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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17326A2011999-08-23023 August 1999 LER 99-004-00:on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With 990823 Ltr ML20029C7321994-04-22022 April 1994 LER 94-004-00:on 940221,discovered Corrosion of Three Nuts on One of Incor Instrumentation Reactor Vessel Head.Caused by Increase of Wet Boric Acid.Leaking Flanges Repaired.W/ 940422 Ltr ML20046B4731993-07-30030 July 1993 LER 93-005-00:on 930630,TS 3.0.3 Entered Due to Both Containment Spray Sys Inoperable.Replaced CCW Outlet Valve Actuator Connecting Link Assembly from Number 11 SDC Heat exchanger.W/930730 Ltr ML20046A4911993-07-22022 July 1993 LER 93-003-00:on 930625,SG Tripped Due to Low Water Level. Caused by Insufficient Feedwater Addition Due to Inadequate Communication.Reemphasis on Improved Communication Stressed. W/930722 Ltr ML20045G8611993-07-0909 July 1993 LER 93-003-00:on 930610,dual Unit Trip Occurred Due to Partial Loss of Offsite Power.Flashover Protection Relay for Breaker 552-61 Replaced & Training for Personnel W/ Access to Relays Will Be reinforced.W/930709 Ltr ML20045G7281993-07-0808 July 1993 LER 93-002-00:on 930608,inadvertent Arw Actuation Sys & RPS Actuations Experienced During Performance of Awf Sys Large Flow Surveillance Testing.Caused by Failure to Note Differential Pressure Condition.Valve opened.W/930708 Ltr ML20045G8661993-07-0808 July 1993 LER 93-004-00:on 930611,reactor Tripped Due to Turbine Trip Resulting from Inadequate Procedure.Procedure Changes Made to Open Appropriate FW Heater High Level Dump Valves During Plant startup.W/930708 Ltr ML20045E7361993-06-29029 June 1993 LER 93-002-01:on 930205,software Vendor Discovered Error in User Manual for Updating Basss data-input Library.Caused by Failure of QA Procedures to Require Independent Review of User Manuals.Manual Surveillances performed.W/930629 Ltr ML20029B1261991-02-28028 February 1991 LER 91-001-00:on 910129,tubing in Air Start Sys for Emergency Diesel Generator Failed During Seismic Event. Caused by Error in Design of EDG Air Start Sys.Permanent Mod to Sys installed.W/910228 Ltr ML20028H8011991-01-24024 January 1991 LER 90-002-01:on 900116,determined That 891211 Reconstitution of More than One Spent Fuel Assembly Per Time in Violation of Fuel Handling Incident Safety Analysis. Caused by Deficient procedure.W/910124 Ltr ML20044A1861990-06-20020 June 1990 LER 87-002-01:on 861203,section of Thin Wall Found on Main Steam Line W/Readings Below Allowable Min of 0.95 Inches. Caused by Grinding of Edge of Pipe to Achieve Proper fit-up for Welding.Relief from IWB-3610 granted.W/900620 Ltr ML20043G1071990-06-13013 June 1990 LER 89-019-01:on 891128,determined That for Approx 10 Yrs, from 1979-1989,requirement to Lock HPSI Discharge Header Isolation Valves Shut Not Implemented.Caused by Inadequate Mgt Attention.Test Procedures modified.W/900613 Ltr ML20043F1221990-06-0404 June 1990 LER 90-017-00:on 900505,pin Hole Leak Observed in Discharge Piping of Saltwater Pump 13.Caused by Localized Corrosion. Leaking Spool Piece Removed & Blank Flange Installed. W/900604 Ltr ML20043A7871990-05-21021 May 1990 LER 90-016-00:on 900421,determined That Waste Gas Decay Tank (Wgdt) 13 Discharged Instead of (Wgdt) 11 for Discharge Permit Issued.Caused by Inadequate Communications.Training Performed for Operators Re event.W/900521 Ltr ML20043A3441990-05-14014 May 1990 LER 90-014-00:on 900413 & 19,unit Entered Tech Spec Limiting Condition of Operation 3.0.3 Due to Potential Inoperability of Three Out of Four Reactor Protection Sys Delta T Power Channels.Caused by Lack of Procedure guidance.W/900514 Ltr ML20043A3401990-05-14014 May 1990 LER 90-013-00:on 900413,determined That Axial Shape Index Channels Out of Spec & Inoperable.Caused by Inadequate Understanding of Design Basis for Excore/Incore Comparison. Design Basis for Excore/Incore improved.W/900514 Ltr ML20042G4521990-05-0707 May 1990 LER 90-015-00:on 900407,discovered That Relay Contact Which Actuates Reactor Trip Breaker Shunt Trip Not Adequately Functionally Tested.Caused by Failure to Examine Circuit in Detail When Test developed.W/900507 Ltr ML20042F5801990-05-0404 May 1990 LER 90-012-00:on 900406,identified That Procedure for LOCA Would Not Ensure post-LOCA Core Flush Would Be Initiated in Time to Prevent Boron Precipitation.Caused by Personnel Error.Configuration Mgt Program strengthened.W/900504 Ltr ML20012E9931990-03-29029 March 1990 LER 90-008-00:on 900227,determined That Surveillance Procedure M-280-0 Did Not Include Steps to Fully Test Control Room Recorder for Hydrogen Analyzers.Caused by Personnel Error.Procedure Revised on 900308.W/900329 Ltr ML20012F0001990-03-28028 March 1990 LER 89-006-01:on 890508,containment Iodine Filters Outside Design Basis Due to Equipment Qualification.Recalculation of Total Integrated Radiation Dose to Cables for Filter Fans Demonstrated Cable qualified.W/900328 Ltr ML20012E9951990-03-28028 March 1990 LER 89-014-01:on 890723,determined That Salt Water Header Not Capable of Withstanding Seismic Event Intact.Caused by Inadequate Welding of Blind Spool Pieces in Pipe.Insp Revealed Spools Capable as installed.W/900328 Ltr ML20012E0101990-03-26026 March 1990 LER 90-009-00:on 900224,failure to Meet Action Requirement Re Tech Spec 3.7.12.Caused by Personnel Error.Cables Removed from Doorway in Charging Pump Room & Not Allowed to Be Placed in doorway.W/900326 Ltr ML20012C4971990-03-15015 March 1990 LER 90-007-00:on 900216,discovered That Supervised Circuits Associated W/Fire Detection Instruments Located in Reactor Coolant Pump Bays Not Been Included in Surveillance Test Procedure.Caused by Personnel error.W/900315 Ltr ML20012C4861990-03-12012 March 1990 LER 90-006-00:on 900209,determined That Four Fire Dampers Missing.Caused by Not Identifying Penetrations as Requiring Dampers When Fire Hazards Analysis of Plant Conducted.Hourly Fire Watch Continued.Missing Dampers installed.W/900312 Ltr ML20012B8991990-03-12012 March 1990 LER 89-023-01:on 891220,determined That Pipe Rupture in nonsafety-related Svc Water Subsystem Could Result in Rapid Draining of Subsystems That Serve Auxiliary Bldg.Task Force Formed to Determine Corrective actions.W/900312 Ltr ML20012B4221990-03-0606 March 1990 LER 89-012-01:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed.Caused by Procedural Deficiency.Procedures Revised to Include Valve & Surveillance Test Program Instruction revised.W/900306 Ltr ML20011F2701990-02-27027 February 1990 LER 90-001-01:on 900109,determined That Surveillance Tests Used to Perform Channel Calibr Tests for Acoustic Flow Monitoring Devices Inadequate.Caused by Personnel Error & Inadequate Procedures.Swapped Leads restored.W/900227 Ltr ML20011F2091990-02-27027 February 1990 LER 89-026-00:on 891128,determined That Particulate Levels in Samples Taken from Lower Third of Tanks Exceeded Allowable Limits.Caused by Inadequate Sampling Technique. Tanks Cleaned & Filled W/Clean fuel.W/900227 Ltr ML20006F8601990-02-22022 February 1990 LER 90-004-00:on 900123,discovered Fire Barrier Penetration Seal Open for Indeterminate Time W/O Performing Tech Spec 3.7.12.a Required Actions.Caused by Personnel Error. Temporary Fire Seal installed.W/900222 Ltr ML20006E0521990-02-0808 February 1990 LER 90-001-00:on 891221,discovered That Acoustic Indications for One PORV & One Safety Valve Were Reversed During Surveillance Test.Caused by Personnel Error.Swapped Leads Restored to Proper configuration.W/900208 Ltr ML20006B4801990-01-26026 January 1990 LER 89-022-00:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed,Violating Tech Specs.Caused by Procedural Deficiency.Surveillance Test Procedure Revised to Include Deleted valves.W/900126 Ltr ML19354D8931990-01-17017 January 1990 LER 89-024-00:on 891218,determined That Wires Which Connect Actuation Device Logic Relay Contacts to Remainder of Circuit Not Tested During Channel Calibr Test.Caused by Inadequate Test.Test Program Upgrade underway.W/900117 Ltr ML20005F1921990-01-10010 January 1990 LER 89-025-00:on 891208,Tech Spec Action Statement Entered When Ventilation Ducts Penetrating Fire Barrier Could Not Be Accessed to Determine If Fire Dampers Installed.On 891211, Fire Watch Missed.Caused by Personnel error.W/900110 Ltr ML20005E3971989-12-28028 December 1989 LER 89-019-00:on 891128,discovered That HPSI Discharge Header Isolation Valves Not Locked Shut When RCS in Water Solid Condition,Resulting in Operation Outside Design Basis. Procedure Revised to Require Valves closed.W/891228 Ltr ML19351A4551989-12-13013 December 1989 LER 89-020-00:on 891113,determined That Some Solenoid Valves & Valve Power Supplies for Saltwater Sys May Not Be Able to Perform Design Function After Design Basis Seismic Event. Cause Undetermined.Power Supplies upgraded.W/891213 Ltr ML20005D6611989-12-0606 December 1989 LER 89-018-00:on 891106,discovered That Many Air Operated Control Valves & piston-operated Dampers Which Utilize safety-related Air Accumulators Would Not Have Performed as Expected After Loss of air.W/891206 Ltr ML19325F3951989-11-10010 November 1989 LER 89-002-01:on 890228,discovered That Fire Barrier Penetration Inoperable & Action Statement Requirements Not Satisfied.Caused by Inadequate Administrative Controls. Penetration Returned to Operable status.W/891115 Ltr ML19325E8221989-11-0303 November 1989 LER 89-007-01:on 890505,evidence of Reactor Coolant Leakage from 120 Pressurizer Vessel Heater Penetrations Discovered. Caused by IGSCC of Inconel 600.All Penetrations Using J-welds & Inconel 600 Visually inspected.W/891103 Ltr ML19324B2511989-10-27027 October 1989 LER 89-012-01:on 890720,discovered That Master Solenoid to Switchgear Room Halon Sys Disconnected Since 890629.Caused by Personnel Error Resulting from Lack of Written Procedure. Procedure Revised to Apply Temporary mods.W/891027 Ltr ML19325C3281989-10-10010 October 1989 LER 89-016-00:on 890908,determined That as-found Condition of Resistance Temp Detectors Did Not Match Tested Configuration.Cause Not Stated.Subj Detectors Will Be Sealed,Per Environ Qualification requirements.W/891010 Ltr ML19325C3701989-10-0909 October 1989 LER 89-017-00:on 890907,determined That Discrepancy in Acceptance Criteria of Surveillance Test Procedure M-452-0 Resulted in Failure to Fully Comply W/Requirements of Tech Spec 3.9.12.Main Cause undetermined.W/891009 Ltr ML20024F3771983-08-25025 August 1983 LER 83-044/03L-0:on 830808,diesel Generator 12 Tripped on Low Jacket Cooling Water Pressure While Verifying Operability.Cause Not Stated.Coolant Jacket Vented & Large Amount of Air Found.No Evidence of leakage.W/830825 Ltr ML20024F5731983-08-25025 August 1983 LER 83-040/03L-0:on 830727,control Room Air Conditioner 11 Discovered W/Damaged Condenser Fan.Caused by Loose Set Screws Securing Fan in Position.Set Screws Restored. W/830825 Ltr ML20024E6761983-08-0404 August 1983 Updated LER 83-011/03X-1:on 830207,during Surveillance Testing ESFAS a Logic Sequencer Failed,Rendering Diesel Generator 12 Inoperable.Caused by Intermittent Operation of Module Test Push Button.Part replaced.W/830804 Ltr ML20024E1721983-07-14014 July 1983 Updated LER 81-015/03X-1:on 810226,sample Pump for Control Room Radiation Monitor Found Out of Svc,Rendering Automatic Recirculation of Control Room Ventilation Sys on High Radiation Inoperable.Caused by seizure.W/830714 Ltr ML20024D0071983-07-0808 July 1983 LER 83-035/03L-0:on 830610,during Normal Power Operation,Esf Actuation Sys Channel Zg Steam Generator Level Tripped. Caused by Failed Vitro Isolator Module.Module Replaced.W/ 830708 Ltr ML20024D0091983-07-0808 July 1983 LER 83-033/03L-0:on 830603,fire Detection Instrumentation in Containment Southeast Electrical Penetration Determined Inoperable.Repair Impossible Due to Inaccessability of Protecto wire.W/830708 Ltr ML20024B8231983-06-23023 June 1983 LER 83-029/03L-0:on 830524,during Normal Operation, Surveillance Testing Indicated Neither Spent Fuel Pool Exhaust Fans 11 or 12 Would Maintain Required Negative Pressure.Caused by Clogged HEPA filters.W/830623 Ltr ML20024C0141983-06-22022 June 1983 Updated LER 81-080/03X-1:on 811116,discovered Weep from Cracked Weld on Spent Fuel Cooling Pump Discharge Vent Line 12.Caused by Inadequate Support of Vent Line.Support Assembly installed.W/830622 Ltr ML20024A8881983-06-16016 June 1983 LER 83-032/03L-0:on 830523,containment Isolation Sys B Logic Module Would Not Actuate.Caused by Defective Vitro Labs Std Logic Module.Module Replaced.Failed Module Returned to Vitro Labs for Repair & testing.W/830616 Ltr 1999-08-23
[Table view] Category:RO)
MONTHYEARML17326A2011999-08-23023 August 1999 LER 99-004-00:on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With 990823 Ltr ML20029C7321994-04-22022 April 1994 LER 94-004-00:on 940221,discovered Corrosion of Three Nuts on One of Incor Instrumentation Reactor Vessel Head.Caused by Increase of Wet Boric Acid.Leaking Flanges Repaired.W/ 940422 Ltr ML20046B4731993-07-30030 July 1993 LER 93-005-00:on 930630,TS 3.0.3 Entered Due to Both Containment Spray Sys Inoperable.Replaced CCW Outlet Valve Actuator Connecting Link Assembly from Number 11 SDC Heat exchanger.W/930730 Ltr ML20046A4911993-07-22022 July 1993 LER 93-003-00:on 930625,SG Tripped Due to Low Water Level. Caused by Insufficient Feedwater Addition Due to Inadequate Communication.Reemphasis on Improved Communication Stressed. W/930722 Ltr ML20045G8611993-07-0909 July 1993 LER 93-003-00:on 930610,dual Unit Trip Occurred Due to Partial Loss of Offsite Power.Flashover Protection Relay for Breaker 552-61 Replaced & Training for Personnel W/ Access to Relays Will Be reinforced.W/930709 Ltr ML20045G7281993-07-0808 July 1993 LER 93-002-00:on 930608,inadvertent Arw Actuation Sys & RPS Actuations Experienced During Performance of Awf Sys Large Flow Surveillance Testing.Caused by Failure to Note Differential Pressure Condition.Valve opened.W/930708 Ltr ML20045G8661993-07-0808 July 1993 LER 93-004-00:on 930611,reactor Tripped Due to Turbine Trip Resulting from Inadequate Procedure.Procedure Changes Made to Open Appropriate FW Heater High Level Dump Valves During Plant startup.W/930708 Ltr ML20045E7361993-06-29029 June 1993 LER 93-002-01:on 930205,software Vendor Discovered Error in User Manual for Updating Basss data-input Library.Caused by Failure of QA Procedures to Require Independent Review of User Manuals.Manual Surveillances performed.W/930629 Ltr ML20029B1261991-02-28028 February 1991 LER 91-001-00:on 910129,tubing in Air Start Sys for Emergency Diesel Generator Failed During Seismic Event. Caused by Error in Design of EDG Air Start Sys.Permanent Mod to Sys installed.W/910228 Ltr ML20028H8011991-01-24024 January 1991 LER 90-002-01:on 900116,determined That 891211 Reconstitution of More than One Spent Fuel Assembly Per Time in Violation of Fuel Handling Incident Safety Analysis. Caused by Deficient procedure.W/910124 Ltr ML20044A1861990-06-20020 June 1990 LER 87-002-01:on 861203,section of Thin Wall Found on Main Steam Line W/Readings Below Allowable Min of 0.95 Inches. Caused by Grinding of Edge of Pipe to Achieve Proper fit-up for Welding.Relief from IWB-3610 granted.W/900620 Ltr ML20043G1071990-06-13013 June 1990 LER 89-019-01:on 891128,determined That for Approx 10 Yrs, from 1979-1989,requirement to Lock HPSI Discharge Header Isolation Valves Shut Not Implemented.Caused by Inadequate Mgt Attention.Test Procedures modified.W/900613 Ltr ML20043F1221990-06-0404 June 1990 LER 90-017-00:on 900505,pin Hole Leak Observed in Discharge Piping of Saltwater Pump 13.Caused by Localized Corrosion. Leaking Spool Piece Removed & Blank Flange Installed. W/900604 Ltr ML20043A7871990-05-21021 May 1990 LER 90-016-00:on 900421,determined That Waste Gas Decay Tank (Wgdt) 13 Discharged Instead of (Wgdt) 11 for Discharge Permit Issued.Caused by Inadequate Communications.Training Performed for Operators Re event.W/900521 Ltr ML20043A3441990-05-14014 May 1990 LER 90-014-00:on 900413 & 19,unit Entered Tech Spec Limiting Condition of Operation 3.0.3 Due to Potential Inoperability of Three Out of Four Reactor Protection Sys Delta T Power Channels.Caused by Lack of Procedure guidance.W/900514 Ltr ML20043A3401990-05-14014 May 1990 LER 90-013-00:on 900413,determined That Axial Shape Index Channels Out of Spec & Inoperable.Caused by Inadequate Understanding of Design Basis for Excore/Incore Comparison. Design Basis for Excore/Incore improved.W/900514 Ltr ML20042G4521990-05-0707 May 1990 LER 90-015-00:on 900407,discovered That Relay Contact Which Actuates Reactor Trip Breaker Shunt Trip Not Adequately Functionally Tested.Caused by Failure to Examine Circuit in Detail When Test developed.W/900507 Ltr ML20042F5801990-05-0404 May 1990 LER 90-012-00:on 900406,identified That Procedure for LOCA Would Not Ensure post-LOCA Core Flush Would Be Initiated in Time to Prevent Boron Precipitation.Caused by Personnel Error.Configuration Mgt Program strengthened.W/900504 Ltr ML20012E9931990-03-29029 March 1990 LER 90-008-00:on 900227,determined That Surveillance Procedure M-280-0 Did Not Include Steps to Fully Test Control Room Recorder for Hydrogen Analyzers.Caused by Personnel Error.Procedure Revised on 900308.W/900329 Ltr ML20012F0001990-03-28028 March 1990 LER 89-006-01:on 890508,containment Iodine Filters Outside Design Basis Due to Equipment Qualification.Recalculation of Total Integrated Radiation Dose to Cables for Filter Fans Demonstrated Cable qualified.W/900328 Ltr ML20012E9951990-03-28028 March 1990 LER 89-014-01:on 890723,determined That Salt Water Header Not Capable of Withstanding Seismic Event Intact.Caused by Inadequate Welding of Blind Spool Pieces in Pipe.Insp Revealed Spools Capable as installed.W/900328 Ltr ML20012E0101990-03-26026 March 1990 LER 90-009-00:on 900224,failure to Meet Action Requirement Re Tech Spec 3.7.12.Caused by Personnel Error.Cables Removed from Doorway in Charging Pump Room & Not Allowed to Be Placed in doorway.W/900326 Ltr ML20012C4971990-03-15015 March 1990 LER 90-007-00:on 900216,discovered That Supervised Circuits Associated W/Fire Detection Instruments Located in Reactor Coolant Pump Bays Not Been Included in Surveillance Test Procedure.Caused by Personnel error.W/900315 Ltr ML20012C4861990-03-12012 March 1990 LER 90-006-00:on 900209,determined That Four Fire Dampers Missing.Caused by Not Identifying Penetrations as Requiring Dampers When Fire Hazards Analysis of Plant Conducted.Hourly Fire Watch Continued.Missing Dampers installed.W/900312 Ltr ML20012B8991990-03-12012 March 1990 LER 89-023-01:on 891220,determined That Pipe Rupture in nonsafety-related Svc Water Subsystem Could Result in Rapid Draining of Subsystems That Serve Auxiliary Bldg.Task Force Formed to Determine Corrective actions.W/900312 Ltr ML20012B4221990-03-0606 March 1990 LER 89-012-01:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed.Caused by Procedural Deficiency.Procedures Revised to Include Valve & Surveillance Test Program Instruction revised.W/900306 Ltr ML20011F2701990-02-27027 February 1990 LER 90-001-01:on 900109,determined That Surveillance Tests Used to Perform Channel Calibr Tests for Acoustic Flow Monitoring Devices Inadequate.Caused by Personnel Error & Inadequate Procedures.Swapped Leads restored.W/900227 Ltr ML20011F2091990-02-27027 February 1990 LER 89-026-00:on 891128,determined That Particulate Levels in Samples Taken from Lower Third of Tanks Exceeded Allowable Limits.Caused by Inadequate Sampling Technique. Tanks Cleaned & Filled W/Clean fuel.W/900227 Ltr ML20006F8601990-02-22022 February 1990 LER 90-004-00:on 900123,discovered Fire Barrier Penetration Seal Open for Indeterminate Time W/O Performing Tech Spec 3.7.12.a Required Actions.Caused by Personnel Error. Temporary Fire Seal installed.W/900222 Ltr ML20006E0521990-02-0808 February 1990 LER 90-001-00:on 891221,discovered That Acoustic Indications for One PORV & One Safety Valve Were Reversed During Surveillance Test.Caused by Personnel Error.Swapped Leads Restored to Proper configuration.W/900208 Ltr ML20006B4801990-01-26026 January 1990 LER 89-022-00:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed,Violating Tech Specs.Caused by Procedural Deficiency.Surveillance Test Procedure Revised to Include Deleted valves.W/900126 Ltr ML19354D8931990-01-17017 January 1990 LER 89-024-00:on 891218,determined That Wires Which Connect Actuation Device Logic Relay Contacts to Remainder of Circuit Not Tested During Channel Calibr Test.Caused by Inadequate Test.Test Program Upgrade underway.W/900117 Ltr ML20005F1921990-01-10010 January 1990 LER 89-025-00:on 891208,Tech Spec Action Statement Entered When Ventilation Ducts Penetrating Fire Barrier Could Not Be Accessed to Determine If Fire Dampers Installed.On 891211, Fire Watch Missed.Caused by Personnel error.W/900110 Ltr ML20005E3971989-12-28028 December 1989 LER 89-019-00:on 891128,discovered That HPSI Discharge Header Isolation Valves Not Locked Shut When RCS in Water Solid Condition,Resulting in Operation Outside Design Basis. Procedure Revised to Require Valves closed.W/891228 Ltr ML19351A4551989-12-13013 December 1989 LER 89-020-00:on 891113,determined That Some Solenoid Valves & Valve Power Supplies for Saltwater Sys May Not Be Able to Perform Design Function After Design Basis Seismic Event. Cause Undetermined.Power Supplies upgraded.W/891213 Ltr ML20005D6611989-12-0606 December 1989 LER 89-018-00:on 891106,discovered That Many Air Operated Control Valves & piston-operated Dampers Which Utilize safety-related Air Accumulators Would Not Have Performed as Expected After Loss of air.W/891206 Ltr ML19325F3951989-11-10010 November 1989 LER 89-002-01:on 890228,discovered That Fire Barrier Penetration Inoperable & Action Statement Requirements Not Satisfied.Caused by Inadequate Administrative Controls. Penetration Returned to Operable status.W/891115 Ltr ML19325E8221989-11-0303 November 1989 LER 89-007-01:on 890505,evidence of Reactor Coolant Leakage from 120 Pressurizer Vessel Heater Penetrations Discovered. Caused by IGSCC of Inconel 600.All Penetrations Using J-welds & Inconel 600 Visually inspected.W/891103 Ltr ML19324B2511989-10-27027 October 1989 LER 89-012-01:on 890720,discovered That Master Solenoid to Switchgear Room Halon Sys Disconnected Since 890629.Caused by Personnel Error Resulting from Lack of Written Procedure. Procedure Revised to Apply Temporary mods.W/891027 Ltr ML19325C3281989-10-10010 October 1989 LER 89-016-00:on 890908,determined That as-found Condition of Resistance Temp Detectors Did Not Match Tested Configuration.Cause Not Stated.Subj Detectors Will Be Sealed,Per Environ Qualification requirements.W/891010 Ltr ML19325C3701989-10-0909 October 1989 LER 89-017-00:on 890907,determined That Discrepancy in Acceptance Criteria of Surveillance Test Procedure M-452-0 Resulted in Failure to Fully Comply W/Requirements of Tech Spec 3.9.12.Main Cause undetermined.W/891009 Ltr ML20024F3771983-08-25025 August 1983 LER 83-044/03L-0:on 830808,diesel Generator 12 Tripped on Low Jacket Cooling Water Pressure While Verifying Operability.Cause Not Stated.Coolant Jacket Vented & Large Amount of Air Found.No Evidence of leakage.W/830825 Ltr ML20024F5731983-08-25025 August 1983 LER 83-040/03L-0:on 830727,control Room Air Conditioner 11 Discovered W/Damaged Condenser Fan.Caused by Loose Set Screws Securing Fan in Position.Set Screws Restored. W/830825 Ltr ML20024E6761983-08-0404 August 1983 Updated LER 83-011/03X-1:on 830207,during Surveillance Testing ESFAS a Logic Sequencer Failed,Rendering Diesel Generator 12 Inoperable.Caused by Intermittent Operation of Module Test Push Button.Part replaced.W/830804 Ltr ML20024E1721983-07-14014 July 1983 Updated LER 81-015/03X-1:on 810226,sample Pump for Control Room Radiation Monitor Found Out of Svc,Rendering Automatic Recirculation of Control Room Ventilation Sys on High Radiation Inoperable.Caused by seizure.W/830714 Ltr ML20024D0071983-07-0808 July 1983 LER 83-035/03L-0:on 830610,during Normal Power Operation,Esf Actuation Sys Channel Zg Steam Generator Level Tripped. Caused by Failed Vitro Isolator Module.Module Replaced.W/ 830708 Ltr ML20024D0091983-07-0808 July 1983 LER 83-033/03L-0:on 830603,fire Detection Instrumentation in Containment Southeast Electrical Penetration Determined Inoperable.Repair Impossible Due to Inaccessability of Protecto wire.W/830708 Ltr ML20024B8231983-06-23023 June 1983 LER 83-029/03L-0:on 830524,during Normal Operation, Surveillance Testing Indicated Neither Spent Fuel Pool Exhaust Fans 11 or 12 Would Maintain Required Negative Pressure.Caused by Clogged HEPA filters.W/830623 Ltr ML20024C0141983-06-22022 June 1983 Updated LER 81-080/03X-1:on 811116,discovered Weep from Cracked Weld on Spent Fuel Cooling Pump Discharge Vent Line 12.Caused by Inadequate Support of Vent Line.Support Assembly installed.W/830622 Ltr ML20024A8881983-06-16016 June 1983 LER 83-032/03L-0:on 830523,containment Isolation Sys B Logic Module Would Not Actuate.Caused by Defective Vitro Labs Std Logic Module.Module Replaced.Failed Module Returned to Vitro Labs for Repair & testing.W/830616 Ltr 1999-08-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G6971999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Calvert Cliffs Npp,Units 1 & 2.With ML20216J8731999-09-10010 September 1999 Rev 52 to QA Policy for Calvert Cliffs Nuclear Power Plant ML20212A4441999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Ccnpp,Units 1 & 2. with ML17326A2011999-08-23023 August 1999 LER 99-004-00:on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With 990823 Ltr ML20210S6091999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ccnpp,Units 1 & 2. with ML20210N6001999-07-27027 July 1999 ISI Summary Rept for Calvert Cliffs Unit 2. Page 2 of 3 in Encl 1 of Incoming Submittal Not Included ML20210B7941999-07-15015 July 1999 SER Denying Licensee Request for Changes to Current Ts,Re Deletion of Tendon Surveillance Requirements for Calvert Cliffs LD-99-039, Part 21 Rept Re Defect of Abb 1200A 4kV Vacuum Breakers. Initially Reported on 990625.Defect Results in Breaker Failing to Remain in Closed Position.Root Cause Evaluation & Corrective Action Plan Being Developed.Licensee Notified1999-06-30030 June 1999 Part 21 Rept Re Defect of Abb 1200A 4kV Vacuum Breakers. Initially Reported on 990625.Defect Results in Breaker Failing to Remain in Closed Position.Root Cause Evaluation & Corrective Action Plan Being Developed.Licensee Notified ML20209F1721999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Calvert Cliffs Npp.With LD-99-035, Part 21 Rept Re Abb 1200A 4KV Vacuum Breakers Performing Trip Free Operation When Close Signal Received by Breaker. Defect Results in Breaker Failing to Remain in Closed Position.Root Cause & CAP Being Developed1999-06-25025 June 1999 Part 21 Rept Re Abb 1200A 4KV Vacuum Breakers Performing Trip Free Operation When Close Signal Received by Breaker. Defect Results in Breaker Failing to Remain in Closed Position.Root Cause & CAP Being Developed ML20196C6981999-06-21021 June 1999 Safety Evaluation Concluding That Use of ASME Section XI Code Including Summer 1983 Addenda as Interim Code for Third 10-year Insp Interval at Calvert Cliffs Units 1 & 2 Until Review of 1998 Code Completed,Would Be Acceptable ML20195K2811999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Ccnpp,Units 1 & 2. with ML20206R5871999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ccnpp,Units 1 & 2. with ML20195B3891999-04-30030 April 1999 0 to CENPD-279, Annual Rept on Abb CE ECCS Performance Evaluation Models ML20205N2951999-04-13013 April 1999 Special Rept:On 990314,fire Detection Sys Was Removed from Svc to Support Mod to Replace SRW Heat Exchangers in Unit 2 SRW Room During Unit 2 Refueling Outage.Contingency Measure 15.3.5.A.1 Will Continue Until Fire Detection Sys Restored ML20210T5211999-04-0101 April 1999 Rev 0 to Ccnpp COLR for Unit 2,Cycle 13 ML20205P5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20204H6471999-03-21021 March 1999 SER Re License Renewal of Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20207M8321999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Calvert Cliffs Nuclear Power Plant.With ML20203D4311999-02-0505 February 1999 Safety Evaluation Accepting Procedure Established for long-term Corrective Action Plan Related to Containment Vertical Tendons ML20199G4671999-01-20020 January 1999 SER Accepting USI A-46 Implementation for Plant ML20206Q3221999-01-11011 January 1999 Special Rept:On 981226,wide Range Noble Gas Effluent RM Was Removed from Operable Status.Caused by Failure of mid-range Checksource to Properly Reseat.Completed Maint & post-maint Testing & RM Was Returned to Operable Status on 990104 ML20207L0451999-01-0808 January 1999 Cost-Benefit Risk Analyses:Radwaste Sys for Light Water Reactors ML20199F4781999-01-0808 January 1999 Safety Evaluation Concluding That Bg&E Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves Susceptible to Pressure Locking.Concludes GL 95-07 Actions Were Addressed ML20198S7591999-01-0707 January 1999 SER Accepting Quality Assurance Program Description Change for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20207M2281998-12-31031 December 1998 1998 Annual Rept for Bg&E. with ML20199E2931998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Calvert Cliffs Npp. with ML20206R9911998-12-0808 December 1998 Rept of Changes,Tests & Experiments (10CFR50.59(b)(2)). with ML20198B2631998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20195H1001998-11-16016 November 1998 Safety Evaluation of First Containment Insp Interval Iwe/Iwl Program Alternative ML20196E2211998-10-31031 October 1998 Non-proprietary Rev 03-NP to CEN-633-NP, SG Tube Repair for Combustion Engineering Designed Plant with 3/4 - .048 Wall Inconel 600 Tubes Using Leak Limiting Alloy 800 Sleeves ML20195E5281998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Calvert Cliffs Nuclear Power Station,Units 1 & 2.With ML20154Q7191998-10-21021 October 1998 Special Rept:On 980923,unit 1 Wrngm Was Removed from Operable Status.Caused by Failure of Process Flow Transducer.Completed Maint to Remove Process Flow Transducer Input to Wrngm Microprocessor & Completed Formal Evaluation ML20154G3931998-10-0505 October 1998 Safety Evaluation Concluding That Flaw Tolerance Evaluation for Assumed Flaw in Inboard Instrument Weld of Pressurizer Meets Rules of ASME Code ML20154M5841998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Calvert Cliffs Nuclear Plant,Units 1 & 2.With ML20153C2571998-09-18018 September 1998 Special Rept:On 980830,wide Range Noble Gas Monitor (Wrngm) Channel Was Removed from Operable Status.Caused by Need to Support Performance of Required 18-month Channel Calibr.Will Return Wrngm to Operable Status by 980925 ML20153C1091998-09-18018 September 1998 Part 21 Rept Re Defective Capacity Control Valves.Trentec Personnel Have Been in Contact with Bg&E Personnel Re Condition & Have Requested Potentially Defective Valves ML20151U5441998-09-0404 September 1998 Bg&E ISI Summary Rept for Calvert Cliffs ML20151T5281998-09-0101 September 1998 Special Rept:On 980819,declared Rv Water Level Monitor Channel a Inoperable.Caused by Failure of Three Heated Junction Thermocouples (Sensors) in Lower Five Sensors. Channel a & B Rv Water Level Probes Will Be Replaced ML20151Y1191998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Calvert Cliffs Nuclear Power Plant Units 1 & 2.With ML20237D4981998-08-19019 August 1998 Safety Evaluation Accepting Licensee Request for Extension of Second ten-year Inservice Insp Interval ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20237B9371998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Calvert Cliffs Nuclear Power Plant ML20237D5941998-07-22022 July 1998 Rev 2 to Ccnpp COLR for Unit 2,Cycle 12 ML20236L7521998-07-0606 July 1998 Safety Evaluation Granting Bg&E 980527 Request for Relief from Requirement of Section IWA-5250 of ASME Code for Calvert Cliffs Unit 2.Alternatives Provide Reasonable Assurance of Operational Readiness ML20236F7791998-06-30030 June 1998 Safety Evaluation Authorizing Request for Temporary Relief from Requirement of Subsection IWA-5250 of ASME Code,Section XI for Plant,Unit 1 ML20236R0881998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20236X3101998-06-19019 June 1998 Rev 1 to Calvert Cliffs Nuclear Power Plant COLR for Unit 2,Cycle 12 ML20249A9571998-06-15015 June 1998 Special Rept:On 980430,fire Detection Sys Was Removed from Svc to Support Mod to Purge Air Sys 27-foot Elevation & 5-foot Elevation East Piping Penetration Rooms.Installed Temporary Alteration & Returned Fire Detection Sys to Svc ML20249A7711998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Ccnpp,Units 1 & 2 1999-09-30
[Table view] |
Text
., ..
B A LTIMORE G AS AND
, ELECTRIC -
CALVERT CLIFFS NUCLEAR POWER PLANT 1650 CALVERT CLIFFS PARKWAY
- LUS8Y, MARYLAND 20657-4702 CHARLES H. CRUSE DLANT GENE AAL MANAGER cAtvent ct;rrs July B,1993 U.S. Nuclear Regulatory Commission
'Ja shing ton , D.C. 20555 ATTENTION: Document Control Desk
SUBJECT:
Calvert Cliffs Nuclear Power Plant Unit No. 2; Docket No. 50-318; License No. DPR 69 Licensee Event Report 93-002 Inadvertent ESF Actuations 'Jhile Performing Surveillance -
Testing N
The attached report is being sent to you as required under 10 CFR 50.73 guidelines. Should you have any questions regarding this report, we vill be pleased to discuss them with you.
Very truly yours, s
f}r" y'j '., f l / l /.
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_ ~$lif 7.h l-:V CHC/RCG/bj d Attachment cc: D. A. Brune, Esquire J. E. Silberg, Esquire R. A. Capra, NRC D. C. Mcdonald, Jr., NRC T. T. Martin, NRC P. R. 'Jilson, NRC R. I. McLean, DNR J . H . 'Ja l t e . PSC Director, Office of Management Information and Program Control 9307250106 930708
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NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION RE l N ESTIMATED BURDEN FER RESPotCE TO COMPT,YWIT)4 THtS INFORMATION i Cou.ECTON EoVEST: 50.0 HRS. F0FMIARD CC%tMENTS REGAlote0 i MW EGNATE TO NE INFORMATON AND RECcm3 MMEMENT LICENSEE EVENT REPORT (LER) OR4CH (MNB8 7714). uS6 NUCLEAR REGULATOfN COMMISScit J
- WASHINGTON, DC affbao1 AND TO mE PAPERWORK REDUCTON PRQ)ECT 01500104). OFFICE OF kW4GEMENT AND DVDGET,WASHINGTOtt DC 3rlu fSee reverse for reaosred number of dia'ts/charsc'ers for each block)
FActuTY NAME (1) DOCKET NUMBER (2) PAGE (3)
C alvert Clif f s, U nit 2 05000 318 1 OF 07 l TITLE (4)
Inadvertent ESF Actuations While Performing Surveillance T.esting EVENT DATE (5) LER NUMBER 16) REPORT DATE (7) { oTHER FACluTIES INVOLVED i8)
SEQUENTIAL REVISION MONTH DAY YEAR YEAR MONTH DAY YEAR NUMBER NUMBER 06 08 93 93 - 002 -
00 07 08 93 05000 OPERATING THIS AEPO AT l$ SUOMITTED DURSUANT TO THE AEoVIREMENTS OF 'O CFR Ched ona or more) (11)
MODE (9) 20.402M 20.405(c) l )( l 5013(an2)(rv) 73 7,433 POWER 73 MCI LEVEL 0 20.4054an1160 l 50.36tc)(2) 150.73(a)(2)(vic gg l ~
IlO 20.405/a)(1)6i4 l 50 73(aH2}6) l 5033(aH2)(vni)(A) (Specty in Abstract below and in i 50 73(a)(2)(viiO(B) Toxt. NRC Form 366A) 20.40$ial(1)0v) l l 50.73(aH2)(ii) l 20 405(a)(1)M l l 5033(aH2)(ii0 l 50.73(aH2)<x)
UCENSEE CONTACT FCR THIS LER (12) l NAME TELEPHONE NUMBER (include Area Code) l R. C. Gradle 410 260-3738 COMPLETE ONE UNE FOR EACH COMPONENT FAILURE DESCRIBE 0 IN THIS REPORT (13) i MAN RENRTARE TO '
CAUSE COMPONENT NPROS CAUSE SYSTEM COMPONENT l SYSTEM TURER TURER NPROS l l SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH I DAY I YEAR i 3 SUBMISSION i YES X NO 4f ves comolete EYPECTED SUOMIS$10N DATE) DATE (15)
ABST RACT (Larmt to 1400 spaces,i.e approximateey15 sing #e-space typewntten knes) (16)
On June 8, 1993, at 9:59 a.m., Calvert Cliffs Unit 2 experienced inadvertent Auxiliary Feedwater Actuation System (AFAS) and Reactor Protective System actuations during performance of Auxiliary Feedwater (ATJ) System large flow !
surveillance testing when excessive differential pressure developed between !
the steam generators. At the time of the event, Unit 2 was in MODE 3, HOT ;
STANDBY, with the Reactor Coolant System at 2250 psia and 532 degrees Fahrenheit. The main steam isolation valves (MSIVs) were Shut. There were no safety consequences resulting from this event. The AFAS actuation signal immediately stopped ATJ flow to the affected (lower pressure) steam generator.
The cause of this event was that neither the test procedure nor the operators' j assessment of the expected plant response identified the potential for the {
development of this plant condition. Appropriate procedure changes will be !
l made to warn operators of the potential for this condition to occur. Both !
MSIVs will be required to be open during the test. Management expectations
- that operators identify and evaluate potential problems prior to task I
{i performance, has been re-emphasited.
i irwire
_,. :r f NRC FCRM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 315o-0104 Sea . . EXPIRES 5/31/95 EStMATEo BURoEN PER RESPONSE To compt,Y wrTH THS fNFoRMATION Col.15C*loN REoVEST: 50 0 HRS. FoRWARo LICENSEE EVENT REPORT (LER) coMuESTs rec 4RoiNo eURoEN EsTruATE To THE NFeRurTioN ANo RECoRoS MANAGEMENT BRANCH (MNB0 77141. U.S. NUCLEAR TEXT CONTINUATION Recut.AroRy couu:sses wASHiNoTcN. oc rosss Coot. ANo to THE P&PERWoRK REoUCTON PROJECT (3150 0104). oFFCE OF MANAGEMENT ANo SuoGET.WASHINoToN. oC 20S03. ,
FActuTY NAME (1) DOCKET NUMBER (2) . L.ER NUMBER (3) P AGE (4) l I
.. Calvert Cliffs, Unit 2 05000 3 1.8 93 -
002 - 00 02 0F 07 i rtxt or == we. . . .omeoc o, NRC ro, asum I DESCRIPTION OF EVENT On June 8,1993, at 9:59 a.m. , inadvertent actuations of the Auxiliary Feedwater ;
Actuation System (AFAS) and the Reactor Protective System (RPS) occurred at Calvert Cliffs Unit 2. The AFAS and the RPS are Engineered Safety Fcatures (ES F) . The actuations occurred when a high differential pressure developed between No. 21 and No. 22 steam generators during performance of Auxiliary Feedwater (AW) System large flow surveillance testing. The AFAS actuation initiated an "AFAS BLOCK" signal that immediately isolated AW flow to the affected (lower pressure) No. 21 steam generator. At the time of the event, Unit 2 was in MODE 3, HOT STANDBY, with the Reactor Coolant System (RCS) at 2250 psia and 524 degrees Fahrenheit in the No. 21 steam generator associated loop. All control element assemblies (CEAs) were fully inserted with the RPS trip circuit breakers closed to support previous CEA rod-drop testing that had been suspended. The RPS asymmetric steam generator transient (ASGT) actuation signal tripped opened the RPS trip circuit breakers.
3 The AW system is designed to provide feedwater to the steam generators to cool the RCS if the Main Feedwater System is inoperable. Two AW trains , consisting of one of two selected steam driven pumps, one motor driven pump, and associated flow paths, are capable of automatically initiating flow to either steam generator. In the event of a ruptured steam generator (i.e., main steam line break), blocking valves automatically shut and stop AW flow to the affected steam generator to pravent a continuation of steam generator blowdown to ,
containment. The AFW pump turbines (No. 21 and No. 22) are normally driven by '
j main steam (MS). The MS piping for the AFW pump turbines comes off each MS line upstream of the corresponding main steam isolation valve (MSIV).
An AFAS actuation automatically starts the AW pumps upon detection of Ic - level.
in either steam generator. An AFAS actuation caused by high steam generator differential pressure causer an "AFAS BLOCK"' signal to be generated shutting the -
blocking valves to the low pressure steam generator. This action mitigates the effects of a MS line rupture.
The RFS ASCT trip utilires steam generator pressure inputs to the RPS thermal !
margin / low pressure (TM/LP) trip calculator. When the difference in pressure between the two steam generators exceeds the trip serpoint then the RPS ASGT trip causes a reactor trip. ?
On June 3,1993, Unit 2 was in the final week of a scheduled refueling outage.
Plant heacup to MODE 3 was complete. Both MSIVs were shut with RCS temperature f
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NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 315o-0104 !
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. ESSMATEo BURCEN PER RESPONSE To COMPLY WITH THis WFoRMATON COLLECT oN REoVEST: 50.0 HRS. FCPWARo LICENSEE EVENT REPORT (LER) cowuEuts RcaARoma suncEN EsnMATt To TwE mFoRuArcN ANo REcoRoS MANAGEMENT BMNCH (MNB8 7714L U.S. NUCLEAR TEXT CONTINUATION aEcutAtoav ceuwsscN. wAssmoroN. oc rosss.000t Ano To THE PAPEPWoRK REOUC*loN pro.iEc7 Qt50 0104). OFFICE CF WANAGEMENT AND BUDoET. WASMNGToN. oC 20$01 F Aclu TY NAME (1) DOCKET NUMBER p) LER NUMBER {3) PAGE (4)
Calvert Cliffs, Unit 2 05000 3 1 8 93 -
002 - 00 03 0F 07 TEXT m . c. o. .at,, e., co o, NRc F.,- seeA iiri being maintained at approximately 532 degrees Fahrenheit by passing steam ,
through the bypass valve around No. 21 MSIV to the main condenser. t At approximately 3:00 a.m., operations shift personnel conducted a pre-evolution briefing for the scheduled performance of Surveillance Test Procedure ,
(STP) 0-73H-2, " Auxiliary Feedvater Pumps No. 21/22/23 1.arge Flow Test." This test procedure is required to be performed every refueling outage. The test ,
coordinator, a licensed Control Room Operator, conducted a complete review of STP 0-73H-2. This review included a discussion of the test procedure's purpose, scope, prerequisites (initial required conditions), precautions and a walk-through of the steps in the procedure. The brief also included actions to be taken in the event of unexpected conditions.
The test coordinator also reviewed the current plant conditions and expected ,
plant responses for the performance of STF 0-73H-2 as required by the procedure.
The procedure required that a single steam driven A W pump be supplied from a single steam generator. The AW pump would feed approximately 300 gallons per minute of relatively cool condensate storage tank water to both steam generators. The procedure requires maintenance at this flowrate for a 5 minute stabilization period prior to recording test data (AFW pump suction flowrate, temperature, and pressure, pump discharge pressure, and pump bearing vibration .
measurement). In addition, test personnel were to record 10 A W pump and A turbine vibration data points for trend analysis. The procedure has a precaution which states that the steaming and feeding rates affect.RCS cooldown rate and references the plant's Technical Specifications for permissible RCS ;
cooldown rates. Personnel involved in the test were sensicl:ed to the cooldown effect that the test would have on the RCS temperature and steam generator ,
pressure. The following precautions were reviewed: (1) RCS cooldown rate limits, (2) maintaining steam generator levels, and (3) close monitoring of RCS ,
temperatures, pressurizer level, and steam generator pressures during the steaming / feeding transient. Plant operators were aware that, following the 5 minute stabilization period, the recording of test data was to be conducted expeditiously to minimize RCS cooldown.
i At approximately 9: 40 a.m., the test was commenced. During the 5 minute stabilization period it was discovered that a vibration monitor test equipment connector was missing. The connector was obtained and installed, but this -
action delayed the recording of test data for an additional two or three minutes. Control Room personnel informed AW pump room personnel that RCS ;
temperature was decreasing and to expedite the data collection. ,
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NRC FCRM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 315o-01o4 (Sea .
EXPIRES 5/31/95 ESTIMATE 3 BURoEN PEA RESPONSE To CouPLY WITH THis WFoRMATioN COLLECTION REcuE37 $0 0 MHS. FoRwAAo LICENSEE EVENT REPORT (LER) CouuCNTs nE24aoWo auncEN EsTuArE To TsE nFonuATioN ANo AECoRCS MANAGEMENT SAANCH (uNB9 7714). U S NUCLEAR TEXT CONTINUATION aEcutATosY CouusscN. WASMWoToN, oC 2055S4@1. ANo To THE PAPEAwoM AEouCTioN PROJECT (31504104). oFFCE of r l
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FACluTY NAME (1) DOCKET NUMBER (23 LIR NUMBER (3) PAGE g4)
Calvert Cliffs, Unit 2 05000 3 1 8 93 -
002 -
00 04 0F 07 TEXT [lf more spue is reowred wae adetsana, copies of NRC Form :i66A) (17)
At 9:59 a.m., as final test data were being obtained, the AFAS BLOCK to No. 21 steam generator and the RPS ASGT (TM/LP) trips actuated. Alarm annunciation was received and acknowledged by Control Room personnel. The test coordinator observed that the AFJ blocking valves to No. 21 steam generator went shut. He verified that a valid high steam generator differential pressure condition existed as he observed pressure indications for No. 21 and No. 22 steam generator to be approximately 810 and 920 psia, respectively. The licensed Control Room Supervisor (CRS) directed the test coordinator to open the bypass valve around No. 22 MSIV which lowered No. 22 steam generator pressure. The '
test coordinator secured No. 21 AFJ pump.
II. CAUSE OF EVENT :
Neither the procedure nor the operators' assessment of the expected plant response identified the potential concern for the possible development of a high steam generator differential pressure condition. -
A cause of this event was the lack of procedural measures to prevent creation of an excessive differential pressure between steam generators. Surveillance Test
, Procedure 0-73H-2 did not warn operators of the potential for steam generator differential pressure to approach safety trip setpoints. The procedure did not specifically recognite that testing could occur with the MSIVs and the MSIV bypass valves shut. At the time of the event, with these valves closed and
We recognize that all plant conditions and configurations cannot be accounted for in a written procedure. We expect the pre-evolution brief to identify and evaluate potential problems. Despite the operators' review of the test procedure and expected plant response, they did not identify the potential for '
the subsequent excessive steam generator differential pressure condition.
An additional factor that contributed to the event was extension of the test duration on No. 21 AFJ pump due to a missing test equipment connector.
4
- III. A'IALYSIS OF EVENT
here were no safety consequences resulting from this event. No plant systems ar component failures resulted from this event. 'The.RPS is designed to respond
) to transients while the reactor is operating at power. The differential pressure between steam generators is not a safety concern. The test procedure
MRC FCRM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO,315o-o104 4 02)
EXPIRES 5/31/95 ESTMATEo BURCEN PER RESPONSE To COMPLY V4TH THrs NFoRMATioN CoLLECTTON REoVEST, $0.O HRS. FoHWAAo '
LICENSEE EVENT REPORT (LER) CeuMEuTs neGAnoso aunoEN EsTuATE To THE mroAMATCN ANo AECORDS MANAGEMENT BRANCH (MNBS 77141, U.S NUCLEAR TEXT CONTINUATION nEcut4TCav CoMMrsscN. wAssmoToN. oc 2055$4001, ANo To
'HE PAPEHWoRK REOUCD PAoJECT (3150 01041. OFFICE OF MANAoEMENT ANo BUoGET,WASHINoToN. oC 20503.
- l FACluTY NAME (1) DOCKET NUMBER (2) LER NUMBER (3) PAGE (4)
Calvert Cliffs, Unit 2 05000 3 1 8 93 -
002 - 00 05 0F 07 ,
TEXT no. .pc. . a. ean., com at NaC p mAnm requires the plant to be in MODE 3, therefore, this event could not have occurred during plant power operation. .
The Updated Final Safety Analysis Report (UFSAR) Chapter 14, " Safety Analysis" defines the asymmetric steam generator event as any initiator that affects only one of the two steam generators. The UFSAR describes the most limiting case as !
a loss of load to one steam generator at hot full power. This event is initiated by the inadvertent closure of the MSIV for the affected steam generator. The resultant non-uniform core inlet ti aperature distribution produces local power peaking in the core. The analysis concludes that no safety ;
limits are exceeded. At the time of this event, Unit 2 was in MCDE 3 with all CEAs fully inserted. The R?S ASGT trip actuation was not required to prevent t
exceeding any safety limits.
The UFSAR Chapter 14, " Safety Analysis" describes the most limiting steam line ,
break (SL3) event to be a guillotine-type non-isolable main steam line break ;
between the steam generator and the MSlV at hot full power. The purpose of the ;
AFJ BLOCK signal is to limit plant cooldown during the SLB event (limiting the '
potential return to power peak following reactor trip CEA insertion). The safety analysis takes credit for the AFJ isolation (AFAS BLOCK) signal stopping i AF'4 flow to the affected steam generator terminating the RCS cooldown when the affected steam generator subsequently blows dry. Since the procedure required I the plant to be in MODE 3 and all CEAs were fully inserted, then this event is 'l; bounded by our current safety analysis. Based on this. it is concluded that this event resulted in no real or potential significant safety consequences.
This event is reportable in accordance with 10 CFR 50.73(a)(2)(iv) in that.it resulted in automatic actuation of engineered safety features. These occurred as unplanned AFAS and RPS actuations. '
IV. CORRECTIVE ACTIONS 1 Immediate A. Control Room Operators confirmed that a valid high steam generator -
differential pressure condition existed, verified that AFJ-flow was ,
stopped to No. 21 steam 5enerator and that the RPS trip circuits 4 ,
breakers had opened, and shutdown No. 21 APJ pump. They opened the I bypass valve around No. 22 MSIV to reduce pressure in No. 22 steam j generator. This action alleviated the steam generator differential i pressure condition.
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NRC FCAM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-o104 is-sa EXP!RES 5/31/95 EST1MATEo SURCEN PER RESPONSE To COMPLY wrTH THis INFoAMATICN CoLLEC'ICN REOUEsT; So D HRS. FoRWARo LICENSEE EVENT REPORT (LER) CcuuENTs REGARoiNo suRCEN EsTuATE to THE iNFoRuATioN AND REOoRoS MANAGEuENT OFuNC.M {MNBB T714). U S NUCLEAR TEXT CONTINUATION REGULATORY CoMWSSON. WASHINGTON. oC 20555 0001, ANo To THE PAPEPWoRK REoVCTioN PROJECT (31500104). OFFICE CF MANAGEMENT ANo Buo0ET. WASHINGTON, oC 20503.
FACluTY MAME (1) DOCKET NUMBER (2) LER NUMBER (3) PAGE (4)
Calvert Cliffs, Unit 2 05000 3 1 8 93 -
002 - 00 06 0F 07 s
' EXT W more space is Hwed, use scations copies at NRC Form 3tWi.4 p /)
B. Control Room Operators identified and discussed the need to closely monitor steam generator differential pressure during performance of STP 0-73H-2. Subsequent testing on No. 22 AFW pump was completed -'
without incident.
Actions to Prevent Recurrence: .
C. A caution statement will be-incorporated into STP 0-73H-1 (the similar procedure for Unit 1) and STP 0-73H-2 warning plant operators of the potential for steam generator differential pressure to approach safety setpoints.
D. A requirement will be added to STP 0-73H-1 and STP 0-73H-2 for both MSIVs to be open during this test.
The General Supervisor-Nuclear Plant Operations has re-emphasized to E.
operators management expectations that tasks be fully evaluated to ensure that potential problems that could exist or dev,elop during
, implementation are considered. ,
F. Management expectations that all appropriate test equipment be available prior to test initiation will be emphasized to appropriate ,
test personnel.
V. ADDITIONAL INFORMATION A. Identification of Components and Systems Referred to in this LER:
IEEE 803A/83 IEEE 805/84 Component or System Funct Ident System Code Reactor Protective System NA JC Engineered Safety Feature NA JE Auxiliary Feedwater System NA BA !
Reactor Coolant System NA AB Steam Generator SG NA Main Steam Isolation Valve ISV NA AFW Pu=p P BA
1 NRC FORM 366A U.S. NUCLEAR REGULATCRY COMMISSION APPROVED BY OMB NO. 3150 0104 !
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EXPIRES 5/31/95 EST1 MATED BURCEN PER RESPONSE To CouPLY WITH 74:s WFoRMATCN COLLECTION REQUEST: 20 HRS. FORWARD UCENSEE EVENT REPORT (LER) COMMENTS REGARDING BURDEN EST1 MATE TO THE WFORMATCN AND RECORCS MANAGEMENT BRANCH (MNBS 7714), U.S NUCLEAR TEXT CONTINUATION REGULATORY COMMISSON WASHWGTON, DC 20$$$@01. MD To THE PAPEPWORK REDUCTION PROJECT (31504104i. OFFICE oF MANAGEMENT AND BUDGET. WASHINGTON. DC 20503.
F ACIUTY NAME (1) DOCKET NUMBER (3 LER NUMBER {3) PAGE (4)
Calvert Cliffs, Unit 2 05000 3 1 8 93 -
002 - 00 07 0F 07 TEXT i n - .o.c. a .aomone. or NRC F sasAi o 7,
- 3. Previous Similar Events :
There has been one previous reported ecent. involving an inadvertent.
ESF (RPS ASGT) trip actuation due to high steam generator differential pressure conditions, but the cause (MSIV hydraulic :'
system malfunction) was not related to this event. LER 318/92-006 documented the event.
LER 317/85-05 reported an inadvertent ESF actuation due to not having the handswitch keys in the handswitches used for blocking an
ESF signal prior to reaching the setpoint during plant cooldown.
The lack of procedure guidance to prepare for the required ESF signal blocking during plant cooldown centributed to the event. The i appropriate procedures were revised to ensure adequate guidance is provided for the anticipated plant response. This event has not recurred.
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