ML18102A445

From kanterella
Jump to navigation Jump to search
Insp Repts 50-272/96-12 & 50-311/96-12 on 960811-0914. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support
ML18102A445
Person / Time
Site: Salem  PSEG icon.png
Issue date: 10/01/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18102A443 List:
References
50-272-96-12, 50-311-96-12, NUDOCS 9610080266
Download: ML18102A445 (33)


See also: IR 05000272/1996012

Text

Docket Nos:

License Nos:

Report No.

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved by:

U. S. NUCLEAR REGULATORY COMMISSION

50-272, 50-311

DPR-70, DPR-75

REGION I

50-272/96-12, 50-311 /96-12

Public Service Electric and Gas Company

Salem Nuclear Generating Station, Units 1 & 2

P.O. Box 236

Hancocks Bridge, New Jersey 08038

August 11, 1996 - September 14, 1996

C. S. Marschall, Senior Resident Inspector

J. G. Schoppy, Reside,nt Inspector

T. H. Fish, Resident Inspector

J. D. Noggle, Senior Radiation Specialist

J; C. Jang, Senior Radiation Specialist

J .. J. Kottan, Laboratory Specialist

N. T. McNamara, Emergency Preparedness Specialist

J. Laughlin, Emergency Preparedness Specialist

Larry E. Nicholson, Chief, Projects Branch 3

Division of Reactor Projects

9610080266 6~688~72

~DR ADOCK

PDR

EXECUTIVE SUMMARY

Salem Nuclear Generating Station

NRC Inspection Report 50-272/96-12, 50-311/96-12

This integrated inspection included aspects of licensee operations, engineering,

maintenance, and plant support. The report covers a 5-week period of resident inspection;

in addition, it includes the results of announced inspections by regional radiation,

emergency preparedness, and chemistry inspectors.

Operations

During the inspection period, the inspectors found a significant failure of the Salem line

organization to take corrective action. In December 1995, operators filled the refueling

cavity and detensioned the reactor head without insuring that Salem Unit 2 met the

refueling reactivity requirements specified in Technical Specification 3.9.1. An operator

identified the failure after the fact and appropriately initiated a Condition Report. In

response to the report, however, the operations staff inappropriately made a change to the

refueling cavity fill procedure that effectively changed implementation of Technical

Specification 3.9.1 and 4.9.1.1 requirements. The 1 OCFR50.59 applicability review failed

to identify that the procedure change required a Technical Specification change. In

addition, the operations staff failed to identify that procedures used to prepare the reactor

coolant system and refueling cavity for entry into mode 6 (refueling) did not insure that

plant conditions met the more restrictive of the reactivity requirements stated in TS 3.9.1.

The inspectors concluded that the operations and staff acted to serve the outage activities,

rather than insuring safety and quality in refueling activities (Section 03.1 ). The Salem

staff promptly initiated corrective action for minor discrepancies in meeting administrative

requirements for Station Operating Review Committee documentation.

The plant staff had

already implemented corrective action for a self-identified violation (Section 02.1 ).

Although operators caused an unexpected depressurization of a service water header, it

resulted in no safety consequence, since it did not diminish the supply of service water

from the redundant header. The inspectors will assess the results of licensee corrective

actions in the next inspection period (Section 04.1 ).

Maintenance

Inspectors noted several examples of poor maintenance staff performance. They included:

planning service water pump repacking steps out of sequence (Section M4. 1); failure to

properly secure temporary control air fittings (Section M4.2); and swapping high and low

pressure freon sensing lines following a chiller instrument calibration (Section M4.3).

During Emergency Diesel Generator post-maintenance testing, technicians discovered that

the fuel injector test rig did not work properly. The technicians also learned that, since

they did not und*erstand the operation of the test rig, they misinterpreted results obtained

while using it. The technicians subsequently discovered that ineffective foreign material

exclusion caused a minor fuel oil leak from a fuel line. The inspectors concluded that

neither training or procedures insured quality maintenance in these instances (Section

M4.4). Ineffective maintenance practices have become increasingly evident during the

outage. As documented in NRC Inspection Report 50-272&311 /96-08, during this

ii

reporting period Nuclear Business Unit and Salem senior management initiated a major

effort to provide training for all Salem maintenance staff (Section M4.5).

Engineering

Although the quality in engineering activities varied somewhat, inspectors concluded that it

was generally good during the inspection period. The system manager did not inform the

Management Review Committee (MRC) that RHR minimum flow valve 22RH29 continued

to malfunction. As a result, the MRC inappropriately accepted the package for closure

(Section E1 .1 ). The Salem staff developed and implemented a satisfactory corrective

action plan for the Salem Unit 2 PORV problems, and planned to implement the actions for

Unit 1 PO RVs (Section E2.1)

Salem staff completed effective corrective action for the

Unit 2 positive displacement pump (PDP) reliability problems, however, they have not yet

completed action for the Unit 1 PDP pump (Section E2.3). The quality of MRC reviews, an

NRC concern identified in previous inspections, improved significantly during the

inspection period (Section E7. 1).

Plant Support

In general, the plant support organizations effectively supported outage activities.

Chemistry technicians accurately quantified hydrazine, ammonia, and copper in the NRC

standards during an inspection (Section R1 .1 ). Sufficient radiological safety resources

have been planned for the Salem Unit 1 steam generator replacement project. The Salem

staff continued to formulate the radiological safety planning with less than two months

remaining before the project, however, the inspector did not detect any significant planning

deficiencies (Section R3.3). A radiation protection technician did not meet managements

expectations for control of access to the radiologically controlled area.(Section R4.1 ). The

NRC will document the details of an inspection of the emergency preparedness program in

NRC Inspection Report 50-354/96-07.

iii

,\\

TABLE OF CONTENTS

EXECUTIVE SUMMARY ............................................. ii

TABLE OF CONTENTS .............................................. iv

I. Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

1

II. Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

Ill. Engineering

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

12

IV. Plant Support . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

17

V. Management Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 25

iv

Report Details

Summary of Plant Status

Unit 1 and Unit 2 remained defueled for the duration of the inspection period.

I. Operations

01

Conduct of Operations

01 .1

General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations. In general, the conduct of operations was professional

and safety-conscious; specific events and noteworthy observations are detailed in

the sections below.

02

Operational Status of Facilities and Equipment

02.1

Stetion Operations Review Committee (SORC)

a .

Inspection Scope (7*1707)

The inspector reviewed procedures governing the Station Operations Review

Committee (SORC) activities, and reviewed examples of SORC meeting minutes and

the distribution of those minutes.

b.

Observations and Findings

The inspector found that procedure NC.NA-AP.ZZ-0004(0), Revision 6, Statiof!

Operations Review Committee, Step 5.5.3 states:

"If changes to a document are required before a recommendation for approval will

be made, then the recommendation for approval may be granted contingent upon

such changes being incorporated. The specified changes should be entered in the

meeting minutes and a statement made that approval is predicated upon these

changes being made. The SORC Chairman or an assigned designee should verify

that the changes are correct before the document is submitted to the General

Manager."

During his review, the inspector found that required changes for a SORC reviewed

document, Design Change Package (DCP), 2EC-3266, Pkg. 1, Rev. 0, were properly

entered in the SORC meeting minutes # 96-034. However, one of the comments

which required a change to section 3.2 of the DCP's 1 OCFR50.59 evaluation, was

never incorporated. The inspector concluded that the omission did not affect the

results of the 1 OCFR50.59 evaluation. Through review of an additional thirteen

required changes for other SORC-reviewed documents, the inspector found that all

had been properly incorporated.

2

The inspector also found that the SORC procedure, step 5.6.8, states:

"The Secretary should have the minutes copied and submitted to the TOR

[Technical Document Room] for distribution within 30 working days of the SORC

meeting." ,

The inspector learned through discussions with document room personnel that

SORC no longer sends meeting minutes to the TOR. The inspector confirmed that

plant staff distributed SORC minutes directly via E-mail as directed in a memo

initiated by the Salem Project Manager. Although this change was intended as an

improvement to the method of distribution, it is not in compliance with the current

revision of the SORC procedure.

The inspector also learned PSE&G had identified a procedural noncompliance in that

SORC meeting minutes were not being distributed to required recipients within the

30 day requirement. Additional staff has been assigned to reduce the backlog and

the problem is being tracked to closure utilizing the Salem site deficiency tracking

system.

c.

Conclusions

The licensee promptly initiated corrective action for inspector identified violations of

procedure requirements for SORC administration.

Plant staff had already

implemented corrective action for a self-identified violation. These minor examples

of procedural noncompliance will be treated as a Non-Cited Violation, consistent

with Section IV of the NRC Enforcement Policy.

03

Operations Procedures and Documentation

03.1

Refueling Cavity Fill

a.

Inspection Scope (71707)

The inspector reviewed control room narrative logs, operating procedures, and plant

status concerning fill of the Unit 2 refueling canal.

b.

Observations and Findings

On September 11, 1996, Unit 2 operators used S2.0P-SO.SF-0003, Revision 7,

Filling the Refueling Cavity, to commence filling the refueling cavity. The operating

shift demonstr~ted a good questioning attitude. The shift appropriately used the

"on-the-spot change" process to improve the procedure and subsequently stopped

filling the cavity due to a question concerning available instrumentation.

The inspector noted that S2.0P-SO.SF-0003 step 5.1.8 could be strengthened to

provide additional guidance. Step 5.1.8 specifies actions "when desired fuel

transfer canal level is reached," however, the procedure does not specify a desired

level. Two operating shifts interpreted "desired level" differently, resulting in tw-o

3

different approaches to cavity fill. In both cases, the shift operated within

procedure guidance and maintained good control of the evolution. A specified

minimum level minimizes the potential for high airborne activity due to excessive

spill-over (splashing) from the vessel to the canal. A specified maximum level

minimizes potential foreign material exclusion (FME) concerns involved with

overflowing the refueling canal into the reactor vessel. The Senior Nuclear Shift

Supervisor (SNSS) initiated a procedure revision request to improve the procedure.

The inspector noted that operators did not perform an independent verification (IV)

of repositioned valves, required by 'step 5.1.10, in a timely manner. The Nuclear

Shift Supervisor (NSS) acted promptly to ensure IV completion following inspector

reminder.

Technical Specification 3.9.1 requires that Salem maintain the boron concentration

of all filled portions of the reactor coolant system and the refueling canal uniform

and sufficient to ensure thi;it the more restrictive of the following reactivity

conditions is met: (a) either a Keff of .95 or less, or (a) a boron concentration of

greater than or equal to 2000 ppm. Technical Specification (TS) 4.9.1.1 requires

that the more restrictive of the above reactivity conditions be determined prior to

removing or unbolting the reactor vessel head and withdrawal of any full length

control rod in excess of three feet from its fully inserted position. The inspector

identified that on July 22, 1996, operations staff added step 3.6 to procedure

S2.0P-SO.SF-0003. Step 3.6 provided guidance to operators that "filling the

transfer canal in preparation for flooding the refueling cavity does not constitute a

filled portion of the refueling canal and therefore TS surveillance requirement 4.9.1.1 is not applicable." The inspectors determined that the fuel transfer canal

consists of the lower portion of the refueling canal below the level of the reactor

cavity. As described in the Salem UFSAR, section, 9.1 .4.1.4, the refueling canal

encompasses the transfer canal. The inspectors concluded that step 3.6 to

procedure S2.0P-SO.SF-0003 contradicts TS 3.9.1 and the UFSAR. The inspectors

reviewed the 1 OCFR50.59 review associated with the addition of step 3.6 and

determined that the licensee incorrectly concluded that the addition of step 3.6 to

procedure S2.0P-SO.SF-0003 did not require a Technical Specification change.

In addition, the inspectors determined that the operations management changed

procedure SF-0003 in response to a condition that existed in December 1995. On

December 7, 1995, a SNSS questioned whether operators violated TS 3.9.1

because operators failed to ensure that they maintained adequate boron

concentration in the refueling canal prior to entering the refuel mode on December*

6, 1995 (Condition Report 951207066). Salem licensing staff stated that "since

the refueling canal was not filled at the tirne, there was no communication link with

the reactor .coolant system and therefore no potential to affect reactor criticality"

(Memo CR-1955746). Operations management determined that if the refueling canal

is not filled and the vessel head has not been removed, then TS 4. 9. 1 . 1 is not

applicable. In addition, operations' response to CR 95120766 stated "A more

conservative approach would be to require verification that any water in the

refueling canal is greater than 2000 ppm boron prior to head detensioning. An

4

uncontrolled RCS dilution and inadvertent criticality with all rods inserted and the

reactor head studs detensioned could result in a serious accident with severe

consequences" (PIR 951207066).

The inspector determined that operators did, in fact, fail to meet TS 3.9.1

requirements on December 6, 1995. Operators did not ensure that the filled portion

of the refueling canal (eight inches of demineralized water) met the more restrictive

of the TS 3.9.1 reactivity conditions prior to detensioning the reactor head and

entering the refueling mode. In addition, by their failure to take thorough and

effective corrective actions, Salem licensing and operations staff failed to identify

that procedures S2.0P-SO.SF-0003, 2-IOP-7, Revision 10, "Integrated Operating

Procedure Cold Shutdown to Refueling and S2.0P-IO.ZZ-007, Revision 0, Cold

Shutdown to Refueling" did not require operators to meet the more restrictive of the

two reactivity conditions required by TS 3.9.1. Inspectors concluded that

operations management, expected to implement high standards for corrective

action, failed to take appropriate corrective action for a TS violation identified by an

operator. Failure to take action to preclude repetition of a violation of Technical

Specification requirements is a violation of 10 CFR 50, Appendix B, Criterion XVI,

Corrective Action(VIO 50-272 & 311 /96-12-01 ).

c.

Conclusion

By failing to ensure required boron concentration prior to entering the refueling

mode in December 1995, operators failed to meet TS 3.9.1 requirements. In

addition, in July 1996, Salem staff failed to determine, as required by 10 CFR

50.59, that a proposed cavity fill procedure change in contradiction to the UFSAR

and the requirements of TS 3.9.1 required a TS change approved by the NRC. In

addition, the operations staff response to the Condition Report that documented the

failure to meet TS 3.9.1 did not identify and correct conditions adverse to quality.

Specifically, the cavity fill procedures did not insure that boron concentration met

the more restrictive of the TS 3.9.1 reactivity requirements. The inspectors

concluded that the operations staff justified the incorrect operator actions of

December 1995, rather than taking action to prevent the repetition of those actions.

04

Operator Knowledge and Performance

04.1

Service Water Bay Depressurization

a.

Inspection Scope (71707)

The inspector reviewed control room narrative logs and strip chart recordings

following an unexpected operator-induced service water (SW) bay depressurization.

In addition, the inspector conducted a SW system walkdown and interviewed the

operating shift.

b.

5

Observations and Findings

At 3:55 a.m. on September 2, 1996, Unit 2 operators closed 22SW17, SW pump

discharge header crossover valve, in preparation for 21SW17 valve maintenance.

Due to the SW system alignment, closing the 22SW17 resulted in no. 4 SW bay

depressurization. At 4:53 a.m. operators restored no. 4 SW bay pressure and

reopened the 22SW17. Operators cross-connected the SW nuclear headers in the

auxiliary building prior to closing 22SW17 and did not expect to depressurize no. 4

SW bay. Operators did not account for a SW check valve that prevented flow

backward from the auxiliary building to the SW bay. The cross-connect of the SW

nuclear headers in the auxiliary building prevented depressurization of the no. 22

SW nuclear header and resulted in no safety consequence. The Unit 2 senior

reactor operator initiated a condition resolution (CR) report.

c.

Conclusions

The inspector considered this item open pending Operations' completion and NRC

review of corrective a~tions. (IFI 50-272&311 /96-12-02)

07 .1

(Closed) LER 50-272/95-001: both trains of Solid State Protection System (SSPS)

inoperable due to inadequate design. In February 1995 Salem staff learned that

Diablo Canyon identified a possible common mode failure of SSPS wiring near high

energy lines in the non-seismic turbine building .. Although the NRC initially granted

enforcement discretion to allow Salem to make changes at power, the NRC

1

rescinded the enforcement discretion in response to SSPS power supply failures.

The power supply failures resulted from lack of preventive maintenance resulting in

age related component failures.

The licensee attributed the inoperable SSPS to inadequate design and lack of

preventive maintenance. Since the NRC has taken significant enforcement action

for Salem's failure to identify and correct conditions adverse to quality, and since

PSE&G voluntarily maintained both Salem units shut down to address equipment

and enforcement deficiencies, the NRC will not take additional enforcement action

in these cases.

07 .2 (Closed) LER 50-272/95-003: four planned Technical Specification entries to

support correction of Analog Rod Position Indication (ARPI) system drift affecting

rods 2SA 1, 2SA4, and 2SA2.

Salem Unit 1 Technical Specification 3.1.3.2.1

required the ARPI system to provide rod position indication within twelve steps of

the respective rod group demand counter. The Technical Specification did not allow

any Limiting Condition of Operation action time for corrective action. The control

rod indication drift resulted from temperature related instrument drift. Salem staff

subsequently submitted and the NRC approved a Technical Specification change

request to allow short periods to perform instrument adjustments. These licensee-

identified and corrected violations are being treated as Non-Cited Violations,

consistent with Section Vll.B.I of the NRC Enforcement Policy.

6

08

Miscellaneous Operations Issue

08.1

(Closed) LER 50-272/95-025: single failure conditions that could have

compromised the ability of the service water system to complete its safety function

during the recirculation phase; During the Salem system Restart Readiness

Reviews, Problem Reports (PRs) were identified describing conditions which could

have resulted in Service Water System (SW) alignments with the potential for

runout/cavitation. The licensee concluded that the applicable mode of operation

was not clearly defined in plant design basis documents. Further, normal and

emergency operating procedures did not provide adequate operating instructions for

this mode of operation.

PSE&G initiated Performance Improvement Request No. 9510122244 to document

the problem and to identify the corrective action items to resolve the issue. The

inspector has determined that Salem has corrected the procedural deficiencies and

initiated. a design change notice to revise the system Configuration Baseline

Document to clarify the design basis.

The inspectors concluded that the procedural inadequacies constitute a violation of

10 CFR 50, Appendix 8, Criterion V, "Procedures." The inadequate design basis

document constitute a violation of 10 CFR 50, Appendix 8, Criterion Ill, "Design

Control." These licensee-identified and corrected violations are being treated. as

Non-Cited Violations, consistent with Section Vll.8.1 of the NRC Enforcement Policy.

08.2 (Closed) LER 50-272/95-026: main steam safety valves failed lift set test. During

scheduled surveillance testing, it was discovered that nine out of twenty Salem Unit

1 Main Steam Safety Valves (MSSVs) exceeded the allowable lift set pressure

tolerance specified in Technical Specification Table 4. 7-1. The causes of this event

were ring setting adjustments made without post adjustment lift setpoint testing,

and the prior use of test equipment that was inaccurate. PSE&G reviewed the work

history of the Salem Unit 2 MSSVs and determined that although they had

undergone ring settings, setpoints had been corrected as appropriate utilizing

alternate test equipment. PSE&G concluded that the problems identified on the

Salem Unit 1 MSSVs do not exist on the Salem Unit 2 MSSVs.

PSE&G initiated Performance Improvement Request No. 951023245 to document

the problem and to identify the corrective action items to resolve the issue. The

inspector has determined that Salem has discontinued the use of the inaccurate test

equipment and an action item has been identified to revise procedure SC.MD-

ST.MS-0001 (0) to require lift set testing following ring sitting changes. The

inspector verified that work orders have been issued for the removal, testing, and

replacement of the Salem Unit 1 MSSVs. These work orders are in various stages of

completion.

The inspectors concluded that the original procedures were inadequate in that post

maintenance testing was not required following ring setting. This procedural

inadequacy constitutes a violation of 10 CFR 50, Appendix 8, Criterion V,

7

"Procedures." This licensee-identified violation is being treated as a Non-Cited

Violation, consistent with Section Vll.B.1 of the NRG Enforcement Policy.

08.3 (Closed) LER 50-272/95-027: operation of Positive Displacement Pump (PDP) during

a safety injection could have resulted in exceeding 1OCFR100 and GDC ,19 dose

limit criteria. Previous analyses assumed that the PDP tripped after a safety

injection (SI) signal. However, the PDP trips after a safety injection signal only with

a concurrent loss of offsite power. During a LOCA, in the recirculation mode, the

PDP seal leakage can increase the total contaminated leakage to the auxiliary

building.

Additionally, the original dose evaluation was determined to be in error in that it

assumed the Auxiliary Building Ventilation (ABV) system charcoal filter was aligned

to provide filtration during the cold leg recirculation phase of a LOCA. The ABV

system charcoal filter is not automatically aligned.

The cause of this event is-inadequate design basis information. This resulted in the

development and use of inadequate procedures regarding operation of the PDP and

the ABV system.

PSE&G initiated Performance Improvement Request No. 951026244 to document

the problem and to identify the corrective action items to resolve the issue. The

corrective action items include a proposed revision to the Emergency Plant

Implementing Procedures to manually place the Auxiliary Building Ventilation

System charcoal absorber in service following a LOCA, and a proposed modification

to the Auxiliary Building Ventilation System design to provide local manually

operated valves to operate the charcoal absorber outlet dampers in the event of a

control or mechanical failure. Another corrective action is identified to conduct a

compr~hensive review to ensure consistency between design assumptions, plant

configuration, and operations. The inspector confirmed that these activities are

being tracked in the corrective action tracking system. The inspector also verified

that changes have been made to emergency operating procedures 1-EOP-LOCA-3 &

2-EOP-LOCA-3, "Transfer to Cold Leg Recirculation" to require operators to trip the

PDP prior to placing the plant in the recirculation mode.

Although not all corrective action activities are complete, the licensee has

committed to complete 'these items prior to Restart as stated in the LER corrective

action section. The inspector has concluded that the corrective action tracking

system and the documented commitment in the LER provide reasonable assurance

that the activities will be tracked to completion.

The procedural inadequacies constitute a violation of 10 CFR 50, Appendix B,

Criterion V, "Procedures." The inadequate design basis documentation constitute a

violation of 10 CFR 50, Appendix B, Criterion Ill, "Design Control." These licensee-

identified violations are being treated as Non-Cited Violations, consistent with

Section Vll.B.I of the NRC Enforcement Policy.

8

08.4 (Closed) LER 50-272/95-28: lack of effective leakage monitoring program required

by TS 6.8.4.a. The technical specification requires a program to monitor and

reduce leakage from those portions of systems outside containment that could

contain highly radioactive fluids during a postulated accident. PSE&G determined

that although elements of this leakage monitoring program exist, they had not been

controlled as an integrated program which would meet the requirements.

PSE&G initiated Performance Improvement Request No. 950920589 to document

the problem and to identify the corrective action items to resolve the issue. The

inspector has determined that procedure SC.SA-AP.ZZ-0051 (Q), Leakage

Monitoring Program, has been developed and issued. As a result of discussions with

PSE&G personnel, and a brief review of this procedure, the inspector was able to

conclude that it was designed specifically to satisfy the requirements of TS 6.8.4.a.

The inspectors concluded that prior to this event, adequate procedures were not in

place to prescribe activities necessary to meet the requirements of the technical

specifications. This procedural inadequacy constitutes a violation of 10 CFR 50,

Appendix 8, Criterion V, "Procedures." This licensee-identified and corrected

violation is being treated as a Non-Cited Violation, consistent with Section Vll.8.1 of

the NRC Enforcement Policy.

08.5 (Closed) LER 50-272/95-029: GE S8M Control Switch Degradation. During the

Salem Unit 1 outage, a design change for the replacement of mechanical linkages *

on 4KV vital bus breakers was implemented. Post modification testing revealed an

electrical failure of the 1 A vital bus high limit switch. Subsequent inspections by

the licensee revealed subsurface cracking on the cam follower. During additional

investigation, cracks were found on other switches. As a result, all 4KV vital

busses were declared inoperable for Salem Unit 1 and 2.

The licensee's corrective action for this event is to replace all switches in the 4KV

vital busses prior to mode 6 and 4KV group busses prior to mode 2. Additional

corrective action is planned to locate and replace any suspect switches used in

other applications.

The cause of this event was identified as an inadequate design of the component by

the manufacturer. The inspector determined that this event did not constitute a

violation of NRC requirements. This LER is considered closed.

9

II. Maintenance

M 1

Conduct of Maintenance

M 1 . 1 General Comments

a.

Inspection Scope (62707)

The inspectors observed all or portions of the following work activities:

WO 960515214:

WO 960727074:

no. 26 service water pump strainer

troubleshooting

no. 1 C emergency diesel generator engine low

lube oil level alarm troubleshooting

The inspectors observed that the plant staff performed the maintenance effectively

within the requirements of the station maintenance program.

b.

Inspection Scope (61726)

The inspectors observed all or portions of the following surveillance:

S2.0P-ST.RHR.0001:

no. 21 residual heat removal pump performance

test

The inspectors observed that plant staff did the surveillance safely.

M4

Maintenance Staff Knowledge and Performance

M4. 1 Proper Pre-Job Planning

0-n September 2, technicians removed no. 25 SW pump from service and repacked

the pump. On September 3, a maintenance supervisor identified a planning

deficiency. Planning issued a work order (960805200) to repack *no. 25 SW pump

with another work order (960517060) in the system to add a sixth ring of packing

in accordance with the SW pump design change package. After repacking the

pump but prior to installing the sixth packing ring, a Salem worker initiated an

additional work order to repack the pump due to packing leakage. Planners did not

identify that they should have expected the leakage and implemented the work

order to install the sixth packing ring. Instead, they planned to develop another

work order to repack the pump. The maintenance supervisor demonstrated a good

questioning attitude and initiated a condition report (960903102) to document the

problem. The inspector concluded that poor maintenance planning resulted in

increased SW pump outage time .

10

M4.2 Equipment Restoration

On September 5, 1996, the inspector observed an unattended temporary control air

connection blowing air in the Unit 2 turbine building. Technicians believed that they

isolated the connection on September 3, when they last performed work under

work order no. 950110121. The Unit 2 Senior Reactor: Operator (SRO) entered

SH.OP-AP.ZZ-0007, Revision 0, Suspected Tampering. The SRO determined that

no malicious intent existed concerning the control air leakage. Technicians removed

the temporary connection from' the control air source. The. inspector concluded that

technicians' failure to properly secure equipment following maintenance represented

a poor maintenance practice.

M4.3 Configuration Control

On September 8, 1996, Unit 2 operators placed no. 21 chiller in service following

maintenance. Operators stopped the chiller when the chiller condenser relief valve

opened unexpectedly. The relief valve discharged approximately 10 pounds of

Freon to the atmosphere. The work supervisor determined that technicians

inadvertently switched the chiller compressor suction and discharge pressure

sensing lines following instrument calibration. The vendor determined that the high

discharge pressure did not damage _the chiller unit. Maintenance initiated corrective

maintenance (CM 9608096) and an action request (CR 9608096) to address the

performance issues. The inspector determined that maintenance supervisors failed

to ensure proper configuration control following pressure sensing line work. In

addition, unlabeled compressor suction and discharge valves contributed to the

misalignment.

M4.4 Quality of Maintenance

a.

Scope

The inspectors observed portions of the 28 emergency diesel generator (EDG)

engine overhaul and reviewed the controlling procedures to assess procedure

adequacy.

b.

Observations and Findings

On August 18, maintenance technicians completed an eighteen-month overhaul on

the 28 l;DG and performed a post-maintenance test run. During the test, operators

noted four cylinders leaking small amounts of fuel around the injector seats.

Technicians removed the injectors to inspect and perform a pressure test on them.

Although the technicians did not see any defects, all four injectors failed the

pressure test. The staff subsequently removed and tested the remaining fourteen

injectors; twelve failed.

Maintenance personnel investigated the cause of the injector seat leakage and the

failure of 1 6 of 18 injectors during the pressure test. The technicians noted that all

injectors had passed the pressure test prior to installation. Technicians determined

11

that inadequate seating caused the leaking. The technicians also determined that

the injectors failed pressure tests because the test pump leaked. In response, they

added a procedure requirement to perform a blue check of the injector seating

surface and replaced the test pump and associated piping. Technicians retested the

injectors and all but one passed. Personnel replaced the defective injector and,

following satisfactory blue checks, reinstalled all injectors.

On August 22, operators commenced a second post-maintenance run and noted

that no injector seat leakage. Operators did detect, however, a slight fuel oil leak

from the fuel line fitting on top of a fl:Jel pump. Technicians found three small paint

chips on the seat area of the tubing. The subsequent EDG run was satisfactory.

The inspectors reviewed the procedure governing the overhaul, SC.MD-PM.DG-

0019 (Q), Diesel Engine Overhaul, Revision 21 and concluded technicians complied

with the procedure. Based on the problems noted above, however, the inspector

noted several deficiencies. The procedure had no guidance for technicians to

calibrate or check for proper operation of the pressure test pump; it lacked adequate

direction to achieve proper injector nozzle seating; and it lacked requirements for

fuel pump fitting cleanliness. The inspectors noted these deficiencies contributed to

EDG unavailability and also permitted a fuel line fitting to become fouled, a

condition that could lead to a clogged fuel line and therefore adversely affect EDG

performance.

The deficiencies are a violation of the requirements of Technical Specification 6.8.1

for written procedures. The inspectors did not cite the non-compliance, however,

because NRC Inspection Report 50-272 & 311 /96-08 issued a violation for other

examples of procedure deficiencies and Salem staff has not had the opportunity to

respond to this issue.

c.

Conclusions

Although maintenance personnel complied with the EDG overhaul procedure,

deficient procedures combined with poor foreign material exclusion, lack of fit

testing for injector seating, and inadequate training for fuel injector testing

contributed to delayed EDG restoration. Salem staff initiated actions to improve the

procedure and Salem management implemented a maintenance training interv~ntion

intended to address training and workmanship deficiencies.

M4.5 Maintenance Staff Knowledge and Performance Conclusions

During the inspection period, maintenance staff demonstrated several examples of

poor planning, workmanship, training, and procedures. Ineffective maintenance

practices have become increasingly evident during the outage. As documented in

NRC Inspection Report 50-272&311 /96-08, during this reporting period Nuclear

Business Unit and Salem senior management initiated a major effort to provide

training for all Salem maintenance staff.

12

Ill. Engineering

E1

Conduct of Engineering

E1 .1

Reliability of Residual Heat Removal (RHRl Valves, NRC Restart Item 111.30 (Open)

a.

Inspection Scope (37551 l

Inspectors reviewed the basis for closure of this package to determine if Salem staff

had corrected valve reliability problems.

b.

Conclusions

Although the MRC accepted this package for closure, the system manager did not

inform them that 22RH29 did not perform reliably during testing on or about August

15, 1996. The 22RH29 valve malfunctioned again on August 30. The inspectors

concluded that plant staff had not determined and corrected the cause for 22RH29

valve malfunctions. This NRC Restart Item remains open pending resolution of

22RH29 malfunctions.

E2

Engineering Support of Facilities and Equipment

E2.1

Pressure Operated Relief Valve (PORVl Seat Leakage, NRC Restart Issue 11.22

(Closed)

a.

Inspection Scope

An inspection of PORV's by PSE&G in April 1994 revealed degradation of the

internal components. The condition included cracking, significant unexpected wear,

and galling. The inspector reviewed the closure package which was prepared by

Salem staff and reviewed by the Salem Management Review Committee (MRC) on

August 20, 1996. The package included root cause analysis documentation,

laboratory test results, industry reliability data and summary information regarding

two Design Change Packages (DCPs). In addition to the closure package

documents,. the inspector also reviewed the completed work documents for the

valve internal replacement work, engineering and vendor information, and test

documents related to post modification testing.

b.

Observations and Findings

The inspector found that the root cause analysis indicated that degraded conditions

of the PORV internals was primarily due to the selection of materials being utilized.

The inspector found that PSE&G had extensive testing conducted in December

1994, where 5 different valve designs were cycled open and closed 2000 times

each. The valve designs varied in the selection of materials used and differed

slightly in physical configuration.

The inspector noted that PSE&G evaluated the

test results and selected the valve design which exhibited the most favorable test

results as replacement components for the Salem Unit 1 & 2 PORV internals.

13

The inspector reviewed the Design Change Package No. 2EE-0083 for the Unit 2

PORV modification and found the information adequate for the proposed change.

The inspector also reviewed the completed work documentation, Work Order No.

950919133 and Work Order No. 950919136, for the installation of the Unit 2

PORV internals. The inspector found the documentation to be adequate. The

inspector reviewed the applicable design drawings and vendor fabrication records to

verify that the internals which were installed were fabricated of the desired material.

Finally, the inspector confirmed that operability testing will be required prior to the

Restart of the Salem Units.

c.

Conclusions

Based on the review of related documents, the inspector concluded that PSE&G has

developed and* implemented a satisfactory corrective action plan for the Salem Unit

2 PORV wear related problems. Corrective action documentation such as the work

orders and DCPs have been generated for the Salem Unit 1 PORV work and

provides reasonable assurance that the PORV internal wear problem will be

satisfactorily resolved for Unit 1 as well. This item is closed.

E2.2

(Closed) Inspector Follow-up Item 50-311/94-11-01, PORV Operability

This issue pertains to the excessive wear and the cracking of the PORV internals. It

is identified as Item 11.22 of the NRC Restart Action Plan for Salem.

The NRC conducted a review of the licensee's actions to address this issue and

found them acceptable. The details of the NRC review are contained in Section

E2.1 of this Inspection Report. This item is closed.

E2.3

Poor Reliability of the Positive Displacement Pumps, NRC Restart Issue 11.18 -

(Open .-Unit 1 , Closed-Unit 2)

a.

Inspection Scope

The Salem Unit 1 & 2 Positive Displacement Pumps (PDPs) have a history of

maintenance and operating problems. In order to improve operational reliability, a

root cause analysis was performed to identify the cause or causes and to prescribe

corrective action for short and long term implementation. The inspector reviewed

the closure package prepared by Salem staff and had been reviewed by the Salem

Management Review Committee (MRC) on June 21, 1996. The package included

the PSE&G root cause analysis documentation and the recommended corrective

action plans and a root cause analysis conducted for PSE&G by an independent

technical consultant. The inspector also met with the Chemical and Volume Control

System (CVCS) system manager to obtain additional information such as

implementing document numbers for maintenance work orders and design change

packages. The inspector reviewed a sample of these implementing documents to

verify completion of the work.

14

b. Observations and Findings

The root cause analysis included a review of the maintenance history for the period

from January 1, 1987 to April 24, 1995. The analysis concluded that the failures

resulted from numerous failure mechanisms. The 'analysis identified five

primary areas for corrective action as follows:

Packing Failures

Pump Valve Cracking Failures

Pump Valve Seat Cracks

PDP Cylinder Block Cracking Failures

Failure of the Suction Stabilizer

The inspector learned that the most frequent failure mode was packing failure.

Packing failures accounted for 49 PDP failures in approximately nine years. Design

changes, DCP 1 S00402 and DCP 2S00303, were implemented early in 1994 to

change the packing style. The inspector reviewed* the operating data and confirmed

that this has resulted in a significant improvement in continuous running time

between packing failures for Unit 2. Running time has increased to over 2500

hours, an increase of about a factor of two. However, the operating data for Unit 1

indicates that although one 3900 hour0.0451 days <br />1.083 hours <br />0.00645 weeks <br />0.00148 months <br /> run was achieved between packing failures,

two subsequent packing related problems indicate that the problem is not resolved.

The inspector reviewed maintenance procedure SC.MD-CM.CVC-0001 (Q),

"Charging Pump Repacking, Plunger & Valve Repair or Replacement", and verified

that changes had been incorporated per the corrective action plan to aid in ensuring

that packing installation is correct and that the initial run-in was successful.

Numerous corrective action items were identified in the closure package which are

intended to reduce the frequency of problems in the other four areas. These include

the following:

Activity

Plans to change the material used for valve

disks.

Design changes to reduce pump nozzle stress

loading.

Procedure changes to S1 (2).0P-SO.CVC-

0002(0), Charging Pump Operation, to

provides a method for venting the pump

discharge.

Design changes to reduce the failure suction

stabilizers.

Status

Design Change Package

identified, not yet complete.

Complete for Unit 2, not

necessary for Unit 1 .

Complete for both Units.

Complete for Unit 2, work

started for Unit 1 .

15

During a review of work order history for Unit 1 and Unit 2 PDPs, the inspector

found there were numerous work orders incomplete for Unit 1, *including one for an

inspection of the pump internals and one for the inspection of the suction stabilizer.

The inspector also found that the Unit 1 pump discharge valves were replaced early

in January, 1993. Because the system manager had pointed out that these valves

have experienced cracking failures after 2 to 3 years of operation, the inspector

noted that these valves were likely to be near the end of their service life. By

comparison, the Unit 2 pump discharge valves were replaced in April, 1995.

The inspector verified that the PDP will be tested to verify proper operation prior to

core load as part of the Salem Restart Test Plan. In addition, future pump

performance will be monitored and trended to assess whether the corrective action

items have been successful in achieving reliable PDP operation.

c. Conclusions

The inspector considered the root cause analysis comprehensive and the corrective

action plan aggressive. Although the effectiveness of the corrective action plan can

only be determined by monitoring future performance, the inspector concluded that

the PDP reliability issue received satisfactory attention and that for Salem Unit 2,

the corrective action items which are complete provide reasonable assurance that

PDP operating reliability will be improved. Because of the continued packing

problems on Salem Unit 1, and because of the incomplete work orders and the

length of time the discharge valves have been in service, the inspector was not able

to reach the same conclusion for Unit 1 . This technical issue is closed for Unit 2

but will remain open for Unit 1 .

E7

Quality* Assurance in Engineering Activities

E7 .1

Management Review Committee (MRC)

a.

Inspection Scope (37551)

b.

Inspectors assessed MRC review of NRC restart inspection item closure packages,

final system readiness reviews, and system affirmations to determine the

effectiveness of the reviews.

Observations and Findings

Early in the inspection period, the MRC inappropriately approved closure of RH29

valve closure package without determining that the controls for the 22RH29 valve

had recently malfunctioned. Later in the period, the MRC did not approve final

affirmation of the radioactive waste gas system readiness, since the system review

team reviewed an uncontrolled operability determination list instead of reviewing the

controlled Condition Resolution Operability Determinations. The MRC appropriately

concluded that the service water system readiness depended on demonstration of

reliable system performance. As recommended by the System Manager, the MRC

concluded that service water was not ready for the final system readiness review

16

since they had not yet observed reliable service water performance.

Members of

the MRC also deferred approval of the final affirmation of 4KV system readiness,

since they identified that each vital bus did not have at least one spare breaker

cubicle in good working order.

c.

Conclusions

The MRC improved the quality of reviews during the inspection period. They

accomplished the improved performance by insuring that MRC membership

consisted of senior Salem managers and through use of specific closure package

review criteria.

ES

Miscellaneous Engineering Issues

E8.1

RHR Pump Minimum Flow Instruments (37551)

a.

Observations and Findings

Inspectors discovered that the Updated Final Safety Analysis Report (UFSAR),

section 6.3.5.3, Flow Indication, Residual Heat Removal Pump Minimum Flow,

states that a flow indicator is installed in each RHR pump minimum flow line. The

inspectors noted that the RHR pump minimum flow line does not have a flow

indicator. The inspectors discussed the lack of a flow instrument with plant staff

from licensing, system engineering, the operations staff (an SRO), and the Salem

General Manager's staff. The licensing staff and the General Manager's staff

appropriately concluded that procedures required them to initiate an Action Request

(AR). The Salem managers concluded that failure to initiate an AR constituted an

additional condition adverse to quality; they initiated an AR to address it.

Inspectors learned from the SRO that flow indication had previously existed for the

RHR minimum flow line, .but plant staff removed it. The inspectors could not

determine, prior to the end of the inspection period, why Salem staff had not

updated the UFSAR to reflect current RHR configuration. This issue will remain

unresolved pending assessment of licensee compliance with 10 CFR 50.59 and 10

CFR 50.71 (e) (UNR 50-272&311/96-10-03).

b.

Conclusions

When inspectors discovered a minor discrepancy between UFSAR description of

RHR minimum flow line instrumentation and actual plant configuration, only two of

four plant staff recognized this as a condition adverse to quality that required them

to initiate an AR. Plant managers subsequently initiated an AR to address the

failures to initiate an AR. The discrepancy between the UFSAR and RHR

configuration will remain unresolved pending inspector assessment of compliance

with 10 CFR 50.59 and 10 CFR 50.71(e) .

17

IV. Plant Support

R1

Radiological Protection and Chemistry {RP&C) Controls

R1 .1

LWR Water Chemistry Control and Chemical Analysis (79701 l

a.

Inspection Scope

Standard chemical solutions were submitted to the licensee for analysis. The

standards were prepared by the Oak Ridge National Laboratory (ORNL) for the NRC

and were analyzed by the licensee using current routine methods and equipment.

The analysis of standards is used to verify the licensee's capability to monitor

chemical parameters in various plant systems (steam generators in the case of this

inspection) with respect to Technical Specifications and other regulatory

requirements. In addition, the analysis of standards is used to evaluate the

licensee's analytical procedures with respect to accuracy and precision. The

standards were submitted to the licensee for analysis in triplicate at three

concentrations spread over the licensee's normal calibration and analysis range.

However, the ammonia standards were analyzed at five concentrations in order to

duplicate the concentrations normally analyzed by the licensee.

b.

Observation and Findings

The results of the standards measurements comparisons indicated that all of the

measurement results were in agreement or qualified agreement under the criteria

used for comparing results. (See Attachment 1 to Table I.) The data are presented

in Table I. The hydrazine and copper analyses were performed in both the primary

laboratory and the secondary laboratory, while the ammonia analyses were

performed in the secondary laboratory only. The primary laboratory is the

laboratory used to analyze reactor systems samples and the secondary laboratory is

the laboratory used to analyze non-reactor systems samples such as steam

generator samples. During shutdown conditions steam generator samples are taken

in containment, and, therefore, the primary laboratory is sometimes used to analyze

these samples for hydrazine and copper.

c.

Conclusion

R2

The licensee accurately quantified the hydrazine, ammonia, and copper in the NRC

standards. Therefore, the licensee can accurately quantify these analyses in steam

generator samples.

Status of RP&C facilities and Equipment

During this inspection, the inspector conducted tours of the plant during outage

conditions and noted that all required radiological postings and locked areas met

regulatory requirements and that the areas were free of safety hazards.

R3

18

RP&C Procedures and Documentation

During this inspection period, the steam generator replacement project staff (SGRP)

was engaged in a planning preparation phase and a review was made with respect

to the radiological safety plans for the project. The SGRP project is intended to

effect the complete replacement of four steam generators at Salem Unit 1 during

the fall of 1996, utilizing replacement steam generators from the mothballed

Seabrook Unit 2 nuclear power plant.

R3.1

RP & ALARA Planning

a.

Scope (50001)

The inspector reviewed the licensee's planning documents and interviewed

cognizant project staff to determine the adequacy of radiation protection (RP) and

ALARA preparations for conducting the SGRP.

b.

Observations and Findings

The inspector reviewed the licensee's resource commitments and radiological

control plans for the SGRP. The planning documents included incorporation* of

lessons learned from the following SGRPs: Millstone, V.C. Summer, Surrey,

North Anna (1 &2), and Ginna.

\\

At the time of this inspection, the licensee had completed a preliminary exposure

estimate of 164 person-rem. The inspector reviewed the details of the estimate and

determined that no contingency was built into the estimate and that it consisted of

a mixture of detailed project-based estimating and historical information derived

from other SGRPs. As it now exists, this preliminary exposure estimate represents

a challenging exposure standard for the project.

To allow the additional personnel access to the Salem Unit 1 containment, the

SGRP will provide a temporary access facility (T AF) adjacent to the Unit 1 Service

Building to include protective clothing change facilities, RP briefing location, RP

Command Center, and a radiological control area (RCA) access control station.

Additional electronic dosimeters, readers, and electronic turnstiles are planned for

the TAF. In addition, cellular phones will be issued to the work groups to allow for

direct communication with the RP group from the TAF's RP Command Center.

Extensive video camera monitoring of containment work areas is also planned with

three remote monitoring stations located in the RP Command Center.

Mockup training is planned for pipe cutting, beveling, and welding; pipe end

decontamination; and feedwater thermal sleeve modifications. Mockup training and

schedule details were not available for review during this inspection.

At the time of this inspection, approximately 20,000 pounds of temporary lead

blankets were installed in the Unit 1 containment to shield many of the transit paths

and miscellaneous sources. SGRP plans call for an additional 25,000 pounds of

19

lead to be installed around the primary piping, inside severed primary piping, and

around the steam generator platform areas to further reduce working area dose

rates.

The licensee has recently been piloting the use of radiation work permits (RWPs) to

focus on limiting individual RCA entry doses via customized electronic dosimetry

setpoints, and through RP technician dialogue before and after RCA entries with the

workers. This approach is planned to be continued during conduct of the SGRP.

Individual administrative exposure limits have been established at 500 mrem per

year:

The radioactive material control organization has elected to not pursue large-scale

onsite equipment decontamination. The SGRP is considering offsite vendor services

for the decontamination and release of project .equipment and materials.

Work package design included the incorporation of ALARA requirements. Hold

points and records of hold point signoffs were made available to RP/ALARA for use

in the work packages. At the time of this inspection, the work packages had not

been approved and were not available for review.

Detailed RP contingency planning had not been evaluated by the licensee at the

time of this inspection.

For reducing internal exposure hazards, the licensee plans on utilizing eight

2000 cfm HEPA ventilation units for the reactor cooling system (RCS) loop areas.

At the time of this inspection, the licensee had not established a plan for providing

investigational whole body count measurements. Currently-the licensee does not

have the measurement capability onsite, however a memorandum of understanding

exists for providing bioassay services at Brookhaven National Laboratory in

Long Island, New York.

c.

Conclusions

R3.2

a.

The inspector determined that sufficient radiological safety resources have been

planned. The radiological safety planning was ~till being formulated with less than

two months remaining before the project, however, the inspector did not detect any

significant planning deficiencies.

Shipment Classification of Old Steam Generators

Scope (50001)

As of April 1, 1996, the DOT radioactive material shipping regulations were

significantly revised. In particular, a new shipping category of surface contaminated

object (SCO) was defined. The licensee has determined that the four old steam

generators meet the new SCO II definition and can be transported under the new

DOT regulations. The inspector reviewed the licensee's SCO evaluations, DOT

correspondence, and conducted interviews with cogn-izant licensee personnel.

- I

b.

20

Observations and Findings

The licensee determined that the steam generators met the contamination

concentration limits for SCO II through utilizing external dose rate measurements

from the outside of each steam generator and* by taking smear scrapings from the

inside of a steam generator primary manway. The fixed contamination

concentration was determined by computer modeling the steam generator as a

simple cylinder with homogenous air/iron contents and utilizing the highest external

dose reading, and calculating the source radioactivity estimated to produce the

external dose readings. The resultant source activity was divided over the known

surface area of the steam generator tubes and channel heads to determine the

surface contamination concentration. The smear scrapings were analyzed by an

offsite laboratory to determine radionuclide constituents, which were also utilized in

the radioactivity calculations. The licensee determined that the average total

surface contamination for the worst-case steam generator was 3.01 uCi/cm

2 as

compared to the SCO II limit of 20 uCi/cm 2 * The licensee had also determined,

through analysis, that the highest unshielded dose rate at three meters was

410 mrem/hr as compared to the DOT limit of 1000 mrem/hr.

The inspector questioned the accuracy of the computer model method of deriving

the contamination concentration and unshielded dose rate values. In response, the

licensee committed to provide an uncertainty analysis. Also, due to the possibility

of fairly large uncertainty values, the inspector asked if a benchmaking calculation

had been considered utilizing an independent method. The licensee indicated that

there were available steam generator tube samples and that direct measurements

would be made and those survey results would be compared to the computer

calculation results. Future evaluation of this additional information will provide the

basis for evaluating the adequacy of the licensee's classification of the steam

generators as SCO II. The licensee has issued a letter ta the Department of

Transportation (DOT), dated August 5, 1996, providing the preliminary waste

characterization information mentioned above, and an engineering evaluation

concluding* that the steam generators can meet the one-foot drop test as specified

for an Industrial Package 2 package. This letter also requested DOT approval for an

exemption to the packaging requirement of SCOs as specified in 49 CFR

173.427(b)(1 ).

.

c.

Conclusions

While no significant weakness in the licensee's assessment and approach for

handling the eventual shipment of steam generators was detected, additional study

by the licensee and regulatory review of additional characterization remains to

assess the adequacy of the licensee's determination of shipping classification.

21

R3.3

Steam Generator Water Chemistry

a.

Inspection Scope (79701)

The inspectors reviewed the following analytical procedures:

SC.CH-CA.ZZ-0332(Z), Hydrazine by PE Lambda-2 Spectrophotometer,

SC.CH-CA.ZZ-0348(0), Metals by Perkin-Elmer Model 5100 PC Atomic

Absorption Spectrometer, and

SC.CH-Tl.ZZ-0351 (Q), Ion Chromatograph Applications.

b.

Observation and Findings

c.

R4

R4.1

a.

The inspector noted that the above procedures were well written, easy to follow,

and contained sufficient level of detail. The inspector also noted that these

procedures contained QC requirements for verifying analytical results.

Conclusion

Based on the above reviews, the inspector determined that the licensee had very

good analytical procedures to quantify hydrazine, copper, and ammonia in steam

generator water samples.

Staff Knowledge and Performance in RP&C

Radiation Area Access Control

Inspection Scope (71707)

The inspector observed radiologically controlled area access controls and postings.

b.

Observations and Findings

c .

On August 26, 1996, the inspector observed the radwaste truck bay door open, the

associated gate unlocked, and no radiation protection personnel monitoring the

access point. Failure to maintain access point vigilance did not meet radiation

protection managements' expectations for the area. Although the assigned

radiation protection technician lost visual contact of the access point, technicians

had established proper radiation area postings. Radiation protection management

counseled the technician.

Conclusions

A radiation protection technician did not meet managements expectations for

control of access to the radiologically controlled area.

R5

a.

22

Staff Training and Qualification in RP&C

Scope (83750)

Since June 25, 1996, the Salem Radiation Protection Manager (RPM) has been

assigned to a ter:nporary position in the Salem Unit 2 Outage Management group.

The RPM designated the Senior ALARA Supervisor as the acting RPM in his stead.

In addition, the acting RPM has been designated as an alternate RPM member of the

SORC. The inspector reviewed the individual's qualifications for RPM with respect

to regulatory requirements.

b.

Observations and Findings

Salem TS 6.3.1 specifies the RPM qualifications as those contained in Regulatory

Guide 1.8, September 1975. These requirements specify a bachelor's degree in

science or engineering or equivalent, and five years professional experience in

applied radiation protection. The inspector reviewed an RPM qualification evaluation

dated June 26, 1996 that was signed by the current RPM. This evaluation

indicated that a bachelor's degree had not been' completed and indicated that the

individual had accrued nine years of supervisory experience including one year as

the Senior ALARA Supervisor. The inspector noted that the RPM qualification

evaluation form (NC.NA-AP.ZZ-0014-4) required the general manager or a director's

signature when education exemption was granted based on experience. -The

evaluation form was not signed as specified by the procedure. Upon further review

of the individual's resume, it was determined that he acted as an RP Operations

Supervisor and an ALARA Supervisor for a combined period of eight years and that

he has held the position of Senior ALARA Supervisor for the past one year. Based

on the inspector's knowledge of the Salem RP organization, ALARA supervisors are

the technical lead for an RP support area, known at other power plants as lead

technicians. The inspector was not provided enough details of the individual's

activities/duties while acting as a RP Operations and ALARA Supervisor to enable

the inspector to make a specific determination of professional -RP experience. The

need for additional information has resulted in an unresolved item (50-272/96-12-

04), which was communicated by telephone to the station licensing engineer on

August 27, 1996.

The inspector also reviewed the use of RPM duty delegation as applied to SORC

membership. Station procedure (NC.NA-AP.ZZ-0004(0)) indicates that SORC

alternate members should meet the* same qualification requirements as SORC

members. The inspector reviewed a letter dated April 25, 1995 that designated the

subject acting RPM individual as an alternate RPM representative on the SORC.

This letter was supported with a verification of qualification form for RPM dated

April 28, 1995 that referenced ANSI N18.1-1971 as the standard of comparison as

requiring eight years in responsible positions. The subject individual has, since that

time, represented the RPM at SORC meetings.

23

c.

Conclusions

The inspector reviewed two evaluations of an acting RPM individual that determined

the individual to be RPM qualified that were based on two different standards. The

correct standard, Regulatory Guide 1.8, September 1975, was most recently used

with the result that bachelor's degree equivalency was given and a determination

that five years of professional level experience had been met. Station procedure

requirement for General Manager or Director approval was not evidenced. Details of

experience as an RP supervisor require further review in order to verify and validate

the qualifications of the individual.

R6

RP&C Organization and Administration

The inspector reviewed the SGRP staffing plans for the project. The licensee plans

on providing approximately 58 contractor senior RP technicians and 24 contractor

junior/decon RP technicians to provide the additional RP control for the project. The

inspector noted that the licensee intends on utilizing 10 permanent station RP

technicians in lead technician positions and that there will exist an additional pool of

25 contractor RP technicians, assigned to the Unit 2 restart, that may be available if

necessary. The inspector did not note any discrepancy or lack of manpower

associated with the above plans.

R7

Quality Assurance in RP&C Activities

a.

Inspection Scope (79701 l

The laboratory QA/QC programs were reviewed in order to evaluate the licensee's

control with respect to analyzing and evaluating data for the implementation of the

chemical analysis program.

The inspectors reviewed the licensee's Quality Assurance (QA) and Quality Control

(QC) Programs for analytical measurements of chemical parameters in various plant

water samples including, interlaboratory and intralaboratory comparison programs.

The following procedures were reviewed:

b.

Observation and Findings

Salem Chemistry Data Trending Program Roles and

Responsibilities,

Technical Calculation Preparation and Validation,

Salem Chemistry Independent Verification Program

Guidelines,

Laboratory Quality Control Program,

Chemical Shelf Life Program,

Laboratory Quality Control Chart Preparation, and

Laboratory Quality Control Chart Evaluation and

Corrective Actions.

The laboratory maintained internal/external QA/QC programs including: (1 l spike

samples; (2) blind samples; (3) intralaboratory comparisons; (4) instrument and

24

procedures control charts; (5) trending and tracking analyses; and (6) QC Reports.

The inspector also noted that when discrepancies were found, reasons for the

discrepancies were investigated, resolved, and reported in QC Reports. During the

review, the inspector noted that the licensee used actual matrix samples (e.g., SIG

water) for preparing QC spike samples. The inspector stated that this was the best

method to evaluate analytical technique and capability because the analyst could

encounter the chemical interferences present in actual samples.

During a discussion with the Chemistry staff, the inspector noted that the

responsible individuals had very good knowledge in the areas of: ( 1) importance of

QA/QC; (2) plant water systems; (3) potential chemical interference in various

system water samples; and (4) validating of measurement results.

c.

Conclusion

Based on the above reviews and discussions, the inspectors determined that the

licensee had excellent laboratory QA/QC programs.

RS

Miscellaneous RP&C Issues

RB. 1

Other Issues Previously Identified

(Closed) Violation 50-272/96-01-05:

During late 1995, the licensee reported several instances of entering the RCA

without electronic dosimetry monitoring and other related access control procedure

violations. The repetitive nature of these procedure violations resulted in issuance

of a violation against 10 CFR 50 Appendix B, Criteria XVI, failure to provide

effective corrective actions to prevent recurrence.

a.

Scope (83750)

During this inspection, the inspector reviewed the licensee's root cause and

corrective actions associated with the violation as well as verified completion of the

corrective actions.

b.

Observations and Findings

The result of the licensee's investigation determined that there had been 17

recorded instances of RCA access control procedure violations during 1995.

Several root causes were identified that were all associated with human

performance weaknesses. Corrective actions included incorporating two software

changes in the electronic dosimeter reader program that resulted in producing

dosimeter alarms if an electronic dosimeter is removed from the battery charger rack

and is not placed into a reader within three minutes, and in causing the dosimeter to

alarm if the dosimeter is left in the reader for more than four seconds after

completing sign-in to the RCA. Additionally, positive control electronic turnstiles

were installed at the entrance to the RCA and at the exit from the protective

25

clothing change area. To access the station radiological controlled area requires

passage through an electronic gate turnstile. In order to unlock the turnstiles, an

electronic dosimeter must be inserted and if the dosimeter is found to be activated

and functional, the gate is unlocked permitting entry. During this inspection, the

inspector verified that the above changes had been completed.

To alert the workers of this plant access change, a training video will be developed

to be shown to radiation workers during general employee training. The training

video had not been completed at the time of this inspection. The licensee projected

a completion date of September 15, 1996 for producing the video training aide.

c.

Conclusions

The inspector determined that establishing the electronic locking turnstiles at the

RCA entrance provided substantial positive control over workers accessing the RCA

to ensure each worker's exposure is monitored by an electronic dosimeter. Two

software system modifications were made that served to enhance worker

performance during RCA entry procedures. Although the training video has not

been completed, the inspector determined that all of the controls necessary to

prevent recurrence of the violation have all been completed and were verified to be

in place. This violation is closed.

R8.2

Review of UFSAR Commitments

A recent discovery of a licensee operating their facility in a manner contrary to the

Updated Final Safety Analysis Report (UFSAR) description highlighted the need for a

special focused review that compares plant practices, procedures and/or parameters

to the UFSAR descriptions.

While performing the inspection discussed in this report, the inspector reviewed

Section 12.3 of the Salem Station UFSAR that related to the areas inspected. The

inspector verified that the UFSAR wording was consistent with the observed plant

practices, procedures and/or parameters.

V. Management Meetings

X 1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the

conclusion of the inspection on September 18, 1996. The licensee acknowledged the

findings presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified .

TABLE I

Salem Chemistry Test Results

Chemical

Method of *

NRC Known **

Analysis

Analysis

Hydrazine

SP

(Secondary Lab

Analysis)

Ammonia

IC

(Secondary Lab

Analysis)

Copper

AA

(Secondary Lab

Analysis)

Hydrazine

SP

(Primary Lab

Analysis)

Copper

AA

(Primary Lab

Analysis)

  • Methods:

AA= Atomic Absorption

IC= Ion Chromatography

Value

34.1 +/-0.5

56.1+/-1.0

68.2+/-1.0

22.0+/-0.8

30.5+/-0.8

48.2+/- 1.2

110+/-4

305+/-8

40.4+/-0.6

80.6+/-1.2

162+/-3

34.1 +/-0.5

56.5+/-1.0

85.2+/-1.2

40.4+/-0.6

80.6+/-1.2

162+/-3

SP= UV-Vis Spectrophotometry

Licensee **

Value

' 34.97 +/- 0.15

55.9+/-0.7

68.8+/-0.4

22+/-2

31.0+/-1.1

48.3+/-0.5

102+/-2

283'+/-6

34.3+/-1.5

89+/-2

167+/-3

34.8+/-0.4

57.1+/-0.4

86.9+/-1.1

41+/-3

76.3+/-1.5

160+/-4

All reported uncertainties are +/- one standard deviation (1 s).

Comparison

Agreement

Agreement

Agreement

Agreement

Agreement

Agreement

Agreement

Agreement

Qualified

Agreement

Agreement

Agreement

  • Agreement

Agreement

Agreement

Agreement

Agreement

Agreement

ATTACHMENT 1 TO TABLE I "

Criteria for Comparing Analytical Measurements from Table II

This attachment provides criteria for comparing results of capability tests. In these criteria

the judgement limits are based on data from Table 2.1 of NUREG/CR-5244, "Evaluation of

Nonradiological Water Chemistry at Power Reactors". Licensee values within the plus or

minus two standard deviation range { +/- 2Sd) of the ORNL known values are considered to

be in agreement. Licensee values outside the plus or minus two standard deviation range

but within the plus or minus three standard deviation range { +/- 3Sd) of the ORNL known

values are considered to be in qualified agreement. Repeated results which are in qualified

agreement will receive additional attention. Licensee values greater than the plus or minus

three standard deviations range of the ORNL known value are in disagreement. The

standard deviations were computed using the average percent deviation values of each

analyte in Table 2.1 of the NUREG.

The ranges for the data in Table I are as follows.

Agreement

Qualified Agreement

Analyte

Range

Range

Chloride

+/- 8%

+/- 12%

Fluoride

+/- 12%

+/- 18%

Sulfate

+/- 10%

+/- 15%

Silica

+/- 10%

+/- 15%

Sodium

+/- 14%

+/- 21 %

Copper

+/- 10%

+/- 15%

Iron

+/- 10%

+/- 15%

Boron

+/- 2%

+/- 3%

Ammonia

+/- 10%

+/- 15%

Hydrazine

+/- 10%

+/- 15%

Lithium

+/- 14%

+/- 21%

IP 50001:

IP 61726:

IP 62707:

IP 71707:

IP 79701:

IP 83750:

INSPECTION PROCEDURES USED

Steam Generator Replacement

Surveillance Observations

Maintenance Observations

Plant Operations

LWR Water Chemistry Control and Chemical Analysis-Program

Occupational Radiation Exposure

ITEMS OPENED, CLOSED, AND DISCUSSED

50-272&311 /96-12-01

50-272&311 /96-12-02

50-272&311 /96-12-03

50-272&311/96-12-04

UNR

IFI

UNR

UNR

Ineffective corrective action

Inspector followup of SW operation

RHR flow instrument not present as stated in UFSAR

Acting radiation protection manager qualifications

Closed

50-272/96-01-05

VIO

Repetitive RCA access control procedure violations

'*

ALARA

DOT

FME

IV

NSS

NRC

ORNL

PDR

PSE&G

QA

QC

RCA

RCS

RP

RP&C

RPM

RWPs

sco

SGRP

SNSS

SORC

SRO

SW

TAF

TLD

TS

UFSAR

WO

LIST OF ACRONYMS USED

As Low As Reasonably Achievable

  • Department of Transportation

Foreign Material Exclusion

Independent Verification

Nuclear Shift Supervisor

Nuclear Regulatory Commission

Oak Ridge National Laboratory

Public Document Room

Public Service Electric and Gas

Quality Assurance

Quality Control

Radiological controlled area

Reactor Coolant System

Radiation Protection

Radiological Protection and Chemistry

Radiation Protection Manager

Radiation Work Permits

Surface Contaminated Object

Steam Generator Replacement Project

Senior Nuclear Shift Supervisor

Station Operations Review Committee

Senior Reactor Operator

Service Water

Temporary Access Facility

Thermoluminescent dosimeter

Technical Specification

Updated Final Safety Analysis Report

Work Order