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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17326A2011999-08-23023 August 1999 LER 99-004-00:on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With 990823 Ltr ML20029C7321994-04-22022 April 1994 LER 94-004-00:on 940221,discovered Corrosion of Three Nuts on One of Incor Instrumentation Reactor Vessel Head.Caused by Increase of Wet Boric Acid.Leaking Flanges Repaired.W/ 940422 Ltr ML20046B4731993-07-30030 July 1993 LER 93-005-00:on 930630,TS 3.0.3 Entered Due to Both Containment Spray Sys Inoperable.Replaced CCW Outlet Valve Actuator Connecting Link Assembly from Number 11 SDC Heat exchanger.W/930730 Ltr ML20046A4911993-07-22022 July 1993 LER 93-003-00:on 930625,SG Tripped Due to Low Water Level. Caused by Insufficient Feedwater Addition Due to Inadequate Communication.Reemphasis on Improved Communication Stressed. W/930722 Ltr ML20045G8611993-07-0909 July 1993 LER 93-003-00:on 930610,dual Unit Trip Occurred Due to Partial Loss of Offsite Power.Flashover Protection Relay for Breaker 552-61 Replaced & Training for Personnel W/ Access to Relays Will Be reinforced.W/930709 Ltr ML20045G7281993-07-0808 July 1993 LER 93-002-00:on 930608,inadvertent Arw Actuation Sys & RPS Actuations Experienced During Performance of Awf Sys Large Flow Surveillance Testing.Caused by Failure to Note Differential Pressure Condition.Valve opened.W/930708 Ltr ML20045G8661993-07-0808 July 1993 LER 93-004-00:on 930611,reactor Tripped Due to Turbine Trip Resulting from Inadequate Procedure.Procedure Changes Made to Open Appropriate FW Heater High Level Dump Valves During Plant startup.W/930708 Ltr ML20045E7361993-06-29029 June 1993 LER 93-002-01:on 930205,software Vendor Discovered Error in User Manual for Updating Basss data-input Library.Caused by Failure of QA Procedures to Require Independent Review of User Manuals.Manual Surveillances performed.W/930629 Ltr ML20029B1261991-02-28028 February 1991 LER 91-001-00:on 910129,tubing in Air Start Sys for Emergency Diesel Generator Failed During Seismic Event. Caused by Error in Design of EDG Air Start Sys.Permanent Mod to Sys installed.W/910228 Ltr ML20028H8011991-01-24024 January 1991 LER 90-002-01:on 900116,determined That 891211 Reconstitution of More than One Spent Fuel Assembly Per Time in Violation of Fuel Handling Incident Safety Analysis. Caused by Deficient procedure.W/910124 Ltr ML20044A1861990-06-20020 June 1990 LER 87-002-01:on 861203,section of Thin Wall Found on Main Steam Line W/Readings Below Allowable Min of 0.95 Inches. Caused by Grinding of Edge of Pipe to Achieve Proper fit-up for Welding.Relief from IWB-3610 granted.W/900620 Ltr ML20043G1071990-06-13013 June 1990 LER 89-019-01:on 891128,determined That for Approx 10 Yrs, from 1979-1989,requirement to Lock HPSI Discharge Header Isolation Valves Shut Not Implemented.Caused by Inadequate Mgt Attention.Test Procedures modified.W/900613 Ltr ML20043F1221990-06-0404 June 1990 LER 90-017-00:on 900505,pin Hole Leak Observed in Discharge Piping of Saltwater Pump 13.Caused by Localized Corrosion. Leaking Spool Piece Removed & Blank Flange Installed. W/900604 Ltr ML20043A7871990-05-21021 May 1990 LER 90-016-00:on 900421,determined That Waste Gas Decay Tank (Wgdt) 13 Discharged Instead of (Wgdt) 11 for Discharge Permit Issued.Caused by Inadequate Communications.Training Performed for Operators Re event.W/900521 Ltr ML20043A3441990-05-14014 May 1990 LER 90-014-00:on 900413 & 19,unit Entered Tech Spec Limiting Condition of Operation 3.0.3 Due to Potential Inoperability of Three Out of Four Reactor Protection Sys Delta T Power Channels.Caused by Lack of Procedure guidance.W/900514 Ltr ML20043A3401990-05-14014 May 1990 LER 90-013-00:on 900413,determined That Axial Shape Index Channels Out of Spec & Inoperable.Caused by Inadequate Understanding of Design Basis for Excore/Incore Comparison. Design Basis for Excore/Incore improved.W/900514 Ltr ML20042G4521990-05-0707 May 1990 LER 90-015-00:on 900407,discovered That Relay Contact Which Actuates Reactor Trip Breaker Shunt Trip Not Adequately Functionally Tested.Caused by Failure to Examine Circuit in Detail When Test developed.W/900507 Ltr ML20042F5801990-05-0404 May 1990 LER 90-012-00:on 900406,identified That Procedure for LOCA Would Not Ensure post-LOCA Core Flush Would Be Initiated in Time to Prevent Boron Precipitation.Caused by Personnel Error.Configuration Mgt Program strengthened.W/900504 Ltr ML20012E9931990-03-29029 March 1990 LER 90-008-00:on 900227,determined That Surveillance Procedure M-280-0 Did Not Include Steps to Fully Test Control Room Recorder for Hydrogen Analyzers.Caused by Personnel Error.Procedure Revised on 900308.W/900329 Ltr ML20012F0001990-03-28028 March 1990 LER 89-006-01:on 890508,containment Iodine Filters Outside Design Basis Due to Equipment Qualification.Recalculation of Total Integrated Radiation Dose to Cables for Filter Fans Demonstrated Cable qualified.W/900328 Ltr ML20012E9951990-03-28028 March 1990 LER 89-014-01:on 890723,determined That Salt Water Header Not Capable of Withstanding Seismic Event Intact.Caused by Inadequate Welding of Blind Spool Pieces in Pipe.Insp Revealed Spools Capable as installed.W/900328 Ltr ML20012E0101990-03-26026 March 1990 LER 90-009-00:on 900224,failure to Meet Action Requirement Re Tech Spec 3.7.12.Caused by Personnel Error.Cables Removed from Doorway in Charging Pump Room & Not Allowed to Be Placed in doorway.W/900326 Ltr ML20012C4971990-03-15015 March 1990 LER 90-007-00:on 900216,discovered That Supervised Circuits Associated W/Fire Detection Instruments Located in Reactor Coolant Pump Bays Not Been Included in Surveillance Test Procedure.Caused by Personnel error.W/900315 Ltr ML20012C4861990-03-12012 March 1990 LER 90-006-00:on 900209,determined That Four Fire Dampers Missing.Caused by Not Identifying Penetrations as Requiring Dampers When Fire Hazards Analysis of Plant Conducted.Hourly Fire Watch Continued.Missing Dampers installed.W/900312 Ltr ML20012B8991990-03-12012 March 1990 LER 89-023-01:on 891220,determined That Pipe Rupture in nonsafety-related Svc Water Subsystem Could Result in Rapid Draining of Subsystems That Serve Auxiliary Bldg.Task Force Formed to Determine Corrective actions.W/900312 Ltr ML20012B4221990-03-0606 March 1990 LER 89-012-01:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed.Caused by Procedural Deficiency.Procedures Revised to Include Valve & Surveillance Test Program Instruction revised.W/900306 Ltr ML20011F2701990-02-27027 February 1990 LER 90-001-01:on 900109,determined That Surveillance Tests Used to Perform Channel Calibr Tests for Acoustic Flow Monitoring Devices Inadequate.Caused by Personnel Error & Inadequate Procedures.Swapped Leads restored.W/900227 Ltr ML20011F2091990-02-27027 February 1990 LER 89-026-00:on 891128,determined That Particulate Levels in Samples Taken from Lower Third of Tanks Exceeded Allowable Limits.Caused by Inadequate Sampling Technique. Tanks Cleaned & Filled W/Clean fuel.W/900227 Ltr ML20006F8601990-02-22022 February 1990 LER 90-004-00:on 900123,discovered Fire Barrier Penetration Seal Open for Indeterminate Time W/O Performing Tech Spec 3.7.12.a Required Actions.Caused by Personnel Error. Temporary Fire Seal installed.W/900222 Ltr ML20006E0521990-02-0808 February 1990 LER 90-001-00:on 891221,discovered That Acoustic Indications for One PORV & One Safety Valve Were Reversed During Surveillance Test.Caused by Personnel Error.Swapped Leads Restored to Proper configuration.W/900208 Ltr ML20006B4801990-01-26026 January 1990 LER 89-022-00:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed,Violating Tech Specs.Caused by Procedural Deficiency.Surveillance Test Procedure Revised to Include Deleted valves.W/900126 Ltr ML19354D8931990-01-17017 January 1990 LER 89-024-00:on 891218,determined That Wires Which Connect Actuation Device Logic Relay Contacts to Remainder of Circuit Not Tested During Channel Calibr Test.Caused by Inadequate Test.Test Program Upgrade underway.W/900117 Ltr ML20005F1921990-01-10010 January 1990 LER 89-025-00:on 891208,Tech Spec Action Statement Entered When Ventilation Ducts Penetrating Fire Barrier Could Not Be Accessed to Determine If Fire Dampers Installed.On 891211, Fire Watch Missed.Caused by Personnel error.W/900110 Ltr ML20005E3971989-12-28028 December 1989 LER 89-019-00:on 891128,discovered That HPSI Discharge Header Isolation Valves Not Locked Shut When RCS in Water Solid Condition,Resulting in Operation Outside Design Basis. Procedure Revised to Require Valves closed.W/891228 Ltr ML19351A4551989-12-13013 December 1989 LER 89-020-00:on 891113,determined That Some Solenoid Valves & Valve Power Supplies for Saltwater Sys May Not Be Able to Perform Design Function After Design Basis Seismic Event. Cause Undetermined.Power Supplies upgraded.W/891213 Ltr ML20005D6611989-12-0606 December 1989 LER 89-018-00:on 891106,discovered That Many Air Operated Control Valves & piston-operated Dampers Which Utilize safety-related Air Accumulators Would Not Have Performed as Expected After Loss of air.W/891206 Ltr ML19325F3951989-11-10010 November 1989 LER 89-002-01:on 890228,discovered That Fire Barrier Penetration Inoperable & Action Statement Requirements Not Satisfied.Caused by Inadequate Administrative Controls. Penetration Returned to Operable status.W/891115 Ltr ML19325E8221989-11-0303 November 1989 LER 89-007-01:on 890505,evidence of Reactor Coolant Leakage from 120 Pressurizer Vessel Heater Penetrations Discovered. Caused by IGSCC of Inconel 600.All Penetrations Using J-welds & Inconel 600 Visually inspected.W/891103 Ltr ML19324B2511989-10-27027 October 1989 LER 89-012-01:on 890720,discovered That Master Solenoid to Switchgear Room Halon Sys Disconnected Since 890629.Caused by Personnel Error Resulting from Lack of Written Procedure. Procedure Revised to Apply Temporary mods.W/891027 Ltr ML19325C3281989-10-10010 October 1989 LER 89-016-00:on 890908,determined That as-found Condition of Resistance Temp Detectors Did Not Match Tested Configuration.Cause Not Stated.Subj Detectors Will Be Sealed,Per Environ Qualification requirements.W/891010 Ltr ML19325C3701989-10-0909 October 1989 LER 89-017-00:on 890907,determined That Discrepancy in Acceptance Criteria of Surveillance Test Procedure M-452-0 Resulted in Failure to Fully Comply W/Requirements of Tech Spec 3.9.12.Main Cause undetermined.W/891009 Ltr ML20024F3771983-08-25025 August 1983 LER 83-044/03L-0:on 830808,diesel Generator 12 Tripped on Low Jacket Cooling Water Pressure While Verifying Operability.Cause Not Stated.Coolant Jacket Vented & Large Amount of Air Found.No Evidence of leakage.W/830825 Ltr ML20024F5731983-08-25025 August 1983 LER 83-040/03L-0:on 830727,control Room Air Conditioner 11 Discovered W/Damaged Condenser Fan.Caused by Loose Set Screws Securing Fan in Position.Set Screws Restored. W/830825 Ltr ML20024E6761983-08-0404 August 1983 Updated LER 83-011/03X-1:on 830207,during Surveillance Testing ESFAS a Logic Sequencer Failed,Rendering Diesel Generator 12 Inoperable.Caused by Intermittent Operation of Module Test Push Button.Part replaced.W/830804 Ltr ML20024E1721983-07-14014 July 1983 Updated LER 81-015/03X-1:on 810226,sample Pump for Control Room Radiation Monitor Found Out of Svc,Rendering Automatic Recirculation of Control Room Ventilation Sys on High Radiation Inoperable.Caused by seizure.W/830714 Ltr ML20024D0071983-07-0808 July 1983 LER 83-035/03L-0:on 830610,during Normal Power Operation,Esf Actuation Sys Channel Zg Steam Generator Level Tripped. Caused by Failed Vitro Isolator Module.Module Replaced.W/ 830708 Ltr ML20024D0091983-07-0808 July 1983 LER 83-033/03L-0:on 830603,fire Detection Instrumentation in Containment Southeast Electrical Penetration Determined Inoperable.Repair Impossible Due to Inaccessability of Protecto wire.W/830708 Ltr ML20024B8231983-06-23023 June 1983 LER 83-029/03L-0:on 830524,during Normal Operation, Surveillance Testing Indicated Neither Spent Fuel Pool Exhaust Fans 11 or 12 Would Maintain Required Negative Pressure.Caused by Clogged HEPA filters.W/830623 Ltr ML20024C0141983-06-22022 June 1983 Updated LER 81-080/03X-1:on 811116,discovered Weep from Cracked Weld on Spent Fuel Cooling Pump Discharge Vent Line 12.Caused by Inadequate Support of Vent Line.Support Assembly installed.W/830622 Ltr ML20024A8881983-06-16016 June 1983 LER 83-032/03L-0:on 830523,containment Isolation Sys B Logic Module Would Not Actuate.Caused by Defective Vitro Labs Std Logic Module.Module Replaced.Failed Module Returned to Vitro Labs for Repair & testing.W/830616 Ltr 1999-08-23
[Table view] Category:RO)
MONTHYEARML17326A2011999-08-23023 August 1999 LER 99-004-00:on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With 990823 Ltr ML20029C7321994-04-22022 April 1994 LER 94-004-00:on 940221,discovered Corrosion of Three Nuts on One of Incor Instrumentation Reactor Vessel Head.Caused by Increase of Wet Boric Acid.Leaking Flanges Repaired.W/ 940422 Ltr ML20046B4731993-07-30030 July 1993 LER 93-005-00:on 930630,TS 3.0.3 Entered Due to Both Containment Spray Sys Inoperable.Replaced CCW Outlet Valve Actuator Connecting Link Assembly from Number 11 SDC Heat exchanger.W/930730 Ltr ML20046A4911993-07-22022 July 1993 LER 93-003-00:on 930625,SG Tripped Due to Low Water Level. Caused by Insufficient Feedwater Addition Due to Inadequate Communication.Reemphasis on Improved Communication Stressed. W/930722 Ltr ML20045G8611993-07-0909 July 1993 LER 93-003-00:on 930610,dual Unit Trip Occurred Due to Partial Loss of Offsite Power.Flashover Protection Relay for Breaker 552-61 Replaced & Training for Personnel W/ Access to Relays Will Be reinforced.W/930709 Ltr ML20045G7281993-07-0808 July 1993 LER 93-002-00:on 930608,inadvertent Arw Actuation Sys & RPS Actuations Experienced During Performance of Awf Sys Large Flow Surveillance Testing.Caused by Failure to Note Differential Pressure Condition.Valve opened.W/930708 Ltr ML20045G8661993-07-0808 July 1993 LER 93-004-00:on 930611,reactor Tripped Due to Turbine Trip Resulting from Inadequate Procedure.Procedure Changes Made to Open Appropriate FW Heater High Level Dump Valves During Plant startup.W/930708 Ltr ML20045E7361993-06-29029 June 1993 LER 93-002-01:on 930205,software Vendor Discovered Error in User Manual for Updating Basss data-input Library.Caused by Failure of QA Procedures to Require Independent Review of User Manuals.Manual Surveillances performed.W/930629 Ltr ML20029B1261991-02-28028 February 1991 LER 91-001-00:on 910129,tubing in Air Start Sys for Emergency Diesel Generator Failed During Seismic Event. Caused by Error in Design of EDG Air Start Sys.Permanent Mod to Sys installed.W/910228 Ltr ML20028H8011991-01-24024 January 1991 LER 90-002-01:on 900116,determined That 891211 Reconstitution of More than One Spent Fuel Assembly Per Time in Violation of Fuel Handling Incident Safety Analysis. Caused by Deficient procedure.W/910124 Ltr ML20044A1861990-06-20020 June 1990 LER 87-002-01:on 861203,section of Thin Wall Found on Main Steam Line W/Readings Below Allowable Min of 0.95 Inches. Caused by Grinding of Edge of Pipe to Achieve Proper fit-up for Welding.Relief from IWB-3610 granted.W/900620 Ltr ML20043G1071990-06-13013 June 1990 LER 89-019-01:on 891128,determined That for Approx 10 Yrs, from 1979-1989,requirement to Lock HPSI Discharge Header Isolation Valves Shut Not Implemented.Caused by Inadequate Mgt Attention.Test Procedures modified.W/900613 Ltr ML20043F1221990-06-0404 June 1990 LER 90-017-00:on 900505,pin Hole Leak Observed in Discharge Piping of Saltwater Pump 13.Caused by Localized Corrosion. Leaking Spool Piece Removed & Blank Flange Installed. W/900604 Ltr ML20043A7871990-05-21021 May 1990 LER 90-016-00:on 900421,determined That Waste Gas Decay Tank (Wgdt) 13 Discharged Instead of (Wgdt) 11 for Discharge Permit Issued.Caused by Inadequate Communications.Training Performed for Operators Re event.W/900521 Ltr ML20043A3441990-05-14014 May 1990 LER 90-014-00:on 900413 & 19,unit Entered Tech Spec Limiting Condition of Operation 3.0.3 Due to Potential Inoperability of Three Out of Four Reactor Protection Sys Delta T Power Channels.Caused by Lack of Procedure guidance.W/900514 Ltr ML20043A3401990-05-14014 May 1990 LER 90-013-00:on 900413,determined That Axial Shape Index Channels Out of Spec & Inoperable.Caused by Inadequate Understanding of Design Basis for Excore/Incore Comparison. Design Basis for Excore/Incore improved.W/900514 Ltr ML20042G4521990-05-0707 May 1990 LER 90-015-00:on 900407,discovered That Relay Contact Which Actuates Reactor Trip Breaker Shunt Trip Not Adequately Functionally Tested.Caused by Failure to Examine Circuit in Detail When Test developed.W/900507 Ltr ML20042F5801990-05-0404 May 1990 LER 90-012-00:on 900406,identified That Procedure for LOCA Would Not Ensure post-LOCA Core Flush Would Be Initiated in Time to Prevent Boron Precipitation.Caused by Personnel Error.Configuration Mgt Program strengthened.W/900504 Ltr ML20012E9931990-03-29029 March 1990 LER 90-008-00:on 900227,determined That Surveillance Procedure M-280-0 Did Not Include Steps to Fully Test Control Room Recorder for Hydrogen Analyzers.Caused by Personnel Error.Procedure Revised on 900308.W/900329 Ltr ML20012F0001990-03-28028 March 1990 LER 89-006-01:on 890508,containment Iodine Filters Outside Design Basis Due to Equipment Qualification.Recalculation of Total Integrated Radiation Dose to Cables for Filter Fans Demonstrated Cable qualified.W/900328 Ltr ML20012E9951990-03-28028 March 1990 LER 89-014-01:on 890723,determined That Salt Water Header Not Capable of Withstanding Seismic Event Intact.Caused by Inadequate Welding of Blind Spool Pieces in Pipe.Insp Revealed Spools Capable as installed.W/900328 Ltr ML20012E0101990-03-26026 March 1990 LER 90-009-00:on 900224,failure to Meet Action Requirement Re Tech Spec 3.7.12.Caused by Personnel Error.Cables Removed from Doorway in Charging Pump Room & Not Allowed to Be Placed in doorway.W/900326 Ltr ML20012C4971990-03-15015 March 1990 LER 90-007-00:on 900216,discovered That Supervised Circuits Associated W/Fire Detection Instruments Located in Reactor Coolant Pump Bays Not Been Included in Surveillance Test Procedure.Caused by Personnel error.W/900315 Ltr ML20012C4861990-03-12012 March 1990 LER 90-006-00:on 900209,determined That Four Fire Dampers Missing.Caused by Not Identifying Penetrations as Requiring Dampers When Fire Hazards Analysis of Plant Conducted.Hourly Fire Watch Continued.Missing Dampers installed.W/900312 Ltr ML20012B8991990-03-12012 March 1990 LER 89-023-01:on 891220,determined That Pipe Rupture in nonsafety-related Svc Water Subsystem Could Result in Rapid Draining of Subsystems That Serve Auxiliary Bldg.Task Force Formed to Determine Corrective actions.W/900312 Ltr ML20012B4221990-03-0606 March 1990 LER 89-012-01:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed.Caused by Procedural Deficiency.Procedures Revised to Include Valve & Surveillance Test Program Instruction revised.W/900306 Ltr ML20011F2701990-02-27027 February 1990 LER 90-001-01:on 900109,determined That Surveillance Tests Used to Perform Channel Calibr Tests for Acoustic Flow Monitoring Devices Inadequate.Caused by Personnel Error & Inadequate Procedures.Swapped Leads restored.W/900227 Ltr ML20011F2091990-02-27027 February 1990 LER 89-026-00:on 891128,determined That Particulate Levels in Samples Taken from Lower Third of Tanks Exceeded Allowable Limits.Caused by Inadequate Sampling Technique. Tanks Cleaned & Filled W/Clean fuel.W/900227 Ltr ML20006F8601990-02-22022 February 1990 LER 90-004-00:on 900123,discovered Fire Barrier Penetration Seal Open for Indeterminate Time W/O Performing Tech Spec 3.7.12.a Required Actions.Caused by Personnel Error. Temporary Fire Seal installed.W/900222 Ltr ML20006E0521990-02-0808 February 1990 LER 90-001-00:on 891221,discovered That Acoustic Indications for One PORV & One Safety Valve Were Reversed During Surveillance Test.Caused by Personnel Error.Swapped Leads Restored to Proper configuration.W/900208 Ltr ML20006B4801990-01-26026 January 1990 LER 89-022-00:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed,Violating Tech Specs.Caused by Procedural Deficiency.Surveillance Test Procedure Revised to Include Deleted valves.W/900126 Ltr ML19354D8931990-01-17017 January 1990 LER 89-024-00:on 891218,determined That Wires Which Connect Actuation Device Logic Relay Contacts to Remainder of Circuit Not Tested During Channel Calibr Test.Caused by Inadequate Test.Test Program Upgrade underway.W/900117 Ltr ML20005F1921990-01-10010 January 1990 LER 89-025-00:on 891208,Tech Spec Action Statement Entered When Ventilation Ducts Penetrating Fire Barrier Could Not Be Accessed to Determine If Fire Dampers Installed.On 891211, Fire Watch Missed.Caused by Personnel error.W/900110 Ltr ML20005E3971989-12-28028 December 1989 LER 89-019-00:on 891128,discovered That HPSI Discharge Header Isolation Valves Not Locked Shut When RCS in Water Solid Condition,Resulting in Operation Outside Design Basis. Procedure Revised to Require Valves closed.W/891228 Ltr ML19351A4551989-12-13013 December 1989 LER 89-020-00:on 891113,determined That Some Solenoid Valves & Valve Power Supplies for Saltwater Sys May Not Be Able to Perform Design Function After Design Basis Seismic Event. Cause Undetermined.Power Supplies upgraded.W/891213 Ltr ML20005D6611989-12-0606 December 1989 LER 89-018-00:on 891106,discovered That Many Air Operated Control Valves & piston-operated Dampers Which Utilize safety-related Air Accumulators Would Not Have Performed as Expected After Loss of air.W/891206 Ltr ML19325F3951989-11-10010 November 1989 LER 89-002-01:on 890228,discovered That Fire Barrier Penetration Inoperable & Action Statement Requirements Not Satisfied.Caused by Inadequate Administrative Controls. Penetration Returned to Operable status.W/891115 Ltr ML19325E8221989-11-0303 November 1989 LER 89-007-01:on 890505,evidence of Reactor Coolant Leakage from 120 Pressurizer Vessel Heater Penetrations Discovered. Caused by IGSCC of Inconel 600.All Penetrations Using J-welds & Inconel 600 Visually inspected.W/891103 Ltr ML19324B2511989-10-27027 October 1989 LER 89-012-01:on 890720,discovered That Master Solenoid to Switchgear Room Halon Sys Disconnected Since 890629.Caused by Personnel Error Resulting from Lack of Written Procedure. Procedure Revised to Apply Temporary mods.W/891027 Ltr ML19325C3281989-10-10010 October 1989 LER 89-016-00:on 890908,determined That as-found Condition of Resistance Temp Detectors Did Not Match Tested Configuration.Cause Not Stated.Subj Detectors Will Be Sealed,Per Environ Qualification requirements.W/891010 Ltr ML19325C3701989-10-0909 October 1989 LER 89-017-00:on 890907,determined That Discrepancy in Acceptance Criteria of Surveillance Test Procedure M-452-0 Resulted in Failure to Fully Comply W/Requirements of Tech Spec 3.9.12.Main Cause undetermined.W/891009 Ltr ML20024F3771983-08-25025 August 1983 LER 83-044/03L-0:on 830808,diesel Generator 12 Tripped on Low Jacket Cooling Water Pressure While Verifying Operability.Cause Not Stated.Coolant Jacket Vented & Large Amount of Air Found.No Evidence of leakage.W/830825 Ltr ML20024F5731983-08-25025 August 1983 LER 83-040/03L-0:on 830727,control Room Air Conditioner 11 Discovered W/Damaged Condenser Fan.Caused by Loose Set Screws Securing Fan in Position.Set Screws Restored. W/830825 Ltr ML20024E6761983-08-0404 August 1983 Updated LER 83-011/03X-1:on 830207,during Surveillance Testing ESFAS a Logic Sequencer Failed,Rendering Diesel Generator 12 Inoperable.Caused by Intermittent Operation of Module Test Push Button.Part replaced.W/830804 Ltr ML20024E1721983-07-14014 July 1983 Updated LER 81-015/03X-1:on 810226,sample Pump for Control Room Radiation Monitor Found Out of Svc,Rendering Automatic Recirculation of Control Room Ventilation Sys on High Radiation Inoperable.Caused by seizure.W/830714 Ltr ML20024D0071983-07-0808 July 1983 LER 83-035/03L-0:on 830610,during Normal Power Operation,Esf Actuation Sys Channel Zg Steam Generator Level Tripped. Caused by Failed Vitro Isolator Module.Module Replaced.W/ 830708 Ltr ML20024D0091983-07-0808 July 1983 LER 83-033/03L-0:on 830603,fire Detection Instrumentation in Containment Southeast Electrical Penetration Determined Inoperable.Repair Impossible Due to Inaccessability of Protecto wire.W/830708 Ltr ML20024B8231983-06-23023 June 1983 LER 83-029/03L-0:on 830524,during Normal Operation, Surveillance Testing Indicated Neither Spent Fuel Pool Exhaust Fans 11 or 12 Would Maintain Required Negative Pressure.Caused by Clogged HEPA filters.W/830623 Ltr ML20024C0141983-06-22022 June 1983 Updated LER 81-080/03X-1:on 811116,discovered Weep from Cracked Weld on Spent Fuel Cooling Pump Discharge Vent Line 12.Caused by Inadequate Support of Vent Line.Support Assembly installed.W/830622 Ltr ML20024A8881983-06-16016 June 1983 LER 83-032/03L-0:on 830523,containment Isolation Sys B Logic Module Would Not Actuate.Caused by Defective Vitro Labs Std Logic Module.Module Replaced.Failed Module Returned to Vitro Labs for Repair & testing.W/830616 Ltr 1999-08-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G6971999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Calvert Cliffs Npp,Units 1 & 2.With ML20216J8731999-09-10010 September 1999 Rev 52 to QA Policy for Calvert Cliffs Nuclear Power Plant ML20212A4441999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Ccnpp,Units 1 & 2. with ML17326A2011999-08-23023 August 1999 LER 99-004-00:on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With 990823 Ltr ML20210S6091999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ccnpp,Units 1 & 2. with ML20210N6001999-07-27027 July 1999 ISI Summary Rept for Calvert Cliffs Unit 2. Page 2 of 3 in Encl 1 of Incoming Submittal Not Included ML20210B7941999-07-15015 July 1999 SER Denying Licensee Request for Changes to Current Ts,Re Deletion of Tendon Surveillance Requirements for Calvert Cliffs LD-99-039, Part 21 Rept Re Defect of Abb 1200A 4kV Vacuum Breakers. Initially Reported on 990625.Defect Results in Breaker Failing to Remain in Closed Position.Root Cause Evaluation & Corrective Action Plan Being Developed.Licensee Notified1999-06-30030 June 1999 Part 21 Rept Re Defect of Abb 1200A 4kV Vacuum Breakers. Initially Reported on 990625.Defect Results in Breaker Failing to Remain in Closed Position.Root Cause Evaluation & Corrective Action Plan Being Developed.Licensee Notified ML20209F1721999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Calvert Cliffs Npp.With LD-99-035, Part 21 Rept Re Abb 1200A 4KV Vacuum Breakers Performing Trip Free Operation When Close Signal Received by Breaker. Defect Results in Breaker Failing to Remain in Closed Position.Root Cause & CAP Being Developed1999-06-25025 June 1999 Part 21 Rept Re Abb 1200A 4KV Vacuum Breakers Performing Trip Free Operation When Close Signal Received by Breaker. Defect Results in Breaker Failing to Remain in Closed Position.Root Cause & CAP Being Developed ML20196C6981999-06-21021 June 1999 Safety Evaluation Concluding That Use of ASME Section XI Code Including Summer 1983 Addenda as Interim Code for Third 10-year Insp Interval at Calvert Cliffs Units 1 & 2 Until Review of 1998 Code Completed,Would Be Acceptable ML20195K2811999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Ccnpp,Units 1 & 2. with ML20206R5871999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ccnpp,Units 1 & 2. with ML20195B3891999-04-30030 April 1999 0 to CENPD-279, Annual Rept on Abb CE ECCS Performance Evaluation Models ML20205N2951999-04-13013 April 1999 Special Rept:On 990314,fire Detection Sys Was Removed from Svc to Support Mod to Replace SRW Heat Exchangers in Unit 2 SRW Room During Unit 2 Refueling Outage.Contingency Measure 15.3.5.A.1 Will Continue Until Fire Detection Sys Restored ML20210T5211999-04-0101 April 1999 Rev 0 to Ccnpp COLR for Unit 2,Cycle 13 ML20205P5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20204H6471999-03-21021 March 1999 SER Re License Renewal of Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20207M8321999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Calvert Cliffs Nuclear Power Plant.With ML20203D4311999-02-0505 February 1999 Safety Evaluation Accepting Procedure Established for long-term Corrective Action Plan Related to Containment Vertical Tendons ML20199G4671999-01-20020 January 1999 SER Accepting USI A-46 Implementation for Plant ML20206Q3221999-01-11011 January 1999 Special Rept:On 981226,wide Range Noble Gas Effluent RM Was Removed from Operable Status.Caused by Failure of mid-range Checksource to Properly Reseat.Completed Maint & post-maint Testing & RM Was Returned to Operable Status on 990104 ML20207L0451999-01-0808 January 1999 Cost-Benefit Risk Analyses:Radwaste Sys for Light Water Reactors ML20199F4781999-01-0808 January 1999 Safety Evaluation Concluding That Bg&E Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves Susceptible to Pressure Locking.Concludes GL 95-07 Actions Were Addressed ML20198S7591999-01-0707 January 1999 SER Accepting Quality Assurance Program Description Change for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20207M2281998-12-31031 December 1998 1998 Annual Rept for Bg&E. with ML20199E2931998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Calvert Cliffs Npp. with ML20206R9911998-12-0808 December 1998 Rept of Changes,Tests & Experiments (10CFR50.59(b)(2)). with ML20198B2631998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20195H1001998-11-16016 November 1998 Safety Evaluation of First Containment Insp Interval Iwe/Iwl Program Alternative ML20196E2211998-10-31031 October 1998 Non-proprietary Rev 03-NP to CEN-633-NP, SG Tube Repair for Combustion Engineering Designed Plant with 3/4 - .048 Wall Inconel 600 Tubes Using Leak Limiting Alloy 800 Sleeves ML20195E5281998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Calvert Cliffs Nuclear Power Station,Units 1 & 2.With ML20154Q7191998-10-21021 October 1998 Special Rept:On 980923,unit 1 Wrngm Was Removed from Operable Status.Caused by Failure of Process Flow Transducer.Completed Maint to Remove Process Flow Transducer Input to Wrngm Microprocessor & Completed Formal Evaluation ML20154G3931998-10-0505 October 1998 Safety Evaluation Concluding That Flaw Tolerance Evaluation for Assumed Flaw in Inboard Instrument Weld of Pressurizer Meets Rules of ASME Code ML20154M5841998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Calvert Cliffs Nuclear Plant,Units 1 & 2.With ML20153C2571998-09-18018 September 1998 Special Rept:On 980830,wide Range Noble Gas Monitor (Wrngm) Channel Was Removed from Operable Status.Caused by Need to Support Performance of Required 18-month Channel Calibr.Will Return Wrngm to Operable Status by 980925 ML20153C1091998-09-18018 September 1998 Part 21 Rept Re Defective Capacity Control Valves.Trentec Personnel Have Been in Contact with Bg&E Personnel Re Condition & Have Requested Potentially Defective Valves ML20151U5441998-09-0404 September 1998 Bg&E ISI Summary Rept for Calvert Cliffs ML20151T5281998-09-0101 September 1998 Special Rept:On 980819,declared Rv Water Level Monitor Channel a Inoperable.Caused by Failure of Three Heated Junction Thermocouples (Sensors) in Lower Five Sensors. Channel a & B Rv Water Level Probes Will Be Replaced ML20151Y1191998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Calvert Cliffs Nuclear Power Plant Units 1 & 2.With ML20237D4981998-08-19019 August 1998 Safety Evaluation Accepting Licensee Request for Extension of Second ten-year Inservice Insp Interval ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20237B9371998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Calvert Cliffs Nuclear Power Plant ML20237D5941998-07-22022 July 1998 Rev 2 to Ccnpp COLR for Unit 2,Cycle 12 ML20236L7521998-07-0606 July 1998 Safety Evaluation Granting Bg&E 980527 Request for Relief from Requirement of Section IWA-5250 of ASME Code for Calvert Cliffs Unit 2.Alternatives Provide Reasonable Assurance of Operational Readiness ML20236F7791998-06-30030 June 1998 Safety Evaluation Authorizing Request for Temporary Relief from Requirement of Subsection IWA-5250 of ASME Code,Section XI for Plant,Unit 1 ML20236R0881998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20236X3101998-06-19019 June 1998 Rev 1 to Calvert Cliffs Nuclear Power Plant COLR for Unit 2,Cycle 12 ML20249A9571998-06-15015 June 1998 Special Rept:On 980430,fire Detection Sys Was Removed from Svc to Support Mod to Purge Air Sys 27-foot Elevation & 5-foot Elevation East Piping Penetration Rooms.Installed Temporary Alteration & Returned Fire Detection Sys to Svc ML20249A7711998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Ccnpp,Units 1 & 2 1999-09-30
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B A LTIMORE
. GAS AND ELECTRIC <
l CALVERT CLIFFS NUCLEAR POWER PLANT 1650 CALVERT CLIFFS PARKWAY
- LUSBY, MARYLAND 20657-4702 j CHARLES H CAUSE PLANT GENERAL MANAGER cAtvEntcurrs July 8, 1993 U.S. Nuclear Regulatory Commission Washington, D.C. 20555 ATTENTION: Document Control Desk
SUBJECT:
Calvert Cliffs Nuclear Power Plant Unit No. 1; Docket No. 50-317; License No. DPR 53 Licensee Event Report 93-004 Reactor Trip Due to Turbine Trip Resulting from Inadequate Procedure The attached report is being sent to you as required under 10 CFR 50.73 guidelines. Should you have any questions regarding this report, we will be pleased to discuss them with you.
Very truly yours, ,
, X CHC/JV/bj d Attachment cc: D. A. Brune, Esquire J. E. Silberg, Esquire R. A. Capra, NRC D. G. Mcdonald, Jr. , NRC T. T. Martin, NRC P. R. Wilson, NRC R. I. McLean, DNR J. H. Valter, PSC Director, Office of Management Information and Progra,a Control l
140047 l 9307160085 930708 "'l
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PDR ADDCK 05000317 w l )
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NRC FORM 368 U S. NUCLEAR REGULATORY COMMISSION .
- 2) ESTEMTED BURDEN PER RESPONSE TO COMPLYWITH THIS INFORMATION i
- CXX. LECT)ON REQUEST. 50.0 HHS. FORWARD COMMENTS RECADDtNG suf 0EN ESTIMATE TO TPE INFORMADoN AND RECOFOS MAtAGEMENT LICENSEE EVENT REPORT (LER) DR/4CH (MND87714). U S. NUCLEAR RECULATORY COMMtSSON.
WASHINGTOR DC 2MHX01. ANoToTHE PAPERWOfM REDUCTION P50)ECT (See reverse for reouired number of rficits/ characters for each blocky 01500104). OFFCE OF MAtAGEMENT AND DVDGET,WASHJNGTCM DC 2@0:L ;
F ACILIW NAME (1) DOCKET NUMBER (2) PAGE (3) <
Calvert Clif f s, Unit 1 05000 317 1 OF 05 !
TITLE (4) L Reactor Trip Due to Turbine Trip Resulting From inadequate Procedure EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) oTHER F AC:llTIES INVOLVED (B)
S EQUENTIAL REVISION I MONTH DAY YEAR YEAR M ONTH DAY YEAR NUMBER NUMBER >
06 11 93 93 - 004 -
00 07 08 93 05000 OPERATING THIS AEPORT IS SUBurTTED PURSUANT To THE DECUtREMENTS OF 10 CFR MChaci< one or mnre) (11)
MODE (9)
I 20.402 M 20 405.c) l )( 50.73(a)(2)(iv) 73 71(b) ,
, 20 405(a)(1)(i) 50.36(c)(1) 50.73(a)(2)(v) 73.73 gc3 LEVEL 16 20 405(aH1)60 50.36(c)(2) 50.73(a)(2)(vii)
- 00) 20.405(aH1)6ii) 50.73(a)(2)(0 50.73(a)(2)(viii)(A) - (Srecdy in Abstract below and in Ted NRC Fonn 366A) 20.405(aH1)(iv) 50.73 a)(2)(ii) 50 73(a)(2)(viiO(B) 20.405(a)(1)M J 50.73(a)(2)(iii) 50 73(a)O(x)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER (include Area Code) j John Volkoff, Compliance Engineer 410-260-3649 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 113) i EMABLE TO ##
CAUSE SYSTEM CO M PONENT CAUSE SYSTEM COMPC NENT TURER NPRDS TURER NPRDS i i l SUPPLEMENTAL REPCRT EXPECTED (14) EXPECTED MONTH t DAY l YEAR 1 SUBMISSION YES X No l af ves comowe EYPECTED SUBMISSION DATE) DATE (15) l >
ABSTRAC T (urmt to 1400 spaces. Le . apprommately15 single-space typewntten knes) (16)
On June 11, 1993, Unit 1 tripped due to an automatic wtuation of the Reactor Protection System (RPS). An RPS loss of load si pal was generated when the turbine tripped due to a low pressure feedwater heater (F'a) high level turbine trip signal. The signal was generaced because the Fa high level dump -l (HLD) valve handswitch was left Closed during startup. The unit was au <
16 percent power. ,
A Cause of the event was that opening the WH HLD valves for plant startup was not adequately proceduralited. One Contributing factor was that one operating i crew questioned the valves position but did not effectively follow-up on the j question or pass it along to the next Crew who did not detect the improper handswitCh positions. Procedure Changes were made to open the appropriate F'a HLD valves during plant startup. The design of the WH high and high-high l l
level alarm Circuits was reviewed. Reactor trip and normal shutdown j procedures and valve lineups will be reviewed for similar valve position j i problems. Troubleshooting of the Fa water level alarm Circuits will be l performed.
i I i W 6n.nWs l
l NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 315o 0104 l
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> EXPIRES 5/31/95 l CSTtMATED BURoEN PER RESPONSE To COMPLY WffN THIS INFoRMATCN CoLLEcTON REoVEST; 50 0 HRS. FoRW ARo l LICENSEE EVENT REPORT (LER) couuENTs eccARoiNo euRoEN EsT: MATE to THE iuFoRuATCN ANo RE0oPoS MANAoEMENT BRANCH lMNB8 7714), U.S NUCLEAR TEXT CONTINUATION RoutATcRv couuissCN. wAsHacToN. oc rosas.ooot. Ano To THE PAPERWORK REoVCTCN PROJECT (3150 o104), oFFCE oF 'l MANAGEMENT ANo BUoGET, WASHWGToN. oc 20503 F ACIUTY MAME (1) DOCKET NUMBER (2) LER NUMSER (3) PAGE (4)
Calvert Cliffs, Unit 1 05000 3 1 7 93 -
004 - 00 02 0F 05 TEXT or . .u. w.a = .amo= c . or NRc F.mi sesAi (173 I. DESCRIPTION OF EVENT ,
1 At 12:59 p.m. on June 11, 1993, the Unit 1 reactor tripped due to an automatic actuation of the Reactor Protection System (RPS). An RPS loss of load signal -
was generated when the Unit 1 Turbine tripped due to a 12C low pressure i feedwater heater (SH) high level turbine trip signal. The signal was generated ;
because the 12C FkH high level dump (HLD) valve handswitch was left closed during a Unit 1 startup, allowing a high water level in the FAM. At the time, l Unit 1 was at 16 percent power (MODE 1). ,
l Feedwater heaters use steam extracted from various stages of low and high I pressure turbines to preheat feedwater. Unit 1 has six FkH stages, 11 - 16. i Stage 12 has three parallel F4Hs located inside the condenser, 12A, 12B and 12C. l During normal power operation, the condensed extraction steam that collects in j the F'JHs is drained in a controlled manner to prevent the FbHs from completely I flooding or draining. DHs 12A, 123 and 12C each a have a HLD valve and contain two float switches, high and high-high level. The high level float ';
switch has two contacts, one that initiates a high level alarm on the Control Room (CR) feedwater panel and opens the 53 HLD valves, the othe? is the first ,
i of two contacts for a turbine trip signal. The high-high level float switch also has two contacts , one that initiates a plant computer high-high level alarm, the other is the second of the two contacts for a turbine trip signal. 1 The turbine trip is to protect the turbine from an overspeed condition, klien '
both turbine trip contacts are closed, a turbine trip signal is generated. The circuit has a 1.5 second time delay to prevent float chattering from causing a turbine trip.
k~ hen the plant is at a low power level, WM pressures fluctuate with steam flow changes. As FbH pressure changes, liquid flashes to steam in the FbH and causes i the float level to chatter. To preclude an inadvertent turbine trip signal generated by pressure surges from flashing liquid, the DH HLD valves are lef t l open during plant startup. The FbH HLD valves are controlled by handswitches from the feedwater panel in the CR.
Operating Procedure (OP)-2, " Plant Startup from Hot Standby to Minimum Load," l Attachment (2), Checklist (Reactor Trip Recovery), requires checking initial l conditions for turbine startup per Operating Instruction (01)-43A, " Main Turbine and Generator / Exciter Operation Unit 1." One of the initial conditions for 01-43A is that FbH vents and drains are aligned per OI-8B. "Feedwater Heater Vents and Drains." OI-8B Attachment (1), a valve lineup for the Feedwater ,
Heater Vents and Drains, sho1s the difference between ene startup (OPEN) and 1 l
1
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's4 NRC FORM 366A . U.S. NUCLEAR REGULATORY COMMISSION AFPROVED BY OMB NO. 315o-0104 ,
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EsTuATEo BURDEN PER RESPONSE To COMP (Y WTH TH,9 )
McAuATION CoLLECTCN REQUEST: 50 0 MFG FoRWAAo l
LICENSEE EVENT REPORT (LER) couuEuTs neoAsowa sunoEN EsTuATE To TsE wosu . Tion mo arconos umAcEuENT enmemuNas n14. U S. NUCLEAn l nEcut4 Tony couwssCN. wAsn NoToN. oc moss 3.oooi, wo To j TEXT CONTINUATION THE P APEAwbnK REDUCTCN pro. JECT c3150-0104). of FiCE of l MANAoEuCNT ANo SuoGET. WASHINGTON, oc 20503. !
l F AcruTv NAuf m ooexET uuusEn ca (En muuaEn <st Pace tai Calvert Cliffs, Unit 1 05000 3 1 7 93 -- 004 - 00 03 0F 05 TEXT Of mom space e requewa. use addet:onal copes of NPC Form 366A) (17) normal operating (SHUT) positions for the AT HLD valves, but OI-43A does not specifically refer to Attachment (1) of 01-83.
On the morning of June 11, 1993, preparations were being made for a Unit 1 startup af ter tripping the day before (see LERs 317/93-03 and 318/93-03). The Unit 1 Reactor Operator (RO) was_ tasked with completing OP-2 Attachment (2) for Unit 1. The Control Room Operator (CRO) coordinated various activities related to Unit 1. A Senior Reactor Operator (SRO) was dedicated to Unit 1 startup.
The SRO reported to the R0 that SH vents and drains were arranged per OI-8B '
after he checked the initial conditions, in 01-8B,Section II, Startup (Normal).
The RO signed off step 5 of the OP-2 checklist. Indicating that the initial conditions of OI-43A were met, including the 01-8B conditions.
Later during startup preparations, the SRO noted that the SH HLD valve handswitches on the feedwater panel in the CR were in the shut position. He questioned this condition, knew they should be OPEN during the startup and ;
discussed with the RO whether the valves should be opened. The SRO reviewed procedure steps he had completed, found no step placing the WH HLD valve handswitches in the OPEN position, and thought a later step in the startup '
procedures would OPEN the WH HLD valves prior to increasing power.
Independently, the CR0 cycled the n'H HLD valves per OP-2 step C.5 open and then shut. The OP-2 step does not specify valve position only to cycle the valves.
The CR0 thought that SH relief valve work going on required the valves to '
remain shut after cycling.
The operators on the shift brought the reactor critical just prior to the '
June 11 shift turnover. The next shift did not detect that the WH HLD valves were shut and should be open. Unit 1 reached 16 percent power at 12:53.
Approximately one minute before the trip, the plant computer received four 12B '
WH high-high level alarms, each lasting approximately 2-2.5 seconds and resetting prior to tripping the turbine. The signals were_ listed on the plant computer alarm list. The plant computer alarm list is not routinely monitored '
because it is the secondary source of alarms for the operators. These were four i of 63 plant computer alarms listed during the minute at 12:58. No high level alarms were observed on the feedwater control panel in the CR.
At 12:59, a 12C RH high-high level signal lasted for 2.4 seconds, meeting conditions for initiating a turbine trip and the subsequent RPS trip.
Appropriate actions were taken for the plant trip. ,
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9 NRC FORM 366A . U.S. NUCLEAR REGULATORY COMMISSION . APPROVED BY OMB NO. 3150-0104
- 5.sa - EXPfRES 5/31/95 l EST MATED BURDEN PER RESPONSE To COMPLY WITH THIS INFORMAT1oN COLLECT 1oN REQUEST
- 50 0 NFG. FoRWARo LICENSEE EVENT REPORT (LER) ceMuENTs RecARoma suRcEN EsnMATE To THE MoRMATloN AND PECoRDS MANAGEMENT BRANCH (MNBS 7714). U.S. NUCLEAR TEXT CONTINUATION REauuTORY CoMMISSloN. WASHfNGToN. oC 20555-0001. ANo TO THE PAPERWoR4 REDUCTION PROJECT p1So-0104L OFFICE OF MANAGEMENT ANo BUDGET, WASHINGTON, DC 20503.
F ACIUTY NAME (1) DOCKET NUMBER (2) LER NUMBER (3) PAGE H) t Calvert Cliffs, Unit 1 05000 3 1 7 93 - 004 - 00 04 0F 05 f TEXT [N more scace is required, use addibonal copies of NRC Form 366A) tt 7)
II. CAUSE OF EVENT l t
A cause of the event was that opening the F.H HLD valves for plant startup was not adequately proceduralized. Operators were aware that the FaH HLD valves needed to be open for startup, but thought the procedures would open them at the appropriate time. OI-43A did not direct the operators to verify the feedwater '
va.ve lineup, Attachment (1) in 01-8B, and no other procedural steps opened the FH HLD valves for unit startup.
4 A contributing factor was that on-shift personnel preparing the unit for startup !
questioned why the AH HLD handswitches were not open but did not pursue where in the procedure the valves should be opened.. They assumed the valves would be opened later in the procedure and therefore did not convey this question to the oncoming shift. Additionally, the oncoming crew did not detect the handswitches were out of position during shift turnover or. subsequent activities.
If the FJH high level alarms on the feedwater panel in the CR had alarmed before the trip, they might have alerted the operators to the fact that .the AH HLD valve handswitches were in the SHUT position in time to prevent th'e trip.
However, during Unit startup, when flashing in the P.Hs is more likely to cause spurious alarms than during normal operations, such trips are prevented'by opening the SH HLD valves as a routine part of the startup.
III. ANALYSIS OF EVENT The event is reportable under 10 CFR 50.73(a)(2)(iv), as a condition that <
resulted in an automatic RPS actuation. The reactor tripped as designed for a loss of load trip. All protective systems performed as expected and operators performed their tasks correctly and interpreted indications properly. The turbine trip signal from the 12C F H was probably generated by liquid flashing to steam in the F.3 during startup. The 123 F.H high-high level alarms may have occurred due to localized steam flashing causing the high-high level float to close its contacts, while the high level float did not experience simultaneous ;
flashing, resulting in no plant trip. It is unclear why no high level alarm was observed for 12C FwH and the turbine trip signal was still generated. The-turbine trip signal protects the turbine, not the reactor. The loss of load reactor trip performed properly. There were no significant safety consequences as a result of this event.
IV. CORRECTIVE ACTIONS Appropriate actions were taken for the plant trip.
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1 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 31So-oto4 I NRC FORM 366A .*
cs.ea .
EXPIRES 5/31/95 ESTNATED BURoEN PER RESPONSE To COMPLY Wf7H THis INFoRMATON CoLLECTON REcuEST: So.0 HRS. FoRWARo LICENSEE EVENT REPORT (LER) CoMuENTs REGARo.NG euRoEN EsruATE To twE woRMATON ANo RECoRoS MANAGEMENT BRANCH (MNDO 77ial, U $. NUCLEAR TEXT CONTINUATION REOULAToRY CoMMISSON. WASHINGTON, DC 20$55{C01, ANo To THE PAPERWORK REoUCTON PRCUECT pt50-0104h OFFICE CF MANAGEMENT AND BUoGET, WASHINGTON, oC 20503.
F ACluTY NAME (1) DOCKET NUMBER (a LER NUMBER (3) PAGE (4)
Calvert Cliffs, Unit 1 05000 3 1 7 93 -
004 -
00 05 0F.05 ]
TEXT g , . ,. . o. .amooco. .f NRC F.,. seaAi it7) i Procedure changes were made to open the appropriate F%H HLD valves during plant startup.
We understand that procedures are not the only barrier to ensure event free ;
operation. We expect operators to pay careful attention to detail while i performing tasks. The General Supervisor-Nuclear Plant operations has recently reemphasi::ed these expectations via his daily Notes and Instructions to the crews.
Reactoe trip and normal shutdown procedures and valve lineups will be reviewed for tr: p-sensitive valves lef t in a post-trip or shutdown position different ;
from the required startup position. .
We evaluated the design of the 12 F%H high and high-high level alarm circuits i and found them to be appropriate for their intended function. This evaluation identified no explanation why the high level alarm was not observed for the 12C !
F%H high level condition.
Troubleshootingofthe12FWHhighandh2gh-highlevelalarmcircuitswillbe performed to try to determine why the turbine trip occurred without receiving ,
F.H high level alarms. l l
V. ADDITIONAL INFORMATION ,
A. Affected Component Identification EIIS EIIS f Component Funct Code System Code FWH HLD valve LSV SJ
- 3. Previous Similar Events There have been three previous events involving plant trips related to the P.H HLD valves, but the previous causes were unrelated to ;
this event. They were documented in Unit 1 LERs85-011, 85-012. and 88-005.
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