ML20151E239

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Insp Rept 50-382/88-13 on 880501-0617.Violations Noted.Major Areas Inspected:Monthly Maint Observation,Ler Followup, Containment Integrated Leak Rate Test,Plant Status & Followup of Previously Identified Items
ML20151E239
Person / Time
Site: Waterford 
Issue date: 07/14/1988
From: Chamberlain D, Will Smith, Staker T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20151E230 List:
References
50-382-88-13, NUDOCS 8807250423
Download: ML20151E239 (22)


See also: IR 05000382/1988013

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APPENDIX B

U. S. NUCLEAR REGULATORY COMMISSION

REGION IV

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NRC Inspection Report: 50-382/88-13

License:

NPF-38

Docket: 50-382

Licensee: Louisiana Power & Light Company (LP&L)

142 Delaronde Street

New Orleans, Louisiana 70174

Facility Name: Waterford Steam Electric Station, Unit 3

Inspection At: Taft, Louisiana

Inspection Conducted: May 1 through June 17, 1988

Iitspectors:

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W. F.(/5mith, SenTor ResEdent Inspector

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T. R.&Staker, Resident Inspector

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Approved:

D. D. Ghamberlain,"Chief,' Project Section A

Date

Division of Reactor Projects

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Inspection Sumary

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-Inspection Conducted May 1 thro' ugh June 17. 1988 (Report 50-382/88-13)

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Areas Inspected: Routine, unannounced inspection consisting of: (1) monthly

maintenanceobservation.(2)verificationofcontainmentintegrity,(3)onsite

followup.of events, .(4) operational safety verification, (5) monthly

' surveillance observation, (6) followu of previously identified items,-

licensee event report followup, ( ) containment integrated leak rate test,

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refueling activity. observations, 10)'startup testing observations,

) emergency diesel generator inspection, and (12) plant status.

Results: ,Within the areas-inspected, three violations were identified. The

first Wolation involved inadequate maintenance work instructions

(paraoraph2). The second violation involved failure to implement quality,

assurance procedures (paragraph 3)(.

The third violation involved a failure to

identify and correct deficiencies paragraph 3).

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DETAILS

1.

Persons Contacted

Principal Licensee Employees

  • R. P. Barkhurst, Vice President, Nuclear Operations
  • N. S. Carns, Plant Manager, Nuclear

S. A. Alleman, Nuclear Quality Assurance Manager

P. V. Prasankumar, Assistant Plant Manager, Technical Support

D. P. Packer, Assistant Plant Manager, Operations and Maintenance

  • J. J. Zabritski, Manager of Operations QA

L. W. Myers, Manager of Nuclear Operations Support and Assessments

J. R. McGaha, Manager of Nuclear Operations Engineering

W. T. Labonte, Radiation Protection Superintendent

D. E. Baker, Manager of Events Analysis Reporting & Responses

  • L. W. Laughlin, Onsite Licensing Coordinator
  • C. R. Gaines, Events Analysis Reporting and Response Supervisor

D. W. Vinci, Maintenance Superintendent

A. F. Burski, Acting Manager of Nuclear Safety and Regulatory Affairs

R. S. Starkey, Operations Superintendent

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R. A. Legere, Plant Engineering

  • Present at exit interview.

In addition to the above personnel, the NRC inspectors held discussions

with various operations, engineering, technical support, maintenance,

quality assurance, and administrative members of the licensee's staff.

2.

Monthly Maintenance Observation (62703)

The below listed station maintenance activities affecting safety-related

systems and components were observed and documentation reviewed to

ascertai. that the activities were conducted in accordance with approved

procedures, technical specifications, and appropriate industry codes or

standards,

a.

Work Authorization 01017878. While performing post maintenance

testing on Emergency Diesel Generator "B," it was observed that the

emergency diesel start air to the control air interface check

valve (EGA-4218) was leaking and preventing proper operation of the

control air system. The NRC inspector observed the replacement of

EGA-421B per the above work authorizetion which originally contained

instructions only to adjust a control air system pressure regulator.

The work authorization had been updated with additional instructions,

including the check valve replacement and a general statement to

troubleshoot. After the check valve was replaced, the control air

system was pressurized by attempting to start the diesel with the

starting air distributor disconnected from the engine.

The diesel

generator starting air distributor inputs had been disconnected and

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the air filter output capped to allow start sequencing without

crankshaft rotation.

In addition, the field flash DC supply breaker

was opened. After performing-a successful simulated start, the

breaker was closed, and the air start system reconnected.

At that

point, the NRC inspector inquired as to what work authorization

instructions controlled these tasks. Supervisory personnel at the

worksite stated that such controls were not required because they

were "troubleshooting." After completion of the troubleshooting, the

diesel was started for the retest, and then a trip occurred on high

connecting rod bearing temperature. An iavestigation revealed that

the rod bearing temperature instrument isolation valve (EGA-432B) was

shut. Apparently, the valve had been shut during the above

troubleshooting activities. After repositioning Valve EGA-432B, the

diesel was started and subsequently ran, but more problems developed

during the cooldown cycle. Work was secured until further

instructions could be obtained. The NRC inspector later noted that

cleanliness control measures, as required by Procedure UNT-7-005,

Revision 2, "Cleanliness Control," were not established when opening

the diesel generator air system.

This system is referenced in

Attachment 2 of the procedure as a class "C" cleanliness system. The

cleanliness of the diesel generator air system should have been of

particular interest since a recent licensee investigation revealed

that dirt particles on a check valve may have contributed to a

previous problem with spurious low turbo lube oil trips on diesel

generator "A."

The inspector held a discussion with plant management personnel

regarding the degree of required procedural controls on

troubleshooting activities.

It was acknowledged that more stringent

controls would have been appropriate and that better guidance in this

area should have been implemented.

The extent of the work above appears to be extensive and outside of

the limitations stipulated in Regulatory Guide 1.33 for

"troubleshooting."

Further, the work authorization failed to

implement the cleanliness controls required by UNT-7-005.

Failure to

provide an adequate procedure is an apparent violation of Technical Specification 6.8.1.a which states, in part, written procedures

shall be established and implemented as recommended in Appendix A of

Regulatory Guide 1.33, Revision 2, February 1978(382/8813-01).

During the previous inspection period of March 16 through April 30,

1988, the resident inspectors identified a similar

violation (382/8808-03) where maintenance instructions were not

appropriate to circumstances while disassembling the "B" main steam

isolation valve.

In recent months, the licensee and the NRC have

identified several other deficiencies in the implementation of

As a consequence of the repeat nature of these

procedures.

deficiencies, the corrective actions taken in response to the

apparent violation in this area should reflect substantive efforts to

preclude recurrences.

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b.

Work Authorization 01006550. The NRC inspector observed performance

of preventive maintenance on the 3B32 station service

transformer 4160 volt isolation breaker. Observations included

cleaning, inspecting, measurement of primary contact wipe, arcing

contact wipe, and primary contact gap. Two phases of primary contact

wipe were not within the acceptance criteria and were adjusted. Work

was performed per Procedure ME-04-131, Revision 5, "Maintenance

Procedure 4.16 KV G. E. Magne-Blast Breaker." The NRC inspector

identified the following minor typographical errors in

Procedure ME-04-131, Revision 5:

(1) Step 8.3.23.2 rec;uires continuation of the procedure starting at

Step 8.3.14.

The procedure must be continued at Step 8.3.24.

(2) Step 8.3.7.1 requires Steps 8.3.3 and 8.3.4 to be repeated.

Step 8.3.5 must also be repeated.

The licensee committed to correct these errors. The inspectors will

verify completion during a later inspection.

No formal followup is

requi red.

c.

Work Authorization 0108683. The NRC inspector observed the packing

replacement on the emergency feedwater header bypass isolation

valve (EFW-228A). The packing configuration included upper and lower

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packing rings separated by a lantern ring. Attempts to remove the

lantern ring without valve disassembly were unsuccessful.

Appropriate changes were made to the work instructions, and only the

upper packing rings were replaced. This action appeared to be

adequate.

d.

Work Authorization 0101929. The NRC inspector observed the

replacement of a buffer amplifier circuit card in core protection

calculator channel "A."

Subsequent testing per Procedure MI-3-121,

Revision 3, "CEAC Functional Test," was also witnessed. The NRC

inspector noted that all data points met the acceptance criterion in

the procedure.

3.

Verification of Containment Integrity (61715, 71710, & 37700)

This inspection was performed to verify that the licensee had established

containment integrity prior to reactor coolant system heatup to above

200"F. The NRC inspectors verified the proper positioning of mechanical

and electrical barriers at selected containment penetrations. A system

designed to assure containment integrity was walked down by the NRC

inspectors.

In addition, the NRC inspectors witnessed cerformance of the

personnel air lock local leak rate test.

On May 24 and 25, 1988, the NRC inspectors verified the integrity of

containment penetration Nos. 61, 65, 66, 67, 70, 114, 115, 116, 119, and

146. No problems were identified.

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On May 27, 1988, the inspectors witnessed the leak test of the containment

personnel _ air lock inner and outer door seals. The test was done in

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accordance with Procedure OP-903-111, Revision 0, "Containment Air Lock

Door Seal Leakage Test." The results were well within limits, and no

- problems were identified.

-The inspectors conducted a walkdown of the hydrogen analyzer system in

accordance with Inspection Procedure 717M, "Engineered Safety Feature

System Walkdown." .This effort was performed to accomplish two objectives.

The first was to walk down a system designed to maintain containment

Mtegrity in the event of a loss of coolant accident (LOCA), and the

seend was to independently verify the status of an engineered safety

featcre (ESF) system that had.been replaced, for the most part, during the

refueiing outage. -A review was performed to confirm that the licensee's

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(2) Several valve descriptions in the standby system valve lineup

were either wrong or inaccurate.

For example, Valve HRA-1251A

was described as the sample line isolation to analyzer "A."

Valve HRA-1251A.is either an auxiliary connection or a drain

valve.

c.

During performance of a system walkdown, all valves appeared to be

lined up correctly.

Problems with incorrect and inaccurate valve

. descriptions on the identification tags were noted.

The licensee was

aware 'of this and attempted to correct this~ problem by installation

of new valve identification tags. On a subsequent walkdown, the NRC

inspector found the hydrogen analyzer "A" sample supply and return

isolations and two vent valves labeled incorrectly.

This invalidated

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the system operating procedure because the sample supply and return

isolation valves were now required to be shut. The licensee

subsequently corrected this deficiency by installing the correct

valve identification tags.

d.

System Operating Procedure OP-8-010, requires hydrogen analyzer local

control panel sample switch numbers one through seven to be in the

"0N" position when the analyzers are in the standby mode. Sample

switches two through seven were found in the "0MIT" position. This

alignment would not render the hydrogen analyzers inoperable. The

system would, when initdated, sample from one area (top of

containment) continuously instead of automatically sequencing samples

from additional locations.. The system operating procedure ~ alignment

for standby operation should be in agreement with the actual system

setup during this mode,

The system drawing for the hydrogen analyzers, LOV-1564-B-430-SP-01,

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only shows the "B" analyzer system. A drawing note states that

system "A" is similar. Several system "A" valves (auxilisry

connections) are not included. The licensee stated that because the

"A" train was not depicted on the drawing, the retultant confusion

led to operations personnel installing valve identification tags on

the wrong valves.

f.

The sample line supplying hydrogen analyzer "B" is heat traced and

insulated. Sections of the insulation were removed in order to

install Station Modification 983. During the system walkdown, the

NRC inspector noted that some sections of insulation were not

reinstalled and other sections were left hanging from supports.

No

condition identification tag was observed, and the SMP was cicsed

with the exception of cid cabinet removal and a system walkdown for

human factors and "touch up."

The NRC inspector noted that the

insulation was reinstalled prior to the end of the inspection period.

During review of the SMP for Station Modification 983, the NRC

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inspector noted from the documentation that during testing a

transistor was burned out and a pressure transmitter had been damaged

due to incorrect wire terminations. The installation had been

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inspected and accepted by the licensee's quality assurance

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inspectors. Quality Assurance Inspection Report 88-012, dated

= April 21,-1988, documented these findings. Quality Assurance

Procedure QAP-012, Revision 6, "Corrective Actions," requires-

= initiation of a Quality Notice (QN) when conditions adverse to

quality are identified.so that appropriate reviews and corrective

actions as to cause can be accomplished. The NRC inspector noted

.that no QN_ had been written on the above condition. = The NRC

inspectors discussed this with Itcensee management.

The issuance of

a QN for the above condition, as well as-the licensee's "threshold"

- for issuance of QN in general was addressed.

It was acknowledged

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.that a QN should have been issued-for the condition above and that

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the threshold;for the issuance of- QNs may be too high for some

licensee personnel.

The licensee then issued a QN on the incorrect-

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termination described above.

Failure to issue a Quality Notice in

accordance with QAP-012.when the above condition was identified is an

apparent' violation (382/8813-02).

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Previous valve identification tag and valve lineup deficiencies with the

hydrogen analyzer system were . identified in NRC Inspection

Rcport 50-382/88-22. Those deficiencies were subsequently corrected.

Previous deficiencies with equipment labeling and safety system operating

procedures (valve lineups) have been idantified in NRC Inspection

Reports 50-382/86-02,86-11,86-15,86-29,87-01,87-10,87-22,87-25,

l88-04 .and 88-08. The specific deficiencies of this type identified by

.the NRC inspectors appear _to be corrected by the licensee, but the

licensee does not appear to be taking adequate corrective action to

preclude recurrences or:to identify and correct similar problems in other

safety systems.

Failure of the licensee to promptly identify, correct,

and preclude recurrences of these deficiencies is an apparent violation of

the requirements of Criterion XVI of Appendix B to 10 CFR Part 50

(382/8813-03).

4.

Onsite Followup of Fvents (93702)

a.

Failure of Main Steam Isolation Valves

On April 9,1988, the plant was shut down and cooled down in

operational Mode 5 for the second refueling outage. When the No. 1

Main Turbine Throttle Valve was opened for routine inspection, the

licensee found a piece of steel about 33 inches long by 2 1/2 inches

wide by 1 3/8 inches thick which had been caught by the basket

strainer upstream of the throttle valve. The piece was broken nearly

in half and was slightly bent. A few broken fasteners were also

found. The piece of metal had a part number which identified it as

part of a gate guide assembly for one of the two main steam isolation

valves (MSIVs).

Since MSIV "B" (MS-1248) had a more direct

downstream path which was most likely to transport the debris to the

main turbine throttles, the licensee elected to inspect about 100 of

the 200 feet of main stream piping upstream of the turbine throttle

leading to MS-124B.

No additional parts were found. The MSIVs at

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Waterford-3 were manufactured by WKF Valve Division of

ACF. Industries. They are 40x30x40 Class 600 hydraulically opened,

nitrogen pressure closed, Model D-2 "Pow-R-Seal" gate valves. This

event was initially reported in NRC Inspection deport 50-382/88-08.

During this inspection period, the licensee fully disassembled both

MSIVs "A" and "B".

Tests and investigations were conducted to

determine the causes of the failure and to establish a viable

corrective action plan. The resident inspectors followed the

licensee's activities with assistance'and support provided by

Region IV engineering personnel and NRR technical project staff.

WKM, the valve manufacturer, performed a component failure analysis

and design enhancement study.

Kalsi Engineering, Inc., was

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contracted by the licensee to perform an engineering

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technical evaluation of the root cause and a worst case safety

analysis for MSIV operability with failed guide rails.

The licensee performed a material evaluation of the failed parts

which included an evaluation of the guide rail fasteners which had

not yet failed. The licensee has committed to provide the NRC with a

detailed report by June 24, 1988, on the results of these efforts

thereby documenting the root causes of _ the failures, the corrective

actions, the safety implications of having operated for the past

three years with the valves as-built, and the margin of safety

afforded by operation in the future after repairs and design

improvements had been implemented.

Resolution of these issues is

already being tracked by Unresolved Item 382/8808-01.

The failure mechanism appeared to be centered around the fasteners

which attached the guide rails to the guide rail skirts. These

fasteners appeared to fail in shear due to excessive stresses set up

by a combination of unfavorable conditions which are discussed in the

following paragraphs.

Typically, the gate in a standard gate valve withdraws into the upper

bonnet and is wedge shaped so that when it is shut the gate wedges

itself between the seats.

The WKM "Pow-R-Seal" gate is a longer

two-piece gate with parallel seating surfaces.

Rather than

disappearing into the valve bonnet, just the top half of this longer

gate moves up into the bonnet, and the lower half stays in the

process stream with a hole as large as the seat to allow process

flow. The gate halves are cut on diagonals so that when they move

relative to each other, they wedge apart and against the seats

providing a seal. There is a lever lock assembly on the gate which

keeps the gate from wedging itself while in transit. This assembly

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rides between the guide rails until the end of the valve strokes

where the rails release the lever thus allowing the gate to wedge in

either the open or shut position.

Each time the valve begins to

stroke, the lever lock shoe impacts against the end of the rails.

Because of the angles of contact and sharp corners, the rails and

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lever lock shoes are galled at the contact points. This put a heavy

load on the fasteners that attach the guide rails to the guide rail

skirt, resulting in the eventual failure of the fasteners for

MSIV "B."

The licensee stated that the valve design (parts configuration)

resulted in excessive galling of the lever lock shoes and guide

rails, thus imparting large stresses to the guide rail fasteners.

Pre-existing cracks and corrosion on the fasteners may have weakened

the fasteners.

Rail and skirt misalignment during fabrication may

have placed additional stresses in the fasteners, as they were flat

head screws which are more vulnerable to bending stresses unless the

holes are carefully aligned.

The design ;;as enhanced by (1) changing the angle of contact between

the lever lock shoes and the guide rails, (2) stelliting the contact

surfaces between the lever lock shoes and the guide rails,

(3) changing the bolt material from low alloy steel to 17-4PH

stainless steel, (4) nondestructively examining the

fasteners for defects, (5) aligning the tapped holes in the guide

rails with the drilled holes in the guide rail skirts to within

0.005 inches axis to axis, and (6) verifying torque at 150 foot

pounds for each fastener.

The NRC inspectors witnessed portions of the reassembly process.

The

valve internals were installed with care and in the presence of a WKM

representative. When the valves were tested, some licensee operators

observed that the MSIVs operated smoother and quieter than in the

past.

By all observed tests and technical data provided to the

inspectors, the MSIVs appear to be adequate to perform their intended

safety function,

b.

Pressurizer Low Range Pressure Instrument Failure

On June 8,1988, a pressurizer low range pressure transmitter

(RC-IPT-0106) ruptured. When this occurred, unidentified reactor

coolant system leakage increased to 2.22 gallons per minute.

Additionally, the pressurizer safety channel "0" wide and narrow

range instruments and the Y-level control channel were indicating

incorrec tly. After isolating the leak, capping the failed instrument

line, and returning the safety instruments to service, the licensee

began an investigation to determine the cause of the failure of the

Barton Model 783 pressure transmitter (Range 0-750 PSI).

Later the

licensee determined that RC-IPT-0106 had been replaced during the

refueling outage (April 1 through June 1,1988), with a transmitter

rated for 150 percent of the maximum indication range or 1125 pounds

per square inch (PSI). The gauge was subjected to reactor coolant

system normal operating pressure (2250 PSI).

The licensee found that

the purchase documentation used to order the replacement transmitter

did not include adequate information to obtain the required pressure

rating. The licensee initiated a Quality Notice to follow up on the

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inadequate purchasing documents.

Additionally, the licensee has

verified that all similar instruments meet the applicable design

requirements. This action appears to be adequate.

No violations or deviations were identified.

5.

Operational Safety Verification (71707, 71709, 71881)

The objectives of this inspection are (1) to ensure that this facility is

being operated safely and in conformance with regulatory requirements,

(2) to ensure that the licensee's management controls are effectively

discharging the licensee's responsibilities for continued safe operation,

(3) to assure that selected activities of the licensee's radiological

protection programs are implemented in conformance with plant policies and

procedures and in compliance with regulatory requirements, and (4) to

inspect the licensee's compliance with the approved physical security

plan.

When onsite, the NRC inspectors visited the control room daily.

Control

room staffing, access, operator behavior and shift turnovers were

observed. The NRC inspector reviewed operators' logs and control panels

to verify compliance with technical specification limiting conditions for

operation. No problems were identified.

The NRC inspectors toured accessible areas of the plant in order to

observe hausekeeping and equipment condition.

During the tours, the NRC

inspectors observed that fire impairments were identified and fire watches

were established as required. The NRC inspectors verified proper use of

dosimetry and anticontamination equipment in accordance with approved

radiation work permits.

In addition, condition of security barriers and

implementation of compensatory measures during impairments were also

observed.

Some minor housekeeping problems were identified in

paragraph 10 of this report.

No other problems were noted.

No violations or deviations were identified.

6.

Monthly Surveillance Observation (61726},

The NRC inspectors observed the below listed surveillance testing of

safety-related systems and components to verify that the activities were

being performed in accordance with the technical specifications. The

applicable procedures were reviewed for adequacy, test instrumentation was

verified to be in calibration, and test data was reviewed for accuracy and

completeness. The inspectors ascertained that any deficiencies identified

were properly reviewed and resolved.

a.

Procedure OP-903-032, Revision 5, "Quarterly ISI Valve Tests." On

fiay 21, 1988, the NRC inspector witnessed the quarterly cycling of

Main Steam Isolation Valve "A" and Main Feedwater Isolation

Valve "B."

Although the valves stroked satisfactorily, two

annunciators alarmed which the licensee's representatives considered

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abnormal and requiring correction. They were "MSIV-1 TEST FAILURE

TROUBLE" and "MSIV-1 HYDRAULIC SYSTEM TROUBLE." The anomolies were

corrected by minor repairs to the electro-hydraulic actuator systems,

and the valves were subsequently retested satisfactorily,

b.

Procedure OP-903-033, Revision 7, "Cold Shutdown ISI Valve Tests."

On May 21, 1988, the NRC inspector witnessed a full stroke timing

test of Main Steam Isolation Valve "A" following the major

maintenance-discussed in paragraph 3.

The valve must shut within

three seconds -as required by Technical Specification 4.7.1.5.

The

inspector independently measured the stroke time at the value with a

digital stopwatch and noted the valve shut smoothly and well within

the time required. No other problems were noted.

No violations or deviations were identified.

7.

-Followup of Previously Identified Items (92701)

a.

(Closed) Violation 382/8602-03:

Failure to comply with Technical Specification 3.0.4 which prohibits changing modes while relying on

action statements to satisfy limiting conditions for operation. On

December 16, 1985, the licensee entered Mode 3 without containment

spray operable, as required, due to an isolation valve (CS-111B)

reach rod being disconnected. This condition misled the operator

into thinking he had opened the valve when in fact all he did was

turn the reach rod handwheel. Control room operators were further

confused by a typographical error in the Operations Annunciators

Response procedure. On May 16, 1986, the licensee's response to the

violations comitted to revise certain procedures, change the label

on the appropriate annunciator window, compile a list of all manual

valves operated by reach rods, and install warning tags on or near

all reach rod handwheels to instruct plant operators to verify actual

valve positions when using the reach rods. The NRC inspectors

verified that all of the above actions had been taken and noted,

after nearly two years, that most of the warning tags were still

installed. A few had broken off, and the licensee promptly

reinstalled them. None have been found broken off lately. The

inspectors expressed concern that the all-inclusive installation of

warning tags may have been carried out to excess. Many of the reach

rods were installed to reduce radiological exposure. To gain access

to the valve and verify position may involve worse consequences in

terms of radiological exposure than finding the valve out of position

later. The licensee committed to re-evaluate the list and take these

concerns into account, thus possibly reducing the list to only those

valves which are important to safety. This action would be an ALARA

improvement which need not be formally tracked.

This violation is

closed.

(Closed)OpenItem 382/8608-01: NRR evaluation of licensee's failure

b.

to perform the monthly logarithmic power level channel functional

test when at power. Table 4.3-1 of the Technical Specifications

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requires this test in Modes 1, 2, 3, 4, and 5.

Table 3.3-1 requires

the instrument to be operable while the reactor is critical, but when

above' 0.0001 percent power, the trip function may be manually

bypassed.

If it is not bypassed, the reactor will trip at about

0.25 percent power. The licensee's surveillance procedure, written

to satisfy the above technical specification requirement, takes

exception to performing the above functional test when the reactor is

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critical, because the trip is bypassed above 0.0001 percent power and

to do the test would require disconnecting input cabling. Since the

Technical S)ecifications permit bypassing the trip function thus

rendering t1e instrument inoperable, it stands to reason that there

is no need to do a functional test while the instrument is

inoperable. However, the instrument should be tested promptly after

shutting down the reactor. A technical specification change request

has been submitted to this effect and is presently under review by

NRR. The purpos'e of this item was to track the licensee's actions to

initiate documentation to resolve the. issue. The change request

accomplished this, therefore, the item is. closed.

No violations or deviations were identified.

8.

Licensee Event Report (LER) Followup (92712)

The LERs listed below were reviewed and closed. The NRC inspector

verified that reporting requirements had=been met, causes had been

. identified, corrective actions appeared appropriate, generic applicability

had been considered, and that the LER forms were complete. The NRC

inspector confirmed that unreviewed safety questions and violations of

technical specifications, license conditions, or other regulatory

requirements had been adequately described.

a.

(Closed)LER 382/87-012. "Two Reactor Trips Due to Inadequate

Procedures."

b.

(Closed)LER 382/87-014. "Fire Hose _ House and Computer Halon System

Surveillance Intervals Exceeded Due to Personnel Error."

c.

(Closed)LER 382/87-026, "Containment Electric Penetration Backup

Protection Inoperable Due to Inadequate Construction Documentation."

d.

(Closed)LER 382/88-004, "Containment Isolation Valve Position

Indication Not Environmentally Qualified Due to Inadequate

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Engineering Review."

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No violations or deviations were identified.

9.

Containment Integrated Leak Rate Test (70313, 70307, & 70323)

The objective of this inspection was to ascertain through direct

observation, records review, and independent calculations whether the

containment Integrated Leak Rate Test (CILRT) was conducted in compliance

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with the licensee's procedure and as required by the Waterford-3 Technical

Specifications, 10 CFR 50, Appendix J, and ANSI N45.4-1972, "Leakage-rate

Testing of Containment Structures for Nuclear Reactors."

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The NRC resident inspectors witnessed portions of the preparations for,

and conduct of, the test.

Emphasis was placed on compliance with the

required plant conditions, test procedure requirements and administrative

requirements. The inspectors also performed rough calculations to

establish a confidence in the licensee's computer programs which were used

to determine the containment leak rate.

An NRC regional inspector was unavailable to witness the preparations for

the test and the actual test performance, but subsequently reviewed the

local leak rate test (LLRT) and CILRT data as discussed below.

The CILRT commenced on May 22, 1988, at 2:10 a.m. as pressurization of the

reactor containment began.

Preparation had been underway for several days

preceding the start of the test. The resident inspectors verified

accomplishment of prerequisites such as a general inspection of the

accessible portions of the interior and exterior containment surfaces; a

containment area survey for temperature differentials; closure of the

maintenance hatch; removal of fire extinguishers; and installation and

calibration of instrumentation. The inspectors reviewed Surveillance

Procedure PE-5-001, Revision 1, Change 2, "Containment Integrated Leak

Rate Test." All of the appropriate prerequisites, conditions, required

equipment, and valve / breaker lineups were satisfactorily completed and

signed off as required.

The resident inspectors conducted a walkdown of

the test air lines from the compressors to the point of entry into the

containment using the test procedure containment pressurization flow

diagram ( Attachment 10.8) and test instrument schematic (Attachment 10.9).

The equipment required for satisfactory completion of the test was

installed in a professional manner. There were a few minor disparities

identified by the inspector which the licensee's representative in charge

of the test explained to the inspector's satisfaction. They were as

follows:

a.

There was a portable process radiation monitor connected to

Valve LRT-112. This did not appear on Attachment 10.8.

It was

installed to monitor the effluent when the containment is vented

through LRT-105 at the conclusion of the test.

b.

The pressure and temperature indicators upstream of LRT-101 were not

present as shown on Attachment 10.8.

Since a dew point instrument

was installed at LRT-102 (also not shown on Attachment 10.8), there

was no need for these instruments. The air dryers and the air

compressors provided adequate and redundant pressure indication,

An absolute pressure instrument and some tubing and valves were

c.

connected at the sight glass flowmeter used during the verification

This was not shown on Attachaent 10.9 but is needed to obtain

test.

corrected flow readings from the flow meter.

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d.

The atmospheric vent valve shown at the Heise Gauge on

Attachment 10.9 was missing.

This might only be needed as a

convenience item to check the gauge.

The licensee's representative stated that he intended to improve

Attachments 10.8 and 10.9 for the next CILRT. This action is acceptable

and does not require followup.

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~ The licensee elected to perfom the abbreviated leakage rate test in

accordance with Topical Report BN-TOP-1, Revision 1, "Testing Criteria for

Integrated Leakage Rate Testing of Primary Containment Structures for

Nuclear Power Plants," provided by Bechtel Corp (oration and currently

permitted by the NRC.

This is an 8-hour test afterstabilizing)in

lieu of the 24-hour test.

Containment pressurization was achieved at about I p.m. on May 22, 1988.

After stabilizing for about five hours, the 8-hour test period was

implemented at 6:00 p.m.

Data was taken using the plant monitoring

computer with 2 pressure indication transmitters,10 humidity measuring

devices, and 40 platinum element dry bulb resistance temperature

detectors.

For the eight hours that followed, the computer obtained and recorded

weighted average temperature and humidity, pressure and vapor pressure.

- dry air mass, and leakage rates every 15 minutes. At the end of eight

hours, the computer calculated a containment leakage rate of about

0.05 percent per day. Technical Specification 3.6.1.2 requires an overall

integrated leakage rate of less than or equal to 0.50 percent per day,

therefore, the results appeared well within the limit. Upon completion of

the CILRT, the licensee conducted the supplemental test required by

Technical Specification 4.6.1.2.c.

This is a 4-hour test where a known

leak is superimposed to verify the accuracy of the CILRT. The results of

the supplemental test were well within the acceptance criterion of

25 percent of the allowed leakage.

The resident inspector conducted independent rough calculations using a

programmable calculator and verified with reasonable confidence that the

licensee's results were accurate and valid.

The regional inspector later reviewed the completed copy of CILRT Test

Procedure PE-5-001, Revision 1, Change 2.

This review was performed to

verify that the signatures required throughout the test procedure were

present, and to verify that the post-test valve realignment had been

performed. The inspector verified that all the valves that had been

addressed in the pre-test valve alignment had been addressed again.

The regional inspector also interviewed the CILRT test director and other

personnel involved in the test. The purpose of the interviews was to

detemine how the test was performed, if any equipment was repaired that

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might have affected the as-found conditions for the CILRT, and if there

were any other conditions that the NRC should be made aware of. No

problems were identified.

Finally, the inspector input the CILRT data provided by the CILRT test

director into the NRC computer program "CILRT 2" to verify the results

'that the licensee had calculated.

The results were satisfactory.

No ' violations or deviations were identified.

10.

Refueling Activity Observations (86700)

On May 9,1988, while lowering the in-core instrument (ICI) thimble

support plate into the upper reactor internals, the plate started rotating

and cocking. The licensee halted the' lowering operations.

ICI location

A-14 thimble tube end was observed to be bowed approximately 60 degrees

out of_line. Upon further inspection, it was. discovered that the ICI

thimble tube was missing from the lower end of the coupling with the ICI

protruding from the coupling and continuing into the upper internals. The

ICI coming out of the tube took a sharp bend back towards its tube in the-

upper internals. . Upon inspection of the discharged fuel assembly from the

A-14 location, the lower section of the ICI thimble was found protruding

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above the top of the fuel upper end fitting. The upper section of the

thimble, from the ICI thimble support plate to the coupling nut along with

the ICI, was cut off and permanently removed from the upper internal

assembly.

Combustion Engineering prepared an evaluation report for the licensee.

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The report postulated the failure to be an isolated manufacturing anomaly,

i.e., insufficient torque, cross threading, or improper lock pin

installation. The report stated that there are a total of 356 thimbles in

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various plants with an accumulated 50 plant-operating years. This is the

first and only failure of this type reported. The report provided a basis

for continued operation without an ICI at position A-14, which appeared to

be sound.

Combustion Engineering recommended installation of a dummy ICI

to provide a dampening effect against vibration of the curved tubes, make

some physical and administrative adjustments to the movable in-core

detector system to prevent entry to location A-14, and to consider impact

on the core operating limit supervisory system (COLSS). The inspectors

discussed this with the licensee, and all of these recommendations were

followed. A copy of the Combustion Engineering report along with the

licensee's evaluation was forwarded to NRC Region IV for review.

On May 7, 1988, the inspector monitored cleanup activities and removal of

the reactor vessel ultrasonic test equipment in preparation for final core

mapping. Radiological work practices appeared to be adequate, however,

housekeeping, particularly in' the area of the refueling crane, was

degraded. Pieces of trash, loose hand tools, and other debris were

scattered about. This was a concern because the reactor vessel was still

apen, though no core alterations were in progress.

Based on other

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observations, this was an isolated occurrence because housekeeping in the

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refueling trea has been satisfactory.

Imediately upon identifying this

to the refueling supervisor, the area was cleaned up.

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No violations or deviations were identified.

11. Startup Testing-Refueling (72700)

The objective 6f this inspection was to verify that facility operaticn

following refueling was in conformance with NRC requirements and licensee

procedures.

The NRC inspector ~ observed the withdrawal of the shutdown, part-length,

and regulating control element assemblies (CEAs) in preparation for

insertion time measurement per Procedure NE-2-020, Revision 1, "CEA

Insertion Time Measurement." When attempting to withdraw Regulatory

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Group 3, Control Element Assembly 61 would not transfer from the lower to

upper gripper assembly. After repairs, all control elements were

withdrawn and then,successfully inserted within three seconds as required

by NE-2-020 and the Technical Specifications.

On May 28, 1988, the motor for containment cooling fan "C" failed.

The

plant was in Mode 3 (hot standby) with preperations underway to commence

the initial approach to criticality following refueling. Technical Specification 3.6.2.2 requires all four cooling fans to be operable during

Modes 1, 2, 3, and 4.

If one fan becomes inoperable in Mode 3, it must be

restored within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> or the plant cooled down within the following

30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />. The licensee obtained enforcement discretion to allow startup

and low power physics-testing while repairing or replacing the motor. A

justification for continued operation was submitted to the Region IV

Regional Administrator showing that it was safe to operate with the three

remaining fans at power levels below 0.1 percent power.

On May 29, 1988, at 8:35 a.m., the plant entered Mode 2, and at

10:57 a.m., reactor criticality was achieved.

The inspectors witnessed

the startup and portions of the following startup test procedures:

a.

NE-2-030, P.evision 0, "Initial Criticality Following Refueling." The

inspectors observed the initial approach to criticality by boron

dilution.

The reactor was observed to be critical with Control

Element Assembly Regulating Group 6 at 75 inches withdrawn and a

boron concentration of 1523 ppm.

b.

NE-2-003, Revision 0, "Post-Refueling Startup Testing Controlling

Document." On May 29, 1988, the inspectors witnessed part of the

establishment of base power level limits for low power physics

testing per Attachment 9.8 and then reviewed the completed data. No

problems were found.

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NE-2-040, Revision 0, "CEA Group Watch and CEA Coupling Check." On

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'May 29, 1988, the inspectors witnessed the CEA coupling checks for

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about 15 CEAs. Subsequent review of the data confirmed that all CEAs

were in' fact coupled to the drive motors. On May 30, 1988, the

inspectors witnessed detennination of the reference group (Group B)

worth.

During this test, the amount of negative reactivity inserted

with Group B was plotted on the test recorder / computer as Group B was

driven into the core concurrent with compensating boron dilution.

This information will be used in the determination of the other CEA

group worths later.

On May 31, 1988, the licensee requested a tenporary waiver of compliance

from Technical Specification 3.6.2.2 to allow progress to full power based

on a re-analysis.that only one containment cooling fan per train is needed

for safe operation. This was granted by NRR in a letter dated June 2,

1988. Technical Specification 3.6.2.2 has since been permanently changed

to reflect the single fan requirement by Amendment 39.

No violations or deviations were identified.

12. Emergency Diesel Generator Inspection (62702)

A representative of NRR conducted an inspection of the licensee's

maintenance activities on Emergency Diesel Generators (EDG) A and B during

the period of May 23-26, 1988. The purpose of the inspection was to

evaluate the licensee's maintenance program in terms of how it would or

would not enhance EDG reliability.

The primary focus of the inspection

was.(1) a review of the five year inspection of EDGs, and (2) a review of

the licensee's implementation of recommendations contained in bulletins

issued by the EDG vendor.

In December 1987, an inspection of the licensee's vendor interface program

was conducted. This was documented in NRC Inspection Report 50-382/87-19,

dated May 12,.1988. Results of this inspection showed that the licensee

had not implemented a number of EDG vendor recommendations.

In early

1988, problems with EDG pneumatic shut down devices were identified.

Both

issues were compounded by questions regarding reportability of certain EDG

operational events. The combination of incidents served to create a

perception of poor EDG reliability.

A previous inspection of the problems

with EDG pneumatic devices showed that the licensee's EDG maintenance

program was in fact an excellent program, and that the perception of poor

EDG reliability was incorrect.

See NRC Inspection Report 50-382/88-08.

This inspection was conducted for the purpose of verifying the previous

findings and to assess the licensee's current position regarding vendor

recommendations.

The following documents were reviewed during the inspection:

Mechanical Maintenance Procedure MM-3-015. "Surveillance Procedure

a.

Emergency Diesel Engine Inspection."

b.

Work Package associated with implementation of MM-3-015 for EDG "A".

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c.

LP&L Pre-Summary of EDG Outage During Refuel 2, dated May 17, 1987.

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d.

LP&L Letter dated May 17, 1987, suggesting changes to inspection

procedures in Section 15'of EDG . technical manual.

e.

Cooper Energy Services (CES) letter dated June 23, 1987, in response

to LP&L suggested changes to.the EDG Technical Manual.

f.

CES letter dated March 21, 1988, supplementing CES letter of June 23,

1987.

, eport dated April 18, 1988, - Electronic Engine Analysis of EDG

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Surveillance Procedure OP-903-069, "Integrated EDG/ESF Test."

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Vibration data for EDG A - April 15, 1988.

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Vibration data for EDG B - May 14, 1988.

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Section 15 of the EDG technical manual.

In addition to reviewing.the above documentation, the inspector discussed

the vibration monitoring program for EDGs with the licensee's

representatives. This discussion covered points on the engines and what

engine auxiliaries were monitored for vibration, the type of equipment

used, and the frequency of monitoring. The licensee also demonstrated how

the raw vibration data was processed and some of the different ways the

data can be retrieved from computer storage and displayed or printed out.

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On the basis of the review of the above data and discussions with

cognizant personnel, the inspector found that the licensee is following

the EDG vendor's reconnended five year inspection program.

Procedure MM-3-015 includes all of the inspection steps called out in

Chapter 15 of the EDG technical manual as modified by agreement between

the licensee and the vendor.

The modifications to the technical manual

primarily cover deletion of certain requirements to disassemble the diesel

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engines for the purpose of inspecting internal components for wear and/or

degradation. The agreement to delete certain inspection requirements is

made on the basis of the predictive maintenance program the licensee has

implemented. This program utilizes data from an electronic engine

analyzer, vibration data, trending of engine operating parameters, and

boroscope inspections as a substitute for physical disassembly to evaluate

engine condition. The modifications to the vendor reconnended inspection

program are acceptable because the licensee's predictive maintenance

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program will provide adequate information to assess engine condition

witho;c major disassembly and the attendant possibility for incorrect

reassanbly. Results of the five year inspection, including electronic

engine analyzer data, show the diesel generators to be in excellent

condition except for the engine cylinder load balance.

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In NRC Inspection Report 50-382/87-19 covering vendor interface, the

licensee was cited for not having implemented the recomendations

contained in 17 bulletins issued by the diesel generator vendor. This

inspection included a review of licensee actions since the vendor

interface inspection to' implement vendor recommendations with the

following results. Two of the 17 vendor bulletins were not applicable to

' Waterford-3 and required no action. Of the remaining 15, all have been

implemented as of this inspection.

It should be noted, however, that of

the above-15 vendor recommendations, 12 did not require any immediate

action because they involved such things as product improvements,

information, clarification, or modifications only if troubles had been

observed. Lack of implementation of these recommendations did/would not

impair diesel generator reliability._ The remaining three recomendations,

if_not implemented, could have impaired diesel generator reliability. The

most serious of the three concerns modifications to the turbocharger

supports. The turbocharger, however, is included in the vibration

monitoring portion of the diesel generator predictive ma1ntenance program,

and any problems arising from inadequate supports would have been noted

through a change in vibration data. Therefore, diesel-generator

reliability was not materially affected by failure to implement this

recommendation at the time it was issued. Viewed in perspective, there

are only two cases where the licensee was delinquent in implementing

vendor recommendations affecting diesel generator reliability or providing

compensating measures, as opposed to the 17 cases previously reported. As

of this inspection, all applicable vendor recomendations had been

implemented.

In conclusion, the results of this inspection confirm previous findings,

i.e., the licensee has developed and implemented a strong predictive

maintenance program for the diesel generators. On the basis of this

program, the licensee has completed an effective five year inspection of

the diesel generators in accordance with modified vendor recommendations.

In addition, the inspector verified that all applicable vendor

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recomendations for dietel generator improvements had been implemented.

In sumary, the results of the five year inspection and the implementation

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of vendor recomendations, when viewed in light of the ongoing predictive

maintenance program, provide assurance that the diesel generaters at

Waterford-3 are, and will continue to be, highly reliable.

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On the basis of the inspection results, the following recomandations are

made:

The cylinder to cylinder load balance on the diesel engines should be

a.

brought within vendor recommendation tolerances at the earliest

opportunity. The degree of imoalance on the engines at Haterford-3

will have a detrimental effect on engine reliability if not

corrected.

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The ' predictive maintenance progra'n could be improved by expanding the

vibration monitoring portion to include all diesel generator

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auxiliaries.

No violations or deviations were identified.

13. Plant Status (71707)

The inspection period began with the core completely off-loaded and

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reactor vessel inspection in progress. Core reloading was connenced on

May 3, 1988, and completed on May 6, 1988. The reactor head was placed

back on the vessel on May 12, 1988.

Reactor coolant system filling and

venting was completed on May 20, 1988. On May 26, 1988, the plant entered

Mode 3.

Reactor criticality was achieved on May 29, 1988. The plant

entered Mode 1 and was placed on the grid on June 1,1988. On June 9,

1988, the plant reached full power.

Power was reduced to 60 percent on June 10, 1988, to remove the "A" main

feed pump from service for an inspection because of high vibration

readings. After the inspection was complete, the main feed pump was

placed back in service.

Power was then maintained at 60 percent because

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of low demand on the power grid.

On June 13, 1988,-the unit was shut down from 70 percent power because of

a reactor coolant system unidentified leak rate exceeding the Technical

Specification limit of one gallon per minute.

The source of excessive

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leakage was determined to be through two series reactor coolant drain

valves. After torquing the valves in the shut direction and verifying

reactor coolant system leakage within the TS limit, startup was commenced

on June 14. 1988.

During the June 14 startup), _the reactor tripped from 17 percent power d

to low steam generator (SG water level. All systems appeared to respond

The licensee was conducting a main turbine overspeed protection

nonnally(.OPC) system test at 1800 RPM. This test is routinely done at

control

about 500 RPM.. When the operator enabled the turbine to recover, there

was a 'large speed error in the controls which caused the governor valves

to open rapidly, thus causing SG swell. This, in turn, tripped the

feedwater isolation valves shut on high SG 1evel. By the time the

operators restored feedwater flow, the reactor tripped on low SG level.

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The licensee intends to add a caution to the procedure to prevent the

operator from introducing a high speed error in the future when the

turbine OPC test is done.

The reactor was critical again on June 15, 1988, and subsequently returned

to full power where it remained through the completion of the inspection

period.

No violations or deviations were identified.

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The inspection scope and findings were sumarizea on June 17, 1988, with

those persons indicated in paragraph 1 above. The licensee acknowledged

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the NRC inspectors' findings. The licensee did not identify as

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' proprietary any of the material provided to or reviewed by the NRC

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inspectors during this inspection.