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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M6631999-10-19019 October 1999 Forwards Insp Rept 50-277/99-07 & 50-278/99-07 on 990920.No Violations Noted ML20217K9241999-10-14014 October 1999 Forwards Amend 234 to License DPR-56 & Se.Amend Consists of Changes to TS in Response to Application & Suppls ,1001 & 06,which Will Support PBAPS Mod P00507,which Will Install Digital Pr Neutron Mining Sys ML20217F7391999-10-14014 October 1999 Requests Addl Info Re Peach Bottom Atomic Power Station Units 2 & 3 Appendix R Exemption Requests ML20217F6841999-10-13013 October 1999 Forwards Senior Reactor Operator Initial Exam Repts 50-277/99-302(OL) & 50-278/99-302(OL) Conducted on 990913- 16.All Applicants Passed All Portions of Exam ML20217F3021999-10-12012 October 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at PBAPS Have Been Completed.Ltr Also Confirms Completion of Actions Required by Confirmatory Order Modifying Licenses, ML20217E7451999-10-0808 October 1999 Forwards Response to NRC 990820 RAI Concerning Proposed Alternatives Associated with Third ten-yr Interval ISI Program for Pbaps,Units 2 & 3 ML20217B7701999-10-0606 October 1999 Submits Corrected Info to NRC 980528 RAI Re Util Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions ML20217B9151999-10-0606 October 1999 Provides Clarifying Info to Enable NRC to Complete Review of License Change Request ECR 98-01802,re Changes Necessary to Support Installation of Digital Pr Neutron Monitoring & Incorporate long-term T/H Stability Solution Hardware ML20217C4141999-10-0606 October 1999 Forwards Response to NRC 981109 RAI Re Resolution of USI A-46 for Pbaps.Proprietary Excerpts from GIP-2,Ref 25 Results of BWR Trial Plant Review Section 8 Also Encl. Proprietary Excerpts Withheld ML20217B3181999-10-0505 October 1999 Advises That Info Submitted in 990712 Application,Which Contained Attachment Entitled, Addl Info Re Cycle Spec SLMCPR for Peach Bottom 3 Cycle 13,dtd 990609, with Affidavit,Will Be Withheld from Public Disclosure ML20217B4051999-10-0505 October 1999 Forwards Amend 233 to License DPR-56 & Safety Evaluation. Amend Changes Minimum Critical Power Ratio Safety Limit & Approved Methodologies Referenced in Core Operating Limits Report 05000278/LER-1999-004, Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv)1999-10-0101 October 1999 Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv) ML20217B8891999-10-0101 October 1999 Forwards Response to RAI Re Request to Install Digital Power Range Neutron Monitoring Sys & Incorporate long-term,thermal-hydraulic Stability Solution Hardware. Revised TS Table 3.3.2.1-1 Encl ML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20212J6851999-09-29029 September 1999 Informs of Completion of mid-cycle PPR of Peach Bottom Atomic Power Station on 990913.No Areas Identified in Which Licensee Performance Warranted Addl New Insps Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212J5751999-09-28028 September 1999 Informs of Individual Exam Results for Applicants on Initial Exam Conducted on 990913-16 at Licensee Facility.Without Encls ML20216J0191999-09-27027 September 1999 Forwards Request for Addl Info Re Util 990301 Request to Support Installation of Digital Power Range Neutron Monitoring Sys & Incorporation of long-term thermal- Hydraulic Stability Solution Hardware,For Plant ML20212H6171999-09-24024 September 1999 Forwards Rev 2 to COLR for Pbaps,Unit 2,Reload 12,Cycle 13, IAW TS Section 5.6.5.d.Rept Incorporates Revised Single Loop Operation MAPLHGR Flow Multiplier ML20216H6451999-09-24024 September 1999 Forwards Notice of Withdrawal of Util 990806 Application for Amends to Fols DPR-44 & DPR-56.Proposed Change Would Have Involved Temporary Change to Increase Limit for Average Water Temp of Normal Heat Sink ML20212H5431999-09-24024 September 1999 Informs of Decision to Inspect H-3 & H-4 Shroud Welds During Upcoming 3R12 Outage Scheduled to Begin Late Sept 1999 ML20216H6751999-09-24024 September 1999 Forwards Amends 229 & 232 to Licenses DPR-44 & DPR-56, Respectively & Ser.Amends Will Delete SR Associated Only with Refueling Platform Fuel Grapple Fully Retracted Position Interlock Input,Currently Required by SR 3.9.1.1 ML20216F8811999-09-23023 September 1999 Withdraws 990806 Exigent License Change Application.Tech Spec Change to Allow Continued Power Operation with Elevated Cooling Water Temps During Potentially Extreme Weather Conditions No Longer Needed Due to Favorable Weather ML20212E8661999-09-22022 September 1999 Discusses GL 98-01 Y2K Readiness of Computer Sys at NPPs & Supplement 1 & PECO Response for PBAPS Dtd 990630. Understands That at Least One Sys or Component Listed May Have Potential to Cause Transient During Y2K Transition ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212D1191999-09-17017 September 1999 Forwards SE Re Proposed Alternatives to ASME Section XI Requirements for Containment Inservice Insp Program at Plant,Units 2 & 3 ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211P2961999-09-0707 September 1999 Provides Authorization to Administer NRC Approved Initial Written Exams to Listed Applicants on 990913 at Peach Bottom Npp,Delta,Pennsylvania ML20211K7031999-08-30030 August 1999 Forwards Response to NRC 990826 RAI Re License Change Application ECR 99-01255,revising TSs 2.1.1.2 & 5.6.5 ML20211E6941999-08-26026 August 1999 Forwards Request for Addl Info Re Min Critical Power Ratio. Response Should Be Submitted within 30 Days of Ltr Receipt ML20211Q4491999-08-25025 August 1999 Responds to Re Changes to PBAPS Physical Security Plan,Safeguards Contingency Plan & Guard Training & Qualification Plan Identified as Revs 13,11 & 9, Respectively.No NRC Approval Is Required,Per 10CFR50.54(p) ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20211D5421999-08-23023 August 1999 Forwards Amends 228 & 231 to Licenses DPR-44 & DPR-56, Respectively & Se.Amends Revise TSs to Correct Typographical & Editorial Errors Introduced in TSs by Previous Amends ML20211A9721999-08-20020 August 1999 Forwards Request for Addl Info Re Third 10-year Interval Inservice (ISI) Insp Program Plan for Plant,Units 2 & 3 ML20210T5451999-08-12012 August 1999 Forwards Copy of Environ Assessment & Findings of No Significant Impact Re Licensee Request for Amends to Plant. Amends Consist of Changes to TS to Correct Typos & Editorial Errors Introduced in TS by Previous Amends ML20210P8321999-08-11011 August 1999 Responds to NRC 990715 Telcon Re Util 990217 Submittal of Proposed Alternatives to Requirements of 10CFR50.55a(g)(6)(ii)(B)(1) Re Containment Inservice Insp Program ML20210P8151999-08-11011 August 1999 Forwards Final Pages for Pbaps,Unit 2 & 3 OLs Re License Change Application ECR 99-01497,which Reflects Change in Corporate Structure at Pse&G ML20211B6521999-08-10010 August 1999 Informs That Dp Lewis,License SOP-11247,has Been Permanently Reassigned & No Longer Requires License,Per 10CFR50.74.Util Requests That Subject Individual Be Removed from List of License Holders ML20210P1561999-08-10010 August 1999 Submits Response to Requests for Addl Info Re GL 92-01,rev 1,Suppl 1, Rv Structural Integrity, for Pbap,Units 1 & 2. NRC Will Assume That Data Entered Into Rvid Are Acceptable for Plants,If Staff Does Not Receive Comments by 990901 ML20211B7881999-08-10010 August 1999 Transmits Summary of Two Meetings with Risk-Informed TS Task Force in Rockville,Md on 990514 & 0714 ML20210N7831999-08-0909 August 1999 Forwards Copy of Notice of Consideration of Issuance of Amends to Fols,Proposed NSHC Determination & Opportunity for Hearing, Re 990806 Request for License Amends.Amends Incorporate Note Into PBAPS TS to Permit One Time Exemption ML20210P0801999-08-0404 August 1999 Forwards Initial Exam Repts 50-277/99-301 & 50-278/99-301 on 990702-14 (Administration) & 990715-22 (Grading).Six of Limited SRO Applicants Passed All Portion of Exam ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response NUREG-1092, Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls1999-08-0303 August 1999 Informs J Armstrong of Individual Exam Results for Applicants on Initial Exam Conducted on 990702 & 990712-14 at Facility.All Six Individuals Who Were Administered Exam, Passed Exam.Without Encls ML20210J0161999-07-30030 July 1999 Forwards Copy of Notice of Consideration of Approval of Transfer of FOL & Issuance of Conforming Amends Re 990723 Application ML20210H5341999-07-27027 July 1999 Forwards Insp Repts 50-277/99-05 & 50-278/99-05 on 990518- 0628.NRC Determined That Two Severity Level IV Violations of NRC Requirements Occurred & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20210F3731999-07-23023 July 1999 Submits Confirmation That,Iaw 10CFR50.80,PSE&G Is Requesting NRC Approval of Transfer of Ownership Interests in PBAPS, Units to New Affiliated Nuclear Generating Company,Pseg Nuclear LLC ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20210E5811999-07-21021 July 1999 Forwards Final Tech Specs Pages for License Change Application.Proposed Change Will Revise Tech Specs to Delete Requirement for Refuel Platform Fuel Grapple Fully Retracted Position Interlock Currently Required by TS ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217F3021999-10-12012 October 1999 Provides Written Confirmation That Thermo-Lag 330-1 Fire Barrier Corrective Actions at PBAPS Have Been Completed.Ltr Also Confirms Completion of Actions Required by Confirmatory Order Modifying Licenses, ML20217E7451999-10-0808 October 1999 Forwards Response to NRC 990820 RAI Concerning Proposed Alternatives Associated with Third ten-yr Interval ISI Program for Pbaps,Units 2 & 3 ML20217C4141999-10-0606 October 1999 Forwards Response to NRC 981109 RAI Re Resolution of USI A-46 for Pbaps.Proprietary Excerpts from GIP-2,Ref 25 Results of BWR Trial Plant Review Section 8 Also Encl. Proprietary Excerpts Withheld ML20217B9151999-10-0606 October 1999 Provides Clarifying Info to Enable NRC to Complete Review of License Change Request ECR 98-01802,re Changes Necessary to Support Installation of Digital Pr Neutron Monitoring & Incorporate long-term T/H Stability Solution Hardware ML20217B7701999-10-0606 October 1999 Submits Corrected Info to NRC 980528 RAI Re Util Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions ML20217B8891999-10-0101 October 1999 Forwards Response to RAI Re Request to Install Digital Power Range Neutron Monitoring Sys & Incorporate long-term,thermal-hydraulic Stability Solution Hardware. Revised TS Table 3.3.2.1-1 Encl 05000278/LER-1999-004, Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv)1999-10-0101 October 1999 Forwards LER 99-004-00 Re Multiple Unplanned ESF Actuations During Planned Mod Activities in Main Cr,Per Requirements 10CFR50.73(a)(2)(iv) ML20217D5211999-09-30030 September 1999 Informs That Remediating 3D Monicore Sys at Pbaps,Units 2 & 3 & 3D Monicore/Plant Monitoring Sys at Lgs,Unit 2 Has Been Completed Ahead of Schedule ML20216J3981999-09-29029 September 1999 Submits Comments for Lgs,Unit 1 & Pbaps,Units 2 & 3 Rvid,Rev 2,based on Review as Requested in GL 92-01,rev 1,suppl 1, Reactor Vessel Structural Integrity ML20212H6171999-09-24024 September 1999 Forwards Rev 2 to COLR for Pbaps,Unit 2,Reload 12,Cycle 13, IAW TS Section 5.6.5.d.Rept Incorporates Revised Single Loop Operation MAPLHGR Flow Multiplier ML20212H5431999-09-24024 September 1999 Informs of Decision to Inspect H-3 & H-4 Shroud Welds During Upcoming 3R12 Outage Scheduled to Begin Late Sept 1999 ML20216F8811999-09-23023 September 1999 Withdraws 990806 Exigent License Change Application.Tech Spec Change to Allow Continued Power Operation with Elevated Cooling Water Temps During Potentially Extreme Weather Conditions No Longer Needed Due to Favorable Weather ML20212F5481999-09-20020 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing, for Pbaps,Units 2 & 3 & Lgs,Units 1 & 2 ML20212A0091999-09-0909 September 1999 Provides Notification That Licenses SOP-11172 & SOP-11321, for SO Muntzenberger & Rh Wright,Respectively,Are No Longer Necessary as Result of Permanent Reassignment ML20211K7031999-08-30030 August 1999 Forwards Response to NRC 990826 RAI Re License Change Application ECR 99-01255,revising TSs 2.1.1.2 & 5.6.5 ML20211E9191999-08-24024 August 1999 Forwards fitness-for-duty Program Performance Data for Jan-June 1999 for PBAPS & LGS IAW 10CFR26.71(d).Data Includes Listed Info ML20210P8321999-08-11011 August 1999 Responds to NRC 990715 Telcon Re Util 990217 Submittal of Proposed Alternatives to Requirements of 10CFR50.55a(g)(6)(ii)(B)(1) Re Containment Inservice Insp Program ML20210P8151999-08-11011 August 1999 Forwards Final Pages for Pbaps,Unit 2 & 3 OLs Re License Change Application ECR 99-01497,which Reflects Change in Corporate Structure at Pse&G ML20211B6521999-08-10010 August 1999 Informs That Dp Lewis,License SOP-11247,has Been Permanently Reassigned & No Longer Requires License,Per 10CFR50.74.Util Requests That Subject Individual Be Removed from List of License Holders ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML20210F3731999-07-23023 July 1999 Submits Confirmation That,Iaw 10CFR50.80,PSE&G Is Requesting NRC Approval of Transfer of Ownership Interests in PBAPS, Units to New Affiliated Nuclear Generating Company,Pseg Nuclear LLC ML20210E6211999-07-22022 July 1999 Submits Rev to non-limiting Licensing Basis LOCA Peak Clad Temps (Pcts) for Limerick Generating Station (Lgs),Units 1 & 2 & Pbaps,Units 2 & 3 ML20210E5811999-07-21021 July 1999 Forwards Final Tech Specs Pages for License Change Application.Proposed Change Will Revise Tech Specs to Delete Requirement for Refuel Platform Fuel Grapple Fully Retracted Position Interlock Currently Required by TS ML20216D8041999-07-19019 July 1999 Submits Summary of Final PECO Nuclear Actions Taken to Resolve Scram Solenoid Pilot Valve Issues Identified in Info Notice 96-007 05000278/LER-1999-002, Forwards LER 99-002-01 to Correct Title Contained in Box (4) of LER Coversheet Form.Rev Does Not Change Reportability Requirements or Any Other Info Contained in Original Submittal of LER1999-07-12012 July 1999 Forwards LER 99-002-01 to Correct Title Contained in Box (4) of LER Coversheet Form.Rev Does Not Change Reportability Requirements or Any Other Info Contained in Original Submittal of LER ML20209G9121999-07-0909 July 1999 Informs That Ja Hutton Has Been Appointed Director,Licensing for PECO Nuclear,Effective 990715.Previous Correspondence Addressed to Gd Edwards Should Now Be Sent to Ja Hutton ML20209D9781999-07-0808 July 1999 Forwards Addl Info to Support EA of Proposed 990212 License Application ECR 98-01675,correcting Minor Administrative Errors in TS Figure Showing Site & Exclusion Areas Boundaries & Two TS SRs ML20209D8821999-07-0707 July 1999 Submits Estimate of Number of Licensing Actions Expected to Be Submitted in Years 2000 & 2001,as Requested by Administrative Ltr 99-02.Renewal Applications for PBAPS, Units 2 & 3,will Be Submitted in Second Half of 2001 ML20209D2671999-07-0202 July 1999 Responds to NRC 990322 & 0420 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20209E1131999-06-30030 June 1999 Forwards Proprietary NRC Form 398, Personal Qualification Statement-Licensee, for Renewal of RO Licenses for EP Angle,Md Lebrun,Jh Seitz & Zi Varga,Licenses OP-10646-1, OP-11081,OP-11082 & OP-11085,respectively.Encls Withheld ML20209B7001999-06-30030 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20209C1201999-06-30030 June 1999 Informs of Util Intent to Request Renewed License for PBAPS, Units 2 & 3,IAW 10CFR54.Licensee Anticipates That License Renewal Application Will Be Submitted in Second Half of 2001 05000277/LER-1999-004, Forwards LER 99-004-00 Re Unplanned ESF Actuations During Planned Electrical Bus Restoration Following Maint Activities1999-06-20020 June 1999 Forwards LER 99-004-00 Re Unplanned ESF Actuations During Planned Electrical Bus Restoration Following Maint Activities ML20196A5291999-06-14014 June 1999 Forwards Final Pbaps,Unit 3 TS Pages for License Change Request ECR 98-01802 Re Installation of Digital Power Range Neutron Monitoring (Prnm) Sys & Incorporation of long-term thermal-hydraulic Stability Solution Hardware ML20195E6051999-05-27027 May 1999 Requests Exemption from Requirements of 10CFR72.44(d)(3) Re Submittal Date for Annual Rept of Principal Radionuclides Released to Environ.Exemption from 10CFR72.72(d) Re Storage of Spent Fuel Records,Additionally Requested ML20195B8171999-05-25025 May 1999 Forwards Final TS Pages for License Change Application ECR 96-01511 Re Rev to Loss of Power Setpoints for 4 Kv Emergency Buses ML20195B6191999-05-19019 May 1999 Forwards PBAPS Units 2 & 3 Annual Radiological Environ Operating Rept 56 for 980101-1231, Per Section 6.9.2 of Ol. Trace Concentrations of Cs-137 Were Found in Sediment Consistent with Levels Observed in Previous Years ML20206P9171999-05-10010 May 1999 Updates Some of Transmitted Data Points Provided in Data Point Library ERDS for Pbaps,Units 2 & 3.Data Point Info Format Consistent with Guidance Specified in NUREG-1394 ML20206K6581999-05-0404 May 1999 Forwards PBAPS Bases Changes Through Unit 2 Bases Rev 25 & Units 3 Bases Rev 25.Bases Reflect Change Through Apr 1999, Thereby Satisfying Frequency Requirements of 10CFR50.71 ML20206D4651999-04-29029 April 1999 Forwards Rev 16 to UFSAR & Rev 11 to Fire Protection Program (Fpp), for Pbaps,Units 2 & 3.Page Replacement Instructions for Incorporating Rev 16 to UFSAR & Rev 11 to Fpp,Encl ML20207B8431999-04-23023 April 1999 Forwards Final Rept for 981117,plume Exposure Pathway Exercise of Offsite Radiological Emergency Response Plans site-specific for Peach Bottom Atomic Power Station.One Deficiency & 27 Areas Requiring C/A Identified ML20206C5461999-04-20020 April 1999 Forwards Radioactive Effluent Release Rept 41 for Jan-Dec 1998 for Pbaps,Units 1 & 2. Revs Made to ODCM & Station Process Control Program (PCP) During Rept Period,Encl 05000277/LER-1999-003, Forwards LER 99-003-00 Re 990318 Failure to Maintain Provisions of Fire Protection Program to Properly Address Effects of Flooding1999-04-16016 April 1999 Forwards LER 99-003-00 Re 990318 Failure to Maintain Provisions of Fire Protection Program to Properly Address Effects of Flooding ML20205K4541999-04-0808 April 1999 Forwards Revised Info Re 990330 NRC Nuclear Power Reactor Licensee Financial Qualifications & Decommissioning Funding Assurance Status Rept 05000278/LER-1999-001, Forwards LER 99-001-00 Re 990312 ESF Actuation of Rcics Due to High Steam Flow Signal During Sys Restoration.Rept Submitted Per 10CFR50.73(a)(2)(iv)1999-04-0808 April 1999 Forwards LER 99-001-00 Re 990312 ESF Actuation of Rcics Due to High Steam Flow Signal During Sys Restoration.Rept Submitted Per 10CFR50.73(a)(2)(iv) ML18106B1431999-03-31031 March 1999 Forwards Pse&G Rept on Financial Min Assurance for Period Ending 981231 for Hope Creek,Salem,Units 1 & 2 & Pbaps,Units 2 & 3,IAW 10CFR50.75 ML20205F8981999-03-31031 March 1999 Provides Info Re Status of Decommissioning Funding for LGS, Units 1 & 2,PBAPS,Units 1,2 & 3 & Sgs,Units 1 & 2,per Requirements of 10CFR50.75(f)(1) ML18106B1411999-03-30030 March 1999 Forwards Decommissioning Info on Behalf of Conectiv Nuclear Facility License Subsidiaries,Atlantic City Electric Co & Delmarva Power & Light Co,For Listed Nuclear Facilities ML20205J0831999-03-26026 March 1999 Requests Enforcement Discretion from Requirements of PBAPS, Units 2 & 3 Ts.Enforcement Discretion Pursued to Avoid Unneccessary Plant Transient Which Would Result from Compliance with TS ML20205B6421999-03-24024 March 1999 Submits 1998 Annual Decommission Rept for Pbaps,Unit 1. There Were No Reportable Events Involving Unit 1 for 1998 1999-09-09
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-. P . 14014 PillLADELPillA ELECTRIC COMPANY Pf ACH halTOM AIUMIC POWIR STATION It D.1. Box 208 Delta. Itnns)1vanta 17314 rsu n sortu%Tus emir of areitem n (71)4 W 70ld D 11. Mmet, Jr.
Vice Prestent February 5, 1991 Docktt Hos. 50-277 50-278 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, OC 20S55
SUBJECT:
Peach Bottom Atomic Power Station - Units 2 & 3 '
Reply to Notice of Violations (CombinedInspectionReportHos. 50-277/90-22; 50-278/90-22)
Dear Sir,
In response to your letter dated December 28, 1990, which tras mitted the Notice of Violations concerning the referenced Inspection Report, we submit the attached responses. The subject Inspection Report concerned a routine resident safety inspection during the period October 30 through December 3, 1990.
If you have any questions or require addittoral information, please do not hesitate to contact us. ('
kb,k' / /4 ,
/-
cc: R. A. Burricelli, Public Service tiectric & Gas T. M. Gerusky, Commonwealth of Pennsylvania J. J. Lyash, USNRC Senior Resident inspector T. T. Martin, Administrator, Region 1. USNRC H. C. Schwemm. Atlantic Electric rt. 1. McLean, State of Maryland J. Urban, Delmarva Power h
9102110200 910205 # l PDR ADOCK 05000277 l/ l I
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Document Control Desk -
n- 'F5bruary.5,1991
- d ' .
- Page-2 bcc: J..A. Basilio 52A-5,-Chesterbrook
- G. J.-Beck 52A-5, Chesterbrook J. A.-Bernstein 51A-13 Chesterbrook R. N.. Charles- .
51A-1, Chesterbrook Commitment Coordinator- .
52A-5, Chesterbrook Correspondence Control Program 618-3, Chesterbrook J. B. Cotton- 53A-1, Chesterbrook E.1J. Cullen S23-1, Main Office A. D. Dycus A3-IS, Peach Bottom
~E. P. Fogarty A4-4N, Peach Bottom J. F. Franz A4-15,-Peach Bottom An A. fulvio- A4-1S, Peach Bottom D. R. Helwig 51A-11, Chesterbrook '
R.-J.-Lees,.NRB- 53A-1. Chesterbrook
- C. J McDermott S13-1. Main Office D. B. Miller. Jr. SM0-1, Peach Bottom. !
=PB~ Nuclear Records A4-25, Peach; Bottom J. M. Pratt B-2-S, Peach Bottom L. B. Pyrih 638-5 Chesterbrook J. T. Robb- 51A-13, Chesterbrook
- D..M. Smith: 52C-7, Chesterbrook J
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- Pebruary.5, 1991-
, Page_3 K;JLY TO NOTICE OF VIOLATION 90-22-01 Restatement of Violation A. The. Code of federal Regulations, Title 10, Part 50, Appendix 8. Criterion XVI, " Corrective Action," states in pcrt that measures shall be established to assure thet conditions adverse.to quality, such as defective materiel and equipment, are promptly identified and corrected.
- 1. Contrary to the above, on November 5, 1990, a leak was caused and identified in the-supply line from the' seismically qualified nitrogen l supply to.the boot seal of inboard primary. containment isolation valve A0-2520. Immediate corrective actions were not implemented and the bottle depressurized to zero psig. Since the outboard valve was already inoperable with its boot seal deflated, a potential. primary containment. leak path would have existed in the ,
event of a design basis accident.
2.. Contrary to the above on May 3-4, 1990, and since August 29,=1990,
. primary l containment isolation valve A0-2519 was inoperable. Data collected during daily.surveillances indicated that, leakage in excess of the allowable existed.. making the seismically qualified ;
backup nitrogen supply inadequate toLassure valve operability. '
Philadelphia Electric Company did not declare the valve inoperable,-
and did not initiate' action to promptly repair _the valve. .
ThisisaSeverity'LevelIVViolation(Supplement!).
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Document Control Desk F6bruary 5, 1991
- Page 4 Event Description A.1 The valve operator and boot seal of the Containment Isolation Valves are supplied pressure by the Instrument Air System under normal operation.
In the event of a loss of instrument air, backup nitrogen (N2) is supplied from compressed gas cylinders to maintain boot seal pressure.
For a Design Basis seismic event or loss of offsite power, the normal I supply to the valves would be lost, and the boot seals would be supplied by the N2 cylinders to maintain containment integrity.
On November 5, 1990, an operator replacing the compressed nitrogen gas cylinder that supplies backup gas pressure to the A0-2505 valve disturbed the N2 supply line to the A0-2520 valve causing it to leak. The operator made a temporary repair and then immediately notified the Shift Supervisor in the control room that the leak was stopped but would require further maintenance. The Shift Supervisor initiated a Maintenance Request form which was to be completed the next day.
During the porformance of Surveillance Test (ST) 7.9.2-2, " Daily Check of Seismic Gas Supply 80ttic Pressures" on November 6, 1990, the N2 cylinder that supplied A0-2520 was discovered empty. An Equipment Trouble Tag was in place at that time identifying the tubing leak. While replacing the cylinder, the Operator noticed that the leak was rapidly bleeding down the gas pressure so he isolated the bottle and notified the Control Room Supervisor who requested immediate maintenance repair. The System Engineer also became involved at this time and noted that the A0-2520 valve was in line with the Outboard A0-2521A valve, which had its boot seal deflated in order to perform maintenance.
An operability ietermination was then initiated to evaluate the Primary Containment isolation Capability of the A0-2520 valve. The importance of the backup N2 supply was not well understood and the lack of guidance given in the Technical-Specifications delayed the operability determination. A determination was made to declare A0-2520 inoperable for the purpose of the primary containment isolation due to the lack of backup H2 to the boot seal. Technical Specification 3.7.'u.2 was entered for an inoperable isolation valve. The N2 tubing on A0-2520 was repaired a short time later re-establishing the N2 supply and the valve was returned to an operable status. Although a p7tential containment leak path existed through the boot seals of the inboard and outboard Containment Isolation Valves due to the condition of the backup N2 supply, the boot seal was continually supplied pressure from instrument air. The actual integrity of the boot seal and primary containment was never compromised. During the investigation of the event, it was determined that Tech Spec 3.7,0.2 did not apply since A0-2521A was already considered an inoperable isolation valve due to maintenance activities. It-was concluded that Tech Spec 3.7.A.3 involving containment integrity should have been entered. Tech Spec 3.7.A.3 allows 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to re-establish containment integrity, or the reactor must be placed in cold shutdown in the next 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Tech Spec compliance was
Document Control Desk
. February 5, 1991 o Page 5 met but there was confusion in determining the appropriate Tech Spec to us9.
Event Description A.2 A resident NRC inspector discovered on November 8, 1990, that the bottle pressure for the backup N2 supply to A0-2519 was less than the acceptable value specified in ST 7.9.2-2. The Shift Supervisor was immediately notified. The bottle was found with a leaking regulator and was replaced. The inspector then reviewed a sample of surveillance test data recorded for A0-2519 since January, 1990, and identified that A0-2519 was inoperable on May 3-4, 1990. Subsequently, additional reviews performed by the System Engineers determined that the valve was inoperable since August 29, 1990. During these periods the leakage rate was such that the seismic backup N9 supply to A0-2519 would not have provided the required 20 day supply in case of a Design Basis seismic event or loss of offsite power. The 20 day supply requirement was contained in a Justification for Continued Operation (JCO) tnat was not adequately addressed in the. 1T 3 at shift personnel were not aware of this requirement. Additionally, toe ST only monitored bottle pressure and did not address leak-rates.
Notification of the Syttem Engineer on bottle change-out was also not being accomp'lished in accordance with the ST. Operations personnel did not understand that the reason the System Engineers were to be notified-was to evaluate. abnormal leak rates. Although the backup N2 supply for A0-2519 was in a degraded condition, the boot seal integrity was maintained by the normal supply of instrument air.
Reasons for the Violation The operability requirements and importance of the Backup N2 System were
-not fully understood by Operations. Additionally, the ambiguity of the Tech Specs was also a contributing factor. ST 7.9.2-2 was inadequate in that it did not address leak rates, JC0 requirements, or the importance of notifying System Engineers after bottle replacement.
Corrective Steps Taken and the Results Achieved The tubing _ leak on A0-2520 was repaired on November 6, 1990, re-establishing the back-up H2 supply. The N2 cylinder that supplied A0-2519 was replaced on November 8, 1990. Evet Investigations were initiated for both incidents to determine caues and develop corrective measures to prevent recurrence. On November 36, 1990, a meeting was held with staff management and the NRC to discuss the results of these investigations and planned corrective arthat Operations personnel were verbally informed of these incidents and the resulting impact on operability determinations. A follow-up package of information was provided to appropriate Operations personnel on December 7, 1990, to further enhance their awareness and ur<derstanding of the backup nitrogen supply system and associated operability requirements.
Additionally, this package also contained information concerning the
Document Control Desk j February 5, 1991
' + Page 6 importance and reasoning why the system engineer is required to be notified whenever a bottle is replaced. This discussion was also provided to heighten Operations sensitivity to proper review and disposition of the surveillance test results.
Operations personnel were also provided with an analysis of Technical Specification 3.7,0.2 and 3.7 A.3 as they pertained to these events.
This discussion examined the operability determinations and the interpretations proposed during and after the incident, and provided guidance on how to correctly interpret these Tech Soecs.
Criteria to address allowable leakage rates and sign-offs for System Engineer notification were also provided through a temporary change to ST 7.9.2-2. In addition, System Engineers now monitor the results of ST 7.9.2-2 to correct any problem where excess leakage could result in an inability to successfully maintain the 20 day back-up supply.
Corrective Steps That Will Be Taken To Avoid future Violations A modification (Mod 1316) is currently in progress on Unit 2 to install a backup pressure supply to the boot seals of the Containment Isolation
-valves from the Containment Atmospheric Dilution (CAD) system. This modification, which has already been installed on Unit 3, will eliminate the requirement for the bottle supplied backup N2 system for these valves. The projected date of completion for this modification is March 15, 1991. Once Mod 1316 is completed, ST 7.9.2-2 will be permanently revised to comnletely address the operability concerns for N2 bottles used in other applications.
Existing JCO's will be reviewed for required procedure revisions and training issues. A tracking mechanism will he established for action items resulting from JCO's.
Date When full Compliance Was Achieved full compliance was achieved November 8, 1990, when the N2 cylinder supplying A0-2519 was replaced and the 20 day backup supply was achieved.
'The H2 backup supply to A0-2520 was re-established on November 6, 1990, when the N2 supply line leak was repaird.
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10pcumentCont'rol?0esk Lf.ebruary 5, 1991
- O .Page 7 I
REPLY TO NOTICE OF VIOLATION 90-22-03 R'estatement of Violation B. Technical Specification (TS) 6.S.1 states that written procedures and administrative policies shall be established and implemented that meet the requirements.of ANSI N18.7-1972,_ Section 5.3, and Regulatory Guide (RG)1.33(1972). ANSI N18-7. Section 5.3.6, and RG 1.33, Section ti, ;
require procedures'for the control, storage and use of measuring and test.
equipment (M&TE). TS 6.5.16 states that the Plant Operation Review Committee (DORC) shall be responsible for review of all procedures required by TS 6,8. ,
Contrary to the above, as of December 3, 1990, the licensee had not established or implemented a PORC approved procedure addressing the control, storage and use of-M&TE as required by the TS 6.8.1'and 6.5.16.
This is.a Severity Level-IV Violation (Supplement !).
Event Description-
-The~ Instrument and Controls (l&C) Shop was originally the Station Test .
Section of the Research and Testing-(R&T) and.later Testing and Laboratories--(T&L). The R&T Divisiorrwas identified in the Quality Assurance (QA)Plantobe"responsibletotheElectricProduction Department for the performance of maintenance of instrumentation as
= delegated." Additionally, the R&T--Division Administrative Procedures for the controls of-instrument maintenance activities were to be prepared and
- approved.in!accordance with the QA Plan.- These procedures required
. approval by management 11evel personnel in'both R&T and QA.
In addition to site equipment maintenance and calibrations, R&T was-cresponsible for the c$libration of the test standards used by the site. ,
This was accomplished off-site and was controlled by appropriate .
t
- procedures. These procedures, though not PORC approved, .had significant technical and quality review.
The Construction. Division and Maintenance Department were also major-
, users.of measuring and-test equipment (H&TE). To control the use of M&TE-Construction utilized the Construction Division-Implementing Procedures
. (C0!P). Maintenance eventually developed their own PORC and QA approved
- Maintenance Administrative (MA)-procedures. Control of M&TE however, was
- considered R&T Department responsibilities.
i .- -
- As a result-of.the shutdown of Peach Bottom in 1987, signifIcant :
' organizational and personnel changes were implemented. One of these :
. reorganizations consisted of removing the I&C Group from T&L and
. including it within the Station organization. T&L Administrative L
procedures were not adequately addressed during this reorgy Ization and original personnel famillar with the requiraments of T&L procedures were I
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- Opcument' Control Desk--
- ' February 5, 1991-
- PageL8 re-assigned, resulting in a lack of experienced personnel and administrative control.
Nuclear Qual 1ty Assurance (HQA) conducted an audit (PA-89-24) of M&TE Control f_ rom October 10-25, 1989. During this audit _NQA identified several performance discrepancies, including the lack of an approved method to control M&TE. HQA noted that.the station was awi 0 of the need for an administrative procedure and that one was in development, it was believed that the procedure would be approved in the near term and was not tracked to a firm completion date. Reassignment of personnel and changes in the Maintenance /l&C Organization were made however, and the procedure was never issued. Corrective Action Request PA-89-24-02 remains open until the Administrative procedure is PORC approved.
During the Unit 3 mid-cycle outage, I&C personnel identified some Rosemount transmitters outside of their expected calibration band. Upon review of the corrective actions to address this problem, the Resident NRC-. Inspector identified that a PORC and QA approved procedure establishing and implementing a M&TE program had not bcen established, lt Reasons for'the Violation The, reasons for the violation include less than adequate turnover of-responsibilities during the transfer of I&C personnel to the station and previously not having T&L procedures PORC approved. - The transition of the_I&C-Group from T&L to the station without adequately incorporating
- appropriate T&L administrative controls resulted in not having a controlling document for M&TE in place.
Correct'ive Steps Taken And Results Achieved A-Maintenance Guideline has been established for Maintenance /l&C use which contains the appropriate direction for use, control, issue,.
segregation, review and storage of M&TE until a M&TE Administrative Procedure is implemented. Other T&L-. procedures are currently being incorporated into PORC approved station procedures as necessary.
-Additionally, actions have been taken to improve the M&TE process. The I&C M&TE Room was enlarged to allow better control and organization of test equipment as well as establishing improved access centrol. A computer bar code system has also been implemented-to imptove equipment traceability.
.An Administrative Foreman position has been established, whose duties
-include control of.the M&TE Room and review of Out-of-Tolerance reports.
Additional personnel have been assigned to the M&TE-Room and procedure development.
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Documert Control Desk
- j. .. february 5,_1991 Page 9 Corrective Steps lhat Will Be Taken To Avoid Future Violations An Administrative Procedure has been drafted for the control of M&TE at PBAPS which includes provisions fce the use, issue, segregation and storage of M&TE as well as the review for cut-of-tolerance reports. This procedure will-be appropriately reviewed and approved by the Plant OperatingReviewCommittee(PORC)andQualityAssurance. This procedure will be approved for use by March 15, 1991.
Date When Full Compliance Will Be Achieved Full compliance will _be achieved upon the completion of a PORC approved
-procedure addressing the control, storage and use of M&TE. This procedure will be completed and PORC approved by March 15, 1991.
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