Similar Documents at Surry |
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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML20086S5861984-09-10010 September 1984 SR-S1-74-03:on 740403,safety Injection Experienced Due to Spurious High Steam Flow Signals in Conjunction W/Low Temp Average or Low Steam Line Pressure Signals.Caused by Fluctuations of Steam Flow Signals Above Setpoint ML20087B9541975-10-17017 October 1975 Telecopy AO:751011,containment Leak Rate Tests Revealed Containment Leakage Rate Greater than Acceptable Criteria ML20087B9651975-10-16016 October 1975 Telecopy AO:on751015,recirculation of Boron Injection Tank 2 Interrupted for Period of 15 Minutes.Caused by Failure of Boric Acid Transfer Pump D Motor ML20087C0771975-10-0101 October 1975 Telecopy Ao:On 750928,during Refueling Performance Test 18.2,safety Injection Master Relay Failed to Latch,Violating Tech Spec 3.3 ML20087C1041975-09-25025 September 1975 Telecopy Ao:On 750924,loop a Instrumentation Drifted Low Resulting in Safety Sys Setting Being Less Conservative than Tech Spec Limit ML20087B8501975-08-25025 August 1975 Telecopy Ao:On 750823,channel of Protection Found Unconservative Due to Failure of Resistance Temp Detector ML20087B7821975-08-25025 August 1975 Telecopy Ao:On 750823,leak Developed in Boric Acid Transfer Sys Decreasing Level in Boric Acid Storage Tank C Below Tech Spec Limit ML20087B8921975-08-22022 August 1975 Telecopy Ao:On 750822,channel of Protection Found Unconservative Due to Failure of Resistance Temp Detector ML20087B9321975-08-0707 August 1975 Telecopy Ao:On 750807,boron Injection Tank Recirculation Valves TV-2884 A,B & C Found in Closed Position ML20087C1461975-07-30030 July 1975 Telecopy Ao:On 750729,boron Concentration in Boron Injection Tank 2 Found to Be 11.4% ML20087C1691975-07-21021 July 1975 Telecopy Ao:On 750720 Low Level Amplifier Failed Causing One Temp Change Protection Channel to Be Unconservative ML20087C2041975-07-0707 July 1975 Telecopy Ao:On 750706,reactor Trip Occurred.Caused by Sudden Closure of Trip Valve in Main Steam Line B.Investigation Underway to Determine Cause of Malfunction & Corrective Action ML20087C2241975-07-0101 July 1975 Telecopy Ao:On 750630,discovered That Undervoltage Reactor Trip Circuit Inoperable ML20086Q3091975-05-21021 May 1975 Notifies That AO Reported on 750514 Re Perforation of Fuel Assembly During Fuel Operation in Error.Perforation Occurred During Normal Operation.Rept No Longer Considered AO ML20086Q2891975-05-16016 May 1975 Telecopy Ao:On 750516,chemical Addition Tank Valve MOV-CS-10IB Failed to Operate Properly ML20086Q3261975-05-14014 May 1975 Telecopy Ao:On 750513,manipulator Crane Stopped Due to Overload.Caused by Perforation in Fuel Clad ML20086Q3681975-05-0101 May 1975 Telecopy Ao:On 750430,emergency Diesel Generator 3 Failed While in Svc Due to Internal Problem in turbo-blower ML20086Q5871975-04-28028 April 1975 Telecopy Ao:On 750427,consequence Limiting Safeguards Channel 3,Train B Matrix Relay Coil Found to Be Open Circuit During Performance Test 8.5A ML20086Q6211975-04-28028 April 1975 Ao:On 750427,sample Sys Trip Valve on Pressurizer Relief Tank Failed to Stroke on Initiation of Safety Injection During Performance Test 18.2 ML20086Q5111975-04-28028 April 1975 Telecopy Ao:On 750427,circulating Water Sys Valve MOV-CW-206D Failed to Shut After Receiving Close Signal ML20086S4491975-03-26026 March 1975 Corrections to AO-S2-74-09 Re Steam Generator Support Couplings.Studs Not Welded to Encl Plate as Previously Reported Due to Potential Welding Problems ML20086R0291975-02-24024 February 1975 AO-S1-75-01:on 750118,boron Concentration Observed to Be 1,842 Ppm & Primary Grade Water Flow Controller 1114A Found in Manual Mode of Operation W/Demand Position Corresponding to Full Open Position of Valve FCV-1114A ML20086Q9391975-02-24024 February 1975 AO-S1-75-02:on 750118,containment Isolation Valves 2-IA-446 & 2-IA-447 Found Open.Caused by Operator Error.Operators Advised of Importance of Following Procedures & Verifying Actions ML20086Q9291975-02-24024 February 1975 AO-S1-75-03:on 750115,process Vent Particulate Monitor Alarm Occurred Followed by Ventilation Vent Particulate Monitor Alarm.Caused by Pressure Control Valve PCV-GW-107 Stuck Open Causing Relief Valve RV-GW-107 to Lift ML20086Q7671975-02-18018 February 1975 Telecopy Ao:On 750217,core Quadrant Tilt of 2.2% Existed W/Reactor at 100% Power ML20086Q8181975-02-18018 February 1975 Telecopy Ao:On 750215,overpower Low Level Amplifier Failed Causing Inoperable Overpower Protection ML20086Q7801975-02-14014 February 1975 Telecopy Ao:On 750214,steam Generator Narrow Range Level Detector Drifted High.Cause Not Determined ML20086S4261975-02-14014 February 1975 AO-S2-74-10:on 741129,unsatisfactory Leakage Ovserved While Performing Periodic Test 16.4.Caused by Stress to Four Keyways of Rockshaft Due to Valve Closure.Counterweights Modified & Repositioned on Weight Lever ML20086Q8771975-02-14014 February 1975 Telecopy Ao:On 750214,pressurizer Pressure Comparator Failed.Caused by Setpoint Drift.Comparator Replaced ML20086Q8941975-02-0303 February 1975 Telecopy Ao:On 750201,steam Generator Blowdown Activity Not Continuously Recorded & Monitored by Steam Generator Blowdown Sample Monitor Sys ML20086R0801975-01-24024 January 1975 AO-S2-75-02:on 750110,channel 1 of Steam Generator C Level Instrumentation Indication Drifted Beyond Allowable Limits. Caused by Packing Leak at Isolation Valve.Replacement of Packing Will Be Performed as Necessary to Minimize Leakage ML20086R1891975-01-24024 January 1975 AO-S2-75-01:on 750109,discovered High Water Level Existed in Sump Area of High Pressure Heater Drain Pump.Caused by Turbine Bldg Sump Pumps Shut Off for Test.Test Instructions Revised to Require Surveillance ML20086S3061975-01-23023 January 1975 AO-S1-74-16:on 741220,radiation Monitor Alarm Accurred on RM-SW-107 Which Monitors Svc Water Leaving Component Cooling Hxs.Caused by Pin Holes in Component Cooling HX 1-CC-E-1C Tubes.Hx Isolated from Svc Water Sys ML20086S3171975-01-23023 January 1975 AO-S1-74-15:on 741219,abnormal Degradation Found of One of Several Boundaries Designed to Contain Radioactive Matls Resulting from Fission Process.Caused by Sheet Sludge Deposits & Deleterious Effects of Sodium Phosphate Control ML20086Q9471975-01-20020 January 1975 Telecopy Ao:On 750119,two Valves in Station Instrument Air Supply to Containment Instrument Air Sys Found Open.Valves Shut & Locked ML20086Q9671975-01-20020 January 1975 Telecopy Ao:On 750118,chemical Vol & Control Sys Found Open Causing Dilution of Primary Coolant Sys ML20086S3471975-01-10010 January 1975 AO-S1-74-13:on 741107,tube Rupture Occurred in Component HX 1-CC-E-1D.Caused by Equipment Malfunction.Hx Isolated & Component Cooling Surge Tank Refilled & Observed to Verify No Further Leakage ML20086R0961975-01-10010 January 1975 Telecopy Ao:On 750110,control Room Log Readings Indicated Level Transmitter 2-1T-494 Drifted Above Prescribed Limits. Transmitter Trip Bistables Deenergized ML20086S4301975-01-10010 January 1975 Telecopy Ao:On 750109,valve Pit Containing Svc Water Valves MOV-SW-203 A-D Became Flooded.Condition May Have Temporarily Incapacitated Heat Removal Feature of Recirculation Spray Sys ML20086S3321975-01-0303 January 1975 AO-S1-74-14:on 741119,magnetic Amplifiers for Low Level Alarm LS-CW-1018 & Turbine Trip LS-CW-101C Found Out of Calibr.Caused by Changes in Temp & Humidity & Aging of Components.Test Initiated to Verify Calibr ML20086S2931974-12-31031 December 1974 Ao:On 741230,crack Found in Containment Spray Check Valve. Containment Spray Check Valve & All Cracked Rackshafts Being Replaced ML20086S3611974-12-20020 December 1974 Telecopy Ao:On 741219,tube Leaks in Component Cooling HX Resulted in Low Level Release of Radioactive Component Cooling Water Into James River.Source of Leakage Located & Repaired.Hx Isolated ML20086S3691974-12-19019 December 1974 Ao:On 741218,steam Generator Tube Wall Deterioration Found in Excess of 50% in 137 Tubes ML20086S4371974-12-16016 December 1974 AO-S2-74-09:on 741017,cracks Discovered in Some Steam Generator Lower Ring Support Swivel End Couplings.Caused by Lateral Load in Direction of Reactor Pressure Vessel.Support Couplings Redesigned ML20086S4621974-10-25025 October 1974 AO-S2-74-09:on 741017,cracks Found in Concrete Supporting Steam Generator A.All Couplings Being Removed to Be Radiographed & Inspected.Rept Will Be Submitted by 750103 ML20086S8821974-10-22022 October 1974 AO-S2-74-06:on 740803,during Six Degree Freedom of Movement Portion of PT-14,no Response Received from Any of Three Valves.On Second Test of TV-MS-201B W/Air Bled from Cylinders,Valve Went Fully Closed ML20086S5731974-10-0101 October 1974 AO-S2-74-08:on 740912,neither Fuel Oil Supply Flow Paths for Emergency Diesel Generator 2 Operable.Caused by Solenoid Valves Disconnected in Terminal Box.Personnel Instructed in Procedure ADM-37 ML20086S5761974-09-26026 September 1974 AO-S2-74-07:on 740810,summator TM-2-412G Drift Allowed Overpower Trip Setpoint to Be Approx 5% High.Caused by Defective Summator.Summator Removed & Replaced & Module Calibr ML20086S5781974-09-26026 September 1974 AO-S1-74-11:on 740820,during Depressurization Procedure, Alarm Indicated High Surge Tank Pressure Received in Control Room.Cause Not Listed.Overhead Gas Compressor Stopped & Pressure within Gas Stripper Surge Tank Reduced ML20086S5841974-08-21021 August 1974 AO-S1-74-10:on 740802,one Spent Fuel Pit to Boron Recovery Sys Temporary Hose Line Connection Separated from Fitting, Spraying Primary Grade Pump House Interior.Caused by Inadequate Design of Clamping Arrangement 1984-09-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML18152B3531999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Surry Power Station,Units 1 & 2.With 991012 Ltr ML18152B6651999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Surry Power Station Units 1 & 2.With 990915 Ltr ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18151A3981999-08-13013 August 1999 SPS Unit 2 ISI Summary Rept for 1999 Refueling Outage. ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B3791999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Surry Power Station,Units 1 & 2.With 990811 Ltr ML18152B3911999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Surry Power Station,Units 1 & 2.With 990713 Ltr ML18152B4341999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Surry Power Station,Units 1 & 2.With 990614 Ltr ML20195E2401999-05-31031 May 1999 Rev 2 to COLR for SPS Unit 2 Cycle 16 Pattern Ag ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4161999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Surry Power Station Units 1 & 2.With 990512 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18152B6511999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Surry Power Station Units 1 & 2 ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7331999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Surry Power Station,Units 1 & 2.With 990310 Ltr ML18152B5421999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Surry Power Station,Units 1 & 2.With 990210 Ltr ML18151A3031999-01-29029 January 1999 ISI Summary Rept for 1998 Refueling Outage,Including Form NIS-1, Owners Rept for ISIs & Form NIS-2, Owners Rept for Repairs & Replacements. ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B6011998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Surry Power Station,Units 1 & 2.With 990115 Ltr ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B7081998-11-30030 November 1998 Rev 0 to COLR for Surry 1 Cycle 16,Pattern Un. ML18152B5721998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Surry Power Station,Units 1 & 2.With 981214 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6241998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Surry Power Station Units 1 & 2.With 981111 Ltr ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B6881998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Surry Power Station Units 1 & 2.With 981012 Ltr ML18153A3271998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Surry Power Station,Units 1 & 2 ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A3161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Surry Power Station Units 1 & 2.W/980807 Ltr ML18152B7621998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Surry Power Station,Units 1 & 2.W/980707 Ltr ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML18153A3141998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Surry Power Station,Units 1 & 2.W/980610 ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B8161998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Surry Power Station Units 1 & 2.W/980508 Ltr ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML20217P9941998-04-0707 April 1998 Safety Evaluation Granting Licensee Third 10-yr Inservice Insp Program Relief Requests SR-018 - Sr-024 ML18153A2951998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Sps,Units 1 & 2.W/ 980408 Ltr ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket 1999-09-30
[Table view] |
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i Ur. Wornen C. Moseley, Dircctor Serial No. 203 Directorato of Regulatory Operations POMf/JTBaclw Unit.cd States Atonic Energy Co::cinaion Region II - Suita 818 Docket No. 50-281 230 Peachtreo Street, Northvcot Licenso No. DPR-37 Aticata, Goorgia 30303
Dear Mr. Moucicy:
Pursuant to Surry Power Station Technical Specification 6.6.3.1, the Virginia Electric and Pover Coc:pany hereby culmits ferty (40) cepion of' Abnoreal Occurrence Report No. AO-S2-74-04.
The cubstance of this rcport han been revicued by the Station Nucicar Safety e-nd Operating Con:nitteo cud will be placed on the agenda for the 3
next necting of tha Systca Nuclear Sciety and Operating Crm'itteo.
Very truly yourc,
&,t/ ,' ' lyt s't fn C. M. Stall.ings ,
Vico Procident-Pcvor Supply and Production Operationa l Enclosurco 40 copica of.A0-32-74-04 ! +
cc: Mr. K. R. Collor, Assistant Director v
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for Operating Reactors 6533
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REPORT NO. A0-S2-74-04 i
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O. O I. INTRODUCTION In accordance with Technical Specification 6.6.B.1 for Surry Power Station, Operating License Number'DPR-37, this report describes an abnormal occurrence which was identified on June 27, 1974. The Directorate
, of Regulatory Operations, Region II, was notified on June 28, 1974.
The occurrence reported herein is classified as an abnormal occurrence pursuant to Technical Specification 1.0.I.6 which states that "An abnormal occurrence is defined as: Engineered Safeguard System malfunction or other component or system malfunction which rendered or could render the Engineered Safeguard System incapable of performing its intended safety function." The occurrence described herein resulted in the failure of the three (3) main steam non-return valves (NRV's).
II.
SUMMARY
OF THE OCCURRENCE On June 17, 1974, following an extended shutdown period for maintenance and reactor coolant pump modifications, unit start-up commenced. As the reactor approached approximately four'(4) per cent of rated power, instrumentation ~ indicated that main steam non-return valve "C" had not opened. The unit was brought to a_ hot- _
shutdown condition to' free the valve. The main steam trip valves
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were closed and the' secondary-steam header pressure reduced using the steam dump valve. With a pressure differential of 225 psi.across' the valve, the valve opened. The "C" NRV was cycled utilizing.the motor operator and steam, pressure, and all parameters indicated the valve.was fully operational. Therefore,. start-up was resumed.' ,
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As reactor power increased, temperature; pressure and steam flow
. Indications from "B"' steam generator were different.than'those oft s team - generators "A" and "C.
'It appeared that1"B" NRV'was not
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fully opening with the steam flow. -Attempts were made to increase the flow through "B" NRV by manipulating the valve piston and to increase the differential pressure across the valve by increasing the power level. Both methods proved' unsuccessful. The unit was brought to cold shutdown condition and all three (3) non-return valves were dis-
- mantled for inspection. The valve' manufacturer, Rockwell Manufacturing Company, was contacted and a representative was present when the valves were dismantled. As the piston / disc unit was removed from
- "C" NRV, it was discovered that the disc had separated from the assembly. Subsequent investigation of "A" and "B" NRV's revealed similar failures. Following onsite preliminary evaluations, the disc and piston parts were shipped to the manufacturer.
111. ANALYSIS OF OCCURRENCE Three (3) non-return valves are' installed in the main steam a
lines between the main steam trip valves and the main steam header, and are located outside the containment in a missile-protected-enclosure. The internals of the _stellited disc are joined to the
, piston by means of a filleted butt weld at the disc. Tlie function 4
of the piston / disc' unit.is to prevent reverse steam flow. The valve
. ster is normally withdrawn to permit unobstructed movement of the' t
piston / disc, although, when-necessary, it is inserted against the disc'to' block steam flow.
i Following1 the removal of.the piston'_section from "C" non-return valve, station personnel performed a dye penetrant test to-determine -
j if additional damage' to the internals had occurred. An internal-t -
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rh y (v inspection of "B" non-return valve revealed that the separated disc had stuck at a point in the valve body. This had prevented full steam flow through the valve.
An independent testing laboratory was requested to perform an analysis of the valve failure. Their preliminary findings indicated that a crack had initiated at the inside surface of the piston assembly, above the weld that joins the disc to the piston. This crack propagated by fatigue, until failure occurred. In addition, it was noted that a thinning of the piston wall had occurred at and around the point of failure.
The valve manufacturer, after preliminary evaluation of the failed piston / disc assemblies determined that the failure was the result of nonuniform forces imposed on the disc during prolonged unit start-ups. The steam initially produced at start-up has a high moisture content. This low quality steam impinges on the disc, imparting a greater force than normally experienced with the production of high quality steam. Steam builds up beneath the disc until sufficient pressure has been produced to lift the disc / piston assembly off its seat. The lift force on the disc is greater at the point of steam exit than at any other point on the disc. This nonuniform force exerted on the disc is increased by the steam's high moisture content. During a unit start-up, this cyclic pressure buildup and release, or perking, may continue for several hours.
This perking of the valve disc, together with thermal gradient buildup, caused the failure.
IV. CORRECTIVE ACTION TO PREVENT RECURRENCE The damage to the "B" non-return valves body was corrected by grinding and the valve seats were lapped.
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As prenously stated, the valve manufacturer was contacted, and a
- design modification was developed. The modification will consist of re-placing the Schedule 100 pipe of the present piston assembly with Schedule i 160 pipe, and installing a transition. piece between the assembly and the disc. The transition piece will afford the machining of a larger radius from the piston to the disc, thus reducing thermal gradients and lowering stress intensity. The larger radius and the increased wall thickness of the piston will enhance the dampening of nonuniform forces normally experienced during start-ups.
Three (3) piston / disc assemblies of the old design have been in-stalled on Unit Nos. 1 and 2. With the installation of the old designed internals, a maximum limit of 75 hours8.680556e-4 days <br />0.0208 hours <br />1.240079e-4 weeks <br />2.85375e-5 months <br /> " perking" time per -
valve has been established to prevent failure of the valves due to prolonged periods of stress. This limit is approximately 25 per cent of the " perking" hours experienced by the valves which failed. In the event that this limit is attained, prior tn refueling in September 1974 for Unit No. I and November 1974 for Unit No. 2,:the unit will i
be shutdown and ;he new piston / disc assemblies will.be installed.
The valves will be modified on Unit No. I and Unit No. 2 during the refueling outage, scheddled for September and November 1974,,respectively.
The non-return valves on Unit No. I were disassemblied and inspected, with no degradation detected. However, as a precautionary measure new piston / disc assemblies of_the old design were installed.
The licensee has experienced no previous failures of the' main steam non-return valves (Rockwell Manufacturing, Model 607 MY), and considers the proposed modification of the piston / disc. assembly to be 1
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V. ANALYSIS AND EVALUATION OF SAFETY IMPLICATIONS OF THE OCCURRENCE Each main steam line has a fast closing trip valve and a non-return valve. These six (6) valves prevent blowdown of more than one steam generator for any steam break location, even if one valve fails to close. The occurrence described herein could have rendered a portion of the engineering safeguards system incapable of performing its intended function. However, the main steam trip valves were operable the entire time and would have precluded the blowdown of more than one steam generator.
Based on the above, there were no significant safety implications associated with this occurrence.
V1. CONCLUSIONS The licensee concludes that:
- 1. The failure of "A", "B", and "C" non-return valves internals was due to cyclic fatigue stresses ex-perienced during prolonged start-up periods.
- 2. The occurrence described herein did not affect the safe operation of the station.
- 3. The occurrence described herein did not affect the health or safety of the general public.
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