ML18078A928

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IE Insp Repts 50-272/78-28 & 50-311/78-47 on 781119-1216.No Noncompliance Noted.Major Areas Inspected:Log & Records, Plant Cleanliness,Licensee Event Followups,Ie Circulars, Followup on Previous Insp Items,Test Procedures & Training
ML18078A928
Person / Time
Site: Salem  PSEG icon.png
Issue date: 01/19/1979
From: Keimig R, Nicholas H, Norrholm L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18078A927 List:
References
50-272-78-28, 50-311-78-47, NUDOCS 7903080025
Download: ML18078A928 (20)


See also: IR 05000272/1978028

Text

Report No.

U.S. NUCLEAR REGULATORY COMMISSION

OFFICE OF INSPECTION AND ENFORCEMENT

50-272/78-28

50-311/78-47

50-272

Region I

Docket No. 50-311


0 PR -70

c

License No.

CPPR-53


Priority -------

Category __

....;:;;B ...... l ___ ____

Licensee:

Public Service Electric and Gas Comoany

80 Park Place

Newark, New Jersey 07101

Facility Name:

Salem Nuclear Generating Station - Units 1 and 2

Inspection at:

Hancocks Bridge, New Jersey

Inspection

16, 1978

Approved by:

Inspection Summary:

, Chief ~~actor Projects

o. 1, RO(/F Branch

I- s-- 7 7

date signed

date s'i gned

Ins ections on November 19 - December 16, 1978 (Combined Re art Nos. 50-272/78-28

and 50-311/78-47

Unit 1 Areas Inspected:

Routine inspections by the resident inspector and

regional based inspectors of plant operations including tours of the facility;

log and record reviews;.plant cleanliness; followup on licensee events; IE

Circulars; and followup on previous inspection items.

The inspections involved

29 inspector-hours by the NRC resident inspector and 38 inspector-hours by one

regional based inspector and one intern.

Unit 2 Areas Inspected:

Routine inspections by the resident inspector and a

regional based inspector of plant preoperational testing including tours of

facility; test program controls; QA/QC surveillance of testing; test program

lementation; test procedu~e review and verification; *Witnessing of Hot

ctional Testing and other selected preoperational tests; comparison of

as-built plant with FSAR description; preoperational staff training; preparedness

for operating license including startup test program; followup on IE Bulletins

Region I Form 12

(Rev. April 77)

790308 () 0 :J- ~

1-

~spection Summary

2

and Circulars; and followup on previous inspection items.

The inspections

involved 84 inspector-hours by the NRC resident inspector and 132 inspector-

hours by one NRC regional based inspector.

Results:

One item of noncompliance was identified in one area with respect

to Unit 2 (Infraction - failure to identify status of turned-over equipment

and components, Paragraph 4).

No items of noncompliance were identified with

respect to Unit 1 .

DETAILS

l.

Persons Contacted

2.

PSE&G

R. Griffith, Site QA Engineer

C. Johnson, Startup Engineer

S. LaBruna, Maintenance Engineer

A. Meyer, Site QA Engineer

E. Meyer, Project QA Engineer

H. Midura, Manager - Salem Generating Station

W. Reuther, Site QAD

F. Schnarr, Station Operating Engineer

R. Silverio, Assistant to the Manager

J. Stillman, Station QA Engineer

W. Treston, Site QAD

J. Zupko, Chief Engineer

The inspector also interviewed other licensee personnel during the

course of the inspections including management, clerical, mainten-

ance, operations, performance, quality assurance, testing, and

construction personnel.

Status of Previous Inspection Items

(Closed) Follow Item (272/77-10-02):

Control Room bezel light bulb

reliability.

Based on performance testing, the licensee had concluded

that the type 376, 28 volt bulb would provide the longest servi~e

life in control room bezel indicators. The inspector verified that

action had been taken to assure that the correct bulb is reordered

when current stock is depleted.

(Closed) Unresolved Item (272/78-14-01):

Records of emergency kit

dosimeter drift checks.

The inspector verified that emergency kit

dosimeters* drift checks were conducted and documented by sampling

two dosimeters in one emergency kit ..

4

(Closed) Unresolved Item (272/78-19-01):

Revision to AP-24 to

clearly define the area of elevation 130' in containment which is

accessible during power operation.

Revision 2 to Administrative.

Procedure 24, Radiological Safety Program, issued November 14,

1978, defines in Section 6.5 the accessible area of containment

when the plant is at power, The inspector had no further questions

on this i tern.

(Closed) Noncompliance (272/78-21-01): Failure to maintain clear

isolation zone.

The inspector verified corrective actions taken by

the licensee to ensure that a clear isolation zone is maintained in

the vicinity of the protected area boundary.

(Closed) Noncompliance (272/78-22-01): Failure to retain surveil-

lance records.

The inspector conducted a sampling inspection of

surveillance records to verify.the effectiveness of licensee cor-

rective action.

No failure to produce the required records was

  • identified.

(Closed) Noncompliance (272/78-22-02): Failure to submit 30-day

report required by Technical Specifications.

The inspector reviewed

a revision to AP-6, Operational Incidents - Report Initiation,

Investigation and Followup, and the new AP-6-1 form.

The revised

procedures and form should be effective in preventing recurrence

of a failure to report items required by Technical Specifications.

No subsequent failures to report have been identified.

(Closed) Unresolved Item (272/78-24-01): Control room log minimum

operating limit for reactor coolant flow rate.

Based on a review

conducted by the licensee, Revision 9 to the Console Reading

Sheet was issued on November 7, 1978 establishing 94% as the

minimum loop flow rate. The inspector had no further questions

on this item.

(Closed) Unresolved Item (311/77-00-19): Testing of valve motor

operators. The inspector .made a random selection of thirteen

motot operated valves and verified that all had been tested com-*

pletely during Phase I tests:in April-June 1978.

The GTP-9

data sheet provided documentation of this testing for all motor

operated valves .

5

(Closed) Unresolved Item (311/78-20-01): Updating certificates of

qualification. Certificates of qualification for maintenance

department personnel have been updated to indicate currency.

In

addition, expiration dates hav~ been entered into the station

Inspection Order system to assure that future expirations of cer-

tificatiori does not octur.

  • (Closed} Unreso_lved Item (311/78-35-01)':. Controls on jurisd;-cational

tagging. This item has beerr upgraded to an item of noncompliance

-~ s~-~ _Detail,_ ~_aragraph 4).

Unit 1

2.

Review of Plant Operations

a.

The inspectors reviewed representative samplings of logs

and operating records for the period of September through

November, -1978.

Examples of the types of material reviewed

inc 1 uded the fo 11 owing:

1)

Senior Sf.lift Supervisor Log Book (not official)

2)

Control Operators Narrative. Logs (#2)

3)

Control Console Logs (#3)

4)

Primary Plant Logs (#6)

5}

Secondary Plant Logs (#7)

6)

Night Order Book

7)

Operations Directive Manual

8)

Rad Waste Operators Log Book

9}

Jumper/lifted Lead Records

10)

Operations Incident Reports

6

The inspector~ verified that logs are properly filled out

and initialed, provide adequate detail, do not conflict with

Techni~al Specifications or procedures; and, are being

reviewed by the staff. The inspectors verified the retriev-

ability of logs and records placed on microfilm.

No items

of*noncompliance or deviations were identified.

b.

The inspectors made a faci 1 i ty tour concentrating on general

plant housekeeping, fire protection and prevention, evidence

of leaks, excessive vibrations, radiation controls, etc. The

tour included observations of control room activities, log

taking, alarm responses, and manning requirements.

The inspectors observed that a large number of areas in the

Auxiliary Building were contaminated, and upon discussion

with licensee representatives, it became apparent that proper

control and decontamination of these areas was questionable.

The licensee agreed to improve controls and cleanup times

in this area.

The resident inspector will observe these

efforts on a continuing basis.to ensure that proper measures

are insti.tuted.

No items of noncompliance were identified.

c.

The resident inspector conducted a continuing review of plant

operations through daily, random inspection tours of the

facility with emphasis placed on control room operations.

During these tours, inspection is made relative to compli-

ance with selected Technical Specification Limiting Conditions

for Operation, maintenance of operating logs, control room

manning in accordance with the Technical Specifications and

10 CFR 50.54(k), and follow up on operational events.

The inspector noted that the licensee has clearly defined,

in a memorandum from the Chief Engineer dated December 4,

1978, the area within the control room which must be occupied

by the assigned "operator at the controls" of the reactor.

The inspector found that the definition provided is within

the guide 1 i nes of Regulatory Gui de 1 . 114 (Gui dance on Being

the Operator at the Controls of a Nuclear Power Plant).

No

failure to comply with the guidelines has been identified

by the inspector.

The lic~nsee stated that the definition

provided currently by memorandum will be included in a

revision to AP-5 (Operating Practices) to be issued prior

to February 1, 1979.

d.

Unit 2

7

On November 27, 1978, a loss of the 18 Vital Instrument Bus

resulted in a plant trip due to loss of one Reactor Coolant

Rump breaker status indication while operating above the P8

permissive setpoint.

The loss of the instrument bus was *.

caused by fai 1 ure qf the. inverter output transformer and

two regulating r-esistors. The bus 'failure also caused. all

steam lines to *1ndicate high steam flow (1 of 2).

Following

the trip~ auctioneered average temperature went low, apparently

due to undershoot as a result of steam dump operation. This

action caused a .safety injection due to the * combination of

high steam flow and low Tave.

Several ECCS components and

  1. 13 Auxiliary Feedwater Pump failed to start on the safety

injection. Subsequent analysis indicated that the ECCS

failures td start were directly attributed to loss of the

instrument bus and, therefore, to be expected by design.

The failure of the automatic start for #13 Auxi 1 i ary Feed-

water Pump is attributed to a misadjustment of the over.speed

mechanism.

The plant returned to.power on November 29 after

operability of the 18 Vital Instrument Inverter and #13

Auxiliary Feedwater Pump were verified .

The above events are detailed in Licensee Event Report 78-73/

OlT.

Final review of.this event will be made by the inspector

when a more detailed analysis of the transformer failure is.

available and potentially generic considerations have been

made.

No items of noncompliance were identified during review of

the above event.

3.

Preoperational Testing Quality Assurance

During witnessing of preoperational testing, the inspector verified

that QC/QA personnel were present conducting surveillance activities

and observing mandatory witness points.

QC personnel employ check-

1 ists to ensure all required aspects of test procedures in progress

have been addressed.

8

Through review of system turnover packages (POTT 10-01, Auxiliary

Feed and POTT 95-01, Reactor Solid State Protection System),

the inspector verified that QC/QA input ts solicited to ensure

that outstanding deficiencies are identified and tracked through

the turnover process.

Deficiencies noted during tonstruction and testing were identified

and tracked to.resolution.

The inspector reviewed Site QA Audit. SC-78-825 dated November.

17, 1978, which addresses test and startup activities. Three

items requiring followup were identified .. Resolution of two

was verified by.the inspector. The third item* relating to

jurisdictional tagging had not been adequately addressed by the

licensee at the conclusion of the inspection period. This item

identified items of a nature similar to those found by the inspec-

tor and which constitute noncompliance as delineated in Detail 4

of this report.

The inspector had no further questions r~lative to this area.

4.

Preoperational Test Program Implementation Controls

a. * To review the implementation of preoperational testing

controls, the inspector reviewed the following Preoperational

Test and Turnover (POTT) packages:

POTT 10-01 Auxiliary Feedwater System

POTT 95~01 Reactor Solid State Protection System

Further review of jurisdictional controls maintained in

these and other systems which had undergone turnover included

field observations of jurisdictional tagging and verification

that all parties at the site respected jurisdictional boundaries

such that post-turnover and post-test status remained valid.

The area of jurisdictional .controls was identified as a potential

probl~m area in NRC Inspection Report 50-311/78-35.

More de-

tailed review of the jurisdictional controls program identified

the following failures to maintain adequate controls:

9

During the week of October 9, 1978, valves 2SJ135,

21SJ134, 22SJ134, and interconnecting piping were found

not to have PSSUG jurisdictiOnal tags applied.

POTT of

the Safety Injection system was accomplished September

11, 1978.

  • .,._

During the week of October 2, 1978, the Safety I nj ecti on

Pump ammeter, located in the control room, was found not

to have PSSUG jurisdicti0nal tagging applied.

POTT of

the Safety Injection system was accomplished on September

11 ' 1978.

During the week of September 18~ 1978, Component Cooling

Pumps 21 and 22 4 KV breakers did not have PSSUG juris-

dictional tagging applied.

POTT of the Component Coolin~

system was accomplished on September 8, 1978.

Those portions of the Auxiliary Feed System bounded by

valves 23AF52, 23AF3, and the pipe junction downstream

of valve 23AF4 were found not to be jurisdictionally

tagged to the PSSUG on December 13, 1978.

POTT of the

system was accomplished on November 7, 1978 .

. On December 15, 1978, the 4 KV breakers for #21 and #22 *

Charging Pumps were found not to bear PSSUG jurisdictional

tags.

The pumps had already undergone preoperational

testing and POTT was accomplished on* October 31, 1978:

On December 13, 1978, construction personnel were observed

working on a suction flange for #22 Charging Pump.

The

system properly bore PSSUG orange jurisdictional tags.

No

authorization to work on the system was i'dentified.

POTT

of the system was accomplished on October 31, 1978.

10 CFR 50, Appendix B, Criterion XIV states, "Measures shall

be established to indicate by the use of markings such as

stamps, tags, labels, routing cards, or other suitable

means, the status of inspections and tests performed upon

individual items of* the nuclear power plant *.. These measures

shall provide for the identification of items which have

satisfactorily passed the required inspections and tests,

where necessary to preclude inadvertent bypassing of such

inspections and tests,

11

I --

10

Salem Startup Manual, Revision OA, Section 5.5, requires that

orange Turnover Identification Tags be applied by Public

Service at the time of Preoperational Test and Turnover

(POTT) and further states that respect for these tags is

  • mandatery. to prevent degradation of previously tested systems

and components.

Together, the above listed fai'lures to provide and maintafo

status indication for turned-over systems constitute an item

of noncompliance at the -Infraction level (311)78-47-01).

b.

Additional inspection was made to verify that a schedule of

peroperational. testing was maintained, that the quality of

. chemistry in safety related systems was maintained, that

preventive maintenance of turned-over systems is specified

and accomplished, and that corrective maintenance is accom-

plished by qualified persons using approved procedures.

With respect to the last item, the inspector observed corrective

maintenance being performed on #23 Charging Pump on December

13, 1978.

The work was being performed by qualified EPD

Maintenance Department personnel under Work Order TM-1049

using an approv.ed maintenance procedure and with Qt coverage.

Retest of the pump was still outstanding and scheduled to be

performed at the end of this inspection peri ad*.

The inspector* had no questions relative to the above.

5.

Preoperational Test Procedure Review

\\

a.

The office ~f Inspection and Enforcement (IE) Preoperational

Inspection Program dealing with Test Procedure Review has.

the objective of reviewing safety related tests for consistency

with regulatory requirements, guidance, and licensee commitments.

Uniform criteria are applied in the test procedure review

to assure the technical and administrative adequacy of the

procedures. This program is a sampling program which is an

ongoing effort conducted prior to.the performance*of said

tests and prior to the issuance of an operating license.

~

11

b.

The following approved tests were reviewed and verified:

SUP 19. 1 , Revis ion 1 , Approved October 26, 1978, Auxiliary

Building Ventilation

SUP 20~1, Revision 0, Approved November 22, 1978, Reactor

Protection/Emergency Safeguards Time Response Measurement

c.

The procedures were reviewed for technical and administrative

adequacy; and, to verify that adequate testing is planned to

satisfy regulatory guidance and licensee commitments.

The procedures were reviewed for the following:

Management approval,

Appropriate Committee review,

. Procedure *format,

Test objectives,

Prerequisites,

Environmental conditions,

Acceptance criteria,

References,

Initial conditions,

Performance verification,

Recording conduct of test,

Restoration of system to normal after test,

Evaluation of test data, and,

Quality control verification.

No discrepancies were noted in the review of these procedures.

12

6.

Witnessing of Preoperational Testing

a.

On Novemb~r 6, 1978, the licensee began a heat up of the

plant using Reactor Coolant Pump heat to actiieve normal

operating temperature and pressure (547°F at 2235 psig) for

the performance of Hot Functional Testing.

The heatup

sequence and testing at normal operating temperature were

witnessed by the NRC inspectors on site.

Plant cooldown was required twice prior to the completion

of testing due to system problems requiring repair on November

21 and November 30.

The final cool down, completing the Hot

Functional Test sequence was accomplished on December 9~

1978.

For a 11 testing witnessed and described below, the fa 11 owing

aspects, as a minimum, were verified by the inspector on a

  • sampling basis:

--

The latest procedure with appropriate approved changes

was available and in use by crew members .

The minimum crew requirements had been met.

Briefings had been conducted with test personnel as

required.

Adequate dry runs were held by all inspection teams.

Test prerequisites were met.

Special test equipment and instrumentation required by

the procedure was calibrated, inservice and manned by

test personnel.

  • Testing was being performed as required by the procedure.

Crew actions appeared to be correct and timely during the

performance of the test.

An data were collected for final analysis, by the .cog-

nizant test* personnel.

Test results observed by the inspectors indicated that

test*acceptance criteria had been met.

13

b.

Portions of the following specific tests were witnessed by the

inspectors:

SUP 50.0 ... Hot Functional Testfog - Heatup and Cooldown

This is the overall procedure governing the evoluti-0n and

establiihes prerequisites for heatup as well as sequencing

-other specific SUP

1 s to be conducted at temperature

plateaus of 150°f, 250°F, 345°F, 450°F, and 547°F.

SUP 50.6 - Pressurizer Pressure and Level Control Test

This test verifies operation of pressurizer heaters,

spray and the level control systems.

SUP 50.8 - Steam Generator Safety Valve Test

This test verifies the lift setting of each of the twenty

installed steam generator safety-valves.

SUP 50. 11 - Chemical and Volume Centro l System - Hot

This test is a comprehensive verification of the letdown,

charging, demineralizer, pump seal supply and boration

systems at normal operating conditions.

SUP 50.14 - Auxiliary Feed System Performance Test

This test verifies the design performance of each of the

three auxiliary feedwater pumps - two motor driven and

one steam driven.

SUP 50.15 - Control Room Inaccessibility

This test is a verification that the following functions

can be performed outside the control room to maintain the

plant in a safe, hot shutdown condition: charging and

letdown, makeup, pressure control, auxiliary feedwater,

and atmospheric steam relief .

14

c.

One instance was noted by the inspector in which QC. personnel

were not present when a Mandatory Witness Point step in SUP

50.0 was performed (Step 10.1.47.3).

The master copy of the

procedure was subsequently annotated to indicate that the

point was waived.

No items of noncompliance were identified during the witnessing

of preoperational testing.

7.

Operational Staff Training

To assess preparations for Unit 2 operation the inspector attended

training being conducted for Production Department operations,

performance and maintenance personnel. These personnel, currently

assigned.to Unit l, will be working at Unit 2 when operating.

The following training was observed by the inspector:

QA Level II Training for Supervisors

One session of SRO/RO Requalification Training

Two sessions of Technician-Nuclear (HP) Refresher training

The inspector verified that:

the specified training was conducted;

personnel on the attendance list were in attendance;

an unbi~sed test was administered;

environmental conditions were not detrimental to training;

instructor was adequately prepared; and,

the presentation addressed the assigned topics.

The inspector noted that, during the 1.icensed operat6r qualifi-

.

cation session, noise levels in the classroom were extremely dis-

tracting due to construction activity in the vicinity. Thi.s obser-

. vat ion was passed on* to station management.

The inspector had no further questions relative to the training

activities observed.

J

15

8.

Plant Tour

The inspector conducted periodtc tours of all accessible areas

in the plant.

During these tours, the following specific items

were evaluated:

Hot Work.

Adequacy of fire prevention/protection measures

used.

Fire Equipment..

Operability and evidence of periodic inspec-

tion of fire suppression equipment.

Housekeeping.

Minimal accumulations of debris and maintenance

of required cleanness levels in systems under or following

testing.

Equipment preservation. Maintenance o.f special preservative

measures for installed equipment as applicable.

Component Tagging.

Implementation and observance of equipment

tagging for safety or equipment protection.

Maintenance.

Corrective maintenance in accordance with

established procedures.

Instrumentation. Adequate protection for installed instru-

mentation.

Cable Pulling. Adequate measures taken to protect cable from

damage while being pulled;

Communication.

Effectiveness of public address system in

all areas of the site.

Equipment Controls. Effectiveness of jurisdictional controls

in precluding unauthorized work on systems *in test or which

have been tested (see Detail Paragraph 4).

Logs.

Completeness of logs maintained and resolution of

identified problems.

Foreign Material Exclusion. Maintenance of controls to assure

systems which have been cleaned and flushed are not reopened

to admit foreiqn material.

.

'

~

1'6

Security. Implementation of security prov1 s1 ans.

Parti -

cular attention to maintenance of the Unit 1 protected area

boundary.

Testing.

Spot-checks of testing in progress were made.

Except as identified in other sections of this report, the inspector

had no

questiCms~r..e*la.tive:-to*- p.lan*t tours.

9.

Comparison of As-Built Plant to FSARDescription

As a continuing effort until licensing. of the unit, the inspector

is performing a verification, using construction prints and field

observations, that various safety-related systems have been con-

structed as described in the facility Final Safety Analysis Report.

During this inspection period~ the inspector made a series of field

observations related to the Emergency Diesel Generator Systems and

the Solid State Protection System, to verify that arrangements

were as described in Sections 7 and 8 of the Final Safety Analysis

Report~ These observations included diesel generator arrangement

and capacity, separation criteria for -control cable, arrangement

of pressurizer level indication piping, reactor coolant flow rate

instrumentation, measurement (independent by the inspector) of

ambient temperatures of safety related instrumentation during Hot

Functional Testing to verify temperatures less than 120°F.

In addition, the following prints were reviewed to verify that

the Solid State Protection System provides the functions stated

in the Final Safety Analysis Report:

PSBP 221050

Revision 2

PSBP 221051

Revision 2

PSBP 221052

Revision 2

PSBP 221053

Revision 2

PSBP 221054

Revision 2

PSBP 221055

-*Revision 3

PSBP.221056

Revision 2

PSBP 221057

Revision 4

PSBP 221058

Revision 1

17

10.

PSBP 221059

Revision 3

PSBP 221060

Revision 2

PSBP 221061

Revision 2

PSBP 221062

Revision 2

PSBP 221063

Revision 2

PSBP 221064

Revision 3

PSBP 221065

Revision 2

The inspector had no questions relative to the items reviewed ..

O~erational Readiness

a.

10 CFR 50.57 states that the issuance of an operating license

is, in *part, contingent upon a finding that construction of

the facility has been substantially completed, in conformity

with the construction permit and -the application, as amended,

the provision of the Act, and the rules and regulations of the

Commission; and that the facility will be operated in conformity

with the applications as amended, the provisi~ns of the Act,

and the rules and regulations of the Commission.

In order to provide a basis for this finding, the inspector

_is conducting a continuing review of licensee readiness to

operate the facility. Thi.s review includes, but is not

limited to, the following areas:

Completion of the NRC inspection program to assess construc-

tion, testing and operational preparedness.

Status of facility operating procedures and personnel

training.

Status of all enforcement items and unresolved matters.

Status of the pteoperational test program.

Status of constructibn activities. *

Review of licensee outstanding items, particularly those

identified for completion or resolution after core load.

Site

18

Implementation of corrective measures for Unit 2 as a

result of items identified in Unit 1 from Reportable Occur-

rences, inspection findings, and IE Bulletins*and Circulars.

Operational safety.concerns arising from the above reviews will

be promptly identified to facility management for resolution

prior to the inspector reaching a finding of operational

readiness.

No specific safety concerns have been identified

to date.

b.

As part of the above evaluation, the inspector selected a

sampling of 43 Design Change Requests describing changes

made to Salem Unit 1 pursuant to 10 CFR 50.59.

These 43

DCR's were .reviewed to ensure that appropriate consideration.

had been given to their applicability in the design of Salem

Unit 2.

No failure to incorporate applicable design changes

into the origirlal design, drawings, or through Engineering

.

Change Notices (ECN's) for Unit 2 were identified.

For those

determined to be non-applicable, the inspector had no questions.

c.

The inspector initiated a review of the Phase II (Startup

and Power Ascension) Test program.

The program is expected

to parallel the testing conducted for Unit 1.

However, no

documented program definition, sequence or test procedures

have been issued to date.

The inspector stated the Regulatory

Guide 1.68 requirement that test procedures should be

available for NRC review 60 days prior to proposed testing.

This was acknowledged by the licensee.

11.

IE Bulletin and Circular Followup

a.

The IE Bulletins discussed below were reviewed to verify that:

Licensee management forwarded copies of the response to

the bulletin to appropriate onsite management represen-

tatives.

Information discussed in the licensee's reply was sup-

ported by facility records or by visual examination of

the facility.

Corrective action taken was effected as de~c~ibed in the

reply.

19

The licensee's reply was prompt and within the time

period described in the bulletin.

The review included discussions with Hcensee personnel and

observation and review of items discussed in the details

below.

b.

By correspondence dated February 21, 1978, the licensee

responded to IE Bulletin 78-01 (Flammable Contact Arm

Retainers in GE CR~l20A Relays)~ stating that the subject

relays were not in use at either Salem facility. This

has been verified at Unit 1 (NRC Inspection Report 50-272/

78-09).

During the course of this inspection, the inspector

veftfied that no .GE CR-120A relays were in use at Salem

Unit 2.

c .. By correspondence dated March 23, 1978, the licensee responded

~

to IE Bulletin 78-04 (Environmental Qualification of Certain

Stem Mounted Limit Switches Located Inside Reactor Containment)

stating that seal-in circuit modifications or replacement of

the suspect switches would be accomplished prior to issuance

of an operating license for Unit 2.

The inspector reviewed

the implementing Engineering Change Notice (ECN 35195) and

noted that circuit changes only were addressed.

Inspection

of containment isolation valves indicated that several

employed NAMCO D2400X limit switches for position indication.

A licensee representative stated that the switches in ques-

tion would. also be replaced.

The inspector stated that

this item will be reviewed again when replacement of the

switches is complete (311/78-47-02).

d.

IE Circulars .di.scussed: below were reviewed to verify that

they had been reviewed for applicability by cognizant manage-

ment, and appropriate action initiated.

The review included discussions with licensee personnel and

bbservation and review of* items .discussed.in the details

below.

....

I

20.

--

IE. Circular 77-15 (Degradation of Fuel Oil Flow to the

Emergency Diesel Generators) is addressed in Safety

Evaluation SGS/M~SE-025 dated June 27, 1978 which is

further implemented by surveillance procedure SP (0)

4.8.1.1.2. The inspector had no further questions

on this item.

IE Circular 78-02 (Proper Lubricating Oil for Terry Tur-

bines) is addressed in NRC Inspection Report 50-272/78-15

for Unit 1.

The inspector had no additional concerns

relative to Unit 2 in this* area.

IE Circular 78-17 (Inadequate Guard Training/Qualification

and Falsified Training Records) had* been received and

reviewed by cognizant licensee personnel.

Despite a

concluston that the problems delineated in the Circular

do not apply to Salem Generating Station, the licensee

has elected to perform a comprehensive audit of guard

training and qualification.

In addition, the inspector

verified, through observation of security force requalifi-

cation, that scores recorded at the firing range reflected

actua 1 performance of the persons observed .. The inspector

had ho further questions in this area.

12.

Unresolved Items

Areas for which more information is required to determine accept-

ability are considered unresolved.

An unresolved item is contained

i~ Paragraph llc. of this report'.

13.

Exit Interview

At periodic intervals during the course of this inspection, meetings

were held ~lith senior facility management to discuss inspection

scope and findings .