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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17326A2011999-08-23023 August 1999 LER 99-004-00:on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With 990823 Ltr ML20029C7321994-04-22022 April 1994 LER 94-004-00:on 940221,discovered Corrosion of Three Nuts on One of Incor Instrumentation Reactor Vessel Head.Caused by Increase of Wet Boric Acid.Leaking Flanges Repaired.W/ 940422 Ltr ML20046B4731993-07-30030 July 1993 LER 93-005-00:on 930630,TS 3.0.3 Entered Due to Both Containment Spray Sys Inoperable.Replaced CCW Outlet Valve Actuator Connecting Link Assembly from Number 11 SDC Heat exchanger.W/930730 Ltr ML20046A4911993-07-22022 July 1993 LER 93-003-00:on 930625,SG Tripped Due to Low Water Level. Caused by Insufficient Feedwater Addition Due to Inadequate Communication.Reemphasis on Improved Communication Stressed. W/930722 Ltr ML20045G8611993-07-0909 July 1993 LER 93-003-00:on 930610,dual Unit Trip Occurred Due to Partial Loss of Offsite Power.Flashover Protection Relay for Breaker 552-61 Replaced & Training for Personnel W/ Access to Relays Will Be reinforced.W/930709 Ltr ML20045G7281993-07-0808 July 1993 LER 93-002-00:on 930608,inadvertent Arw Actuation Sys & RPS Actuations Experienced During Performance of Awf Sys Large Flow Surveillance Testing.Caused by Failure to Note Differential Pressure Condition.Valve opened.W/930708 Ltr ML20045G8661993-07-0808 July 1993 LER 93-004-00:on 930611,reactor Tripped Due to Turbine Trip Resulting from Inadequate Procedure.Procedure Changes Made to Open Appropriate FW Heater High Level Dump Valves During Plant startup.W/930708 Ltr ML20045E7361993-06-29029 June 1993 LER 93-002-01:on 930205,software Vendor Discovered Error in User Manual for Updating Basss data-input Library.Caused by Failure of QA Procedures to Require Independent Review of User Manuals.Manual Surveillances performed.W/930629 Ltr ML20029B1261991-02-28028 February 1991 LER 91-001-00:on 910129,tubing in Air Start Sys for Emergency Diesel Generator Failed During Seismic Event. Caused by Error in Design of EDG Air Start Sys.Permanent Mod to Sys installed.W/910228 Ltr ML20028H8011991-01-24024 January 1991 LER 90-002-01:on 900116,determined That 891211 Reconstitution of More than One Spent Fuel Assembly Per Time in Violation of Fuel Handling Incident Safety Analysis. Caused by Deficient procedure.W/910124 Ltr ML20044A1861990-06-20020 June 1990 LER 87-002-01:on 861203,section of Thin Wall Found on Main Steam Line W/Readings Below Allowable Min of 0.95 Inches. Caused by Grinding of Edge of Pipe to Achieve Proper fit-up for Welding.Relief from IWB-3610 granted.W/900620 Ltr ML20043G1071990-06-13013 June 1990 LER 89-019-01:on 891128,determined That for Approx 10 Yrs, from 1979-1989,requirement to Lock HPSI Discharge Header Isolation Valves Shut Not Implemented.Caused by Inadequate Mgt Attention.Test Procedures modified.W/900613 Ltr ML20043F1221990-06-0404 June 1990 LER 90-017-00:on 900505,pin Hole Leak Observed in Discharge Piping of Saltwater Pump 13.Caused by Localized Corrosion. Leaking Spool Piece Removed & Blank Flange Installed. W/900604 Ltr ML20043A7871990-05-21021 May 1990 LER 90-016-00:on 900421,determined That Waste Gas Decay Tank (Wgdt) 13 Discharged Instead of (Wgdt) 11 for Discharge Permit Issued.Caused by Inadequate Communications.Training Performed for Operators Re event.W/900521 Ltr ML20043A3441990-05-14014 May 1990 LER 90-014-00:on 900413 & 19,unit Entered Tech Spec Limiting Condition of Operation 3.0.3 Due to Potential Inoperability of Three Out of Four Reactor Protection Sys Delta T Power Channels.Caused by Lack of Procedure guidance.W/900514 Ltr ML20043A3401990-05-14014 May 1990 LER 90-013-00:on 900413,determined That Axial Shape Index Channels Out of Spec & Inoperable.Caused by Inadequate Understanding of Design Basis for Excore/Incore Comparison. Design Basis for Excore/Incore improved.W/900514 Ltr ML20042G4521990-05-0707 May 1990 LER 90-015-00:on 900407,discovered That Relay Contact Which Actuates Reactor Trip Breaker Shunt Trip Not Adequately Functionally Tested.Caused by Failure to Examine Circuit in Detail When Test developed.W/900507 Ltr ML20042F5801990-05-0404 May 1990 LER 90-012-00:on 900406,identified That Procedure for LOCA Would Not Ensure post-LOCA Core Flush Would Be Initiated in Time to Prevent Boron Precipitation.Caused by Personnel Error.Configuration Mgt Program strengthened.W/900504 Ltr ML20012E9931990-03-29029 March 1990 LER 90-008-00:on 900227,determined That Surveillance Procedure M-280-0 Did Not Include Steps to Fully Test Control Room Recorder for Hydrogen Analyzers.Caused by Personnel Error.Procedure Revised on 900308.W/900329 Ltr ML20012F0001990-03-28028 March 1990 LER 89-006-01:on 890508,containment Iodine Filters Outside Design Basis Due to Equipment Qualification.Recalculation of Total Integrated Radiation Dose to Cables for Filter Fans Demonstrated Cable qualified.W/900328 Ltr ML20012E9951990-03-28028 March 1990 LER 89-014-01:on 890723,determined That Salt Water Header Not Capable of Withstanding Seismic Event Intact.Caused by Inadequate Welding of Blind Spool Pieces in Pipe.Insp Revealed Spools Capable as installed.W/900328 Ltr ML20012E0101990-03-26026 March 1990 LER 90-009-00:on 900224,failure to Meet Action Requirement Re Tech Spec 3.7.12.Caused by Personnel Error.Cables Removed from Doorway in Charging Pump Room & Not Allowed to Be Placed in doorway.W/900326 Ltr ML20012C4971990-03-15015 March 1990 LER 90-007-00:on 900216,discovered That Supervised Circuits Associated W/Fire Detection Instruments Located in Reactor Coolant Pump Bays Not Been Included in Surveillance Test Procedure.Caused by Personnel error.W/900315 Ltr ML20012C4861990-03-12012 March 1990 LER 90-006-00:on 900209,determined That Four Fire Dampers Missing.Caused by Not Identifying Penetrations as Requiring Dampers When Fire Hazards Analysis of Plant Conducted.Hourly Fire Watch Continued.Missing Dampers installed.W/900312 Ltr ML20012B8991990-03-12012 March 1990 LER 89-023-01:on 891220,determined That Pipe Rupture in nonsafety-related Svc Water Subsystem Could Result in Rapid Draining of Subsystems That Serve Auxiliary Bldg.Task Force Formed to Determine Corrective actions.W/900312 Ltr ML20012B4221990-03-0606 March 1990 LER 89-012-01:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed.Caused by Procedural Deficiency.Procedures Revised to Include Valve & Surveillance Test Program Instruction revised.W/900306 Ltr ML20011F2701990-02-27027 February 1990 LER 90-001-01:on 900109,determined That Surveillance Tests Used to Perform Channel Calibr Tests for Acoustic Flow Monitoring Devices Inadequate.Caused by Personnel Error & Inadequate Procedures.Swapped Leads restored.W/900227 Ltr ML20011F2091990-02-27027 February 1990 LER 89-026-00:on 891128,determined That Particulate Levels in Samples Taken from Lower Third of Tanks Exceeded Allowable Limits.Caused by Inadequate Sampling Technique. Tanks Cleaned & Filled W/Clean fuel.W/900227 Ltr ML20006F8601990-02-22022 February 1990 LER 90-004-00:on 900123,discovered Fire Barrier Penetration Seal Open for Indeterminate Time W/O Performing Tech Spec 3.7.12.a Required Actions.Caused by Personnel Error. Temporary Fire Seal installed.W/900222 Ltr ML20006E0521990-02-0808 February 1990 LER 90-001-00:on 891221,discovered That Acoustic Indications for One PORV & One Safety Valve Were Reversed During Surveillance Test.Caused by Personnel Error.Swapped Leads Restored to Proper configuration.W/900208 Ltr ML20006B4801990-01-26026 January 1990 LER 89-022-00:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed,Violating Tech Specs.Caused by Procedural Deficiency.Surveillance Test Procedure Revised to Include Deleted valves.W/900126 Ltr ML19354D8931990-01-17017 January 1990 LER 89-024-00:on 891218,determined That Wires Which Connect Actuation Device Logic Relay Contacts to Remainder of Circuit Not Tested During Channel Calibr Test.Caused by Inadequate Test.Test Program Upgrade underway.W/900117 Ltr ML20005F1921990-01-10010 January 1990 LER 89-025-00:on 891208,Tech Spec Action Statement Entered When Ventilation Ducts Penetrating Fire Barrier Could Not Be Accessed to Determine If Fire Dampers Installed.On 891211, Fire Watch Missed.Caused by Personnel error.W/900110 Ltr ML20005E3971989-12-28028 December 1989 LER 89-019-00:on 891128,discovered That HPSI Discharge Header Isolation Valves Not Locked Shut When RCS in Water Solid Condition,Resulting in Operation Outside Design Basis. Procedure Revised to Require Valves closed.W/891228 Ltr ML19351A4551989-12-13013 December 1989 LER 89-020-00:on 891113,determined That Some Solenoid Valves & Valve Power Supplies for Saltwater Sys May Not Be Able to Perform Design Function After Design Basis Seismic Event. Cause Undetermined.Power Supplies upgraded.W/891213 Ltr ML20005D6611989-12-0606 December 1989 LER 89-018-00:on 891106,discovered That Many Air Operated Control Valves & piston-operated Dampers Which Utilize safety-related Air Accumulators Would Not Have Performed as Expected After Loss of air.W/891206 Ltr ML19325F3951989-11-10010 November 1989 LER 89-002-01:on 890228,discovered That Fire Barrier Penetration Inoperable & Action Statement Requirements Not Satisfied.Caused by Inadequate Administrative Controls. Penetration Returned to Operable status.W/891115 Ltr ML19325E8221989-11-0303 November 1989 LER 89-007-01:on 890505,evidence of Reactor Coolant Leakage from 120 Pressurizer Vessel Heater Penetrations Discovered. Caused by IGSCC of Inconel 600.All Penetrations Using J-welds & Inconel 600 Visually inspected.W/891103 Ltr ML19324B2511989-10-27027 October 1989 LER 89-012-01:on 890720,discovered That Master Solenoid to Switchgear Room Halon Sys Disconnected Since 890629.Caused by Personnel Error Resulting from Lack of Written Procedure. Procedure Revised to Apply Temporary mods.W/891027 Ltr ML19325C3281989-10-10010 October 1989 LER 89-016-00:on 890908,determined That as-found Condition of Resistance Temp Detectors Did Not Match Tested Configuration.Cause Not Stated.Subj Detectors Will Be Sealed,Per Environ Qualification requirements.W/891010 Ltr ML19325C3701989-10-0909 October 1989 LER 89-017-00:on 890907,determined That Discrepancy in Acceptance Criteria of Surveillance Test Procedure M-452-0 Resulted in Failure to Fully Comply W/Requirements of Tech Spec 3.9.12.Main Cause undetermined.W/891009 Ltr ML20024F3771983-08-25025 August 1983 LER 83-044/03L-0:on 830808,diesel Generator 12 Tripped on Low Jacket Cooling Water Pressure While Verifying Operability.Cause Not Stated.Coolant Jacket Vented & Large Amount of Air Found.No Evidence of leakage.W/830825 Ltr ML20024F5731983-08-25025 August 1983 LER 83-040/03L-0:on 830727,control Room Air Conditioner 11 Discovered W/Damaged Condenser Fan.Caused by Loose Set Screws Securing Fan in Position.Set Screws Restored. W/830825 Ltr ML20024E6761983-08-0404 August 1983 Updated LER 83-011/03X-1:on 830207,during Surveillance Testing ESFAS a Logic Sequencer Failed,Rendering Diesel Generator 12 Inoperable.Caused by Intermittent Operation of Module Test Push Button.Part replaced.W/830804 Ltr ML20024E1721983-07-14014 July 1983 Updated LER 81-015/03X-1:on 810226,sample Pump for Control Room Radiation Monitor Found Out of Svc,Rendering Automatic Recirculation of Control Room Ventilation Sys on High Radiation Inoperable.Caused by seizure.W/830714 Ltr ML20024D0071983-07-0808 July 1983 LER 83-035/03L-0:on 830610,during Normal Power Operation,Esf Actuation Sys Channel Zg Steam Generator Level Tripped. Caused by Failed Vitro Isolator Module.Module Replaced.W/ 830708 Ltr ML20024D0091983-07-0808 July 1983 LER 83-033/03L-0:on 830603,fire Detection Instrumentation in Containment Southeast Electrical Penetration Determined Inoperable.Repair Impossible Due to Inaccessability of Protecto wire.W/830708 Ltr ML20024B8231983-06-23023 June 1983 LER 83-029/03L-0:on 830524,during Normal Operation, Surveillance Testing Indicated Neither Spent Fuel Pool Exhaust Fans 11 or 12 Would Maintain Required Negative Pressure.Caused by Clogged HEPA filters.W/830623 Ltr ML20024C0141983-06-22022 June 1983 Updated LER 81-080/03X-1:on 811116,discovered Weep from Cracked Weld on Spent Fuel Cooling Pump Discharge Vent Line 12.Caused by Inadequate Support of Vent Line.Support Assembly installed.W/830622 Ltr ML20024A8881983-06-16016 June 1983 LER 83-032/03L-0:on 830523,containment Isolation Sys B Logic Module Would Not Actuate.Caused by Defective Vitro Labs Std Logic Module.Module Replaced.Failed Module Returned to Vitro Labs for Repair & testing.W/830616 Ltr 1999-08-23
[Table view] Category:RO)
MONTHYEARML17326A2011999-08-23023 August 1999 LER 99-004-00:on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With 990823 Ltr ML20029C7321994-04-22022 April 1994 LER 94-004-00:on 940221,discovered Corrosion of Three Nuts on One of Incor Instrumentation Reactor Vessel Head.Caused by Increase of Wet Boric Acid.Leaking Flanges Repaired.W/ 940422 Ltr ML20046B4731993-07-30030 July 1993 LER 93-005-00:on 930630,TS 3.0.3 Entered Due to Both Containment Spray Sys Inoperable.Replaced CCW Outlet Valve Actuator Connecting Link Assembly from Number 11 SDC Heat exchanger.W/930730 Ltr ML20046A4911993-07-22022 July 1993 LER 93-003-00:on 930625,SG Tripped Due to Low Water Level. Caused by Insufficient Feedwater Addition Due to Inadequate Communication.Reemphasis on Improved Communication Stressed. W/930722 Ltr ML20045G8611993-07-0909 July 1993 LER 93-003-00:on 930610,dual Unit Trip Occurred Due to Partial Loss of Offsite Power.Flashover Protection Relay for Breaker 552-61 Replaced & Training for Personnel W/ Access to Relays Will Be reinforced.W/930709 Ltr ML20045G7281993-07-0808 July 1993 LER 93-002-00:on 930608,inadvertent Arw Actuation Sys & RPS Actuations Experienced During Performance of Awf Sys Large Flow Surveillance Testing.Caused by Failure to Note Differential Pressure Condition.Valve opened.W/930708 Ltr ML20045G8661993-07-0808 July 1993 LER 93-004-00:on 930611,reactor Tripped Due to Turbine Trip Resulting from Inadequate Procedure.Procedure Changes Made to Open Appropriate FW Heater High Level Dump Valves During Plant startup.W/930708 Ltr ML20045E7361993-06-29029 June 1993 LER 93-002-01:on 930205,software Vendor Discovered Error in User Manual for Updating Basss data-input Library.Caused by Failure of QA Procedures to Require Independent Review of User Manuals.Manual Surveillances performed.W/930629 Ltr ML20029B1261991-02-28028 February 1991 LER 91-001-00:on 910129,tubing in Air Start Sys for Emergency Diesel Generator Failed During Seismic Event. Caused by Error in Design of EDG Air Start Sys.Permanent Mod to Sys installed.W/910228 Ltr ML20028H8011991-01-24024 January 1991 LER 90-002-01:on 900116,determined That 891211 Reconstitution of More than One Spent Fuel Assembly Per Time in Violation of Fuel Handling Incident Safety Analysis. Caused by Deficient procedure.W/910124 Ltr ML20044A1861990-06-20020 June 1990 LER 87-002-01:on 861203,section of Thin Wall Found on Main Steam Line W/Readings Below Allowable Min of 0.95 Inches. Caused by Grinding of Edge of Pipe to Achieve Proper fit-up for Welding.Relief from IWB-3610 granted.W/900620 Ltr ML20043G1071990-06-13013 June 1990 LER 89-019-01:on 891128,determined That for Approx 10 Yrs, from 1979-1989,requirement to Lock HPSI Discharge Header Isolation Valves Shut Not Implemented.Caused by Inadequate Mgt Attention.Test Procedures modified.W/900613 Ltr ML20043F1221990-06-0404 June 1990 LER 90-017-00:on 900505,pin Hole Leak Observed in Discharge Piping of Saltwater Pump 13.Caused by Localized Corrosion. Leaking Spool Piece Removed & Blank Flange Installed. W/900604 Ltr ML20043A7871990-05-21021 May 1990 LER 90-016-00:on 900421,determined That Waste Gas Decay Tank (Wgdt) 13 Discharged Instead of (Wgdt) 11 for Discharge Permit Issued.Caused by Inadequate Communications.Training Performed for Operators Re event.W/900521 Ltr ML20043A3441990-05-14014 May 1990 LER 90-014-00:on 900413 & 19,unit Entered Tech Spec Limiting Condition of Operation 3.0.3 Due to Potential Inoperability of Three Out of Four Reactor Protection Sys Delta T Power Channels.Caused by Lack of Procedure guidance.W/900514 Ltr ML20043A3401990-05-14014 May 1990 LER 90-013-00:on 900413,determined That Axial Shape Index Channels Out of Spec & Inoperable.Caused by Inadequate Understanding of Design Basis for Excore/Incore Comparison. Design Basis for Excore/Incore improved.W/900514 Ltr ML20042G4521990-05-0707 May 1990 LER 90-015-00:on 900407,discovered That Relay Contact Which Actuates Reactor Trip Breaker Shunt Trip Not Adequately Functionally Tested.Caused by Failure to Examine Circuit in Detail When Test developed.W/900507 Ltr ML20042F5801990-05-0404 May 1990 LER 90-012-00:on 900406,identified That Procedure for LOCA Would Not Ensure post-LOCA Core Flush Would Be Initiated in Time to Prevent Boron Precipitation.Caused by Personnel Error.Configuration Mgt Program strengthened.W/900504 Ltr ML20012E9931990-03-29029 March 1990 LER 90-008-00:on 900227,determined That Surveillance Procedure M-280-0 Did Not Include Steps to Fully Test Control Room Recorder for Hydrogen Analyzers.Caused by Personnel Error.Procedure Revised on 900308.W/900329 Ltr ML20012F0001990-03-28028 March 1990 LER 89-006-01:on 890508,containment Iodine Filters Outside Design Basis Due to Equipment Qualification.Recalculation of Total Integrated Radiation Dose to Cables for Filter Fans Demonstrated Cable qualified.W/900328 Ltr ML20012E9951990-03-28028 March 1990 LER 89-014-01:on 890723,determined That Salt Water Header Not Capable of Withstanding Seismic Event Intact.Caused by Inadequate Welding of Blind Spool Pieces in Pipe.Insp Revealed Spools Capable as installed.W/900328 Ltr ML20012E0101990-03-26026 March 1990 LER 90-009-00:on 900224,failure to Meet Action Requirement Re Tech Spec 3.7.12.Caused by Personnel Error.Cables Removed from Doorway in Charging Pump Room & Not Allowed to Be Placed in doorway.W/900326 Ltr ML20012C4971990-03-15015 March 1990 LER 90-007-00:on 900216,discovered That Supervised Circuits Associated W/Fire Detection Instruments Located in Reactor Coolant Pump Bays Not Been Included in Surveillance Test Procedure.Caused by Personnel error.W/900315 Ltr ML20012C4861990-03-12012 March 1990 LER 90-006-00:on 900209,determined That Four Fire Dampers Missing.Caused by Not Identifying Penetrations as Requiring Dampers When Fire Hazards Analysis of Plant Conducted.Hourly Fire Watch Continued.Missing Dampers installed.W/900312 Ltr ML20012B8991990-03-12012 March 1990 LER 89-023-01:on 891220,determined That Pipe Rupture in nonsafety-related Svc Water Subsystem Could Result in Rapid Draining of Subsystems That Serve Auxiliary Bldg.Task Force Formed to Determine Corrective actions.W/900312 Ltr ML20012B4221990-03-0606 March 1990 LER 89-012-01:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed.Caused by Procedural Deficiency.Procedures Revised to Include Valve & Surveillance Test Program Instruction revised.W/900306 Ltr ML20011F2701990-02-27027 February 1990 LER 90-001-01:on 900109,determined That Surveillance Tests Used to Perform Channel Calibr Tests for Acoustic Flow Monitoring Devices Inadequate.Caused by Personnel Error & Inadequate Procedures.Swapped Leads restored.W/900227 Ltr ML20011F2091990-02-27027 February 1990 LER 89-026-00:on 891128,determined That Particulate Levels in Samples Taken from Lower Third of Tanks Exceeded Allowable Limits.Caused by Inadequate Sampling Technique. Tanks Cleaned & Filled W/Clean fuel.W/900227 Ltr ML20006F8601990-02-22022 February 1990 LER 90-004-00:on 900123,discovered Fire Barrier Penetration Seal Open for Indeterminate Time W/O Performing Tech Spec 3.7.12.a Required Actions.Caused by Personnel Error. Temporary Fire Seal installed.W/900222 Ltr ML20006E0521990-02-0808 February 1990 LER 90-001-00:on 891221,discovered That Acoustic Indications for One PORV & One Safety Valve Were Reversed During Surveillance Test.Caused by Personnel Error.Swapped Leads Restored to Proper configuration.W/900208 Ltr ML20006B4801990-01-26026 January 1990 LER 89-022-00:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed,Violating Tech Specs.Caused by Procedural Deficiency.Surveillance Test Procedure Revised to Include Deleted valves.W/900126 Ltr ML19354D8931990-01-17017 January 1990 LER 89-024-00:on 891218,determined That Wires Which Connect Actuation Device Logic Relay Contacts to Remainder of Circuit Not Tested During Channel Calibr Test.Caused by Inadequate Test.Test Program Upgrade underway.W/900117 Ltr ML20005F1921990-01-10010 January 1990 LER 89-025-00:on 891208,Tech Spec Action Statement Entered When Ventilation Ducts Penetrating Fire Barrier Could Not Be Accessed to Determine If Fire Dampers Installed.On 891211, Fire Watch Missed.Caused by Personnel error.W/900110 Ltr ML20005E3971989-12-28028 December 1989 LER 89-019-00:on 891128,discovered That HPSI Discharge Header Isolation Valves Not Locked Shut When RCS in Water Solid Condition,Resulting in Operation Outside Design Basis. Procedure Revised to Require Valves closed.W/891228 Ltr ML19351A4551989-12-13013 December 1989 LER 89-020-00:on 891113,determined That Some Solenoid Valves & Valve Power Supplies for Saltwater Sys May Not Be Able to Perform Design Function After Design Basis Seismic Event. Cause Undetermined.Power Supplies upgraded.W/891213 Ltr ML20005D6611989-12-0606 December 1989 LER 89-018-00:on 891106,discovered That Many Air Operated Control Valves & piston-operated Dampers Which Utilize safety-related Air Accumulators Would Not Have Performed as Expected After Loss of air.W/891206 Ltr ML19325F3951989-11-10010 November 1989 LER 89-002-01:on 890228,discovered That Fire Barrier Penetration Inoperable & Action Statement Requirements Not Satisfied.Caused by Inadequate Administrative Controls. Penetration Returned to Operable status.W/891115 Ltr ML19325E8221989-11-0303 November 1989 LER 89-007-01:on 890505,evidence of Reactor Coolant Leakage from 120 Pressurizer Vessel Heater Penetrations Discovered. Caused by IGSCC of Inconel 600.All Penetrations Using J-welds & Inconel 600 Visually inspected.W/891103 Ltr ML19324B2511989-10-27027 October 1989 LER 89-012-01:on 890720,discovered That Master Solenoid to Switchgear Room Halon Sys Disconnected Since 890629.Caused by Personnel Error Resulting from Lack of Written Procedure. Procedure Revised to Apply Temporary mods.W/891027 Ltr ML19325C3281989-10-10010 October 1989 LER 89-016-00:on 890908,determined That as-found Condition of Resistance Temp Detectors Did Not Match Tested Configuration.Cause Not Stated.Subj Detectors Will Be Sealed,Per Environ Qualification requirements.W/891010 Ltr ML19325C3701989-10-0909 October 1989 LER 89-017-00:on 890907,determined That Discrepancy in Acceptance Criteria of Surveillance Test Procedure M-452-0 Resulted in Failure to Fully Comply W/Requirements of Tech Spec 3.9.12.Main Cause undetermined.W/891009 Ltr ML20024F3771983-08-25025 August 1983 LER 83-044/03L-0:on 830808,diesel Generator 12 Tripped on Low Jacket Cooling Water Pressure While Verifying Operability.Cause Not Stated.Coolant Jacket Vented & Large Amount of Air Found.No Evidence of leakage.W/830825 Ltr ML20024F5731983-08-25025 August 1983 LER 83-040/03L-0:on 830727,control Room Air Conditioner 11 Discovered W/Damaged Condenser Fan.Caused by Loose Set Screws Securing Fan in Position.Set Screws Restored. W/830825 Ltr ML20024E6761983-08-0404 August 1983 Updated LER 83-011/03X-1:on 830207,during Surveillance Testing ESFAS a Logic Sequencer Failed,Rendering Diesel Generator 12 Inoperable.Caused by Intermittent Operation of Module Test Push Button.Part replaced.W/830804 Ltr ML20024E1721983-07-14014 July 1983 Updated LER 81-015/03X-1:on 810226,sample Pump for Control Room Radiation Monitor Found Out of Svc,Rendering Automatic Recirculation of Control Room Ventilation Sys on High Radiation Inoperable.Caused by seizure.W/830714 Ltr ML20024D0071983-07-0808 July 1983 LER 83-035/03L-0:on 830610,during Normal Power Operation,Esf Actuation Sys Channel Zg Steam Generator Level Tripped. Caused by Failed Vitro Isolator Module.Module Replaced.W/ 830708 Ltr ML20024D0091983-07-0808 July 1983 LER 83-033/03L-0:on 830603,fire Detection Instrumentation in Containment Southeast Electrical Penetration Determined Inoperable.Repair Impossible Due to Inaccessability of Protecto wire.W/830708 Ltr ML20024B8231983-06-23023 June 1983 LER 83-029/03L-0:on 830524,during Normal Operation, Surveillance Testing Indicated Neither Spent Fuel Pool Exhaust Fans 11 or 12 Would Maintain Required Negative Pressure.Caused by Clogged HEPA filters.W/830623 Ltr ML20024C0141983-06-22022 June 1983 Updated LER 81-080/03X-1:on 811116,discovered Weep from Cracked Weld on Spent Fuel Cooling Pump Discharge Vent Line 12.Caused by Inadequate Support of Vent Line.Support Assembly installed.W/830622 Ltr ML20024A8881983-06-16016 June 1983 LER 83-032/03L-0:on 830523,containment Isolation Sys B Logic Module Would Not Actuate.Caused by Defective Vitro Labs Std Logic Module.Module Replaced.Failed Module Returned to Vitro Labs for Repair & testing.W/830616 Ltr 1999-08-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G6971999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Calvert Cliffs Npp,Units 1 & 2.With ML20216J8731999-09-10010 September 1999 Rev 52 to QA Policy for Calvert Cliffs Nuclear Power Plant ML20212A4441999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Ccnpp,Units 1 & 2. with ML17326A2011999-08-23023 August 1999 LER 99-004-00:on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With 990823 Ltr ML20210S6091999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ccnpp,Units 1 & 2. with ML20210N6001999-07-27027 July 1999 ISI Summary Rept for Calvert Cliffs Unit 2. Page 2 of 3 in Encl 1 of Incoming Submittal Not Included ML20210B7941999-07-15015 July 1999 SER Denying Licensee Request for Changes to Current Ts,Re Deletion of Tendon Surveillance Requirements for Calvert Cliffs LD-99-039, Part 21 Rept Re Defect of Abb 1200A 4kV Vacuum Breakers. Initially Reported on 990625.Defect Results in Breaker Failing to Remain in Closed Position.Root Cause Evaluation & Corrective Action Plan Being Developed.Licensee Notified1999-06-30030 June 1999 Part 21 Rept Re Defect of Abb 1200A 4kV Vacuum Breakers. Initially Reported on 990625.Defect Results in Breaker Failing to Remain in Closed Position.Root Cause Evaluation & Corrective Action Plan Being Developed.Licensee Notified ML20209F1721999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Calvert Cliffs Npp.With LD-99-035, Part 21 Rept Re Abb 1200A 4KV Vacuum Breakers Performing Trip Free Operation When Close Signal Received by Breaker. Defect Results in Breaker Failing to Remain in Closed Position.Root Cause & CAP Being Developed1999-06-25025 June 1999 Part 21 Rept Re Abb 1200A 4KV Vacuum Breakers Performing Trip Free Operation When Close Signal Received by Breaker. Defect Results in Breaker Failing to Remain in Closed Position.Root Cause & CAP Being Developed ML20196C6981999-06-21021 June 1999 Safety Evaluation Concluding That Use of ASME Section XI Code Including Summer 1983 Addenda as Interim Code for Third 10-year Insp Interval at Calvert Cliffs Units 1 & 2 Until Review of 1998 Code Completed,Would Be Acceptable ML20195K2811999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Ccnpp,Units 1 & 2. with ML20206R5871999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ccnpp,Units 1 & 2. with ML20195B3891999-04-30030 April 1999 0 to CENPD-279, Annual Rept on Abb CE ECCS Performance Evaluation Models ML20205N2951999-04-13013 April 1999 Special Rept:On 990314,fire Detection Sys Was Removed from Svc to Support Mod to Replace SRW Heat Exchangers in Unit 2 SRW Room During Unit 2 Refueling Outage.Contingency Measure 15.3.5.A.1 Will Continue Until Fire Detection Sys Restored ML20210T5211999-04-0101 April 1999 Rev 0 to Ccnpp COLR for Unit 2,Cycle 13 ML20205P5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20204H6471999-03-21021 March 1999 SER Re License Renewal of Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20207M8321999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Calvert Cliffs Nuclear Power Plant.With ML20203D4311999-02-0505 February 1999 Safety Evaluation Accepting Procedure Established for long-term Corrective Action Plan Related to Containment Vertical Tendons ML20199G4671999-01-20020 January 1999 SER Accepting USI A-46 Implementation for Plant ML20206Q3221999-01-11011 January 1999 Special Rept:On 981226,wide Range Noble Gas Effluent RM Was Removed from Operable Status.Caused by Failure of mid-range Checksource to Properly Reseat.Completed Maint & post-maint Testing & RM Was Returned to Operable Status on 990104 ML20207L0451999-01-0808 January 1999 Cost-Benefit Risk Analyses:Radwaste Sys for Light Water Reactors ML20199F4781999-01-0808 January 1999 Safety Evaluation Concluding That Bg&E Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves Susceptible to Pressure Locking.Concludes GL 95-07 Actions Were Addressed ML20198S7591999-01-0707 January 1999 SER Accepting Quality Assurance Program Description Change for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20207M2281998-12-31031 December 1998 1998 Annual Rept for Bg&E. with ML20199E2931998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Calvert Cliffs Npp. with ML20206R9911998-12-0808 December 1998 Rept of Changes,Tests & Experiments (10CFR50.59(b)(2)). with ML20198B2631998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20195H1001998-11-16016 November 1998 Safety Evaluation of First Containment Insp Interval Iwe/Iwl Program Alternative ML20196E2211998-10-31031 October 1998 Non-proprietary Rev 03-NP to CEN-633-NP, SG Tube Repair for Combustion Engineering Designed Plant with 3/4 - .048 Wall Inconel 600 Tubes Using Leak Limiting Alloy 800 Sleeves ML20195E5281998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Calvert Cliffs Nuclear Power Station,Units 1 & 2.With ML20154Q7191998-10-21021 October 1998 Special Rept:On 980923,unit 1 Wrngm Was Removed from Operable Status.Caused by Failure of Process Flow Transducer.Completed Maint to Remove Process Flow Transducer Input to Wrngm Microprocessor & Completed Formal Evaluation ML20154G3931998-10-0505 October 1998 Safety Evaluation Concluding That Flaw Tolerance Evaluation for Assumed Flaw in Inboard Instrument Weld of Pressurizer Meets Rules of ASME Code ML20154M5841998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Calvert Cliffs Nuclear Plant,Units 1 & 2.With ML20153C2571998-09-18018 September 1998 Special Rept:On 980830,wide Range Noble Gas Monitor (Wrngm) Channel Was Removed from Operable Status.Caused by Need to Support Performance of Required 18-month Channel Calibr.Will Return Wrngm to Operable Status by 980925 ML20153C1091998-09-18018 September 1998 Part 21 Rept Re Defective Capacity Control Valves.Trentec Personnel Have Been in Contact with Bg&E Personnel Re Condition & Have Requested Potentially Defective Valves ML20151U5441998-09-0404 September 1998 Bg&E ISI Summary Rept for Calvert Cliffs ML20151T5281998-09-0101 September 1998 Special Rept:On 980819,declared Rv Water Level Monitor Channel a Inoperable.Caused by Failure of Three Heated Junction Thermocouples (Sensors) in Lower Five Sensors. Channel a & B Rv Water Level Probes Will Be Replaced ML20151Y1191998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Calvert Cliffs Nuclear Power Plant Units 1 & 2.With ML20237D4981998-08-19019 August 1998 Safety Evaluation Accepting Licensee Request for Extension of Second ten-year Inservice Insp Interval ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20237B9371998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Calvert Cliffs Nuclear Power Plant ML20237D5941998-07-22022 July 1998 Rev 2 to Ccnpp COLR for Unit 2,Cycle 12 ML20236L7521998-07-0606 July 1998 Safety Evaluation Granting Bg&E 980527 Request for Relief from Requirement of Section IWA-5250 of ASME Code for Calvert Cliffs Unit 2.Alternatives Provide Reasonable Assurance of Operational Readiness ML20236F7791998-06-30030 June 1998 Safety Evaluation Authorizing Request for Temporary Relief from Requirement of Subsection IWA-5250 of ASME Code,Section XI for Plant,Unit 1 ML20236R0881998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20236X3101998-06-19019 June 1998 Rev 1 to Calvert Cliffs Nuclear Power Plant COLR for Unit 2,Cycle 12 ML20249A9571998-06-15015 June 1998 Special Rept:On 980430,fire Detection Sys Was Removed from Svc to Support Mod to Purge Air Sys 27-foot Elevation & 5-foot Elevation East Piping Penetration Rooms.Installed Temporary Alteration & Returned Fire Detection Sys to Svc ML20249A7711998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Ccnpp,Units 1 & 2 1999-09-30
[Table view] |
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g-BALTIMORE GAS AND ELECTRIC
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CALVERT CLIFFS NUCLEAR POWER PLANT 1650 CALVERT CLIFFS PARKWAY
CHARLES H. CRUSE PLANT GENERAL MANAGER CALVERT CurrS J uly 9, 1993 U.f. Nuclear Regulatory Commission Uc-hington, D.C. 20555 ATTENTION: Document Control Desk
SUBJECT:
Calvert Cliffs Nuclear Power Plant Unit Nos. 1 and 2; Docket Nos. 50-317 and 50-318; License Nos. DPR 53 and DPR 69 Licensee Event Report 93-003 Dual Unit Trip Due to Partial Loss of Offsite Power The attached report is being sent to you as required under 10 CFR 50.73 guidelines. Should you have any questions regarding this report, we will be pleased to discuss them with you.
Very truly yours,
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.NRC FORM E36 (5-92)
- U. S. NUCLEAR REGULATORY COMMISSION h ,3 ESTMTID BlflDEM PER FESPONSE TO COMRYWiTHTK3 INFC% TION
- cot 1ECIlON FEQUEST: 50.0 HFiS F0FWAFD COMMENTS FEGNUNO LICENSEE EVENT REPORT (LER) se ESTWTE TOTHE INF OfmTM MECORDS WNEMENT
- BRr#CH (MNBB 7714). U S. NUCLEAR FEGULATORY tmmeent WASHINGTOPI DC206550001, AND TOTFE PAPEFWORKFEDUCTION PIDFiCT (See teverse for required number of dioits/ characters for each block) AM MW NM AND N,MMW DCM FACILITY NAME (1) DOCKET NUMBER (2) PAGE (3)
Calvert Cliff s, Unit 1 05000 317 1 OF 07 TITLE (4)
Dual Unit Trip Due to Partial Loss of Offsite Power EVENT DATE (5) LER NUMBL3 (6) REPORT DAT E (7) OTHER FACILITIES INVOLVED (a)
MONTH S EN RNSION DAY YEAR YEAR MONTH DAY YEAR NUMBER N M ER Calvert Cliffs, U2 05000 318 06 10 93 93 - 003 -
00 07 09 93 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENT *, OF 10 CFR fCheck one or more) f11)
MODE (9) 20.402(b) 20 405(c) ,. )( 50 73(a)(2)(iv) 73 71(b) 20.405(a)(1)0) 50.36(c)(1) 50.73(a)(2)(v) 73,73 ge)
LEVEL 100 20.405(a)0)0i) 50 36(c)(2) Sn73(a)mQ OTHEn
- 00) 20.405(a)(1)(iii) 50.73(a)(2)C) 50.73(a)(2)(viii)(A)
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(Specity in Abstract below and in 20.405(a)(1)(iv) Text, NRC form 366A) 50.73(a)(2)0i) 50.73(a)(2)(viQ(B) 20.405(a)(1)(v) 50.73(a)(2)0ii) 50,73(a)(2)(x)
LICENSEE CONTACT FOR THIS LER (12)
NAME TE LEPHONE NUMBER (include Area Code)
D. W. Muth, Compliance Engineer 410 260-3592 COMPLETE ONE LINE FOR EACH COMPONENT F AILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT A R R o CAUSE SYSTEM COMPONENT
" 0 TURER NPRDS TUPER NPRDS I
SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH DAY YEAR YES SusuiSSiON (if yes, enmplete EXPECTED SUBMISSloN DATE)
X e DAT E (15)
ABST RACT (Lim #t to 1400 spaces, i.e., apprommately15 single space typewntten imes) (16)
On Thursday, June 10, 1993 at 8:28:13 a.m., a flashover relay in the Calvert Cliffs switchyaro ectuated, causing the loss of the 500 kv " Red" bus feeding Unit 2. Unit 2 inw:diately tripped on low coolant fl ow. Unit I was manually tripped 25 seconds later by operators anticipating a total loss of offsite power.
The most probable cause of the Unit 2 trip is induced vibration of the ,
flashover relay. The decision to trip Unit 1 resulted from the Control Room Supervisor's having concluded that a loss of offsite power was underway.
We will train appropriate personnel on avoiding inadvertent relay actuation.
We will minimize the protective features Icft operative wher. breakers are opened for extended periods. We will evaluate improvements to operator training.
IdC Fesm356}50
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l NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 )
Fea EXPIRES 5/31/95 1
, ESTIMATED BURDEN PER RESPONSE To COMPLY WITH THIS INFoRMATON CoLLECTON REcuEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COMMENTS REGAFONG DUHDEN ESTIMATE To THE MoRMATON AND RECoHDS MANAGEMENT BRANCH (MNBS 7714). U S. NUCLEAR TEXT CONTINUATION REGutAToRy CoMMissON wamGToN, Do rosss.onoi. AND To THE PAPERWORK REDUCTON PROJECT (3t504104), OFFICE oF MANAGEMENT AND BUDGET. WASHINGTON, DC 20503.
F AcluTV NAME (1) DOCKET NUMBER (2) (IR NUMBER (3) PAGE (4)
Calvert Cliffs, Unit 1 05000 3 1 7 93 -
003 -
00 02 0F 07 TEXT (if moes space is foquired, use addetsonal cope of NRC Form 306A) (17)
I. DESCRIPTION OF EVENT on Thursday, June 10, 1993 at 8:28:13 a.m., a flashover relay in the Calvert-Cliffs switchyard actuated, causing the loss of the 500 kv " Red" bus feeding Unit 2. Unit 2 tripped on a low reactor coolant flow signal. Unit 1 was manually tripped 25 seconds later. Unit 2 wrs in MODE 3 at 2250 psia and 532 degrees Fahrenheit and Unit 1 was in MODE 1 at 100 percent power at the time of the event.
At the time of the trip, modifications were being made in the switchyard to accommodate a new 500 kV transmission line. All 500 kv breakers were closed at t the time of the trip except 552-61, 62, and 63, which were tagged out for the i modification work (see Figure 1). The work was being done to connect the new line between breakers 552-62 and 552-63. Workers had finished constructing new )
panels and adding new wiring and relays and were performing wiring checks and l cleaning up when the flashover protection relay for breaker 552-61 actuated.
Flashover protection is designed to isolate a generator breaker if the breaker ;
is open and current is still present either due to an are across the breaker gap (a "flashover") or failure of the breaker to open. For breaker 552-61 flashover protection is provided by a Westinghouse Type KC-4 relay which contains a fast acting overcurrent device for each phase (A, B, and C). Current transformers located at the breaker and main generator sense current through the breaker, indicating flashover. Breaker auxiliary switches permit flashover protection when the breaker is open.
When the relay actuated, it tripped breakers 552-21, 41, and 63 (which was already open), isolating the 500 kv Red Bus (see Figure 1). Loss of the Red Bus deenergized 13 kv Reactor Coolant Pump (RCP) Buses 21, 22, 23, and 24 which power the four Unit 2 RCPs; and 13 kv Service Buses 21 and 22 which power 4 kv Buses 14, 22, 23, and 24. Bus 14 supplies power to Unit 1 safety-related equipment, including Control Room panel 1Y10 which provides primary indication of Unit 1 control rod position. 4 kv Bus 24 supplies power to Unit 2 safety- !
related equipment and 4 kv Buses 22 and 23 supply non-safety-related Unit 2 i equipment. The loss of power to the Unit 2 RCPs caused Unit 2 to trip on a low )
flow signal at 8:28:13 a.m.
As a result of the loss of 4 kv Buses 14 and 24, all normal Control Room lighting went out. Emergency lighting came on as designed. Plant operators are trained to recognize that one of the symptoms of a loss of offsite power is the loss of Control Room lighting. In addition to noting the loss of Control Room light ag, the Unit 1 Control Room Supervisor (CRS) noted that the Red Bus I
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,- - , ,.w a , v-
.NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 gHra EXPIRES 5/31/95 ESTIMATED BLADEN PER RESPONSE To COMPLY WITH THIS INFoRMATioN COLLECTION REQUEST. 50 0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COMMENTS REGARoWG BUHDEN ESTNATE TO THE WFORMATioN AND RECORDS MANAGEMENT BRANCH (MNBB 7714). U.S NUCLEAR TEXT CONTINUATION REautAToRy CouuissioN. WASHINGTON. oC 20$ssami. ANo To THE PAPERWORK REDUCTION PROJECT (3150 0104). OFFICE oF MANAGE MENT AND BUDGET, WASHINGTON. oC 20503 FACIUTY NAME (1) DOCKET NUMBEM (a LER NUMBER (a PAGE (4)
Calvert Cliffs, Unit 1 05000 3 1 7 93 -
003 - 00 03 0F 07 TEXT (it more space is required, use additional copH,e of NRC Fon 366A) (17) potential light was out and that he had lost all but the backup control rod position indication. He noted that the Trip Circuit Breakers had not tripped but was aware that work was going on in the switchyard and believed that the plant was in the process of losing power to both units. He therefore ordered j the Unit 1 Reactor Operator to trip the unit. Unit 1 tripped at 8:28:38 a.m.,
25 seconds after the Unit 2 trip.
Emergency Diesel Generators (EDGs) 12 and 21 started up on the loss of power to 4 kv Buses 14 and 24, respectively. Emergency Diesel Generator 21 breaker automatically closed in on 4 kv Bus 24 and the Shutdown Sequencer loaded the bus. As designed, EDG 12 had to be manually aligned to 4 kv Bus 14 since this was an Underyc1tage Trip vice a Safety Injection Actuation Signal condition.
EDG 12 was manually aligned to 4 kv Bus 14 at 8:34:23, roughly five minutes after event initiation. Since 4 kv Bus 11 was not deenergized, EDG 11 was not required to start.
1 The Shift Supervisor declared an Unusual Event at 8:50 a.m. After verifying that a common fault did not exist, the switchyard configuration was returned to its pre-event alignment by 11:50 a.m. After completing additional recovery actions, the plant exited the Unusual Event at 1:05 p.m.
II. CAUSE OF EVENT The most probable cause of the Unit 2 trip is ir.duced vibration of the KC-4 relay. However, the specific source of the induced vibration could not be absolutely established. While work was in progress in the general area, none needed to be done in the immediate vicinity of the relay. None of the workers in the Switchyard Control House reported being near the relay at the time of the trip. All other means of relay failure, including valid breaker flashover, accidental electrical operation, internal ground fault, and defect in the relay, have been examined and eliminated as possible causes. The breaker was electrically disconnected, preventing possible flashover. No work was ongoing in circuitry connected to the relay that could have accidentally energized it.
Inspection and testing found the relay within specifications and acceptable for use.
Contributing to the Unit 2 trip was that the flashover protection for breaker 552-61 was enabled when it was not needed to protect an electrically isolated breaker. Only breakers 552-62 and 63 actually needed to be tagged out for the work being performed. The decision to open breaker 552-61 was made after the crews reported to the switchyard and was an unnecessary change in system configuration. The protective circuitry for breaker 552-61 should have been
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 ,
pean EXPIRES 5/31/95
, ESTIMATED BURDEN PER RESPONSE To COMPLY WITH THtS INFoRMATON COLLECTION REoUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) CouuENTs REGARDiNo sURDEN ESriuATE To THE iNroRuAfioN AND RECORDS MANAGEMENT ORANCH lMNBB 7714), U S. NUCLEAR +
TEXT CONTINUATION Recut 4ToRv comssoN. WASHINGTON. oC roess-000i, AND To THE PAPERWORK REDUCTION PROJECT (31S0104), OFFICE oF ,
MANAGEMENT AND DVDGET, WASHINGTON, DC 20503.
F AC8UTY NAME (1) DOCKET huMBER (2) . LER NUMBER (3) PAGE (4)
Calvert Cliffs, Unit 1 05000 3 1 7 93 -
003 - 00 04 0F 07 TEXT lit more spac.e a recuved, une additional copes of NRC Form 366A) (17) considered as part of the change in the system configuration and not been left enabled when the breaker was opened.
The decision to trip Unit 1 resulted from the CRSs having quickly analyzed various inputs and concluded that a loss of offsite power was underway. Ilis decision was conservative. However, manual trip of the unit was not optimal
- since Unit 1 would not have tripped on loss of the Red Bus. The CRS believed, based on the loss of Control Room lighting and trip of Unit 2, that the plant was in the process of losing power to both units. He did not fully recognize ;
and synthesize all available information. This was due in part to distractions caused by the automatic shutdown of Unit 2. The CRS had been recently trained l on the loss of 4 kv Bus 14 and the resultant loss of panel 1Y10. He had also received training on loss of offsite power. The situation in which he found ;
himself in this event, however, was sufficiently unfamiliar that he appropriately took conservative action.
III. ANALYSIS OF EVENT l i
The worst-case Loss of Coolant Flow transient described in the Updated Final l Safety Analysis Report assures a simultaneous loss of all four RCPs on a unit .
l operating at 100 percent power and concludes that no significant safety i consequences will result from this event. This analysis is bounding for the Unit 2 trip. Unit 1 was tripped manually and shut down normally. There are no ;
significant safety consequences resulting from this event. l l
This item is reportable under the provisions of 10 CFR 50.73 (A)(2)(iv) as a Reactor Protection System actuation.
IV. CORRECTIVE ACTIONS Immediate Corrective Actions A. The flashover protection relay for breaker 552-61 was replaced. The old relay was examined for possible defects. None were found.
Preventive Actions A. Access to relay protection equipment is restricted. However, in light of the number of people working in the Switchyard Control House at the time of this incident, and the number of inadvertent relay actuations that have occurred in the Baltimore Gas and Electric Company system, we will review possible additional relay
NHC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (5 s2) , EXPlRES 5/31/95 ESTIMATED BURDEN PER RESPONSE To COMPLY WITH THts INFoRMATION COLLECTION FIEQUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) CouMENTs RtGARDiNG BURoEN EstiuArE To THE iNFORuATiON AND RECoHDS MANAGEMENT BRANCH (MNBB 7714), U.S NUCLEAR TEXT CONTINUATION REGouTORY CoMMSSM WASHWGToN. DC 205554XH, AND To '
THE PAPERWORK FIEDUCTION PROJECT 0150 0104). oFFICF oF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
F ActuTV NAME (1) DOCKET NUMBER (M LER NUMBER (M PAGE (4)
Calvert Cliffs, Unit 1 05000 3 1 7 93 -
003 -
00 05 0F 07 TEXT (It more space is reqwred, use additenal copees of NRC Form 366A; (17) protection. This review will consider different methods to desensitize the relay as much as possible, including increased relay gap, as well as additional panel bracing. We will also evaluate the use of distinctive colors, labels, or signs to identify the relays that are more sensitive and susceptible to trips.
B. We will reinforce training for personnel with access to relays on the methods employed to indicate sensitive relays and the means to avoid inadvertent actuation.
C. We will evaluate a policy that requires review of protective features when transmission system breakers are opened for an -
extended period of time. The goal of such a policy would be to ensure that protective features are left enabled only if they are needed.
D. To assist operators in maintaining a questioning attitude when contacted about switchyard operation and maintenance, we plan to develop a matrix of protective features associated with 500 kv breakers and incorporate it into the Operations procedure governing operation of the 500 kv switchyard.
E. We will discuss this event in operator training, with particular
- emphasis on the organization's support for taking conservative actions even when, in hindsight, the result is less than optimal from the power production standpoint.
F. We will expand operator training to provide add.itional criteria for operators to evaluate events involving loss power.
G. We will evaluate improvements to simulator training to better model distractions associated with dual-unit transients.
HRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO,3150-0104 m sa - EXPIRES 5/31/95 ESTIMATED BUFOEN PER RESPONSE TO COMPT.Y WITH THis INFOP'4A10N (XX.LECTON FEQUEST: 60.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COMMENTS REGARDING BURDEN ESDMATE TO THE INFORMATON AND RECORDS MANAGEMENT BRANCH (MNBB m4), U B. NUCLEAR TEXT CONTINUATION REGUMTORY CoMMGSON, WASHINGTON, DC N0001, AND TO THE PAPERWORK REDUCTON PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACluTV NAME (1) DOCKET NUMBER (a EER NUMBER (3) PAGE l4)
Calvert Cliffs, Unit 1 05000 3 1 7 93 -
003 - 00 06 OF 07 TEXT (if more space is required, use addthonal copies of NRC Form 300N {17)
V. ADDITIONAL INFORMATION A. Affected Component Identification:
IEEE 803 IEEE 805 Component or System EIIS Funct System ID Flashover Protection Relay BDMP FK 500 kv Breaker BKR FK Reactor Coolant Pump P AB Reactor Trip Breakers BKR JC Emergency Diesel Generator DG EK B. Previous Similar Events:
LER 50-318/87-012 described a similar condition involving a dual unit trip on loss of both 500 kv buses due to a tree touching one line and a defective logic circuit card tripping breakers on the other line. This event did not involve induced vibration on a relay.
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NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 pan - EXPIRES 5/31/95
~
ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS WORMATON COLLECTON REQUEST: so.0 HRS. FORWARD LlCENSEE EVENT REPORT (LER) OOMMENTS REGMONG BURDEN ESTNATE TO THE MORMATON AND RFCORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR TEXT CONTINUATION REGutatoRY OOMussoN.wASHmTON, DC aosssaci. ANo TO j THE PAPERWORK REDUCTON PROJECT (31500104) OFFCE OF MANAGEMENT AND BUDGET, WASHINGTON DC 20503
)
FACIUTY NAME (1) OOCKET NUMBER (@ LER NUMBER (4 PAGE (4)
Calvert Cliffs, Unit 1 05000 3 1 7 93 - 003 - 00 07 0F 07 TEXT or .p.c. N n auw = mons cop.es W NFC Form 366A) i 7) r To 13 kv System ;
500 kv Red Dus3 Switchyard._-, 552-21 552-41 552-61 Breaker :
From Unit 2 Generator 552-22 552-43 552-62 '
From Unit 1 Generator 552-23 552-63 ,
j; 500 kv Black Bus I J } [
Existing 500 kv Existing 500 kv To 13 kv New 500 kv Transmission Line TransmFssion Line System Line i
FIGURE 1 500 kv SWITCHYARD RING BUS F
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