Similar Documents at Surry |
---|
Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML20086S5861984-09-10010 September 1984 SR-S1-74-03:on 740403,safety Injection Experienced Due to Spurious High Steam Flow Signals in Conjunction W/Low Temp Average or Low Steam Line Pressure Signals.Caused by Fluctuations of Steam Flow Signals Above Setpoint ML20087B9541975-10-17017 October 1975 Telecopy AO:751011,containment Leak Rate Tests Revealed Containment Leakage Rate Greater than Acceptable Criteria ML20087B9651975-10-16016 October 1975 Telecopy AO:on751015,recirculation of Boron Injection Tank 2 Interrupted for Period of 15 Minutes.Caused by Failure of Boric Acid Transfer Pump D Motor ML20087C0771975-10-0101 October 1975 Telecopy Ao:On 750928,during Refueling Performance Test 18.2,safety Injection Master Relay Failed to Latch,Violating Tech Spec 3.3 ML20087C1041975-09-25025 September 1975 Telecopy Ao:On 750924,loop a Instrumentation Drifted Low Resulting in Safety Sys Setting Being Less Conservative than Tech Spec Limit ML20087B8501975-08-25025 August 1975 Telecopy Ao:On 750823,channel of Protection Found Unconservative Due to Failure of Resistance Temp Detector ML20087B7821975-08-25025 August 1975 Telecopy Ao:On 750823,leak Developed in Boric Acid Transfer Sys Decreasing Level in Boric Acid Storage Tank C Below Tech Spec Limit ML20087B8921975-08-22022 August 1975 Telecopy Ao:On 750822,channel of Protection Found Unconservative Due to Failure of Resistance Temp Detector ML20087B9321975-08-0707 August 1975 Telecopy Ao:On 750807,boron Injection Tank Recirculation Valves TV-2884 A,B & C Found in Closed Position ML20087C1461975-07-30030 July 1975 Telecopy Ao:On 750729,boron Concentration in Boron Injection Tank 2 Found to Be 11.4% ML20087C1691975-07-21021 July 1975 Telecopy Ao:On 750720 Low Level Amplifier Failed Causing One Temp Change Protection Channel to Be Unconservative ML20087C2041975-07-0707 July 1975 Telecopy Ao:On 750706,reactor Trip Occurred.Caused by Sudden Closure of Trip Valve in Main Steam Line B.Investigation Underway to Determine Cause of Malfunction & Corrective Action ML20087C2241975-07-0101 July 1975 Telecopy Ao:On 750630,discovered That Undervoltage Reactor Trip Circuit Inoperable ML20086Q3091975-05-21021 May 1975 Notifies That AO Reported on 750514 Re Perforation of Fuel Assembly During Fuel Operation in Error.Perforation Occurred During Normal Operation.Rept No Longer Considered AO ML20086Q2891975-05-16016 May 1975 Telecopy Ao:On 750516,chemical Addition Tank Valve MOV-CS-10IB Failed to Operate Properly ML20086Q3261975-05-14014 May 1975 Telecopy Ao:On 750513,manipulator Crane Stopped Due to Overload.Caused by Perforation in Fuel Clad ML20086Q3681975-05-0101 May 1975 Telecopy Ao:On 750430,emergency Diesel Generator 3 Failed While in Svc Due to Internal Problem in turbo-blower ML20086Q5871975-04-28028 April 1975 Telecopy Ao:On 750427,consequence Limiting Safeguards Channel 3,Train B Matrix Relay Coil Found to Be Open Circuit During Performance Test 8.5A ML20086Q6211975-04-28028 April 1975 Ao:On 750427,sample Sys Trip Valve on Pressurizer Relief Tank Failed to Stroke on Initiation of Safety Injection During Performance Test 18.2 ML20086Q5111975-04-28028 April 1975 Telecopy Ao:On 750427,circulating Water Sys Valve MOV-CW-206D Failed to Shut After Receiving Close Signal ML20086S4491975-03-26026 March 1975 Corrections to AO-S2-74-09 Re Steam Generator Support Couplings.Studs Not Welded to Encl Plate as Previously Reported Due to Potential Welding Problems ML20086R0291975-02-24024 February 1975 AO-S1-75-01:on 750118,boron Concentration Observed to Be 1,842 Ppm & Primary Grade Water Flow Controller 1114A Found in Manual Mode of Operation W/Demand Position Corresponding to Full Open Position of Valve FCV-1114A ML20086Q9391975-02-24024 February 1975 AO-S1-75-02:on 750118,containment Isolation Valves 2-IA-446 & 2-IA-447 Found Open.Caused by Operator Error.Operators Advised of Importance of Following Procedures & Verifying Actions ML20086Q9291975-02-24024 February 1975 AO-S1-75-03:on 750115,process Vent Particulate Monitor Alarm Occurred Followed by Ventilation Vent Particulate Monitor Alarm.Caused by Pressure Control Valve PCV-GW-107 Stuck Open Causing Relief Valve RV-GW-107 to Lift ML20086Q7671975-02-18018 February 1975 Telecopy Ao:On 750217,core Quadrant Tilt of 2.2% Existed W/Reactor at 100% Power ML20086Q8181975-02-18018 February 1975 Telecopy Ao:On 750215,overpower Low Level Amplifier Failed Causing Inoperable Overpower Protection ML20086Q7801975-02-14014 February 1975 Telecopy Ao:On 750214,steam Generator Narrow Range Level Detector Drifted High.Cause Not Determined ML20086S4261975-02-14014 February 1975 AO-S2-74-10:on 741129,unsatisfactory Leakage Ovserved While Performing Periodic Test 16.4.Caused by Stress to Four Keyways of Rockshaft Due to Valve Closure.Counterweights Modified & Repositioned on Weight Lever ML20086Q8771975-02-14014 February 1975 Telecopy Ao:On 750214,pressurizer Pressure Comparator Failed.Caused by Setpoint Drift.Comparator Replaced ML20086Q8941975-02-0303 February 1975 Telecopy Ao:On 750201,steam Generator Blowdown Activity Not Continuously Recorded & Monitored by Steam Generator Blowdown Sample Monitor Sys ML20086R0801975-01-24024 January 1975 AO-S2-75-02:on 750110,channel 1 of Steam Generator C Level Instrumentation Indication Drifted Beyond Allowable Limits. Caused by Packing Leak at Isolation Valve.Replacement of Packing Will Be Performed as Necessary to Minimize Leakage ML20086R1891975-01-24024 January 1975 AO-S2-75-01:on 750109,discovered High Water Level Existed in Sump Area of High Pressure Heater Drain Pump.Caused by Turbine Bldg Sump Pumps Shut Off for Test.Test Instructions Revised to Require Surveillance ML20086S3061975-01-23023 January 1975 AO-S1-74-16:on 741220,radiation Monitor Alarm Accurred on RM-SW-107 Which Monitors Svc Water Leaving Component Cooling Hxs.Caused by Pin Holes in Component Cooling HX 1-CC-E-1C Tubes.Hx Isolated from Svc Water Sys ML20086S3171975-01-23023 January 1975 AO-S1-74-15:on 741219,abnormal Degradation Found of One of Several Boundaries Designed to Contain Radioactive Matls Resulting from Fission Process.Caused by Sheet Sludge Deposits & Deleterious Effects of Sodium Phosphate Control ML20086Q9471975-01-20020 January 1975 Telecopy Ao:On 750119,two Valves in Station Instrument Air Supply to Containment Instrument Air Sys Found Open.Valves Shut & Locked ML20086Q9671975-01-20020 January 1975 Telecopy Ao:On 750118,chemical Vol & Control Sys Found Open Causing Dilution of Primary Coolant Sys ML20086S3471975-01-10010 January 1975 AO-S1-74-13:on 741107,tube Rupture Occurred in Component HX 1-CC-E-1D.Caused by Equipment Malfunction.Hx Isolated & Component Cooling Surge Tank Refilled & Observed to Verify No Further Leakage ML20086R0961975-01-10010 January 1975 Telecopy Ao:On 750110,control Room Log Readings Indicated Level Transmitter 2-1T-494 Drifted Above Prescribed Limits. Transmitter Trip Bistables Deenergized ML20086S4301975-01-10010 January 1975 Telecopy Ao:On 750109,valve Pit Containing Svc Water Valves MOV-SW-203 A-D Became Flooded.Condition May Have Temporarily Incapacitated Heat Removal Feature of Recirculation Spray Sys ML20086S3321975-01-0303 January 1975 AO-S1-74-14:on 741119,magnetic Amplifiers for Low Level Alarm LS-CW-1018 & Turbine Trip LS-CW-101C Found Out of Calibr.Caused by Changes in Temp & Humidity & Aging of Components.Test Initiated to Verify Calibr ML20086S2931974-12-31031 December 1974 Ao:On 741230,crack Found in Containment Spray Check Valve. Containment Spray Check Valve & All Cracked Rackshafts Being Replaced ML20086S3611974-12-20020 December 1974 Telecopy Ao:On 741219,tube Leaks in Component Cooling HX Resulted in Low Level Release of Radioactive Component Cooling Water Into James River.Source of Leakage Located & Repaired.Hx Isolated ML20086S3691974-12-19019 December 1974 Ao:On 741218,steam Generator Tube Wall Deterioration Found in Excess of 50% in 137 Tubes ML20086S4371974-12-16016 December 1974 AO-S2-74-09:on 741017,cracks Discovered in Some Steam Generator Lower Ring Support Swivel End Couplings.Caused by Lateral Load in Direction of Reactor Pressure Vessel.Support Couplings Redesigned ML20086S4621974-10-25025 October 1974 AO-S2-74-09:on 741017,cracks Found in Concrete Supporting Steam Generator A.All Couplings Being Removed to Be Radiographed & Inspected.Rept Will Be Submitted by 750103 ML20086S8821974-10-22022 October 1974 AO-S2-74-06:on 740803,during Six Degree Freedom of Movement Portion of PT-14,no Response Received from Any of Three Valves.On Second Test of TV-MS-201B W/Air Bled from Cylinders,Valve Went Fully Closed ML20086S5731974-10-0101 October 1974 AO-S2-74-08:on 740912,neither Fuel Oil Supply Flow Paths for Emergency Diesel Generator 2 Operable.Caused by Solenoid Valves Disconnected in Terminal Box.Personnel Instructed in Procedure ADM-37 ML20086S5761974-09-26026 September 1974 AO-S2-74-07:on 740810,summator TM-2-412G Drift Allowed Overpower Trip Setpoint to Be Approx 5% High.Caused by Defective Summator.Summator Removed & Replaced & Module Calibr ML20086S5781974-09-26026 September 1974 AO-S1-74-11:on 740820,during Depressurization Procedure, Alarm Indicated High Surge Tank Pressure Received in Control Room.Cause Not Listed.Overhead Gas Compressor Stopped & Pressure within Gas Stripper Surge Tank Reduced ML20086S5841974-08-21021 August 1974 AO-S1-74-10:on 740802,one Spent Fuel Pit to Boron Recovery Sys Temporary Hose Line Connection Separated from Fitting, Spraying Primary Grade Pump House Interior.Caused by Inadequate Design of Clamping Arrangement 1984-09-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML18152B3531999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Surry Power Station,Units 1 & 2.With 991012 Ltr ML18152B6651999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Surry Power Station Units 1 & 2.With 990915 Ltr ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18151A3981999-08-13013 August 1999 SPS Unit 2 ISI Summary Rept for 1999 Refueling Outage. ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B3791999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Surry Power Station,Units 1 & 2.With 990811 Ltr ML18152B3911999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Surry Power Station,Units 1 & 2.With 990713 Ltr ML18152B4341999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Surry Power Station,Units 1 & 2.With 990614 Ltr ML20195E2401999-05-31031 May 1999 Rev 2 to COLR for SPS Unit 2 Cycle 16 Pattern Ag ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4161999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Surry Power Station Units 1 & 2.With 990512 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18152B6511999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Surry Power Station Units 1 & 2 ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7331999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Surry Power Station,Units 1 & 2.With 990310 Ltr ML18152B5421999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Surry Power Station,Units 1 & 2.With 990210 Ltr ML18151A3031999-01-29029 January 1999 ISI Summary Rept for 1998 Refueling Outage,Including Form NIS-1, Owners Rept for ISIs & Form NIS-2, Owners Rept for Repairs & Replacements. ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B6011998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Surry Power Station,Units 1 & 2.With 990115 Ltr ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B7081998-11-30030 November 1998 Rev 0 to COLR for Surry 1 Cycle 16,Pattern Un. ML18152B5721998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Surry Power Station,Units 1 & 2.With 981214 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6241998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Surry Power Station Units 1 & 2.With 981111 Ltr ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B6881998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Surry Power Station Units 1 & 2.With 981012 Ltr ML18153A3271998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Surry Power Station,Units 1 & 2 ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A3161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Surry Power Station Units 1 & 2.W/980807 Ltr ML18152B7621998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Surry Power Station,Units 1 & 2.W/980707 Ltr ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML18153A3141998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Surry Power Station,Units 1 & 2.W/980610 ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B8161998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Surry Power Station Units 1 & 2.W/980508 Ltr ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML20217P9941998-04-0707 April 1998 Safety Evaluation Granting Licensee Third 10-yr Inservice Insp Program Relief Requests SR-018 - Sr-024 ML18153A2951998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Sps,Units 1 & 2.W/ 980408 Ltr ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket 1999-09-30
[Table view] |
Text
r -- c== <
, . . ,c
) O j Vinot$sA Ex.ncrnic Asp Powen Com Paxd j It ac t Ft O N D. YI H OI N t A 23361 September 26, 1974 Mr. Norman C. Moseley, Director Serial No. 288 Directorate of Pegulatory Operations P0&M/JTB:clu United States Atomic Energy Commission ..
Region 11 - Suite 818 h Docket No. 50-280 230 Peachtree Street, Northwest License No. DPR-32 Atlanta, Georgia 30303
Dear Mr. Moseley:
Pursuant to Surry Power Station Technical Specification 6.6.B.1, the Virginia Electric and Power Company hereby submits forty (40) copies of Abnormal Occurrence Report No. A0-SI-74-11.
The substance of this report has been reviewed by the Station Nucicar '
Safety and Operating Committee and uill be placed on the agenda for the next meeting of the System Nucicar Safety and Operating Committee.
Very truly yours,
, f. PAObic-C. M. Stallings Vice President-Power Supply and Production Operations Enclosures '3 '4 ,
V 40 copies of A0-S1-74'-11 .g t-pgCliv[ 0 ,.\
cc: Mr. K. R. Goller, Assistant Director _
10 g r. $
for Operating Reactors E,i gg, m$?sth?"' (l ClN
.een=usw m
- OL G l
D o Noaso .
"'7 M ,,,r 1 10*9 PDR _
. GOEX SENE'B1X110N r
F-O O 4
ABN0RMAL OCCURRENCE REPORT REPORT NO. A0-SI-74-11 GASEOUS RELEASE FROM CAS STRIPPER SURGE TANK AUGUST 29, 1974
_ DOCKET NO. 50-280 LICENSE NO. DPR-32 SURRY POWER STATION VIRGINIA ELECTRIC AND POWER COMPAhT l
l n
l'b (~b V V I, INTRODUCTION In accordance with Technical Specification 6.6.B.1 for Surry Power Station, Operating License No. DPR-32, this report describes an abnormal occurrence which was identified on August 20, 1974. The Directorate of Regulatory Operations, Region II, was notified on August 21, 1974.
The occurrence reported herein is classified as an abnormal occurrence pursuant to Technical Specification 1.0.I.3 which states that "An abnormal occurrence is defined as: "Any uncontrolled or unplanned release of radio-activity from the site."
The occurrence described herein resulted in an insignificant, unplanned gaseous release from the station.
~
II.
SUMMARY
OF OCCURRENCE On August 20, 1974, Unit No. I was operating at approximately 99 per cent of rated power and 805 MWe generator output. Unit No. 2 was at cold shutdown conditions for maintenance of a pressurizer spray valve. Three (3) freeze seals were being used to isolate the pressurizer spray volume from the reactor coolant system. To ensure the freeze seal intergrity, it was necessary to depressurize the reactor coolant system below 450 psig.
During the depressurization (letdown) procedure, an alarm indicating a high surge tank (overhead gas compressor discharge) pressure was received and acknowledged in the control room. However, simultaneous station evolutions prevented immediate corrective action by the boren recovery panel operator.
Upon his subsequent return to the boron recovery panel, the opetatuc discovered a release was in progress and immediately terminated it.
T 1 o o
, III. ANALYSIS OF OCCURRENCE The maintenance on the pressurizer spray valve required the establishment of freeze seals to isolate the pressurizer spray volume. In accordance with HMP-S-021, Special Maintenance Procedure for Freeze Seals of Stainless Steel Piping, the reactor coolant system was being depressurized from 450 psig to 150 psig, minimizing the differential pressure across the seals. The letdown was directed to the primary drain tank (PDT), increasing the PDT level and reducing the gas space in the tank. The displaced gases of the PDT were transferred to the vent gas system.
The gases which are transferred to the vent gas system are compressed by the overhead gas system compressors which take suction from the vent gas system and are stored in the stripper surge tank. When the stripper surge tank pressure exceeds approximately 120 psig, the gas is automatically transferred to the hydrogen catalytic recombiner system or to the waste gas system directly via two (2) pressure regulator valves in series, PCV-BR-132A at approximately 120 psig and PCV-GW-107 at approximately 7 psig. A relief valve (RV-BR-120) set at approximately 150 psig protects the gas stripper surge tank from over-pressurization. The relief path is to the process vent header and then to the atmosphere. In addition, there is a high/ low pressure alarm on the gas stripper surge tank, set to alarm on a high pressure signal of 140 psig.
At the time of the occurrence, the hydrogen recombiner system was not in operation. The direct flow to the waste gas system was isolated by valve 1-BR-79, because the waste gas decay tank in service was at its upper operating pressure.
During the depressurization of the reactor coolant system, one of the
-overhead gas compressors was being run in the manual mode. An operator was monitoring the PDT level and gas stripper surge tank pressure (overhead I
o o gas compressor discharge pressure). Due to the occurrence of a number of simultaneous station evolutions, observation of these parameters was curtailed.
The pressure in the surge tank increased to 140 psig, an alarm was received and acknowledged, but no immediate corrective action was taken. A continuing increase in pressure resulted in the eventual lifting of RV-BR-120, releasing the gases of the surge tank to the process vent system and activating the process vent gaseous monitor alert, RI-GW-102, (set at 8 x 10* cpm). The operator, upon noting the condition, took immediate steps to terminate the release.
IV. CORRECTIVE ACTION TO PREVENT RECURRENCE The immediate action taken by the operator following the detection of the release was to stop the overhead gas compressor. Pressure within the gas stripper surge tank was reduced by opening pressure control valve -
PCV-BR-130A. This diverted the contents of the overhead gas tank to the gas stripper overhead system, reducing the pressure of the gas stripper surge tank to approximately 130 psig. At no time did the pressure in the gas stripper surge tank exceed 150 psig. The Health Physics Department was notified and a representative sample was obtained from the gas stripper surge tank for analysis.
Following the return to normal, a check was made of the alarm setpoints.
It was found that the setpoint on the high pressure alarm, which had been-changed to 140 psig from 180 psig '(abnormal occurrence report, A0-S1-7'3-14, dated November 15, 1973) still alarmed at 140 psig. The setpoint was lowered,_
however to 130 psig, to ensure sufficient time for an operator to take-corrective action in' event of future alarms._ Both high~and low pressure alarms on the over-i headagas compressor discharge-were tested and found.to be operating properly, f
9 a
F
.. .. . g Tha licensW is precently investigating the casibility of installing a high pressure cutout switch to operate in conjunction with the overhead gas compresaor's high pressure alarm.
V. ANALYSIS AND EVALUATION OF SAFETY IMPLICATION OF TilP. OCCURRENCE An estimated twenty-five (25) cubic feet of radioactive gas was discharged to the process vent system via relief valve RV-LR-120 and released to the atmosphere. The release lasted approximately ten (10) minutes with the 5
maximum reading on the process vent gaseous radiation monitor of 2 x 10 cpm (5.04 x 10-7 pCi/cc).
Based on a representative sample taken from the gas stripper tank immediately following the occurrence, the total activity released was approximately 5.91 curies, including Xel33 = 5.87 Ci; Xel33 (metastable) L O.04 Ci; 1131 = 0.546 x 10-6 Ci; 1133 = 0.220 x 10-6 Ci; Gross By = 0.560 x 10-9 Ci.
The rate of release was well below the allowable controlled release rate as delineated in Section 3.11.B.1 of the Technical Specifications. The specified maximum release rate for gaseous and airborne particulate waste limit is as follows:
5 3 IQ1/(MPC)g $2.0 x 10 m /sec where:
Q1 = controlled release rate (curies per second of-any radioisotope 1)
(MPC)1 = defined in Column I, Table 11 of Appendix B to 10 CFR 20 (microcuries per cubic centimeter)
For the release reported herein; 4 3 IQg/(MPC)g = 3.98 x 10 m /sec 4 /sec The release rate of 3.98 x 10 m 3 was approximately 19.9 per cent of that permitted by the Technical Specifications for norma'l. controlled-
T O O releases.
It is evident from the release rate calculated above that the radio-activity discharged to the environment was insignificant and did not adversely affect the health and safety of the general public or station employees. Upon failure of operator or instrumentation to prevent overpressurization, the appropriate system safety equipment (RV-BR-120) functioned as designed and the release was terminated immediately af ter detection.
VI. CONCLUSIONS The licensee concludes that:
- 1. Simultaneous station evolutions prevented the control room operator from adequately monitoring the overhead gas compressor discharge pressure and rr.sulted in the subsequent lifting of relief valve RV-BR-120.
- 2. t.n insignificant amount of radioactivity was released to the environment.
- 3. The occurrence described herein did not affect the safe operation of the station.
- 4. Tr.c occurrence described herein did not adversely affect the health or safety of the general public.
l w