ML18102B431

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Integrated Insp Repts 50-272/97-12 & 50-311/97-12 on 970427-0621.Violations Noted.Major Areas Inspected: Operations,Engineering,Maint & Plant Support
ML18102B431
Person / Time
Site: Salem  PSEG icon.png
Issue date: 07/01/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18102B428 List:
References
50-272-97-12, 50-311-97-12, NUDOCS 9707110369
Download: ML18102B431 (31)


See also: IR 05000272/1997012

Text

  • Docket Nos:

License Nos:

Report No.

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved by:

U. S. NUCLEAR REGULATORY COMMISSION

50-272, 50-311

DPR-70, DPR-75

REGION I

50-272/97-12, 50-311 /97-12

Public Service Electric and Gas Company

Salem Nuclear Generating Station, Units 1 & 2

P.O. Box 236

Hancocks Bridge, New Jersey 08038

April 27, 1997 - June 21, 1997

C. S. Marschall, Senior Resident Inspector

J. G. Schoppy, Resident Inspector

R. K. Lorson, Resident Inspector

T. H. Fish, Operations Engineer

P. H. Bissett, Senior Operations Engineer

E. H. Gray, Project Manager

L. A. Peluso, Radiation Physicist

J. D. Noggle, Senior Radiation Specialist

James C. Linville, Chief, Projects Branch 3

Division of Reactor Projects

9707110369 970701

PDR

ADOCK 05000272

G

PDR

EXECUTIVE SUMMARY

Salem Nuclear Generating Station

NRC Inspection Report 50-272/97-12, 50-311 /97-12

This integrated inspection included aspects of licensee operations, engineering,

maintenance, and plant support. The report covers an 8-week period of resident

inspection; in addition, it includes the results of announced inspections by regional health

physics and engineering inspectors.

Operations

The inspectors observed good operator performance during routine plant evolutions and

during response to several emergent equipment problems (Section 01 . 1 l.

The Operations Technical Support Superintendent effectively eliminated operator reliance

on Technical Specification interpretations. The operations staff placed needed operator

guidance in plant operating procedures. In a few cases, however, the staff did not

thoroughly review resultant procedure revisions to ensure strict Technical Specification

compliance, alignment with the design basis, and clear operator guidance. The staff

initiated appropriate action to correct these procedure weaknesses (Section 01.3).

Operators did not comply with station procedures requiring operators to update Tagging

Request and Inquiry System (TRIS). Operators did not meet operations management's

expectations in conducting TRIS reviews. The operating shift failed to take adequate

action to document the deficient conditions to prevent recurrence. Operations

management, when presented the aggregate problem, initiated corrective actions to

address operator weaknesses in this area (Section 02.1 ).

Plant personnel maintained the *unit 2 containment in very good condition and ready to

support the plant mode change to Mode 4 (Section 02.2).

Station personnel were using the corrective action system to identify and report quality

issues. The inspectors identified a few minor performance issues where condition reports

were not self-initiated indicating a need for continued focus in this area (Section 07.2).

Maintenance

A reactor operator used a good questioning attitude to identify degraded auxiliary

feedwater alternate supply piping. Maintenance and operations supervision, however,

failed to ensure prompt and appropriate corrective actions (Section M2.1 ).

Two inspectors reviewed Salem's implementation of the maintenance rule during May 27 -

June 3, 1997. The inspectors concluded that Salem's implementation of the maintenance

rule involving scoping and performance criteria was acceptable. Inspectors concluded that

Salem staff completed significant efforts in these areas, and that problems similar to those

identified at the Hope -Creek station did not exist at the Salem plant (Section M3. 1 ) .

ii

Engineering

System managers were actively involved in the resolution of several emergent equipment

problems (Section E2.1 ).

For the construction and engineering aspects of the SGRP, the inspections found a

generally high level of project performance in the areas inspected and identified no safety

significant project deficiencies. The planning for and initial steps of the turnover to the

plant were in progress (Section E2.2).

The licensee implemented adequate corrective actions to support Unit 2 restart in response

to the concerns regarding operation of the emergency core cooling systems(ECCS)

identified in NRC Inspection Report 50-272&311 /97-07 (Section E8.1 ).

Plant Support

Based on the direct observations, discussions with personnel, and examination of

procedures and records for calibration of equipment, the inspector determined that, overall,

the licensee effectively maintained and calibrated the meteorological monitoring

instrumentation. The data were available as required and were easily accessed from

several locations, including the control room and the EOF as specified in the UFSAR. The

licensee's actions to complete a DCP were not timely, and require further review. (Section

R1 .1)

The licensee implemented adequate measures to monitor the areas affected by the cable

tray fire wrap concerns documented in NRC Inspection Report 97-09 (Section F1 .1 ).

The solid radwaste program oversight was good for off site shipment review,

however, some improvements are needed for providing QA audits of radwaste

processing vendors.

The solid radwaste/transportation procedures generally met the new DOT

requirements, however, one violation was identified in shipping paper

documentation of contaminated laundry shipments. Some improvements are

needed in the Process Control Program and implementing procedures to ensure that

essential solid radwaste processing parameters and criteria that are contained in

federal, state and burial license requirements are captured and properly referenced.

Retired solid radwaste processing equipment was verified to be drained, isolated,

and in proper long-term laidup condition. Low solid radwaste volume generation

and efficient shipping efforts at Salem have resulted in no onsite storage of solid

radwaste .

iii

TABLE OF CONTENTS

EXECUTIVE SUMMARY ............................................. ii

TABLE OF CONTENTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . iv

I. Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

1

II. Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

8

Ill. Engineering ........ * . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

12

IV. Plant Support . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .. . . .

17

V. Management Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

25

iv

Report Details

Summary of Plant Status

Unit 1 remained defueled for the duration of the inspection period.

Unit 2 began the period in Mode 5, Cold Shutdown. On June 15, operators increased

average coolant temperature above 200°F and entered Mode 4, Hot Shutdown. Operators

maintained Unit 2 in Mode 4 for the remainder of the period.

I. Operations

01

Conduct of Operations

01 . 1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations. In general, the conduct of operations was professional

and safety-conscious; specific events and noteworthy observations are detailed in

the sections .below.

01.2 Routine Operator and Plant Performance Observations (71707)

The inspectors observed good control room operator performance during normal

plant evolutions including a plant depressuriz*ation and recovery to support a battery

bus maintenance outage, containment fan cooler unit modification testing, and

routine surveillance testing. The control room operators demonstrated good

procedure adherence, communications, and plant control during these evolutions.

The control room operators responded properly to plant alarms and equipment

problems including a safeguards equipment cabinet test circuit lock-up, a pressurizer

relief stop valve failure, and an overheated 1 B EOG field flash circuit. In each case,

the operators made conservative operability determinations and initiated prompt

actions to address the equipment problems.

The plant material condition and housekeeping conditions were good. The

inspectors identified some minor material deficiencies such as a missing service

water system valve handwheel, and a watertight door blocked open by a temporary

electrical cable. The operations staff responded promptly to correct the identified

concerns.

01.3 Technical Specification lnteroretations

a.

Inspection Scope (71707)

The operations staff previously established technical specification (TS)

interpretations to aid operators in understanding TS requirements. Such TS

interpretations risked changing the wording, meaning, or intent of a TS requirement.

2

The inspector reviewed the remaining Unit 2 TS interpretation and TS-related

procedure revisions to ensure guidance did not conflict with TS requirements.

b.

Observations and Findings

The Operations Technical Support Superintendent eliminated 16 of 17 TS

interpretations. The licensee retained a TS 3.8.2.1 interpretation to provide

operator guidance concerning the "D" vital instrument bus (VIB) inverter. The TS 3.8.2.1 interpretation provides more restrictive operating guidance for the "D" VIB

than imposed by TS 3.8.2.1. Licensing initiated a License Change Request (LCR

95-18) to permanently incorporate "D" VIB guidance into TS 3.8.2.1.

The technical support staff eliminated the 16 TS interpretations through license

change requests, procedure revisions, and deletions. The inspector identified that

three resultant procedure revisions contained guidance that conflicted with TS

requirements, did not align with design basis requirements, and did not provide clear

operator guidance. In each case, the operations staff initiated procedure revisions

to correct procedure weaknesses~

The inspector noted that S2.0P-ST.MS-0002,Revision 7, lnservice Testing Main

Steam and Main Feedwater Valves, step 5. 7.5.D did not require operators to.

comply with TS 3.3.2.1 action 20 if any two inoperable MS169 or MS171 valves

(MSIV vent valves) were associated with the same MSIV. Action 20 allows 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />

to restore a channel (MSIV vent valve) prior to requiring a shutdown to mode 4. In

the case of two inoperable vent valves on one MSIV, step 5.7.5.E directs operators

to TS 3. 7. 1 . 5, which allows continued operation in mode 2 if operators shut the

associated MSIV. The inspector noted that in this case shutting the applicable

MSIV completes the MSIV safety function, however, does not comply with TS 3.3.2. 1 requirements. The Shift Technical .Advisor (STA) initiated CR 970424309

to affect a procedure change to correct this discrepancy. The inspector determined

that the failure to ensure TS 3.3.2.1 compliance constitutes a violation of minor

significance and is being treated as a- non-cited violation, consistent with Section IV

o_f the NRC Enforcement Policy. (NCV 50-272&311/97-12-03)

Operating Procedure, Revision 7, Service Water System Operation, Attachment 2

Section 6.0 allowed operators to consider both containment spray (CS) pumps

operable with one CS room cooler inoperable provided service water (SW)

temperature ~ 79~6 °F. Section 9.2.1.2 of the FSAR states that the SW pumping

requirements are based on a maximum river temperature of 90 °F. The total

capacity of the room coolers in a given area, in conjunction with the exhaust air

flow rate, is designed to limit the area temperature to the design values. The

operations staff used engineering calculation S-C-ABV-NDC-0750 to support

operation of the CS pumps with one inoperable CS room cooler, however, the

inspector concluded that procedure S2.0P-SO-SW-0005 permitted operability of the

CS pumps under service water operating conditions less conservative than

described in the FSAR. The Operations Technical Support Superintendent viewed

the guidance as conditional operability and initiated a procedure revision to require

appropriate TS 3.6.2.1 entry given an inoperable CS room cooler.

3

Operating procedure S2.0P-SO.SW-0001, Revision 7, Service Water Pump

Operation, Attachment 1 Section 4.0 provided guidance to operators concerning

manual operation of SW traveling screens and strainers to ensure sufficient diesel

load margin. The procedure provided ambiguous guidance and had the potential to

adversely affect diesel load margin. The operations staff initiated a procedure

revision to improve the procedure.

c.

Conclusion

The Operations Technical Support Superintendent effectively eliminated operator

reliance on TS interpretations. Operations staff placed needed operator guidance in

plant operating procedures. In a few cases, however, the staff did not thoroughly .

review resultant procedure revisions to ensure strict TS compliance, design basis

alignment, and clear operator guidance. The staff initiated appropriate action to

correct these procedure weaknesses.

02-

Operational Status of Facilities and Equipment

02.1

Configuration Control Deficiencies

a.

Inspection Scope (71707)

Salem operators use, update, and audit a Tagging Request and Inquiry System

(TRIS) database to assist in the establishment and maintenance of configuration

control. Operators use TRIS for information on normal valve lineup, current

position, and tagging status. The inspector reviewed TRIS "off-normal and off-

normal tagged" reports and evaluated operator's ability to maintain the TRIS

database to ensure adequate configuration control.

b.

Observations and Findings

The inspector noted the following TRIS discrepancies:

Breaker 2BDC1 AX22, "B7G (Reg) and A7G (Erner) 125 VDC distribution

panel"

Actual Position: open

TRIS Position: closed

Breaker 2CY1AX10Y-1, "2A2 125 VDC Batt. Chg"

Actual Position: open

TRIS Position: closed

Valves PS48, PS49, PS52, PS53 (pressurizer spray valves used for RCS

vacuum fill)

Actual Position: closed

TRIS Position: open

Breaker 2BDC1AX15 (Unit 2 backup power supply to Unit 1 circulating water

460Vl

Actual Position: open

TRIS Position: closed

4

Blank flange 21 PAEXFN-BLK, "Penetration Area Exhaust Fan Suction"

Actual Position: flange removed

TRIS Position: flange installed

Valve 2CS14, "Containment Spray Additive Tank Isolation Valve"

Actual Position: closed

TRIS Position: open

Valves 21SW23,22SW23, "SW Header Cross Connect Valves"

Actual Position: closed

TRIS Position: open

Valve 21 SW593 "21 SW Accumulator Header Isolation Valve"

Actual Position: open

TRIS Position: closed

Desired position: closed

Valves 21 SW465, 21SW468,22SW465, 22SW468, 22SW464, 22SW472,

2SW932,2SW931,22SW413,22SW414

Actual Position: off-normal

TRIS Position: normal

On May 9, inspectors presented the initial seven observations to operations

management. On May 13, operations staff initiated CR 970513226 to document

the TRIS discrepancies.

In the above cases, operators did not follow guidance provided in section 5.4.7 of

SC.OP-AP.ZZ-0103, revision 5, TRIS Configuration Control to update TRIS. In

addition, Unit 2 control room operators did not discover these discrepancies even

though section 5.14.2 of S2.0P-DL.ZZ-0014, revision 6, Shift Routines, requires

operators to review the TRIS off-normal report once per shift. Following inspector

identification, operators promptly updated TRIS, however, in each case operators

failed to document the deficiencies via the Action Request (AR) process to ensure

corrective action to prevent recurrence. Inspectors previously noted TRIS

performance problems in NRC Inspection Report 50-272&311 /96-0Sand Inspection

Report 50-272&311 /96-15. Failure to identify and take prompt and appropriate

actions to correct conditions adverse to quality is a violation of 10 CFR 50,

~ppendix B, Criterion XVI. (VIO 50-272&311/97-12-02)

The inspector noted that the configuration control deficiencies resulted in no safety

consequence. In one case (21 SW593) operators actually lost configuration control.

Maintaining valve 21 SW593 closed ensured isolation between modified SW

accumulator piping and an operating SW header. On May 11, operators performed

a temporary release on 21 SW593 with guidance to maintain the valve closed except

as needed to fill no. 21 SW accumulator. On May 13, the inspector found valve

21 SW593_open with no accumulator fill in progress. The operating shift did not

know the status of 21 SW593. (Operators had left the valve open after filling no.

21 accumulator on May 11 .) Inspectors concluded that leaving the valve open had

no immediate safety consequence for the existing plant conditions. In the remaining

cases, operators appropriately positioned components per approved procedures,

although TRIS status did not reflect correct position .

5

c.

Conclusions

Operators failed to comply with station procedures requiring operators to update

TRIS. Operators did not meet operations management's expectations in* conducting

TRIS reviews. The operating shift failed to take adequate action to document the

deficient conditions to prevent recurrence. Operations management, when

presented the aggregate problem, initiated corrective actions to address operator

weaknesses in this area.

02.2 Unit 2 Containment Closeout Inspection (71707)

The inspectors toured the Unit 2 containment prior to the plant mode change to

Mode 4. The tour involved approximately 10 inspector-hours of effort and included

the pressurizer, annulus, reactor sump area, reactor cavity, and inside the biological

shield. The inspectors identified a small number of minor housekeeping and material

deficiencies. The Director - Salem Operations initiated prompt actions to address

the deficiencies. The inspectors concluded, based on the extent of the tour and the

limited number of findings that plant personnel maintained the containment in very

good condition and ready to support the plant heat up.

07

Quality Assurance in Operations

07. 1 Commitment Management. NRC Restart Item Ill. 14 (Closed)

In NRC Inspection Report 50-272/97-03, 50-311197-03, the inspectors kept NRC

Restart Item 111.14 open pending licensee completion of improvements to the

commitment management procedures.

The NRC has reviewed the following procedures as they apply to commitment

management:

Commitment Management, NC.NA-AP.ZZ-0030(0) - Rev. 2

Licensing Department Commitment Management Program, NC.LR-AP.ZZ-

0030(0) - Rev. 0

Nuclear Licensing and Reporting, NC.NA-AP.ZZ-0035(0)- Rev. 7

Action Tracking Program, NC.NA-AP.ZZ-0057(0) - Rev. 4

The review of the above procedures indicates that responsibility for commitment

tracking is assigned within the licensee's organization, that the licensee has

established requirements that commitments will be properly tracked from

establishment to completion of any modifications, and that commitments can be

reevaluated and changed in an orderly fashion with appropriate documentation.

Based upon the above, Commitment Management, NRC Restart Item 111.14, is

closed.

6

07.2 Corrective Action Program Review

a.

Inspection Scope (71707)

The inspector compared the plant activities to the initiated condition reports (CRs)

to determine whether the plant staff was appropriately identifying and entering

potential quality issues into the corrective action system.

b.

Observations and Findings

The plant staff generated approximately 550 condition reports (CRs) over a one

month period indicating a low threshold for use of the corrective action program.

The plant staff primarily identified significance level three (low significance) issues.

The inspector reviewed the condition report summary list and noted that the CRs

covered a wide range of plant activities.

The inspector identified that in a few minor programmatic or human performance

issues wherein the plant staff did not initiate a CR including:

The operator secured the 1 8 EOG during a post-maintenance test run on May

31 upon receipt of a "pre-lube pump failure" alarm and a low lubricating oil

header pressure indication. The field supervisor investigated and attributed

the apparent EOG oil pressure problem to an isolated lubricating oil pressure

gage. The gage had been isolated during the EOG maintenance outage and

the operator should have unisolated and vented the gage during the test run.

The inspectors determined that the operators did not maintain good

configuration control of the gage.

The Unit 2 control room operator attempted unsuccessfully to reset the "A"

train of the control area ventilation system during modification testing on

May 17. The train did not reset since its electrical supply breaker had been

blocked open for a maintenance activity. The operator's attempt to reset the

~rain while it was blocked demonstrated a weakness in the control of plant

equipment.

The inspector's identified several examples noted where the actual position

of a plant component differed from the position documented in the Tagging

Request and Inquiry System (TRIS). The shift operations staff corrected the

individual deficiencies but did not initiate a CR as discussed in Section 02.1.

The inspectors discussed the above findings with the Operations Manager and the

Corrective Actions Program Supervisor to ensure a proper review of the issues.

c.

Conclusions

Inspectors concluded that station personnel routinely used the corrective action

system to identify and report quality issues. For a few performance issues,

inspectors found that plant staff did not initiate condition reports. The inspectors

  • 08

08.1

7

concluded that achieving a low reporting threshold for adverse conditions warranted

continued management focus.

Miscellaneous Operations Issue

(Closed) LER 50-272/96-026: inadequate testing of residual heat removal (RHR) hot

leg flow path. On October 2, 1996 the Salem staff identified inadequate full flow

testing through the RH27 check valves in the RHR hot leg injection lines. The RH27

valves are in two parallel lines that are fed from a common header. The check

valves full-stroke testing was performed by measuring flow in the common header.

Position 1 of NRC Generic Letter 89-04 states that knowledge of only the total flow

through multiple parallel lines does not provide verification of flow rates through the

individual valves and is not a valid full-stroke exercise." The Salem staff found that

they disassembled the valves on a 36 month frequency to satisfy recommendations

in INPO SOER 86-03. Although the surveillance procedure contained an inadequate

test method, the disassembly and the full flow testing provides confidence that the

check valves remained functional and the safety consequences and implications

were minor. Forward flow testing was satisfactorily performed for the Unit 2 RH27

check valves on October 24, 1996 using a temporary change to the test procedure.

A revision request was initiated to permanently revise the test procedure.

Since the NRC has taken significant enforcement actions for Salem's performance

problems, and since PSE&G voluntarily maintained both Salem units shut down to

address equipment and personnel performance deficiencies, the NRC will not take

additional enforcement action in this case. In particular, Salem management took

extensive measures to correct IST program deficiencies as part of NRC restart issue

11-16, NRC & QA identified numerous IST program deficiencies. This item is closed.

08.2 (Closed) LER 50-311 /94-015:waste gas holdup tank not sampled in accordance

with Technical Specification 3.3.3.9. During testing activities, the Gas Analyzer

Sample Isolation Valve was placed in the closed "off normal " position. On 9/27 /94

a.nd 10/1 /94, the associated Waste Gas Decay Tank was placed in service with the

sample isolation valve still in the closed position and sampling was not performed as

required.

The cause was attributed to personnel error with regard to inadequate review of the

tagging list. Since the NRC has taken significant enforcement actions for Salem's

performance problems, and since PSE&G voluntarily maintained both Salem units

shut down to address equipment and personnel performance deficiencies, the NRC

will not take additional enforcement action in this case. In particular, Salem

management took extensive measures to enhance the tagging program as part of

NRC Restart Issue 111-12, Tagging. This item is closed.


8

II. Maintenance

M 1

Conduct of Maintenance

M 1 . 1 General Comments

a.

Inspection Scope (62707)

b .

The inspectors observed all or portions of the following work:

  • * * *

970321239:

970513280:

970320074:

980407016:

950731104:

pressurizer heater bus cable modification

no. 26 SW strainer repairs

no. 21 reactor shield vent fan installation

no. 2 reactor protection system safeguards emergency

cabinet vital bus 28 panel relay and time response

testing

condenser outlet flange leak repair

The inspectors observed that the plant staff performed the maintenance effectively

within the requirements of the station maintenance program.

Inspection Scope (61726)

The inspectors observed all or portions of .the following surveillances:

S2.0P-ST.ZZ-0003:

S2.0P-ST.PZR-0002:

S2.0P-ST.DG-0001:

S2.0P-ST.DG-0005:

S2.RE-ST.ZZ-0002, rev.9:

SC.OP-ST.CAV-0001:

SC.OP-ST .CAV-0002:

SC.OP-ST.CAV-0003:

S2.0P-ST.RC-0008:

S2.0P-ST.CS-0001:

inservice testing miscellaneous valves,

inservice testing PORV and PORV block valves*

modes 1-6,

2A diesel generator surveillance test,

diesel generator auxiliary no. 22 fuel oil transfer

system operability test,

shutdown margin calculation,

plant systems control room ventilation,

control room emergency air conditioning system,

control room emergency air conditioning system

manual operation,

reactor coolant system water inventory balance,

and

inservice testing - 21 containment spray pump.

The inspectors observed that plant staff did the surveillances safely, effectively

demonstrating operability of the associated system.

9

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1 Auxiliary Feedwater Alternate Su.pply Piping Corroded

a.

Inspection Scope (71707)

The inspector toured accessible plant areas and evaluated the licensee's

performance in identifying, tracking, and correcting deficiencies.

b.

Observations and Findings

On January 23, 1997, a reactor operator identified corroded auxiliary feedwater

(AFW) piping upstream and downstream of 1 AF71 and 1 AF72 (AR 970123203).

These valves are check valves in the emergency backup water supply piping from

the demineralized water storage tanks and fire protection storage tanks,

respectively. The reactor operator recommended that engineering perform an

ultrasonic (UT) pipe wall thickness test. On March 12, inservice inspection (ISi)

engineers performed an UT on 1 AF71 and maintenance supervisors closed work

order 970123203 on April 13.

On May 16, *1997, the inspector identified the following deficiencies associated

with this activity to the Operations Superintendent:

Following work completion, maintenance technicians failed to remove the

associated equipment malfunction information system tag (EMIS 47569) as

required by work standards.

Technicians closed the work order with no UT inspection of the 1 AF72

piping.

The technicians closed the work order even though the 1 AF71 UT inspection

identified a thickness reading less than the nominal wall thickness. This

required an engineering evaluation.

The STA closed a TS 3.7.1.3 tracking item (97-040T) on the degraded AFW

piping based on the closed work order.

The Operations Superintendent initiated actions to address the above deficiencies

(AR 970604181 ). Technical Specifications did not require operable AFW piping

during the time frame in question. On June 18, ISi engineers completed a UT

inspection and determined that the AFW piping in question possessed adequate wall

thickness. Failure to take appropriate actions to correct conditions adverse to

quality is another example of violation of 10 CFR 50, Appendix B, Criterion XVI.

(VIO 50-272&311 /97-12-02)

10

c.

Conclusions

A reactor operator used a good questioning attitude to identify degraded auxiliary

feedwater alternate supply piping. Maintenance and operations supervision,

however, failed to ensure prompt and appropriate corrective actions.

M3

Maintenance Procedures and Documentation

M3.1 Maintenance Rule Overview

a.

Inspection Scope

b.

The inspectors reviewed parts of Salem's maintenance rule program to determine

whether deficiencies previously identified at the Hope Creek Generating Station also

existed at the Salem facility.

Observations and Findings

The inspectors focused their inspection on two areas of the maintenance rule

program that were the subject of apparent violations (action pending) at Hope Creek

(NRC Inspection Report 50-354/97-80). These areas were 1) failure to establish

adequate performance criteria for monitoring the effectiveness of preventive

maintenance on several systems; and 2) failure to include appropriate SSCs within

the scope of the rule.

The Hope Creek report documented ten examples of safety significant and standby

systems that did not have performance criteria established (e.g., reactor protection,

control rod drive, control air, and remote shutdown). In some cases, the systems

had reliability performance criteria, but did not have unavailability performance

criteria; in other cases, systems did not have performance criteria established at the

system/train level. The inspectors reviewed the analogous systems at the Salem

plant and determined that the Salem staff had established appropriate performance

c_riteria. The inspectors also reviewed a large sample of the remaining safety and

standby systems and noted they all had performance criteria. There was however,

one instance in which the inspectors identified one system not having designated

unavailability performance criteria. Reliability performance criteria for the reactor

controls and protection system had been established, but unavailability performance

criteria had not been designated. The Salem maintenance rule manager

subsequently provided to the inspectors appropriate unavailability performance

criteria for this system and also stated that a complete review of the performance

criteria area was scheduled for completion by July 3, 1997. As a result of not

identifying any other omissions of performance criteria, the inspectors considered

this as an isolated instance.

The inspectors also reviewed those SSCs at the Salem plants that were determined

to be "in-scope" and "out-of-scope" in regard to the maintenance rule. A total of

148 SSCs had been identified, of which, 86 were determined to be "in-scope" and

62 were "out-of-scope." The inspectors reviewed documentation that supported

c.

11

the facility's decision to include or not include a SSC under the maintenance rule.

These decisions were adequately documented under station procedure

SE.MR.SA.02 "System Functional Level Maintenance Rule Scoping vs. Risk

Reference." Maintenance rule scoping efforts were outlined in the maintenance rule

scoping document DTG-NSE-030. This document specifically defined the

evaluations needed to be performed by system engineers in determining whether an

SSC fell under the maintenance rule requirements. As specified in the regulations,

each SSC was evaluated against 5 specific criteria, which included the following:

Safety-related SSCs.

Non safety-related SSCs that are relied upon to mitigate accidents or

transients.

Non safety-related SSCs that are used in station emergency operating

procedures and provide a substantial mitigation function.

Non safety-related SSCs whose failure could prevent safety-related SSCs

from fulfilling their safety-related function.

Non safety-related SSCs whose failure could cause a reactor scram or

actuation of a safety-related system.

The inspectors determined that all of the above evaluations, for each function of

each SSC had been adequately evaluated and subsequently documented in

SE.MR.SA.02.

The inspectors also reviewed expert panel meeting minutes which documented final

disposition of an SSC's status in regard to the maintenance rule. The inspectors

determined that the documentation of the various meetings were very detailed and

comprehensive; however, it was noted that several changes to various evaluations

on SSCs maintenance rule functions, as approved during expert panel meetings, had

not been updated in SE.MR.SA.02. These discrepancies were brought to the

attention of the maintenance rule manager, who stated that a complete review of all

meeting minutes would be made to ensure that SE.MR.SA.02 reflected final

approved changes. There were no instances in which the inspector noted a SSC

function was incorrectly designated "out-of-scope" in regards to maintenance rule

applicability.

The inspectors also held discussions with system managers, responsible for several

SSCs, in an effort to assess their knowledge of their responsibilities under the

maintenance rule.

The inspectors found the system managers to be knowledgeable

of the rule and well informed of their responsibilities as a result of the rule.

I

Conclusions

The inspectors determined that the Salem engineers had established performance

criteria for safety and standby systems and have also appropriately scoped

structures, systems, and components for maintenance rule applicability. The

inspectors concluded that the Salem staff was complying with the maintenance rule

in those areas reviewed and that maintenance rule program issues identified at Hope

Creek in February 1997 did not exist at Salem.

12

MS

Miscellaneous Maintenance Issues

M8.1 (Closed) LER 50-272/96-031: plant in unanalyzed condition due to qualification of

Magnacraft-Struthers Dunn Series 8255 relays. PSE&G became aware bf this

condition when they were notified by the relay supplier that one of two test relays

failed during seismic testing. Investigation determined that the failure resulted from

a design change which inadvertently reduced the latching force.

The corrective action was a redesign of the relay and replacement of all relays at

Salem Units 1 and 2. The inspector reviewed test certification documentation for

the redesigned relays to verify the new design was satisfactory. The inspector also

reviewed documentation and held discussions with the PSE&G staff to verify the

relays have been replaced for Salem Unit 2 and are in the process of being replace

for Unit 1. This LER is closed.

Ill. Engineering

E2

Engineering Support of Facilities and Equipment

E2. 1

System Manager Support For Operating Plant Conditions

The inspector reviewed the system manager support for the resolution of several

emergent plant conditions including: a 2A safeguards equipment cabinet automatic

test circuit lock-up, a failure of the pressurizer stop valve (2PR7) to operate, and an

inadvertent energization of the 1 B emergency diesel generator field flash circuit.

The inspector interviewed the system managers for each problem and determined

that they knew about the equipment problems, and became actively involved in the

troubleshooting and follow-up corrective actions. The inspector concluded that the

system managers provided good support for the resolution of plant equipment

problems.

E2.2 Steam Generator Replacement Project (50001 l

a.

Inspection Scope

Inspections were performed to obtain an overview of current and planned work,

related procedures, documentation, quality inputs and progress of the Salem Unit 1

steam generator replacement project (SGRP).

-Specific areas inspected included observation of the restoration of affected

components including insulation and the condition of SG snubbers including the

hydraulic oil reservoirs. The inspector reviewed the replacement steam generator

report, identification of and plans for testing of SGRP affected components and

systems, the transition of responsibilities from the SGRP team to the respective

systems managers and plant operations, the 10 CFR 50.59 process for the SGRP,

instrumentation reinstallation planning, the selection and controls for bolting

materials, post weld heat treatment of feedwater and main steam piping welds, a

13

sample of completed work control packages, a sample of project nonconformance

reports, differences and similarities between the original Model 51 (OSG) and the .

replacement steam generators Model F (RSG), and the operational plant water

chemistry conditions for the primary and secondary sides of the plant.

The site inspection included observations of conditions and work in and outside the

containment structure.

b.

Observations and Findings

By May 6, 1997, the four replacement steam generators were in place in the Unit 1

containment building with welding of the steam generator nozzles to the reactor

coolant piping, feedwater and main steam piping complete and accepted by

radiographic examination. Post weld heat treatment (PWHT) of the feedwater and

main steam piping welds was complete. Restoration or replacement of items

removed as a part of the SGRP including thermal insulation was continuing. The

installation of instrumentation components was defined in work control packages

but deferred to the plant for completion and testing.

The Replacement Steam Generator Report (77-1258763-00)summarizes the

. differences between the OSGs and replacement Model F (RSG) steam generators

and provides references to more detailed en'gineering analysis. From this report, its

references and discussions with project staff, including the Principal Chemist, there

is a reasonable basis from which to expect an improvement in performance of the

RSGs over that of the OSGs. These factors include the presence of thermally

treated alloy 600 tubes that have been shown to be more resistant to intergranular

stress corrosion (IGSCC) than the mill annealed alloy 600 of the OSGs, type 405

stainless steel support plates to minimize support plate degradation, an

improvement in secondary side water chemistry over that initially used in Unit 1, the

elimination of copper bearing alloys in secondary side heat exchangers including the

main condenser and moisture separator reheaters, and a slight reduction in

operating tube temperature.

The tracking and processing of work control packages was examined. The work

control packages sampled were found to be appropriate for the work tasks and

provisions were in place to check and close out work control packages at the

completion of work. A review of a sample of completed work packages identified

no safety significant problems.

The hydraulic snubbers, the associated hydraulic reservoirs and pipe lines for the

upper supports of the steam generators were observed. The snubbers, hydraulic oil

reservoirs and oil lines were in place although the lines were disconnected from the

snubbers. The snubbers and oil lines examined were properly capped to prevent

fluid loss or intrusion of moisture.

Bolting materials for permanent plant components including manway studs and nuts

were purchased as new safety related material.

'

c.


14

The SGRP inspections found generally good steam generator project performance

and identified no safety significant project deficiencies. Overall, the steam

generator replacement, restoration of affected components and systems (except for

instrumentation) and the related engineering evaluations to establish the extent of

changes resulting from the replacement as a part of the 10 CFR 50.59 process were

effective. The reinstallation and testing of instrumentation was-planned and work

package inputs developed for turnover as tasks to be completed by the plant

outside the SGRP work scope. Actual changes to plant operating and maintenance

procedures, training of plant operators to the specific parameters of the new steam

generators and testing are to be handled by existing processes for design change

packages (DCPs) by the plant organization. Transfer of the replaced steam

generators and related systems to the plant with involvement of the plant system

engineer/managers was in progress.

Conclusions

The replacement project staff properly controlled the SGRP replacement and the

followup work, including instrumentation installation, procedure changes and testing

were appropriately turned over to the plant for completion as part of the operational

readiness process.

ES

Miscellaneous Engineering Issues

E8.1

(Closed) LER 50-272/97-009 and (Closed) NRC Restart Inspection Item 11.44, ECCS

Swapover: This LER discussed the past operation of the ECCS outside of the plant

design basis. These issues had been previously identified and discussed in NRC

Special Inspection Report 50-272 & 311/97-07. Based on the NRC's findings, the

licensee determined that prior to March 1996, Salem operated in a condition that

was outside the design basis of the plant for the following reasons: 1) potential

excessive RHR system flows during the recirculation mode of loss of coolant

accident (LOCA) mitigation, and 2) the inability to ensure the successful completion

of the switchover from the injection to the recirculation mode of LOCA mitigation

without the potential for interruption of the ECCS pump flow since the installation of

the semiautomatic switchover modification in 1989.

The inspectors intended to determine whether the licensee took acceptable

corrective actions to support Salem Unit 2 restart. The licensee identified the

following corrective actions to resolve the concerns identified with ECCS operation

outside of the design basis: (Note: The following items correspond to the numbered

corrective actions in LER 50-272/97-009)

1.

The licensee performed a new NPSH calculation (S-C-RHR-MDC-1711,

Revision 1) that demonstrated adequate available NPSH for the RHR pumps

without reliance on containment air pressure. The inspectors reviewed the

calculation and its associated safety evaluation (SE) (S97-117, Revision 1)

and found them acceptable. The inspector noted a minor error in the

calculation in that engineers did not include two of six pipe elbows in the

Unit 2 line loss input to the NPSH calculation. The licensee initiated a

2.

3.

4.

5.

6.

7.

8 .

15

condition report and determined that despite a small decrease in NPSH, the

RHR pumps would still have adequate NPSH. The inspectors agreed with

this assessment.

To eliminate the potential for exceeding RHR pump flow requirements during

hot leg recirculation, the licensee, in 1994, eliminated the use of the hot leg

flow path through valve RH26 by revising the LOCA EOPs.

The licensee revised the Unit 2 RWST drain-down evaluation to ensure the

operators had sufficient time to complete the manual actions for switchover

-*tram the injection to recirculation mode without interruption of ECCS pump

flow. The inspector reviewed the revised RWST drain down safety

evaluation (S97-165), and UFSAR change notice 97-071, and concluded that

the licensee's evaluation was acceptable. Additionally, the inspector

considered the operator action times specified the evaluation consistent with

the times specified in the proposed corrections submitted to the safety

evaluation report (SER) for TS Amendment 69.

The licensee revised and validated Unit 2 emergency procedure, 2-EOP-

LOCA-3, Revision 21, Transfer to Cold Leg Recirculation, to support the

RWST drain down re-evaluation. The inspector reviewed the revised

emergency procedure and found it acceptable.

The licensee trained all operating crews on the revised 2-EOP-LOCA-3

procedure. The NRC Restart Assessment Team Inspection observed an

operating crew satisfactorily perform the transfer to recirculation evolution

on the plant simulator. The inspector reviewed the 2-EOP-LOCA-3 simulator

training results _and found the measured operating crews critical action times

for various LOCA accident scenarios satisfactory.

The licensee performed a root cause investigation for the safety evaluation

deficiencies identified with this issue, as well as other NRC and self-identified

safety evaluation problems. The licensee documented corrective actions

were in a supplemental package for NRC Restart Issue 111-11, dated May 23,

1997. The NRC determined the licensee's actions were acceptable as

documented in Inspection Report 50-272 & 311 /97-08.

The licensee attributed the failure to report the RHR deficiencies (potential

runout condition) in 1 994 to corrective action programmatic deficiencies. An

improved corrective action program was implemented in July 1995 which

provides guidance for performing a more vigorous initial operability and

reportability assessment. The NRC found the changes to the licensee's

corrective action program acceptable during the review of Salem Restart

Issue 111.10, as documented in NRC IR 50-272& 311/96-08and 96-18.

The licensee took action to address performance issues associated with the

RWST drain down evaluation. Training on the issues discussed in the LER

was given to the appropriate engineering personnel. The inspector reviewed


16

a memorandum from the NSSS/BOP Design Engineering Supervisor

documenting the lessons learned training and found it acceptable.

9.

The licensee established a Salem Engineering Review Team (SERT) to provide

ongoing additional multi-disciplinary review of engineering SEs. The NRC

found the licensee's supplemental corrective actions associated with the

1 OCFR50.59 SE process effective and documented this in NRC IR 50-272 &

311 /97-08.

10.

The licensee attributed the failure to report the deficiencies associated with

the RWST drain down analysis in 1996 to human error (misjudgment).

Specifically, the personnel failed to issue a condition report to document the

deficiencies, and thus did not perform a reportability evaluation. The failure

to initiate a condition report by the engineering staff was previously cited by

'*

the NRC in IR 50-272 & 311 /96-08-04. The corrective actions from this

violation also addressed the failure to initiate a CR associated with the RWST

drain down analysis. This violation was closed in NRC IR 50-272 & 311 /97-

07.

11.

The licensee will review the Unit 1 drain down analysis and re-evaluate Unit

1 NPSH calculation to determine whether any additional corrective actions

are necessary to support the restart of Unit 1 .

12.

The licensee determined that use of the RHR26 hot leg flowpath during a

Mode 4 LOCA was necessary to maintain RHR flowpath redundancy. The

licensee approved these changes under SE S97-158 and UFSAR CN#97-069.

The inspector reviewed these documents and found them acceptable.

13.

The licensee revised the shutdown LOCA procedure S2.0P-AB.LOCA-

0001 (0) to recognize the use of the RH26 flowpath if the safety injection

flowpath is not available. The inspector reviewed this procedure and found it

acceptable.

14.

The licensee reinstated valve RH26 in the IST program for use during a Mode

4 LOCA. This inspector verified that the IST testing included RH26.

15.

The licensee notified the NRC, by letter (LR-N970293 dated May 27, 1997),

of proposed corrections to License Amendment 69 SER. The corrections

included: 1) revising the available switchover operator action times from

"approximately 18 minutes" to "approximately 8.5 minutes", 2) correctly

characterizing fOP actions associated with-the switchover evolution, 3)

clarification of uninterrupted flow to the core, and 4) revision of PSE&G's

commitment on operator omission and commission as it relates to the semi-

automatic switchover design.

16.

The licensee submitted a LCR on April 25, 1997 to clarify TS 3.5.2 regarding

hot leg injection flow paths required for Modes 1 through 3 .

I

17.

17

The licensee obtained a revised RHR pump curve that expands the NPSH

curve to 5500 gpm confirming the extrapolation performed by Westinghouse

was accurate. The inspector reviewed the revised pump curve and

determined that the revised curve supported the previous extrapolated

values.

The inspector considered the licensee's completed corrective actions acceptable to support

Salem Unit 2 restart.

IV. Plant Support

R 1

Radiological Protection and Chemistry (RP&C) Controls

R 1 . 1

Meteorological Monitoring Program (MMP)

a.

Inspection Scope (84750)

b.

)

The MMP was inspected against Sections 2.3.3.2 and 7.7.1.13 of Salem UFSAR

and Sections 2.3.3 and 7. 7 .1.11 of Hope Creek UFSAR. The following activities

were conducted to assess the licensee's ability to implement the program.

Review of calibration procedures, calibration results, and channel check logs;

Review of calibration results of individual sensors;

Discussion of data acquisition and availability of data;

Observation of the material condition of meteorological equipment; and

Reviewed status of the meteorological monitoring facility drawings.

Observations and Findings

The inspector observed the contractor, J. Healy Co., perform the quarterly

calibration of the meteorological monitoring instrumentation. The inspector noted

that the licensee performed the calibrations according to the implementing

procedures. The licensee does not submit the wind speed sensors to a wind tunnel

test. The licensee relies on the contractor's knowledge and experience to ensure

the sensors are performing properly. Every quarter, the contractor performs a visual

check for cup damage and performs shaft alignment tests at the logic board from -

the sensor, zero and span checks are performed, and known signals generated by a

calibrated Fluke digital voltmeter are traced through the loop and the bearings are

replaced semi-annually to assure the low starting speed threshold is met. The

results of this calibration were within the acceptance criteria. The inspector

reviewed calibration data from 1995 to 1997. The calibrations were performed

quarterly, checks were performed monthly, and the results were within the

acceptance criteria as required by the procedure ND.RS-SC.MET-1201 (Q) Rev. 3,

18

Artificial Island Meteorological Monitoring Program Calibration and Maintenance

Procedure.

The inspector reviewed the UFSAR for Salem and Hope Creek and the

meteorological administrative procedure. Hope Creek received approval from the

NRC to transfer the meteorological program requirements from the TS to the Hope

Creek UFSAR on September 25, 1996. Administrative procedure ND.RS-AP.MET-

1201 (Q), Artificial Island Meteorological Monitoring Program Administrative

Procedure, dated July 1995 had not been changed to reflect the transfer. In

response, the licensee initiated actions to update the administrative procedure.

The inspector reviewed the status of thirty one (31) meteorological monitoring

facility drawings and noted that the drawings were in the process of revision. The

31 drawings consisted of electrical, mechanical, piping, and instrument drawings.

The inspector noted that the licensee had not taken action to complete a design

change package (DCP 1AE-1075) relative to making corrections (red-line) to the

drawings since the DCP had been initiated. The DCP had been initiated in 1994 in

response to an action request opened during the 1 993 quality assurance audit. The

1993 audit identified deficiencies in 31 meteorological monitoring facility drawings.

The 1995 quality assurance audit identified, during follow up of corrective actions

relative to the 1993 action request, that DCP 1EA-1075 had not been completed

and that no action had been taken by the responsible department. Another action

request was opened and the auditor received a completion commitment date of

November 15, 1995. The inspector noted, as of May 16, 1997, that DCP 1 EA-

1075 had remained open, the revised drawings were not validated, and were not

considered controlled drawings. The inspector discussed this issue with the auditor

and Technical Services and noted that no action had been taken to complete the

DCP. The licensee representatives stated that they planned to review the drawings

and the current configuration applicable to the drawings to ensure the current

revisions are correct, make further revisions if necessary, and complete the DCP

after the restart of the Salem Unit 2.

The inspector noted that these drawings may not be related to the safety of the

plants, but have been used on at least two occasions to make repairs to the tower

(i.e., a power transmitter relay and an inverter). Notwithstanding, without

controlled drawings in place, potential exists for improper or inadequate repair,

modification, or design change to components and systems that affect the

meteorological monitoring program.

Based on the above findings, the inspector determined that completion of the DCP

was not timely and that this matter represented a weakness in the licensee's ability

to effect timely corrective action for self-identified deficiencies. This matter is

considered an unresolved item pending review of the licensee's process and

procedures for maintaining control of configuration and design relative to this

matter. (URI 50-272197-12-01;50-311197-12-01;AND 50-354197-03-02)

T

,.

c.

19

Conclusions

Based on the direct observations, discussions with personnel, and examination of

procedures and records for calibration of equipment, the inspector .determined that,

overall, the licensee's performance of maintaining and calibrating the meteorological

monitoring instrumentation was very good. The data were available as required and

were easily accessed from several locations, including the control room and the EOF

as specified in the UFSAR. The licensee's actions to complete the DCP were not

timely, and require further review.

R1 .2 * Liguid-To:..Solid Radwaste Processing

a.

Inspection Scope (86750)

b.

c.

Through review of liquid radwaste processing documents, radwaste system

walkdowns, and interviews with licensee staff, the inspector reviewed Salem

Station liquid radwaste processing and resulting solids generation with respect to

requirements.

Observations and Findings

The liquid radwaste processes as described in the UFSAR were verified. At the time

of this inspection, the licensee was completing installation of a tubular ultra filtration

unit (down to 0.01 micron particles). This equipment was designed to reduce the

radioactivity level of liquid discharges from the station. The licensee targeted

equipment startup for July 1997. The inspector questioned the method of sampling

the solid effluent from this new filtration process. The licensee indicated that they

would develop a solid radwaste sampling procedure prior to system startup, The

solids recovered by this reverse osmosis filtration equipment will be added to spent

resins and dewatered. The plant staff did not expect the additional radwaste to

increase the volume of solid radwaste generated at Salem Station, however, the

radioactivity level of the solid radwaste should increase, while returning cleaner

water to the Delaware River. The solid radwaste burial volume for Salem Station for

1996 was 1633 cubic feet, down from 2083 cubic feet in 1995.

Conclusions

The licensee is installing an ultra filtration to improve the quality of liquid effluent

discharges from the station without any expected increase in solid radwaste burial

volumes. This is an excellent radwaste system improvement .

' .

20

R2

Status of RP&C facilities and Equipment

R2.1

Onsite Radwaste Storage

a.

Inspection Scope (86750)

The inspector reviewed the condition and radwaste storage inventory of the low

level radwaste storage facility (LLRWSF).

b.

Observations and Findings

c.

The inspector noted an accumulation of 24, 200 cubic foot resin liners being stored

in the LLRWSF. However, this material came from Hope Creek Station and Salem

Station generated none of the solid radwaste materi~I. The inspector reviewed

records indicating plant staff had performed quarterly surveillances of the resin

liners as specified by procedures. The inspector reviewed a video tape of the latest

LLRWSF vault inspection performed by robot on May 30, 1997. Although the

inspector considered this method of surveillance an excellent approach, it may

require some enhancements. The enhancements may include different placement of

resin liners to allow an access path for the robot to perform complete vault

inspections and adjustment to the camera arm to allow viewing into the drainage

trench located inside the vault area. Review of the robot surveillance indicated no

deterioration of the resin liners stored in the facility .

Conclusions

The inspector noted that the RP technicians properly locked and controlled the

LLRWSF, met required facility surveillances, and the radiation levels associated

with the LLRWSF were well below regulatory requirements.

R2.2

Radwaste Equipment

a.

Inspection Scope (86750)

b.

The inspector reviewed the status of formerly utilized radwaste processing

equipment for safe long-term lay up. This review was made with reference to the

US FAR and interviews with licensee staff. The inspector verified of equipment

status through observations in the plant.

Observations and Findings

The Unit 1 waste evaporator was shutdown in 1983 after approximately one year of

use. Through a site-glass, the inspector verified that this equipment was drained.

The Unit 2 waste evaporator was never connected to the plant liquid waste systems

and never used. The two Unit 1 waste monitor tanks were drained with lower

manways ajar. The two Unit 2 waste monitor tanks were tagged-out and these

tanks were verified to be empty .

21

c.

Conclusions

The inspector verified that all of the laid-up solid radwaste processing equipment

was properly drained and laid-up for long-term storage.

R3

RP&C Procedures and Documentation

R3.1

RadwasteCTransportation Procedures

a.

Inspection Scope (Tl 133)

Due to a major revision of Title 49 CFR 171-178 effective April 1, 1996, a

comprehensive procedure review was conducted at the Salem Nuclear Generating

Station.

b.

Observations and Findings

The inspector reviewed the following procedures:

Salem Process Control Program, Rev. 2

Salem TUF Process System Operating Procedure, SALEM-TUF-01, Rev. 1

Salem TUF Cleaning Procedure, SALEM_TUF-02, Rev. 0

Shipment of Radioactive Materials Excluding Waste for Burial, NC.RP-RW .zz-

0909(0), Rev. 1

Shipment of Radioactive Waste for Burial, NC.RP-RW.ZZ-0906(0), Rev. 1

Shipment and Receipt of Laundry, NC.RP-Tl.ZZ-091 5 (0), Rev. 2

Radioactive Waste Packaging, SC.RP-RW.ZZ-0806(0), Rev. O

Sluicing of Spent Resins to a Shipping Container, SC.RP-RW.ZZ-0807(0), Rev. 0

Radioactive Waste Sampling and Classification, SC.RP-RW.ZZ-0902(0), Rev. 0

Use of the Radwaste Computer Code, SC.RP-RW.ZZ-0903(0), Rev. 1

Doserate to Curie Conversion Calculations, SC.RP-RW.ZZ-0904(0), Rev. 0

Use, Dewatering, and Handling of CNS/ 14-215 or Smaller Liners, SC.RP-RW.ZZ-

0908(0), Rev. 0

Use of the 14-210or 14-215Radioactive Materials Shipping Package, SC.RP-

RW.ZZ-0911 (0), Rev. 1

Laundry Shipment Preparation, SC.RP-RW.ZZ-0913(0); Rev. 0

The Process Control Program did not specify the regulatory and burial license waste

processing parameters and criteria. _Although the implementing radwaste

dewatering procedures provided appropriate methods, these procedures were not

defined as part of the Process Control Program and did not reference the regulations

and burial license requirements that they were designed to meet. Most of the above

procedures were not affected by the revision in the DOT regulations. Procedure

errors were minor and were discussed with the licensee during a detailed inspection

debrief. One exception was procedure NC.RP-Tl.ZZ-0915(0), Rev. 2, "Shipment

and Receipt of Laundry." This procedure did not include the new requirement to

classify LSA shipments as LSA-1, LSA-11, or LSA-111. In addition, dose conversion

factors were poorly documented and referenced.

22

c.

Conclusions

Radwaste transportation procedures were generally adequate, and revised DOT

regulations were effectively represented. The Process Control Program and

implementing procedures should be enhanced to ensure waste form processing

parameters are consistently and properly controlled.

R4

Staff Knowledge and Performance in RP&C

R4. 1

Radwaste Sampling and Characterization

b.

Observations and Findings

The inspector verified that the transport characterization tables (A 1 /A2 values) had

been updated to reflect current regulations.

Four solid radioactive waste streams (CVCS resin, radwaste resin, filters, and dry

active waste) were properly sampled and subsequently characterized by an outside

radiochemical laboratory between September 1995 and May 1996. These waste

stream characterizations were appropriately applied to each waste shipment to

account for non-gamma emitting radionuclides, while using direct waste shipment *

sample gamma spectral analyses for reporting radioactivity of the gamma emitters.

c.

Conclusions

R4.2

b.

The waste stream characterizations were timely and appropriately utilized by the

licensee to report radionuclide activities of each radioactive material/waste shipment

during the 1996 - May 1997 timeframe.

Radioactive Material Shipping Documentation Review

Observations and Findings

The inspector reviewed selected radioactive material shipping records since April 1,

1996. The shipping papers were well documented, included an independent QC

inspection review (for all but excepted quantity shipments), and all consignee

licenses and shipping cask certificates of compliance were on file as required. The

inspector noted that all shipment records except contaminated laundry shipment

records were printed using the Radman computer code. These shipping records

were found to be complete and accurate. The contaminated laundry shipping

records were produced manually in-accordance with procedure NC.RP-Tl.ZZ-

0915(0), Rev. 2, and these shipping records, failed to correctly specify the LSA

group specification on any of the laundry shipments since April 1, 1996, as required

by 49CFR172.203(d)(11 ). Examples include: Salem shipment Nos.97-108, 97-103, and 97-101. This is a violation of regulatory requirements (VIO 50-272&

311/97-12-03). The inspector also noted that the dose conversion factors used to

determine radioactivity content of the laundry shipments were not included in the

ship.ping papers nor was the date of derivation of these conversion factors.

23

c.

Conclusions

The inspector's review of selected radioactive material shipments made during

April 1996-1997 indicated that the shipments met regulatory requirements, except

for the laundry shipments which resulted in a violation.

RS

Staff Training and Qualification in RP&C

R5.1

Radwaste Transportation Training for Shippers and RP Technicians

b.

Observations and Findings

The Salem Station authorized radioactive material shippers, and QA personnel

attended a week-long regulations training course in February of 1995 which fulfilled

regulatory training requirements. In addition, in January 1996, a one day revised

shipping regulations update workshop was well attended by PSE&G RP and QA

personnel. The RP technicians were also provided a radioactive material shipping

training course during continuing RP technician training during the 3rd and 4th

quarters of 1996. Currently, the Services Group is planning for another week-long

regulations training course to be held during the summer of 1997.

c.

Conclusions

The licensee met the training requirements for radioactive material shippers and RP

technicians.

R7

Quality Assurance in RP&C Activities

b.

Observations and Findings

c.

The licensee conducted a radioactive material control audit between July 22, 1996

and August 13, 1996. The audit included shipping activities from both Salem and

Hope Creek Stations, included offsite technical expertise and appeared to be a

thorough program review. However, the audit tailed to identify the inadequacies in

the laundry shipment procedure. The QC organization continues to be active in

independently verifying all radioactive material shipments, except for the excepted

quantity shipments, to ensure regulatory requirements are met.

QA audits of radwaste processing vendors were inconsistently performed with

regard to NRC Bulletin 79-19 which directs licensees to establish and implement a

management controlled audit function of all transfers, packaging and transport

activities.

Conclusions

The licensee's audit program for the radwaste/transportation program was found to

be adequate. The licensee stated that the vendor audit program for this program

area would be reevaluated and modified as required.

1

. 24

RS

Miscellaneous RP&C Issues

RB.1 * Updated Final Safety Analysis Report (UFSARl

a.

Inspection Scope

The inspector reviewed current Salem Station practices with respect to

Sections 11.2 and 11.5 of the UFSAR.

c.

Conclusions

The UFSAR description of solid radwaste processing was accurate and correctly

reflected current plant operations.

F1

Control of Fire Protection Activities

F1 .1

Fire Barrier Compensatory Measures, NRC Restart Inspection Item 111.1 (Closed)

a.

Inspection Scope

The inspector reviewed the interim compensatory measures implemented in

response to the cable tray fire barrier wrap performance issues discussed in NRC

Inspection Report 50-272&311 /97-09. PSE&G described their compensatory

measures for the cable tray fire barrier wrap performance issues in a letter to the

NRC dated May 19, 1997. The primary compensatory measures consisted of hourly

roving fire watches in the affected areas.

b.

Observations and Findings

The inspector toured the affected areas with the assigned fire watches and

observed that the fire watches appeared knowledgeable regarding their duties, and

also noted that the licensee gave the fire watches written job instructions. The fire

watches toured the areas specified and documented their tours on round sheets.

The inspector reviewed the round sheets and noted that the fire watches satisfied

the one hour tour requirement.

The inspector noted a minor deficiency in that the fire watches could not inspect

the conditions inside the 21 waste holdup tank room due to radiological conditions.

The Loss Prevention Supervisor indicated that additional compensatory measures for

this area including: verification that the room was free of combustible material, and

that the room had operable smoke detection devices. The Loss Prevention

Supervisor implemented an additional measure by installing remote cameras in the

room. The inspector determined the compensatory measures for this room

adequate.

The inspector compared the areas listed on the round sheets to the fire wrapped

cable, conduit, and cable tray inspection locations listed in surveillance procedure,

S2.FP-SV-005, Revision 0. The inspector determined that the round sheets were

adequate to ensure that the proper cable tray locations were inspected.

c

25

c.

Conclusions

The licensee implemented adequate measures to monitor the areas affected by the

cable tray fire wrap concerns documented in NRC Inspection Report 50-

272&311 /97-09. In addition, as documented in NRC Inspection Report 50-

272&311 /97-09, the inspectors concluded that the licensee had completed

adequate corrective actions for alternative post-fire safe shutdown MOVs. Based

on these observations, the inspectors considered the licensee's corrective actions

adequate to support Salem Unit 2 restart.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the

conclusion of the inspection on June 26, 1997. The licensee acknowledged the findings

presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified.

X2

ManaQement Meeting Summary

On May 30, the Honorable Frank Lobiondo, Representative to the U.S Congress from the

second congressional district of New Jersey, toured the Salem facility. Mr. H. Miller,

Regional Administrator accompanied Representative Lobiondo during the visit.

Representative Lobiondo and Mr. Miller met with senior PSE&G management to discuss

Salem Unit 2 preparations for restart.

On June 13, representatives of the GAO toured the Salem facility and met with PSE&G

managers. Mr. J. Linville, Chief, Division of Reactor Projects Branch 3, Region I,

accomp~nied the GAO representatives on their tour.

On June 19, Mr. H. Miller, Regional Administrator, Region I, Mr. J. Zwolinski, Deputy

Director, Division of Reactor Projects-I/II, NRR, Mr. C. Hehl, Director, Division of Reactor

Projects, Region I, and Mr. J. Linville, Chief, Projects Branch 3, DRP, Region I, visited the

Salem site. They toured the facility and held discussions with plant personnel at all levels

to assess Salem Unit 2 readiness for restart. The NRC managers met with senior PSE&G

managers at the conclusion of the visit to provide their observations.

..

~

..

26

INSPECTION PROCEDURES USED

IP 50001:

IP 61726:

Steam Generator Replacement Inspection

Surveillance Observations

IP 62707:

Maintenance Observations

IP 71707:

Plant Operations

IP 84750:

Radioactive Waste Treatment, and Effluent and Environmental Monitoring

Opened

50-272&311/97-12-01

50-272&311 /97-12-02

50-272&311 /97-12-03

50-272&311/97-12-04

Closed

50-272/96-026

50-272/96-031

50-311.94-015

Discussed

50-272/97-009

ITEMS OPENED, CLOSED, AND DISCUSSED

URI

VIO

NCV

VIO

procedures for maintaining control of configuration and

design

configuration control deficiencies 1 0 CFR 50 Appendix

B

minor procedure deficiences

Failure to include current LSA group specification (LSA-

1,11,or Ill) on all laundry shipping papers since April 1,

1996.

LER

inadequate testing of RHR hot leg flow path

LER

plant in unanalyzed condition due to qualification of

Magnacraft-Struthers Dunn Series 8255 relays

LER

waste gas holdup tank not samples in accordance with

TS 3.3.3.9

LER

ECCS outside of the plant design basis

..

.~

.

AFW

AR

BOP

CRs

cs

DOT

DCPs

ECCS

EMIS

ISi

LCR

LLRWSF

LOCA

MMP

MSIV

NRC

Nsss*

PDR

PSE&G

PWHT

RHR

RP

RP&C

SE

SER

SERT

SGRP

SS Cs

STA

SW

TRIS

TS

UFSAR

UT

VIB

27

LIST OF ACRONYMS USED

Auxiliary Feedwater

Action Request

Balance of Plant

Condition Reports

Containment Spray

U.S. Department of Transportation

Design Change Packages

Emergency Core Cooling System

Equipment Malfunction Information System

lnservice Inspection

License Change Request

Low level radioactive waste storage facility

Loss of Coolant Accident

Meteorological Monitoring Program

Main Steam Isolation Valves

Nuclear Regulatory Commission

Nuclear Steam Supply System

Public Document Room

Public Service Electric and Gas

Post Weld Heat Treatment

Residual Heat Removal

Radiation protection

Radiological Protection and Chemistry Controls

Safety Evaluation

Safety Evaluation Report

Salem Engineering Review Team

Steam Generator Replacement Project

Structures, Systems, and Components

Shift Technical Advisor

Service Water

Tagging Request and Inquiry System

Technical Specification

Updated Final Safety Analysis Report

Ultrasonic

Vital Instrument Bus