ML18102A190

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Insp Repts 50-272/96-06 & 50-311/96-06 on 960407-0518. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering,Plant Support & Mgt Meetings
ML18102A190
Person / Time
Site: Salem  PSEG icon.png
Issue date: 06/18/1996
From: Larry Nicholson
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18102A189 List:
References
50-272-96-06, 50-272-96-6, 50-311-96-06, 50-311-96-6, NUDOCS 9606240241
Download: ML18102A190 (60)


See also: IR 05000272/1996006

Text

Docket Nos:

License Nos:

Report No.

Licensee:

Facility:

Location:

Dates:

Inspectors:

  • Approved by:

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

50-272' 50-311

DPR-70, DPR-75

50-272/96-06, 50-311/96-06

Public Service Electric and Gas Company

Salem Nuclear Generating Station, Units 1 & 2

P.O. Box 236

Hancocks Bridge, New Jersey 08038

April 7, 1996 - May 18, 1996

C. S. Marschall, Senior Resident Inspector

J. G. Schoppy, Resident Inspector

T. H. Fish, Resident Inspector

Larry E. Nicholson, Chief, Projects Branch 3

Division of Reactor Projects

9606240241 960618

PDR

ADOCK 05000272

G

PDR

EXECUTIVE SUMMARY

Salem Nuclear Generating Station

NRC Inspection Report 50-272&311/96-06

This integrat~d inspection included aspects of licensee operations,

engineering, maintenance, and plant support. The report covers a 6-week

period of resident inspection; in addition, it includes the results of

announced inspections by a regional engineering inspector, attached as a stand

alone feeder to this report.

Operations

The operating shift demonstrated good outage risk management and effective

control of complex evolutions in the successful execution of a component

cooling water (CCW} system outage (Section 01.2}.

Operators repeatedly displayed good awareness of the potential safety impact

of a no. 23 service water (SW} pump strainer trip. They appropriately took

aggressive acti-0ns to insure availability of a heat sink (Section 01.3).

Reactor engineering thoroughly evaluated and maintenance effectively

controlled a transf~r of new fuel from the Unit 1 to the Unit 2 new fuel

storage pit (Section 01.4).

Operators quickly detected a loss of overhead annunciators (OHA} for Salem

Unit- 2.

Technicians caused the problem through use of a faulty probe. * The

technicians should have identified the problem with the probe before using it.

The symptoms of the loss of OHA differed from symptoms previously identified

during system failures. Operators considered the OHA problem resolved when

technicians addressed the symptoms of the failure. Operator failure to insure

that technicians had identified and corrected the underlying cause indicated

poor understanding and application of effective corrective action (Section

01.5).

Operators discovered that river water temperature had exceeded the temperature

limit assumed in a temporary modification for the no. 12 component cooling

water heat exchanger (CCWHX}.

The operations staff appropriately determined

operability based on engineering judgement, and initiated further engineering

analysis. Engineering did not effectively communicate to the control room

operators that the temporary modification restricted operation of the no. 11

CCWHX, nor that the staff had made changes to the CCW operating procedure to

implement those restrictions (Section 02.2}.

Operators made timely and appropriate notification to the. NRC for discovery of

a suspected controlled substance (Section 04.1}.

The management review committee (MRC} appropriately concluded that plans and

actions to address weak root cause skills were acceptable.

The MRC also

concluded that insufficient objective evidence existed to accept that

corrective action effectiveness had sufficiently improved.

As a result, the

MRC deferred approval of this problem statement. The MRC appropriately

ii

questioned the presenter; their decision to defer the approval of corrective

action effectiveness reflected a strong safety ethic (Section 07.1).

Although the MRC frequently added to the quality of efforts by the Salem

staff, inspectors noted inconsistency in the quality of MRC reviews.

The MRC

charter lacks guidance for review of the Restart Action Plans, the Startup and

Power Ascension Plan, the affirmations of NRC Restart Issue Completions, or

the closure of other items affecting startup (Section 07.2).

The Quality Assurance and Nuclear Safety Review (QA/NSR) department reports

for January/February 1996 and March 1996 provided substantive assessment of

Sal em performance.

The reports reflect significant improvement in the

organizations ability to identify performance strengths and weaknesses, and

communicate them to PSE&G management.

The QA/NSR reports, however, missed a

number of opportunities to provide information on performance trends from one

period of assessment to the next (Section 07.3).

The inspectors concluded that Salem did not initiate and complete license

change requests in a timely manner after they identified Technical

Specification discrepancies (Section 08.1).

Maintenance

Salem engineers corrected a licensee-identified omission in the surveillance

procedure for auxiliary feedwater response time (Section Ml.2) .

Maintenance technicians' poor foreign material exclusion practices resulted in

introduction of material from grinding onto safety injection pump internals.

Maintenance technicians provided less than adequate documentation of safety

injection pump repair activities (Section M3.l).

Engineering

Salem had not updated the Final Safety Analysis Report to reflect license

amendments dated May 4, 1994, pertaining to changes to spent fuel pool design.

Since the licensee did not complete the design changes until December 1995,

however, the inspectors concluded that PSE&G met the requirements of 10 CFR

50.7l(e).

(Section El.I)

A recent discovery of a licensee operating their facility in a manner contrary

to the Updated Final Safety Analysis Report (UFSAR) description highlighted

the need for a special focused review that compares plant practices,

procedures, and parameters to the UFSAR description. While performing the

inspections discussed in this report, the inspectors reviewed applicable

portions of the UFSAR that related to the areas inspected.

The following

inconsistencies were noted between wording of the UFSAR and the plant

practices, procedures, and parameters observed by the inspectors: auxiliary

feedwater surveillances (Section Ml.2}, service water strainer malfunctions

(Section E2.l), a degraded jacket water after-cooler heater (Section E2.2),

iii

fuel handling area ventilation discrepancies (Section E7.l), and spent fuel

pool cooling.

(Section El.I)

Service water pump strainer malfunctions represent nonconformance with the

automatic, self-cleaning features specified in the Final Safety Analysis

Report (FSAR section 9.2.1.2) and a ~hallenge to SW system reliability

(Section E2.1).

Engineering did not evaluate a degraded emergency diesel generator jacket

water after~cooler heater with regard to UFSAR requirements.

Failure to

perform a 10 CFR 50.59 safety evaluation is unresolved pending resolution of

similar nonconformances with the UFSAR and licensing basis (control air and

fuel handling building ventilation) (Section E2.2).

Engineering failure to insure that FHAV maintained the required differential

pressure during normal operation is unresolved pending completion of

inspection of related ques:tions concerning compliance with regulatory,

licensing basis, and design basis requirements* (Section E7.1).

Between April 8 and May 14, four station air compressor trips and two

additional compressor failures required operators to take contingency actions ..

Inspectors concluded that maintenance and system engineering staff did not

effectively ensure station air system reliability (Section ES.I).

The inspector's review of five previously identified issues indicated

acceptable resolution in most cases. Calculations and analyses were usually

  • detailed and thorough and the evaluations indicated, in general, good

understanding of the identified issues.

The evaluation of the other two

issues, pertaining to onsite fuel oil availability and EOG load fluctuations

analysis, was less than thorough.

In the first case, the evaluation failed to

ensure the availability of the emergency connection to the diesel fuel oil

storage tank.

In the second case, the root cause analysis failed to address

the changes made to the system while troubleshooting, thereby potentially

invalidating the analysis (Stand alone feeder).

The inspectors concluded the 10 CFR 50.59 evaluations performed for the

advanced feedwater control system (ADFCS) modifications may not have been

performed correctly. This remains an unresolved item.

It appears that the

possibility for a different type of initiating event or a malfunction of a

different type than any evaluated previously in the USFAR may be created, even

though the licerisee stated that the modified analyses show the effects are

bounded in some instances (Section EB.4).

The inspectors determined through interviews that engineering judgement based

on operational experience at other ADFCS plants and computer simulations most

likely formed the bases for the Salem values of the sampling rates and

processing delays (Section EB.4).

The inspectors concluded that the setpoints and control constants were based

on empirical data and analyses from other ADFCS plants, with the necessary

particularization for Salem (Section EB.4) .

iv

The inspectors concluded. that the licensee considered EMI suscepti-bility.

(Section EB.4).

The inspectors concluded, based on their limited scope of V&V audit, that the.

retrofit of a V&V program to the ADFCS increased the accuracy and consistency

of the software with the system drawings (Sectioh E.7).

In the Salem ADFCS, the inspectors concluded that most of the cross".'"connected

data are used in MSS algorithms and the "last .data val~es" are used on loss of

data. These factors tend to moderate any functional problems caused by cross-

connected ~ata corruption or loss {Section E.7).

The inspectors concluded that, prior to DCP closeout, the configurat~on

control process for the ADFCS was successful due to knowledgeable software

engineers, in the absence of software-specific guidance.

The inspectors also

concluded that the software configuration control procedures provided for

post-DCP closeout were adequate for controlling software changes {Section

E. 7) ~

The inspectors concluded that the ADFCS access control provided sufficient

security for the system (Section E.7).

The inspectors concluded that the licensee met their HMI design objective of

minimizing impact on plant operations personnel (Section E.7) .

-

-

~he inspectors concluded that the use of the ADFCS trainer was an effective

method for enhancing the technical quality of the I&C maintenance activities.

{Section E.7).

-

Over-all, the engineering .performed for the ADFCS modification* generally met

design objectives.

The inspectors need to confirm that the feedwater control

reliability problems noted in inspecti-0n report 94-13 were completed.

Therefore, restaft action item II.4 remains open (Section E.7).

Plant Support

Overall, during requalification_training, operators demonstrated significant

improvement in .command and control, technical competence, and teamwork.

In

one case, however, a Senior Nuclear Shift Supervisor {SNSS) incorrectly

classified a postulated event. The lesson plah fci~ the event contained the

incorrect ~lassification, the instructor did not detect the error and did not

take appropriate corrective action until the NRC questioned the corrective

action and the operations manager became involved (Section P4.l).

During an unannounced call out Emergencj Preparedness {EP) exercise, the

Emergency Response Organization {ERO) met the goal of manning the Technical

Support Center (TSC) and the Emergehcy Operations Facility (EOF) within 90

minutes. Overall, the ERO adequately discharged its duties required to protect

the health and safety of the public, however, the EP staff reduced the

effectiveness of the training by not allowing the ERO staff, in some cases, to

make errors (Section PS.I).

v

Salem management responded aggressively and quickly to the report of discovery

of an apparently illegal substance in the protected are~. Their actions were

comprehensive and notifications were timely.

By including a search of Hope

Creek facilities, management showed sensitivity to the generic implications of

discovering an apparently illegal substance in the protected area. The

inspectors concluded Salem management responded appropriately. Laboratory

tests later concluded the substance was a powdered coffee creamer (Section

Sl.1) .

vi

..

EXECUTIVE SUMMARY

TABLE OF CONTENTS

I. Operations ..

II. Maintenance ..... .

III. Engineering

'IV. Pl ant Support .

V. Management Meetings

TABLE OF CONTENTS

0

vii

ii

vi

1

10

13

20

23

Report Details

Summary of Plant Status

Unit 1 and Unit 2 remained defueled for the duration of the inspection period.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent

reviews of ongoing plant operations.

In general, plant staff conducted

professional and safety-conscious operations. Specific events and

noteworthy observations are detailed in the sections below.

01.2 Unit 2 Component Cooling Water Outage. NRC Restart Inspection Item III.7

(71707)

The inspector observed the operating shifts' preparation and execution

of a Unit 2 component cooling (CC) water maintenance outage. Operations

management planned the activity to minimize shutdown risk. This

included a comprehensive contingency plan involving increased spent fuel

pool temperature monitoring and backup cooling strategies.

On April 25,

1996, operators implemented the plan and maintained a good safety

conscious focus throughout the CC system outage.

The operating shift

prioritized and controlled the related activities to effectively shorten

the outage duration (25.6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> actual/46 hours planned) resulting in a

shutdown risk reduction.

In conclusion, the operating shift

demonstrated good outage risk management and effective control of

complex evolutions in the successful execution of a component cooling

water outage.

01.3 Service Water Strainer Trip. NRC Restart Inspection Item III.7

a.

Inspection Scope (71707)

b.

The inspectors assessed operator response to a service water (SW) pump

strainer trip.

Observations and Findings

On April 18, at 9:19 a.m., no. 23 SW pump strainer tripped on thermal

overload. Operators reset the overloads, then restarted the strainer so

that electricians could troubleshoot it. Electricians reported normal

strainer amperes and operators returned the strainer to automatic

operation.

The strainer tripped again at 10:55 a.m .. At the time of

the malfunctions operators had only the nos. 22 and 23 SW pumps

available as the heat sink for Unit 2 Spent Fuel Pit (SFP) cooling.

In

2

response to the second strainer trip, operators established security at

no.- 2 service water bay door, suspended de-silting operations at the

service water intake structure, and expedited returning no. 21 SW pump

to service. Operators started no. 21 SW pump at 12:19 p.m .* The

strainer malfunction did not affect SW header pressure or SFP

temperature.

Operators recognized that the trip of no. 23 SW pump strainer rendered

no. 23 SW pump inoperable and left them with only one operable SW pump

(no. 22) to provide a heat sink for SFP cooling. They also recognized

that when they returned no. 21 pump to service, they could not consider

it operable because technicians had not co~pleted their post maintenance

tests. Finally, operators recognized that since the same vital bus

powers nos. 21 and 22 SW pumps, SFP cooling was vulnerable to any

adverse conditions that could challenge bus reliability.

c. *Conclusions

Operators repeatedly displayed good awareness of the potential safety

impact of a* no. 23 SW pump strainer trip. They appropriately took

aggressive actions to insure availability of a heat sink.

01.4 Transport of New Fuel

a.

Inspection Scopa (60705)

The inspector reviewed reactor engineering's 10 CFR 50.59 safety*

evaluation for the transfer of new fuel from the Unit 1 new fuel storage

pit to the Unit 2 new fuel storage pit.

In addition, the inspector

observed the h*ndling, transfer and storage of the new fuel.

b.

Obse~vations and Findings

On April 21, 1996, reactor engineering completed a thorough 10 CFR 50.59

safety evaluation to address the movement of new fuel between units.

Reactor engineering determined that there was no expected adverse

radiological effects to the station personnel or public.

In addition,

there was no expected adverse effects to the fuel assemblies, plant

systems or structures.

During the week of April 29, maintenance moved 16 fuel assemblies from

Unit 1 to Unit 2. Maintenance used existing procedures and equipment to

support this move.

Reactor engineering conducted a new fuel receipt

inspection of the transferred assemblies ~s if the new fuel arrived

directly from the vendor.

Mechanical maintenance, reactor engineering,

operations, and radiation protection conducted the fuel movements with

methodical precision and tedious attention~to-detail. The mechanical

maintenance supervisor effectively controlled the activity.

In

addition, Quality Assurance provided good oversight of the process .

c.

3

Conclusions

Reactor engineering thoroughly evaluated and maintenance effectively

controlled a transfer of new fuel from the Unit 1 to the Unit 2 new fuel

storage pit.

01.5 Loss of Overhead Annunciators. NRC Restart Item 111.40

a.

Inspection Scope (71707)

b.

The inspectors observed operator and maintenance staff response to a

loss of overhead annunciators.

Observations and Findings

During an 18 month surveillance of the Salem Unit 2 control room

overhead annunciators (OHA) on May 8, operators determined that the OHA

stopped re~ponding to plant conditions. The operators initiated the

steps of abnormal procedure S2.0P-AB.ANN-0001(Q), Loss of Overhead

Annunciator System.

The response directed by the procedure included

increased monitoring of critical plant functions, including service

water, component cooling water and spent fuel pool

co~ling. The

operators also implemented measures to protect these systems from

activities with potential to adversely affect their operation.

As

directed by procedure, operators attempted to shift from Sequence of

Events Recorder (SER) 'A' to SER 'B' with no change in OHA response.

(The SERs are microprocessors that receive input from the plant through

eleven scanner cards, process the information, and pass it through to

control room annunciators, printers, and alarm display monitors.)

Instrumentation and controls (l&C) technicians, with close supervisor

involvement, postulated that the technicians had caused the OHA loss of

function.

They postulated that the technicians used a defective test

instrument probe that momentarily grounded a power supply, causing the

scanner cards to stop communicating to the SERs.

After the technicians

briefly interrupted power to the scanner cards, the cards resumed

communication with the SERs and restored OHA function.

The technicians

continued trouble shooting by demonstrating that the faulty probe caused

comparable symptoms in a partial OHA system set up for training.

Maintenance supervisors concluded that technicians inappropriately used

the faulty probe, since they should have detected the potential for

shorting a power supply through visual inspection of the probe.

After technicians restored OHA function the operators demonstrated that

the OHA system functioned properly, exited the abnormal procedure, and

returned to the previously implemented measures for the degraded OHA

with the reactor defueled.

The inspectors noted that the operators

relaxed their compensatory measures after the technicians restored

functionality to the OHAs, but prior to verifying the suspected cause.

The inspectors concluded that the operators considered corrective action

complete for the immediate problem based on correcting the symptoms

-.

4

without insuring that technicians had identified and corrected the

underlying cause.

c. Conclusions

Operators quickly detected a loss of OHA for Salem Unit 2. Technicians

caused the problem through use of a faulty probe.

The technicians -

should have identified the problem with the probe before using it. The

symptoms of the loss of OHA differed from symptoms previously identified

during system failures. Operators considered the OHA problem resolved

when technicians addressed the symptoms of the fa-i lure. Operator

failure to insure that technicians had identified and corrected the

underlying cause indicated poor understanding and application of

effective corrective action.

02

Operational Status of* Facilities and Equipment

02.1 Control of Plant Configuration. NRC Restart Item 111.2

a.

Inspection Scope (71707)

Inspectors reviewed temporary modification 95-073, revision 0, to insure

that the licensee mainfained a safe plant configuration for the existing

mode of operation.

b.

Observations and Findings

During the current Salem Unit l outage, plant staff removed valves in

the service water system supplying the no. 12- component cooling water

heat exchanger (CCWHX).

The plate type no. 12 CCWHX consists of two

sections, no. 12A and no. 128.

Plant workers installed flanges to

isolate service water to the no. 12A section of the heat exchanger.

Engineering based the acceptability of the temporary modification on an

assumption that the no. 11 CCWHX remained continuously available while

the flanges remained in place. The modification also assumed that the

Delaware River temperature would remain below 58.3 degrees F for the

duration of the modification.

On May 2, the inspectors noted that river water temperature exceeded 60

degrees F.

Operators had previously identified that river temperature

exceeded 58.3 degrees F and initiated a Condition Report.

The operators

  • considered the CC system operable, since engineering based the limit of

58.3 degrees F on the ability of CC to dissipate the heat generated

during plant startup. Operators realized that worst case heat loads for

the defueled unit were substantially less than the assumed conditions.

Engineering subsequently calculated a river water limit of 90 degrees F

for current plant conditions.

The inspectors questioned the controls for insuring no. 11 CCHX remained

in service .. Control room operators did not know that engineering had

initiated a change to the operating procedure requiring that no. 11 CCHX

c.

5

remain in service for the duration of the modification.

In response to

the inspectors' questions, operators initiated a CR to document

ineffective controls to insure the plant remained within analyzed

conditions resulting from a temporary modification, and a CR to document

ineffective communication of procedure changes to the operating staff.

The inspectors noted that, as a result of the operators' concern over

river water temperature, the no. II CCWHX remained available or in

service throughout the duration of the temporary modification.

Conclusions

Operators discovered that river water temperature had exceeded the

temperature limit assumed in a temporary modification for the no. I2

CCWHX.

They appropriately determined operability based on engineering

judgement, and initiated further engineering analysis. Engineering did

not effectively communicate to the control room operators that the

temporary modification restricted operation of the no. II CCWHX, nor

that the staff had made changes to the CC operating procedure to

implement those restrictions.

04 Operator Knowledge and Performance

04.I Event Notification

On April II, the inspectors observed operator response to the report of

a suspicious substance found in a locker room in the Protected Area.

Details are in Section SI.I of this report ..

The inspectors concluded that the operators made timely and appropriate

notification to the NRC, in accordance with* IO CFR 26.73 and 10 CFR

50.72(b)(2)(vi).

07

Quality Assurance in Operations

07.1

NRC Restart Action Plan Item III.IO. Corrective Action Plan COpen)

a.

Scope

The NRC issued its Restart Action Plan (RAP) on February 23, I996 that

defined the scope of activities that the NRC will address prior to

restart.

RAP Sections II and III list 43 technical and 2I programmatic

items that the NRC plans to inspect prior to restart. This inspection

addressed one of those items: the Corrective Action Plan.

b. Observations and Findings

On April I9, I996, the Manager - Corrective Action and Quality Services

(CA & QS), forwarded the closure package for problem statement No. 5 of

their Corrective Action Plan (CAP) which states that, "Root cause

analysis skills and procedures are weak.

Corrective actions are often

6

not effective at preventing recurrence." Licensee policy requires that

this closure plan prdvides the "objective evidence" to ensure that this

item has been satisfactorily addressed.

The plan sponsor, the

Corrective Action Group (CAG), combined each of the problem statement

No. 5 sub-statements into three major initiatives: (1) Improve the

Nuclear Business Units (NBU) overall knowledge of cause analysis, (2)

Improve the procedure for cause analysis, (3) Develop and publish

expectations for root c~use evaluations.

Improve, monitor, and assess

the adequacy of evaluations and effectiveness of corrective actions.

Regarding the first item, the licensee has developed training using

input from industry root cause experts. The licensee's new focus on

root cause (RC) is to train a smaller number of specialists that can be

dedicated to RC on more-or-less a full time basis versus the previous

approach of training every engineer on-site and giving them little or no

experience with actual plant problems or events. This was an

improvement over previous practice.

Regarding the second item, the licensee developed a new Root Cause

Manual (RCM) that incorporated the best ideas from a sample of other

nuclear utilities, including: its layout, use of:illustrations and

diagrams, and overall simplicity. The RCM provides very specific

direction on the scope and content of Root Cause Analysis Reports. This

. was also an improvement over previous practice .

For the third item, the licensee published expectations for level 1 and

2 evaluations in NAP-06, the corrective action program procedure, and

the RC manual.

Regarding improving corrective action effectiveness, the

licensee initiated a Corrective Action Review Board (CARB) to evaluate

the quality of level 1 condition reports (CRs).

The board consists of

the Station General Manager and other key managers and has been

monitoring the quality of level 1 CRs.

Based on a sampling of the

performance indicators and the CARB minutes, the inspector noted that

the quality of these evaluations has improved over the past three

months.

However, ultimately, corrective action effectiveness will be

verified when continued uneventful power operation is achieved.

On April 25, the inspector observed the presentation of Problem

Statement No. 5 of Corrective Action Program to the Management Review

Committee (MRC).

The April 19 closeout package provided the underlying*

basis for the presentation. The p~esenter stated that the root cause

training had been completed and that the RC manual was being actively

used for Level 1*and 2 CRs.

The MRC questioned him at length and

determined that sufficient improvements had been made to accept the

closeout for the root cause problem statement.

Regarding the effectiveness of corrective action, the presenter was

unable to provide firm "objective evidence" that corrective action

effectiveness was sufficiently improved.

The inspector noted that

details contained in the package alternately strengthened and weakened

the presenter's argument.

However, these details were not referred to

during the presentation. For example, the performance indicators on

c.

7

corrective action quality showed a generally improving trend on the

quality of level 1 and 2 CRs, while, in another case, 26 of 34 level 1

CRs were missing effectiveness reviews by department managers. These

details were not discussed by MRC.

Conclusions

Based on a detailed review of the licensee's actions for weak root cause

skills, the inspector concluded that their plans and actions to date

were acceptable. *

The MRC was unable to conclude that corrective action effectiveness was

sufficiently improved.

Thus, MRC deferred approval of this problem

state~ent. The inspector agreed with MRC's conclusion.

MRC questioning

of the presenter was appropriate and their decision to defer the

approval of corrective action effectiveness reflected a strong safety

ethic.

07.2 Management Review Committee Performance. NRC Restart Item 111.21

a.

Inspection Scope (71707).

During the inspection period, inspectors observed MRC activities to

assess the effectiveness of their review of closeout packages for NRC

. manual chapter 0350 inspection items~

b. Observations and Findings

The MRC frequently added to the quality of efforts by the Salem staff.

For example, .the MRC found several packages documenting corrective

actions unacceptable.

The MRC challenged the conclusions presented.with

several of the issues.

As an example, in a summary of valves reviewed

for pressure locking and thermal binding concerns, the MRC noted that

the staff had excluded valves based on their normally open position *.

The MRC noted that emergency operating procedures required operators to

change the valve position. The MRC did, however~ demonstrate

inconsistency in .the quality of NRC review.

For. example, the MRC

members occasionally lost independence by defending the position of a

staff member presenting information.

In addition, the MRC charter does

not provide guidance as to the purpose or basis for MRC review of the

. Restart Action Plans, the Startup and Power Ascension Plan, the

affirmations of NRC Restart Issue Completions, tir the closure of other

items affecting startup.

By contrast, the MRC charter contains very

detailed screening criteria for MRC use in classifying proposed

maintenance or modifications as required for restart, required after

restart, or not required. Without guidance for review of plans and

completion packages, the MRC cannot provide consistently effective

reviews .

  • tt

'

8

c. Conclusions

Although the MRC frequently added to the quality of efforts by the Salem

staff, inspectors noted inconsistency in the quality of MRC reviews.

The MRC charter lacks guidance for review of the Restart Action Plans,

the Startup and Power Ascension Plan, the affirmations of NRC Restart

Issue Completions, or the closure of other items affecting startup.

07.3 Effectiveness of Quality Assurance and Nuclear Safety Review. NRC

Restart Item 111.20

a.

Inspection Scope (71707)

The inspectors reviewed the results of QA and NSR activities documented

in monthly reports for January/February 1996 and for March 1996 to

assess the effectiveness of their contribution to improving Salem

performance.

b. Observations and Findings

The QA/NSR monthly reports indicated substantial improvement in the

number and quality of performance observations.

For example, the

reports identified operator problems with tagging, poor operator

Technical Specification tracking, and maintenance procedure non-

compliances.

The reports identified generic problems with temporary

modifications, radiation worker inattention to detail, and problems with

ERO response timeliness. The QA/NSR staff formatted the reports to

support the electronic performance indicator system.

As a result, the

reports display performance in operations, maintenance, engineering and

plant support using the colors green (excellent), yellow (meets

standard), red (needs improvement), and blue (insufficient data). The

format, including the clearly written executive summary, aids the reader

in gaining perspective on performance strengths and weaknesses in each

functional area.

Based on a comparison of the information, the inspector noted several

performance observations in both reports.

For example, both reports

noted that the backlog of Salem'operator work around remained greater

than 200, yet the March report did not identify that the

January/February report contained the same observation.

Both reports

noted that tagging problems continued in operations and maintenance, and

they noted maintenance training deficiencies, but the March report did

not indicate that the same observation appeared in the previous report.

The reports both noted problems with temporary modifications, overdue

engineering corrective action evaluations, and concern with ERO manning

timeliness. The reports did not assess or document corrective action

for these identified problems.

Both reports concluded that QA/NSR staff

had gathered insufficient data to rate engineering performance, but the

March report did not indicate whether the QA/NSR department had

implemented actions intended to provide engineering assessment in a

future report.

~

9

c. Conclusions

The QA/NSR reports for January/February 1996 and March 1996 provided

substantive assessment of Salem performance.

The reports reflect

significant improvement in the organization's ability to identify

performance strengths and weaknesses, and communicate them to PSE&G

management.

The QA/NSR reports, however, missed a number of

opportunities to provide information on performance trends from one

period of assessment to the next.

08

n;scellaneous Operat;ons Issues

08.1 Timeliness of licensing Submittals

The following are several examples of untimely licensing submittals:

1.

On February 1, 1996, the licensee told NRR that a one,...time change,

to the Technical Specifications would be submitted to allow entry

into Mode 6 with the Control Room Ventilation System inoperable.

On April 2, 1996, the licensee said that this request would *be

submitted by April 12, 1996.

The submittal was made May 7, 1996,

with a requested completion date of June 21, 1996, to support

entry into Mode 6 on July 3, 1996.

2 .

On February 20, 1996, the licensee informed NRR that it was

planning to request an exemption to 10CFR55.31(a)(5).

The

regulation requires that applicants for an operator license

perform five significant control manipulations which effect

reactivity or power level on the facility for which the license is

sought~ The request for the exemption was submitted on May 10,

1996.

The licensee requested that the NRC grant the exemption by

July 3, 1996, to support entry into Mode 6.

3.

An internal licensee memorandum dated October 24, 1995, stated

th~t Unit 2 Technical Specification 4.9.12.d.2 "is inconsistent

with the' system design basis and needs to be changed".

The

Technical Specification required verification, at least once per

18 months, that the system automatically starts on a high

radiation test signal. The actual plant configuration did not

have an automatic start provision.

In May 1996, the licensee,

. because of this discrepancy between the Technical Specification

and the system design, declared the Fuel Handling Building (FHB)

ventilation system inoperable.

An operable FHB ventilation system

is required before any fuel movement in the FHB is allowed.

The

licensee had been planning to move fuel in May and was considering

asking the NRC for some expedited licensing action so that the FHB

ventilation system could be declared operable. The NRC indicated

that it probably would not take expedited license action because

the licensee had ample time to submit the Technical Specification

change prior to actually needing it. By letter dated May 29, 1996,

10

the licensee committed to install the auto-start feature prior to

moving fuel, thus making the system design consistent with the

existing Technical Specification.

The inspectors concluded that Salem did not initiate and complete

license change requests in a timely manner after they identified

Technical Specification discrepancies.

II. Maintenance

Ml

Conduct of Maintenance

Ml.I General Comments

a.

Inspection Scope (62703)

The inspectors observed all or po_rtions of the following activities:

960221159:'

2C diesel generator starting air and turbo boost

system upgrade

960214251:

2C diesel generator motor operating potentiometer

replacement .

960329013:

2C diesel generator/generator control panel/clean

inspect

960228238:

no. 4 service water bay pipe replacement

960228146:

no. 22 service water header piping replacement

and

960320176:

no. 21 safety injection pump suction piping inspection

960516056: Artificial Island Meteorological Monitoring Program

Calibration and Maintenance Procedure

  • The inspectors observed that the pl ant staff performed the maintenance

effectively within the requirements of the station maintenance program.

b.

Inspection Scripe {61726}

The i nspecto.rs observed a 11 or portions of the fo 11 owing survei 11 ances:

S2.0P-ST.DG-0014:

2C diesel generator endurance run

The inspectors observed that plant staff did the surveillance safely,

effectively proving operability of the associated system

Ml. 2 Auxiliary Feedwater Pump Surveillance. NRC Restart Item I I. 42

a.

Inspection Scope (71707) .

The inspectors reviewed the surveillance procedures for the auxiliary

feed water (AFW) system, to determine whether they satisfied the

associated Technical Specification (TS) requi~ements .

11

b. Observations and Findings

On April 3, during the plant status meeting, the inspectors learned that

. Condition Report (CR) 960306246 questioned the adequacy of the AFW TS

surveillances. The inspector reviewed the condition report and

following surveillances:

S2.0P-ST.SSP-00ll{Q), Engineered Safety Features-Response Time

Testing

S2.0P-ST.AS-0004(Q), Inservice Testing Auxiliary Feed Water Valves

Hodes 1-6

S2.IC-TR.ZZ-0002{Q), Unit 2 Master Time Response Procedure.

Salem Unit 2 TS 3.3.2.1, Engineered Safety Feature Actuation System

Instrumentation, states, in part, that the Engineered Safety Feature

Actuation System (ESFAS) shall be operable with response times as shown

in Table 3.3-5. The table requires the AFW pumps to respond to an

initiating signal within 60 seconds.

The CR 960306246 stated that the

steam generator AFW discharge valves to the steam generators (AF21)

response times, when incorporated in the Unit 2 Master Time Response

Procedure, would not meet the 60 second criteria established by TS.

Salem staff had not previously considered opening of the AF21 valves in

meeting the TS 3.3.2.1 requirement.

As a result of CR 960306246, the Nuclear Fuels group performed the

calculation (DSl.6-0145), AFW Response Time Evaluation.

The calculation

determined that the AF21 valve would only open 45% within 60 seconds.

The calculation also determined that although the AF21 valves would not

fully open within 60 seconds, the AFW system would establish sufficient

flow to maintain the steam generators as a heat sink, as described in

Chapter 15 of the Final Safety Analysis Report (FSAR). The inspector

reviewed the calculation and determined that it adequately demonstrated

the ability of the AFW system to deliver required flow in 60 seconds, as

described in the FSAR.

Technical Specification Bases 4.3.1 & 4.3.2 states that the surveillance

requirements specified for the AFW system ensure that the overall system

functional capability is maintained comparable to the original design

standards.

One of the original design standards, the Accident Analysis,

Chapter 15 of the FSAR, requires that during a loss of normal feedwater

and loss of offsite power, two steam generators begin to receive

auxiliary feedwater from one motor-driven auxiliary feedwater pump

(MDAFWP) within 60 seconds.

Prior to the development of calculation DSl.6-0145, the AFW response

time surveillances did not demonstrate the ability to meet the

requirements of TS 3.3.2.1. This licensee identified and corrected

violation is being treated as a Non-Cited Violation consistent with

Section VII.B.1. of the NRC Enforcement Policy .

.

I

12

c; Conclusions

Salem engineers corrected a licensee-identified omission in the

surveillance procedure for auxiliary feedwater response time.

M3

Maintenance Procedures and Documentation

  • M3.1 Safety Injection Pump Inspection and Repair. NRC Restart Items 111.3 and

111.5

a.

Inspection Scope (62703)

b.

The inspector reviewed the.work package and associated procedures for

safety injection (SI) pump maintenance conducte~ under work order 950725243.

The inspector discussed the activity with maintenance

technicians, supervisors, and managers.

Observations and Findings

On May 3, 1996, quality assurance (QA) inspectors performed a

.

cleanliness inspection and maintenance technicians lowered the no. 22 SI

pump upper casing.

On May 6, maintenance technicians cut out 22SJ103,

no. 22 SI pump casing vent valve, under work order 950523070.

This

activity left grinding chips in the pump.

Maintenance technicians,

involved with SI pump assembly, removed the pump casing, cleaned the

pump internals, and wrote a condition report (CR 960507291) to document

the occurrence~ Quality assurance reverified internal cleanliness in

accordance with NC.NA-AP.ZZ-0021 (NAP 21), System Cleanliness Program.

On May 7, maintenance technicians helium arc welded the 22SJ103 valve

back in place and left various grinding shavings on the casing's

external surfaces. The maint~ance technician, involved with pump

assembly, questioned the internal condition of the pump.

The

maintenance supervisor determined that no possibility of internal debris

intrusion existed based on the weld type (no slag) and post-weld

grinding only. Maintenance technicians did not reinspect the pump

internals. *

On May 9, the .inspector reviewed the work package and procedure

documentation.

Based on the above information, the inspector expressed

a foreign material exclusion*(FME) concern, regarding the no. 22 SI

pump, to the Unit 2 Senior Maintenance Supervisor.

On May 10, the

maintenance supervisor noted a shaft rub on the no~ 22 SI pump and

decided to remove tbe upper casing to investigate. The maintenance

supervisor determined that grinding chips internal to the casing wear

'ring, located beneath the 22SJ103 vent valve, caused the shaft rub.

The

maintenance supervisor stated that the foreign material could cause

increased wear on the ring, but did not threaten pump operability. The

maintenance supervisor determined that the grinding chips were most

likely the result of initially cutting out the vent valve. Maintenance

staff disa~sembled the pump and removed the chips. The senior

maintenance supervisor initiated actions to communicate lessons learned

-

I

c .

13

to all maintenance personnel. The inspector noted that poor planning

and coordination of maintenance resulted in poor FME practices on an

assembled component.

Ample opportunity existed to perform the vent

valve replacement with the upper casing removed from the pump.

In

addition, failure to properly restore cleanlines~ is a violation of NAP-

21 requirements. This licensee identified and corrected violation is

being treated as a Non-Cited Violation, consistent wtth Section VII.B.l

of the NRC Enforcement Policy.

Additionally, on May 9, the inspector identified a number of procedure

usage and documentation deficiencies. Contrary to management

expec~ation, maintenance technicians used SC.MD-CM.SJ-0001 (Revision 5),

Safety Injection Pump Disassembly,_Inspection, Repair and Reassembly, in

the field 14 days after the issue date. Technicians validated the

procedure on April 18, and used it to record information until May 6 {18

days). Maintenance technicians repeatedly marked steps "N/A" {non-

applicable) without providing justification in the comments section of

the procedure. Technicians did not initial all steps completed in the

procedure. Technicians did not completely enter all required

-

information on the procedure data sheet {attachment 8). This is a

'violation of NC.NA-AP.ZZ-0001 {Revision 7), Nuclear Procedure System,

requirements.(VIO 50-272&311/96-06-01)

Conclusions

Maintenance technicians' poor foreign material exclusion practices

resulted in introduction of material from grinding onto safety injection

pump internals. Maintenance technicians provided less than adequate

,documentation of safety injection pump repair activities. These

activities resulted in two violations.

III. Engineering

El

Conduct of Engineering

El.I Updates to the Final Safety Analysis Report CFSAR)

a.

Inspection Scope

b.

During a recent evaluation of spent fuel pool decay heat removal and

refueling practices, the inspectors reviewed licensing basis documents

for Salem Units 1 and 2.

The documents included the UFSAR {Updated

Final Safety Analysis Report) and documents related to Amendments 151

and 131 of the Salem license dated May 4, 1994.

Observations and Findings

In a report to the Nuclear Regulatory Commission, the staff noted that

Salem was included in a category of plants where:

c.

14

.... plant-specific FSARs did not reflect information associated

with spent fuel pool decay heat removal from applicable license

amendments.

An NRC regulation, specifically 10 CFR 50.7l(e),

requires that the FSAR be periodically updated to reflect such

i nforlTiat ion.

NRC regulation 10 CFR 50.7l(e) requires that licensees periodically

revise the FSAR to include the effects of: all changes made in the

facility or procedures as described in the FSAR; all safety evaluations

performed by the licensee in support of requested license amendments .*..

The regulation requires that the periodic updates .be submitted annually

or within six months after each refueling outage provided the interval

between successive updates does not exceed 24 months.

During the staff review, the inspectors noted that the Salem FSAR did

not reflect information submitted by the licensee in support of the

rerack amendment.

Specifically, in a letter dated April 28, 1993, the

licensee listed the heatload for a partial core offload as being 23.8

BTU/hr and the resulting maximum spent fuel pool temperature as being

148.94 F.

For the full core offload the heatload was listed as 38.57

BTU/hr and the pool temperature as 179.93 F.

However, FSAR Section

9.1.3.l states that, the fuel pool water temperature is limited to 120 F

for a partial core offload and limited to 150 F for a full core offload.

The FSAR should include the most recent applicable rerack amendment

design information .

The inspectors noted however, that the staff approval of the rerack

amendment was issued in May 1994 and the modification was only completed

in December 1995.

Conclusions

The inspectors concluded that the information regarding the rerack

project need only be included in FSAR revisions subsequent to the

completion of the modification. Thus, the inspectors concluded that

Salem had not exceeded the time period allowed by 10 CFR 50.7l(e) for

periodic revisions to the FSAR.

This item raised in the May 21, 1996

report to the Commission regarding periodic FSAR updates at Salem is

closed.

E2

Engineering Support of Facilities and Equipment

E2.l Service Water Pump Strainer Trips (71707)

During the inspection period, the inspector noted five Unit 2 service

water (SW) pump strainer trips while in service. Continued problems

with no. 23 SW pump strainer accounted for four of the above trips.

These trips resulted in SW pressure reductions and SW pump auto starts,

however, no significant reduction in safety margin due to plant

condition (shutdown and defueled). Engineering worked with maintenance

in an attempt to determine the root cause. At the end of the period,

engineering had not completed their root cause.determination. Service

..

I

'15

water pump strainer malfunctions represent nonconformance with the

automatic, self-cleaning features specified in the Updated Final Safety

Analysis Report (UFSAR section 9.2.1.2) and a challenge to SW system

reliability.

E2.2 Diesel Generator Jacket Water After-Cooler Heater Inoperability. NRC

Restart Item III.19

a.

Inspection Scope C71707l

b.

On May 13, 1996, during a tour of the plant, the inspector noted that

the no. 2A emergency diesel generator (EDG) jacket water (JW) after-

cooler heater breaker was tagged open.

The inspector reviewed the UFSAR

and discussed the UFSAR requirements with the Senior Nuclear Shift

Supervisor.

Observatioris and Findings

The inspector noted that UFSAR section 9.5.5 states that each EDG JW

system is supplied with an after-cooler heater. This 2kw

.

thermostatically controlled heater maintains water temperature in the

after-cooler piping when the engines are not in operation. Contrary to

this UFSAR requirement, the no. 2A EDG JW after-cooler heaters were

inoperable since April 20, 1995.

Engineering did not perform a 10 CFR

50.59 safety evaluation of this change to the UFSAR .

On May 4, 1995, engineering performed an operability determination and

concluded that the EDG was operable, given that the lube oil pre-lube

pump remained operable.

On June 8, 1995, engineering completed a Review

and Assessment of this operability determination.

Engineering concluded

that the 14 days between work order initiation and operability

determination was not consistent with Generic Letter 91-18 requirements .

. In addition~ engineering stated that the JW heater condition (WO 950420252) should be corrected prior to ambient temperature dropping to

50°F to avoid having an inoperable EOG if the pre-lube pump failed.

On March 11, 1996, outage management noted that WO 950420252 was listed

on the tagout as "schedule-hold."

On March 15, 1996, an electrical

supervisor determined that a faulty thermostat and heater required

draining JW to replace. Outage management scheduled this work activity

for the next no. 2A EDG outage window.

On May

14~ the Senior Nuclear Shift Supervisor initiated a condition.

report (960514306) to evaluate the 2kw heater UFSAR requirement with

respect to timeline~s of corrective actions.

c. Conclusions

Engineering did not evaluate a degraded emergency diesel generator

jacket water after-cooler heater condition with regard to UFSAR *

requirements.

Failure to perform a 10 CFR 50.59 safety evaluation is a

violation. However, this item is unresolved pending resolution of

I

E7.

-~

16

similar apparent nonconformances with the UFSAR and licensing bas fs

(control air and fuel handling building ventilation).

(URI 50-

2721311/96-06-02)

ADFCS Modification Engineering Quality Assurance CIP 520021

Software Verification and Validation CV&V)

.The V&V effort was initiated by the Digital Systems Group and was

implemented as a retrofit to the ADFCS design change package.

The V&V

was performed by the Digital Systems Group and independent consultants.

The V&V effort consisted of *five phases~

indep~ndent review of WDPF base (Phase I);

requirements verification (Phase II);

application software verification (Phase Ill);

validation testing (Phase IV);

final integrated report (Phase V).

The inspectors reviewed the V&V plan for the ADFCS and audited results

of the V&V for Phase I, Phase II, and Phase III. Time constraints

prevented the review Phases IV and V and two additional independent

consultant reviews .

During the implementation of each phase, discrepancy reports were

generated for any issues discovered during the revi~w~ At the

completion of each task, a comment/discrepancy review cycle was entered

to resolve any issues raised in that phase.

The next phase was not

initiated until the previous review cycle was satisfactorily completed.

All problems identified during the V&V phases were tracked in the V&V

discrepancy log.

The independent review of WDPF base software (Phase*I) was performed by

Data Refining Technologies. Data Refining Technologies reviewed the

design hardware and process utilized by Westinghouse to deliver the

ADFCS~ with specific emphasis on issues related to the use of

microprocessors and other hardware containing stored programs in control

equipment.

The conclusions of this report found that Westinghouse had

some weak points in the area of software life cycle, but no significant

issues that would affect the functionality of the ADFCS Project. The

inspectors concluded that the review was thorough and arrived at sound

conclusions based on valid reasoning.

The requirements verification (Phase II) resulted in the generation of a

system requirements document (SRO), the detailed design document (DOD),

and the requirements traceability matrix (RTM).

The RTM links the

Salem-specific requirements from the requirements documentation to the

applicable sections in the SRO, ODD, factory acceptance test (FAT), and

site acceptance test (SAT).

Generic requirements were.addressed in the

design analysis section of the Salem ADFCS design change package.

The

inspectors concluded that the RTM provided added assurance that the

17

requirements were properly translated into the design and tested when

necessary.

The inspectors reviewed the discrepancy reports and, with the help of

the licensee, categorized the 128 discrepancies as:

89% drawing

discrepancies; 8% documentation problems; 2% design discrepancies; and

1% software errors. The inspectors noted that the drawing

inconsistencies were discovered in Phase III, the application software

review.

The inspectors noted that the discrepancy log was under

informal control, which could impair accurate tracking of all issues,

although no instances of impaired.tracking were identified.

The application software verification (Phase Ill) resulted in the

generation of several discrepancy reports addressing various drawing and

software discrepancies.

However, there were no major functional or

translation errors found.

The inspectors concluded that this phase

proved to be a beneficial part in resolving inconsistencies in the

documentation and drawings, resulting in a more correct representation

of the as-built system.

The inspectors concluded, based on their limited scope V&V audit, that

the retrofit of a V&V program to the ADFCS increased the accuracy and

consistency of th.e software with the system drawings.

Cross-Connected Data Points

A certain number of software variables is generated in one DPU and

transmitted over the redundant communication bus to the other DPU.

According to the licensee, these cross-connected soft~are variables are

unique to the fleet of ADFCS plants. The inspectors reviewed a portion

of these cross-connected data points to determine the importance of

these cross-connected data points with respect to the correctness and

potential failure modes of the application.

The trace was facilitated by a matrix in the source code that referenced

the appropriate loop/ladder/algorithm and DPU for each cross-connected

data point.

In the event of a bus failure, there was a backup bus.

In

the event that data values were to get corrupted or lost during

transmission, most of the software process blocks were designed to use

the previ6us data values.

The trace to the software block diagram showed that when a cross-

connected data point was for a MSS involved with an important algorithm,

as compared to being used for recording, only one out of the three

inputs involved a cross-connected data point.

By design, if one data

value passed i~ bad, the MSS will function properlj.

The inspectors noted that the use of cross-connected data has the

potential to disrupt proper functioning.

In the Salem ADFCS, the

inspectors concluded that most of the cross~connected data are used in

MSS algorithms and the "last data values" are used on loss of data.

I

18

These factors tend to moderate any functional problems caused by cross-

connected data corruption or loss.

Software Configuration Control

The inspectors reviewed the licensee software configuration control

procedures covering the ADFCS.

Prior to shipment of the ADFCS to PSE&G,

Westinghouse maintained and implemented all software changes.

However,

the inspectors noted that the ADFCS project team also tracked these

changes~ which included changes-initiated as a result of the testing and

the FAT.

Once shipped to PSE&G, the ADFCS design was controlled under PSE&G

design change package (DCP} workbook control procedures.

The associated

software was maintained by the Digital Systems Group (DSG}.

Changes to

the DCP, including software, were controlled using a modification change

request (MCR} form,_ which had to be approved by the ADFCS project team.

.

.

.

The inspectors noted that none of the procedures used prior to DCP

closeout, including the MCR form, were specific to software. Although

this did not appear to be an*issue for this modification, the inspectors*

considered this to be a potential area for diminished control in the

site procedures, especially if the DSG was not involved.

Once the DCP reaches closeout, the ADFCS design descri p.t i.on and the

master system disks are kept in the Document Control Center and

controlled under a software-specific procedure, NC.NA-AP.ZZ-0064(Q},

"Software and Micro-Processor Based Systems (Digital Systems}." The

Digital Systems Group interpreted and expanded this procedure into their

own version; NA.DE-AP.ZZ-0054{Q}, "Process Computer Maintenance and

Modification Control Program."

The Document Control Center maintains a list of engineers in the Digital

Systems Group that have the authority to make changes to the ADFCS

software.

The design change package, including the source code listing,

is stored in a different location in the Document Control Center than

the master disks.

To facilitate a software change, an "approved" engineer will obtain .a

copy of the master disks from the Document Control Center. After

updat i og the ma.ster software disks, the engineer wi 11 download the

updated software to the ADFCS via the engineering workstation or using a

laptop computer.

The engineer will follow a Westinghouse WDPF loading

procedure.

As the data is downloading to the database, a line-by-line

verification is performed to ensure the proper transfer. Once the ..

download is complete, the program-is recompiled and a message is

displayed on the screen indicating that the download was a success/

failure and the number of lines compiled.

The new revised master disks

will replace the master disks in the Document Control Center. Only the

pages in the source code listing affected by the changes will be stored

with the change package .

I

I

19

The licensee stated that there was no contractual provision to ensure

that Westinghouse would notify PSE&G if a problem was found after system

shipment and training.

The inspectors concluded that, prior to DCP closeout, the configuration

control process for the ADFCS was successful due to knowledgeable

software engineers, in the absence of software-specific guidance.

The

inspectors also concluded that the software configuration control

procedures provided for post-DCP closeout were adequate for controlling

software changes.

The inspectors noted that, since previous versions of

7the disks and associated source code listings were not maintained, it

would be difficult to reconstruct and verify a previous version of

software, if the need arose.

Software Access Control

To ensure the integrity of the ADFCS, the ADFCS project team defined

four separate levels of software access.

The Salem Operations

Department (Level 1) is limited to the ability to monitor system status

screens and system parameters.

The Salem I&C Department (Level 2) is

given the ability to remove points from scan and input dummy values for

calibration purposes, to trend points for troubleshooting purposes, to

monitor system status, and to acknowledge and clear system alarms.

In

addition to the Level 2 functions, the Salem Technical Department (Level

3) is given the ability to use the control tuning functions for the

steam flow drift compensation and for entering values and forcing logic

ladders. However, if the system software is reloaded, all bias

adjustments made to the steam flow transmitters will revert to their

original values. All functions will be enabled for the Digital Systems

Group (Level 4).

Each level is password protected. A standard computer keyboard will not

be maintained at the engineering workstation.

Instead, users will

access the system via a keyboard with defined function keys.

The

functions will only be accessible from the operate position of the

keyboard keyswitch.

The keyboard key is maintained by the Digital

Systems Group and Salem Operations.

The inspectors reviewed a memo documenting the Salem ADFCS access

control procedure and observed a hands-on demonstration of the access

limitations on the ADFCS engineering workstation installed in Salem

Unit I. The inspectors verified that there was no system response to

function keys, unless the keyswitch was in the operate position. The

inspectors also verified that an attempt to access a function key not

permitted in a given access level resulted in an error message.

The

inspectors concluded that the ADFCS access control provided sufficient

security for the system.

Conclusions

The inspectors concluded, based on their limited scope V&V audit, that

the retrofit of a V&V program to the ADFCS increased the accuracy and

--,-

I

20

consistency of the software with the system drawings.

In the Salem AOFCS, the inspectors concluded that most of the cross-

connected data are used in MSS algorithms and the "last data values" are

used on loss of data. These factors tend to moderate any functional

problems caused by cross-connected data corruption or loss.

The inspectors concluded that prior to OCP closeout, the configuration

control process for the AOFCS was successful due to knowledgeable

software engineers, in the absence of software-specific guidance.

The

inspectors also concluded that the software configuration control

procedures provided for post-OCP closeout were adequate for controlling

software changes.

The inspectors concluded that the AOFCS access control provided adequate

security for the system.

The inspectors concluded that the licensee met their HMI design

objective of minimizing impact on plant operations personnel.

The inspectors concluded that the use of the AOFCS trainer was an

effective method for enhancing the technical quality of the l&C

maiptenance activities .

E7.1 Operations Safety Review COSRl Group Review Summary Records CRSRl. NRC

Restart Items 111.11 and III.67

a.

Inspection Scope (37550)

The inspector reviewed the following RSRs and associated documentation

to.determine the adequacy of the reviews:

RSR 662, OCR 2EC-3252

RSR 667, OCR 2EC-3242

RSR 343, Review of SORC meeting minutes

b.

Observations and Findings

Section 1.0, General Information, of Nuclear Administrative Procedures

NC.NA-AP.ZZ-0059(Q), 10.CFR 50.59 Applicability Reviews and Safety

Evaluations requires that the preparer should address any mode or

operating condition restrictions, if applicable. The inspector reviewed

the RSR 662, 22 Component Cooling Heat Exchanger System Upgrade, and

noted that the 10 CFR 50.59 evaluation did not address any mode or

operating condition restrictions for installing the flow measurement

gauge.

The inspector determined that no mode or operating condition

restrictions applied, since the upgrade consisted of installation of a

gauge that could be done without affecting system operation .

c.

21

Salem Unit 2 TS 4.9.12.d.3, requires that the fuel handling area

ventilation (FHAV) system maintain a negative building pressure of 0.125

inch water gauge or greater negative pressure.

The UFSAR section

9.4.3.2.2 requires that the differential pressure controller maintains a

0.1 inch water gauge negative pressure in the building. The inspector

noted, while reviewing RSR 667, Fuel Handling Building System Upgrades,

dated 10/25/94, that a change to the differential pressure control

systems setpoint from a -0.1 inch to a -0.2 inch water gauge was

identified in Design Change Request (DCR) 2EC-3242, Rev.3.

The

inspector also noted that 50.59 Review and Safety Evaluation, Rev.I, for

the DCR did not address the change to the setpoint. Although the Salem

staff changed the differential pressure controller setpoint to meet the

requirements of TS 4.9.12.d.3, they did not consider possibility for

adverse consequences of increasing differential pressure on the FHAV

components prior to making the change, as required by 10 CFR 50.59.

Also, the original RSR reviewed identified a change to the setpoint;

however, the second level reviewer inappropriately determined that the

conservative nature of the setpoint change did not necessitate a more

extensive review.

As a result of FHAV problems discovered in August 1995, engineers

completed an analysis that concluded FHAV components could withstand 8.3

inches of water gauge negative pressure. This licensee identified and

corrected violation is being treated as a Non-Cited Violation,

consistent with Section VII.B.l of the NRC Enforcement Policy.

In

Licensee Event Report 95-24 for both Salem units, the licensee

identified several FHAV problems, including that the surveillance

procedure for TS 4.9.12.d.3 did not insure that FHAV maintained the

required differential pressure during normal operation. At the close of

the inspection period, the licensee and the inspectors continued to

pursue additional questions about FHAV compliance with regulatory,

design basis, and licensing basis requirements. These issues will

remain unresolved pending completion of the inspection, and will be

addressed as part of the Unresolved Item discussed in section E2.2,

above.

The inspector reviewed RSR 343, Maintenance Management Information

System Discrep~ncies for Emergency Diesel Generator air receiver valves,

and noted that the RSR documented discrepancies in the MMIS system such

that system functional descriptions and locations for all of the valves

in that system were missing.

The inspector verified that the MMIS

system had been revised for all of the valves identified in the RSR.

The inspector determined that these changes were made in accordance with

the applicable Department Administrative Procedure, NC.DE-AP.ZZ-0015(Q),

MMIS Resource Data Module.

Conclusions

Engineering failure to insure that FHAV maintained the required

differential pressure during normal operation is unresolved pending

completion of inspection of related questions concerning compliance with

regulatory, licensing basis, and design basis requirements.

EB

22 -

Miscellaneous Engineering Issues (92903)

ES.I Reliability of Station Air Compressors. NRC Restart Item II.2

-a.

Inspection Scope C92~03)

During the period, the inspector noted continued problems involving

station air compressors.

b. Observations

On April 8; 1996, no~ 2 station air compressor (SAC) tripped on high

vibration. The system manager recommended a detailed investigation

after plant staff returned the no. 3 SAC to service.

On April 25, no. 2

SAC tripped on high vibration. * The system manager determined that the

multiple trips _warranted a detailed investigation. The operating shift

maintained a station air contingency plan that relied on installed

temporary air compressors.

On May 1, no. 1 SAC tripped due to excessive water level in the moisture

separator. The Unit 1 and Unit 2 emergency control air compressors

(ECACs) started automatically and maintained control air header pressure

at -approximately 85 psig as designed. Control room operators entered

Sl(2).0P-AB.CA~ooo1, Loss of Control Air. Nuclear equipment operators

started and loaded the temporary air compressors.

The system manager

determined that rust particles from corroded carbon steel piping blocked

the ~oisture separator drain piping, causing the compressor trip.

On May 5, operators placed no. 3 SAC in service following maintenance.

Later in the day, operators removed no. 3 SAC-from service_ due to air_

leakage at the aftercooler inlet.

On May 6, operators placed no. 3 SAC

back in service. , On May 11, operators prepared to unload no. 3 SAC to

investigate high compressor current swings. While loading ho. 1 SAC,

operators noticed water spraying from air piping. The system manager

determined that condensation in the discharge piping and leaking flanges

caused this effect.

On May 14, operators returned no. 1 SAC to service

following maintenance.

As operators unloaded no. 3 SAC~ however, it

tiipped on high vibration.

c. Conclusions

Between April 8 and May 14, four station air compressor trips and two

additional compressor failures required operators to take contingency

actions. Inspectors concluded that maintenance and system engineering

staff did not effectively ensure station air system reliability.

ES.2

(Open) Inspector Follow-up Item 50-272&311/95-21-02: Service water (SWi

reliability issues. This issue was open pending NRC review of licensee

corrective actions stemming from condition reports addressing challenges

to SW.

23

The first concern involved SW bay desilting.

In the recent past,

maintenance closed out a work order for multiple SW pump silt

inspections prior to performing all activities. -Engineering determined

that a separate work order for each SW pump bay si.lt inspection would

preclude recurrence (PR 00960113315).

The inspector noted that the corrective action addressed the particular

case of missed silting inspections, however, did not fully answer silt

build-up concerns.

The system engineer stated that 92-day silt

inspections routinely found more than 3 feet of silt build-up. The

system engineer attributed this to the present shutdown condition .

(usually only one SW pump operating per unit). The inspector observed

that operations does not implement a SW pump rotation plan to preclude a

similar condition during normal power operation. Silt build-up

increases shutdown risk when defueled and may prevent the SW system from

fulfilling its design basis safety function at power (see NRC inspection

report 95-21).

The second concern involved the ability of the SW system to perform its

design function under worst case conditions. This concern evolved from

challenges to SW from grass, debris, silt, and ice given the non-safety

related and seismic class III construction of the instruments and

controls associated with the SW traveling screens.

In addressing the

above concern, engineering determined that operator error and

inattention, not material deficiency, caused the January 7, 1996, SW

pressure perturbation (PR 00960107144).

The inspector determined that the Service Water System (SWS) functioned

as designed on January 7, 1996.

However, PR 00960107144 did not address

or allay inspector concern regarding potential SWS vulnerabilities.

In

particular, the ability of SW to function as designed with traveling

screens in place, but not *rotating; given worst case river grass loading

as experienced in the l~st two years.

Inspector assumed traveling

screens not rotating based on non-safety related, seismic class Ill,

screen permissive pressure switches and seismic class III screen motors.

In addition, SW screen differential pressure switches are non-safety

  • related and cannot be relied upon to provide control room operators

sufficient warning of a blocked screen. A control room operator's first

indication would be a low SW pressure alarm.

The inspector determined that this item remains open pending NRC review

of '(l) licensee's siltation control program, (2) susceptibility of SW

traveling screens to debris clogging, (3) licensee's interpretation of

UFSAR {section 9.2.1.2) statement "The SWS is designed for class I

(seismic) conditions except for the turbine area service water piping

outside of the service water intake structure" relative to seismic

classification of SW components in the intake structure.'

I

24

E8.3

Hagan Modules R~furbishment and Replacement

a.

Inspection Scope

On February 23, 1996, the NRC issued their Restart Action Plan for the

  • Salem Units. This plan contains the programs and corrective actions

that the NRC.will inspect prior to .the restart of the Salem plants. The

reliability and configuration control' of the Westinghouse Model 7100

process instruments, al so known as Hagan modules, are i terns I 1.16 *and

111.2 of the NRC restart action plan.

The NRC concerns with the Hagan modules stemmed from a number of

previous inspection observations and findings and several plant events,

including: (1) the automatic reactor shutdown and actuation of the

safety injection system at Salem Unit 1, on April 7, 1994 (augmented

team inspection report 50-272 and 50-311/94-80); and (2) recurring

problems with the main steam atmospheric relief (MSlO) valves of both

units, in February 1995 (resident inspection report 50-272 and

50-311/95-02). The NRC concerns included component reliability,

configuration control, and application issues,. such as cabinet

temperature and susceptibility to electromagnetic radio frequency

interference (EMl/RFI).

The application concerns were identified in

inspection report No. 50-272 and 50-311/96-01.

The pu~pose of this inspection ~as to review PSE&G's resolution of the

various NRC concerns and to eva 1 uate their acceptability.

b.

Observations and Findings

PSE&G Program for the Hagan Modules

The Hagan module reliability and configuration control were the subject

of numerous problem reports.

To address all concerns in these areas,

PSE&G established a project team.

The objectives of this team were to

evaluate the identified anomalies and failures and to develop a program

for resolving them.

PSE&G resolution of the Hagan module concerns

involved the replacement of some modules and the refurbishment of

others. The replacement modules were furnished by Nuclear Utility

Services (NUS).

The replacement and refurbishment decisions were based

primarily on availability of spare parts and components and their

recognition of the decreased reliability of the existing Hagan modules

due to aging.

The results of the NRC review of the licensee program are

described in the sections below.

Design & Procurement of Replacement Modules

During the current outage the licensee will *replace three types of

modules: signal summators, signal isolators, and RTD low.level

amplifiers. The req*uirements for these and other modules scheduled to

be replaced in the future were described in Purchase Specification No.

S-C-RCP-EDS-0308, Revision 2 ..

I

25

In general, the technical and performance requirements for all NUS

  • modules were derived from those specified by Westinghouse for the Hagan

modules.

Qualification requirements were based on applicable industry

standards and Regulatory Guides.

The inspector's review of this

document identified no discrepancies, except for the maximum specified

ambient temperature (110 °F)-which was less than the one specified for

.the-Hagan modules {120 °F).

Further review determined that the

furnished NUS modules have a maximum temperature rating of 122 °F for

normal operation and 135 °F for abnormal {200 hr) operation. Therefore,

the discrepancy was not a concern.

The environmental and seismic qualification of the above modules had

been addressed.

For instance, reports EIP-QR-MBA800, Revision 0, and

EIP-QR-800, Revision 1, addressed qualification of the summators and

.isolators, respectively. - The inspector reviewed these documents and

identified no disc~epancies.

Change Package Process for Replaced Modules

The replacement of the Hagan modules with NUS modules was addressed by

design change 2EC-3450, package No. 1.

The inspector's review of this

document determined that the technical aspects of the change had been

evaluated in sufficient detail to ensure the acceptability of the new

replacement modules.

The changes had undergone multi-disciplinary

review and had been evaluated in accordance with lOCFR 50.59 to ensure

that the changes did not constitute an unreviewed safety question.

The

licensee had addressed the impact of the change on instrument loop

accuracy (engineering evaluation No. s~c-RCP-CEE-1037) a~d on the vital

bus total harmonic distortion. Regarding the instrument loop accuracy

calculation, the inspector observed that, in assessing the loop error

due to*calibration temperature, the licensee had assumed the normal

rather than the minimum ambient temperature.

The inspector's review of the safety evaluation, NC.NA-AP.ZZ-0059-3,

Revision 0, determined that the licensee based its conclusion that the

change did not constitute an unreviewed safety question on a detailed

review of the replacement components and their difference from the

replaced components.

The inspector identified no areas of concern with

the change package.

However, the instrument loop accuracy is unresolved

pending the licensee's revision of calculation S-C-RCP-CEE-1037 to

include minimum calibration temperature and maximum operating

temperature.

(50-272;311/96-06-03)

Module Refurbishment

~he scape and process for the refurbishment of fhe Hagan modules were

described in the Salem maintenance procedure, SC.IC-PM.ZZ-0023{Q),

Revision 10, "Hagan Module Refurbishment."

The method for conducting

the work was described in Procedure SC.IC-TI.ZZ-OOOl(Q), Revisio~ 3,

"Soldering/Desoldering."

-1

I

26

As described below, problems with configuration control resulted in the

existence at Salem of modules with different revision level. The intent

of the refurbishment was not only to perform needed repairs, replace

aged components, and bring the modules to a like-new status, but also to

upgrade all modules to their latest revision level. The procedure did

that in great detail and included drawings as well as check list tables

to identify the scope of work.

Fourteen types of modules in various

configurations were addressed by the procedure.

Subsequent to its repair*and upgrading, the licensee planned to subject

each module to bench testing, calibration, and a 50-hour burn-in period.

The licensee developed bench testing requirements for each type of

module and generated the required response to the various inputs. The

module bench testing process and the test acceptance criteria were

described in a series of procedures developed purposely for the task.

For instance, procedure SC.IC-GP.ZZ-0123(Q), Revision 4, was prepared*

for the bench testing of the Hagan loop power supplies and SC.1C-GP.ZZ-

0125(Q), Revision 1, was used for the Hagan Model 118-MVI amplifiers.

The inspector's review of the refurbishment procedures and of a sample

of bench testing procedures identified no areas of concern.

Change Package Process for Upgraded Modules

The licensee developed generic design change packages (DCPs) for each

type of module using the equivalent replacement process. For each type

of module, the licensee provided a table describing the module

specifications in both the present and upgraded versions.

Sine~ no

changes were identified in the table, the licensee concluded that the

upgrading would not affect the form, fit and function of the module.

The design change package also included a list of upgraded parts and

changes.

For instance, the upgrades of manual/automatic setpoint

station modules type 6627007-GOl and -G02, involved the addition of two

capacitors and the replacement of three transistors, three relays, and

one diode with Westinghouse components.

The DCP, however, did not

describe either the function of the two capacitors or the bases and

impact for using different piece parts.

Because the licensee considered the modified modules as equivalent

replacements, they did not perform an evaluation of the changes in

accordance with lOCFR 50.59.

Instead, in a note on the first page of

the DCP, they simply referred to a generic safety evaluation, No. A-O-

VARX-NSE-0727-1, as applicable. This document, titled, "Equivalent

Replacement and Document Update Generic Evaluation," generically

addressed and answered "no" to each question regarding whether or not

the change constituted an unreviewed safety question.

The document

never referred to the Hagan module refurbishment.

The inspector disagreed that the upgraded modules were equivalent

replacements in that the upgrading constituted in itself a functional

change of the module.

In addition, the design change package had not

I

27

described either the functions of the added components or the impact of

the replaced components on the performance of the module.

Therefore,

the licensee had not proven either that the upgraded module was an

equivalent replacement or that a safety evaluation was not warranted.

The acceptability of the design change packages for upgraded Hagan

modules is unresolved pending the licensee's revision and NRC's review

of the applicable documents to:

(1) identify the function of all module

upgrades, (2) describe the impact of these upgrades on the performance

of the modules, (3) clarify why the changes do not constitute all

unreviewed safety question, and (4) show the applicability of the

equivalent replacement process.

(50-272;311/96-06-04)

(Updated) Unreso~ved Item 50-272 and 50-311/96-01-01: Operating

Temperature of the Modules

During a January 1996 review of the Hagan upgrade program (NRC report

50-272 and 50-311/96-01), the inspector discovered that some modules

might be "normally" operated close to their design temperature limit of

120 °F.

Therefore, he expressed a concern that, under extreme ambient

conditions, the same modules might be used beyond such limit.

As a followup to the above observation, the inspector reviewed the

licensee evaluation of the operating temperature of the modules and

actions to address any discrepancies found.

The inspector determined

that, in December 1995, the licensee had conducted a temperature mapping

of a rack to determine the need for door and module housing

modifications.

They conducted six tests during which they measured the

ambient temperature both inside and outside the rack with three types of

doors and with vented as ~ell as unvented module side panels.

The

results of these tests were described in Test Report File 11-229/11-278,

Revision 1, dated March 15, 1996.

Based on the results of the above tests, the licensee concluded that the

currently used solid rack door and module side panels were acceptable.

The licensee's conclusions were based on their finding that, with a

normal room ambient temperature of 76 °F, the maximum rack ambient

temperature would be 91 °F and, hence, well below the design (rack

ambient) temperature specified by Westinghouse.*

For the equipment room, Section 3.11.1.3 of the FSAR specified a normal

operating ambient temperature of 70 °F +/- 15 °F.

The inspector also

determined that the design basis for the control area air-conditioning

system was based on its ability to maintain 76 °F with an outside summer

temperature of 95 °F.

Following a station blackout and loss of all

ventilation, a licensee calculation, No. S-C-AUX-MDC-0737, Revision 0,

showed that the control equipment room could reach a maximum temperature

pf 117 °F.

.

In discussing the result of the temperature test with the licensee, the

inspector determined that Westinghouse had conducted similar tests in

February 1971, although a report of these tests was apparently never

28

received by the licensee. The inspector's review of the report obtained

during the inspection (No. HC-25205, "Temperature Test on Racks and

- Modules of the Nuclear Protection System Public Service Electric & Gas

Company") revealed that, with considerable fewer modules and, hence,

with less heat load, the temperature in the rack rear airspace was

slightly higher than the one measured by PSE&G.

The inspector also

noted that the temperature in the rack front airspace and in the

airspace under the module shelves, not measured by PSE&G, was several

degrees higher than the one in the rack rear airspace.

The tables provided with the above Westinghouse report clearly indicated

that, when the rack fill _is considered, the modules located in the upper

shelves of the rack could be exposed to an ambient temperature higher

than 120 °F when the room temperature is within the "normal" range (less

_than 85 °F).

For instance, Table 19 of the report shows that, with a

room temperature of approximately 92 °F, the temperature in the airspace

under the shelf was as high as 122 °F.

The racks tested by Westinghouse

were sparsely loaded, when compared to the Salem racks.

The results of the Westinghouse tests raised several questions, such as

temperature effects on module accuracy and calibration, surveillance

requirements to ensure detectability of degraded module conditions, and

common cause failures due to heat during an abnormal event (station

blackout). Westinghouse addressed some of these issues in their

analysis of the results. For instance, on page 14 of the report,

Westinghouse pointed out the "definite temperature dependence" of the

module accuracy and, on page 16, recommended that the "rack ambient"

temperature not exceed 100 °F for normal operation. Because, however,

the rack heat load in the Westinghouse tests did not appear to envelop

that of the Salem racks, further analysis is required to determi~e the

applicability of all Westinghouse conclusions to Salem and to establish

the actions that are required to resolve the temperature issue.

The inspector discussed his concerns about the operating temperature of

the modules with the licensee who pointed out that the NUS modules

consumed less power and, therefore, would result in a lower temperature

in the racks.

The total impact, however, of the current changes was not

known without an evaluation by the licensee.

The operating temperature of the modules remains unresolved pending the

NRC evaluation of PSE&G's reconciliation of PSE&G and Westinghouse

temperature test results; determination of the "normal" ambient

temperature range for safety-related Hagan and NUS modules (considering

worst-case rack and module arrangements); determination of the impact of

this temperature on the maintenance, surveillance, and calibration

requirements of the modules; confirmation of acceptable module

performance under normal operating temperatures; and assurance of the

operability and performance of the modules under worst abnormal and

accident conditions affecting the equipment room ambient temperature .

' \\

29

(Updated) Unresolved Item 50-272 and 50-311/96-01-02: Electromagnetic *

and Radio Frequency Interference

During the January 1996 review of the Hagan module refurbishment and

replacement project, the inspector asked the licensee whether the

current program would address electromagnetic and radio frequency

interference (EMI/RFI).

Because of the NRC questions, the licensee

contracted the services of a consultant to evaluate whether the

replacement of the Hagan modules with NUS modules would represent an

increased EMI risk. A secondary objective of the review was to evaluate

whether the refurbishment of Hagan modules would similarly represent an

increased EMI risk.

The consultant's evaluation, described in Report No. CSR082, dated

April 11, 1996, concluded that the replacement of Hagan modules with NUS

modules would increase the immunity of the Hagan 7100 plant protection

and control system. Their conclusion was based on EMI immunity tests

performed on the modules, as well as on their review of the design

improvement included in the modules.

Regarding the refurbished module,

the consultant concluded that the replacement of aged electronic

components with new ones would improve module performance and,

therefore, reduce the potential for electromagnetic emission due to

deficient components.

The inspector reviewed the evaluation report and identified no areas of

concern regarding the replacement of the Hagan modules with NUS type

modules.

The inspector, however, observed that the report had not

specificallf addressed the increased speed of new solid state components

in the upgraded modules and the impact of the switching, integrated

power supplies used in the NUS modules on these components.

This item

remains open pending PSE&G's evaluation of these two issues and the NRC

review of the licensee's conclusions.

Configuration Control

The Salem Hagan 7100 series process control modules were supplied by

Westinghouse.

Although several years jgo Westinghouse sold this product

line to Rosemount, they continued to provide needed technical support to

their customers.

Westinghouse also continued to be the sole source for

replacement modules and spare parts and for the repair of failed units.

Apparently, from the time they were originally supplied to PSE&G, all

modules underwent several upgrades.

As stated in Salem Quality

Assurance audit report No. SNA95-092, dated October 21, 1995; when a new

order was placed, the modules were manufactured to their latest revision

level, unless PSE&G specified otherwise. Repairs, however, were made to

the extent necessary to render the modules functional again.

Drawings

of new or repaired modules were not furnished unless specifically

requested in the purchase order.

Due to this process, the Salem

instrument design used several revisions of the same module .

30

_PSE&G became aware of the existence of these design difference during

audits of Rosemount and Westinghouse in June and October 1995,

respectively, and when they reviewed the latest module drawings that

they had obtained to support their current module refurbishment effort.

The identified discrepancies resulted in the stoppage, on

October 10, 1995, of the refurbishment process, until engineering could

evaluate the impact of such discrepancies and propose a solution.

As

stated previously, a decision was made to upgrade all modules to their

latest revision level.

The inspector reviewed PSE&G's current configuration control process.

He determined that once the modules were refurbished and upgraded to the

latest Westinghouse drawing revision level, they were visually

inspected, catalogued and placed into stock in a controlled storage

facility. The inspector also determined that, when the licensee

received the latest Westinghouse drawings and part lists, they developed

a computerized data base that included both Westinghouse and PSE&G part

numbers.

This data base was then used to develop the bills of material

for the refurbishment of each module.

Components, properly labeled,

were kept in individual wrappers in a controlled storage facility. The

current material control program is described in procedure NC.NA-AP.ZZ-

. 0018(Q), Revision 2, dated April 10, 1996.

The licensee developed configuration control procedures for each type of

module.

The purpose of these procedures was to ensure that design

configuration is maintained when removing from or installing a module

into its assigned location within an instrument rack.

The configuration

process, e.g., procedure SC.IC-TI.ZZ-0102(Q) for the comparator.modules,

involved the dedication of a particular module to a specific instrument

loop, affixing the labeling necessary for its full identification, and

verifying that the design attributes for the specific application of the

module had been implemented.

If a module is removed from service for

any reason, the procedure requires that it be divested of its specific

identification, repaired if necessary, and returned to stock. A new

module is dedicated to the same service.

The inspector also addressed two specific issues regarding past

configuration concerns: first, control of safety and nonsafety-related*

inventory at the work area, and second, availability of adequate

documentation to the instrument and controls (I&C) department to ensure

that modules. were properly configured prior to installation in safety-

related systems.

Regarding the first issue, the inspector's review of the current

procedure, NC.NA-AP.ZZ-0018(Q), determined that it did not prevent

availability of both safety and nonsafety-related components at the work

area.

The procedure, however, included sufficiently specific

instructions about responsibilities and component control to prevent

inadvertent misuse of such components.

The procedure also provided

sufficient guidance regarding return of unused components to stock.

The

inspector considered the current requirements acceptable because of

c.

31

prestaging needs, technical personnel utilization, and existence of

routine as well as emergency work at the same time.

Currently, Hagan modules that are used .in both safety and nonsafety-

related applications are treated as safety-related. Therefore, the

inadvertent use of nonsafety-related parts in this application is

avoided.

The inspector's direct observation of the work area indicated

that materials were clearly labeled and properly controlled."

'Regarding the second issue, the inspector determined that currently,_ the

l&C group assigned to the refurbishment of the Hagan modules had up-to-

date documents available for their use. Until late 1995, the quality of

the documents available to the same group was less than adequate, as

evidenced by the results of the PSE&G's inspection of Rosemount and

Westinghouse, by the discrepancies identified during their review of the *

newly-obtained design drawings, and by the stop-work order on

October 10, 1995.

PSE&G's review of this issue in early 1995 had

incorrectly determined that the ~onfiguration control of the.Hagan

modules.was not a concern.

The inspector has no current concerns in

this area.

Review of UFSAR Commitments

A recent discovery of a licensee operating their facility in a manner

contrary to the Updated Fi.nal Safety Analysis Report (UFSAR) description

highlighted the need for a special focused review that compares plant

practices, procedures and/or parameters to the UFSAR descriptions.

While perfor~ing the inspections discussed in this report, the inspector

reviewed the applicable portions of the UFSAR that related to the areas

inspected. The inspector verified that the UFSAR wordi~g was cotisiste~t

with the observed plant practices, procedures and/or parameters.

Conclusions and General Comments

Based on hi~ review of .the refurbishment, testing, and configuration

  • control of the Hagan module, the inspector concluded* that the licensee

had made progress in developing a viable process to ensure a good

product and a good control of future modifications. The procedures

developed for this effort were detailed and easy to follow.

Based on

his interview of several engineering, technical and supervising_

personnel, the inspector also concluded that they were knowledgeable of

the process and of the module performance requirements.

Effective communication among supervision, engineering, and technical

personnel was evident in their resolution of identified discrepancies.

When discrepancies were identified, whether in the original design or

the refurbishment process, they were documented, discussed, and resolved

  • among appropriate groups.

The design change package process for NUS modules was acceptable,

although the instrument loop error is unresolved pending revision of the

I;)

32

calculation to include minimum calibration temperature and maximum

operating.module temperature.

The acceptability of design change package process for upgraded Hagan

modules is unresolved pending PSE&G's review of the packages to

determine the significance of the changes made to the circuit boards,

whether the design modifications constitute an unreviewed safety

question, and whether the design equivalence.process is applicable to

these modules.

The operating temperature of the NUS and Hagan modules was questioned by

the NRC previously, but a full and effective evaluation of the issue by

the licensee was not performed for its closure. Closure of this issue

is pending the licensee's review and assurance that the modules will be

capable of performing as intended under all anticipated operating

environments.

The inspector identified no EMI/RFI concerns regarding the NUS modules.

The susceptibility of the Hagan modules remains unresolved pending

PSE&G's verification that their performance is not affected by the speed

of new solid state components or by the switching, integrated power*

supplies used 1n the NUS modules on these components.

The review of past experience with the modules indicated the existence

of problems in the area of configuration control, some of which could be*

related to ineffective procurement guidelines in the past.

The licensee

efforts to regain contfol of the Hagan module corifiguration were good

and their development of procedures should enhance their ability to

maintain such control in the future.

E.8.4 Advanced Digital Feedwater Control System CADFCS) Modification*

a.

Scope of Review (IP 52002)

The ADFCS modification is involved in NRC Salem techni~al restart issues

114.

The review of the modification, Desig~ Package 2EC-3178, involved

interviews with members of the design and system engineering-staff,

review of design and software documentation, and a walkdown of the

equipment at the plant and maintenance facility. The inspectors

reviewed documents associated with the modification as follows:

  • * * * * * * * * *

safety analysis and evaluation report;

design basis;

setpoints and control constants;

electromagnetic interference (EMI) susceptibility;

human-machine interface (HMI)

maintenance

software verification and validation (V&V);

cross-connected data points;

software configuration control;

software access control .

33

b.

Background

The ADFCS modification replaced an analog control system for steam

generator water level control with an advanced digital feedwater control

system (ADFCS) by Westinghouse.

The main purpose of the modification

was to minimize plant unavailability due to reactor trips caused by

analog system component failures and low power instability.

--1

The ADFCS equipment was installed in Salem Unit 1, and only wire pulling

was accomplished for Salem Unit 2.

The ADFCS equipment for Salem Unit 2

was set up in a maintenance facility on the Salem site, awaiting the

site acceptance test (SAT).

The ADFCS provides automatic control of steam generator water level

with out operator intervention at a 11 power levels above 2%.

Inventory

in the steam generators is maintained by automatically positioning the

generator.

The ADFCS also controls the main feedwater pump.

In addition, the ADFCS also automatically controls the modulation of the

atmospheric relief valves (ARV).

There are automatic/manual control

stations for all the feedwater valves and the ARVs.

The ADFCS is implemented using the Westinghouse Eagle Distributed

Processing Family (WDPF) and is powered from the redundant vital

instrument buses, which are backed by battery inverter units.* The

system has two distributed processor units (DPU), each internally

connected as a fail-over processor pair. The processors use an Intel

386 microprocessor. Only one part of the internal fail-over pair

processors controls the. system; the backup processor receives current

data over the data highway, monitors the status of the control

processor, and performs diagnostics. Automatic switchover to the backup

processor occurs on power interruption, failur~ of the control processor

itself, or its shared memory, or math co-processor~ or data highway

interface.

When automatic switchover occurs, the backup processor

_

receives active data from the input/output (I/O) bus, and the algorithms

incorporate measures to insure bumpless transfer ..

The two DPUs contain the control algorithms and signal processing, but

do not control identical outputs and are not consjdered to be .redundant.

The processing for the f~edwater flow control valves and ARVs are

divided between the two DPUs. -One DPU controls the main feed pumps.

A

limited set of data points are shared over the redundant data highway

between the DPUs for some algorithms.

The ADFCS control algorithms were developed by Westinghouse.

ADFCS

designs similar to Salem are installed and operating at Prairie Island,

-Catawba, Ginna, and Diablo Canyon nuclear ~ower plants.

The protective system low feedwater flow trip, which involved steam

flow/feed flow mismatch, was ,eliminated. Three narrow range steam

g.enerator 1 evel inputs per loop were added to the ADFCS to compensate

34

for the elimination of the low feedwater flow trip. The narrow range

steam generator level inputs are continuously validated in the ADFCS by

a median signal selection (MSS) software compartson technique.

The

purpose of the MSS is to prevent a failed instrument channel from

causing a disturbance.in the ADFCS, which could then initiate a plant

  • transient that could require protective action.

The elimination of the

RPS low feedwater trip and the use of the MSS software technique was

previously reviewed and approved by NRR.

Three types of input signal validation using software techniques are

employed.

The first technique is the MSS, where the median of three

inputs is used for the control algorithms. This prevents. high or low

failures of a single input from affecting the control system.

The

narrow range steam generator level, steam flow, steam generator

pressure, feedwater flow, feedwater temperature, and feedwater header

pressure are validated using the MSS technique.

The second technique of input signal validation is arbitration, where

two inputs are compared; if they agree to a preset criterion, their

average is used for the control algorithms.

If the two channels differ

from the criterion, they are compared to an estimate of the variable

that ii calculated using other process measurements.

The input that is

closer to the estimate is then used for the control algorithms .. Turbine

first stage pressure is validated using the arbitration technique.

.

.

The third input signal validation technique is data quality check or

signal quality check for single input variables.

Diagnostics are incorporated that are automatically executed during the

normal operation of the system and do not disrupt the real-time

performance of the processor. Should a malfunction occur, the active

processor will fail over to the backup processor, *and a trouble alarm

will be generated.

An engineer/operator workstation connects to the system over the data

highway and provides the software engineering tools required to

configure and maintain the ADFCS.

The. workstation is used primarily for

on-line monitoring of control loops, and process inputs, outputs, alarm

status, hardware status, and high/lbw limits. The operator mode allows

graphics to be presented that allow defined actions, such as changing

selected alarm and process variables along with viewing process values.

The engineer mode allows construction of graphics for the operator mode,

. configuration of software, and downloading of application software for

use in the DPUs.

The workstation access is controlled by keylock and is

intended to.be used by system engineers and l&C technicians.

In normal

operation, after the programs and constants have been downloaded to the

DPUs, the workstations do not perform any control system functions.*

35

I.

c. Observations and Findings

Safety Anafysis/Evaluation

/.

The inspectors reviewed the licensee safety evaluation and noted the

following:

(1)

Any effects of the consolidation of the main feed pump speed

control were not considered. There is the possibility that the

main feed pump control may fail in conjunction with the control of

the feedwater regulator valves and the control of the ARVs.

This

is because the control systems are controlled by the same digital

processor. This possibility co~ld be classified as a different

type of an anticipated operational occurrence initiating event.

(2)

The effects of the consolidation of the ARVs may cause a different

type of an anticipated operational occurrence initiating event.

The licensee stated that the failure of one or more ARVs in

conjunction with one or more feedwater control valves was

analyzed.

The licensee changed the analysis of Chapter 15.4.8.2,

"Mass and Energy Releases Following a Steamline Rupture," to bound

this different type of initiating event.

(3)

The new control mode of the feedwater bypass valves may cause the

possibility of a malfunction of a different kind.

The licensee

stated that this malfunction was considered, and the analysis of

USFAR Chapter 15.2.10, "Excessive Heat Removal Due to Feedwater

System Malfunction," was changed to bound the possible

malfunction.

The above issues apparently conflict wtth 10 CFR 50.59(2)(ii) and the

NRC Inspection Manual Part 9900, "IO CFR Guidance."

The issues need

clarification from a licensing standpoint, since it appears that the

possibility for a different type of initiating event or a malfunction of

a different type than any evaluated previously in the USFAR may be

created, even though the licensee stated that the modified analyses show

the effects are bounded in some instances.

The above issues are considered unresolved pending NRC configuration of

the licensee's analyses and further NR.C regional and headquarters review

(URI 50-272/96-06-05).

Design Basis

The Westinghouse proprietary functional requirements and detailed design

documents covered generic criteria for the process sampling rates and

processing delays based on engineering judgement, but there were no

references to any specific analyses for sampling rates for Salem.

The

licensee calculated a worst~case processing delay and stated that it was

less than processing delays for other ADFCS plants.

' I

36

The inspectors determined through interviews that engineering judgement,

based on operational experience at other ADFCS plants and computer

simulations, most likely formed the bases for the Salem values of the

sampling rates and processing delays.

Setpoints and Control Constants

The inspectors determined through interviews that Westinghouse developed

the design bases for the setpoints and software constants using data

from the analog system and their experience with other PWR plants. * The

setpoints and control constants incorporated the Salem unique

characteristics of the steam piping, feed piping, valve Cv

linearization, and pump performance curves.

The inspectors concluded that the setpoint~ and control constants were

based on empirical data and analyses from other ADFCS plants, with the

necessary particularization for Salem.

EMI Testing

The ADFCS system was tested by Westinghouse for EMI-radiated

susceptibility with the cabinet doors open and closed.

The

configuration tested used the Intel 8086 microprocessor.

The

susceptibility field strength from 20 MHz to I GHz was three

volts/meter; from 20 MHz to 500 MHz the field strength was 20

volts/meter.

The I/O cards have surge-withstand capabilities, according

to Westinghouse documents.

The ADFCS was not tested specifically for conducted EMI susceptibility.

The licensee recognized this and plans to assess the ability of the

ADFCS to handle conducted susceptibility on the 1/0 and power lines.

The inspectors concluded that the licensee considered EMI

susceptibility.

Human-Machine Interface CHMil

.The licensee stated that the design objective for the ADFCS HMI was to

.minimize physical changes to the operator interface so as to minimize

impact on plant operations personnel.

The same console manual/automatic

(M/A) stations, indicators, and status lamps that were used for the

analog design were used for the ADFCS, with the appropriate

hardware/software interfaces. The console arrangement was slightly

changed and enhanced for the ADFCS, and the manual control pushbuttons

on the M/A stations were changed from linear control to exponential

control.

The "ADFCS Trouble" annunciator window was added as an indication for

certain classes of failures, such asi input signal failure, power supply

failure, loss of data highway, or processor hardware or software

diagno~tic failure.

The "ADFCS Switch to Manual" window was added as ari

indication for the operator to take manual control of the M/A stations.

. d.

37

The inspectors reviewed the operator training handouts, lesson plans,

and alarm response procedures.

The differences between the analog

operator controls and the ADFCS operator controls were* identified and

covered in appropriate detail.

The inspectors concluded that the lic~nsee met their HMI design

objective of minimizing impact on plant operations personnel.

l&C Maintenance

The licensee purchased a set *Of ADFCS equipment to use for maintenance

training. The training equipment was used in *a six ~eek_ vendor course

for ~ngineers and technicians that covered hardware and software, which

was held at the PSE&G training center. The maintenance procedures were

debugged on the trainer. The l.icensee plans to use the trainer to test

spare boards before they are installed in the operating system.

The inspectors walked down the trainer. Wrist grounding straps on

coiled leads were installed at the front and rear of the cabinets as a

precaution against electrostatic discharge pulses being introduced into

the electronic components by personnel.

The inspectors concluded that the use of the ADFCS trainer was an

effecti~e method for enhancing the technical quality of the l&C

maintenance activities.

Walkdown

The inspectors walked down the ADFCS installation at the site. The

processing and 1/0 cabinets and the workstation are in the relay room .

. The inspectors observed a demonstration of the monitoring of the ADFCS

. system using the workstation.

The ADFCS cabinets had louvered-doors.

The inspectors observed that

front and rear access to the cabinets were adequate and that the

interior temperature rise of the c*binets was not excessive.

e. Conclusions

The inspectors concluded that there are three 10 CFR 50.59 issues that

need clarification from a licensing standpoint. It appears that the

possibility for a different type of initiating event or a malfunction of

a different type than any evaluated previously in the USFAR may be

created, even though the licensee stated that the modified analyses show

the effects are bounded in- some instances (URI 96-06-05).

The inspectors determined through interviews that engineering judgement

based on operational experience at other ADFCS plants and computer

simulations most likely formed the bases for the Salem values of the

sampling rates and processing delays.

38

The inspectors concl~ded that the setpoints and control constants were

based on empirical data and analyses from other ADFCS plants, with the

necessary particularization for Salem.

The inspectors concluded that the licensee considered EMI

susceptibility.

IV. Plant Support

P4.

Staff Knowledge.and Performance in EP

P4.l Emergency Classification Performance during Training. *NRC Restart Item

III. 7

a.

Inspection Scope (71707)

During operator requalification training, the inspectors observed and

assessed licensed operator performance, senior reactor operator (SRO)

classification of adverse plant conditions, and training staff performance.

b.

Observations and Findings

Notable improvements were observed in operator performance.

For example,

operators showed significant improvement in repeating back instructions and

information relating to equipment status. Senior reactor operators

demonstrated better command and control in that the NSS led operator

response* by reading procedures and directing the NCO response while the SNSS

monitored overall plant and operator performance.

The NCOs displayed much

improved division of responsibilities, knowledge of plant system~, and

familiarity with procedures. Also, the operators demonstrated noticeable

improvement in team work, such as the NCOs insuring the NSS understood the

impact of a particular equipment problem on overall plant operation. The - .

instructors also demonstrated improved performance.

For exa~ple, during one

sim~lator sc~nario involving a seismic event, the instructors paused the

simulator after initial operator response to lead a discussion on the design

basis for seismic events.

During an operator requalification exam, however,

the SNSS incorrectly classified a loss of all offsite and onsite power, the

training staff did not notice the error,. and the simulator lesson plan did

not provide the correct classification. In addition, the inspector

. id~ntified that the training ~taff did not consider the incorrect

classification cause for failing the SNSS,'nor.did the lead in~tructor

consider it necessary to ini'tiate a Condition Report (CR) to document the

error in the lesson plan.

The Operations Manager, however, directed the

training staff to consider the SNSS exam a failure, and the other members of

the training staff initiated a CR.

c.

Conclusions

Overall, during requalification training operators demonstrated significant

improvement in command and control, technical competence, and teamwork.

In

one case, however, an SNSS_incorrectly classified a postulated event.

The

lesson plan for the event contained the incorrect classification, the

39

instructor did not detect the error and did not take appropriate corrective

action until the inspectors questioned the corrective acti~n and the

operations manager became involved~

P5

Staff Training and Qualification in EP

PS.I Staff Training and Qualification in EP. NRC Restart Item III.I3

a.

Inspection Scope (7I707)

During an unannounced call out EP exercise, inspectors observed emergency

response organization and EP staff performance.

b. Observations and Findings

The SNSS corr~ctly classified the event in accordance ~ith the event

classification guide.

The technical support center (TSC) and emergency

operating* facility (EOF) staffs met their goal of staffing the facilities

within 90 minutes of declaration of an Alert, despite confusion stemming

from the call out message.

Although a significant number of the ERO

responders expressed confusion over whether the call out message directed

them to respond, they appropriately decided to go to their designated

emergency facility.

The TSC director demonstrated effective leadership.

For example, he called his staff together, briefed them on the nature of the

  • event, and provided goals for event response.

The EOF director, on the

other hand, did not demonstrate effective command and control.

He discussed

the call out message with various EOF staff, and did not provide leadership

in responding to the event scenario. * The EP staff frequently confused their

roles as scenario controllers and referees with the roles of instructor and

player.

In some instahces, they made it difficult to determine the ERO

effectiveness.

For ~xample, one controller prompted the SNSS.to let the

controller perform the role of SNSS for the purpose of the drill.

In the

TSC, a controller showed an engineer coordinator how to perform his duties.

In the EOF, a controller performed the duties of director while the

designated director pursued clarification of the call out message.

c. Conclusions

During an unannounced call out EP exercise, the ERO met the goal of manning

the TSC and the EOF within 90 minutes. Overall, the ERO adequately

discharged. its duties required to protect the health and safety of the

public, however, the EP staff reduced the effectiveness of the traini.ng by

not allowing the ERO staff, in some cases, to make errors.

Sl

Conduct of Security and Safeguards Activities

SI.I Suspicious Substance Found in Protected Area

a.

Scope *cn 750)

The inspectors observed plant management's appropriate response to a

technician's discovery of a packet of white powder in a locker.

-

40

b.

Observations and Findings

On April 11, a temporary radiation protect ion (RP) technician discovered a

packet of white powder in a locker that had been his but that he had vacated

some time ago.

Temporary workers use the locker room located inside the*

Protected Area but outside Vital Areas.

The technician notified his .

supervisor, who notified security management.

Security management sent the

packet to local authorities for analysis. At about 3:30 p.m., authorities

  • notified Salem management that the substance was cocaine and weighed

approximately 1/2 gram.

Subseque~tly, Salem m~nagement initiated a drug

sweep using a drug dog.

The sweep included Salem locker rooms, rest rooms,

the contractor change house, and similar buildings at the Hope Creek

facility.

The search did not uncover any additional examples of illegal

  • substances. Salem management also tested the.thirty-six people that use the

locker room area for drug use.

No individµals tested positive.

At about 5:00 p.m. on April 12, *a temporary RP technician 'admitted that he

had planted the packet as a joke and that the packet contained coffee

creamer.

Because management had already for-cause tested the technician,

they elected not to retest him.

Salem management interviewed the individual

and concluded that his story was credible. They also sent the substance to

the State police crime lab for further testing to resolve what the substance

was.

On April 30, the Lower Alloways County Chief of Police reported that

the contents of the packet tested negative for illicit substances~

confirmi.ng the technician's story .. Salem management took appropriate

disciplinary action.

c. Conclusions

Salem management responded aggressively and quickly to the report of

discovery of an apparently illegal substance in the protected area. Their

actions were comprehensive and notifications were timely.

  • By including a.

search of Hope Creek facilities, management showed sensitivity to the

generic implications of discovering an apparently illegal substance in the

protected area. The inspectors concluded Salem management responded

appropriately.

Laboratory tes.ts later concluded the. substance was a

powdered coffee creamer.

V. Management Meetings

Xl

Exit Meeting Summary

The inspectors presented the overall inspection results to members of licensee

management at the conclusion of the inspection on June 6, 1996.

The licensee

acknowledged the findings presented. Additionally, specialist inspectors

presented their findings on ~arch 22, April 19 and 23, 1996.

The inspectors asked the licensee whether any materials examined.during the

inspection should be considered proprietary .. No proprietary information was

identified.

I

X3

41

Management Meeting Sununary

On May 6 and 7, Mr. James Taylor, Executive Director for Operations, Mr.

Frank Miraglia, Deputy Director, NRR, and Mr. Thomas Martin, Administrator,

NRC Region IJ visited Salem to followup a meeting with the PSE&G Board of

Directors held during 1995 .

INSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 60705:

Preparation for Refueling.

IP 61726:

Surveillance Observations

IP 62703~ * Maintenance Observations

IP 71707:

Plant Operations

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-272&311/96-06-01

VIO

Procedure non-compliance

50-272&311/96-06-02

URI

UFSAR and licensing basis

nonconformances

50-272&311/96-06-03

URI

Instrument loop inaccuracy

50-272&311/96-06-04

URI

Hagon design change

50-272&311/96-06~05

URI

Mods to feed control

Closed

50-272&311/94-18-01

VIO

Inadequate 125VDC acceptance

criteria

50-272&311/93-82-06

URI

UPS output harmonica distortion

50-272&311/93-82-08

URI

Safety related storage tanks volume

calculation

50-272&311/96-01-02

URI

Radio frequency interference

50-272&311/96-01-01

URI

Temperature of modules

Discussed

50-272&311/95021-02

IFI

Service water reliability issues

50-272&311/95029-00

LER

GE SBM control switch degradation

50-272&311/93-82-07

DEV

Onsite fuel oil requirements

50-272&311/94-18-02

URI

EOG load fluctutttions

'

'

I

AFW

CA & QA

CAG

CAP

CARB

ccw

CCWHX

CR

ECACs

.EOG

EOF

ESFAS

EP

ERO

FHAV

FHB

FME

FSAR

FPI

GE

JW

LER

MMIS

MDAFWP

MRC

NAP

NCO

NBU

NRC

NSR

NSS

OHA

OSR

PDR

PSE&G

QA

RAP

RC

RCM

RP

SAC

SF P-

SER

SI

SNSS

SW

sws

TSC

UFSAR

LIST OF ACRONYMS USED

Auxiliary Feedwater

Corrective Action and Quality Services

Corrective Action Group

Corrective Action Plan

Corrective Action Review Board

Component Cooling Water

Component Cooling Water Heat Exchanger

Condition Report

Emergency Control Air Compressors

Emergency Diesel Generator

Emergency Operations Facility

c:;>

Engineered Safety Feature Actuation System

Emergency Preparedness

Emergency Response Organization

Fuel Handling Area Ventilation

Fuel Handling Building

Foreign Material Exclusion

Final Safety Analysis Report

Failure Prevention, Inc.

General Electric

Jacket Water

Licensee Event Report

Maintenance Management Information System

Motor Driven Auxiliary Feedwater Pump

  • Management Review Committee

Nuclear Administrative Manual

Nuclear Controls Operator

Nuclear Business Unit

Nuclear Regulatory Commission

Nuclear Safety Review

Nuclear Shift Supervisor

Overhead Annunciators

Operational Safety Review

Public Document Room

Public Service Electric and Gas

Quality Assurance

Restart Action Plan

Root Cause

Root Cause Manual

Radiation Protection

Station Air Compressor

Spent Fuel Pit

Safety Evaluation Report

Safety Injection

Senior Nuclear Shift supervisor

Service Water

Service Water System

Technical Support Center

Updated Final Safety Analysis Report

I

DOCKET/REPORT NOS.:

LICENSEE:

FACILITY:

LOCATION:

DATES:

INSPECTOR:

APPROVED BY:

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

50-272/96-06 AND 50-311/96-06

Public Service Electric and Gas Company

Salem Nuclear Generating Station

Units 1 and 2

Hancocks Bridge, NJ

March 18-22, 1996

A .. JJJY~l~

---"--/

A. Dell a Greca, Sr. Reactor Engineer

Electrical Engineering Branch

Division of Reactor Safety

[,/~tJ.;UJ

William H. Ruland, Chief*

Electrical Engineering Branch

Division of Reactor Safety

vf-c/l~t

Date

AREAS INSPECTED:

Announced.safety inspection to review ~nd evaluate PSE&G's

actions to address several unresolved issues resulting .from the electrical

distribution system functional inspection of the Salem plant and other

electrical system inspections.

-1

ENGINEERING REPORT DETAILS

50-272/96-06 AND 50-311/96-06

1.0

INSPECTION PURPOSE AND SCOPE

The purpose of the inspection was to review and evaluate PSE&G's actions to

resolve several issues identified previously by the NRC during the

electrical distribution system functional inspection (EDSFI).

Closure of

EDSFI-related issues is one of the items identified by the NRC as requiring

completion prior to the restart of Salem, Units 1 and 2.

The inspector's review, performed in accordance with the guidance of

Inspection Procedure 92903 and Temporary Instruction 2515/111, addressed the

licensee evaluation of each issue, the resulting corrective actions, and the

adequacy of these actions. Five previously identified issues were reviewed,

as detailed in Section 2.0 of this report.

2.0

REVIEW OF PREVIOUSLY IDENTIFIED ISSUES

2.1

(Updated) Deviation 50-272 and 50-31l/93-82-07: Onsite Fuel Oil

Requirement for Seven-Day Emergency Diesel Generator Operation

a.

Inspection Scope

The EDSFI team identified a discrepancy between the statement in Section

9!5.4 of the UFSAR and the available fuel in the diesel fuel oil storage

tank (DFOST).

The UFSAR stated that each 30,000 gallon DFOST could supply

one diesel with enough oil for seven-day operation.

In reality, the

licensee's calculation addressing this issue took credit for fuel available

in a nonsafety-related storage tank, capable of containing 20,000 barrels of

oil, for this commitment.

The licensee's resolution of this issue was reviewed previously

(IR 50-272/94-33 and 50-311/94-33), but it was left open pending the

licensee's resolution of two discrepancies identified by the NRC in the

supporting calculation and the acceptance by the NRC of a license amendment

submitted to the NRC on June 29, 1994.

The two discrepancies pertained to the protrusion of the suction pipe in the

DFOST and the licensee's basis for their use of the EDG-2C consumption rate

in the calculation of record.

The inspectors concern with the first issue

was that, because the tank design had specified only the minimum protrusion*

(1/2 inch), the licensee's assumption (2 inches) might not be sufficiently

conservative. Regarding the second. issue, the inspector understood that

fuel

o~l consumption measurements had been recently taken and their use was

more appropriate.

The purpose of this inspection was to revi~w the licensee's resolution of

the two calculation discrepancies and the status of the license amendment .

2

b *

Observations and Findings

. During the current inspection, a review of Calculation No. S-C-DF-MDC-1316,

Revision 1, determined that neither observation had been addressed.

Discuss ions with licensee engineering, however, determined that: .

1)

They had evaluated the measured consumption rates and concluded that

their bases for using the consumption rate of EDG-2C were appropriate

because:

EDG-28 and EDG-2C were equipped with turbochargers of a newer

design and had higher fuel consumption characteristics than the other

four engines; EDG-2C was more heavily loaded than EDG-28; and EDG-2C

always displayed a higher fuel consumption than the other engines.

2)

A license amendment that increased the minimum required fuel oil in

DFOST from 20,000 to 23,000 gallons per tank had been reviewed and

accepted by the NRC in their letter, dated June 20, 1995.

3)

At the time of the technical specification (TS) amendment request, the

licensee also submitted a FSAR change request. This change that served

as the basis for the TS amendment, specified that the TS minimum fuel

oil volume would be sufficient to operate two diesels for 4-1/2 days.

Operation beyond this time would require replenishment of the DFOSTs

from the onsite 20,000 barrel storage tank or from offsite sources.

4)

The suction pipe protrusion into the tank was not verifiable without

either emptying the tanks or using x-rays.

Because of the TS and FSAR

changes, however, and of the conservative assumptions used in

calculating diesel operating time, a more conservative value for pipe

protrusion would hav~ changed only minimally the estimated time when

more fuel oil was needed.

The inspector was satisfied with the licensee's justification.

Therefore, he evaluated their ability to secure oil within the specified

time and to transfer it to the DFOSTs.

The inspector determined that

the licensee had blanket orders with two fuel oil suppliers and the

ability to obtain oil by land or water within a very short time, if the

onsite 20,000 barrel tank was not available.

In addition, the licensee

had onsite fuel test capabilities.

This review of applicable documents and a walkdown of the fuel oil storage

and transfer systems also identified several discrepancies as follows:

The fuel oil emergency connections* had two different connection

fittings, neither of which was directly usable with hose connectors

typically found on tanker trucks.

A portion of the emergency connection pipe between the ground and the

only external support had not been seismically analyzed .

  • -

3

The use of ~he oil from the 20,000 barrel storage tank relied on the

availability of hoses and pumps.

No hoses or pumps had been dedicated

for this service and no instructions were available on how to obtain

such equipment.

The emergency connections had never been tested to ensure their

availability following an accident.

Following the inspection, on May 20, 1996, the inspector questioned again

the pipe protrusion in the DFOST and licensee's ability to demonstrate the

availability of 23,000 gallons of fuel oil in each of the tanks.

He

determined that:

The licensee had contacted the vendor and had been informed that the

assumed two-inches protrusion was conservative. The specified 1/2-inch

minimum protrusion note was standard practice for fillet weld

inspection.

The li~ensee, nonetheless, issued an action request to

verify the pipe protrusion.

Following the approval of the TS amendment, the licensee had reduced the

administrative limit for minimum tank fill from 97 inches, corresponding

  • to approximately 26,000 gallons (when a 5-inch gauge error is

considered) to 85 inches, corresponding to 23,005 gallons when the same

error is considered.

The change was apparently made to prevent

overfilling of the tank.

The surveillance procedure change did not undergo technical review

because it incorporated an approved TS and FSAR revision.

In addition,

a safety evaluation according to 10 CFR 50.59 was not performed for the

same reason.

  • . The 5-inch gauge error stated in the storage tank volume calculation was

calculated (calculation No. SC-DGOl0-01) assuming a maximum fuel oil

specific gravity of 0.86. This number was based on the licensee review

of the fuel oil analysis history file.

An older version of the TS surveillance requirements (SR 3.8.3.4.b)

specified verification that the fuel oil absolute specific gravity was

greater than or equal to 0.83 and less than or equal to 0.89, in

accordance with ASTM standard 0975~ If 0.89 had been used, the meter

error could be approximately 8.7 inches, rendering the fuel oil lower

limit (85 inches) specified in the surveillance procedure too low.

The

current TS requirements (4.8.1.1.3.b) do not mention specific gravity,

butcontinue to refer to the ASTM standard for verification of viscosity

and water sediment.

A purchase specification was not immediately available to verify

specific gravity requirements .

-*~

  • t

I

c.

4

Conclusions

The inspectrir concluded that sufficierit justifications were available to

support the license amendment regarding minimum volume requirement in the

DFOST and the proposed UFSAR changes regarding onsite fuel oil availability

for continuous EOG operation ( 4. 5 days) and other fue 1 oil sources. The

licensee's ability, however, to verify the quantity of fuel oil in the

storage tanks, is unknown pending measurement of the pipe protrusion and

licensee applicability review of the higher specific gravity value.

The

inspector also concluded that the ability to replenish the tanks for

emergency operation of the EDGs beyond the calculated 4.5 days had not bee_n

fully_ evaluated. This item remains open pending the NRC review of the

licensee actions to address the identified discrepancies.

2.2

(Updated) Unresolved Item 50-272/94-18-02:

Emergency Diesel Generator

Load Fluctuations Root Cause

a.

b.

  • Inspection Scope

On August 16, 1994, during the monthly surveillance of EOG IA, the operator

noticed load fluctuations of approximately 100 kW (typical) from the target

value of 2600 kW.

In the follow-up inspection, Reports 50-272, 50-311, and

50-354/94:...18; the NRC evaluated the subsequent troubleshooting performed by

PSE&G and considered it adequate.

The issue was unresolved pending

completion of the licensee's root_ cause analysis and review by the NRC .

The purpose of this inspection was to determine the status of the corrective

actions initiated by the licensee during the inspection and to evaluate the

results of their root cause analysis.

Observations and Findings

The licensee's troubleshooting to address the event identified a number of

malfunctions, all of which, they believed, were responsible for the load

  • control problem of the diesel. Therefore, the -licensee took a number of

actioris, including: replacement Qf the electrical governor controller -

(EGA); lubrication of the fuel rack (found to be stickirig)~ and replacement

of the mechanical governor controller (EGB).

Following the event, the licensee sent the EGB to the governor manufacturer.

In their analysis report, the manufacturer stated that they had found two

problems:

1) the "electrical P.V. plunger had a slight ring (worn area) on

-the center of control land"; and 2) "it was missing a gasket on the bushing

retainer for the drive shaft."

The manufacturer also stated that, although Problem 1 could cause the

oscillation problem, they could not duplicate the response during their test

of the unit.

Problem 2 could only cause a leak from around the drive shaft.

Neither problem would cause the shifting of null voltage noted by the

licensee when the unit was on the diesel. They faxed their conclusions to

PSE&G with a message that stated, "the oscillation of terminal shaft could

cause load fluctuations ... "


,.,

.f

c.

5

The subsequent root cause analysis by the licensee, that included change,

barrier, and causal-factor analyses, echoed the vendor conclusions and

attributed the oscillation to the worn area found on the P.V. plunger.

The inspector reviewed the root cause analysis and observed that the

licensee had not evaluated the impact of the EGA replacement, the fuel rack

lubrication, and other troubleshooting activities on the analysis results.

Also, they had not discussed the inability by the vendor to reproduce in the

laboratory the symptoms observed during the oscillations.

He discussed

these observations with the licensee who agreed that the analysis could have

addressed the other issues, but reaffirmed their convic;tion regarding the

EGB being the source of the oscillations. The licensee also believed that

it was not necessary to inspect or replace the EGBs of the other five

diesels because they had observed no abnormal symptoms in the performance of

the other diesels.

During the original inspection, the licensee had initiated actions to

enhance the EOG maintenance procedure.

The current inspection evaluated the

status of these actions and found that seven procedures addressing

lubrication, corrective and preventive maintenance, and inspection of the

diesel engine had been revised to address lubrication and maintenance of the

fuel rack and fuel pump adjustments.

While discussing the EOG IA event with licensee engineering personnel, the

inspector determined that on March I3, I996, EOG 2A had experienced load

oscillations. The event occurred while the licensee was returning EOG 2A

from an I8-month scheduled outage test. The licensee stated that the

oscillations were related to a governor oil change performed without proper

venting.

The licensee had corrected the problem and initiated a level I

root cause analysis of this new issue. lhe licensee also stated that the

new root cause analysis would reevaluate the EOG-IA load oscillations.

Conclusions

The inspector concluded that the licensee had taken acceptable actions to

correct the EOG IA malfunctions and to improve lubrication and maintenance

of applicable engine components.

The root cause analysis, however, should

have also evaluated the impact of the troubleshooting activities on the

analysis results.

The inspector deferred his conclusions regarding the cause of the EOG 1A

load oscillations until the oscillations recently observed in the EOG 2A

load control are evaluated and the new root cause analysis is completed.

This issue remains open pending the licensee's completion of the analysis

and the NRC's review of its results and actions.

2.3

(Closed) Violation 50-272 and 50-3II/94-I8-0I: Inadequate I25Vdc

Battery Test Acceptance Criteria

In August I994, during the subject inspection, the NRC found that the

acceptance criteria for the I25 Vdc station batteries service test

procedure, No. SC.MD-ST.I25-0004(Q), did not reflect the result of the

6

125Vdc system study, Calculation No. ES-4.003(Q). Although PSE&G had

already developed a procedure change request to address the discrepancy

before the next 18-month test, the NRC determined that the licensee's

failure to correct the discrepancy previously was a violation of 10 CFR,

Appendix B, Criterion XI requirements.

The same issue had been previously

identified, in early 1992, at Hope Creek.

The licensee did not dispute the violation, as stated for the Salem Station,

and attributed it to inadequate communication within the organization and

their failure to implement a formal requirement to identify procedures

impacted by calculations.

In their response to the NRC, Letter NLR-N94179

dated October 13, 1994, PSE&G proposed several actions to prevent

recurrence.

During the current inspection, the NRC inspector evaluated the adequacy and

status of the PSE&G's proposed actions.

He determined that the licensee had

completed all the actions as described in their letter to NRC to prevent

recurrence.

Because the violation was partly the result of inadequate communications

between the two plants, the inspector questioned the status of two action

items selected at random from a list developed for Hope Creek during a

meeting between the two engineering organizations. One of these issues

pertained to the EOG test procedure that permitted the EOG output voltage to

be below the degraded voltage setting; the other pertained to the need for

verifying the Uninterruptible Power Supply (UPS) output voltage total

harmonic content. *The inspector found that no actions had been taken by

Hope Creek engineering to close either issue and no tracking mechanism was

available to ensure their timely resolution and closure.

By the end of the

inspection, the licensee provided new action items and a schedule for

completing the actions.

The i-nspector concluded that actions taken by Salem engineering to address

the above violation were appropriate and sufficient and the issue is closed.

  • The inspector also concluded that communications between plants continued to

be less-than-effective in that a meeting to evaluate potential issues

affecting the plants had taken place, but Hope Creek had failed to follow up

on the results of this meeting~

Communications between the two plants is part of the NRC restart action plan

for Salem. Actions taken by the licensee to improve communications and the

results of these actions will be evaluated during the inspection of this

area prior to the Salem plant restart.

2.4

(Closed} Unresolved Item 50-272 and 50-311/93-82-06: Uninterruptible

Power Supply Output Harmonic Distortion

a.

Inspection Scope

The purchase specification for the 115 Vac vital instrument bus

uninterruptible power supplies (UPS) required that the total output voltage

harmonic content did not exceed 5% of the fundamental voltage.

The licensee

b.

7

had never verified this attribute of the UPS, but agreed that they should

verify it. The purpose of this inspection was to determine the method and

results of the licensee's verification tests and the acceptability of these

results.

Observation and Findings

The inspector's review of the actions taken by the licensee to verify the

.UPS output voltage total harmonic distortion {THD} determined that:

The licensee had revised the inverter preventive maintenance {PM}

procedure {SC.MD-PM.115-000l{Q}, Rev. 4} to include steps to verify the

output voltage THD each time the inverter underwent PM.

Steps 5.3.56.

through .63 and .68 through .71 of this procedure require the use of a

harmonic distortion analyzer for the voltage THD verification. The

procedure also required adjustment of the inverter and ac line regulator

to less than 5% THD and notification of responsible engineering and

operation personnel if the adjustment could not be made.

Measurements taken in 1994 showed that the output voltage THD ranged

from 4.58% to 4.78%.

An evaluation had been made of the impact of their planned change of 75

Hagan modules to equivalent modules furnished by NUS.

This evaluation

had determined that the proposed changes would result in a THD increase

of only 0.15%.

Plans also had been made to verify the results of their

analysis during the Hagan modules change process.

The licensee was evaluating the UPS loads to determine the maximum

acceptable THD percentage.

c.

Conclusions

Based on his review of the measurements taken during the 1994 PM of the

inverters and the licensee's calculation of the THD change due to the

planned Hagan module changes, the inspector concluded that the licensee had

acceptably verified that the UPS output voltage did not exceed the specified

5% THD.

This item is closed.

2.5

(Closed) Unresolved Item 50-272 and 50-311/93-82-08: Safety-Related

Storage Tanks Volume Calculation

a.

Inspection Scope

While reviewing Calculation No. S-C-VAR-CDC-0095, the EDSFI team determined

that the calculation failed to account for unusable volume {e.g., vortex}

and.level instrument error in the determination of available fluids.

The

calculation applied to 28 tanks for both units.

The purpose of this inspection was to review the action taken by the

licensee to revise the calculation and evaluate the calculation results.

b.

8

Observation and Findings

The inspector's review of the licensee's corrective actions to address the

above finding determined that:

The licensee had revised Calculation No. S-C-VAR-CDC-0095 to delete all

calculations pertaining to safety-related tanks and had issued a new

calculation, No. s~C-VAR-MDC-1429, to address the same tanks.

The new calculation had addressed all the EOSFI team observations,

including vortex and loop accuracy.

The calculation was very detailed in the assumptions and methods used

for the determination of available volumes.

All volumes calculated were

evaluated for impact on technical specification or other requirements.

The revised calculation had only minimal impact on previously calculated

volumes.

In no case was a technical specification requirement affected

by the revised volumes.

c.

Conclusions

The licensee had properly ~ddressed the EOSFI team observations. The

clarity and quality of methods used in the calculation were good.

The

impact of the calculation revised results were pro~erly evaluated. This

item is closed.

3.0

MANAGEMENT OVERSIGHT AND GENERAL CONCLUSIONS

The inspector's review of the five previously identified issues addressed by

this report indicated acceptable resolution of most issues.

The

calculations were us~ally detailed and thorough and the evaluations, in

general, indicated good understanding of the issues. The evaluation of two

issues, however, was.less than thorough.

As a result, insufficient bases

were available for their closure. For instance, acceptable background

documentation had been developed to justify the reduction of onsite fuel

requirement from seven to four and a half days.

The evaluation, however,

had failed to ensure the availability of the emergency connection to the

DFOSTs.

Similarly, a good effort was evident in the troubleshooting of the

EOG load fluctuation.

The root cause analysis, however, had failed to

evaluate the impact of the troubleshooting activities on the analysis

results. Therefore, the acceptability of these results was unknown.

Management involvement in the resolution of the issues was evident in their

knowledge of the issues themselves and in their direct follow-up of more

critical issues. Their involvement, however, was less than effective in the

determination of the root cause analysis for the EOG load fluctuations and

in the emergency connection to the OFOST issues .

.....-------

_,

.

-

9

4.0

REVIEW OF UFSAR COMMITMENTS

A recent discovery of a licensee operating their facility in a manner

contrary to the Updated Final Safety Analysis Report (UFSAR) description

highlighted the need for a special focused review that compares plant

practices, procedures and/or parameters to the UFSAR descriptions. While

performing the inspections discussed in this report, the inspector reviewed

the applicable portions of the UFSAR that related to the areas inspected.

The inspector verified that the UFSAR wording was consistent with the

observed plant practices, procedures and/or parameters.

5.0

MANAGEMENT MEETINGS

The inspector presented the *inspection results to members of licensee

management at the conclusion of the inspection on March 22, 1996.

The

licensee acknowledged the findings presented~

_The inspector also asked the licensee whether any materials examined during

the inspection -should be considered proprietary.

No proprietary information

was identified.

6.0

PARTIAL LIST OF PERSONS CONTACTED

Public Service Electric and Gas Company

C. Manges

M. S. Bursztein

G. J. Overbeck

E. H. Villar

C. Warren

C. Bakker

M. McGough

L. Storz

D. Garver

D. Tauber

D. Garchow

Licensing Engineer

Nuclear Electrical Engineering Manager

Director, System Engineering

Licensing Engineer

General Manager, Salem Station

Operations, Salem Station

Design Engineering and Projects

Senior Vice President, Nuclear Operations

Salem System Engineering

Manager, Quality Assurance, Salem

Director, Engineering S/G Project

U. S. Nuclear Regulatory Commission

W. Ruland

Chief, Electrical Engineering Branch, DRS