ML20202G421
| ML20202G421 | |
| Person / Time | |
|---|---|
| Site: | Farley |
| Issue date: | 01/31/1998 |
| From: | Mcanulty M, Dennis Morey SOUTHERN NUCLEAR OPERATING CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NUDOCS 9802200125 | |
| Download: ML20202G421 (5) | |
Text
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Dave Morey Southern Nuclear Vice Presdent Operating Company
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Fadey Project PO B0 1295 Birmingham. Alabama 35201 Tel 205.992.5131 i
4 February 10, 1998 SOUTHERN h COMPANY Energy to Serve nurWorld' Docket Nos.
50-348 50-364 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D C 20555 Joseph M. Farley Nuclear Plant Monthly Operatina Report Ladies and Gentlemen:
Enclosed are the January 1998 Monthly Operating Reports for Joseph M. Farley Nuclear Plant Units I and 2, as required by Section 6.9.1.10 of the Technical Specifications.
If you have any questions, please advise.
Respectfully submitted, h ( )}lf Dave Morey i
RWC:(mor)
Enclosures
- 1. January Monthly Operating Report for P? ant Farley Unit 1
- 2. January Monthly Operating Report for Plant Farley Unit 2 cc: Mr. L. A. Reyes, Region 11 Administrator Mr. J.1. Zimmerman, NRR Project Manager Mr. T. M. Ross, FNP Sr. Resident inspector i
9802200125 980131 l
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OPERATING DATA REPORT DOCKET No.:
50-348 UNIT NAME:
J. M. Farley Unit 1 DATE:
February 2,1998 COMPLETED BY:
M. W. McAnuity TELEPIIONE:
(334) 899 5156, ext.3640 OPIRATING STATUS 1.
Reporting Period:
January 1998 2.
Design Electrical Rating (Net MWe):
829 3.
Maximum Dependable Capacity (Net MWe):
822 ThisAtonth Year _toSate Cumulative 4.
Number OfIlours Reactor Was Critical:
744.0 744.0 143,025.6 5.
Ilours Generator On line:
744.0 744.0 140,963.4 6.
Unit Reserve Shutdown Ilours:
0.0 0.0 0.0 7.
Net Electrical Energy Generated (MWII):
618,677.0 618,677.0 110,919,005.0 CIIALLENGES TO PRESSURIZER PORY OR PRESSURIZER SAFETY VALVES Date i Tag No.
I Event Description There were no challenges to Pressurizer PORV or Pressurizer Safety Valves.
El-1
UNIT SHUTDOWNS DOCKET NO.:
50 348 UNIT NAME:
J. M. Farley Un:t 1 DATE:
February 2,1998 COMPLETED BY:
M. W. McAnultL REPORTING PERIOD: January.1998 TELEPIIONE:
(334) 899 5156, ext.3640 Type Method of F: Forced Duration Reason Shutting Down Cause/ Corrective Actions No.
Date S: scheduled j (llours)
(1)
(2)
Comments There were no unit shutdowns during the month, t1) Kt.AhWN.
til Mt.4 IIUU.
A I:quipment raiture (Explain)
I. Manual D Maintenance or Test 2 ManualTrip/ Scram C - Refueling 3 Automatic Trip / Scram D. Regulatory Restriction 4 Continuation E Operator Training /t.icense Examination 5 - Other (Explain)
F. Administrative o -Operational Error (Explain) 11.Other (Explain)
CAUSE/ CORRECTIVE ACTION / COMMENTS 4
NARRATIVE REPORT There were no significant power reductions or major safety related maintenance during the month.
El-2
OPERATING DATA REPORT DOCKET No.:
50-364 UNIT NAME:
J. M. Farley Unit 2 DATE:
February 2,1998 COMPLETED BY:
M. W. McAnuity TELEPIIONE:
(334) 899-5156, ext.3640 t
OPERATJKGETAT11S 1.
Reporting Period:
January 1998 2.
Design Electrical Rating (Net MWe):
829 3.
Maximum Dependable Capacity (Net MWe):
828 IhitMonth Year _to_Date Cumulative 4.
Number Of Hours Reactor Was Critical:
744.0 744.0 125,621.0 5.
Hours Generator On-line:
744.0 744.0 123,874.9 6.
Unit Reserve Shutdown Hours:
0.0 0.0 0.0 7.
Net Electrical Energy Generated (MWH):
627,105.0 627,105.0 98,458,469.0 CIIALLENGES TO PRESSURIZER PORY OR PRESSURIZER SAFETY VALVES Date i Tag No.
I Event Description There were no challenges to Pressurizer PORV or Pressurizer Safety Valves.
E2-1
UNIT SilUTDOWNS DOCKET NO.:
50 364 UNIT NAME:
J. M. Farley Nnit 2 DATE:
February 2,1998 COMPLETED BY:
M. W. McAnuity__
REPORTING PERIOD: January 1998 TELEPilONE:
(334) 899-5156, ext.3640 Type Method of F: Forced Duration Reason Shutting Down Cause/ Corrective Actions No.
Date S: Scheduled (Hours)
(1)
(2)
Comments There were no unit shutdowns during the month.
(1) KI ASUN.
(4) MLillVLA A Equipment railure (Explain)
I. Manual l
D Maintenance or Test 2 ManualTrip5 cram C. Refocling 3 Au9matic Trip / Scram D. Regulatory Restriction
- 4. Continuation E. operator Traininga.icense Examination 5.Other (Explain)
F. Administrative G. Operational Error (Explain)
- 11. other (Explain)
CAUSE/ CORRECTIVE ACTION / COMMENTS NARRATIVE REPORT There were no significant power reductions or major safety related maintenance during the month.
E2-2
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