ML20153D431

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Insp Rept 50-382/88-19 on 880618-0731.Violations Noted. Major Areas Inspected:Enforcement Followup on Quality Verification Function Insp,Monthly Maint Observation, Allegation Followup & Operational Safety Verification
ML20153D431
Person / Time
Site: Waterford Entergy icon.png
Issue date: 08/19/1988
From: Chamberlain D, Michaud P, Will Smith, Staker T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20153D424 List:
References
50-382-88-19, IEB-88-005, IEB-88-5, NUDOCS 8809020201
Download: ML20153D431 (19)


See also: IR 05000382/1988019

Text

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e -, U. S. NUCLEAR REGULATORY COMISSION ' , .4 REGION IV

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                     NRC Inspection Report:        50-382/88-19                 License: 'NPF-38

I' Docket: 50-382 .

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                     Licensee: Louisiana Power & Light Company (LP&L)                        ,                   .

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                                   142 Delaronde Street
                                   New Orleans, Louisiana        70174                         ,
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                     Facility Name: Waterford Steam Electric Station, Unit 3
                     Inspection At:      Taft:    Louisiana
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                     Inspection Conducted:        June 18 through July 31, 1988                                          <
                     Inspectors:                    .-                                                 8     &
                                     W. F. Smith, Senior Resident Inspector                            Date
                                                                                                       7-1-6s
                                     T. R. St4ke?,      lesident Inspector                             Date
                                                 We                                                    7-2 2 -28
                                     P. W. Michaud, Res'i ant Inspector, Region IV                     Date
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                     Approved:         C               ,                                               &llT/00
                                     D. D/LTainberlain, Chief, Project Section A                       Date              !
                                      Division of Reactor Projects
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                Inspection Summary
                Inspection Conducted June 18 through July 31, 1988 (Report 50-382/88-19)
                Areas Inspected:                      Routine, unannounced inspection consisting of:
                TI) enforcement followup on quality verification function inspection,
                (2) monthly maintenance observation, (3) allegation followup, (4) operational
                safety verification, (5) monthly surveillance observation, (6) followup of
                previously identified items, (7) followup of NRC Bulletin 88-05, (8) licensee
                event report followup (9) onsite followup of events, and (10) plant status.
                Results:
                Within the areas inspected, four violations were identified.                      The first
                violation involved four failures to submit Licensee Event Reports within the                  I
                30 days required by 10 CFR 50.73 (paragraph 2). The second and third
                violations involved failures to follow operating and maintenance procedures
                respectively (paragraphs 2 & 3). The fourth violation involved failure to                     .
                perform s)ecial processes using appropriately qualified personnel
                (paragrapi4). There is one new unresolved item in paragraph 3 regarding the
                possibility of unacceptable delays in correcting undersized power cables.
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                                               DETAILS
      1.   Persons Contacted
           Principal Licensee Employees
            R. P. Barkhurst, Vice President. Nuclear Operations
           *N. S. Carns., Plant Manager,' Nuclear
            P. V. Prasankumar, Assistant Plant Manager, Technical Support
            D. F. Packer, Assistant Plant Manager, Operations and Maintenance
            J. J. Zabritski,flanager of Operations Quality Assurance
            J. R. McGaha, Manager of Nuclear Operations Engineering
            W. T. Labonte, Radiation Protection Superintendent
            D. E. Baker, Manager of Nuclear Operations' Support and Assessments
           *A. L. Holder, Fire Protection and Safety Department itead
           *L. W. Laughlin, Site Licensing Support Supervisor
            D. W. Vinci, Maintenance Superintendent
           *N. E. Howard, Trending Compliance & Response Supervisor
            A. F. Burski, Manager of Nuclear Safety and Regulatory Affairs
            R. S. Starkey, Operations Superintendent
            G. M. Woodard, Manager of Events Analysis Reporting & Responses
            J. Sleger, Jr. , Nuclear Safety Review Manager
           *Present at exit uterview.
           In addition to the above personnel, the NRC inspectors held discussions
           with various operations, engineering, technical su) port, maintenance,
           quality assurance, and administrative members of t1e licensee's staff.
      2.   Enforcement Followup on Quality Verification Function Inspection (25578)
           During the period of February 1 through February 12, 1988, the NRC staff
           conducted NRC headquarters-directed quality verification function
           inspections under the guidance of Temporary Instruction 2515/78. The
           Inspection Report (50-382/88-200) was issued on June 2, 1988. Enclosure 1
           of the report identified several potential enforcement findings. The NRC
           Region IV staff has the responsibility to issue the appropriate Notices of
           Violation for items requiring enforcement action. The items are listed
           below:
           a.     Item 1.a:   Failure to report a valid actuation of the broad range
                  toxicgasdetectionsystempursuantto10CFR50'3(a)(2)(iii),which
                  requires a 30-day report when an external condition poses a threat to
                  the safety of the nuclear power plant or significantly hampers site
                  personnel. Neither of these criteria were met when the actuation
                  occurred, therefore, the Region IV staff determined the item did not
                  have to be reported, There will be no enforcement action on this
                  item.
           b.     Item 1.b: Failure to report being outside of the design basis of the
                  plant due to nitrogen pressure indicator taps being located on the

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          Main Steam Isolation Valves (MSIVs) such that pressure could not be
          monitored when the MSIVs were open.     The Region IV staff considered
          the licensee correct in not reporting this condition because the
          design basis of the installation did not include being able to
          monitor this parameter. This was further supported by the monitors
          not being listed in the Technical Specifications. The staff noted
          that LP&L did move the sensing line so that nitrogen pressure could
          be checked, and that the information was provided to the licensee's
          operational assessment group for dissemination to the nuclear
          industry. There will be no enforcement action on this item.
       c. Item 1.b:   Nonreporting of a failure to meet safety to nonsafety
          electr leal distribution separation criteria.     The licensee
          subsequently reported the event in LER 87-029, dated April 18, 1988.
          Failure to report this event within 30 days of the discovery date,
          which
          D CFRwas    April 2,(1987,)is
                   50.73(a)(2)          contrary
                                ii)(b which statestothat
                                                     the requirements  of submit
                                                         the licensee shall
          a 30-day report identifying any event or condition of the nuclear
          power plant, including its principal safety barriers, being in a
          condition that was outside the design basis of the plant. This is
          the first example of where the licensee failed to submit a report
          required by 10 CFR 50.73 and is an apparent violation (382/8819-01).
       d. Item 1.c: Failure to report an event where sampling and analysis of
          the gas decay tank was not performed in accordance with the action
          requirements of Technical Specification (TS) Table 3.3-13. The
          apparent basis for nonreporting was that the 25 percent surveillance
          extension permitted by TS 4.0.2 was not exceeded. This assertion was
          incorrect. TS Action Statements are not under the purview of
          Surveillance Section 4.0.2. LP&L control room personnel appeared to
          be aware of this limitation all along. The licensee published
          LER 87-030 on April 18, 1988, in response to the NRC concern but
          improperly identified the LER as "vcluntary" instead of pursuant to
          10 CFR 50.73(a)(2)(1)(B), which requires a 30-day report of any
          operation or condition prohibited by the plant's Technical
          Specifications. It will be necessary for the licensee to revise the
          LER cover sheet to indicate that it is not a voluntary report. Since
          the event date was August 19, 1987, this is the second example of the
          licensee's failure to submit a report required by 10 CFR 50.73 and is
          part of apparent violation 382/8819-01.
       e.  Item 1.c: Failure to report a missed surveillance. The licensee
          failed to perform stroke testing of Containment Atmosphere Purgr
          Valve CAP-205 within the required interval in accordance with
          TS 4.0.5. This was discovered on October 21, 1987. The licensee's
          basis of nonreporting was that the action statements which ~rcquired
           that the penetration be isolated was unwittingly satisfied by otM r
          valves. Although this mitigated the safety significance of the
          event, it did not eliminate the fact that TS surveillance
           requireme.its were not met. The licensee published LER 87-031, dated
          April 18, 1988, in response to the NRC concern but improperly

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               identified the LER as "voluntary" instead of pursuant to
               10CFR50.73(a)(2)(1). It will be necessary for the licensee to
               revise the LER cover sheet to indicate that it is not a voluntary
               report. This is the third example of the licensee's failure to
               submit a 30-day report as required by 10 CFR 50.73 and is part of
               apparent violation 382/8819-01.
          f.   Item 1.d: Failure to report a wiring error that occurred during a
               routine relay replacement. The relay was related to the automatic
               start of a switchgear ventilation recirculation fan with an ESF
               actuation. The fan had redundant controls as well as the other train
               being available. The licensee did not consider that the errue alone
                                                                       fu
               could   have
               structures or prevented
                             systems asthe   fulfillment
                                         described   in 10ofCFR
                                                             the 50.73
                                                                 safety (a)nction
                                                                          (2)(v). of safety
               Therefore, the licensee did not report the incident. The Region IV
               staff agrees and will take no enforcement action on this item.
          g.   Enforcement action related to reporting of emergency diesel generator
               valid and nonvalid failures has been taken in NRC Inspection
               Report 50-382/88-08,
          h.   While in the control room, the inspection team observed standing
               signals, which had not been acknowledged at various times during the
               inspection, including February 5 and 9, 1988. Further, the
               inspectors observed signal actuations at about 1:00 p.m. on
               February 8 (annunciator No. 6, Trains A and B - Containment
               Isolation) and at about 3:20 p.m. on February 10 (annunciator No.1
               Trains A, B, and AB - Emergency Feedwater). On neither occasion was
               the signal acknowledged as specified by procedure. This is contrary
               to Technical Specification 6.8.1.a which requires the implementation
               of procedures covering activities recommended in Appendix A of
               Regulatory Guide 1.33, Revision 2, including the procedures for
               abnormal, off-normal, or alarm conditions. Operating
               Procedure OP-4-020, Revision 0, "Bypassed and Inoperable Status
               Indication System " requires the monitoring of safety equipment
               status by way of computer and requires operator acknowledgement and
               evaluation of systems that have been computed to be inoperable. This
               is an apparent violation (382/8819-02).
     3.   Monthly Maintena_nce Observation (62703)
          The below listed station maintenance activities affecting safety-related
          systems and components were observed and documentation reviewed to
          ascertcin that the activities were conducted in accordance with approved
          procedures, technical specifications, and appropriate industry codes or
          standards,
          a.   Work Authorization 99000212.      The NRC ins)ector observed the
                performance of hardness examinations on tie inlet and outlet flanges
                for component cooling water system Valves CC-8083AB, CC-8085AB,
                CC-8244AB, and CC-8246AB. These flanges were part of the recently
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          installed piping used to connect a temporary chiller to the
          containment coolers during long duration outages. The flanges were
          examined in response to NRC Bulletin 88-05, "Nonconforming Materials
          Supplied by Piping Supplies, Inc., at Folre , New Jersey, and West
          Jersey Manufacturing Company at Williamst w.i, New Jersey." Testing
          was performed with an Equotip hardness tuter. Two of the eight
          flanges tested had satisfactory hardness measurements but six were
          unsatisfactory. After consulting the NUMARC and the Equotip vendor,
          the licensee decided the following:
          (1) The acceptance criteria would be reduced from a hardness
                corresponding to 70,000 pounds per square inch strength (70 KSI)
                to that which corresponds to 66 KSI.
          (2) The test surface would have to be prepared using 120 grit
                flapper wheels only (60 grit was previously used) in order to
                get accurate measurements.
          (3) The hardness test sample size for each flange would be increased
                from four to five with the highest and lowest readings discarded
                before averaging the readings.
          (4) Acceptance criteria for the variation in readings was provided
                by the hardness tester vendor.     If all readings in a sample did
                not meet this criteria, testing would be performed at a new
                location.
          After the appropriate procedure changes, all eight flanges were
          retested satisfactorily.
          The NRC inspectors also observed the hardness testing of Essential
          Service Chilled Water Flanges 3AC-2208, 3AC-2218, and 3AC-2228.              The
          flanges did not meet the specified minimum hardness corresponding to
          66 KSI. The lowest reading corresponded to 63.3 KSI. The licensee
          promptly performed an analysis which determined that the flanges were
          suitable for their present application.        This is a low pressure, low
          energy system. The inspector reviewed the completed work package,
          including the analysis and a justification for continued operation,
          and no problems were noted.
       b. Work Authorization WA-01020904.      The NRC inspector witnessed portions
          of the overhaul of the motor-driven firewater pump during the week of
          July 18, 1988. The inspector reviewed the work authorization to
          determine if it contained adequate instructions, references, and hold
          points. The inspector also verified that Quality Assurance,
          Maintenance Administrative Supervisor, and Shift Supervisor reviews
          and approvals were received prior to starting work. The inspector
          verified the materials to be used met the appropriate specifications
          and had the proper documentation. Some packing material was upgraded

3 for use in this application in accordance with licensee

          Procedure UNT-07-021, Revision 6, "Spare Parts Equivalency Evaluation
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            Report / Parts Quality Level Determination." The NRC inspector
            reviewed this procedure and the evaluation for the packing material
            in this application and found this acceptable.
            Three instances of procedural noncompliance were observed during the
            pump reassembly. Work Authorization 01020904 referenced Technical
            Manual 457000514 Volume 2, "Type A Centrifugal Pumps," for
            instructions for pump reassembly. The manual contained FMC
            Corporation, Peerless Pump Division, Bulletin No. 2880551, "Repair
            Instructions, Type A Centrifugal Pumps." Step 3-2.f of this document
            provided instructions which stated, "Cover the top side of the casing
            gasket with a mixture of graphite and oil." The NRC inspector noted
            that this step was not performed prior to the pump casing assembly.
            Steps 3-2.f and 3-2.h provided instructions which stated, "Rotate
            shaft by hand to check that it runs free," after the casing
            reassembly and after the packing gland reassembly. These rotational
            checks were not performed. Step 3-2.g provides instructions which
            state, "Insert the glands and set the nuts finger tight-00 NOT USE A
            WRENCH." The NRC inspector observed the packing rings inserted with
            the use of a wrench.
            The instances above did not represent a significant degradation of
            the work product but rather indicated a lack of sensitivity to
            procedural compliance. This lack of adherence to procedural
            requirements is an apparent violation of NRC regulations
            (382/8819-03).
         c. Work Authorization 01022087. The NRC inspectors monitored the
            licensee's efforts to repair the AB Essential Services Chilled Water
            System Chiller. This chiller is a "swing" unit which can serve as a
            backup to either the A or B chiller. The AB chiller is not normally
            in operation and does not corre under the purview of the technical
            specifications, unless it is being used in place of the A or B
            chiller in that respective essential services chilled water loop.
            The problems with the AB chiller may have been caused or aided by the
            fact that it was not run on a routine basis. This indicates that its
            availability may be questionable if lef t out of service for extended
            time periods. The licensee is evaluating the preventive maintenance
            and reliability aspects of the AB chiller and intends to do more work
            during the next inspection period. The inspectors will continue to
            mor.itor licensee activity on this unit.
         d. Work Authorization 01005480. The NRC inspector observed the
            replacement of the wiring and conduit in an auxiliary control panel
            to the "A" Shield Building Ventilation System Heater Control
Panel (EHC-51(3A-5A)). The installed wire was observed to be brittle

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            and discolored. No problems were noted during the installation.
            During work package documentation review, the NRC inspector observed
            that the wire and conduit were being replaced in response to

i Nonconformance Condition Identification Work '

            Authorization (CIWA) 016612, dated March 24, 1985.                                                  The
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                  nonconformance was written after determining that the installed wire
                  (No.12 AWG) was not adequate for the load requirements and No. 8 AWG
                 wire was the minimum required size. In March 1985, licensee
                  personnel observed that this undersized wiring was discolored and
                 brittle.     It was also noted that a backup contactor in the "B" Train
                 Heater Control Panel (EHC(3B-5B)) was overheating during operation.
                 This indicated that proper contact was not being made and/or a high
                 contact resistance condition existed. The engineering evaluation in
                 CIWA 016612 required immediate action to replace the backup contactor
                  to avoid further damage and immediate expediting of replacement power
                 cables. The backup contactor was replaced in January 1986
                  (approximately nine months later). The power cables for the "A"
                 Train Heater were not replaced until July 1988, almost two and one
                 half years later. The NRC inspector requested that the licensee
                 provide additional information on the basis for the delays in
                 correcting these nonconformances. Determination of the causes for
                  the delays and of the safety significance of this issue shall be the

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                  subject of an Unresolved Item (382/8819-04).
       4.   Allegation Followup (92701)
            The NRC inspector performed a review to determine the safety significance
            of the following concerns and to ensure that appropriate corrective action
            was taken.
            a.    (Closed) Concern 4-87-A-0030
                 The following issues on fire wrap of cable installations were
                  identified by a concerned individual:
                                                                                   been
                  (1) The   individual
                        adequately     did not consider
                                    addressed             his concerns
                                                by the licensee's QualityasTeam.
                                                                            having(The
                        Quality Team is a licensee organization that provides a
                        confidential means by which employee safety and quality concerns   -
                        can bs. received, investigated, and acted upon as appropriate.
                        Exiting employees and contractors are encouraged to check out
                        through the Quality Team. If they do not, a fonn letter is sent
                        to their forwarding address thus
                        mail or by telephone "hot line.")providing the opportunity by
                  (2) At the time these concerns were received by the NRC, the
                        individual stated that he had been unjustly terminated because
                        of his previous concerns. (It is understood by the staff from
                        discussions with the individual that this is no longer an issue
                        and thus will not be addressed in this report.)
                  (3) The LP&L insulation inspector is not doing a correct or adequate
                        job.
                  The NRC inspectors reviewed the practices and policies of the LP&L
                  Quality Team on July 29, 1988. It appeared that the Quality Team was
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                                 carrying out their charter as required by company policies and
                                 procedures. The inspector noted, however, that the followup closure
                                 letters sent to the individuals are very short and somewhat cryptic.
                                 Comparison of sample letters with the activity files indicated that
                                 disposition letters sent to individuals do not fully represent what
                                 action was taken and to what extent. The licensee's representative
                                 stated that it is LP&L's policy to avoid detailed technical
                                 discussion in the responses. The inspector acknowledged this as
                                 LP&L's prerogative. The brief notifications may be the cause for
                                 some individuals concluding that little or no action was taken on
                                 their concerns. Their only recourse is to take the concerns to the
                                 NRC.   This appears to resolve Item (1) above. The staff intends to
                                 take no further action on this.
                                 The inspector reviewed Quality Team files related to fire wrap and

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                                 fire seals in 1987 and 1988. The concerns appeared to have been

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                                 adequately addressed with the exception of one area. In one file,
                                 there was concern that fire wrap was not being properly installed;
                                 that people were leaving trash and debris in cable trays and wrapping
                                 trash along with the cables. A letter to the Assistant Plant
                                 Manager, Technical Services, dated March 5, 1987, was in the Quality         :
                                 Team file requesting action in response to the concern. No response
                                 was in the file nor could the Quality Team Supervisor produce an
                                 appropriate disposition. The Quality Team Supervisor comitted to
                                 provide an answer for the inspector. On August 2, 1988, the
                                 inspector was provided with the response, which was dated August 1,
                                 1988. The letter stat?d that there was a delay in the response
                                 because a 100 percent surveillance of fire wrap was underway. On
                                 January 12, 1988, the surveillance was completed, and any
                                 deficiencies discovered were repaired and reinspected.
                                 The inspectors reviewed documentation of completed fire wrap and fire
                                 seals. There was no indication that the LP&L insulation inspectors
                                 were failing to follow the procedural requirements of inspection and
                                 verifying correct work in these areas. The inspectors also reviewed
                                 a sampling of completed fire seal surveillances. It appeared that
                                 roughly five percent of the results were unsatisfactory and thus
                                 requiring repairs due to expected wear and tear from people working
                                 in the areas. There was not a preponderance of evidence that would
                                 lead the inspectors to the conclusion that improper inspection
                                 activities existed, thus Item (3) could not be substantiated,
                       b.        (Clused) Concern 4-88-A-0032
                                 The following issues on fire seal installation / rework were identified
                                 by a concerned individual.
                                  (1) Ropes were left protruding from fire barrier seals after rework.

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     (2) Quality Assurance inspectors did not always verify the required
           dimensions (two inches around the periphery) of the void before
           it was filled with repair material and sealed during fire seal
           rework operations.
     (3) Fire seal installation / rework was being performed by t.nqualified
            individuals.
     (4) Quality Control inspectors were completing signoffs in the fire
           seal installation procedure accepting fire seals that were not
            installed.
     The NRC inspector observed a fire seal and found a cable pull rope
     protruding from the seal. The licensee later stated during
     discussions that there is no degradation due to cable pull ropes
     protruding from fire seals. Additionally, the licensee provided
     copies of Southwest Research Institute Reports 01-8305-058A and
     01-8305-058B which supported this. The inspector concluded that
     Item (1) above was not a valid cor.cern.
     The NRC inspector reviewed Procedure ME-13-100, Revision 6 "Fire
     Barrier Installation and Rework," and observed that a quality hold
     point to verify the removal of two inches (minimum) of material
     around repair areas was sequenced before the void was filled. The
     inspector also noted that a recent change was incorporated into the
     procedure to change the sequence of this hold point from after
     filling the void to prior to filling. Licensee personnel stated that
     this procedure change was issued after a concern nad been raised by
     an individual performing fire seal repair work.     -1 NRC inspector
     discussed the sequence of perfomance of this verilication with a
     Quality Assurance inspector who had been responsible for performing
     these inspections. The Quality Assurance inspector stated that
     verification of removal of two inches of material was always
     performed prior to filling the void. The results of thw NRC
     inspector's review of documentation indicated that although the hold
     point in ME-13-100 had been listed out of sequence, it would have to
     have been performed prior to installation of the seal material
     otherwise the Quality Assurance inspector could not have accomplished
     the action. The inspector found no reason to pursue the matter
     further short of removing seals to see if the two-inch requirement
     was met. There was insufficient evidence to require such action.
     The licensee's corrective action to change ME-13-100 to the proper
      sequence appeared adequate to preclude future questions in this area.
      Item (2) above is therefore resolved.
     The NRC inspector discussed training requirements for fire seal
      repair personnel with the licensee. Tra1oing records were then
      reviewed to ascertain the qualifications of individuals involved in
      fire seal repair. The inspector noted thet the licensee has not
      implemented a training course on fire seal installation /rewt,rk.
      Personnel performing these repairs were contractors, and
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                  qualifications were determined by a licensee department head based on
                  previous training and work experience. Some of the people installing
                  fire seals, however, had no record of prior work experience nor any
                  formal training in fire seal installation, thus they should not have
                  been considered qualified.    Failure to perfonn this special process
                 with appropriately qualified personnel is contrary to the
                  requireaents of 10 CFR 50, Appendix B, Criterion IX, which states (in
                  part) that measures shall be established to assure that special
                                                              ersonnel. This is an
                  processes
                  apparent     are accomplished
                             violation             by qualified
                                       (382/8819-05).   Item    p(3) above is apparently
                  substantiated.
                 ME-13-100, Paragraph 3.2, states, "Maintenance personnel directly
                  supervising installation or rework activities in accordance with this
                    rocedure shall have su::cessfully completed the training program
                  p(either B&B Training Program or LP&L Training Program or applicable
                  instruments) covering Cable Wrap Protective System or Penetration
                  Seals, Fire Barriers, and Water Seals." The wording does not appear
                  to implement adequate measures to ensure people who are supervising,
                  inspecting, and performing fire seal work will be properly qualified.

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                 The licensee identified this in LP&L Quality Assurance
                 Audit SA-88-010.1, "Control of Special Processes," dated April 28,
                  1988. The audit was performed during the period February 19 thrcugh
                 March 18, 1C88. Quality Notice QA-88-036, of March 9, 1988,
                  identified the deficiency for processing under the licensee's
                 corrective action program.
                 The licensee's fire seal installation / rework program did require
                 acceptance by Quality Control (QC) inspectors after work completion.
                  In addition, third-party inspections were performed prior to
                  returning the seals to an operable status in accordance with
                  surveillance procedures. These inspections were performed by
                 experienced parsonnel in the electrical maintenance department. The
                  NRC inspector reviewed inspection documentation and discussed the
                  inspection results with the department supervisor responsible for the
                  third party inspections. No significant problems were identified to
                  indicate a lack of QC inspections during fire seal installations.
                  Item (4) above does not appear to be a valid concern.
            Specific actions taken pursuant to apparent violation 382/8819-05 will be
            documented in a future inspection report.
       5.   Operational Safety Verification (71707, 71709, & 71881)  _
            The objectives of this inspect'on are (1) to ensure that this facility is
            being operated sately and in conformance with regulatory requirements,
            (2) to ensure that the licensee's management controls are effectively
            discharging the licensee's responsibilities for continued safe operation,
            (3) to assure that selected activities of the licensee's radiological
            protection programs are implemented in conformance with plant policies and

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       procedures and in compliance with regulatory requirements, and (4) to
       inspect the licensee's compliance with the approved physical security
       plan.
       The NRC inspector attended the quarterly ALARA committee meeting held on
       June 27, 1988, and noted that the licensee's ALARA program appears to be
       effective in reducing Man-Rem expenditure as evidenced by the following:
       a.     The licensee estimates that 5-10 Man-Rem were saved by use of
              improved reactor head shielding during the recent refueling
              operation,
       b.     New aluminum foreign material exclusion covers versus steam generator
              nozzle dams for a cleanliness boundary during tube inspections
              reduced installation / removal time by a factor of ten. This resulted
              in significant Man-Rem savings.   In addition, when nozzle dam
              installation was required, mockup training appeared to be effective
              because exposure rates were reduced by a factor of four from the
              previous refueling outage.
       c.     The licensee's contaminated area reduction program has been effective
              resulting in a contaminated area reductior. from 13 percent to
              2.4 percent of plant area (outside of containment).
       The inspectors visited the control room on a daily basis when onsite and
       verified that control room staffing, operator behavior, shift turnover,
       adherence to technical specification limiting conditions for operation,
       and overall control room decorum were being conducted in accordance with
       NRC requirements. No prnblems were identified.
       Tours were conducted in various locations of the plant to observe work and
       operations in progress. Radiological work practices, posting of barriers,
       and proper use of personnel dosimetry were observed. The inspectors noted
       considerable effort underway to reduce areas containing surface
       contamination in the Reactor Auxiliary Building.
       General housekeeping, condition of fire protection equipment, and physical
       condition of safety related equipment were inspected with particular
       emphasis on engineered safety feature systems.
       The inspectors verified, on a Sr.n.pling basis, that the licensee's security
        force was functioning in compliance with the approved physical security
       plan. Search equipment such as X-ray machines, metal detectors, and
       explosive detectors were observed to te operational. The inspectors noted
        that the protected area was we.Il maintained and not compromised by erosion
       or unauthorized openings in the area barrier.
        No violations or deviations were idercified.
                        ,

1

 .    ,
                                            13
   6.   Monthly Surveillance Observation (61726)
        The NRC inspectors observed the below listed surveillance testing of
        safety-related systems and components to verify that the activities were
        being performed in accordance with the technical specifications. The
        applicable procedures were reviewed for adequacy, test instrumentation was
        verified to be in calibration, and test data was reviewed for accuracy and
        completeness. The inspectors ascertained that any deficiencies identified
        were properly reviewed and resolved,
        a.    Procedure OP-903-032, Revision 6, "Quarterly ISI Valve Tests." On
              July 19, 1988, the NRC inspector observed the performance of
              Quarterly ISI Valve Tests on the component cooling water system by
              the licensee's control room operators. These surveillance tests were
              perfomed in accordance with Section 8.7 of Procedure OP-903-032.
              The NRC inspector reviewed the procedure to verify the appropriate
              administrative reviews and approvals were obtained prior to
              performing the test. The control room operators were observed using
              the procedure to perfom these tests in a step-by-step manner.
              Communications between operations personnel in the control room and
              operators out in the plant were observed to be accurate and clear.
              The surveillance tests were completed satisfactorily, and no problems
              were identified,
        b.    Procedure OP-903-056, Revision 6, "Fire Protection Systems Functional
              Test." During the period July 26 through July 29, 1988, the
              inspectors witnessed portions of the annual flow capacity testing of
              the motor-driven and both diesel-driven fire pumps. The operators
              appeared to follow the procedure satisfactorily in a step-by-step
              manner. The motor-driven pump performed well within the acceptance
              criteria, which was expected because the pump had just been
              overhauled during the week of July 18, 1988. The diesel pumps
              performed marginally. The raw data indicated that the
              have been delivering at least 2000 gallons per minute          (pumps
                                                                      GPM) while  at may not
              a pump head of 100 pounds per square inch differential (psid).
              Technical Specification (TS) 4.7.10.1.1.f.1 requires each of the
              pumps to deliver at least 2000 GPM at a total head of 100 psid by
              verifying at least three points on the pump performance curve during
              performance testing. Acceptance Criterion 7.2 of OP-903-056 appears
              to have the same requirements. The operator brought this to the
              attention of the system engineer who then evaluated the data using
              correction factors. The operator explained to the inspector that the
              pumps were perfoming satisfactorily based upon the engineer's
              calculations. The test was completed with what appeared to be
              marginal results. The NRC inspector decided that further review was
               necessary.
               On July 30, 1988, the inspector reviewed the completed fire pump flow
               data that had been presented to the Shift Supervisor. Diesel Fire
               Pump No. 1, although it only delivered 1966.6 GPM, was running below
               rated speed. By applying correction factors for speed in accordance

.

 .    ,
                                            14
             with OP-903-056, the pump would deliver at least 2000 GPM at 100 asid
             if running at or above rated speed. The TS was silent as to whetler
             the pump should deliver at least 2000 GPM at 100 psid when called
             upon during testing or actual need or just be proved capable of the
             same by applying correction factors. By taking a liberal
             interpretation of the TS and by applying cc,rrection factors for
             speed, the three Joint pump curve established by this test places the
             pump just above t1e 2000 GPM point at 100 psid.
             Diesel Fire Pump No. 2 was running slightly above rated speed but
             delivered only 1991.5 GPH. Application of correction factors in
             accordance with OP-903-056 placed the pump below the 2000 GPM point
             at 100 psid. Although this was well within the acceptable -ange set
             up by ASME, Section XI, Table IWP-3100-2, which i                 +3 percent and
             -10 percent, it did not comply with the TS as written. When the
             inspector brought this to the attention of the Shift Supervisor, he
             agreed and declared the pump inoperable. Since only two of the three
             fire pumps must be operable at all times, this did not place the
             plant in a TS L niting Condition for Operation (LCO). By the strict
             interpretation of the acceptance criteria in 0P-903-056, the operator
             (assisted by the system engineer) failed to follow the procedure
             acceptance Section 8.8 which requires the operator to identify
             unsatisfactory test results and to inform the Shift Supervisor.
             Instead, the procedure was signed off as satisfactory. In light of
             the arrbiguities associated with the TS and the procedure,
             particularly when the ASME Code allows a negative tolerance of
             10 percent, the staff will not issue a Notice of Violation.                 The
             licensee has comitted to obtain a TS change and clarify 0P-903-056
             acceptance criteria such that the intended operability requirements
             of the fire pumps will be met. The Waterford 3 FSAR,
             Section 9.5.1.2, calls for a maximum demand of 1844 GPM. As such,
             the TS value could be lowered to accommodate normal pump wear and
             still be within the safety analysis. This shall be tracked under
             Open Item 382/8819-06.
        No violations or deviations were identified.
   7.   Followup of Previously Identified items (92701)
        a.    (Closed) Unresolved Item 382/8615-03: Conflicts and inconsistencies
             between the Technical Specifications, FSAR, and Operating
             Procedure OP-10-001, Revision 6. "Cooldown to Hot Shutdown (Mode 3 to
             Mode 4)." These inconsista cies were related to Reactor Coolant
             System (RCS) Low Temperature Overpre"urization Protection (LTOP).
             Appendix 5.2B.3 of the FSAR state 5 that administrative controls
             necessary to provide LTOP are limited to those controls that open the
              shutdown cooling system isolation valves, which in turn place the
              shutdown cooling system relief alvr in service. The NRC inspector
             was concerned that there were idi             ' administrative controls
              addressed in Section 6.3.2.5
                                                         3   \R. The language of
                                                             licensee to be poorly worded
              Section 6.3.2.5.1 was dett
                                                                 _ _ _ - - - -
                                 .    ___
                                            -_ _ _____-.-
    _____ _ __           _       _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ .___ ____
               ,     .
                   .   ,
                                                                                                                                       f
                                                                                           15
                              and subject to misinterpretation. This section of the FSAR has since
                              been rewritten and will be included in the 1988 revision of the FSAR.
                              The other inconsistencies identified by the NRC inspector were also
                              addressed and corrected by the revision to Section 6.3.2.5.1 of the
                              FSAR. This item is closed,
                           b. (Closed)OpenItem 382/8710-01: Followup on the basis for
                              modification to core protection calculator auxiliary cabinet fans.
                              The licensee provided a copy of Field Action Request 9270-422, dated
                              February 24, 1984, which documented Combustion Engineering's approval
                              of modifications to the fans. The modifications included rerouting
                              of the power cord and bypassing of the "high/ low" switch. In
                              addition, the licensee added a precaution to the SIMS - Instrument
                              Information Sheet for the applicable control panel (CP-22) addressing
                              fan modifications. This item is closed.
                           c. (0 pen) Open Item 382/8710-03:                                  Followup on the licensee's actions to

, install and ensure adequate control of seismic restraining bolts on

                              480 volt switchgear breaker cabinet hoists during maintenance
                              activities. The NRC inspector verified that the seismic restraining
                              bolts were installed. The NRC inspector also verified that
                              instructions to reinstall these bolts after maintenance had been
                              incorporated into the applicable breaker maintenance procedures,                                       t
                              However, the instructions referenced Drawing 506760500. This drawing
                              could not be obtained by the NRC inspector from the document control
                              center at the Waterford-3 site, which places its existence or perhaps
                              the drawing number in question. As of the end of this inspection
                              period, about a week had passed and the licensee had not yet provided
                              the drawing. Consequently, this item could not be closed,
                           d. (Closed) Open Item 382/8717-03:                                   Followup on the licensee's           '

3

                              implementation of corrective actions taken because a containment                                       '
                              pressure instrument was lef t isolated durin" maintenance. The NRC
                              inspector verified that Procedure OP-903-02), Revision 2, "Inspection

4

                              of Containment," has been changed to require and provide instructions                                 '
                                                                                                                                     !

4

                              for containment pressure detector operability checks when

<

                              establishing containtent integrity. These enecks are now performed                                     +

4

                              bv measuring the pressure difference with the containment purge                                        .
                              system operating and secured. The NRC inspector reviewed the results
                              of the check as performed after the recent refueling outage. No
.

l

                              problems were noted. The licensee has issued a letter, W3M87-0244,                                    ;
                              dated September 15, 1987, to clarify policy requiring "in-hand"

- procedure use in radiological controlled areas. This position is

                              also addressed in Procedures MD-1-014. Revision 2. "Conduct of                                        f
                              Maintenance," and UNT-4-009, Revision 7. "Control, Distribution,                                      :'
 ;
                              Handling, and Use of POM Procedures." This item is closed.
                           e.  (Closed) Open Item 382/8804-03:                                  Followup of licensee actions on
                               items identified during controlled area ventilation system walkdown,
                               The NRC inspector verified that the licensee had corrected the
 ,
  l
                               identified items. This item is closed,
                                                                                                                                    i
    ,_.          -
                                                          _ _ _ _ _ _ _ _ _ _ _ _
 .   .
   .      .
                                                 16
            f.     (Closed)OpenItem 382/8731-02: Followup on final outcome of
                   licensee staff reviews of vendor information packages. During the
                   period of December 7 through December 18, 1987, the NRC conducted a
                   Procurement / Vendor Information Audit at Waterford 3 The NRC
                   inspectors identified cases where service bulletins issued by the
                   emergency diesel generator vendor, Cooper-Bessemer, were not acted
                   upon by the licensee. The specifics were corrected as reported in
                   NRC Inspection Report 50-382/87-31, however, the licensee committed
                   to conduct a two-phase review of a population of 769 items which had
                   presumably been processed through the licensee's Vendor Equipment
                   Technical Information Program (VETIP). The first phase consisted of
                   345 VETIP packages which the licensee determined to have a potential
                   for significant impact on plant equipment. This was completed on a
                   priority basis by January 5, 1988. The second phase was a review of
                   the remaining 424 VETIP packages which was completed by March 1,
                   1988. A total of 208 packages required additional plant staff
                   review, and as a result, 20 required procedure changes. Quality
                   Notice 88-01 was written to document the failure to ensure that
                   proper reviews of vendor infonnation packages are performed. With
                   the exception of the Cooper-Bessemer service bulletins already
                   identified, no significant program or procedure changes resulted from
                   the rescreening effort. Details on the licensee's actions were
                   documented and transmitted from LP&L to the NRC on March 19, 1988, by
                   cover letter serial number W3P88-0040. This item is closed.
            No violations or deviations were identified.
       8.   Followup On NRC Bulletin 88-05 (92703)
            The inspectors conducted followup inspections on NRC Bulletin 88-05,
            "Nonconforming Materials Supplied by Piping Supplies, Inc., at Folsom, New

l

            Jersey, and West Jersey Manufacturing Company at Williamstown, New

l

            Jersey." The licensee promptly initiated a program to carry out the

i instructions in the bulletin. They determined the number of affected

            flanges onsite, and then initiated actions to locate and test the flanges.
            By review of procurement documents, the licensee determined that 534 of
            the affected flanges were potentially onsite. Records were traced to
             locate each flange.     The licensee determined that 259 flanges were
            currently installed in safety-related systems,138 flanges vere in the
            warehouse, and the remaining 137 flanges were not installed in
             safety-related systems.
             As flange locations were determined, the licensee perfonned hardness
             testing using an Equotip hardness tester to detennine whether material
             design strength requirements were met. Several flanges were tested onsite
             and then at an independent testing laboratory to verify results of the
             onsite testing. In addition, several flanges were destructively tested
             offsite to verify onsite test results. The material strength determined
             offsite were found to correspond with onsite measurements. At the end of
              this inspection period,16 flanges (in safety-related systems) were found
                                                                                           l
                               _.                                                        m
   .   .
     .      ,
                                                 17
              to have lower than acceptable strength of 66 KSI. Seven of these flanges
              (HeatNumberG631889) were installed on the inlet to main steam relief
              valves ~The licensee performed an analysis, based on the lowest strength
              flange (58 KSI) and the highest calculated loading, and determined that
              these flanges met the ASME, Section III NC-3658.1, requirements and were
              acceptable for their intended use.
              Five essential service chilled water system flanges and four containment
              atmosphere release system fbges (the lowest were at 60 KSI) were found
              to have lower thtn required strength of 66 KSI. These flanges were
              detemined to be acceptable after an analysis was performed and
              conformance with ASME, Section III, was verified.
              The licensee has identified three flanges which are located in the
 l            containment. Two of these flanges are in the containment atmosphere
i             release system and one on the component cooling water return to Reactor

J Coolant Pump 2A cooler. Because these flanges are in a high radiation and

i
              high temperature area, the licensee has published a justification for
 '
              continued operation, which states that testing can be delayed until the
              next forced outage without introducing a significant hazard. These are
              low pressure, low energy systems.

4

              No violations or deviations were identfied.
         9.   Licensee Event Report (LER) Followup (92700)
              In early June 1988, the inspector conducted a review of Potentially
              Reportable Event (PRE) Report 88-055 which was the licensee's internal
              identification that a snubber had been discovered missing from the
              shutdown cooling system (Safety Injection System) during maintenance.
              On May 17, 1988, maintenance personnel were reinstalling the shutdown
              cooling relief Valve SI-404A after maintenance when they noted
              Snubber SISR-1352 missing. The Shift Supervisor was appropriately
              notified, and a work authorization was initiated to promptly replace the
              snubber. In accordance with Technical Specification (TS) 3.7.8, the

, !

              absence (and thus the inoperability) of this snubber placed the shutdown
cooling system in an inoperable status for an indeterminate amount of

'

              time, a condition prohibited by technical specifications. The plant was
              in a refueling outage, and there were times when TS 3.9.8.2 required
              shutdown cooling Train A to be operable. The PRE indicated that this
              event was not reportable because subsequent evaluation determined that the
              snubber could be removed permanently. The subsequent evaluation which
              showed the snubber was not required mitigated the consequences of the
              event but it did not affect the reportability of the event.
              During an exit meeting on June 17, 1988, the inspector expressed concern
              to plant management regarding implementation of the reporting requirements
              of 10 CFR 50.73. On July 11, 1988, LER 88-017 was published describing

,

               the above event. This is a fourth example (see paragraph 2 of this

I L .

, _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

                       .
                    .              .
                                                                                       18
                                           report) of failure to comply with the reporting requirements of
                                           10 CFR 50.73. This is part of apparent violation 382/8819-01.
                                          Since the issues are already identified in apparent violation 382/8819-01,
                                           the staff will not issue a second Notice of Violation citing the failure
                                          of the licensee to maintain shutdown cooling Train A operable when it was
                                          required by TS 3.9.8.2. It appears that issues and corrective actions
                                          that would normally be discussed in the response to such a violation were
                                          addressed in LER 88-017, thus no purpose would be served in the issuance
                                          of another Notice of Violation. Although the LER stated that a root cause
                                          of this event could not be detennined because it could not be ascertained
                                          when or why the snubber was disconnected, the event implies that someone
                                           removed the snubber without authority after April 8,1988, (when it was
                                           surveillance inspected in place). The inspector expressed concern that
                                          on-going licensee efforts to eliminate procedure violations (which
                                           includes doing work affecting quality without procedural controls) are not
                                          achieving satisfactory results to date. The licensee acknowledged the
                                          inspector's concerns in the procedure compliance area and discussed
                                          additional plans and programs being implemented to achieve procedure
                                          compliance. The resident inspectors will continue to monitor this area.
                                          LER 88-017 is closed.
                            10. Onsite Followup of Events (93702)
                                          a.             Failure of Main Feed Pump "A"
                                                        During the week of July 18, 1988, the licensee noted increasing
                                                        vibration on the Main Feed Pump (MFP) "A". The plant was at full
                                                         power with both MFPs in service. By the end of the week, the
                                                        vibration had approached approximately 8 mils displacement, which was
                                                         the licensee's decision point for reducing power and securing MFP "A"
                                                         for investigation and repairs. By 3:00 p.m. on July 22, 1988, power
                                                        was reduced to about 65 percent. The pump was disconnected from the
                                                         turbine, and the turbine was tested for vibration, with satisfactory
                                                         results. The pump was then disassembled to repair an already leaking
                                                         inboard seal. The licensee found the inboard pump bearing badly
                                                        damaged with melted babbit, and two of the 26 socket head bolts that
                                                         secured the diffuser were missing. One of the bolts was found jauned
                                                         in the impeller. The bolt and the impeller were both damaged. This
                                                         seemed to point toward the cause of vibration. Attempts to find the
                                                         second    boltimposed
                                                         restrictions   were unsuccessful   due to
                                                                               by minor steam      access
                                                                                                (hot        and
                                                                                                     flashing   visibility ) leakage
                                                                                                              feedwater
                                                         into the suction piping. Although the remaining 24 diffuser bolts
                                                        were tack welded in place, two other bolts were found with the bolt
                                                         heads broken off. The licensee connented that earlier revisions of
                                                         the MFP technical manual did not specify a torque value for these
                                                         bolts, but the current revision did, thus the bolts may have been
                                                         over torqued during initial installation. The licensee replaced all
                     ,                                   26 diffuser bolts, the pump bearings, the impeller, and the pump
                                                         seals.

r

 . .
   .     .
                                               19
                 On July 26, 1988, MFP "A" was started up after completion of repairs.
                 At about half speed, a metallic sound was heard in the pump, and
                 again severe vibration of 8 to 10 mils was observed. On July 27,
                 1988, MFP "A" was again disassembled to determine the cause of
                 vibration. The inboard seal was opened to look in the impeller for
                 the bolt that could not be found. The feedwater isolation valves
                 seated better this time allowing removal of a short section of the
                 suction piping, and the bolt was found. The pump was reassembled,
                 and by 6:00 a.m. on July 29, the plant was restored to full power.
           No violations or deviations were identified.
     11. Plant Status (71707)
           The plant was at full power from the beginning of the reporting period
           until about 3:00 p.m. on July 22, 1988. Then power was reduced to
           65 percent for Main Feedwater Pump "A" repairs, and stroke testing of the
           main turbine throttle, governor and intercept valves. Also, while at
           reduced power, the monthly reactor control element assembly movement test
           was done.
           On July 22, 1988,
                               at about
           on low electro-hydraulic     9:25 p(.m.
                                      control   EHC), pressure.
                                                      the plant experienced   a turbine trip
                                                                 Maintenance mechanics
           were replacing a test solencia valve while at reduced power. A check
           valve used for isolation leaked due to a missing "0" ring when they
           attempted to remove the solenoid valve. This depressurized the EHC and
           the turbine tripped. The Steam Bypass Control System responded properly,
           and the reactor remained at power. Minimum power was about 30 percent
           until the plant was restored to the grid at about 9:30 a.m. on July 23,
           1988, and then power was increased back to 60 to 65 percent.
           As discussed in paragraph 10 above, by 6:00 a.m. on July 29, 1988, full
           power was restored and remained such as of the end of this inspection
           period.
           No violations or deviations were identified.
     12.   Exit Interview
           The inspection scope and findings were sunnarized on August 1,1988, with
           those persons indicated in paragraph 1. The licensee acknowledged the NRC
           inspectors' findings. The licensee did not identify as proprietary any of
           the material provided to or reviewed by the NRC inspectors during this
            inspection.
                                                                                             1

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