ML19274F816

From kanterella
Jump to navigation Jump to search
LER 79-048/01T-0 on 790719:w/reactor Shut Down for Refueling,Overcurrent Trip Devices in Supply Breakers for Reactor Bldg Motor Control Ctr Were Found to Be 300 Amp Instead of 600 Amp.Caused by Personnel Error
ML19274F816
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 07/30/1979
From: Coggin C
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19274F814 List:
References
LER-79-048-01T, LER-79-48-1T, NUDOCS 7908060474
Download: ML19274F816 (3)


Text

ti-ill LICENSEE EVENT REPORT CONTPOL BLC,CK: l l l l l l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

O fo [~l [G l Al E l I ! H j l l@L' l o 01010

't 14 LICENSE NVVBE 4 oIo olololol@l4 t il 11111@lbl C AI T b3l@

25 i%

F d LIC E YA E CGL E Is LICL'.st T)PE JJ CON'T oli []Z l L i@l 0l 5 l 010 j 0 l 3 l 2 l 1 ]@l 0 l 711 l 9 l 7 l 9 l@l0 l 7 l 3101719dJ @ 14 i 8 60 to t LOLF.E T *.UYilt a td 6) (VENT OATE 15 HEPONT DATE 1: VENT DESCNIPTICN AND PROCAaLE CONSEQUENCES h o . I With the reactor shutdown for refuelinq, while performing preventative maintenance I o ai l on the 600V G.E. AK-25 breakers, it was discovered that the over current trip l o .: l devices in the supply breakers for the reactor building motor control centers 1 B l loisi (R24-S011) and IC (R24-5012) were 300 amp trip devices instead of 600 amp trip devices l o r, I as desiqned. Because both divisions of the same system were involved both motor l 017' I control centers could have tripped if certain high load or fault conditions had l o ,!

! occurred. The busses have not been inoperable because of the 300 amp

~

(Continued) l 7 8 9 80 S C. T E \1 CAUST C A USE C O*,f P VALVE' COLE CCCE SU6CCUE CO'.iPONEN T CODE SU8 CODE SueCOCE olol d

lElB @ W @ 10 X l@ l Cl Kl Tl Bl Rl Kj@ l A @ l Zl@

i 3 Il 12 13 1 F> 13 20 SE QUE' ' I AL OCCURPENCE REFORT REVISION EVENTYEAR REPor NO CCDE TYPE N

@ g;g .g a pg 11 91 [---J l 0l ,l 8l l/l l 0l 1l lTl l -- l l 0l

_il 22 23 24 in 21 28 29 30 31 32 T E A TC O PL A T T HOVHS 22) S

  • ti D FOH 1 LB. PPLIE A' A T JJ A lglJ4Zl@ h Zl@ lZl@
6 l0 l0 l0 l 3/ 40 l

[Y l@

41 l fllg l A jg 42 43 l Gl 0l U"l R0lg 44 47 cau;E ot:CillPTION AND CORREC flVE ACTIONS h iso l Originally G E type AK-25 300 i amp breakers were specified, but when a design change ;

i i 1 l enlarged the motor control center busses and upgraded the feeder breaker amp ratings [

[ the trip devices were not replaced. This was due to personnel error in not implem g

, , l enting the change in the breaker size as indicated by the revised drawing. The , r ;

i .i I correct size trip devices have been installed and tested and the breakers (Cont.)  ;

7 8 9 80 ST t * *b POWE R OTHE R ST A TUS ISCOV FY DISCOV ERY DESCRIPTION 32 i

{ < l l Hi@ l 010 i 0 l@l fi/A l l lgl Routine preventative Mainte' Trance l A TIVITY CON TE N T HELE ASED OF RE Lf ASE A*.'OUNT OF ACTIVI TY LOC ATION OF RELE ASE i r> II/A ] fl/A

'LZ_l @ l Z !@l l

pen a N ,'tte<,o MEs Nu nts TvPt ot:CniPTiON@

l i l 7 l ] 0l 0l 0j@]@l ft/A l

' " ' ,EHsON.d',NiuPCs " So No..o n oEstn,TinN@

1 iI4 84 l0l0l01@l

') 11 12 ft/A 80 L OLS OF 09 OAVAGE TO F ACILIT Y YYP8 C E 0CHW f lON IiI,IIZl@l fi/A l 7 e 'J 10 80 e

2lo #l 7,Lfy E ' $[& 3Cll'P T)*J fi/A j lj;;;;;;;;; jj

' ' > ti8 69 80 .

~ ~

790806cm  %, . 9 2-367-7781 0

Georgia Power Company Plant E. I Hatch Baxley, Georgia 31513 Event Description and Probable Consequences (Continued) trip devices at anytime since initial energization. This is not a repeti tive occurrence. Public health and safety were not affected by this incident.

Cause Description and Corrective Actians (Continued) returned to service. The 600V breakers in both Unit 1 and Unit 2 have been checked and were found to contain the correct size trip devices.

Narrative Sumary LER 1-79-48 E,3._ " nit 1 was shut down for refueling, routine preventative maintenance was being performed on 600V AK-25 circuit breakers.

On 7-19-79, it was found that the supply breaker trip device for the reactor building 600/208V essential motor control centers IC (01VII R24-5012) were 300 ampere instead of 600 ampere as designed.

Trip devices are interchangeable on these breakers so it is possible to change trip settings by changing trip devices.

A check of documentation revealed that these were the original breakers with 300 amp trip devices that were preoperationally tested and engerized in May 1973. Further checking revealed that originally the design had calle for 300 amp trip devices and a drawing change prior to the preoperational test had changed these to 600 amp. This was in conjuction with an enlargement of the motor control center. When the motor control centers were preoperationally tested and energized in 1973, personnel failed to detect a drawing change and 300 breakers were left installed.

This error affects both divisions of the AC distribution system in the reactor building. Th' affected motor control centers are classified as "e ssenti al . " Neither motor control center has been inoperable because of the error at any time since initial energization. It has not been detennined whether an actual overload trip problem due to a heavily le:ded bus or many simultaneous motor starts or a breaker trip coord-inaticn problem existed during this time; however, as previously stated no prcalem was encountered during preoperational or startup testing or several years of operation. The correct breaker trip devices are now instailed and no further action is deemed necessary.

,,