ML20214J019
ML20214J019 | |
Person / Time | |
---|---|
Site: | Diablo Canyon |
Issue date: | 04/30/1987 |
From: | Hug M, Keller A, Thornberry R PACIFIC GAS & ELECTRIC CO. |
To: | NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM) |
References | |
NUDOCS 8705270595 | |
Download: ML20214J019 (9) | |
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MONTHLY NARRATIVE REPORT OF OPERATION !
AND MAJOR MAINTENANCE EXPERIENCE Th'is report describes the operating and major maintenance experience for
! the month of April, 1987. This narrative report was prepared by the
- plant staff and is submitted in accordance with Section 6.9.1.7 of the Units 1 and 2 Technical Specifications.
On April 1, 1987 Unit 1 started the month at 100% power.
Unit 2 started the month at 100% power.
4 0n April 3, 1987 Unit'2 decreased power to 78%'to reduce chlorides due to leaking condenser tubes.
Unit 2 experienced a turbine generator trip due to antimotoring relay actuation and subsequent reactor trip while operators were shutting down the unit in
> preparation for a. refueling outage.
On April 5,-1987 Unit 2 entered Mode 4 and then Mode-5.
2 On April 10, 1987 Unit 2 residual heat removal flow was interrupted for 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and'28 minutes. The reactor coolant j system (RCS) had_just been drained to mid-loop
! level to-facilitate removal of steam generator l
primary manways and subsequent nozzle dam i installation. In addition, preparation for a local i' leak rate test on containment isolation valves was in progress (including draining the penetration).
! Due to leaking valves in the penetration being i drained, RCS inventory was lost to the_ reactor i coolant drain tank. Loss of inventory caused a y decrease in RCS water level and resulted'in air 4
entrainment in the operating RHR pump because of vortexing in the pump suction line. The RHR pump was manually tripped.-After verifying that the steam generator manways were still installed'and after venting the RHR pumps, RCS was flooded from the RWST and a RHR pump was' restarted. This event resulted in some localized boiling but no damage to the core or significant radiological release.
i on April-14, 1987 Unit 2 entered Mode-6.
- On April 21, 1987 Unit 2 reactor head removed in preparation for
, refueling.
On April 22, 2987 On-site biologists made a preliminary determination that approximately 68 pcinds of ferric sulfate
- inadvertently discharged from the Seawater Reverse Osmosis Facility to the intake cove on April 21, 1987, had an environmental impact. Based on this result a Non-emergency Four Hour Report report was 5
8705270595 870430 G' PDR ADOCK 05000275 R ppg _ ll}
l made in accordance with 10CFR50.72.(b)(2)(vi).
Commenced removing fuel from Unit 2 reactor.
- on April 28, 1987 Completed Unit 2 reactor core offload. Exited mode
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6.
On April 30, 1987 Unit 1 ended the month at full power. Unit 2 ended the month shut down for a refueling outage.
Unit l~ operated this month with a unit availability factor of 100% and a unit capacity factor of 100%.
Unit 2 operated this month with a unit availability factor of.10.0%.and
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a unit. capacity factor of 7.0%. Unit 2 reduced power once this month to '
reduce' chlorides due to leaking condenser tubes. Unit 2 tripped once this month due to antimotoring relay actuation with subsequent turbine trip - reactor trip while operators were shutting down the unit in preparation for a refueling outage. The reactor remained shutdown for ,
the Unit 2 refueling' outage.
Significant safety related maintenance consisted'of Unit 2 reactor head removal and core offload, Unit 2 testing of safety valves to verify set points and repairs to plant vent radiation monitor.
During the-April 3, 1987 Unit 2 reactor trip, loop 4 atmospheric steam dump valve PCV-22 did not open when steam generator pressure exceeded its lift setpoint which subsequently caused a loop 4 main steam line code safety valve actuation. No other challenges to the steam generator safety valves or pressurizer power operated relief valves were made.
l No major changes to the radwaste treatment-systems as required by l
Technical Specification 6.15.1 were made.
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OPERATING DATA REPORT DOCKET NO. 50-275 DATE 05/06/87 COMPLETED BY A.T. Keller TELEPHONE (805)S95-7351 OPERATING STATUS
- 1. Unit Name: Diablo Canyon Unit 1
- 2. Reporting Period: April 1987
- 3. Licensed Thermal Power (W t): 3338
- 4. Nameplate Rating (Gross We): 1137
- 5. Design Electrical Rating (Net W e): 1086
- 6. Maximum Dependable Capacity (Gross MWe): 1125
- 7. Maximum Dependable Capacity (Net MWe): 1073
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report.
Give Reasons:
N/A
- 9. Power Level To Which Restricted. If Any (Net MWe): N/A
- 10. Reasons For Restrictions, If Any: None This Month Yr-to-Date Cumulative *
- 11. Hours In Reporting Period 719.0 2879.0 17373.3
- 12. Number Of Hours Reactor Was Critical 719.0 2732.0 13997.6
- 13. Reactor Reserve Shutdown Hours 0.0 0.0 0.0
- 14. Hours Generator On-Line 719.0 2670.4 13635.8
- 15. Unit Reserve Shutdown Hours 0.0 0.0 0.0
- 16. Gross Thermal Energy Generated (WH) 2394500 7841891 41383961
- 17. Gross Electrical Energy Generated (MWH) 814300 _2636000 13769732
- 18. Net Electrical Energy Generated (MWH) 777186 2494066 13021887
- 19. Unit Service Factor 100.0 92.8 78.5
- 20. Unit Availability Factor 100.0 92.8 78. 5 _ _
- 21. Unit Capacity factor (Using MDC Net) 100.7 80.7 69.9
- 22. Unit Capacity Factor (Using DER Net) 99.5 79.8__ 69.0
- 23. Unit Forced Outage Rate 0.0 7.2 5.5
- 24. Shutdowns Scheduled Over Next 6 Months (Type. Date, and Duration of Each):
N/A
- 25. If Shut Down At End Of Report Period. Est. Date of Startup: N/A
- As of commercial operation on 5-7-85 at 0243.
M0.RPT
OPERATING DATA REPORT DOCKET NO. 50-323 DATE 05/06/87 COMPLETED BY A.T. Keller TELEPHONE (805)S95-7351 OPERATING STATUS
- 1. Unit Name: Diablo Canyon Unit 2
- 2. Reporting Period: April 1%7
- 3. Licensed Thermal Power (W t): 3411
- 4. Nameplate Rating (Gross We): 1164
- 5. Design Electrical Rating (Net We): 1119
- 6. Maximum Dependable Capacity (Gross MWe): 1130
- 7. Maximum Dependable Capacity (Net MWe): 1079
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report.
Give Reasons:
N/A
- 9. PowerLevelToWhichRestricted.IfAny(NetMWe): N/A
- 10. Reasons For Restrictions If Any: None This Month Yr-to-Date Cumulative *
- 11. Hours In Reporting Period 719.0 2879.0 9932.0
- 12. Number Of Hours Reactor Was Critical 71.9 2133.2 8990.1
- 13. Reactor Reserve Shutdown Hours 0.0 0.0 0.0
- 14. Hours Generator On-Line 71.9 1911.1 8641.5
- 15. Unit Reserve Shutdown Hours 0.0 0.0 0.0
- 16. Gross Thermal Energy Generated (WH) 190948 5978045 27058764
- 17. Gross Electrical Energy Generated (MWH) 62400 1972100 8884599
- 18. Net Electrical Energy Generated (MWH) 54034 1851218 8399392
- 19. Unit Service factor 10.0 66.4 87.0
- 20. Unit Availability Factor 10.0 66.4 87.0
- 21. Unit Capacity Factor (Using MDC Net) 7.0 59.6 78.4
- 22. Unit Capacity factor (Using DER Net) 6.7 57.5 75.6
- 23. Unit Forced Outage Rate 0.0 14.9 7.0
- 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
Refueling Outage. April 3, 1987. 70 days
- 25. If Shut Down At End Of Report Period Est. Date of Startup: June 16. 1987
- As of consercial operation on March 13, 1986 at 0300 PST.
M0.RPT
AVERAGE DAILY UNIT POWER LEVEL DOCKET N0. 50-275 UNIT Diablo Canyon Unit 1 DATE 05/06/87
. COMPLETED BY A.T. Keller TELEPHONE (805)595-7351 MONTH April 1987 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (We-Net) (We-Net) 1 1083 17 1088 j
2 1087 18 1088 3 1081 19 1071 4 1076 20 1088 5 1012 21 1092 6 1074 22 1076 7 1074 23 1088 8 1071 24 1092 9 1079 25 1080 10 1081 26 1079 11 1085 27 1088 i 12 1077 28 1076 _
13 1081 29 1080 14 1082 30 1084 15 1082 16 1090 INSTRUCTIONS On this format, list the average daily unit power level in We-Net for each day in the reporting month. Compute to the nearest whole megawatt.
The Average Monthly Electrical Power Level for April, 1987 = 1079.42 We-Net.
M0.RPT
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-323 UNIT Diablo Cartyon Unit 2 DATE __ 05/06/87 COMPLETED BY- A.T. Keller TELEPHONE (805)S95-7351 MONTH April 1987 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (We-Net) (We-Net) 1 855 17 -6 2 856 18 -6 3 733 19 -6 4 -38 20 -6 5 -19 21 -6 6 -10 22 -6 7 -9 23 -7 8 -8 24 -7 9 -5 25 -7 10 -3 26 -6 11 -3 27 -6 12 -3 28 -5 13 -3 29 -5 14 -3 30 -5 15 -3 16 -3 INSTRUCTIONS On this format, list the average daily unit power level in We-Net for each de in the reporting month. Compute to the nearest whole megawatt.
The Average Monthly Electrical Power Level for April, 1987 = 75.05 W e-Net.
M0.RPT
UNIT SHUTDOWNS Page 1 ef 1 DOCKET NO. 50-275 .
UNIT NAME Diablo Canyon Unit 1 +
DATE 05/06/87 i COMPLETED BY M.T. HUG REPORT MONTH APRIL 1987 TELEPHONE (805)S95-7351 Duration Method of System Component Ac i o 2 4 5 No. Date Type l (Hours) Reason Shutdown3 Report # Code Code Prevent Recurrence None a
.i 4
1 2 3 4 F: Forced Reason: Method: Exhibit G - Instructions S: Scheduled A-Equipment failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (LER) File D-Regulatory Restriction 4-Continuation from (NUREG-1022)
E-Operator Training & License Examination previous month F-Administrative 5-Power reduction 5 ,
G-Operational Error (Explain) 6,7,8-N/A Exhibit I - Same Source H-Other (Explain) 9-Other MD.RPT
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UNIT SHUTDOWNS -
Page 1 of 1 DOCKET NO. 50-323 -
UNIT NAME Diab 17 Canyon Unit 2 .
DATE 05/06/87 COMPLETED BY M.T. HUG REPORT MONTH APRIL 1987 TELEPHONE (805)S95-7351 Ucensee System Component "S' '
- I'*
Duration Method of Event Action to 2 4 Shutdown3 S
No. Date Type l (Hours) Reason Report # Code Code Prevent Recurrence el 04/03/87 F 647.1 G 3 2-87-004-00 TA TRB Unit 2 experienced a turbine generator trip at 12% reactor power when differential pressure switch PS-30 reached its setpoint and caused antimotoring relay actuation and subsequent reactor trip while operators were shutting down the unit in preparation for a refueling outage.
Approximately 23 seconds after the reactor trip, a safety injection occurred on high steam flow signal coincident with low-low Tavg.
Operators were unaware of the antimotoring relay actuation.
Providing annunciation of this relay actuation as well as reducing the
, setpoint is being considered.
- Since this reactor trip occurred during the scheduled shutdown there was no attempt to restart the reactor.
I 2 3 4 F: Forced Reason: Method: Exhibit G - Instructions S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (LER) File D-Regulatory Restriction 4-Continuation from (NUREG-1022)
E-Operator Training & License Examination previous month F-Administrative 5-Power reduction 5 G-Operational Error (Explain) 6,7,8-N/A Exhibit I - Same Source H-Other (Explain) 9-Other MO.RPT
PACIFIC GAS AND E LE C T RI C C O M PANY DIABLO CANYON POWER PLANT
[gllglllllj + PO. Box 56. Avila Beach, Cahfornia 93424 (805) 595 7351 m_ _ _ _ ,
R C. THORNBERRY PLAP47 MANAGER i
May 15,1987 U.S. Nuclear Regulatory Comission Attn: Document Control Desk
! Washington, DC 20555 RE: Docket No. 50-275 and 50-323 License No. OPR-80 and DPR-82 Monthly Operating Report for April, 1987 Gentlemen:
Enclosed are the completed monthly operating report forms for Diablo Canyon Units 1 and 2 for April, 1987. This report is submitted in accordance with Section 6.9.1.7 of the Units 1 and 2 Technical Specifications.
Sincerely, l
eeT W ROBERT C. Ti10RNBERRY h RCT:lm Enclosures I
cc Mr. John B. Martin, Regional Administrator Region V - USNRC l
l M0.RP1