ML20116J642

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Monthly Operating Repts for Jul 1996 for Jm Farley Nuclear Plant Units 1 & 2
ML20116J642
Person / Time
Site: Arkansas Nuclear, Farley  Southern Nuclear icon.png
Issue date: 07/31/1996
From: Mcanulty M, Dennis Morey
SOUTHERN NUCLEAR OPERATING CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9608130309
Download: ML20116J642 (9)


Text

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~.: Southern Nuciser Operating Company

, . Post Offico Box 1295 BirminDham, Alabama 35201 T,eliphon. (205) 868 5131 l . .

o.v. uor.y Southern Nudear Operating Company l Vice President Farley Project the southem electoc system -

August 9, 1996 l

l Docket Nos. 50-348 l 50-364

l. U. S. Nuclear Regulatory Commission
l. ATTN: Document Control Desk Washington, D C 20555 l

Joseph M. Farley Nuclear Plant Monthly Operating Report l Ladies and Gentlemen:

Attached are the July 1996 Monthly Operating Reports for Joseph M. Farley Nuclear Plant Units 1 and 2, as required by Section 6.9.1.10 of the Technical Specifications.

l If you have any questions, please advise.

Respectfully submitted, l lLt"W Dave Morey RWC:(mor)

Attachments cc: Mr. S. D. Ebneter, Region 11 Administrator

- Mr. B. L Siegel, NRR Senior Project Manager Mr. T. M. Ross, FNP Resident Inspector i 9608130309 960731

! PDR ADOCK 05000348 R PM

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Joseph M. Farley Nuclear Plant Unit 1 Narrative Summary of Operations July 1996 l

i At 1800 on July 13,1996, with the unit operating in mode 1 at 100% reactor  :

power, the unit was ramped down to 33% reactor power to repair service j water leaks in Containment Coolers l A & 1C.  ;

All repairs were completed and the unit was returned to 100% reactor power at 0104 on July 15,1996.

There was no major safety related maintenance performed during the month.

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OPERATING DATA REPORT DOCKET NO. 50-348 l

DATE August 5,1996 COMPLETED BY M. W. McAnulty_

TELEPilONE (334) 899-5156, ext.3640 OPERATING. STATUS J

1. Unit Name: Joseph M. Farley - Unit 1 Notes 1
2. Rcporting Period: July 1996 1) Cumulative data since 12-01-77, l
3. Licensed Thermal Power (MWt): 2,652 date of commercial operation. I
4. Nameplate Rating (Gross MWe): 860 l
5. Design Electrical Rating (Net MWe): 829 j
6. Maximum Dependable Capacity (Gross MWe): 855.7 )
7. Maximum Dependable Capacity (Net MWe): 812 j
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) 5mee Last Report, Give Reasons: N/A
9. Power Level To Which Restricted, If Any (Net MWe): N/A
10. Reasons For Restrictions,If Any: N/A i

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This Month Yr. to Date Cumulative l

11. Hours in Reporting Period 744.0 5,111.0 163,631.0
12. Number Of Hours Reactor Was Critical 744.0 5,082.3 131,771.7  !
13. Reactor Reserve Shutdown Hours 0.0 0.0 3,650.0 i
14. Hours Generator On-line 744.0 5,067.0 129,742.7 1
15. Unit Reserve Shutdown Hours 0.0 0.0 0.0
16. Gross Thermal Energy Generated (MWH) 1,930,947.7 13,225,667.3 333,980,040.2
17. Gross Electrical Energy Generated (MWH) 624,089.0 4,334,617.0 107,826,771.0
18. Net Electrical Energy Generated (MWH) 591,753.0 4,116,179.0 101,855,831.0
19. Unit Senice Factor 100.0 99.1 79.3
20. Unit Availability Factor 100.0 99.1 79.3_
21. Unit Capacity Factor (Using MDC Net) 98.0 99.2 76.7
22. Unit Capacity Factor (Using DER Net) 95.9 97.1 75.1
23. Unit Forced Outage Rate 0.0 0.0 5.7

, 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

mm

25. If Shut Down at End Of Report Period, Estimated Date of Startup: N/A
26. Units In Test Status (Prior To Commercial Operation): Forecast Achieved

, Initial Criticality 08/06/7_7 08/09/77 Initial Elcetricity 08/20/77 08/18/77 Commercial Operation 12/01/77 12/01/77

4 UNIT SilUTDOWNS AND POWER REDUCTIONS '

DOCKET NO. 50-348 UNIT NAME J. M. Farley - Unit 1 DATE August 5,1996 COMPLETED BY M. W. McAnulty i REPORT MONTil July TELEPIIONE 1334) 899-5156, ext.3640 7 _

R M E E S i

T A T Y '

Y S 11 SC

, P o O TO CAUsE AND CORRECTIVE E DURATION N D ED COMPONENT ACTION TO

! No. DATE (1) (llOURS) (2) (3) LER # ME CODE (5) PREVENT RECURRENCE in mode I at 100% reactor power, the unit was l ramped down to 33% reactor power to repair service water leaks in Containment Coolers 1 A and IC. The leaks were due to corrosion <

at the tube end area of one section on each i

, cooler. The leaks were stopped by installing jblind flanges on the leaking section of eaca cooler.

All repairs were completed and the unit was returned to 100% reactor power at 0104 on 960715.

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1: 2: 3: EVENTS REPORTED i

[ F: Forced Reason Method INVOLVE A s: scheduled A - Equipment Failure (Explain) 1 - Manual GREATER TilAN 20%

i D Maintenance or Test 2 - Manual Scram REDUCTION IN

! C Refueling 3 - Automatic scram AVERAGE DAILY D - Regulatory Restriction 4 - Other (Explain) POWER LEVEL FOR E - Operator Training & License Examination TIIE PRECEDING 24 f Administrative llOURS.

G OperationalError(Explain) 11-Other(Explain)

DOCKET NO. 50-348 UNIT 1

. . DATE August 5,1996  :

COMPLETED BY M. W. McAnulty I TELEPHONE (334) 899-5156 ext 3640 MONTII July l l

DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 818 17 816  !

2 817 18 817  :

3 815 19 815 4 819 20 810 ,

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5 817 21 809 ,

6 815 22 811 7 814 23 813  !

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8 816 24 814 9 812 25 817 ,

r l 10 817 26 817 ,

11 816 27 815 12 819 28 817 ,

13 738 29 820 t

! 14 269 30 818 i

I 15 814 31 816 16 817 1

, 1 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reponing period. Compute to the nearest whole megawatt.

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l Joseph M. Farley Nuclear Plant Unit 2 Narrative Summary of Operations July 1996 There was no major safety related maintenance perfonned during the month.

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OPERATING DATA REPORT DOCKET NO. 50-364 DATE August 5,1996 l

COMPLETED BY M. W. McAnulty_

l TELEPIIONE (334) 899-5156, ext.3640 i

l OPERATING STATUS l

1. Unit Name: Joseph M. Farley - Unit 2 Notes
2. Reporting Period: _ July 1996 1) Cumulative data since 07-30-81,
3. Licensed Thermal Power (MWt)- 7652 date of commercial operation.
4. Nameplate Rating (Gross MWe): 860
5. Design Electrical Rating (Net MWe): 829 l 6. Maximum Dependable Capacity (Gross MWe): 863.6
7. Maximum Dependable Capacity (Net MWe): 822 j
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Smce Last Report, Give Reasons: N/A i

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9. Power Level To Which Restricted, if Any (Net MWe): N/A ,
10. Reasons For Restrictions, If Any: N/A j This Month Yr. to Date Cumulative
11. Ilours in Reporting Period 744.0 5,111.0 _

131,544.0 l

12. Number Ofliours Reactor Was Critical 744.0 5,111.0- 114,014.4 l
13. Reactor Reserve Shutdown llours _

0.0 0.0 138.0_ l

14. liours Generator On-line 744.0 5,111.0 112,321.2
15. Unit Reserve Shutdown liours 0.0 0.0 0.0
16. Gross Thennal Energy Generated (MWli) 1,973,088.0 13,165,403.3 286,139,193.7
17. Gross Electrical Energy Generated (MWii) 640,955.0 4,322,390.0 93,784,869.0 l 18. Net Electrical Energy Generated (MWII) 610,259.0 4,112,314.0 88,925,965.0_
19. Unit Service Factor 100.0 100.0 85.4
20. Unit Availability Factor 100.0 100.0 85.4
21. Unit Capacity Factor (Using MDC Net) 99.8 97.9 82.5
22. Unit Capacity Factor (Using DER Net) _

98.9 _

97.1 81.5

23. Unit Forced Outage Rate 0.0 0.0 3.8 l 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

l Refueling Outage scheduled for October 12,1996 with a duration of 48 days l 25. If Shut Down at End Of Report Period, Estimated Date of Startup: N/A

26. Units In Test Status (Prior To Commercial Operation): Forecast Achieved Initial Criticality 05/06/81 05/08/81 Initial Electricity 05/24/81 05/25/81 Commercial Operation 08/01/81 07/30/81 i

, i UNIT SHUTDOWNS AND POWER REDUCTIONS

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. - . DOCKET NO. 50-364 UNIT NAME .I. M. Farley - Unit 2 DATE August 5,1996 COMPLETED BY M. W. McAnuity REPORT MONTil - July TELEPilONE (334) 899-5156, ext.3640 R M E E S T A T Y Y S II SC P O O TO CAUSE AND CORRECTIVE E DURATION N D ED COMPONENT ACTION TO NO. DATE (1) (IIOURS) (2) (3) LER # ME CODE ($) PREVENT RECURRENCE I L. -

_ _.d There were no Shutdowns Or power reductions during the month.

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I i: 2: 3: EVINTS REPORTED F: Forced Reason Method INVOLVE A S: Scheduled A - Equipment failure (Explain) 1 - Manual GREATER TilAN 20%

B - Maintenance or Test 2 - Manual Scram REDUCTION IN C Refueling 3 - Automatic Scram AVERAGE DAILY D - Regulatory Restriction 4 Other(Explain) POWER LEVEL rOR E - Operator Training & License Examination TIIE PRECEDINO 24 F- Administrative llOURS. j G Operational Error (Explain)

II-Other(Explain)  !

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DOCKET NO. 50-364

- UNIT 2 August 5,1996

. _ ,, DATE COMPLETED BY M. W. McAnuity l TELEPHONE (334) 899-5156 ext 3640 l

MO'4TH July l DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) j I 822 17 821 ,

2 820 18 820 3 820 19 819 l

l 4 824 20 814 l

l 5 821 21 814 l

6 819 22 816 7 817 23 818 )

8 821 24 820 9 817 25 823 10 823 26 823 11 _

822 27 820 12 823 28 823 13 820 29 826 I

14 818 30 823 15 820 31 822_

16 822 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting period. Compute to the nearest whole megawatt.