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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17326A2011999-08-23023 August 1999 LER 99-004-00:on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With 990823 Ltr ML20029C7321994-04-22022 April 1994 LER 94-004-00:on 940221,discovered Corrosion of Three Nuts on One of Incor Instrumentation Reactor Vessel Head.Caused by Increase of Wet Boric Acid.Leaking Flanges Repaired.W/ 940422 Ltr ML20046B4731993-07-30030 July 1993 LER 93-005-00:on 930630,TS 3.0.3 Entered Due to Both Containment Spray Sys Inoperable.Replaced CCW Outlet Valve Actuator Connecting Link Assembly from Number 11 SDC Heat exchanger.W/930730 Ltr ML20046A4911993-07-22022 July 1993 LER 93-003-00:on 930625,SG Tripped Due to Low Water Level. Caused by Insufficient Feedwater Addition Due to Inadequate Communication.Reemphasis on Improved Communication Stressed. W/930722 Ltr ML20045G8611993-07-0909 July 1993 LER 93-003-00:on 930610,dual Unit Trip Occurred Due to Partial Loss of Offsite Power.Flashover Protection Relay for Breaker 552-61 Replaced & Training for Personnel W/ Access to Relays Will Be reinforced.W/930709 Ltr ML20045G7281993-07-0808 July 1993 LER 93-002-00:on 930608,inadvertent Arw Actuation Sys & RPS Actuations Experienced During Performance of Awf Sys Large Flow Surveillance Testing.Caused by Failure to Note Differential Pressure Condition.Valve opened.W/930708 Ltr ML20045G8661993-07-0808 July 1993 LER 93-004-00:on 930611,reactor Tripped Due to Turbine Trip Resulting from Inadequate Procedure.Procedure Changes Made to Open Appropriate FW Heater High Level Dump Valves During Plant startup.W/930708 Ltr ML20045E7361993-06-29029 June 1993 LER 93-002-01:on 930205,software Vendor Discovered Error in User Manual for Updating Basss data-input Library.Caused by Failure of QA Procedures to Require Independent Review of User Manuals.Manual Surveillances performed.W/930629 Ltr ML20029B1261991-02-28028 February 1991 LER 91-001-00:on 910129,tubing in Air Start Sys for Emergency Diesel Generator Failed During Seismic Event. Caused by Error in Design of EDG Air Start Sys.Permanent Mod to Sys installed.W/910228 Ltr ML20028H8011991-01-24024 January 1991 LER 90-002-01:on 900116,determined That 891211 Reconstitution of More than One Spent Fuel Assembly Per Time in Violation of Fuel Handling Incident Safety Analysis. Caused by Deficient procedure.W/910124 Ltr ML20044A1861990-06-20020 June 1990 LER 87-002-01:on 861203,section of Thin Wall Found on Main Steam Line W/Readings Below Allowable Min of 0.95 Inches. Caused by Grinding of Edge of Pipe to Achieve Proper fit-up for Welding.Relief from IWB-3610 granted.W/900620 Ltr ML20043G1071990-06-13013 June 1990 LER 89-019-01:on 891128,determined That for Approx 10 Yrs, from 1979-1989,requirement to Lock HPSI Discharge Header Isolation Valves Shut Not Implemented.Caused by Inadequate Mgt Attention.Test Procedures modified.W/900613 Ltr ML20043F1221990-06-0404 June 1990 LER 90-017-00:on 900505,pin Hole Leak Observed in Discharge Piping of Saltwater Pump 13.Caused by Localized Corrosion. Leaking Spool Piece Removed & Blank Flange Installed. W/900604 Ltr ML20043A7871990-05-21021 May 1990 LER 90-016-00:on 900421,determined That Waste Gas Decay Tank (Wgdt) 13 Discharged Instead of (Wgdt) 11 for Discharge Permit Issued.Caused by Inadequate Communications.Training Performed for Operators Re event.W/900521 Ltr ML20043A3441990-05-14014 May 1990 LER 90-014-00:on 900413 & 19,unit Entered Tech Spec Limiting Condition of Operation 3.0.3 Due to Potential Inoperability of Three Out of Four Reactor Protection Sys Delta T Power Channels.Caused by Lack of Procedure guidance.W/900514 Ltr ML20043A3401990-05-14014 May 1990 LER 90-013-00:on 900413,determined That Axial Shape Index Channels Out of Spec & Inoperable.Caused by Inadequate Understanding of Design Basis for Excore/Incore Comparison. Design Basis for Excore/Incore improved.W/900514 Ltr ML20042G4521990-05-0707 May 1990 LER 90-015-00:on 900407,discovered That Relay Contact Which Actuates Reactor Trip Breaker Shunt Trip Not Adequately Functionally Tested.Caused by Failure to Examine Circuit in Detail When Test developed.W/900507 Ltr ML20042F5801990-05-0404 May 1990 LER 90-012-00:on 900406,identified That Procedure for LOCA Would Not Ensure post-LOCA Core Flush Would Be Initiated in Time to Prevent Boron Precipitation.Caused by Personnel Error.Configuration Mgt Program strengthened.W/900504 Ltr ML20012E9931990-03-29029 March 1990 LER 90-008-00:on 900227,determined That Surveillance Procedure M-280-0 Did Not Include Steps to Fully Test Control Room Recorder for Hydrogen Analyzers.Caused by Personnel Error.Procedure Revised on 900308.W/900329 Ltr ML20012F0001990-03-28028 March 1990 LER 89-006-01:on 890508,containment Iodine Filters Outside Design Basis Due to Equipment Qualification.Recalculation of Total Integrated Radiation Dose to Cables for Filter Fans Demonstrated Cable qualified.W/900328 Ltr ML20012E9951990-03-28028 March 1990 LER 89-014-01:on 890723,determined That Salt Water Header Not Capable of Withstanding Seismic Event Intact.Caused by Inadequate Welding of Blind Spool Pieces in Pipe.Insp Revealed Spools Capable as installed.W/900328 Ltr ML20012E0101990-03-26026 March 1990 LER 90-009-00:on 900224,failure to Meet Action Requirement Re Tech Spec 3.7.12.Caused by Personnel Error.Cables Removed from Doorway in Charging Pump Room & Not Allowed to Be Placed in doorway.W/900326 Ltr ML20012C4971990-03-15015 March 1990 LER 90-007-00:on 900216,discovered That Supervised Circuits Associated W/Fire Detection Instruments Located in Reactor Coolant Pump Bays Not Been Included in Surveillance Test Procedure.Caused by Personnel error.W/900315 Ltr ML20012C4861990-03-12012 March 1990 LER 90-006-00:on 900209,determined That Four Fire Dampers Missing.Caused by Not Identifying Penetrations as Requiring Dampers When Fire Hazards Analysis of Plant Conducted.Hourly Fire Watch Continued.Missing Dampers installed.W/900312 Ltr ML20012B8991990-03-12012 March 1990 LER 89-023-01:on 891220,determined That Pipe Rupture in nonsafety-related Svc Water Subsystem Could Result in Rapid Draining of Subsystems That Serve Auxiliary Bldg.Task Force Formed to Determine Corrective actions.W/900312 Ltr ML20012B4221990-03-0606 March 1990 LER 89-012-01:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed.Caused by Procedural Deficiency.Procedures Revised to Include Valve & Surveillance Test Program Instruction revised.W/900306 Ltr ML20011F2701990-02-27027 February 1990 LER 90-001-01:on 900109,determined That Surveillance Tests Used to Perform Channel Calibr Tests for Acoustic Flow Monitoring Devices Inadequate.Caused by Personnel Error & Inadequate Procedures.Swapped Leads restored.W/900227 Ltr ML20011F2091990-02-27027 February 1990 LER 89-026-00:on 891128,determined That Particulate Levels in Samples Taken from Lower Third of Tanks Exceeded Allowable Limits.Caused by Inadequate Sampling Technique. Tanks Cleaned & Filled W/Clean fuel.W/900227 Ltr ML20006F8601990-02-22022 February 1990 LER 90-004-00:on 900123,discovered Fire Barrier Penetration Seal Open for Indeterminate Time W/O Performing Tech Spec 3.7.12.a Required Actions.Caused by Personnel Error. Temporary Fire Seal installed.W/900222 Ltr ML20006E0521990-02-0808 February 1990 LER 90-001-00:on 891221,discovered That Acoustic Indications for One PORV & One Safety Valve Were Reversed During Surveillance Test.Caused by Personnel Error.Swapped Leads Restored to Proper configuration.W/900208 Ltr ML20006B4801990-01-26026 January 1990 LER 89-022-00:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed,Violating Tech Specs.Caused by Procedural Deficiency.Surveillance Test Procedure Revised to Include Deleted valves.W/900126 Ltr ML19354D8931990-01-17017 January 1990 LER 89-024-00:on 891218,determined That Wires Which Connect Actuation Device Logic Relay Contacts to Remainder of Circuit Not Tested During Channel Calibr Test.Caused by Inadequate Test.Test Program Upgrade underway.W/900117 Ltr ML20005F1921990-01-10010 January 1990 LER 89-025-00:on 891208,Tech Spec Action Statement Entered When Ventilation Ducts Penetrating Fire Barrier Could Not Be Accessed to Determine If Fire Dampers Installed.On 891211, Fire Watch Missed.Caused by Personnel error.W/900110 Ltr ML20005E3971989-12-28028 December 1989 LER 89-019-00:on 891128,discovered That HPSI Discharge Header Isolation Valves Not Locked Shut When RCS in Water Solid Condition,Resulting in Operation Outside Design Basis. Procedure Revised to Require Valves closed.W/891228 Ltr ML19351A4551989-12-13013 December 1989 LER 89-020-00:on 891113,determined That Some Solenoid Valves & Valve Power Supplies for Saltwater Sys May Not Be Able to Perform Design Function After Design Basis Seismic Event. Cause Undetermined.Power Supplies upgraded.W/891213 Ltr ML20005D6611989-12-0606 December 1989 LER 89-018-00:on 891106,discovered That Many Air Operated Control Valves & piston-operated Dampers Which Utilize safety-related Air Accumulators Would Not Have Performed as Expected After Loss of air.W/891206 Ltr ML19325F3951989-11-10010 November 1989 LER 89-002-01:on 890228,discovered That Fire Barrier Penetration Inoperable & Action Statement Requirements Not Satisfied.Caused by Inadequate Administrative Controls. Penetration Returned to Operable status.W/891115 Ltr ML19325E8221989-11-0303 November 1989 LER 89-007-01:on 890505,evidence of Reactor Coolant Leakage from 120 Pressurizer Vessel Heater Penetrations Discovered. Caused by IGSCC of Inconel 600.All Penetrations Using J-welds & Inconel 600 Visually inspected.W/891103 Ltr ML19324B2511989-10-27027 October 1989 LER 89-012-01:on 890720,discovered That Master Solenoid to Switchgear Room Halon Sys Disconnected Since 890629.Caused by Personnel Error Resulting from Lack of Written Procedure. Procedure Revised to Apply Temporary mods.W/891027 Ltr ML19325C3281989-10-10010 October 1989 LER 89-016-00:on 890908,determined That as-found Condition of Resistance Temp Detectors Did Not Match Tested Configuration.Cause Not Stated.Subj Detectors Will Be Sealed,Per Environ Qualification requirements.W/891010 Ltr ML19325C3701989-10-0909 October 1989 LER 89-017-00:on 890907,determined That Discrepancy in Acceptance Criteria of Surveillance Test Procedure M-452-0 Resulted in Failure to Fully Comply W/Requirements of Tech Spec 3.9.12.Main Cause undetermined.W/891009 Ltr ML20024F3771983-08-25025 August 1983 LER 83-044/03L-0:on 830808,diesel Generator 12 Tripped on Low Jacket Cooling Water Pressure While Verifying Operability.Cause Not Stated.Coolant Jacket Vented & Large Amount of Air Found.No Evidence of leakage.W/830825 Ltr ML20024F5731983-08-25025 August 1983 LER 83-040/03L-0:on 830727,control Room Air Conditioner 11 Discovered W/Damaged Condenser Fan.Caused by Loose Set Screws Securing Fan in Position.Set Screws Restored. W/830825 Ltr ML20024E6761983-08-0404 August 1983 Updated LER 83-011/03X-1:on 830207,during Surveillance Testing ESFAS a Logic Sequencer Failed,Rendering Diesel Generator 12 Inoperable.Caused by Intermittent Operation of Module Test Push Button.Part replaced.W/830804 Ltr ML20024E1721983-07-14014 July 1983 Updated LER 81-015/03X-1:on 810226,sample Pump for Control Room Radiation Monitor Found Out of Svc,Rendering Automatic Recirculation of Control Room Ventilation Sys on High Radiation Inoperable.Caused by seizure.W/830714 Ltr ML20024D0071983-07-0808 July 1983 LER 83-035/03L-0:on 830610,during Normal Power Operation,Esf Actuation Sys Channel Zg Steam Generator Level Tripped. Caused by Failed Vitro Isolator Module.Module Replaced.W/ 830708 Ltr ML20024D0091983-07-0808 July 1983 LER 83-033/03L-0:on 830603,fire Detection Instrumentation in Containment Southeast Electrical Penetration Determined Inoperable.Repair Impossible Due to Inaccessability of Protecto wire.W/830708 Ltr ML20024B8231983-06-23023 June 1983 LER 83-029/03L-0:on 830524,during Normal Operation, Surveillance Testing Indicated Neither Spent Fuel Pool Exhaust Fans 11 or 12 Would Maintain Required Negative Pressure.Caused by Clogged HEPA filters.W/830623 Ltr ML20024C0141983-06-22022 June 1983 Updated LER 81-080/03X-1:on 811116,discovered Weep from Cracked Weld on Spent Fuel Cooling Pump Discharge Vent Line 12.Caused by Inadequate Support of Vent Line.Support Assembly installed.W/830622 Ltr ML20024A8881983-06-16016 June 1983 LER 83-032/03L-0:on 830523,containment Isolation Sys B Logic Module Would Not Actuate.Caused by Defective Vitro Labs Std Logic Module.Module Replaced.Failed Module Returned to Vitro Labs for Repair & testing.W/830616 Ltr 1999-08-23
[Table view] Category:RO)
MONTHYEARML17326A2011999-08-23023 August 1999 LER 99-004-00:on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With 990823 Ltr ML20029C7321994-04-22022 April 1994 LER 94-004-00:on 940221,discovered Corrosion of Three Nuts on One of Incor Instrumentation Reactor Vessel Head.Caused by Increase of Wet Boric Acid.Leaking Flanges Repaired.W/ 940422 Ltr ML20046B4731993-07-30030 July 1993 LER 93-005-00:on 930630,TS 3.0.3 Entered Due to Both Containment Spray Sys Inoperable.Replaced CCW Outlet Valve Actuator Connecting Link Assembly from Number 11 SDC Heat exchanger.W/930730 Ltr ML20046A4911993-07-22022 July 1993 LER 93-003-00:on 930625,SG Tripped Due to Low Water Level. Caused by Insufficient Feedwater Addition Due to Inadequate Communication.Reemphasis on Improved Communication Stressed. W/930722 Ltr ML20045G8611993-07-0909 July 1993 LER 93-003-00:on 930610,dual Unit Trip Occurred Due to Partial Loss of Offsite Power.Flashover Protection Relay for Breaker 552-61 Replaced & Training for Personnel W/ Access to Relays Will Be reinforced.W/930709 Ltr ML20045G7281993-07-0808 July 1993 LER 93-002-00:on 930608,inadvertent Arw Actuation Sys & RPS Actuations Experienced During Performance of Awf Sys Large Flow Surveillance Testing.Caused by Failure to Note Differential Pressure Condition.Valve opened.W/930708 Ltr ML20045G8661993-07-0808 July 1993 LER 93-004-00:on 930611,reactor Tripped Due to Turbine Trip Resulting from Inadequate Procedure.Procedure Changes Made to Open Appropriate FW Heater High Level Dump Valves During Plant startup.W/930708 Ltr ML20045E7361993-06-29029 June 1993 LER 93-002-01:on 930205,software Vendor Discovered Error in User Manual for Updating Basss data-input Library.Caused by Failure of QA Procedures to Require Independent Review of User Manuals.Manual Surveillances performed.W/930629 Ltr ML20029B1261991-02-28028 February 1991 LER 91-001-00:on 910129,tubing in Air Start Sys for Emergency Diesel Generator Failed During Seismic Event. Caused by Error in Design of EDG Air Start Sys.Permanent Mod to Sys installed.W/910228 Ltr ML20028H8011991-01-24024 January 1991 LER 90-002-01:on 900116,determined That 891211 Reconstitution of More than One Spent Fuel Assembly Per Time in Violation of Fuel Handling Incident Safety Analysis. Caused by Deficient procedure.W/910124 Ltr ML20044A1861990-06-20020 June 1990 LER 87-002-01:on 861203,section of Thin Wall Found on Main Steam Line W/Readings Below Allowable Min of 0.95 Inches. Caused by Grinding of Edge of Pipe to Achieve Proper fit-up for Welding.Relief from IWB-3610 granted.W/900620 Ltr ML20043G1071990-06-13013 June 1990 LER 89-019-01:on 891128,determined That for Approx 10 Yrs, from 1979-1989,requirement to Lock HPSI Discharge Header Isolation Valves Shut Not Implemented.Caused by Inadequate Mgt Attention.Test Procedures modified.W/900613 Ltr ML20043F1221990-06-0404 June 1990 LER 90-017-00:on 900505,pin Hole Leak Observed in Discharge Piping of Saltwater Pump 13.Caused by Localized Corrosion. Leaking Spool Piece Removed & Blank Flange Installed. W/900604 Ltr ML20043A7871990-05-21021 May 1990 LER 90-016-00:on 900421,determined That Waste Gas Decay Tank (Wgdt) 13 Discharged Instead of (Wgdt) 11 for Discharge Permit Issued.Caused by Inadequate Communications.Training Performed for Operators Re event.W/900521 Ltr ML20043A3441990-05-14014 May 1990 LER 90-014-00:on 900413 & 19,unit Entered Tech Spec Limiting Condition of Operation 3.0.3 Due to Potential Inoperability of Three Out of Four Reactor Protection Sys Delta T Power Channels.Caused by Lack of Procedure guidance.W/900514 Ltr ML20043A3401990-05-14014 May 1990 LER 90-013-00:on 900413,determined That Axial Shape Index Channels Out of Spec & Inoperable.Caused by Inadequate Understanding of Design Basis for Excore/Incore Comparison. Design Basis for Excore/Incore improved.W/900514 Ltr ML20042G4521990-05-0707 May 1990 LER 90-015-00:on 900407,discovered That Relay Contact Which Actuates Reactor Trip Breaker Shunt Trip Not Adequately Functionally Tested.Caused by Failure to Examine Circuit in Detail When Test developed.W/900507 Ltr ML20042F5801990-05-0404 May 1990 LER 90-012-00:on 900406,identified That Procedure for LOCA Would Not Ensure post-LOCA Core Flush Would Be Initiated in Time to Prevent Boron Precipitation.Caused by Personnel Error.Configuration Mgt Program strengthened.W/900504 Ltr ML20012E9931990-03-29029 March 1990 LER 90-008-00:on 900227,determined That Surveillance Procedure M-280-0 Did Not Include Steps to Fully Test Control Room Recorder for Hydrogen Analyzers.Caused by Personnel Error.Procedure Revised on 900308.W/900329 Ltr ML20012F0001990-03-28028 March 1990 LER 89-006-01:on 890508,containment Iodine Filters Outside Design Basis Due to Equipment Qualification.Recalculation of Total Integrated Radiation Dose to Cables for Filter Fans Demonstrated Cable qualified.W/900328 Ltr ML20012E9951990-03-28028 March 1990 LER 89-014-01:on 890723,determined That Salt Water Header Not Capable of Withstanding Seismic Event Intact.Caused by Inadequate Welding of Blind Spool Pieces in Pipe.Insp Revealed Spools Capable as installed.W/900328 Ltr ML20012E0101990-03-26026 March 1990 LER 90-009-00:on 900224,failure to Meet Action Requirement Re Tech Spec 3.7.12.Caused by Personnel Error.Cables Removed from Doorway in Charging Pump Room & Not Allowed to Be Placed in doorway.W/900326 Ltr ML20012C4971990-03-15015 March 1990 LER 90-007-00:on 900216,discovered That Supervised Circuits Associated W/Fire Detection Instruments Located in Reactor Coolant Pump Bays Not Been Included in Surveillance Test Procedure.Caused by Personnel error.W/900315 Ltr ML20012C4861990-03-12012 March 1990 LER 90-006-00:on 900209,determined That Four Fire Dampers Missing.Caused by Not Identifying Penetrations as Requiring Dampers When Fire Hazards Analysis of Plant Conducted.Hourly Fire Watch Continued.Missing Dampers installed.W/900312 Ltr ML20012B8991990-03-12012 March 1990 LER 89-023-01:on 891220,determined That Pipe Rupture in nonsafety-related Svc Water Subsystem Could Result in Rapid Draining of Subsystems That Serve Auxiliary Bldg.Task Force Formed to Determine Corrective actions.W/900312 Ltr ML20012B4221990-03-0606 March 1990 LER 89-012-01:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed.Caused by Procedural Deficiency.Procedures Revised to Include Valve & Surveillance Test Program Instruction revised.W/900306 Ltr ML20011F2701990-02-27027 February 1990 LER 90-001-01:on 900109,determined That Surveillance Tests Used to Perform Channel Calibr Tests for Acoustic Flow Monitoring Devices Inadequate.Caused by Personnel Error & Inadequate Procedures.Swapped Leads restored.W/900227 Ltr ML20011F2091990-02-27027 February 1990 LER 89-026-00:on 891128,determined That Particulate Levels in Samples Taken from Lower Third of Tanks Exceeded Allowable Limits.Caused by Inadequate Sampling Technique. Tanks Cleaned & Filled W/Clean fuel.W/900227 Ltr ML20006F8601990-02-22022 February 1990 LER 90-004-00:on 900123,discovered Fire Barrier Penetration Seal Open for Indeterminate Time W/O Performing Tech Spec 3.7.12.a Required Actions.Caused by Personnel Error. Temporary Fire Seal installed.W/900222 Ltr ML20006E0521990-02-0808 February 1990 LER 90-001-00:on 891221,discovered That Acoustic Indications for One PORV & One Safety Valve Were Reversed During Surveillance Test.Caused by Personnel Error.Swapped Leads Restored to Proper configuration.W/900208 Ltr ML20006B4801990-01-26026 January 1990 LER 89-022-00:on 891227,core Alterations Performed W/Only One of Two Containment Vent Valves Closed,Violating Tech Specs.Caused by Procedural Deficiency.Surveillance Test Procedure Revised to Include Deleted valves.W/900126 Ltr ML19354D8931990-01-17017 January 1990 LER 89-024-00:on 891218,determined That Wires Which Connect Actuation Device Logic Relay Contacts to Remainder of Circuit Not Tested During Channel Calibr Test.Caused by Inadequate Test.Test Program Upgrade underway.W/900117 Ltr ML20005F1921990-01-10010 January 1990 LER 89-025-00:on 891208,Tech Spec Action Statement Entered When Ventilation Ducts Penetrating Fire Barrier Could Not Be Accessed to Determine If Fire Dampers Installed.On 891211, Fire Watch Missed.Caused by Personnel error.W/900110 Ltr ML20005E3971989-12-28028 December 1989 LER 89-019-00:on 891128,discovered That HPSI Discharge Header Isolation Valves Not Locked Shut When RCS in Water Solid Condition,Resulting in Operation Outside Design Basis. Procedure Revised to Require Valves closed.W/891228 Ltr ML19351A4551989-12-13013 December 1989 LER 89-020-00:on 891113,determined That Some Solenoid Valves & Valve Power Supplies for Saltwater Sys May Not Be Able to Perform Design Function After Design Basis Seismic Event. Cause Undetermined.Power Supplies upgraded.W/891213 Ltr ML20005D6611989-12-0606 December 1989 LER 89-018-00:on 891106,discovered That Many Air Operated Control Valves & piston-operated Dampers Which Utilize safety-related Air Accumulators Would Not Have Performed as Expected After Loss of air.W/891206 Ltr ML19325F3951989-11-10010 November 1989 LER 89-002-01:on 890228,discovered That Fire Barrier Penetration Inoperable & Action Statement Requirements Not Satisfied.Caused by Inadequate Administrative Controls. Penetration Returned to Operable status.W/891115 Ltr ML19325E8221989-11-0303 November 1989 LER 89-007-01:on 890505,evidence of Reactor Coolant Leakage from 120 Pressurizer Vessel Heater Penetrations Discovered. Caused by IGSCC of Inconel 600.All Penetrations Using J-welds & Inconel 600 Visually inspected.W/891103 Ltr ML19324B2511989-10-27027 October 1989 LER 89-012-01:on 890720,discovered That Master Solenoid to Switchgear Room Halon Sys Disconnected Since 890629.Caused by Personnel Error Resulting from Lack of Written Procedure. Procedure Revised to Apply Temporary mods.W/891027 Ltr ML19325C3281989-10-10010 October 1989 LER 89-016-00:on 890908,determined That as-found Condition of Resistance Temp Detectors Did Not Match Tested Configuration.Cause Not Stated.Subj Detectors Will Be Sealed,Per Environ Qualification requirements.W/891010 Ltr ML19325C3701989-10-0909 October 1989 LER 89-017-00:on 890907,determined That Discrepancy in Acceptance Criteria of Surveillance Test Procedure M-452-0 Resulted in Failure to Fully Comply W/Requirements of Tech Spec 3.9.12.Main Cause undetermined.W/891009 Ltr ML20024F3771983-08-25025 August 1983 LER 83-044/03L-0:on 830808,diesel Generator 12 Tripped on Low Jacket Cooling Water Pressure While Verifying Operability.Cause Not Stated.Coolant Jacket Vented & Large Amount of Air Found.No Evidence of leakage.W/830825 Ltr ML20024F5731983-08-25025 August 1983 LER 83-040/03L-0:on 830727,control Room Air Conditioner 11 Discovered W/Damaged Condenser Fan.Caused by Loose Set Screws Securing Fan in Position.Set Screws Restored. W/830825 Ltr ML20024E6761983-08-0404 August 1983 Updated LER 83-011/03X-1:on 830207,during Surveillance Testing ESFAS a Logic Sequencer Failed,Rendering Diesel Generator 12 Inoperable.Caused by Intermittent Operation of Module Test Push Button.Part replaced.W/830804 Ltr ML20024E1721983-07-14014 July 1983 Updated LER 81-015/03X-1:on 810226,sample Pump for Control Room Radiation Monitor Found Out of Svc,Rendering Automatic Recirculation of Control Room Ventilation Sys on High Radiation Inoperable.Caused by seizure.W/830714 Ltr ML20024D0071983-07-0808 July 1983 LER 83-035/03L-0:on 830610,during Normal Power Operation,Esf Actuation Sys Channel Zg Steam Generator Level Tripped. Caused by Failed Vitro Isolator Module.Module Replaced.W/ 830708 Ltr ML20024D0091983-07-0808 July 1983 LER 83-033/03L-0:on 830603,fire Detection Instrumentation in Containment Southeast Electrical Penetration Determined Inoperable.Repair Impossible Due to Inaccessability of Protecto wire.W/830708 Ltr ML20024B8231983-06-23023 June 1983 LER 83-029/03L-0:on 830524,during Normal Operation, Surveillance Testing Indicated Neither Spent Fuel Pool Exhaust Fans 11 or 12 Would Maintain Required Negative Pressure.Caused by Clogged HEPA filters.W/830623 Ltr ML20024C0141983-06-22022 June 1983 Updated LER 81-080/03X-1:on 811116,discovered Weep from Cracked Weld on Spent Fuel Cooling Pump Discharge Vent Line 12.Caused by Inadequate Support of Vent Line.Support Assembly installed.W/830622 Ltr ML20024A8881983-06-16016 June 1983 LER 83-032/03L-0:on 830523,containment Isolation Sys B Logic Module Would Not Actuate.Caused by Defective Vitro Labs Std Logic Module.Module Replaced.Failed Module Returned to Vitro Labs for Repair & testing.W/830616 Ltr 1999-08-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G6971999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Calvert Cliffs Npp,Units 1 & 2.With ML20216J8731999-09-10010 September 1999 Rev 52 to QA Policy for Calvert Cliffs Nuclear Power Plant ML20212A4441999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Ccnpp,Units 1 & 2. with ML17326A2011999-08-23023 August 1999 LER 99-004-00:on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With 990823 Ltr ML20210S6091999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ccnpp,Units 1 & 2. with ML20210N6001999-07-27027 July 1999 ISI Summary Rept for Calvert Cliffs Unit 2. Page 2 of 3 in Encl 1 of Incoming Submittal Not Included ML20210B7941999-07-15015 July 1999 SER Denying Licensee Request for Changes to Current Ts,Re Deletion of Tendon Surveillance Requirements for Calvert Cliffs LD-99-039, Part 21 Rept Re Defect of Abb 1200A 4kV Vacuum Breakers. Initially Reported on 990625.Defect Results in Breaker Failing to Remain in Closed Position.Root Cause Evaluation & Corrective Action Plan Being Developed.Licensee Notified1999-06-30030 June 1999 Part 21 Rept Re Defect of Abb 1200A 4kV Vacuum Breakers. Initially Reported on 990625.Defect Results in Breaker Failing to Remain in Closed Position.Root Cause Evaluation & Corrective Action Plan Being Developed.Licensee Notified ML20209F1721999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Calvert Cliffs Npp.With LD-99-035, Part 21 Rept Re Abb 1200A 4KV Vacuum Breakers Performing Trip Free Operation When Close Signal Received by Breaker. Defect Results in Breaker Failing to Remain in Closed Position.Root Cause & CAP Being Developed1999-06-25025 June 1999 Part 21 Rept Re Abb 1200A 4KV Vacuum Breakers Performing Trip Free Operation When Close Signal Received by Breaker. Defect Results in Breaker Failing to Remain in Closed Position.Root Cause & CAP Being Developed ML20196C6981999-06-21021 June 1999 Safety Evaluation Concluding That Use of ASME Section XI Code Including Summer 1983 Addenda as Interim Code for Third 10-year Insp Interval at Calvert Cliffs Units 1 & 2 Until Review of 1998 Code Completed,Would Be Acceptable ML20195K2811999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Ccnpp,Units 1 & 2. with ML20206R5871999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ccnpp,Units 1 & 2. with ML20195B3891999-04-30030 April 1999 0 to CENPD-279, Annual Rept on Abb CE ECCS Performance Evaluation Models ML20205N2951999-04-13013 April 1999 Special Rept:On 990314,fire Detection Sys Was Removed from Svc to Support Mod to Replace SRW Heat Exchangers in Unit 2 SRW Room During Unit 2 Refueling Outage.Contingency Measure 15.3.5.A.1 Will Continue Until Fire Detection Sys Restored ML20210T5211999-04-0101 April 1999 Rev 0 to Ccnpp COLR for Unit 2,Cycle 13 ML20205P5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20204H6471999-03-21021 March 1999 SER Re License Renewal of Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20207M8321999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Calvert Cliffs Nuclear Power Plant.With ML20203D4311999-02-0505 February 1999 Safety Evaluation Accepting Procedure Established for long-term Corrective Action Plan Related to Containment Vertical Tendons ML20199G4671999-01-20020 January 1999 SER Accepting USI A-46 Implementation for Plant ML20206Q3221999-01-11011 January 1999 Special Rept:On 981226,wide Range Noble Gas Effluent RM Was Removed from Operable Status.Caused by Failure of mid-range Checksource to Properly Reseat.Completed Maint & post-maint Testing & RM Was Returned to Operable Status on 990104 ML20207L0451999-01-0808 January 1999 Cost-Benefit Risk Analyses:Radwaste Sys for Light Water Reactors ML20199F4781999-01-0808 January 1999 Safety Evaluation Concluding That Bg&E Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves Susceptible to Pressure Locking.Concludes GL 95-07 Actions Were Addressed ML20198S7591999-01-0707 January 1999 SER Accepting Quality Assurance Program Description Change for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20207M2281998-12-31031 December 1998 1998 Annual Rept for Bg&E. with ML20199E2931998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Calvert Cliffs Npp. with ML20206R9911998-12-0808 December 1998 Rept of Changes,Tests & Experiments (10CFR50.59(b)(2)). with ML20198B2631998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20195H1001998-11-16016 November 1998 Safety Evaluation of First Containment Insp Interval Iwe/Iwl Program Alternative ML20196E2211998-10-31031 October 1998 Non-proprietary Rev 03-NP to CEN-633-NP, SG Tube Repair for Combustion Engineering Designed Plant with 3/4 - .048 Wall Inconel 600 Tubes Using Leak Limiting Alloy 800 Sleeves ML20195E5281998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Calvert Cliffs Nuclear Power Station,Units 1 & 2.With ML20154Q7191998-10-21021 October 1998 Special Rept:On 980923,unit 1 Wrngm Was Removed from Operable Status.Caused by Failure of Process Flow Transducer.Completed Maint to Remove Process Flow Transducer Input to Wrngm Microprocessor & Completed Formal Evaluation ML20154G3931998-10-0505 October 1998 Safety Evaluation Concluding That Flaw Tolerance Evaluation for Assumed Flaw in Inboard Instrument Weld of Pressurizer Meets Rules of ASME Code ML20154M5841998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Calvert Cliffs Nuclear Plant,Units 1 & 2.With ML20153C2571998-09-18018 September 1998 Special Rept:On 980830,wide Range Noble Gas Monitor (Wrngm) Channel Was Removed from Operable Status.Caused by Need to Support Performance of Required 18-month Channel Calibr.Will Return Wrngm to Operable Status by 980925 ML20153C1091998-09-18018 September 1998 Part 21 Rept Re Defective Capacity Control Valves.Trentec Personnel Have Been in Contact with Bg&E Personnel Re Condition & Have Requested Potentially Defective Valves ML20151U5441998-09-0404 September 1998 Bg&E ISI Summary Rept for Calvert Cliffs ML20151T5281998-09-0101 September 1998 Special Rept:On 980819,declared Rv Water Level Monitor Channel a Inoperable.Caused by Failure of Three Heated Junction Thermocouples (Sensors) in Lower Five Sensors. Channel a & B Rv Water Level Probes Will Be Replaced ML20151Y1191998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Calvert Cliffs Nuclear Power Plant Units 1 & 2.With ML20237D4981998-08-19019 August 1998 Safety Evaluation Accepting Licensee Request for Extension of Second ten-year Inservice Insp Interval ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20237B9371998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Calvert Cliffs Nuclear Power Plant ML20237D5941998-07-22022 July 1998 Rev 2 to Ccnpp COLR for Unit 2,Cycle 12 ML20236L7521998-07-0606 July 1998 Safety Evaluation Granting Bg&E 980527 Request for Relief from Requirement of Section IWA-5250 of ASME Code for Calvert Cliffs Unit 2.Alternatives Provide Reasonable Assurance of Operational Readiness ML20236F7791998-06-30030 June 1998 Safety Evaluation Authorizing Request for Temporary Relief from Requirement of Subsection IWA-5250 of ASME Code,Section XI for Plant,Unit 1 ML20236R0881998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20236X3101998-06-19019 June 1998 Rev 1 to Calvert Cliffs Nuclear Power Plant COLR for Unit 2,Cycle 12 ML20249A9571998-06-15015 June 1998 Special Rept:On 980430,fire Detection Sys Was Removed from Svc to Support Mod to Purge Air Sys 27-foot Elevation & 5-foot Elevation East Piping Penetration Rooms.Installed Temporary Alteration & Returned Fire Detection Sys to Svc ML20249A7711998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Ccnpp,Units 1 & 2 1999-09-30
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. BALTIMORE GAS AND
. ELECTRIC CALVERT CLIFFS NUCLEAR POWER PLANT 1650 CALVERT CLIFFS PARKWAY
- LUSBY, MARYLAND 20657-4702 CHARLES H. CRUSE ,
PLANT GENERAL MANAGER cALVERT CUFFS July 22, 1993 U.S. Nuclear Regulatory Commission Washington, D.C. 20555 ATTENTION: Document Control Desk .j
SUBJECT:
Calvert Cliffs Nuclear Power Plant Unit No. 2; Docket No. 50-318; License No. DPR 69 Licensee Event Report 93-003 Trip on Low Steam Cenerator Level Due to Insufficient l Feedwater Addition H The attached report is being sent to you . as required under '10 CFR 50.73 .!
i guidelines. Should you have any questions regarding this report, we will be pleased to discuss them with you.
Very truly yours, l
l CHC/DWM/bj d Attachment g/ ./ Mfg /
,7 cc: D. A. Brune, Esquire ;
J. E. Silberg, Esquire ;
R. A. Capra, NRC I D. C, Mcdonald, Jr. , NRC ]
T. T. Martin, NRC ;
P. R. Wilson, NRC =
R. I. McLean, DNR J. H. Walter, PSC Director, Office of Management Information and Program Control 2800as -
S
/19#8
'9307280187 930722 {
DR ADOCKOSOOg8
NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION WW No MM M2) .
ESTIMATED BUF0EN PG KSFONSE TO COMFUTWITH TKB INFC3AAT10N
. CCLIEctlON KOUEST: 5a0 HH1 FOFWAFU COMMENTS KoAFDtG EMN ESTWE TO THE INFCFWON AND KCORDS MAPMGEMENT L1CENSEE EVENT REPORT (LER) BMNCH (MNDB T/14). U.S6 NUCLEAR KoVLATOFNtNme"N, WASHINGTON, DC 2m550001, AND TO THE PAPEFWORK KDUCTION PRCUECT p15)0104), OFTICE OF MAPMOEMENT AND BUDGET, WASHINGTON DC 20Sn (See reverse for reauired number of diaits/ characters for each block)
FACILITY NAME (1) DOCKET NUMBER (2) PAGE (3)
Calvert Clif f s, Unit 2 05000 318 1 OF 06 TITLE (4)
Trip on Low Steam Generator Level Due to insufficient Feedwater Addition EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
MOMTH DAY YEAR YEAR MO*(rH DAY YEAR '
NUMBER NUMBER 06 25 93 93 - 003 -
00 07 22 93 05000 j OPERATING THit REPORT IS SUBMITTED PURSUANT TO THE REoVIREMENTS OF 10 CFR :(Check one or more) [11) 2 20.402(b) 20.405(c) )( 50.73(a)(2)(iv)
MODE (9) 73.7,(3) 20.405(a)(1)(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c)
LEVEL 3 2n405(ani>00 sa36(cx2) Sa73(an2)(va g7gg,,
~
(10) 20.405(a)(1)(iii) 50.73(a)(2)(i) 50.73(a)(2)(viii)(A) (Specify in Abstract below and in Text, NRC Form 30GA) 20.405(a)(1)(iv) 50.73(a)(2)(ii) 50.73(a)(2)(viii)(B) 20.405(a)(1)(v) 50.73(a)(2)0ii) 50.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER (include Area Code)
D. W. Muth, Compliance Engineer 410-260-3592 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBEDIN THIS REPORT (13)
CAUSE SYSTEM COMPONENT
" #0 CAUSE SYSTEM COMPONENT
^
TURER NPRDS TURER NPROS l
l SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH DAY YEAR ygg SUBMISSION (if yes complete EXPFCTED SURMISSION DATF) DATE (15)
ABST RACT (Limit to 1400 spaces Lo., approximately15 singlespace typewritten hnes) (16)
On Thursday, June 25, 1993 at 8:05 p.m., Calvert Cliffs Unit 2 automatically tripped on low level in the 21 Steam Generator (SG). Operators had noted divergent SG 1evel oscillations with the Full Range Digital Feedwater Control System (FCS) in automatic. They took manual control with SG level at
+25 inches but did not provide sufficient feedwater. The reactor tripped on low SG level.
The causes of this event include inadequate communication of pertinent information regarding the response of the FCS at low power, inadequate communication during shif t turnover regarding a just-completed power increase, the lack of Project Team involvement at the time of the incident, and the work practices of the operations personnel involved in this incident.
Operations management will reemphasize expectations for the improvement of communications between operating crews. An FCS Project Team representative will be available to the Control Room for future startups and planned shutdowns until FCS performance meets expectations. We will provide classroom training to all operating crews on the details of this event.
iitFormn(594
I NRC FORM 366A U.S. HUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150 0104 002 EXPIRES 5/31/95
. ESTIMATED DURDEN PER RESPONSE To COMPLY WTTH THis HFoRMATON CoLLECTloN REoUEST: 50.0 HRS, FORWARD LICENSEE EVENT REPORT (LER) COMMENTS REGARDWG BURDEN ESTIMATE To THE MoRMATON AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR TEXT CONTINUATION nEGutAToRv CouuissoN, wasswGToN. DC 20suact, ANoTo THE PAPERWORK REDUCTON PROJECT (31500104), oFFCE oF MANAGEMENT AND BUDGET, WASHINGTON, DC 20003.
FACIUTY NAME (1) DOCKET NUMBER (2) LIR NUMBER (3) PAGE (4)
Calvert Cliffs, Unit 2 05000 3 1 8 93 -
003 - 00 02 0F 06 TEXT pr move space b required, use addmonaJ copes of NRC Form 368A} {17)
I. DESCRIPTION OF EVENT On Thursday, June 25, 1993 at 8:05:09 p.m., Calvert Cliffs Unit 2 automatically tripped on low level in the 21 Steam Generator (SC). Operators had noted divergent level oscillations with the Feedwater Control System (FCS) in automatic. They took manual control with SG 1evel at +25 inches but did not provide sufficient feedwater. The underfeed condition lasted approximately 35 minutes at which time level reached -50 inches, tripping the reactor. The Unit was at 2.8 percent power in MODE 2 at the time of the event.
In response to previous problems controlling feedwater during startup, a new Full Range Digital FCS was installed in Unit 2 during the recently completed refueling outage. The FCS was first used during initial startup on June 12, 1993. It was noted to perform particularly well below 2 percent and above 8 percent power, with minor, gradual oscillations in SG level. However, significant oscillations were observed as power was increased between 2 and 8 percent power. These oscillations had a maximum amplitude of approximately 25 inches and period of about 30 minutes. The Operations crew performing this phase of the startup considered the oscillations acceptable when compared either with the old automatic system or with what was possible in manual and therefore did not communicate them to other Operations shifts.
On June 25, 1993 day shift had begun plant startup and had been controlling feedwater in automatic most of the day with no abnormalities noted. Power was increased from 0.1 percent to 2.8 percent just as day shif t was ending. The change in power was not adequately communicated during shift turnover.
The night shif t came on at about 6:00 p.m. , noting the FCS in automatic cind I reactor power at about 3 percent. They believed that the reactor had been at this power level for some time. At about 6:30 p.m., the Control Room Supervisor (CRS) noted level oscillations beginning in the 21 SG and began monitoring level l closely. At about 7:15 p.m., the CRS directed the Control Room Operator (CRO) I to take manual control. The CRS had previously been informed that the feedwater regulating bypass valve had been modulating in automatic between 18 and 26 percent open throughout most of the previous shift and assumed, since he !
believed the plant had been at about 3 percent power during this time, that this was the proper-valve setting for this power level. At the time he ordered the bypass valve to be taken into manual, the CRS noted the valve to be at 32 percent. He therefore assumed that this was too far open and that the FCS was not controlling properly.
l NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO.3150-0104 (Fea EXPIRES 5/31/95
. EEMATED BURDEN PER RESPONSE To COMPLY WITH THtS lNFoRMAT1oN CouECT1oN REoVEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COMMENTS REGA5DNQ BURDEN ESDMATE To THE INFoRMATM j ANo RECORDS MANAGEMENT BRANCH (MNB8 7714), U.S. NUCLEAR TEXT CONTINUATION REGuuToRv Couuissa, wAsmNGioN. oC 20ssmot AND To THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE oF l
MANAGEMENT AND BUDGET, WA9HINGToN, DC 20503. l l
F ACluTY NAME (1) DOCKET NUMBER (4 LER NUMBER (3) PAGE (4)
Calvert Cliffs, Unit 2 05000 3 1 8 93 -
003 - 00 03 0F 06 TEXT in o,. w. ,.w,.a. .aoiuoa.i cop, oe NRc For. 38e4) (i7)
The CRS did not realize that what had actually happened was that, with the recent increase in power to 2.8 percent, the FCS had entered the region in which increases in power produced significant SG oscillations. At the time the bypass valve was taken into manual, SG 1evel was peaking and the FCS had closed the valve to bring level back down. With the bypass valve at 32 percent, SG 21 was actually in an underfeed condition. 1 The CR0 took manual control with SG level still increasing and at +25 inches.
He used the manual push-button controller to slightly close the valve. He noted that SG 1evel began decreasing almost immediately and assumed that this was the result of his actions. Actually, as noted above, the FCS had already closed the valve sufficiently-and the level decrease was due to this prior automatic action. The CR0 began briefly depressing the control button to provide small open commands to the feedwater bypass valve with the intention of bringing level smoothly to zero. As SG 1evel continued to decrease rapidly (3-4 inches per minute), the CR0 continued to apply slight open commands to the valve that he thought more than compensate 3 for the closure signal with which he started.
The previous SG 1evel control system had used a knob to control valve position.
The new system uses a membrane push-button with a logarithmic response. The longer the button is depressed, the faster the valve opens. The CRO was aware of the functioning of the new controller but was not aware of how little ;
response his short presses of the button actually produced. He did not use controller output indication to obtain feedback on the effectiveness of his j actions. He had previously been successful monitoring only SG 1evel indication and controller knob position when controlling SG 1evel with the old system.
1 Within 10 minutes after manual control was assumed, level dropped below zero and I was not responding appreciably to operator actions with the bypass valve. The CR0 continued single depressions of the controller in hopes of a gradual approach to zero inches. About five minutes later, with level approaching
-15 inches, the CR0 considered more aggressive feedwater injection but was I concerned with the effects of level shrink if large quantities of cold water were injected into the SG. When level reached about -20 inches, the CR0 took additional measures to increase level, including isolation of SG blowdown, placing the 22 feedwater bypass valve in manual and closing it slightly, and increasing 21 SG Feed Pump speed. The combination of these measures were effective in eventually terminating the drop in level at about.-45 inches.
However, minor level oscillations occurred, and low-level trip signals were j received by Safety Channels C and D. The reactor tripped at 8:05:09 p.m. The i total elapsed time for this event was approximately 45 minutes.
NRC FORM 366A ~ U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 pca EXPIRES 5/31/95
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F ACluTY NAME (1) DOCKET NUMBER (4 LER NUMBER (4 PAGE (4)
Calvert Cliffs, Unit 2 05000 3 1 8 93 -
003 - 00 04 0F 06 Ttna .v.c. % .m iwe aNRCr maca w)
The appropriate Emergency Operating Procedures were performed without incident.
II. CAUSE OF EVENT There are several causes of this event. The first is that the response of the FCS at low power was not known by Operations shifts other than the one that initially started up using the new system. This crew had observed the unanticipated oscillations, concluded that they were acceptable, and therefore did not communicate them to any other crews. The oscillations had not been discussed in training or modelled on the simulator as they had not been anticipated by the team developing the training. The crew involved in this event came on shift expecting no significant oscillations from the FCS.
A second cause is that the shift turnover did not address the increase in power that took place shortly before. This left the oncoming shift with no explanation for the SG level oscillations other than problems with the MS.
Knowledge of the power change, particularly if combined with information from the initial startup, may have helped the operators anticipate the level oscillations and either leave the FCS in automatic or understand better the need for increased feed flow in manual.
A third cause is the lack of Project Team involvement on this shif t. The new FCS was sufficiently complicated that not all plant response was anticipated. A similar system at another plant maintained a flat level trend at all power levels. The response of the FCS had been compensated for during initial startup and even during the day shift prior to this event by the presence in the Control Room of a member of the FCS Project Team. This individual had proven valuable during initial startup by discussing the oscillations with the FCS manufacturer and advising the shift crew on how to respond. A member of the team could have provided a similar service during this shift.
A fourth cause of thie event was the work practice of the CRO, who continued to underfeed the SG for about 35 minutes. He did not use controller output indication to verify the amount of movement the valve was making in response to his depressions of the control switch. A better understanding of the relationship of controller operation to valve movement might have resulted in more aggressive actions prior to the point where level shrinkage effects were significant. Crew supervision, including the SRO, failed to provide the CR0 sufficient coaching.
'NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 sea EXPIRES 5/31/95
. ESTIMATED BURDEN PER RESPONSE To COMPLY W"H THIS INFoRMATloN Cou.ECTioN REouEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COMMENTS REGARDING BURDEN ESTIMATE To THE INFoRMAThoN AND RECoRDG MANAoEMENT BRANCH (MNBB 7714), U.S. NUCl. EAR TEXT CONTINUATION REaut4 Tory CouuissoN, wAssNoToN. DC 20ss>ooot. AND To THE PAPERWORK REDUCTON PROJECT (31500104), OFFICE oF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
f ACluTY NAME (1) DOCKET NUMBER (2) LER NUMBER (3) PACE (4)
Calvert Cliffs, Unit 2 05000 3 1 8 93 -
003 - 00 05 0F 06 TEXT (If more space is required, use addmonal copes of NRC Form 300A) (17)
We have since experienced problems with automatic FCS control causing Operators to place FCS in manual. This indicates a need to improve FCS performance to reduce challenges to SG level control.
III. ANALYSIS OF EVENT The worst-case loss of feedwater flow transient described in the Updated Final Safety Analysis Report assumes a total loss of feedwater flow at full power and concludes that no significant safety consequences will result from this event.
This analysis is bounding for this event. There are no significant safety consequences resulting from this event.
This item is reportable under the provisions of 10 CFR 50.73(A)(2)(iv) as a Reactor Protective System actuation.
IV. CORRECTIVE ACTIONS A. Operations managece t will reemphasize expectations for communications bett an operating crews through better use of available mechanist (i.e., operator logs, turnover sheets, and turnover briefings) Operations management will review and discuss situational leadersi p with Shift Supervisors.
B. An FCS Froject Team representative will be available to the Control Room for fdture startups and planned shutdowns until FCS performance l meets expectations, and Operations personnel have gained sufficient i experience with the system.
J C. We will provide classroom training to all operating crews on the details of this event. We will also give Operators additional i hands-on training on the use of the push-button controller in l conjunction with valve controller output indication for the control of steam generator level.
D. FCS will be modified to improve performance.
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NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMD NO. 3150-0104 pea EXPIRES 5/31/95
- EST1 MATED BURDEN PER RESPONSE TO COMPLY WITH THIS i INFORMATION COLLECTION REQUEST: 50.0 HRS FORWARD l LICENSEE EVENT REPORT (LER) cOuuEurS REGARolNG BuRoEN ESTiuATE To THe woRuAToN AND RECORDS MAfuGEMENT BRANCH (MNBB 7714), U S. NUCLEAR TEXT CONTINUATION REGULATORY COMMtSSON, WASHINGTON. DC 20$5S@01, AND TO j THE FAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (3) PAGE (4) l Calvert Cliffs, Unit 2 05000 3 1 8 93 -
003 - 00 06 0F 06 L_
Tr.xT of more .p.co is requ6 red, use adchtional copies of NRC Form 306A) (17)
V. ADDITIONAL INFORMATION A. Affected Component Identification:
IEEE 803 IEEE 805 Component or System EIIS Funct System ID Steam Generator MX SJ Feedwater Control System TC SJ ;
Feedwater Regulating Bypass Valve LCV SJ Manual Push-button Controller LCO SJ B. Previous Similar Events:
LER 50-317/85-009 described a trip on low SG water level from 19 percent power due to underfeeding the SG in manual. ,
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