Similar Documents at Surry |
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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML20086S5861984-09-10010 September 1984 SR-S1-74-03:on 740403,safety Injection Experienced Due to Spurious High Steam Flow Signals in Conjunction W/Low Temp Average or Low Steam Line Pressure Signals.Caused by Fluctuations of Steam Flow Signals Above Setpoint ML20087B9541975-10-17017 October 1975 Telecopy AO:751011,containment Leak Rate Tests Revealed Containment Leakage Rate Greater than Acceptable Criteria ML20087B9651975-10-16016 October 1975 Telecopy AO:on751015,recirculation of Boron Injection Tank 2 Interrupted for Period of 15 Minutes.Caused by Failure of Boric Acid Transfer Pump D Motor ML20087C0771975-10-0101 October 1975 Telecopy Ao:On 750928,during Refueling Performance Test 18.2,safety Injection Master Relay Failed to Latch,Violating Tech Spec 3.3 ML20087C1041975-09-25025 September 1975 Telecopy Ao:On 750924,loop a Instrumentation Drifted Low Resulting in Safety Sys Setting Being Less Conservative than Tech Spec Limit ML20087B8501975-08-25025 August 1975 Telecopy Ao:On 750823,channel of Protection Found Unconservative Due to Failure of Resistance Temp Detector ML20087B7821975-08-25025 August 1975 Telecopy Ao:On 750823,leak Developed in Boric Acid Transfer Sys Decreasing Level in Boric Acid Storage Tank C Below Tech Spec Limit ML20087B8921975-08-22022 August 1975 Telecopy Ao:On 750822,channel of Protection Found Unconservative Due to Failure of Resistance Temp Detector ML20087B9321975-08-0707 August 1975 Telecopy Ao:On 750807,boron Injection Tank Recirculation Valves TV-2884 A,B & C Found in Closed Position ML20087C1461975-07-30030 July 1975 Telecopy Ao:On 750729,boron Concentration in Boron Injection Tank 2 Found to Be 11.4% ML20087C1691975-07-21021 July 1975 Telecopy Ao:On 750720 Low Level Amplifier Failed Causing One Temp Change Protection Channel to Be Unconservative ML20087C2041975-07-0707 July 1975 Telecopy Ao:On 750706,reactor Trip Occurred.Caused by Sudden Closure of Trip Valve in Main Steam Line B.Investigation Underway to Determine Cause of Malfunction & Corrective Action ML20087C2241975-07-0101 July 1975 Telecopy Ao:On 750630,discovered That Undervoltage Reactor Trip Circuit Inoperable ML20086Q3091975-05-21021 May 1975 Notifies That AO Reported on 750514 Re Perforation of Fuel Assembly During Fuel Operation in Error.Perforation Occurred During Normal Operation.Rept No Longer Considered AO ML20086Q2891975-05-16016 May 1975 Telecopy Ao:On 750516,chemical Addition Tank Valve MOV-CS-10IB Failed to Operate Properly ML20086Q3261975-05-14014 May 1975 Telecopy Ao:On 750513,manipulator Crane Stopped Due to Overload.Caused by Perforation in Fuel Clad ML20086Q3681975-05-0101 May 1975 Telecopy Ao:On 750430,emergency Diesel Generator 3 Failed While in Svc Due to Internal Problem in turbo-blower ML20086Q5871975-04-28028 April 1975 Telecopy Ao:On 750427,consequence Limiting Safeguards Channel 3,Train B Matrix Relay Coil Found to Be Open Circuit During Performance Test 8.5A ML20086Q6211975-04-28028 April 1975 Ao:On 750427,sample Sys Trip Valve on Pressurizer Relief Tank Failed to Stroke on Initiation of Safety Injection During Performance Test 18.2 ML20086Q5111975-04-28028 April 1975 Telecopy Ao:On 750427,circulating Water Sys Valve MOV-CW-206D Failed to Shut After Receiving Close Signal ML20086S4491975-03-26026 March 1975 Corrections to AO-S2-74-09 Re Steam Generator Support Couplings.Studs Not Welded to Encl Plate as Previously Reported Due to Potential Welding Problems ML20086R0291975-02-24024 February 1975 AO-S1-75-01:on 750118,boron Concentration Observed to Be 1,842 Ppm & Primary Grade Water Flow Controller 1114A Found in Manual Mode of Operation W/Demand Position Corresponding to Full Open Position of Valve FCV-1114A ML20086Q9391975-02-24024 February 1975 AO-S1-75-02:on 750118,containment Isolation Valves 2-IA-446 & 2-IA-447 Found Open.Caused by Operator Error.Operators Advised of Importance of Following Procedures & Verifying Actions ML20086Q9291975-02-24024 February 1975 AO-S1-75-03:on 750115,process Vent Particulate Monitor Alarm Occurred Followed by Ventilation Vent Particulate Monitor Alarm.Caused by Pressure Control Valve PCV-GW-107 Stuck Open Causing Relief Valve RV-GW-107 to Lift ML20086Q7671975-02-18018 February 1975 Telecopy Ao:On 750217,core Quadrant Tilt of 2.2% Existed W/Reactor at 100% Power ML20086Q8181975-02-18018 February 1975 Telecopy Ao:On 750215,overpower Low Level Amplifier Failed Causing Inoperable Overpower Protection ML20086Q7801975-02-14014 February 1975 Telecopy Ao:On 750214,steam Generator Narrow Range Level Detector Drifted High.Cause Not Determined ML20086S4261975-02-14014 February 1975 AO-S2-74-10:on 741129,unsatisfactory Leakage Ovserved While Performing Periodic Test 16.4.Caused by Stress to Four Keyways of Rockshaft Due to Valve Closure.Counterweights Modified & Repositioned on Weight Lever ML20086Q8771975-02-14014 February 1975 Telecopy Ao:On 750214,pressurizer Pressure Comparator Failed.Caused by Setpoint Drift.Comparator Replaced ML20086Q8941975-02-0303 February 1975 Telecopy Ao:On 750201,steam Generator Blowdown Activity Not Continuously Recorded & Monitored by Steam Generator Blowdown Sample Monitor Sys ML20086R0801975-01-24024 January 1975 AO-S2-75-02:on 750110,channel 1 of Steam Generator C Level Instrumentation Indication Drifted Beyond Allowable Limits. Caused by Packing Leak at Isolation Valve.Replacement of Packing Will Be Performed as Necessary to Minimize Leakage ML20086R1891975-01-24024 January 1975 AO-S2-75-01:on 750109,discovered High Water Level Existed in Sump Area of High Pressure Heater Drain Pump.Caused by Turbine Bldg Sump Pumps Shut Off for Test.Test Instructions Revised to Require Surveillance ML20086S3061975-01-23023 January 1975 AO-S1-74-16:on 741220,radiation Monitor Alarm Accurred on RM-SW-107 Which Monitors Svc Water Leaving Component Cooling Hxs.Caused by Pin Holes in Component Cooling HX 1-CC-E-1C Tubes.Hx Isolated from Svc Water Sys ML20086S3171975-01-23023 January 1975 AO-S1-74-15:on 741219,abnormal Degradation Found of One of Several Boundaries Designed to Contain Radioactive Matls Resulting from Fission Process.Caused by Sheet Sludge Deposits & Deleterious Effects of Sodium Phosphate Control ML20086Q9471975-01-20020 January 1975 Telecopy Ao:On 750119,two Valves in Station Instrument Air Supply to Containment Instrument Air Sys Found Open.Valves Shut & Locked ML20086Q9671975-01-20020 January 1975 Telecopy Ao:On 750118,chemical Vol & Control Sys Found Open Causing Dilution of Primary Coolant Sys ML20086S3471975-01-10010 January 1975 AO-S1-74-13:on 741107,tube Rupture Occurred in Component HX 1-CC-E-1D.Caused by Equipment Malfunction.Hx Isolated & Component Cooling Surge Tank Refilled & Observed to Verify No Further Leakage ML20086R0961975-01-10010 January 1975 Telecopy Ao:On 750110,control Room Log Readings Indicated Level Transmitter 2-1T-494 Drifted Above Prescribed Limits. Transmitter Trip Bistables Deenergized ML20086S4301975-01-10010 January 1975 Telecopy Ao:On 750109,valve Pit Containing Svc Water Valves MOV-SW-203 A-D Became Flooded.Condition May Have Temporarily Incapacitated Heat Removal Feature of Recirculation Spray Sys ML20086S3321975-01-0303 January 1975 AO-S1-74-14:on 741119,magnetic Amplifiers for Low Level Alarm LS-CW-1018 & Turbine Trip LS-CW-101C Found Out of Calibr.Caused by Changes in Temp & Humidity & Aging of Components.Test Initiated to Verify Calibr ML20086S2931974-12-31031 December 1974 Ao:On 741230,crack Found in Containment Spray Check Valve. Containment Spray Check Valve & All Cracked Rackshafts Being Replaced ML20086S3611974-12-20020 December 1974 Telecopy Ao:On 741219,tube Leaks in Component Cooling HX Resulted in Low Level Release of Radioactive Component Cooling Water Into James River.Source of Leakage Located & Repaired.Hx Isolated ML20086S3691974-12-19019 December 1974 Ao:On 741218,steam Generator Tube Wall Deterioration Found in Excess of 50% in 137 Tubes ML20086S4371974-12-16016 December 1974 AO-S2-74-09:on 741017,cracks Discovered in Some Steam Generator Lower Ring Support Swivel End Couplings.Caused by Lateral Load in Direction of Reactor Pressure Vessel.Support Couplings Redesigned ML20086S4621974-10-25025 October 1974 AO-S2-74-09:on 741017,cracks Found in Concrete Supporting Steam Generator A.All Couplings Being Removed to Be Radiographed & Inspected.Rept Will Be Submitted by 750103 ML20086S8821974-10-22022 October 1974 AO-S2-74-06:on 740803,during Six Degree Freedom of Movement Portion of PT-14,no Response Received from Any of Three Valves.On Second Test of TV-MS-201B W/Air Bled from Cylinders,Valve Went Fully Closed ML20086S5731974-10-0101 October 1974 AO-S2-74-08:on 740912,neither Fuel Oil Supply Flow Paths for Emergency Diesel Generator 2 Operable.Caused by Solenoid Valves Disconnected in Terminal Box.Personnel Instructed in Procedure ADM-37 ML20086S5761974-09-26026 September 1974 AO-S2-74-07:on 740810,summator TM-2-412G Drift Allowed Overpower Trip Setpoint to Be Approx 5% High.Caused by Defective Summator.Summator Removed & Replaced & Module Calibr ML20086S5781974-09-26026 September 1974 AO-S1-74-11:on 740820,during Depressurization Procedure, Alarm Indicated High Surge Tank Pressure Received in Control Room.Cause Not Listed.Overhead Gas Compressor Stopped & Pressure within Gas Stripper Surge Tank Reduced ML20086S5841974-08-21021 August 1974 AO-S1-74-10:on 740802,one Spent Fuel Pit to Boron Recovery Sys Temporary Hose Line Connection Separated from Fitting, Spraying Primary Grade Pump House Interior.Caused by Inadequate Design of Clamping Arrangement 1984-09-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML18152B3531999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Surry Power Station,Units 1 & 2.With 991012 Ltr ML18152B6651999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Surry Power Station Units 1 & 2.With 990915 Ltr ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18151A3981999-08-13013 August 1999 SPS Unit 2 ISI Summary Rept for 1999 Refueling Outage. ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B3791999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Surry Power Station,Units 1 & 2.With 990811 Ltr ML18152B3911999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Surry Power Station,Units 1 & 2.With 990713 Ltr ML18152B4341999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Surry Power Station,Units 1 & 2.With 990614 Ltr ML20195E2401999-05-31031 May 1999 Rev 2 to COLR for SPS Unit 2 Cycle 16 Pattern Ag ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4161999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Surry Power Station Units 1 & 2.With 990512 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18152B6511999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Surry Power Station Units 1 & 2 ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7331999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Surry Power Station,Units 1 & 2.With 990310 Ltr ML18152B5421999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Surry Power Station,Units 1 & 2.With 990210 Ltr ML18151A3031999-01-29029 January 1999 ISI Summary Rept for 1998 Refueling Outage,Including Form NIS-1, Owners Rept for ISIs & Form NIS-2, Owners Rept for Repairs & Replacements. ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B6011998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Surry Power Station,Units 1 & 2.With 990115 Ltr ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B7081998-11-30030 November 1998 Rev 0 to COLR for Surry 1 Cycle 16,Pattern Un. ML18152B5721998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Surry Power Station,Units 1 & 2.With 981214 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6241998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Surry Power Station Units 1 & 2.With 981111 Ltr ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B6881998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Surry Power Station Units 1 & 2.With 981012 Ltr ML18153A3271998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Surry Power Station,Units 1 & 2 ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A3161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Surry Power Station Units 1 & 2.W/980807 Ltr ML18152B7621998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Surry Power Station,Units 1 & 2.W/980707 Ltr ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML18153A3141998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Surry Power Station,Units 1 & 2.W/980610 ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B8161998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Surry Power Station Units 1 & 2.W/980508 Ltr ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML20217P9941998-04-0707 April 1998 Safety Evaluation Granting Licensee Third 10-yr Inservice Insp Program Relief Requests SR-018 - Sr-024 ML18153A2951998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Sps,Units 1 & 2.W/ 980408 Ltr ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket 1999-09-30
[Table view] |
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s VIROINIA 15LECTitic AND POWER C NM l niouxoun.vinoi m cocci j
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yL E January 10, 1975 p*JAN1gyg?O' @z.,'JT
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'$ sp Mr. Norman C. Moseley, Director Serial <No. 361 l Directorate of Regulatory Operations P0&M/JTB:clw United States Atomic Energy Commission Region II - Suite 818 Docket No. 50-280 230 Peachtree Street, Northwest License No. DPR-32 Atlanta, Georgia 30303
Dear Mr. Moseley:
Pursuant to Surry Power Station Technical Specification 6.6.B.1, the Virginia Electric and Power Company hereby submits forty (40) copics of Abnormal Occurrence Report No. A0-SI-74-13.
The substance of this report has been reviewed by the Station Nuclear Safety and Operating Committee and will be placed on the agenda for*the next meeting of the System Nuclear Safety and Operating Committee.
Very truly yours,
- 6. 2%,Jkduup C. M. Stallings Vice President-Power Supply and Production Operations Enclosures 40 copies of A0-S1-74-13 cc: Mr. K. R. Goller, Assistant Director for Operating Reactors Mr. B. P. Scholfield Supervisor, Radiological Health Section Department of Health l
j 8403010520 750110 l
- PDR ADOCK 05000280 S PDR 424-Y L COPY SENT REGION m
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't) LJ ABNORMAL OCCURRENCE REPORT REPORT NO. A0-SI-74-13 UNPLANNED RELEASE OF LOW LEVEL RADI0 ACTIVE COMPONENT COOLING WATER TO JAMES RIVER
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DECEMBER 9, 1974 DOCKET NO. 50-280 LICENSE NO. DPR-32
/
SURRY POWER STATION VIRGINIA ELECTRIC AND POWER COMPANY m
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l-1 i
I. INTRODUCTION i
j In accordance with Technical Specification 6.6.B.1 for Surry Power I
Station, Operating License Number DPR-32, this report describes an abnormal occurrence which occurred on November 7, 1974. The Directorate of Regulatory Operations, Region II, was notified on November 8, 1974.
The occurrence reported herein is classified as an abnormal occurrence 2
pursuant to Technical Specification 1.0.I.3 which states that "An abnormal occurrence is defined as: any uncontrolled or unplanned release of radio-
, activity from the site."
! The occurrence described herein resulted in the release of low level i radioactive component cooling water to the James River, i
j II.
SUMMARY
-0F OCCURRENCE i On November 7, 1974 at about 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br />, with both units at cold l shutdown, a tube rupture occurred in component cooling heat exchanger i
4 1-CC-E-1D. This resulted in the release of approximately 8000 gallons of 1
low level radioactive component cooling water to the service water system 4
and ultimately to the James River.
Investigation of this occurrence further revealed that slow leakage
- of the component cooling system to the service water system had been i .
i occurring since early September 1974. . The slow tube. leakage resulted.in i
the release of approximate'ly 35,500 gallons of low' level radioactive component cooling water to the service water system and' ultimately to the JamesIRiver.
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g g V U Therefore, a total of approximately 43,500 gallons of low level radioactive component cooling water was released to the James River as a result of slow heat exchanger tube leakage and subsequent tube rupture.
III. ANALYSIS OF THE OCCURRENCE The annunciating of a component cooling water low pressure alarm in the control room caused the Shift Supervisor to check the level indication for the component cooling system surge tank (1-CC-TK-1). The level indicated an essentially empty tank. Immediate steps were taken to identify and isolate the source of leakage from the system. Approximately 30 minutes after the receipt of the low pressure alarm, component cooling heat ex-changer 1-CC-E-1D was isolated. The surge tank was refilled and no further leakage was observed.
It is estimated that approximately 10 minutes elapsed from the time the surge tank was at normal operating level (%1700 gallons) until it was observed to be empty. Thus, the leak rate from the component cooling system was about 170 gallor s per minute. For conservatism, the leak rate is assumed to be 200 gallons per minute. Therefore, the failure leakage from the heat exchanger resulted in the release of about 8000 gallons of low level radioactive water.
Inspection of chemistry records further revealed that the component cooling system had been undergoing minor dilution since about September 2, 1974. This was assumed to be caused by slow out-leakage of component l
t cooling water to the service water system. An analysis of chemical l
incentration behavior in the component cooling system from September 2, 1974 to November 7, 1974 revealed an average dilution rate of about .37 gallons per minute. This was assumed to be_ equal to the rate of component
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cooling out-leakage to the service water system. This small leakage rate has resulted in'the release of approximately 35,500 gs11ons of low level radioactive water over the 66 day period between September 2, 1974 and November 7, 1974. This quantity of leakage is conservatively high since J there are known leakages in the auxiliary building and containment which are processed as liquid waste. Therefore, the actual release was less than reported herein.
- Investigation of this occurrence revealed that several equipment 1
1 malfunctions contributed to the unplanned release of component cooling water to the service water systems; i.e. the failure of a tube in the heat exchanger 1-CC-E-ID, the failure of the component cooling surge tank i
- low level alarm to sound and the failure of the service water radiation monitor (RM-SW-107) to properly indicate radioactivity in the service water system which is the heat sink for the compoaent cooling water system.
\
l IV. CORRECTIVE ACTION TO PREVENT RECURRENCE 1
The immediate corrective action was to isolate the heat exchanger .
~
l thus terminating the release. The component cooling surge tank was t
refilled and observed to verify no further leakage was occurring.
The heat exchanger was taken out of service, opened and inspected to determine the degree of tube failure. It was found that only one '(1) tube had failed. This tube was plugged, and other. tubes.were inspected for defects. The slow leak was caused by the gradual degradation of the heat exchanger' tube. The other component cooling heat exchangers were?
' inspected _for tube leakage and none found. .This is the first tube' failure-in_any of the component' cooling heat exchangers.
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O O Maintenance on the component cooling heat exchanger was completed and placed back in service at 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br /> on December 8, 1974. After a i short time in service, component cooling system leakage was again dis-covered. During the second inspection for leakage it was noted that the component cooling system surge tank level was decreasing at a rate of 1 approximately 0.65 gallons per minute. On December 9, 1974 at 0640 hours0.00741 days <br />0.178 hours <br />0.00106 weeks <br />2.4352e-4 months <br />, I-CC-E-lD was again isolated. An internal inspection of this heat exchanger revealed pinhole leaks in two (2) tubes. These two leaking tubes resulted 4
in the release of additional low level radioactive component cooling water to the James River.
The failed tubes in the component cooling heat exchanger 1-CC-E-1B i . .
were plugged and returned to service.
The additional' leakage conservatively resulted in the release of 2445 gallons of low level radioactive' water from the component cooling
- water system to the Jcmes River.
The malfunctions of the service water radiation monitor'(RM-SW-107) t t
and the component cooling surge tank low level alarm are being investigated.
Appropriate repairs or design modifications'will be implemented, commensurate-with the investigative findings, to restore these devices to' proper.
1 l working condition.
l V. ANALYSIS AND EVALUATION OF SAFETY IMPLICATION OF THE OCCURRENCE
' The source of radionuclides in . the component cooling ' water. was slow f .leaka'ge from-the reactor' coolant system to the non-regenerative. heat
, exchanger. The concentrations of the radionuclides'present in the~com--
ponent cooling water are assumed to belthe highest measured during the:
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66 day slow leakage period, and at the actual value measured on November 7, i
1974 during the 40 minute tube rupture period. This is considered con-servative since dilution had been occurring since September 2, 1974.
The release of low level radioactive water from the component cooling system has been analyzed as two separate events: a 66 day slow leak and a 40 minute rapid leak. The radionuclides taken into account for purposes of 1
l this analysis are as follows: Iodine-131, Cesium-134, Cesium-137, Cobalt-58, Cobalt-60, Tritium and Dissolved Xenon-133.
3 During the 66 day period of slow tube leakage from the heat exchanger
[ the maximum percentages of MPC released for each radionuclide are as i
follows: 1131 .0133%, Csl34 .0078%, Csl37 .0075%, Coss .000078%,
Co60 .0002%, 1H3 .000096%, Xel33-l% (based on an MPC of 3 x 10-7 pCi/ml).
l The represents a prorated aggregate of 1.0289% of MPC.
During the 40 minute tube rupture period, the maximum percentages of MPC released for each radionuclide are as follows: 1131-0%, Cs134 .278%,
Csl37 .325%, Coss-0%, Co60-0%, 1H3 .012%, Xel33-2.38%. This represents
[ a prorated aggregate of 2.95% MPC.
The total amount of activity released was 2.433 curies. The total amount of. each radionuclide released is as follows: I131-1.1 x 104 pCi, Csl34-20.3 x 104pC1, Cal 37-43.3 x 104 pC1, CoS8-2.0 x 104 pC1, Co60_
1.8 x 104 pCi, IH3-87.4 x '104 pCi, Xel33-86.4 x 104 pCi. The maximum
! percentages of MPC for each radionuclide af ter the release was terminated I
- are as follows
- 1131 .0133%, Csl34.00783%,lCsl37 .00752%, CoS8 .000078%,
.Co60 .0002%, IH3 .00010%, Xe133-1%.(based on an MPC of 3 x 10-7 pCi/ml).
l This represents a prorated aggregate'of.1.03%.
Only two radionuclides were present in the component cooling. water r
- _during the period of the leak which was discovered on' December 9, 1974
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. ~ ~
,-. , ., , - , . = , ~ -, .-..a... . . - , . -. a.- .
,,.. . g n.
(d O,
Cesium-134 and Cesium-137. These radionuclides were present in the following concentrations: Cs134 - 9.83 x 10-5 pCi/ml and Cs137 _
2.04 x 10-4 pCi/ml. During the leak, the maximum percentages of MPC released for each radionuclide are as follows: Csl34 - .886 x 10-3g and Csl37 .828 x 10-3%. This represents a prorated aggregate of 1.71 x 10-3% of MPC.
The above figures are based on the assumptions of no radioactive decay of the radionuclides of interest and four recirculation water C
pumps running for the duration of the release.
All analyses made were conservative and no 10 CFR 20 limits have been exceeded as a result of this unplanned release. Therefore, there were no safety implications associated with this event.
VI. CONCLUSI0tS The licensee concludes that:
- 1. The unplanned release was due to slow tube leakage and subsequent rupture of a tube in component cooling heat exchanger I-CC-E-1D.
- 2. An insignificant amount of radioactivity was released to the environment and all radionuclide concentrations were within 10 CFR 20 limits.
- 3. The occurrence described herein did not affect the safe operation of the station.
! 4. The occurrence described herein did not affect the health and safety 6f the general public.
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