ML20202G421

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Monthly Operating Repts for Jan 1998 for Jm Farley Nuclear Plant,Units 1 & 2
ML20202G421
Person / Time
Site: Farley  Southern Nuclear icon.png
Issue date: 01/31/1998
From: Mcanulty M, Dennis Morey
SOUTHERN NUCLEAR OPERATING CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9802200125
Download: ML20202G421 (5)


Text

-_-, - - . ~. - - -

Dave Morey Southern Nuclear

.* Vice Presdent  !

Operating Company

. Fadey Project PO B0 1295 )

Birmingham. Alabama 35201 Tel 205.992.5131 i

. 4 February 10, 1998 SOUTHERN h COMPANY ,

Energy to Serve nurWorld' l Docket Nos. 50-348 50-364 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D C 20555 Joseph M. Farley Nuclear Plant Monthly Operatina Report Ladies and Gentlemen:

Enclosed are the January 1998 Monthly Operating Reports for Joseph M. Farley Nuclear Plant Units I and 2, as required by Section 6.9.1.10 of the Technical Specifications.

If you have any questions, please advise.

Respectfully submitted, h ( )}lf Dave Morey i

RWC:(mor)

Enclosures

1. January Monthly Operating Report for P? ant Farley Unit 1
2. January Monthly Operating Report for Plant Farley Unit 2 cc: Mr. L. A. Reyes, Region 11 Administrator Mr. J.1. Zimmerman, NRR Project Manager Mr. T. M. Ross, FNP Sr. Resident inspector i

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OPERATING DATA REPORT DOCKET No.: 50-348 UNIT NAME: J. M. Farley Unit 1 DATE: February 2,1998 COMPLETED BY: M. W. McAnuity TELEPIIONE: (334) 899 5156, ext.3640 OPIRATING STATUS

1. Reporting Period: January 1998
2. Design Electrical Rating (Net MWe): 829
3. Maximum Dependable Capacity (Net MWe): 822 ThisAtonth Year _toSate Cumulative
4. Number OfIlours Reactor Was Critical: 744.0 744.0 143,025.6
5. Ilours Generator On line: 744.0 744.0 140,963.4
6. Unit Reserve Shutdown Ilours: 0.0 0.0 0.0
7. Net Electrical Energy Generated (MWII): 618,677.0 618,677.0 110,919,005.0 CIIALLENGES TO PRESSURIZER PORY OR PRESSURIZER SAFETY VALVES Date i Tag No. I Event Description There were no challenges to Pressurizer PORV or Pressurizer Safety Valves.

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UNIT SHUTDOWNS DOCKET NO.: 50 348 UNIT NAME: J. M. Farley Un:t 1

, DATE: February 2,1998 COMPLETED BY: M. W. McAnultL REPORTING PERIOD: January.1998 TELEPIIONE: (334) 899 5156, ext.3640 Type Method of F: Forced Duration Reason Shutting Down Cause/ Corrective Actions No. Date S: scheduled j (llours) (1) (2) Comments There were no unit shutdowns during the month, t1) Kt.AhWN. til Mt.4 IIUU.

A I:quipment raiture (Explain) I . Manual D Maintenance or Test 2 ManualTrip/ Scram C - Refueling 3 Automatic Trip / Scram D. Regulatory Restriction 4 Continuation E Operator Training /t.icense Examination 5 - Other (Explain)

F. Administrative o -Operational Error (Explain) 11.Other (Explain)

CAUSE/ CORRECTIVE ACTION / COMMENTS 4 NARRATIVE REPORT There were no significant power reductions or major safety related maintenance during the month.

El-2

OPERATING DATA REPORT DOCKET No.
50-364 UNIT NAME: J. M. Farley Unit 2 DATE: February 2,1998 COMPLETED BY: M. W. McAnuity TELEPIIONE: (334) 899-5156, ext.3640 t

OPERATJKGETAT11S

1. Reporting Period: January 1998
2. Design Electrical Rating (Net MWe): 829
3. Maximum Dependable Capacity (Net MWe): 828 IhitMonth Year _to_Date Cumulative
4. Number Of Hours Reactor Was Critical: 744.0 744.0 125,621.0
5. Hours Generator On-line: 744.0 744.0 123,874.9
6. Unit Reserve Shutdown Hours: 0.0 0.0 0.0
7. Net Electrical Energy Generated (MWH): 627,105.0 627,105.0 98,458,469.0 CIIALLENGES TO PRESSURIZER PORY OR PRESSURIZER SAFETY VALVES Date i Tag No. I Event Description There were no challenges to Pressurizer PORV or Pressurizer Safety Valves.

E2-1

,... UNIT SilUTDOWNS DOCKET NO.: 50 364 UNIT NAME: J. M. Farley Nnit 2

, DATE: February 2,1998 COMPLETED BY: M. W. McAnuity__

REPORTING PERIOD: January 1998 TELEPilONE: (334) 899-5156, ext.3640 Type Method of F: Forced Duration Reason Shutting Down Cause/ Corrective Actions No. Date S: Scheduled (Hours) (1) , (2) Comments There were no unit shutdowns during the month.

(1) KI ASUN. (4) MLillVLA A Equipment railure (Explain) I . Manual l D Maintenance or Test 2 ManualTrip5 cram C. Refocling 3 Au9matic Trip / Scram D. Regulatory Restriction 4. Continuation E. operator Traininga.icense Examination 5.Other (Explain)

F. Administrative G. Operational Error (Explain)

11. other (Explain)

CAUSE/ CORRECTIVE ACTION / COMMENTS NARRATIVE REPORT There were no significant power reductions or major safety related maintenance during the month.

E2-2

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