9725-10).

Emergency Feedwater Pump Capability (SE 97-165)

The team identified a second example of a change to the facility described in the

UFSAR, which apparently involved an unreviewed safety question. On July 10,1997,

the licensee revised the bases section of the technical specifications to reduce

emergency feedwater pump capability requirements below the assumptions made in the

safety analysis.

The affect of this change on system operability was reviewed in NRC Inspection

Reports 50-382/96-202 and 50-382/97-10. In NRC Inspt ction Report 50-382/96-202, the

NRC noted that Calculation EC-M96-004, " Design Basis Reconstitution for EFW Flow

Rate," Revision A, datermined that minimum required emergency feedwater flow rate

was 575 gpm. This flow rate was needed to provide a 4980 pounds-mass steam

generator margin while using a 10 percent decay heat uncertainty value. The NRC

agreed with the licensee's determination that current pump capability supported the

operability of the emergency feedwater system.

Reduction in the Marcin of Safetv

UFSAR, Section 10.4.9.2, " Emergency Feedwater System Description," stated that the

turbine driven pump or both motor-driven pumps together have been designed to

provide 700 gpm flow to the steam generators upon loss of feedwater flow in order to

remove decay heat and to reduce reactor coolant system temperature and pressure to

the shutdown cooling entry conditions.

,

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From December 18,1984, until July 10,1997, Technical Specification Bases 3/4.7.1.2

stated that each electric-driven emergency feedwater pump is capable of delivering a

total feedwater flow of 350 gpm at a pressure of 1163 psig to the entrance of the steam

generators. The steam-driven emergency feedwater pump is capable of delivering a

total feedwater flow of 700 gpm at a pressure of 1163 psig to the entrance of the steam

generators.

On July 10,1997, the licensee approved Safety Evaluation 97-165 for Licensing

Documen+. Change Request (LDCR) 97-0034. LDCR 97-0034 revised Technical

Specification Bases 3/4.7.1.2 to reduce the pump capability requirements to the

following: "The two electric-driven emergency feedwater pumps combined are capable of

delivering a total feedwater flow of 575 gpm at a pressure of 1102 psig to the entrance of

the steam generators. The steam-driven emergency feedwater pump is capable of

delivering a total feedwater flow of 575 gpm at a pressure of 1102 psig to the entrance of

the steam generator."

The team noted that the safety analysis performed for the current operating cycle,

Cycle 9, was based on two motor-driven pumps producing a combined flow of 630 gpm

at 1102 psig and on the turbine driven pump producing 645 gpm at 1102 osig. The

licensee did not perform a revised safety analysis for the lower emergency feedwater

flow rates,575 gpm at 1102 psig (combined electric pumps or turbine-driven pump).

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The team determined that this change was an apparent reduction in the margin of safety  !

as defined in the basis for a technical specification,

lacigate in the Probability of a Malfunction

Updated Final Safety Analysis Report, Section 15.2.3.1, "Feedwater System Pipe

Breaks," indicated that no operator actions were assumed for the first 30 minutes

following a main feedwater line break. With reduced emergency feedwater flow, the

reactor coolant system will heat up faster, which could cause the pressurizer to become

'

solid and lift the relief valves. The relief valves were designed to discharge steam not

water and cannot be relied upon to close in this situation. If these relief valves were to

stick open, a small break LOCA would occur. Using licensed safety analysis methods,

the nuclear steam supply vendor determined that operator actions to secure charging

was needed 7 minutes after the reactor trip. The licensee determined by alternative and

less conservative analysis rnethods that at the reduced emergency feedwater flow rates

(575 gpm at 1102 psig), operator actbn would be needed within 25 minutes to secure

charging pumps to prevent the pressurizer from going solid rather than the 30 minutes

that was stated in the UFSAR. The team noted that UFSAR Section 15.6.3.4, .

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" inadvertent Opening of a Pressurizer Safety Valve," contained an estimate of the

frequency of inadvertent opening of a pressurizer safety valve. The team determined

that the reduced operator action time increased the probability of a malfunction of the

pressurizer relief valves and increased the probability of a LOCA.

27

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Unreviewed Safety Question Determination

The team determined that the reduction in emergene feedwater pump capability I

requirements reduced the margin of safety as defined in the basis of a technical

specification, increased the probability of a previously evaluated malfunction (stuck open i

pressurizer safety valve) and increased the probability of a LOCA. The change in

emergency feedwater pump capability requirements was considered to be an

unreviewed safety question and the second example of an apparent violation of

10 CFR 50.59 (a)(1) (50-382/9725-10). I

Hydrogen Analyzer (LDCR 98-0032)

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The team identified a third example of a change to the facility as described in the i

UFSAR, which apparently involved an unreviewed safety question.

All accident analyses assume containment is isolated and leakage le less than an

assumed value. To ensure this assumption is valid, the originallicense application

included the following commitments regarding the containment isolation system. Final J

Safety Analysis Report, Section 6.2.4.2.1, " Actuation Signal," included a commitment to

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meet 10 CFR Part 50, Appendix A, General Design Criteria 54," Piping Systems

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Penetrating Containment." General Design Criteria 54 str2s, '

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" Piping systems penetrating primary reactor containment shall be provided with

leak detection, isolation and containment capabilities having redundancy,

reliability, and performance capabilities which reflect the importance to safety of

isolating these piping systems."

Final Safety Analysis Report Section 6.2.4.3.2, " Single Failure Analysis," stated

that wherever two automatic isolation valves are in series, each valve operator is

'

actuated from a separate and redundant containment isolation actuation signal (CIAS) l

channel. The licensee's original technical specifications, issued as NUREG 1117,

" Technical Specifications, Waterford Steam Electric Station, Unit No. 3," Table 3.6-2

designated Hydrogen Analyzer Valves HRAISV0110A(B), HRAISV0109A(B), and

HRAISV0126A(B) as automatic containment isolation valves.

To ensure the availability of the hydrogen analyzer post accident, Final Safety Analysis

Report Section 6.2.5.2.1, " Hydrogen Analyzer System," stated that the system consisted

of two identical units which are completely independent of each other and are powered

from an independent source. Therefore, assuming a single failure, process capability is

available to monitor the hydrogen concentration in containment. Also in this section, it

was noted that the isolation valves for the hydrogen analyzer system are normally locked

closed and the automatic actuation signal can be overridden for analyzing after a LOCA.

<

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In late 1995, the licensee determined that the commitment to have a single failure

proof containment isolation system conflicted with the commitment to have an

available single failure proof post-accident hydrogen analyzer. To operate the hydrogen

'

analyzers, it was necessary to open the associated containment isolation valves. The

licensee reasoned that the commitment to have an available post-accident hydrogen

analyzer implied that the associated containment isolation valves would also be

available. If they used the standard containment isolation design practice of using one

train of power for the inboard isolation valve logic and the other train of power for the

outboard containment isolation valve logic, the failure of one power supply would prevent

use of either hydrogen analyzer. On January 3,1996, the licensee approved a change

to UFSAR, Section 6.2.4.3.2, " Single Failure Analysis," to allow an exception to the

containment isolation single failure commitment for Hydrogen Analyzer

Valves HRAISV0110A(B), HRAISV0109A(B), and HRAISV0126A(B). They added the

following to UFSAR 6.2.4.3.2:

"To maintain compliance with Regulatory Guide 1.7, GDC #14, i.e., to be able to

measure containment hydrogen concentration after LOCA despite the worst

single active failure, Waterford 3 had designed the HRA [ hydrogen recombiner

analyzer] containment isolation valves so that CIAS Channel A is exclusively

used in HRA Train A containment isolation valve control circuits. Similarly, CIAS

Channel B is exclusively used in HRA Train B containment isolation valve control

circuits."

On November 26,1997, the licensee identified that the hydrogen analyzer piping was not

designed to meet 10 CFR Part 50, Appendix A, General Design Criteria 54, " Piping

Systems Penetrating Containment." The licensee determined that this design <d not

meet the General Design Criteria 54 requirement to maintain reliable redundancy to

ensure containment isolation. Failure of one CIAS relay would defeat containment

isolation of the hydrogen analyzer. The licensee reported operation outside of the

Technical Specification 3.6.3 in Licensee Event Report 50-382/97-032.

To resolve the design issue, the licensee reclassified Hydrogen Analyzer Valves

HRAISV0110A(B), HRAISV0r IA(B), and HRAISV0126A(B), from automatic to

manual / remote manual, locket closed, containment isolation valves. This change

effectively substituted operator action for a 5-second automatic closure. The change

introduced the possibility that an operator would not be able to close the valves within 5

seconds of the containment isolation actuation signal, which introduced the possibility of

increased dose consequences to the public. However, the team noted that this

distinction was only important during surveillance testing. At all other times during

normal operation, these valves were required to be locked closed.

The team noted that the accident analyses assumed all containment isolation valves

were closed and leakage was controlled below a minimum value. The licensed

configuration, a single-failure proof redundant automatic isolation, would be less likely to

result in a failure to isolate containment, than reliance on manual / remote manual closure

of the valves. The licensee had not evaluated the dose consequences of the failure to

close the valves or requested NRC staff review of the reclassification. The team

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determined that tNe change described in LDCR 98-0032 introduced the possibility of a

malfunction of a different type than any previously evaluated in the safety analysis report.

The introduction of the possibility of a new malfunction was an unreviewed safety -

question and the third example an apparent violation of 10 CFR 50.59 (a)(1)

(50-382/9725-10).

c. Conclusions ,

The team identified two apparent violations of 10 CFR 50.59. The first apparent violation

involved a failure to perform a written safety evaluation. The second apparent violation l

included three examples of changes to the facility that involved unreviewed safety

questions, which had not been approved by the NRC. Other 10 CFR 50.59 written safety

evaluations reviewed by the team were generally logical and of acceptable quality.

E3 Engineering Procedures and Documentation

E3.1 Engineerina Reauest Process

a. InsDection Scoce (37550.)

The team reviewed Procedure W4.104, " Engineering Request Process," Revision 0, and

25 engineering requests. The team dis Jssed the engineering request process and

some of these engineering requests with appropriate licensee personnel.

b. Observations and Findings

'

The team discussed the engineering request process with the licensee. While not fully

implemented, the licensee planned for the engineering request process to provide a

single process governing initiation of requests for engineering technical support. The

team noted that the engineering request process included requests for changes to plant

related structures, systems, and components. The team found that this process

eliminated the generation of requests in different forraats.

The licensee stated that Phase 1 of the engineering request process was implemented

on April 1,1997. Phase 1 consisted of preparing engineering requests for engineering

replies, administrative changes, and engineering evaluations that had no design changes

associated with them. The management expectation was that there would be no design

changes performed using the engineering request process during Phase 1, The licensee

stated that Phase 1 replaced engineering inputs and problem evaluation /information

requests. The team determined that all of the open problem evaluation /information

requests were converted to engineering requests or were closed.

The licensee stated that Revision 1 of Procedure W4.104 would be in effect on

December 15,1997. The licensee also stated that Phase 2 of the engineering request

process implementation would be completed by March 31,1998. The licensee stated

that Phase 2 would replace the following engineering programs:

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Control of vendor information

+

Temporary alteration requests

Set point changes

-

Design changes

Engineering reviews

-

Substitute part engineering evaluation report

+

Resolving procurement document change requests

+

Design proposals

-

Design change packages

The team reviewed 25 engineering requests generated for the safety injection system

and other safety-related systems. Several concerns were identified by the team and

satisfactorily addressed by the licensee.

c. Conclusions

The team found that the licensee had not completed the transition to the new

engit.eering request process. The licensee satisfactorily resolved concerns identified by

the team related to a review of 25 engineering requests.

E3.2 Desian Bases Documentation - 125V DC Distribution System

a. Insoection Scoos (37550)

The team reviewed Design Basis Document DBD-008, " Electrical Distribution (DC

portion)," dated February 28,1996.

b. Observations and Findings

The team 'ound that the design basis document for the de electrical distribution system

was generally comprehensive and was being appropriately updated by the licensee. The

team did identify some missing references to applicable regulations and commitments,

as well as, some minor update erro s. The team discussed these minor weaknesses

with the licensee. The licensee agreed that they were weaknesses and planned to

correct them.

c. Conclusions

in general, the design basis document for the de electrical distribution system was

comprehensive and was being appropriately updated by the licensee.

'

E33 Seismic Quahfication Documentation - 125V DC Station Batteries

a. 10inection Scoce (37550. 93809)

The team reviewed the documentation related to the seismic qualificatim of the station

batteries.

31

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e

b. Observations and Findinas

The licensee stated that the batteries were installed in 1992 and seismically qualified for

20 years. The team found that the licensee had qualified the batteries by equivalency, i

based on the battery vendor's Qualification Report OR-51155-01. The team identified

that the qualification test included aging-related test failures, which the licer,see argued

were not applicable to the installed batteries. The licensee noted that the installed

batteries were similar to cells, which passed the qualification test. The team noted that

the qualification report did not include documentation of a test of the exact design

installed at Waterford 3.

Subsequent to the exit interview, the licensee provided excerpts from a seismic test

report for the e"act battery cell design installed at Waterford 3. The seismic test was

conducted successfully on 15-year cells, for the Diablo Canyon Nuclear Power Plant, a

facility with more rigorous seismic requirements. The Diablo Canyon test results also

identified failures for 20-year old cells. Since, the Waterford 3 batteries were installed in

1992, these test failures were not presently applicable to the bterford 3 batteries. The

team determined the current seismic qualification of the Waterford 3 batteries was

acceptable.

'

The licensee believed that their seismic qualification test documentation adequately

demonstrated qualification for 20 years. However, based on the Diablo Canyon

test result failures for the 20-year old batteries, they initiated Engineering

Request W3-98-0134 to evaluate whether further testing was needed to qualify the

Waterford 3 batteries for the 15- to 20-year period.

i

c. Conclusions

The current seismic qualification of the Waterford 3 safety-related station batteries was  ?

acceptable. Seismic qualification, from 15- to 20-years qualified life, was not clearly

established. The licensee initiated an engineering request to further evaluate the

qualification of the batteries.

E3.4 Environmental Qualification of the Static Uninterruotible Power Sucolv (SUPS)

a. Inspection Scope (37550,93809)

The team reviewed the documentation related to the seismic qualification of the station

batteries.

b. Observations and Findinos

During the walkdown of the de system, the team noted that the SUPS, or inverters, were j

'

ooerating without fan cooling. The inverters were being cooled by natural draft air

circulation. While this operation was in accordance with design, the team was concerned

1

32

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this design might be vulnerable to loss-of-room cooling. The team requested

documentation related to the inverter's capability to reliably operate for 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, following i

a station blackout. 1

The team found that during a station blackout. a 120 F temperature was used as the

upper design limit for the room where the inverters were located. The team found that

the vendors' documentation for the inverters, indicated an upper ambient temperature

limit for inverter operation of 104' F. The team was concerned that a 120 F limit on room

temperature was inappropriate considering the vendor limit on inverter operation of

104 F. Also, the inverter design did not include any forced drsit cooling. In addition, the

licensee had not established any compensatory measures to enhance cooling in the

event of a station blackout.

The licensee referred the team to their station blackout submittal dated April 14,1989,

and NUMARC 87-00 " Guidelines and Technical Bass; for NUMARC Iritiatives j

'

Addressing Station Blackout." They stated that these documents justified that specific

thermal qualification was not necessary for the inverters, as le'g as the room

temperatures stayed below the 120'F limit. During the insperSon, the licensee contacted

the vendor. The vendor provided a preliminary determination that the SUPS could

operate for 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> at the 120 F limit. The vendor stated that they would perform

additional aniJysis to confirm this determination.

On May 9,1998, the licensee provided additional vendor documentation. The vendor '

found that a similar model or inverter was tested at 122 F for 200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> under both full

and no load with no degradation in performance specifications. The vendor concluded

this test data demonstrated that the inverters at Wate: ford 3 will function in an ambient

temperature of 120 F for a period of 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.

c. Conclusions

l

The team found that the reliability of the safety-related inverters during station blackout

conditions was not clearly established. The licensee contacted the vender and was

provided additional documentation that confirmed the capability of the safety-related

inverters to operate at room temperatures expected during a station blackout.

E4 Engineering Staff Knowledge and Performance

E4.1 Interview of Staff Personnel

a. Inspection Secoe (37550)

During the inspection, the team interviewed a number of engineering personnel

regarding a wide variety of technicalissues.

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b. . Observations and Findings l

In general, licensee personnel were knowledgeable of the equipment and systems,

which were assigned to them. During walkdowns, they comprehensively answered

questions and weo able to discuss relevant equipment issues. In many instances,

during the inspectan. the team identified potential areas for concern, which were readily

resolved by licensea personnel.

c. Conclusions

in general, licensee personnel were knowledge able of the equipment systems assigned

to them.

E6 Engineering Organization and Administration

E6.1 Engineerino Backfoos

i

a. Insoection Scooe (37550)

The team reviewed the engineering request and condition report backlogs to determine

the trend of these backlogs. Since the engineering request process was new, the team

reviewed all of the available backlog data. The team reviewed the backlog of condition

reports for plant engineering from July 1996 to November 1997. The team also .

assessed licensee resolution of specific engineering requests and ( ondition reports as I

documented in Sections E3.1 and E7.1 of this report. l

l

b. Observations and Findinos I

Engineering Requests

The team determined that the engineering request backlog was increasing. The. team

noted that, since May of 1997, the engineering request backlog increased from 10? open

items to 250 open items. The team discussed the plans to reduce the backlog with the

licensee and found that the licensee planned to rM nitor the backlog for a few months

prior to implementing any corrective actions to reouce the backlog. The licensee stated

that the engineering requests were trended biweekly by providing each supervisor a list

of the open items for which they were responsible. In addition, the licensee stated that

the engineering requests were trended monthly by providing management a graph of

engineering requests initiated and closed. The licensee stated that they had plans to

initiate a performance indicator for the average age of open engineering requests.

The licensee acknowledged the backlog was increasing, but viewed the increase as

manageable. They stated that the increase occurred, in part, because of increased

emphasis on completing corrective actions for condition reports.

34

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.

Condition Reports

The team noted that there were 261 open condition reports in July 1996 and 221 open

condition reports in November 1997 for system engineering. The team determined this

was a downward trend for system engineering.

,

For design engineering, the team found that there were 221 open condition reports in

July 1996 and 345 open condition reports in November 1997. The team noted that a

number of condition reports were opened for design engineering during the refueling

outage in March through July 1997. The number of open design engineering condition

reports peaked at 414 in May 1997 and trended down to 345 in Novenicer 1997. After

considering the timing of the refueling outage, the team determined that the number of

open condition reports for design engineering also trended downward.

,

c. Conclusions

The team determined that the engineering requests backlog wr increasing. The

licensee acknowledged the backlog was increasing, but viewed the increase as

manageable. They stated that the increase occurred, in part, because of increased

emphasis on completing corrective actions for condition reports. Based on the

decreasing trend in the number of condition reports and the acceptability of the condition

reports as documented in Section E7.1 of this report, the team concluded that the

licensee was effectively reducing the condition report backlog.

E7 Quality Assurance in Engineering Activities

E7.1 Condition Reoort Review

a. Insoection Scooe (37550)

The team reviewed Procedure W2.501, " Corrective Action." Revision 6, and 22 condition

reports. The team discussed the condition report process w;th licensee personnel. In

addition, the team discussed some of the condition reports with applicable licensee

personnel.

b. Observations and Findinas

The team determined that the purpose of the corrective action procedure was to provide

a means to promptly identify and correct adverse conditions. Adverse conditions were

defined as an event, defect, characteristic, state, or activity that prohibited or detracted

from the safe, efficient operation of the plant. The team determined that adverse

conditions ;ncluded nonconforming conditions, conditions adverse to quality, industrial

safety concerns, and plant reliability concerns.

35

.

.

The team reviewed 22 condition reports associated with the safety injection system.

The team noted that Condition Reports 97-1675 and 97-1288 identified configuration

control problems. As described in Section E3.1, the team also identified Engineering

Request ER-W3-97-0144, which involved a configuration control problem.

-

Condition Report CR-97-1675, dated June 26,1997, identified that the 26.5-inch

diameter round nc:zle strainers, shown on Design Drawing G-907 for the

refueling water storage pool, which should have been installed inside the

box-type pool strainers on each of the lines, were not installed. The licensee did

not have any evidence that the round nozzle strainers had ev6r been installed.

The licensee determined that large box-type pool strainers located at suction

lines were added to the design later to comply with nuclear steam supply vendor

criteria for particulates in the reactor core and the installation of the box strainers

superseded the need for the round strainers. The licensee concluded that the

26.5-inch round strainers were not required since the round screens were on the

design drawings downstream of the box strainers and the round strainers utilized

screen mesh size with much larger openings.

-

The team reviewed Condition Report CR-97-1288, dated May 21,1997, which

determined that there was no seat material on the fitting of the solenoid for

Valve SP ISV0105. The solenoid was the containment isolation solenoid for

the containment sump pump inside containment and the seal material was the

equipment qualification boundary. The licensee declared the solenoid valve

inoperable and repaired the seal. In the reportability determination, the licensee

noted that an electrical failure of the solenoid valve wo ld not prevent the -

containment isolation valve from performing its safety function to close. The

licensee noted that the air-operated containment isolation valve failed closed on

loss-of-power to the solenoid. Once a containment isolation occurs, the solenoid

is de-energized. Therefore, there is no electrical failure mode at the solenoid,

which will result in the valve inadvertently opening. The licensee determined that

the valve had an active iosed requirement only and the missing sealin the

solenoid would not make the containment isolation valve inoperable.

-

The team reviewed Engineering Request ER-W3-97-0144, dated May 23,1997.

The engineering request was initiated for engineering to perform an evaluation of

diesel generator component bolting that was not instaPed in accordance with

vendor drawings. The emergency diesel generator standpipe, Jacket water

heater, and tube oil heater were installed with some of the installed botting snorter

than those shown on the vendor drawings. The licensee stated that they

attempted to install loager bolts in accordance with the vendor drawing. During

bolt changeout, the licensee determined that the longer bolts would not fit in the

areas where the shorter bolts were found. The licensee also identified that four of

the standpipe flange bolts were incorrect material. The vendor drawing specified

SA193, Grade B7 heavy hex bolts. However, four of the installed bolts were SAE

Grade 5, regular hex, which was not as strong as the SA193, Grade B7 material.

The licensee installed SA193, Grade B7 bolting, which was short enough to fit.

36

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.

.

The vendor's design drawings contained the longer bolts and the correct material

bolts. The vendor agreed that the as-built length was correct and the drawing

was in error. In addition, the vendor agreed that the SAE Grade 5 bolts

previously installed were the wrong material and should be SA 193 Grade 67 as

shown on the design drawing. The inspectors determined that this was an

example of a lack of configuration control.

While individually, these conditions were satisfactorily resolved, the team was concerned

that based on the sample size, that a high percentage of the examples involved

configuration control problems. The team determined that these examples rnay indicate

an adverse trend related to configuration control. Additionalinspection is planned to

evaluate the licensee's program for identifying adverse trends as it applies to these

recent configuration control findings. This inspection will be tracked as ar$ !nspection

followup item (50-382/9725-11).

c. Conclusions

The team noted that 2 of the 22 condition reports reviewed had configuration control

problems. Further inspection is planned to determine whether an adverse trend exists

rdateo to configuration control.

E8 Miscellaneous Engineering issues

E8.1

(Closed) Insoection Followuo item 50-382/96202-01: Instrument uncertainties for

component cooling water system and auxiliary component cooling water system.

Backaround - The licensee did not account for measurement and other uncertainties in

the evaluation of flow test results associated with the component cooling water (CCW)

and auxiliary component cooling water (ACCW) systems. The ficansee planned to

address this issue from a generic perspective to ensure that all relevant uncertainties

were accounted for in the evaluation of test acceptance criteria.

,

A corporate-wide instrumentation and control peer group began work on a policy to

consider instrument uncertainties in special test procedures and other related plant

surveillance test parameters. At the time of this inspection, the due date 'or completion I

of this effort was February 28,1998.

Insoection Followuo - The team reviewed Engineering Report ER-W3-97-0174-00-00,

"CCW and ACCW Flow Balance Test Acceptance Criteria," dated May 19,1997. This

document indicated that the design basis minimum ACCW flow to the CCW/ACCW heat

exchanger was 4500 gpm. UFSAR Table 9.2-1 supported this figure. During a flow

b4: lance test conducted May 8,1997, the measured ACCW flow rate was 4662 gpm.

Accurding to the report, the uncertainty in this measured flow was 350 gpm. Therefore,

the acNal flow rate may have been as low as 4312 gpm.

37

f

s ,

.

.

The team found that the licensee determined that it was not necessary to apply any

uncertainty to the flow balance test acceptance criteria, because a flow measurement

uncertainty term was already included in the assessment of system capability during

thermal r rformance testing. The licensee stated that the performance of the

CCW/A' W heat exchanger from the ACCW (shell) side was defined by two i

pararrets t (1) a ficw of 4500 gpm or greater and (2) a fouling factor of 0.0011 or less.

n the above test, the measured fouling factor was approximately 0.0007. The

measurecent of the fouling factor included application of uncertainties for all

measurements. The licensee stated that since flow measurement unwrtainties were

included in the fouling factor measurement it was not necessary to factor uncertainties

into the flow rate measurement in the flow balance test, in the sense that this would be

double-cccounting for the uncertainties of the flow instruments.

The team did not agree. The team noted that thermal performance testing included two

phases. Initially, the licensee used measured flows and temperatures and an estimate of

the associated measurement uncertainties to derive the heat exchanger fouling factor.

Then the licensee used the derived fouling factor, the design heat load, and the design

flow to determine whether the heat exchanger was capable of adequately cooling the

component cooling water system. The team noted that the licensee assumed in the  ;

second phase of the calculation that a design flow of 4500 gpm would be available. The

team determined that this was an analytic value and that the acceptance limits for the

flow balance test should be revised to include sufficient measurement uncertainty to

ensure this analytic assumption would be met.

10 CFR Part 50, Appendix B, Criterion XI, requires, in part, that all testing required to

demonstrate that structures, systems, and components will perform satisfactorily in

service is performed in accordance with written test procedures, which incorporate the

requirements and acceptance limits contained in applicable design documents.

As of December 18,1997, the licensee had not corrected Engineering

Procedure UNT-001-002, "ACCW & CCW System Flow Balance," Revision 14, to

incorporate an acceptance limit allowance for flow instrument uncertainty, as

necessary to ensure that the flow assumptions used in the thermal performance test

were met. The failure to include an appropriate acceptance limit in Engineering

Procedure UNT-001-002, Revision 14, is a further example of an apparent violation of

10 CFR Part 50, Appendix B, Criterion XI (50-382/9725-05).

The licensee also stated that the fouling factor margin (i.e.,0.0007 versus 0.0011)

sufficiently accounted for the flow rate deficit. The reasoning for this position was that

the 4500 gpin ACCW minimum flow was a design basis limit that was intended to be one

of two necessary conditions. A sufficient flow and low fouling factor were necessary to <

demonstrate operability of the heat exchanger. Therefore, the margin in the fouling

38

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.

factor would offset the uncertainty in the flow-rate acceptance criteria. In addition, the

licensee noted that they used a 3-sigma confidence interval to develop their

measurement uncertainties, which is mere restrictive than the 2-sigma interval, which is

usually assumed. The team acknowledged the licensee's reasoning and considered it

adequate to conclude that the CCW/ACCW heat exchanger was operable with flow rates

potentially less than design.

E8.2 (Ocen) Insoection Followuo item 50-382/9708-01: Review licensee evaluation of the

adequacy of instrument uncertainties.

Backaround - The licensee initiated long-term corrective action to use vendor guidelines

to review, evaluate, and document technical specification instrument uncertainty l

calculations and to verify that technical specification surveillance test acceptance criteria

were consistent with these instrument uncertainties. l

Insoection Followuo - The completion date for this effort was June 30,1998, but the

licensee stated that the project should be completed earlier than June 30,1998. At the

time of the inspection, the licensee estimated that the project was 80 to 85 percent

complete. A total of 10 condition repods were written to document identified

discrepancies. However, in all cases the licensee determined that the equipment

remained operable.

E8.3 (Closed) Licensee Event Reoort 50-382/97-007: Voluntary licensee event report on

refueling water storage pool level indication inaccuracies. This event was discussed '

in NRC Inspection Repoit 50-382/97-12, which identified two unresolved items:

50-382/9712-01 and -02. Further review of the event described in this licensee event

report will be tracked by these unrescived items.

E8.4 (Closed) Licensee Event Reoort 50-382/97-015: Ultimate heat sink did not

incorporate conservative assumptions. This event was discussed in NRC Inspection

Report 50-382/97-16. Discretion was granted for this design control violation in

accordance with Section Vll.B.4 of the Enforcement Policy (Reference EA 97-415).

E8.5 (Closed) Violation 50-382/9714-0j: Failure to maintain UFSAR accurate.

Backaround - In NRC Inspection Report 50-382/97-14, the NRC identified three

examples of a failure to update the licensing basis as required by 10 CFR 50.71(e).

The hT concluded that all necessary corrective actions had been initiated and

therefore concluded that no response to the violation was required. In NRC Inspection

Report 50-382/97-21, the NRC verified the completed corrective actions for two of the

examples, but held the violation open pending completion of corrective actions for

the third example, related to updating a technical specification bases section. On

October 20,1997, the licensee submitted a response to Violation 50-382/9714-01,

asking the NRC to reconsider its position that technical specification bases sections

were required to be updated pursuant to 10 CFR 50.71(e). The eensee maintained that

changes to technical specification bases sections should be controlled in accordance

with 10 CFR 50.59.

39

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insoection Followuo - On January 23,1998, the NRC agreed with the licensee's position

that technical specification bases sections were not required to be updated pursuant to

10 CFR 50.71(e), but rather should be controlled pursuant to 10 CFR 50.59. The NRC

withdrew Example 3 of the violation (EA 97-593). Since no further action is required of

the licensee, this violation is closed.

!

Note: In the January 23,1998, correspondence, the NRC stated that futher review of

Safety Evaluation 97-165 would be conducted. This review is documented in

Section E2.3. l

i

V. Manaaement Meetinas I

4

(,

X1 Exit Meeting Summary

The team met with the management of Waterford 3 Steam Electric Station on December 18,

1997, to conduct a technical debrief prior to leaving site. Following additional in-ofGee review

and telephonic discussions of the team's findings, an exit interview was conducted on

February 5,1998, by the team leader, accompanied by the acting engineering branch chief. The

team leader noted that team personnel had reviewed proprietary documentation during the

course of the inspection. Proprietary documentation was not removed from the site. The

licensee acknowledged the team's findings.

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6.TTACHMENT

SUPPLEMENTAL INFORMATION

PARTIAL LIST OF PERSONS CONTACTED

Licensas

T. Brennan, Technical Support Coordinator

C. Dugger, Vice President

E. Ewing, Director, Nuclear Safety & Regulatory Affairs

C. Fugate, Operations Shift Superintendent

T. Gaudet, Manager Licensing

P. Jackson, Supervisor, Electrical / Instrumentation and Control

D. Matthews, Licensing Specialist j

B. Randolph, Licensing Specialist l

J. Reese, Senior Engineer, Mechanical

D. Viener, Supervisor, Applied Mechanics Engineering

A. Wrape, Director, Design Engineering

NBC

J. Keeton, Resident inspector

C. Liang, Office of Nuclear Reactor Regulation  ;

T. Scarbrough, Office of Nuclear Reactor Regulation

Dr. Saba N. Saba, Office of Nuclear Reactor Regulation i

Mr. Frank Ashe, Office of Nuclear Reactor Regulation ]

INSPECTION PROCEDURES USED

37001 10 CFR 50.59 Safety Evaluations

37550 Engineering

92903 Followup - Engineering

93809 Safety System Engineering Inspection (SSEI) 4

ITEMS OPENED, CLOSED, AND DISCUSSED

1

Ooened

50-382/9725-01 URI HPSI and CS NPSH margin inaccurately stated in UFSAR

(Section E1.1).

1

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.

50-382/9725-02 URI Inadequate containment floodir;g calculations resu t in

nonqualified instrumentation (Section E1.1).

50 382/9725-03 URI Main feedwater isolation valve operability questioned

(Section E1.2).

50-382/9725-04 VIO Failure to follow condition reporting procedures as required by

10 CFR Part 50, Appendix B, Criterion V (Section E1.2).

50-382/9725-05 APV Apparent failure to specify sufficiently accurate test

instrumentation, and to consider valve position variability and

measurement uncertainty when establishing test acceptance

criteria as required by 10 CFR Part 50, Appendix B Criterion

XI (Sections E2.2 and E8.1).

50-382/9725-06 APV Apparent failure to assess the affect of lower than assumed

HPSI flow on peak clad temperature as required by 10 CFR

50.46(a)(3)(i) (Section E2.2).

50-382/9725-07 APV Apparent failure to report operation outside of design basis of

facility and apparent failure to submit schedule for

performarce of a new ECCS analysis as required by

10 CFR 50.46(a)(3)(ii) (Section E2.2).

50-382/9725-08 APV Apparent failure to promptly correct HPSI flow balance test to

account for instrument uncertainty as required by l

10 CFR Part 50, Appendix B, Criterion XVI (Section E2.2).

50-382/9725-09 APV Apparent failure to perform written safety evaluation for a

change to LOCA EOP as required by 10 CFR 50.59(b)(1)

(Section E2.2).

50-382/9725-10 APV Prior NRC approval was not obtained for three changes,

which appareatly involved unreviewed safety questions, as

required by 10 CFR 50.59(a)(1) (Section E2.3).

50-382/9725-11 !FI Evaluation of possible adverse configuration control trend

(Section E7.1).

Closed i

50-382/96202-01 IFl CCW and ACCW instrument uncertainties not adequately

accounted for in the evaluation of test results (Section E8.1). l

50-382/97-007 LER Voluntary LER on RWSP level indication inaccuracies l

(Section E8.3).  !

!

50 JB2/97-015 LER Ultimate Heat Sink design basis did not include conservative

assumptions (Section E8.4).

50-382/9714-01 VIO Failure to accurately maintain the UFSAR (Section E8.5).

2 ]

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D?scussed

50-382/9708-01 IFl Review licensee's evaluation of the adequacy of instrument

uncertainties (Section E8.2).

LIST OF ACRONYMS USED

ACCW auxiliary component cooling water

APV apparent violation

CCW component cooling water

CFR Code of Federal Regulations

CS containment spray

CIAS containment isolation actuation signal

~ CIV containment isolation valve

ECCS emergency core cooling system

EFW emergency feedwater

EOP emergency operating procedure

EPRI Electric Power Research Institute

FCV flow control valve

gpm gallons per minute

, HPSI high pressure safety injection

IFl inspection followup item

1

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LDCR licensing document change request

LER licensee event report  !

LOCA loss-of-coolant accident

LPSI low pressure safety injection

NPSH net positive suction head

OEEE operational experience engineering evaluation

PCT peak clad temperature

psi pounds per square inch

psig pounds per square inch gage

3

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..

psia pounds per square inch absolute

QSPDS qualified safety parameter display system

RAS recirculation actuation signal

RWSP refueling water storage pool

SBLOCA small break loss-of-coolant accident

SSEI safety system engineering inspection

TS Technical Specification

UFSAR Updated Final Safety Analysis Report

URI unresolved item

USQ uraeviewed safety question

V de volts direct current

VIO - violation

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,

DOCUMENTS REVIEWED

SAFETY EVALUATIONS

NUMBER DESCRIPTION REVISION

SF.-97-006 DC-3440 - HPSI Flow Control Valve Replacement Revision 0

LDC-98-0032 - Hydrogen Recombiner Analyzer November 28,1997

Containment Isolation Valve Evaluation

SE-97-005 UFSAR Soction 11.2.2.1, Boron Management January 24,1997

System

SE-97-149 LDC 97-0194 - Containment Atmosphere Release June 26,1997

System

SE-97-165 EFW Minimum Flow Requirement EC-S97-016 July 16,1997

SE-97-0115 UFSAR, Section 9.5.1 May 26,1997

SE-97-0119 LDC 97-0170, FSAR, Section 9.5.1 May 28,1997

SE-97-002 DC-3483 - LPSI Minimum Flow Recirculation Line Revision 0

Check Valve Replacement

SE-97-073 DC-3498 - HPSI Flow Control Valve Position Revision 0

Indications 1

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.

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SAFETY EVALUATIONS

NUMBER DESCRIPTION REVISION  !

DC-3528-0 RWSP LevelIndication May 9,1997

SE-9~7-038 FSAR Section 9.5.1 And Table 9.5.1-1 March 31,1997

SE-97-156 Calculation MN (Q)-9-46 July 3,1997 .

!

SE-97-087 STP For Shutdown Cooiing Flow Control Valve - April 17,1997 l

WA#01158897

SE-97-025 Adding Trisodium Phosphate Baskets for SIS Sump February 19,1997

i

SCREENING REVIEWS

NUMBER DESCRIPTION REVISION

OP-100-014 Technical Specification and Technical Requirements Ravision 7

Compliance

HP-001-150 Use of Protective Clothing Revision 9

OP-903-110 RAB Fluid Systems Leak Test Revision 2

W1.109 Project Management Standards and Expectation September 23,1997

Policy

SSP-801 Materials Technical Department Training Program for Revision 0 <

Engineers and Technical Specialists

l

OP-902-002 Loss of Coolant Accident Recovery Procedure July 5,1997

CONDITION REPORTS

NUMBER- DESCRIPTION REVISION

CR 97-1288 Plant equipment configuration did not match design Revision 0

documents

CR-97-1675 Refueling water s+orage pool nozzle strainers were Revision 0

not installed in accordance with drawing

CR-94-0761 Four systems walked down to address drawing Revision 0

errors

CR-97-1158 Seismic supports for safety-related solenoid valve Revision 0

condulets were not installed per instructions

5

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CONDITION REPORTS I

NUMBER DESCRIPTION REVISION '

CR-96-0538 Operator work arounds identified Revision 0

CR-97-0861 Licensee assessment identified a number of valves Revision 0 I

which were preconditioned

CR-97-0852 Valves exceeded their inservice test stroke time Revision 0

CR-97-24SO Low pressure safety injection pump B suction Revision 0

pressure gauge was found to be over ranged

CR-97-2460 Low pressure safety injection pump B suction Revision 0

pressure indicator was pegged high

CR-97-1240 Safety injection tank was not declared inoperable Revision 0

during repressurizing the tank with nitrogen with the

tank connected to a nonsafety nitrogen header

CR-97-1687 The gasket in the safety injection tank top manway Revision 0

flange did not meet accepted industry practices

CR-97-1895 ' While performing the safety injection pump Revision 0

operability test, the safety injaction tank 2A nitrogen

pressure began dropping

CR-97-1913 Safety injection check valve was found leaking Revision 0

during testing

CR-97-0930 Penetration 59 failed local leak rate testing Revision 0

CR-97-1452 Plant procedure required verification of minimura Revision 0

high pressure safety injection flow. However, gages

were inadequate to measure the low flow

CR-97-1030 The snubber on the 10-inch low pressure safety Revision 0

injection pump discharge line was found frozen

~ CR-97-1206 A concern was raised that penetrations connected to Revision 0

closed water filled systems outside of containment

could leak if piping outside the containment valve

was drained

- CR-97-2048 During testing the as-found set pressure of a relief Revision 0

valve exceeded the high set pressure tolerance

CR-97-2390 . During testing, the low pressure safety injection Revision 0

pump A differential pressure exceeded the alert limit

CR-97-1993 Investigate and document the cause of the charging Revision 0

pump B abnormal noise

6

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._ .__ __ _ _________-_____ ____________ _ ___ ___ - - - _ -

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CONDITION REPORTS

NUMBER DESCRIPTION REVISION

CR-97-0853 Pressure in the line between valves CS-1178 and Revision 0

CS-125B exceeded the design pressure by 100 psig

CR-97-1185 Diesel Generator jacket water heater supports have Revision 0

oversized mounting bolt holes that were not shown

on drawing

CR-96-1087 Broken Diaphragms on Air-Operated Valves July 17,1996

CR-96-1155 Hydraulic Pump Running Continuously July 26,1996

CR-97-0220 Damaged Valve Operator January 29,1997

CR-97-0408 Motor-Operated Valve Pinion Key Not Properly Set, February 22,1997

Lack of Grease in Clutch Housing

CR-97-0632 FSAR Discrepancy Regarding AOV Air Filters March 18,1997

CR-97-0982 Bevel Gear Broken on Limitorque Actuator April 23,1997

CR-97-0806 Waterford 3 Condition Report April 8,1997

CR-97-2695 HPSI Flow Loop Uncertainty December 5,1997

CR-97-0649 LPSI Flow Loop Uncertainty March 19,1997

CR 96-0382 EFW Flow Loop Uncertainty March 15,1996

CR-96-0414 Minimum Acceptable Pump Differential Pressure at October 2,1956

the 'nservice Test Flow Rate

CR-95-1126 SlT transmitter static pressure thift input was Revision 0

incorrect

CR-96-1965 Ultrasonic examination of low pressure safety Revision 0

injection piping

CR-96-0671 While performing quarterly check of locked valves Revision 0

per OP-100-009, CHW-152 was found out of position

CR-97-0632 No in line or point of use filters in safety-related air Revision 0

operated valves

CR-97-0806 Review of design basis calculations revealed Revision 0

inconsistencies in Si and CS pumps runout flowrates

CR-96-0516 Root Cause Analysis Report - Recurring Electrical Revision 0

Grounds During Heavy Rainfall

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ENGINEERING RECiUESTS ,

NUMBER DESCRIPTION - REVISION

ER-W3-96-0046 . Operability determination input for SI-405A and Revision 0 .

S-405B

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ER-W3-97-0144 - Emergency diesel generator not per drawing Revision 1

~ KSV-58-4

ER-W3-97-0560 Evaluation of new low pressure safety injection pump Revision 0

B baseline data

ER-W3-97-0417 Design basis operating parameter review Revisiv b

ER-W3-97-0400 Containment spray pump seal sleeve needs to be Revision 0

modified in order to prevent shaft to sleeve leakage

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ER-W3-97-0265 Evaluate possible trend of thermal overload relays Revision 0 I

due to aging  ;

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ER-W3-97-0010 Flow control valve flow rate determination Revision 0

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ER W3-97-0109 Freeze seat evaluation for repacking SI-506A Revision 0

ER-W3-97-0117 Low pressure safety injection pump conduit support Revision 0

ER-W3-97-0130 Sl MVAAA109A valve has seat leakage and is Revision 0

welded into a 20 inch line

ER-W3-97-0247 DC-3536 acceptance test 50.59 support Revision 0

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ER-W3-97-0197 input for Procedure OP-903-001 Revision 0

ER-W3-97-0384 Increased frequency removal justification for high Revision 0 .

pressure safety injection pump B l

ER-W3-97-0067 Lock washers interfere with the flange welds for the Revision 0 l

Target Rock valves  !

ER-W3-97-0081 Wall thinning on drain line due to flow accelerated Revision 0 j

corrosion

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ER-W3-97-0178 Seismic analysis of piping connected to the Revision 0

emergency feedwater terry turbine steam traps

ER-W3-97-0203 P.ipe rusting on discharge structure Revision 0

ER-W3-97-0467 Evaluation of air flow rates measured while Revision 0

perforrning STP-011160647

ER-W3-97-0455 Control room emergency outside air intake linear Revision 0

scale flow indicators requirement to a sequence root

extractor card

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ENGINEERING REQUESTS

NUMBER DESCRIPTION REVISION

ER W3-97-M007 Effect on emergency diesel generator fuel oil storage Revision 0

' tank level due vortexing

ER-W3-97-0562. Charging pum'p B unusual noise Revision 0

ER-W3-97-0430 Overpressure a cfass 2 header respon.e in opening Revision 0

high pressure safety injection flow control valves

ER-W3-97-0395 Verification that the safety injection system is full of Revision 0

water

ER-W3-97-0313 Shut down cooling heat exchanger outlet stop check Revision 0

valve leaks past its seat

ER-W3 97-0128 Colli pring fit up of discharge header relief valve tail Revision 0 j

piece

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ER-W3-97-M001 Evaluation of reactor coolant system drain down Revision 0 '

procedure with one shut down cooling pump

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operating at 4000 gpm

ER-W3-97-0101 Request to use damaged stem for CS-125B May 2,1997

ER-W3-97-0202 SI-205AB Rejected inspection of Shaft May 28,1997

ER-W3-97-0100 Sl MVAAA225 A overthrust condition May 1,1997

ER-W3-98-0134 Qualified life of safety-related batteries February 17,1998

ER W3-97-0263 RWSP maximum level and containment flooding June 27,1997

ER-W3-97-0601 Safety flow curves November 18,1997

ER-W3-97-0390 Instrument accuracy fcr inservice testing September 5,1997

PROCEDURES l

NUMBER- DESCR!PTION REVISION

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W2.501. Corrective Action Revision 6  !

W4.104 Engineering Request Process Revision 0 l

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OP-903-030 Surveillance Procedure - Safety injection Pump Revision 11

Operability Verification

OP-903-108 Surveillance Procedure - Safety injection Flow Revision 4

Balance Test

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PROCEDURES

NUMBER . DESCRIPTION REVISION

UNT-006-021 Pump and Valve inservice Testing Revision 3

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NOECP-258 Control of Waterford 3 Purap and Valve Inservice Revision 0

Test Program

OP-903-010 Surveillance Procedure - ECC System Throttle Revision 5

Valves Position Verification

- OP-903-108 Surveillance Procedure - SI Flow Balance Test Revision 3

ME-007-008 Maintenance Procedure - Motor Operated Valve Revision 10

UNT-006-021 Administrative Procedure - Pump and Valve' Revision 3

Inservice Testing

OP 903-030 - Surveillance Procedure - Safety injection Pump Revision 11

-Operability Verification

OP-902-002 Loss of Coolant Accident Recovery Procedure Revision 7

OP-902-ATT Attachment 5, Minimum HPSI Flow Versus Revision 4

Pressurizer Pressure

OP-902-002 Loss of Coolant Accident Recovery Procedure Revision 7

OP-902-ATT Attachment 5, Minimum HPSI Flow Versus Revision 4

Pressurizer Pressure

OP-902-ATT Attachment 6, Minimum LPSI Flow Versus - Revision 4

Pressurizer Pressure

OP-903-001 Technical Specification Surveillance Logs Revision 19

OP-903-011 High Pressure Safety injection Pump Preservice Revision 8

Operability Check

OP-903-025 Safety injection Tanks and Shutdown Cooling Revision 3

System interlock Verification

OP-903-026 Emergency Core Cooling System Valve Lineup Revision 8

Verification

OP-903-027 Inspection of Containment Revision 5

' OP-903-029 Safety injection Actuation Signal Test Revision 7

OP-903-030 Safety injection Pump Operability Verification Revision 11

OP-903 091 Recirculation Actuation Signal Test Revision 3

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PROCEDURES I

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NUMBER DESCRIPTION REVISION

OP-903-108 Si Flow Balance Test Revision 3

OP-903-121 Safety Systems Quarterly IST Valve Tests Revision 2

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CE-002-100 Chemistry Technical Specification Revision 10

CE-003-163 Testing of Safety injection Sump Trisodium Revision 0

Phosphate i

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CE-003-121 Boron Determination (Autotitration Method) Revision 7

CE-003-122 Determination of Boron (Titration Method) Revision 5

Ml-003-317 Refueling Water Storage Pool Level Loop Check and Revision 6

Calibration  ;

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CALCULATIONS

NUMBER DESCRIPTION REVISION

EC-M95-004 Dynamic, Seating, and Unseating Torque Revision 0

Requirements for Air Operated Valves CC-963A,8

EC-M91-076 SI-405A(B) Actuator Thrust Calculation Revision 2

EC-M91-060 Evaluation of Fisher 9200 Series Butterfly Valves Revision 0

with Fisher Actuators

EC-M89-003 Switchgear Room 3A Heat Load at the inception of Revision 4

SBO

EC-M89-089 Waterford 3 Design Engineering General Revision 5

Computation Sheet

MN(Q)-6-4 Water Level Inside Containment Revision 0 '

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MN(Q)-6-19 Level of Water inside Containment Revision 1

MN(Q)-6-27 NPSH Calculation (HPSI and CS Pumps) Revision 2

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MN(Q)-6-1 NPSH Calculation {This is for HPSI} Revision 2

MN(Q)-6-43 LPSI Pump Minimum NPSH Revision 0

MN(Q)-6-2 Safety injection System {HPSI flow dP) Revision 1 ,

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MN(Q)-6-42 Head Available on Low Pressure Safety injection Revision 0 - Change 1

Pump Minimum Flow Recirculation l

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CALCULATlONS '-

NUMBER DESCRIPTION REVISION

' 612752 - MPS-~ Safety injection System: HPSI Technical Revision 0

5 Calc 001 Specification Development Based on Analysis of

. Rewoted B Pump

EC-M95-010 ~ _ Stem Thrust / Torque Analysis of the Motor Operated Revision 0 - Change 2 -

Globo Valve (Assembly Number 716-002, Report

No 44951)

- HVAC-070 . Hydrogen Generation Gy Station Batteries Revision 1

. HVAC-059 ' Battery Room Air Flow Required to Limit Hydrogen Revision 1

Concen' ration to 1%

F_C-S96-604 Cycle 9 Safety Analys!s_ Ground rules Revision 2

EC-10S-011 SI-HPSI Flow instrumentation Loop Uncertainty Revisions 0 and 1

Calculation

EC 191-052 LPSI Header Flow A & B instrumentation Loop Revisions 0 and 1

Uncertainty Calculation

J-PEC-24 Sizing of HP & LP Safety injection Pump Rewsion 0

DESIGN CHANGES

NUMBER DESCRIPTION REVISION

DCP-3440 High Pressure Safety injection Flow Control Valve Revision 0

Replacement

DCP-3483 Low Pressure Safety injection Pump Minimum Flow Revision 0

Recirculation Line: Check Valve Replacement

DC- 3498 ECCS Flow Control Valve Remote Position Revision 0

Indication Replacement

LICENSING DOCUMENT CHANGE REQUESTS

NUMBER DESCRIPTION REVISION

LDC 97-0176 Revise UFSAR Section 8.0 to address battery Revision 0

upgrade

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CISCELLANEOUS DOCUMENTS

NUMBER DESCRIPTION REVISION

C-PEC-262 Safety injection System: HPSI Technical Revision 0 l

Specification Development and HPSI Restart Data

Analysis

NPF-38107 Technical Specification Change Request February 12,1990

GQRT File E-5 3A-S and 38-S Battery Seismic Reports

Seism;c Simulation Test Program on Four C&D September 7,1993

Power Systems LCUN-33 Battery Cells for Pacific

Gas & Electric Company

DES-E-008 Procurement Specification: Class 1E Emergency August 18,1992

Batteries

TM 457002689 Technical Manual: UPS Elgar Model 103-1-151

Wtfrd3.98.1 Leiter from ELGAR to Entergy Operatlons: Operation February 4,1998

of UPS 103-1-151

W3-DBD-008 Electrical Distribution (DC Portion) Design Basis February 28,1996 1

Document

NUMARC 8700 Guidelines and Technical Bases for NUMARC Revision 1

Initiatives

W3P89-0510 Letter from Louisiana Power & Light to U.S. Nuclear April 14,1989

Regulatory Commission

System Review Self-Assessment - HPSI July 16,1996

Letter from Combustion Engineering to Louisiana November 17,1989

Power & Light Co: High Pressure Safety injection

Pump "B" Pump Operating Condition

Letter from Combustion Engineering to Louisiana December 1,1989

Power & Light Co: High Pressure Safety injection

System Technical Specification Values

Letter from Combustion Engineering to Louisiana February 27,1984

Power & Light Co: Option No. NOL-63, Plant Specific

Inforrnation for Emergency Procedure Guidelines

DBD-C01 Waterford 3 Design Basis Document " Safety Revision 2

Injecticn System,"

Cl-290132 SI Flow Balance Test March 18,1994

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CISCELLANEOUS DOCUMENTS

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. NUMBER DESCRIPTION REVISION l

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PEIR-OM-68 ' HPSI/LPSI Flow Control Valve Remote Position June 22,1994 I

Indication Problem

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