|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17326A2011999-08-23023 August 1999 LER 99-004-00:on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With 990823 Ltr ML20029C7321994-04-22022 April 1994 LER 94-004-00:on 940221,discovered Corrosion of Three Nuts on One of Incor Instrumentation Reactor Vessel Head.Caused by Increase of Wet Boric Acid.Leaking Flanges Repaired.W/ 940422 Ltr ML20046B4731993-07-30030 July 1993 LER 93-005-00:on 930630,TS 3.0.3 Entered Due to Both Containment Spray Sys Inoperable.Replaced CCW Outlet Valve Actuator Connecting Link Assembly from Number 11 SDC Heat exchanger.W/930730 Ltr ML20046A4911993-07-22022 July 1993 LER 93-003-00:on 930625,SG Tripped Due to Low Water Level. Caused by Insufficient Feedwater Addition Due to Inadequate Communication.Reemphasis on Improved Communication Stressed. W/930722 Ltr ML20045G8611993-07-0909 July 1993 LER 93-003-00:on 930610,dual Unit Trip Occurred Due to Partial Loss of Offsite Power.Flashover Protection Relay for Breaker 552-61 Replaced & Training for Personnel W/ Access to Relays Will Be reinforced.W/930709 Ltr ML20045G7281993-07-0808 July 1993 LER 93-002-00:on 930608,inadvertent Arw Actuation Sys & RPS Actuations Experienced During Performance of Awf Sys Large Flow Surveillance Testing.Caused by Failure to Note Differential Pressure Condition.Valve opened.W/930708 Ltr ML20045G8661993-07-0808 July 1993 LER 93-004-00:on 930611,reactor Tripped Due to Turbine Trip Resulting from Inadequate Procedure.Procedure Changes Made to Open Appropriate FW Heater High Level Dump Valves During Plant startup.W/930708 Ltr ML20045E7361993-06-29029 June 1993 LER 93-002-01:on 930205,software Vendor Discovered Error in User Manual for Updating Basss data-input Library.Caused by Failure of QA Procedures to Require Independent Review of User Manuals.Manual Surveillances performed.W/930629 Ltr ML20029B1261991-02-28028 February 1991 LER 91-001-00:on 910129,tubing in Air Start Sys for Emergency Diesel Generator Failed During Seismic Event. Caused by Error in Design of EDG Air Start Sys.Permanent Mod to Sys installed.W/910228 Ltr ML20028H8011991-01-24024 January 1991 LER 90-002-01:on 900116,determined That 891211 Reconstitution of More than One Spent Fuel Assembly Per Time in Violation of Fuel Handling Incident Safety Analysis. Caused by Deficient procedure.W/910124 Ltr ML20044A1861990-06-20020 June 1990 LER 87-002-01:on 861203,section of Thin Wall Found on Main Steam Line W/Readings Below Allowable Min of 0.95 Inches. Caused by Grinding of Edge of Pipe to Achieve Proper fit-up for Welding.Relief from IWB-3610 granted.W/900620 Ltr ML20043G1071990-06-13013 June 1990 LER 89-019-01:on 891128,determined That for Approx 10 Yrs, from 1979-1989,requirement to Lock HPSI Discharge Header Isolation Valves Shut Not Implemented.Caused by Inadequate Mgt Attention.Test Procedures modified.W/900613 Ltr ML20043F1221990-06-0404 June 1990 LER 90-017-00:on 900505,pin Hole Leak Observed in Discharge Piping of Saltwater Pump 13.Caused by Localized Corrosion. Leaking Spool Piece Removed & Blank Flange Installed. W/900604 Ltr ML20043A7871990-05-21021 May 1990 LER 90-016-00:on 900421,determined That Waste Gas Decay Tank (Wgdt) 13 Discharged Instead of (Wgdt) 11 for Discharge Permit Issued.Caused by Inadequate Communications.Training Performed for Operators Re event.W/900521 Ltr ML20043A3441990-05-14014 May 1990 LER 90-014-00:on 900413 & 19,unit Entered Tech Spec Limiting Condition of Operation 3.0.3 Due to Potential Inoperability of Three Out of Four Reactor Protection Sys Delta T Power Channels.Caused by Lack of Procedure guidance.W/900514 Ltr ML20043A3401990-05-14014 May 1990 LER 90-013-00:on 900413,determined That Axial Shape Index Channels Out of Spec & Inoperable.Caused by Inadequate Understanding of Design Basis for Excore/Incore Comparison. Design Basis for Excore/Incore improved.W/900514 Ltr ML20042G4521990-05-0707 May 1990 LER 90-015-00:on 900407,discovered That Relay Contact Which Actuates Reactor Trip Breaker Shunt Trip Not Adequately Functionally Tested.Caused by Failure to Examine Circuit in Detail When Test developed.W/900507 Ltr ML20042F5801990-05-0404 May 1990 LER 90-012-00:on 900406,identified That Procedure for LOCA Would Not Ensure post-LOCA Core Flush Would Be Initiated in Time to Prevent Boron Precipitation.Caused by Personnel Error.Configuration Mgt Program strengthened.W/900504 Ltr ML20012E9931990-03-29029 March 1990 LER 90-008-00:on 900227,determined That Surveillance Procedure M-280-0 Did Not Include Steps to Fully Test Control Room Recorder for Hydrogen Analyzers.Caused by Personnel Error.Procedure Revised on 900308.W/900329 Ltr ML20012F0001990-03-28028 March 1990 LER 89-006-01:on 890508,containment Iodine Filters Outside Design Basis Due to Equipment Qualification.Recalculation of Total Integrated Radiation Dose to Cables for Filter Fans Demonstrated Cable qualified.W/900328 Ltr ML20012E9951990-03-28028 March 1990 LER 89-014-01:on 890723,determined That Salt Water Header Not Capable of Withstanding Seismic Event Intact.Caused by Inadequate Welding of Blind Spool Pieces in Pipe.Insp Revealed Spools Capable as installed.W/900328 Ltr ML20012E0101990-03-26026 March 1990 LER 90-009-00:on 900224,failure to Meet Action Requirement Re Tech Spec 3.7.12.Caused by Personnel Error.Cables Removed from Doorway in Charging Pump Room & Not Allowed to Be Placed in doorway.W/900326 Ltr ML20012C4971990-03-15015 March 1990 LER 90-007-00:on 900216,discovered That Supervised Circuits Associated W/Fire Detection Instruments Located in Reactor Coolant Pump Bays Not Been Included in Surveillance Test Procedure.Caused by Personnel error.W/900315 Ltr ML20012C4861990-03-12012 March 1990 LER 90-006-00:on 900209,determined That Four Fire Dampers Missing.Caused by Not Identifying Penetrations as Requiring Dampers When Fire Hazards Analysis of Plant Conducted.Hourly Fire Watch Continued.Missing Dampers installed.W/900312 Ltr ML20012B8991990-03-12012 March 1990 LER 89-023-01:on 891220,determined That Pipe Rupture in nonsafety-related Svc Water Subsystem Could Result in Rapid Draining of Subsystems That Serve Auxiliary Bldg.Task Force Formed to Determine Corrective actions.W/900312 Ltr ML20012B4221990-03-0606 March 1990 LER 89-012-01:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed.Caused by Procedural Deficiency.Procedures Revised to Include Valve & Surveillance Test Program Instruction revised.W/900306 Ltr ML20011F2701990-02-27027 February 1990 LER 90-001-01:on 900109,determined That Surveillance Tests Used to Perform Channel Calibr Tests for Acoustic Flow Monitoring Devices Inadequate.Caused by Personnel Error & Inadequate Procedures.Swapped Leads restored.W/900227 Ltr ML20011F2091990-02-27027 February 1990 LER 89-026-00:on 891128,determined That Particulate Levels in Samples Taken from Lower Third of Tanks Exceeded Allowable Limits.Caused by Inadequate Sampling Technique. Tanks Cleaned & Filled W/Clean fuel.W/900227 Ltr ML20006F8601990-02-22022 February 1990 LER 90-004-00:on 900123,discovered Fire Barrier Penetration Seal Open for Indeterminate Time W/O Performing Tech Spec 3.7.12.a Required Actions.Caused by Personnel Error. Temporary Fire Seal installed.W/900222 Ltr ML20006E0521990-02-0808 February 1990 LER 90-001-00:on 891221,discovered That Acoustic Indications for One PORV & One Safety Valve Were Reversed During Surveillance Test.Caused by Personnel Error.Swapped Leads Restored to Proper configuration.W/900208 Ltr ML20006B4801990-01-26026 January 1990 LER 89-022-00:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed,Violating Tech Specs.Caused by Procedural Deficiency.Surveillance Test Procedure Revised to Include Deleted valves.W/900126 Ltr ML19354D8931990-01-17017 January 1990 LER 89-024-00:on 891218,determined That Wires Which Connect Actuation Device Logic Relay Contacts to Remainder of Circuit Not Tested During Channel Calibr Test.Caused by Inadequate Test.Test Program Upgrade underway.W/900117 Ltr ML20005F1921990-01-10010 January 1990 LER 89-025-00:on 891208,Tech Spec Action Statement Entered When Ventilation Ducts Penetrating Fire Barrier Could Not Be Accessed to Determine If Fire Dampers Installed.On 891211, Fire Watch Missed.Caused by Personnel error.W/900110 Ltr ML20005E3971989-12-28028 December 1989 LER 89-019-00:on 891128,discovered That HPSI Discharge Header Isolation Valves Not Locked Shut When RCS in Water Solid Condition,Resulting in Operation Outside Design Basis. Procedure Revised to Require Valves closed.W/891228 Ltr ML19351A4551989-12-13013 December 1989 LER 89-020-00:on 891113,determined That Some Solenoid Valves & Valve Power Supplies for Saltwater Sys May Not Be Able to Perform Design Function After Design Basis Seismic Event. Cause Undetermined.Power Supplies upgraded.W/891213 Ltr ML20005D6611989-12-0606 December 1989 LER 89-018-00:on 891106,discovered That Many Air Operated Control Valves & piston-operated Dampers Which Utilize safety-related Air Accumulators Would Not Have Performed as Expected After Loss of air.W/891206 Ltr ML19325F3951989-11-10010 November 1989 LER 89-002-01:on 890228,discovered That Fire Barrier Penetration Inoperable & Action Statement Requirements Not Satisfied.Caused by Inadequate Administrative Controls. Penetration Returned to Operable status.W/891115 Ltr ML19325E8221989-11-0303 November 1989 LER 89-007-01:on 890505,evidence of Reactor Coolant Leakage from 120 Pressurizer Vessel Heater Penetrations Discovered. Caused by IGSCC of Inconel 600.All Penetrations Using J-welds & Inconel 600 Visually inspected.W/891103 Ltr ML19324B2511989-10-27027 October 1989 LER 89-012-01:on 890720,discovered That Master Solenoid to Switchgear Room Halon Sys Disconnected Since 890629.Caused by Personnel Error Resulting from Lack of Written Procedure. Procedure Revised to Apply Temporary mods.W/891027 Ltr ML19325C3281989-10-10010 October 1989 LER 89-016-00:on 890908,determined That as-found Condition of Resistance Temp Detectors Did Not Match Tested Configuration.Cause Not Stated.Subj Detectors Will Be Sealed,Per Environ Qualification requirements.W/891010 Ltr ML19325C3701989-10-0909 October 1989 LER 89-017-00:on 890907,determined That Discrepancy in Acceptance Criteria of Surveillance Test Procedure M-452-0 Resulted in Failure to Fully Comply W/Requirements of Tech Spec 3.9.12.Main Cause undetermined.W/891009 Ltr ML20024F3771983-08-25025 August 1983 LER 83-044/03L-0:on 830808,diesel Generator 12 Tripped on Low Jacket Cooling Water Pressure While Verifying Operability.Cause Not Stated.Coolant Jacket Vented & Large Amount of Air Found.No Evidence of leakage.W/830825 Ltr ML20024F5731983-08-25025 August 1983 LER 83-040/03L-0:on 830727,control Room Air Conditioner 11 Discovered W/Damaged Condenser Fan.Caused by Loose Set Screws Securing Fan in Position.Set Screws Restored. W/830825 Ltr ML20024E6761983-08-0404 August 1983 Updated LER 83-011/03X-1:on 830207,during Surveillance Testing ESFAS a Logic Sequencer Failed,Rendering Diesel Generator 12 Inoperable.Caused by Intermittent Operation of Module Test Push Button.Part replaced.W/830804 Ltr ML20024E1721983-07-14014 July 1983 Updated LER 81-015/03X-1:on 810226,sample Pump for Control Room Radiation Monitor Found Out of Svc,Rendering Automatic Recirculation of Control Room Ventilation Sys on High Radiation Inoperable.Caused by seizure.W/830714 Ltr ML20024D0071983-07-0808 July 1983 LER 83-035/03L-0:on 830610,during Normal Power Operation,Esf Actuation Sys Channel Zg Steam Generator Level Tripped. Caused by Failed Vitro Isolator Module.Module Replaced.W/ 830708 Ltr ML20024D0091983-07-0808 July 1983 LER 83-033/03L-0:on 830603,fire Detection Instrumentation in Containment Southeast Electrical Penetration Determined Inoperable.Repair Impossible Due to Inaccessability of Protecto wire.W/830708 Ltr ML20024B8231983-06-23023 June 1983 LER 83-029/03L-0:on 830524,during Normal Operation, Surveillance Testing Indicated Neither Spent Fuel Pool Exhaust Fans 11 or 12 Would Maintain Required Negative Pressure.Caused by Clogged HEPA filters.W/830623 Ltr ML20024C0141983-06-22022 June 1983 Updated LER 81-080/03X-1:on 811116,discovered Weep from Cracked Weld on Spent Fuel Cooling Pump Discharge Vent Line 12.Caused by Inadequate Support of Vent Line.Support Assembly installed.W/830622 Ltr ML20024A8881983-06-16016 June 1983 LER 83-032/03L-0:on 830523,containment Isolation Sys B Logic Module Would Not Actuate.Caused by Defective Vitro Labs Std Logic Module.Module Replaced.Failed Module Returned to Vitro Labs for Repair & testing.W/830616 Ltr 1999-08-23
[Table view] Category:RO)
MONTHYEARML17326A2011999-08-23023 August 1999 LER 99-004-00:on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With 990823 Ltr ML20029C7321994-04-22022 April 1994 LER 94-004-00:on 940221,discovered Corrosion of Three Nuts on One of Incor Instrumentation Reactor Vessel Head.Caused by Increase of Wet Boric Acid.Leaking Flanges Repaired.W/ 940422 Ltr ML20046B4731993-07-30030 July 1993 LER 93-005-00:on 930630,TS 3.0.3 Entered Due to Both Containment Spray Sys Inoperable.Replaced CCW Outlet Valve Actuator Connecting Link Assembly from Number 11 SDC Heat exchanger.W/930730 Ltr ML20046A4911993-07-22022 July 1993 LER 93-003-00:on 930625,SG Tripped Due to Low Water Level. Caused by Insufficient Feedwater Addition Due to Inadequate Communication.Reemphasis on Improved Communication Stressed. W/930722 Ltr ML20045G8611993-07-0909 July 1993 LER 93-003-00:on 930610,dual Unit Trip Occurred Due to Partial Loss of Offsite Power.Flashover Protection Relay for Breaker 552-61 Replaced & Training for Personnel W/ Access to Relays Will Be reinforced.W/930709 Ltr ML20045G7281993-07-0808 July 1993 LER 93-002-00:on 930608,inadvertent Arw Actuation Sys & RPS Actuations Experienced During Performance of Awf Sys Large Flow Surveillance Testing.Caused by Failure to Note Differential Pressure Condition.Valve opened.W/930708 Ltr ML20045G8661993-07-0808 July 1993 LER 93-004-00:on 930611,reactor Tripped Due to Turbine Trip Resulting from Inadequate Procedure.Procedure Changes Made to Open Appropriate FW Heater High Level Dump Valves During Plant startup.W/930708 Ltr ML20045E7361993-06-29029 June 1993 LER 93-002-01:on 930205,software Vendor Discovered Error in User Manual for Updating Basss data-input Library.Caused by Failure of QA Procedures to Require Independent Review of User Manuals.Manual Surveillances performed.W/930629 Ltr ML20029B1261991-02-28028 February 1991 LER 91-001-00:on 910129,tubing in Air Start Sys for Emergency Diesel Generator Failed During Seismic Event. Caused by Error in Design of EDG Air Start Sys.Permanent Mod to Sys installed.W/910228 Ltr ML20028H8011991-01-24024 January 1991 LER 90-002-01:on 900116,determined That 891211 Reconstitution of More than One Spent Fuel Assembly Per Time in Violation of Fuel Handling Incident Safety Analysis. Caused by Deficient procedure.W/910124 Ltr ML20044A1861990-06-20020 June 1990 LER 87-002-01:on 861203,section of Thin Wall Found on Main Steam Line W/Readings Below Allowable Min of 0.95 Inches. Caused by Grinding of Edge of Pipe to Achieve Proper fit-up for Welding.Relief from IWB-3610 granted.W/900620 Ltr ML20043G1071990-06-13013 June 1990 LER 89-019-01:on 891128,determined That for Approx 10 Yrs, from 1979-1989,requirement to Lock HPSI Discharge Header Isolation Valves Shut Not Implemented.Caused by Inadequate Mgt Attention.Test Procedures modified.W/900613 Ltr ML20043F1221990-06-0404 June 1990 LER 90-017-00:on 900505,pin Hole Leak Observed in Discharge Piping of Saltwater Pump 13.Caused by Localized Corrosion. Leaking Spool Piece Removed & Blank Flange Installed. W/900604 Ltr ML20043A7871990-05-21021 May 1990 LER 90-016-00:on 900421,determined That Waste Gas Decay Tank (Wgdt) 13 Discharged Instead of (Wgdt) 11 for Discharge Permit Issued.Caused by Inadequate Communications.Training Performed for Operators Re event.W/900521 Ltr ML20043A3441990-05-14014 May 1990 LER 90-014-00:on 900413 & 19,unit Entered Tech Spec Limiting Condition of Operation 3.0.3 Due to Potential Inoperability of Three Out of Four Reactor Protection Sys Delta T Power Channels.Caused by Lack of Procedure guidance.W/900514 Ltr ML20043A3401990-05-14014 May 1990 LER 90-013-00:on 900413,determined That Axial Shape Index Channels Out of Spec & Inoperable.Caused by Inadequate Understanding of Design Basis for Excore/Incore Comparison. Design Basis for Excore/Incore improved.W/900514 Ltr ML20042G4521990-05-0707 May 1990 LER 90-015-00:on 900407,discovered That Relay Contact Which Actuates Reactor Trip Breaker Shunt Trip Not Adequately Functionally Tested.Caused by Failure to Examine Circuit in Detail When Test developed.W/900507 Ltr ML20042F5801990-05-0404 May 1990 LER 90-012-00:on 900406,identified That Procedure for LOCA Would Not Ensure post-LOCA Core Flush Would Be Initiated in Time to Prevent Boron Precipitation.Caused by Personnel Error.Configuration Mgt Program strengthened.W/900504 Ltr ML20012E9931990-03-29029 March 1990 LER 90-008-00:on 900227,determined That Surveillance Procedure M-280-0 Did Not Include Steps to Fully Test Control Room Recorder for Hydrogen Analyzers.Caused by Personnel Error.Procedure Revised on 900308.W/900329 Ltr ML20012F0001990-03-28028 March 1990 LER 89-006-01:on 890508,containment Iodine Filters Outside Design Basis Due to Equipment Qualification.Recalculation of Total Integrated Radiation Dose to Cables for Filter Fans Demonstrated Cable qualified.W/900328 Ltr ML20012E9951990-03-28028 March 1990 LER 89-014-01:on 890723,determined That Salt Water Header Not Capable of Withstanding Seismic Event Intact.Caused by Inadequate Welding of Blind Spool Pieces in Pipe.Insp Revealed Spools Capable as installed.W/900328 Ltr ML20012E0101990-03-26026 March 1990 LER 90-009-00:on 900224,failure to Meet Action Requirement Re Tech Spec 3.7.12.Caused by Personnel Error.Cables Removed from Doorway in Charging Pump Room & Not Allowed to Be Placed in doorway.W/900326 Ltr ML20012C4971990-03-15015 March 1990 LER 90-007-00:on 900216,discovered That Supervised Circuits Associated W/Fire Detection Instruments Located in Reactor Coolant Pump Bays Not Been Included in Surveillance Test Procedure.Caused by Personnel error.W/900315 Ltr ML20012C4861990-03-12012 March 1990 LER 90-006-00:on 900209,determined That Four Fire Dampers Missing.Caused by Not Identifying Penetrations as Requiring Dampers When Fire Hazards Analysis of Plant Conducted.Hourly Fire Watch Continued.Missing Dampers installed.W/900312 Ltr ML20012B8991990-03-12012 March 1990 LER 89-023-01:on 891220,determined That Pipe Rupture in nonsafety-related Svc Water Subsystem Could Result in Rapid Draining of Subsystems That Serve Auxiliary Bldg.Task Force Formed to Determine Corrective actions.W/900312 Ltr ML20012B4221990-03-0606 March 1990 LER 89-012-01:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed.Caused by Procedural Deficiency.Procedures Revised to Include Valve & Surveillance Test Program Instruction revised.W/900306 Ltr ML20011F2701990-02-27027 February 1990 LER 90-001-01:on 900109,determined That Surveillance Tests Used to Perform Channel Calibr Tests for Acoustic Flow Monitoring Devices Inadequate.Caused by Personnel Error & Inadequate Procedures.Swapped Leads restored.W/900227 Ltr ML20011F2091990-02-27027 February 1990 LER 89-026-00:on 891128,determined That Particulate Levels in Samples Taken from Lower Third of Tanks Exceeded Allowable Limits.Caused by Inadequate Sampling Technique. Tanks Cleaned & Filled W/Clean fuel.W/900227 Ltr ML20006F8601990-02-22022 February 1990 LER 90-004-00:on 900123,discovered Fire Barrier Penetration Seal Open for Indeterminate Time W/O Performing Tech Spec 3.7.12.a Required Actions.Caused by Personnel Error. Temporary Fire Seal installed.W/900222 Ltr ML20006E0521990-02-0808 February 1990 LER 90-001-00:on 891221,discovered That Acoustic Indications for One PORV & One Safety Valve Were Reversed During Surveillance Test.Caused by Personnel Error.Swapped Leads Restored to Proper configuration.W/900208 Ltr ML20006B4801990-01-26026 January 1990 LER 89-022-00:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed,Violating Tech Specs.Caused by Procedural Deficiency.Surveillance Test Procedure Revised to Include Deleted valves.W/900126 Ltr ML19354D8931990-01-17017 January 1990 LER 89-024-00:on 891218,determined That Wires Which Connect Actuation Device Logic Relay Contacts to Remainder of Circuit Not Tested During Channel Calibr Test.Caused by Inadequate Test.Test Program Upgrade underway.W/900117 Ltr ML20005F1921990-01-10010 January 1990 LER 89-025-00:on 891208,Tech Spec Action Statement Entered When Ventilation Ducts Penetrating Fire Barrier Could Not Be Accessed to Determine If Fire Dampers Installed.On 891211, Fire Watch Missed.Caused by Personnel error.W/900110 Ltr ML20005E3971989-12-28028 December 1989 LER 89-019-00:on 891128,discovered That HPSI Discharge Header Isolation Valves Not Locked Shut When RCS in Water Solid Condition,Resulting in Operation Outside Design Basis. Procedure Revised to Require Valves closed.W/891228 Ltr ML19351A4551989-12-13013 December 1989 LER 89-020-00:on 891113,determined That Some Solenoid Valves & Valve Power Supplies for Saltwater Sys May Not Be Able to Perform Design Function After Design Basis Seismic Event. Cause Undetermined.Power Supplies upgraded.W/891213 Ltr ML20005D6611989-12-0606 December 1989 LER 89-018-00:on 891106,discovered That Many Air Operated Control Valves & piston-operated Dampers Which Utilize safety-related Air Accumulators Would Not Have Performed as Expected After Loss of air.W/891206 Ltr ML19325F3951989-11-10010 November 1989 LER 89-002-01:on 890228,discovered That Fire Barrier Penetration Inoperable & Action Statement Requirements Not Satisfied.Caused by Inadequate Administrative Controls. Penetration Returned to Operable status.W/891115 Ltr ML19325E8221989-11-0303 November 1989 LER 89-007-01:on 890505,evidence of Reactor Coolant Leakage from 120 Pressurizer Vessel Heater Penetrations Discovered. Caused by IGSCC of Inconel 600.All Penetrations Using J-welds & Inconel 600 Visually inspected.W/891103 Ltr ML19324B2511989-10-27027 October 1989 LER 89-012-01:on 890720,discovered That Master Solenoid to Switchgear Room Halon Sys Disconnected Since 890629.Caused by Personnel Error Resulting from Lack of Written Procedure. Procedure Revised to Apply Temporary mods.W/891027 Ltr ML19325C3281989-10-10010 October 1989 LER 89-016-00:on 890908,determined That as-found Condition of Resistance Temp Detectors Did Not Match Tested Configuration.Cause Not Stated.Subj Detectors Will Be Sealed,Per Environ Qualification requirements.W/891010 Ltr ML19325C3701989-10-0909 October 1989 LER 89-017-00:on 890907,determined That Discrepancy in Acceptance Criteria of Surveillance Test Procedure M-452-0 Resulted in Failure to Fully Comply W/Requirements of Tech Spec 3.9.12.Main Cause undetermined.W/891009 Ltr ML20024F3771983-08-25025 August 1983 LER 83-044/03L-0:on 830808,diesel Generator 12 Tripped on Low Jacket Cooling Water Pressure While Verifying Operability.Cause Not Stated.Coolant Jacket Vented & Large Amount of Air Found.No Evidence of leakage.W/830825 Ltr ML20024F5731983-08-25025 August 1983 LER 83-040/03L-0:on 830727,control Room Air Conditioner 11 Discovered W/Damaged Condenser Fan.Caused by Loose Set Screws Securing Fan in Position.Set Screws Restored. W/830825 Ltr ML20024E6761983-08-0404 August 1983 Updated LER 83-011/03X-1:on 830207,during Surveillance Testing ESFAS a Logic Sequencer Failed,Rendering Diesel Generator 12 Inoperable.Caused by Intermittent Operation of Module Test Push Button.Part replaced.W/830804 Ltr ML20024E1721983-07-14014 July 1983 Updated LER 81-015/03X-1:on 810226,sample Pump for Control Room Radiation Monitor Found Out of Svc,Rendering Automatic Recirculation of Control Room Ventilation Sys on High Radiation Inoperable.Caused by seizure.W/830714 Ltr ML20024D0071983-07-0808 July 1983 LER 83-035/03L-0:on 830610,during Normal Power Operation,Esf Actuation Sys Channel Zg Steam Generator Level Tripped. Caused by Failed Vitro Isolator Module.Module Replaced.W/ 830708 Ltr ML20024D0091983-07-0808 July 1983 LER 83-033/03L-0:on 830603,fire Detection Instrumentation in Containment Southeast Electrical Penetration Determined Inoperable.Repair Impossible Due to Inaccessability of Protecto wire.W/830708 Ltr ML20024B8231983-06-23023 June 1983 LER 83-029/03L-0:on 830524,during Normal Operation, Surveillance Testing Indicated Neither Spent Fuel Pool Exhaust Fans 11 or 12 Would Maintain Required Negative Pressure.Caused by Clogged HEPA filters.W/830623 Ltr ML20024C0141983-06-22022 June 1983 Updated LER 81-080/03X-1:on 811116,discovered Weep from Cracked Weld on Spent Fuel Cooling Pump Discharge Vent Line 12.Caused by Inadequate Support of Vent Line.Support Assembly installed.W/830622 Ltr ML20024A8881983-06-16016 June 1983 LER 83-032/03L-0:on 830523,containment Isolation Sys B Logic Module Would Not Actuate.Caused by Defective Vitro Labs Std Logic Module.Module Replaced.Failed Module Returned to Vitro Labs for Repair & testing.W/830616 Ltr 1999-08-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G6971999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Calvert Cliffs Npp,Units 1 & 2.With ML20216J8731999-09-10010 September 1999 Rev 52 to QA Policy for Calvert Cliffs Nuclear Power Plant ML20212A4441999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Ccnpp,Units 1 & 2. with ML17326A2011999-08-23023 August 1999 LER 99-004-00:on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With 990823 Ltr ML20210S6091999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ccnpp,Units 1 & 2. with ML20210N6001999-07-27027 July 1999 ISI Summary Rept for Calvert Cliffs Unit 2. Page 2 of 3 in Encl 1 of Incoming Submittal Not Included ML20210B7941999-07-15015 July 1999 SER Denying Licensee Request for Changes to Current Ts,Re Deletion of Tendon Surveillance Requirements for Calvert Cliffs LD-99-039, Part 21 Rept Re Defect of Abb 1200A 4kV Vacuum Breakers. Initially Reported on 990625.Defect Results in Breaker Failing to Remain in Closed Position.Root Cause Evaluation & Corrective Action Plan Being Developed.Licensee Notified1999-06-30030 June 1999 Part 21 Rept Re Defect of Abb 1200A 4kV Vacuum Breakers. Initially Reported on 990625.Defect Results in Breaker Failing to Remain in Closed Position.Root Cause Evaluation & Corrective Action Plan Being Developed.Licensee Notified ML20209F1721999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Calvert Cliffs Npp.With LD-99-035, Part 21 Rept Re Abb 1200A 4KV Vacuum Breakers Performing Trip Free Operation When Close Signal Received by Breaker. Defect Results in Breaker Failing to Remain in Closed Position.Root Cause & CAP Being Developed1999-06-25025 June 1999 Part 21 Rept Re Abb 1200A 4KV Vacuum Breakers Performing Trip Free Operation When Close Signal Received by Breaker. Defect Results in Breaker Failing to Remain in Closed Position.Root Cause & CAP Being Developed ML20196C6981999-06-21021 June 1999 Safety Evaluation Concluding That Use of ASME Section XI Code Including Summer 1983 Addenda as Interim Code for Third 10-year Insp Interval at Calvert Cliffs Units 1 & 2 Until Review of 1998 Code Completed,Would Be Acceptable ML20195K2811999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Ccnpp,Units 1 & 2. with ML20206R5871999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ccnpp,Units 1 & 2. with ML20195B3891999-04-30030 April 1999 0 to CENPD-279, Annual Rept on Abb CE ECCS Performance Evaluation Models ML20205N2951999-04-13013 April 1999 Special Rept:On 990314,fire Detection Sys Was Removed from Svc to Support Mod to Replace SRW Heat Exchangers in Unit 2 SRW Room During Unit 2 Refueling Outage.Contingency Measure 15.3.5.A.1 Will Continue Until Fire Detection Sys Restored ML20210T5211999-04-0101 April 1999 Rev 0 to Ccnpp COLR for Unit 2,Cycle 13 ML20205P5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20204H6471999-03-21021 March 1999 SER Re License Renewal of Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20207M8321999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Calvert Cliffs Nuclear Power Plant.With ML20203D4311999-02-0505 February 1999 Safety Evaluation Accepting Procedure Established for long-term Corrective Action Plan Related to Containment Vertical Tendons ML20199G4671999-01-20020 January 1999 SER Accepting USI A-46 Implementation for Plant ML20206Q3221999-01-11011 January 1999 Special Rept:On 981226,wide Range Noble Gas Effluent RM Was Removed from Operable Status.Caused by Failure of mid-range Checksource to Properly Reseat.Completed Maint & post-maint Testing & RM Was Returned to Operable Status on 990104 ML20207L0451999-01-0808 January 1999 Cost-Benefit Risk Analyses:Radwaste Sys for Light Water Reactors ML20199F4781999-01-0808 January 1999 Safety Evaluation Concluding That Bg&E Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves Susceptible to Pressure Locking.Concludes GL 95-07 Actions Were Addressed ML20198S7591999-01-0707 January 1999 SER Accepting Quality Assurance Program Description Change for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20207M2281998-12-31031 December 1998 1998 Annual Rept for Bg&E. with ML20199E2931998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Calvert Cliffs Npp. with ML20206R9911998-12-0808 December 1998 Rept of Changes,Tests & Experiments (10CFR50.59(b)(2)). with ML20198B2631998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20195H1001998-11-16016 November 1998 Safety Evaluation of First Containment Insp Interval Iwe/Iwl Program Alternative ML20196E2211998-10-31031 October 1998 Non-proprietary Rev 03-NP to CEN-633-NP, SG Tube Repair for Combustion Engineering Designed Plant with 3/4 - .048 Wall Inconel 600 Tubes Using Leak Limiting Alloy 800 Sleeves ML20195E5281998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Calvert Cliffs Nuclear Power Station,Units 1 & 2.With ML20154Q7191998-10-21021 October 1998 Special Rept:On 980923,unit 1 Wrngm Was Removed from Operable Status.Caused by Failure of Process Flow Transducer.Completed Maint to Remove Process Flow Transducer Input to Wrngm Microprocessor & Completed Formal Evaluation ML20154G3931998-10-0505 October 1998 Safety Evaluation Concluding That Flaw Tolerance Evaluation for Assumed Flaw in Inboard Instrument Weld of Pressurizer Meets Rules of ASME Code ML20154M5841998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Calvert Cliffs Nuclear Plant,Units 1 & 2.With ML20153C2571998-09-18018 September 1998 Special Rept:On 980830,wide Range Noble Gas Monitor (Wrngm) Channel Was Removed from Operable Status.Caused by Need to Support Performance of Required 18-month Channel Calibr.Will Return Wrngm to Operable Status by 980925 ML20153C1091998-09-18018 September 1998 Part 21 Rept Re Defective Capacity Control Valves.Trentec Personnel Have Been in Contact with Bg&E Personnel Re Condition & Have Requested Potentially Defective Valves ML20151U5441998-09-0404 September 1998 Bg&E ISI Summary Rept for Calvert Cliffs ML20151T5281998-09-0101 September 1998 Special Rept:On 980819,declared Rv Water Level Monitor Channel a Inoperable.Caused by Failure of Three Heated Junction Thermocouples (Sensors) in Lower Five Sensors. Channel a & B Rv Water Level Probes Will Be Replaced ML20151Y1191998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Calvert Cliffs Nuclear Power Plant Units 1 & 2.With ML20237D4981998-08-19019 August 1998 Safety Evaluation Accepting Licensee Request for Extension of Second ten-year Inservice Insp Interval ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20237B9371998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Calvert Cliffs Nuclear Power Plant ML20237D5941998-07-22022 July 1998 Rev 2 to Ccnpp COLR for Unit 2,Cycle 12 ML20236L7521998-07-0606 July 1998 Safety Evaluation Granting Bg&E 980527 Request for Relief from Requirement of Section IWA-5250 of ASME Code for Calvert Cliffs Unit 2.Alternatives Provide Reasonable Assurance of Operational Readiness ML20236F7791998-06-30030 June 1998 Safety Evaluation Authorizing Request for Temporary Relief from Requirement of Subsection IWA-5250 of ASME Code,Section XI for Plant,Unit 1 ML20236R0881998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20236X3101998-06-19019 June 1998 Rev 1 to Calvert Cliffs Nuclear Power Plant COLR for Unit 2,Cycle 12 ML20249A9571998-06-15015 June 1998 Special Rept:On 980430,fire Detection Sys Was Removed from Svc to Support Mod to Purge Air Sys 27-foot Elevation & 5-foot Elevation East Piping Penetration Rooms.Installed Temporary Alteration & Returned Fire Detection Sys to Svc ML20249A7711998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Ccnpp,Units 1 & 2 1999-09-30
[Table view] |
Text
. .. . . . . . . . _ .
BALTIMORE GASAND t ELECTRIC CHARLES CENTER e P.O. BOX 1475
R. E. DE NTON MANAGtft i CAtytRT Cuf f 5 ,quCtg AR POW 6R PLANT DtFARTMeest May 21, 1990 U. S. Nuclear Regulatory Commission Docket No. 50 317 Document Control Desk 1.icense No. DPR 53 Wshington, D. C. 20555
Dear Sirs:
The attached LER 90 16, Revision 0, is being sent to you as required under 10 CFR 50.73.
Should you have any questions regarding this report, we would be pleased to discuss them with you.
Very truly yours, i
W~
[O R. E. Denton -
JV/kn ec: Thomas T. Martin Director, Office of Management Information and Program Control Messrs: G. C. Creel C. H. Cruse J. R. Lemons L. B. Russell R. P. Heibel q
t 9005230124 900521 PUR
_ PDC ,
[
tent; D Of;h8 30s6 U $ NUCL E AR ftt GUL ATOR Y COMMISllON E4191 gpppgg p gy, gg y g ping i KP4Hi s 4'wW t
($T iM All O poNDI N F i n 54f spON$t To COMbt v n Yw T wis LICENSEE EVENT REPORT (LER1 '%.f,'li c ,','s'MMANAciMi~ J$n',',lcTL,"i.'. Ts'fiM A ,Y,Z t 7t cM l ann aironis n ANc 64t Gu tATOHV COMMiWON W Ar 4iNGtON ,P on, u s ~, on i An Ynt P Af f f:WOsn Rf DutisON PHOJE CT 014m o.t, A084E DC ?Obh N. D 10 08 VA NA0l VI NT AND SVDGi1 W AKM rNGTON DC ?Oh03 P ACet T v N AMt n i puce t t NUMein tai PAGE i3 Calvert Cliffs, Unit 1 fitit i.:
0 l 510 l 0 l 0 l3 l1 17 1 lorl 013 Waste Gas Decay Tank Mistakenly Discha;ged without Prior Sampling
( VINT DAll it' Ltm NUMelm sei h t >OR T Da f t i yi OTHim 8 ACittf elt INVOtytD ISI MON T .4 DA= v t A s. vtA6 , [g*,',] MONYn Dav s t a te . Al'L o v Na ve s DOC. t ' Nuwht 808' Ca l ve r t Cliffs, Unit 2 0[510l0lo1 3l1 8 1
~ -
0l 4 9 0 2l1 9l 0 0l 1 l6 0 l0 Oj$ 2l1 %0 oi b io 1 0 iog i i g,,,,,, THis atPOpf is sumMiTTt D PunsVANT 70 THt an OvisitMENYs Os to co m t, ,r%. un " mo,. ,, ,a. s.uo n,1 Iti
- * *' 1 ro.oami no .oai. , so > >i. nz n . varimi ponen so.ot nino .o mi.n u no v a,. ns u > > > n i. i ttvtt iioi 9gri 3 no .oii.in n.o no mi. uni no vii. nan..o
- . ,,,OTHe
.,, ar.4,. ,osu e4 ,A. c , ,,,m so .oei.nnoii' X so?>= nano se v s..nz ....n Ai mA ro osmin n... so vsi.nsu . no rai. uni.,...no.
ro .oei.in n i oovai. nan no ,3 .na n. ,
L10tNSI( CONT ACT son THis tim nas NAMt IILt*MONE NdMSIN Aht A CODt
.lohn Volkoff, Compliance Engineer 3101 1 216101 - 13 f> 1419 COMPS (14 ONE L +NI 8 0m L ACH COMPONE NT 8 Alt unt ciscaist D IN THl6 mt PORT s t3:
C Av58 $$ $1 t Y COMPONEN' "
[g p , y (AUSt $ ' E' t V (OVPONIN' g p
.I 1 1 1 1 1 1 l i 1 1 1 I I I 1 1 I I I l i I I 1 ! I I l SUPPL EME NT AL REPOmf I EPI Cit D (1. MONie DA* v t Ace seeM ss,0.,
] , t s a, . ., "'
,,m,... , un ces e s ,M 55,0N o. , a
~% e l l A...AC,-,,,__., . . . . ~ . . . . - , . _ . , _ , - - . . . " . .
At 0030, on April 21, 1990, during shift change, an operator determined t. h a t Waste Gas Decay Tank (WGDT) #13 was being discharged instead of WGDT Wll, for which a discharge permit had been issued. The discharge was stopped and #13 WGDT sampled to calculate the amount of radiological material released. It was detern:ined that the release was wit hin Technical Specifications. It was also determined that in the event of the limiting waste gas incident occurring, dose at the nearest exclusion area boundary would be within the 10CFR100 guideline value. At the time Unit-1 was operating (MODE 1) at 65% power, a temperature of 540 degrees F and a pressure of 2250 psia.
Inadequate communications between the Unit-1 (U-1) Control Room Operator and the U-l Auxiliary Building Operator was the root cause of the event. Inadequate specific directions of Calvert Cliffs Instruction (CCI)-309, Locked Valves, contributed to the event.
Training will be performed for operators on this event emphasizing the importance of the use of formal communications. CCI-309 will be revised to provide more stringent administrative control of locked valve operation. An evaluation will be performed to determine if site wide requirements governing formality in communications are adequate Nac . m m a
, , i.,,., ,, ,, .m , ,, , , . . . -
, . , , . , , , ,, - ,i, , , , , , , . . - - - - - - - - - - - -
l l C PORM 3e6A U.S. NUCL4 Au R$GULATORY CotAMISB40N ExPITES 4/30'92 UCENSEE EVENT REPORT (LER) lM^J&*,7@$PJo!',$Po"j',2%CM7 TR.'"'!
TEXT CONTINU ATlON i&R '"t ,&'lP'21"d Mf'. Mile'0/!E,".' "'jfRA UETAItlw'oE"R"I'$'Eio**E*SC?"6E4% UI?CT OF MANAGEMENT AND DVDGET. WASHINGTON, DC 20b03, 9 ACILitY hAMt (U Doc,LET NUMSS R 42)
LIR NUM0th (Si PA06 43)
TI'" vvNe* NwsN Calvert Cliffs, Unit 1 0 l6 l0 l0 lo l 3 l1 l 7 91 0 -
0 l1l6 -
0 l0 0 12 0F 0 l5 TEKT W mews apose a soppost oss ashesoniW NRC Perm Ws/ (IM I. DESCRIPTION OF EVENT At 0030 on April 21, 1990, during shift change, an operator determined that Waste L Gas Decay Tank (WGDT) #13 was being discharged instead of WGDT #11, for which a j discharge permit had been issued. The discharge was stopped and #13 WGDT sampled to calculate the amount of radiological material released. We determined that the release was within TSs. At the time Unit-1 (U-1) was operating (MODE 1) at !
65% power, a temperature of 542 degrees F, and a pressure of 2250 psia.
- 11. BACKGROUND The WGDTs store waste gas from the plant to allow time for the radionuclides to decay. A WGDT is taken off service when the pressure in the tank reaches i approximately 140 psia. The gas is discharged after the WGDT has been sampled and the activity of the gas has been determined. At 1800 on April 20, 1990, WGDT
- 11 was at 138 psia and UGDT #13 was at 142 psia.
At approximately 1800 on April 20, Plant Chemistry, f delivered a waste gas release permit 1990, to thethe Operations supervisor, . Shift Supervisor.
The permit was for the release of the contents of WGDT #11.. The Shift Supervisor gave the permit to the Control Room Supervisor (CRS). The CRS gave it to the U-1 Control Room Operator (CRO) and directed him to discharge # 11 WGDT. At this time, #11 and #13 WGDTs wet isolated and #12 WGDT was in service.
At 1830, the U-1 Auxiliary Building Operator (ABO) reported to the U 1 Reactor Operator that #13 WGDT pressure was at 142 psig, 2 psi above the high limit on the ABO logs. The ABO also reported that #12 WGDT was verified in service and asked that the information be passed on'to the CRO. 1 At approximately 1915, the U-1 ABO called the U 1.CR0 to verify that he - had received the report about WGDT #12 being verified in service. During this conversation, the CR0 noted that a release permit had been received for #11 WGDT ,I and that the discharge would be done as time permitted. After the event, the ABO did not remember the specific WGDT to be discharged being mentioned in _ the conversation. The ABO believed that #13 WGDT was to be discharged based on its higher pressure which was greater than the maximum specified in his log. The ,
WGDT to be discharged was not specified again in communications subsequent ' to this conversation.
At approximately 2145 the line up to discharge a WGDT was begun. The U l ABO ;
reported to the U 1 CR0 that he was ready to begin'the line up. The CR0 directed I the ABO to perform the applicable steps in Operating Instruction (01)-17, Waste Gas System, for release, but the CR0 thought that WGDT #11 was being discharged, ;
while the ABO thought that WGDT #13 was to be discharged.
NBC Poem 3 eta (649)
+ .i n - n - . - _m
i NRC 70nM 306A U.S. NUCL.EAa tOUL/ TORY COMMIS& TON tXTCt$ u30 2 LICENSEE EVENT REPORT (LER) $6*W1Ro',fiO/cy,'of$g,'!TM#'l*ki' ,T.".'"'!
' ' a
~
TEXT CONTINUATlON iT'ETo',"v!'M21*ciU"f!" TC#^l!2 '".'
U OMft n RiWe"JJ *##$a"a,'Eil?'t&'A'o@iCi OF MANAGEMENT AND DVDGET.W ASHINGTON. DC 20503.
8.CILeiv Naut ns DOCRai NUMeta (t) 488 NUM8ER ISI PA08 (Si i "a= -
" M.;;',', ' 4q l Calvert Cliffs, Unit 1 0 l6 l0 l0 l0 l 311 17 910 -
0l1l6 -
0l0 0l 3 0F 0l5 ftXT M N apose a mesmest. use seas s ioner hg ps,m hW (17)
The step in 01 17B that opens the last valve in the line up, starting the discharge, contains 3 valves. Each valve corresponds to a different WGDT. The U1 ABO reported back to the CR that he had completed the step in 01 17B beginning the discharge, but did not specify which valve.had been opened or which ,
l WGDT was being discharged. The U 1 ABO monitored the discharge locally to ensure the discharge was proceeding as he expected, which was for WGDT #13 pressure to decrease, which it did.
A valve deviation sheet was not used prior to the operation of the locked valves operated in 01-17B. This was procedurally permissible due to a weakness in Calvert Cliffs Instruction (CCI) 309, Locked Valves, i
The WGDT pressure was not monitored in the Control Room (CR) because the U-2 Plant Computer, which provides the only signal to CR instruments that provide indications of WGDT pressures, was Out of-Service (OOS). 1 At approximately 2325, the U 2 ABO, who was assisting the U l ABO, checked to see if a valve deviation sheet had been filled out for the locked valves operated in the discharge procedure. The U-2 ABO discovered that no sheet had been filled out and completed one for two of the valves operated in the procedure. The CR0 checked the valve deviation sheet and found that one of the valves operated had not been entered on the sheet. He entered and initialed for the valve. However, he entered the valve for discharging from #11 WGDT. The U 1 ABO did not initial the valve deviation sheet.
While the next shift was taking the watch from the U 1 ABO, the oncoming ABO noted that at the shif t briefing, #11 WGDT was reported as being discharged. The oncoming ABO determined that #13 WGDT was being discharged and informed the CR.
The release was terminated at 0030 and the Plant Chemistry Unit was notified. A release permit for #13 WGDT was completed based on sample results of the contents remaining in the #13 WGDT.
III. CAUSES l The root cause of this event was inadequate ecmmunications. The -U-1 CR0 identified that #11 WGDT was to be discharged during the shift in a conversation with the U 1 ABO. However, the identity of the WGDT to be discharged was never restated in subsequent communications relating to the release. The ABO did not repeat the order back when he received direction regarding which WGDT was to be discharged. The ABO assumed that the CR0 wanted to discharge #13 WGDT, which he had previously reported as . having a pressure above the normal limit. The CR0 assumed that the ABO would discharge #11 WGDT based on the conversation that took place earlier in the shift.
N2C Form 3sSA (6491
u.. NoCu A ...ouvo., c,-, .
g.,Cgo.7 . u,,ns .mm .
3",25,90fs't.MM'5oM',,'%cf'lJ7 ,"o'."J"'j LICENSEE EVENT REPORT (LER) o TEXT CONTINUATION M",',",'o',';', ,'"Mi 'WM'J"^,'jg L".' "Mfi .
1 PAPER O .t UC ION J (3 60 04 0 IC OF MANAQtMtNT AND DVDGET,ih ASH 6NOTON. DC 70603 F ACILily NAM 4 m DOC 8tti NUneHR (2) ga gpuggR (6) PA06 (31 n- "ww "W.7:
l Calvert Cliffs, Unit 1 01510101013llj7 910 -
0l1 l6 -
Ol0 0l4 0F 0b run w mee neu. e *.< e sen w mc r,m, anu e nn ,
L CCI-309 governs the operation of locked valves to prevent their inadvertent L operation, llowever , the procedure is primarily designed to ensure that locked valves are returned to their normal position. The procedure does not provide effective controls for positioning locked valves out of their normal position. ;
C01-309 is unclear as-to when and how a valve deviation sheet should be used when 1
- taking locked valves out of their normal positions. As a result, a valvo l deviation sheet was not used prior to valve operation and ~ the U.1 ABO did not initial the valve deviation sheet.
Contributing to the event was the lack of the WGDT pressure monitor in. the Control Room because the-U 2 computer was not operational.
IV. ANALYSIS This event is reportable under 10 CFR 50.73(a)(2)(1)(B), an operation prohibited by the plants Technical Specifications-(TS). TSs require that.a sample be-drawn j fron a WGDT prior to its discharge. A sample was not drawn prior to discharging ;
- 13 WGDT.
j l
Based on calculations of the amount of radioactive gas released, the release was within TS limits.
A Chapter 14.22 of the updated Final Safety Analysis Report analyzes a rupture of i the waste gas decay tank to define the limit of the hazard that could result in ,
i any malfunction in the radioactive waste gas system. The maximum activity in any l WGDT is assumed to occur shortly after, n cold start up of .one_ unit near the end !
of an operating cycle. It is also assumed that :this unit has been operating for I an extended period with one percent defective fuel and that all of the coolant is let down. The noble gases from one reactor coolant system volume are stored in ;
one WGDT. i In the unlikely event of a rupture of the WGDT, the. dose-at the nearest exclusion zone boundary is a factor of 50 less than the 10CFR100 guideline value.
Therefore, a WGDT rupture does not represent undue hazard to the public health or .'
safety.
Under-normal circumstances, the activity of the waste gas released from the WGDTs f is.at least two or three orders of magnitude less than the activity considered in ;
the analyzed event. In accordance with Technical Specifications, the main vent 1 radiation monitoring system was operating and readings - were recorded every 15 j minutes during this release. The main vent monitor alarm setpoints were set based on the discharge permit prepared for a WGDT #11. If the alarm setpoint '
had been reached, the release would han a been secured. Thus, if a WGDT containing a substantially higher actWi.tv had been released by mistake, the alarm setpoint would have been reached W. the release secured. These factors further mitigate the safety significance of this event.
NRC form 306A (649) i
C Pomu setA ut5UCLE AM G.50VLATomV CoasmeestoN '
' ' ' *
- tK7tRES 4/30c2 LICENSEE EVENT REPORT (LER) - 'S&"^i', o'd808"Jol'&o",LM.Cf'l*A' ,T."di'!
^
TEXT CONTINUATlON it'4"4'#8 f?MM3'.Mf,'a^l!E".'"',ETfA UI"PIsn"w'oES*n"e'51Ev'E O E EE"(Elo M iEO di OF MANActMENT AND SUDGET, WASHINGTON.DC 20bO3.
PACiblTV Naut lit DOCILif NUe8Dtm (2) LIR Nuhst4R (6) PAOS (31 H
N "
4 -
y,Q Calve rt Cliffs. Unit 1 0 l5 l0 j 0 l0 l3 l 1l7 9)0 -
0l1 l 6 -
0 l0 0l5 0F 0 l 'i l rixi in a m.w. w Nac w menwim V. CORRECTIVE ACTIONS Shift Supervisors will review this event - with their shifts, emphasizing the iniportance of formality in communications. Specifically, according to Operations Section policy, when communicating, directions given shall be clear, precise and component specific. The directions are to be repeated back .in sufficient detail to ensure that they were understood.
An evaluation will be performed to determine if site wide requirements at Calvert Cliffs governing formality in communications are adequate.
CCI 309 will be revised to provide more stringent administrative control of locked valve operation. ,
1 OI 1~/B will be revised to require that during WGDT discharge either WGDT pressure be monitored in the Control Room or an alternate method be used to verify that the correct WGDT is being discharged.
i VI. ADDITIONAL INFORMATION A. Previous similar event.
No previous similar events involving inadvertent discharge of a WGDT have been noted at Calvert Cliffs.
B. Affected component identification.
IEEE 805 IEEE 803 Component System ID Comnonent WGDT WE TK Valve WE VTV NRC Poesn 386A (649)