ML18102B322

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Insp Repts 50-272/97-07 & 50-311/97-07 on 970316-0426. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering,Plant Support & Plant Security
ML18102B322
Person / Time
Site: Salem  PSEG icon.png
Issue date: 05/20/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18102B320 List:
References
50-272-97-07, 50-272-97-7, 50-311-97-07, 50-311-97-7, NUDOCS 9705280116
Download: ML18102B322 (46)


See also: IR 05000272/1997007

Text

Docket Nos:

License Nos:

Report No.

Licensee:

Faciiity:

Location:

Dates:

Inspectors:

Approved by:

U. S. NUCLEAR REGULATORY COMMISSION

50-272, 50-311

DPR-70, DPR-75

REGION I

50-272/97-07, 50-311 /97-07

Public Service Electric and Gas Company

Salem Nuclear Generating Station, Units 1 & 2

P.O. Box 236

Hancocks Bridge, New Jersey 08038

March 16, 1997 - April 26, 1997

C. S. Marschall, Senior Resident Inspector

J. G. Schoppy, Resident Inspector

T. H. Fish, Resident Inspector

R. K. Lorson, Resident Inspector

L. N. Olshan, Project Manager

J. 0. Noggle, Radiation Protection Specialist

E. B. King, Physical Security Specialist

G. C. Smith, Physical Security Specialist

James C. Linville, Chief, Projects Branch 3

Division of Reactor Projects

9705280116 970520

PDR

ADOCK 05000272

Q

PDR

EXECUTIVE SUMMARY

Salem Nuclear Generating Station

NRC Inspection Report 50-272/97-07, 50-311 /97-07

This integrated inspection included aspects of licensee operations, engineering,

maintenance, and plant support. The report covers a 6-week period of resident inspection;

in addition, it included the *results of announced inspections by regional security and

radiation protection inspectors.

Operations

In general, operators continued to exercise conservative and deliberate control over outage

activities. For example, operators generally performed well during the draindown to mid

loop, while in mid-loop, and in restoration from the mid-loop condition. Station and

operations management promptly and appropriately identified and corrected the causes of

minor performance weaknesses that occurred during the evolution. (Section 01.2).

Infrequent lapses in operator performance continued, however, to occur. In this period,

less than adequate technical specification tracking, knowledge deficiencies concerning vital

instrument bus inverter operation, and poor operator turnover resulted in an NRC-identified

violation of technical specifications concerning electrical bus train operability. The

operators and plant management took prompt and appropriate action to restore the correct

electrical configuration, identify the cause, and prevent recurrence. (Section 02.1 ).

A lapse occurred in the attention to proper implementation of the operator workaround

program as a result of operations staff personnel changes. The existing operator

workarounds did not adversely impact plant safety, however, continued inattention to

underlying deficient conditions could adversely impact availability of plant equipment. The

Operations Work Control Superintendent initiated corrective actions to improve

performance in this area (Section 02.2). Operators continued to demonstrate greatly

improved ownership of plant equipment. The operators demonstrated ownership by

notifying plant management that an industry issue affecting emergency diesel generator air

start systems applied to Salem. As a result, support staff initiated corrective actions.

(Section 03.2).

Management oversight has improved the quality of equipment and personnel performance.

For example, inspectors concluded that the PSE&G staff significantly improved the tagging

program. The program changes, combined with improved operator procedure adherence,

sharply reduced the frequency of tagging errors and eliminated breakthrough events. The

tagging program is ready to support restart (Section 03.1 ). In addition, effective

implementation of the Salem Assessment Restart Action Plan resulted in establishment of a

new self assessment, development of procedures to improve the use and effectiveness of

self assessme-n:t;-conduct of comprehensive self assessments that documented

weaknesses, and an increased percentage of self-identified issues. The inspectors

concluded that the area of self assessment is ready for restart. (Section 07 .1)

Implementation of the Salem Human Performance Management Restart Action Plan

resulted in significant improvement in the quality of oversight, teamwork, and assessment

of worker performance. The inspectors concluded that it is too early to judge the

ii

effectiveness of the trending results of the human performance errors, and that

management/supervisory presence in the field needed improvement. However, on balance,

the inspectors concluded that the improvements in human performance management were

adequate to support restart. {Section 07.2)

Maintenance

The inspector concluded that PSE&G made significant improvements in the Foreign

Material Exclusion {FME) program since the shutdown of the Salem units in mid 1995. In

addition, management continues to respond to problems and to make progress in improving

overall FME compliance. Inspectors concluded that the FME program 1s sufficient to

support the restart of Salem Units 1 and 2. (Section M1 .2) The PSE&G staff has also

made significant improvement since the shutdown of the Salem units in mid 1995. In

addition, management continues to respond to problems and continues to make progress in

improving overall tagging compliance. This issue is no longer considered a restraint to the

restart of Salem Units 1 and 2. {Section M1 .3)

The ability to plan and schedule work, then accomplish the work according to the schedule

and plan has been a long-standing weakness at Salem. The Salem management and staff

made significant improvement in the effectiveness of planning and scheduling during the

current shut down. During the current inspection period, plant management implemented

the twelve week work schedule to further improve the effectiveness of planning and

scheduling, and to reduce distractions and potential challenges to control room staff.

{Section M7. 1 )

Engineering

Engineering did not adequately provide sufficient time for installation and testing of the

CFCU modification consistent with the outage plan. Design engineers, quality assurance

inspectors and senior nuclear shift supervisors provided frequent oversight of the

installation. {Section E2.1 ).

In a letter to th.e NRC dated April 10, 1997, PSE&G provided a basis for reasonable

assurance the Salem Technical Specification Surveillances and implementing procedures

are adequate to support restart. (Section E7. 1)

Plant Support

The licensee provided very effective exposure controls limiting individual exposures to only

necessary and expected values. Continued diligence is necessary to ensure accurate

postings reflect survey results and for the timely removal of unnecessary radiological

hazards. The internal exposure assessment program has begun improving, but continues

to exhibit weaknesses in staff training and procedure development. RP corrective action

assignment has improved, however, the guidance has yet to be captured in a station-

approved procedure. For several years, the RP services group has not provided ALARA

program and RP program assessments as required, which resulted in a violation .

iii

. '

The security program was determined to be adequate to protect public health and safety .

Appropriate corrective actions have been implemented to address previously identified

weaknesses in the program. The alarm station operators were knowledgeable of their

duties and responsibilities and security training was being performed in accordance with

the NRC-approved training and qualification plan. Protected area detection equipment

satisfied the NRC-approved Physical Security Plan (the Plan) commitments, security

equipment testing was being performed as required by the Plan, and maintenance of

security equipment was being performed in a timely manner as evidenced by minimal

compensatory posting associated with security equipment repairs. Based on observations

and discussions with security officers, the inspectors determined that they possessed the

requisite bowledge to carry out their assigned duties and that the training program was

effective. As an addition to the inspection, the UFSAR initiative, Section 4.2.2 of the Plan

titled, "Vehicle and Cargo Controls," was reviewed. The inspectors determined, based on

discussions with security supervision, procedural reviews, and observations, that vehicles

were being searched and controlled prior to entry into the protected area as described in

the Plan and applicable procedures.

/

iv

,.

TABLE OF CONTENTS

EXECUTIVE SUMMARY .............................................. ii

TABLE OF CONTENTS .............................................. * v

I. Operations .................... ; . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

1

II. Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

14

Ill. Engineering .............................................. *. . . .

21

IV. Plant Support . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

25

V. Management Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

38

v

Report Details

Summary of Plant Status

Unit 1 remained defueled for the duration of the inspection period.

Operators maintained Unit 2 in Mode 5, Cold Shutdown, for the duration of the period.

I. Operations

01

Conduct of Operations

01.1

General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations. In general, the conduct of operations was professional

and safety-conscious; specific events and noteworthy observations -are detailed in

the sections below.

01.2 Mid-Loop Operations - Unit 2

a.

Inspection Scope

The inspectors reviewed the activities associated with the drain down, operation in

and restoration from a mid-loop condition at Unit 2. Th~ licensee established the

mid-loop conditions to repair several leaking steam generator manway covers. The

operators performed the drain down in accordance with operating procedure S2.0P-

SO.RC-0006, Draining The Reactor Coolant System < 101 FT With Fuel In The

Vessel, and restored the plant in accordance with operating procedure, S2.0P-

SO.RC-0002, Vacuum Refill Of The RCS.

b.

Observations and Findings

The inspectors noted several performance strengths during the drain down and

recovery evolutions including:

Strong plant management oversight as demonstrated by two special planning

meetings and by assignment of a test engineer to supervise the evolutions.

Good control room operator focus on key reactor plant parameters during the

drain down and refill.

.

  • -

A thorough pre-drain down briefing that included discussion of the

compensatory actions for an unplanned loss of the residual heat removal

(RHR) system.

An instrument and controls technician appropriately identified and addressed

a problem involving maintenance procedure S2.IC-CC.RHR-0005, that

verified proper operation of the "Mid Loop" trouble alarm. Additionally, the

licensee initiated an action request to review the alarm logic and setpoints to

minimize the frequency of spurious alarm actuations.

..

2

Proper installation of the temporary equipment including the temporary level

indication tubing, and the establishment of reactor system pressure vent

paths through pressurizer system spray valve (PS25), and through pressure

relief valves (PR 1 and 2).

The inspector reviewed engineering evaluation, S-2-RC-MEE-1198, that evaluated use of

the PS-25 vent path. The evaluation contained conservative assumptions and provided

adequate justification for use of the PS-25 vent path.

Despite the generally good oversight and performance of this evolution the inspector noted

some minor performance weaknesses including:

The plant equipment operator did not consistently close the reactor vessel

water level indication tubing isolation valve, and the 52.0P-SO.RC-0006

procedure did not provide guidance for leaving the valve open. The

operations manager initiated an action request to enhance the procedural

controls for this valve.

The 52.0P-SO.RC-0002 procedure did not provide any limits or precautions

for monitoring the rate of temperature change during the vacuum refill of the

reactor plant. The inspector noted that the measured cooldown rate

remained within the allowable technical specification cooldown rate 100

° F/hour. An operations supervisor initiated an action request to review

whether additional temperature controls were required for this procedure.

The inspector considered the performance weaknesses minor and observed that the

licensee appropriately addressed each issue.

c.

Conclusions.

Operators performed well during the drain down to mid loop, control of the plant

while in mid-loop, and restoration from the mid-loop condition. The inspectors

noted some minor performance weaknesses that station and operations

management addressed promptly.

02

Operational Status of Facilities and Equipment

02.1

Vital Instrument Bus Operability

a.

Inspection Scope (71707)

The inspector reviewed control room narrative logs and equipment status to ensure

operation of the facility in accordance with technical specification (TS)

requirements.

b.

Observations arid Findings

At 11 :01 p.m. on April 7, 1997, with Unit 2 in mode 5 and with the nos. 2A and

28 electrical bus trains operable, operators transferred the no. 2C vital instrument

..

3

bus inverter to its alternate AC source in preparation for no. 2C 1 25 vdc bus

outage. At 12:36 a.m. on April 8, operators locked out the 2C emergency diesel

generator (EOG) as part of the bus outage. Technical Specification 3.8.2.2 for

Salem Unit 2 require.s that, in modes 5 and 6, two operable AC electrical bus trains

energized from sources of power other than a diesel generator but aligned to an

operable diesel generator. Each train consists of one 4KV vital bus, one 460V vital

bus and associated control centers, one 230V vital bus and associated control

centers, and one 115V instrument bus energized from its respective inverter

connected to its respective DC bus. At 1: 13 a.m. on April 8, operators declared the

2A EOG inoperable following a 2A safeguards equipment control trouble alarm. The

safeguards equipment control starts its respective EOG on under voltage or accident

conditions, and controls the sequence of the safeguards equipment onto the

associated vital bus. Th.e Technical Specification 3.8.2.2 action statement requires

that with less than two operable vital bus trains, establish containment integrity

within eight hours. Operators entered the TS 3.8.2.2 action statement and began

to restore the 2C EOG. At 4:42 a.m. on April 8, following a 2C EOG operability

run, operators declared 2C EOG operable and exited TS 3.8.2~2.

At approximately 1 :00 p.m. on April 8, the inspector noted that operators

considered the 2A EDG inoperable and the 2C electrical bus train operable. The

operators had not, however, realigned the 2C vital instrument bus to its inverter as

required by TS 3.8.2.2* .. The operating shift did not know the 2C vital instrument

bus inverter alignment status and did not recognize the importance of that status

relative to TS requirements. During discussions with the inspector, the control

room operator recognized the significance of the inverter alignment, and initiated

action to restore the 2C inverter to its correct alignment. At 4:00 p.m. on April 8,

operators completed the restoration and appropriately exited TS 3.8.2.2.

The operators initiated a significance level 1 root cause analysis of the event (CR

970408283). Operations management improved the TS tracking log and mandated

additional operator training on inverter lineup and operability requirements. In

addition, operations management noted that the action statement requirement to

establish containment integrity would require isolating the residual heat removal

flow path, since the initial accident alignment of RHR in the safety injection mode

takes suction from the refueling water storage tank. Plant management stated their

intent to request a change to the action statement requirement, perhaps similar to

the standard technical specification requirement to suspend operations involving

core alterations, positive reactivity changes, or movement of irradiated fuel and to

initiate corrective action to restore the minimum required vital bus equipment.

_The event had no actual safety consequence, since.a loss of off-site power did not

occur during the period of time (approximately 1 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />) that the licensee did not

maintain containment integrity with less than 2 AC electrical bus trains operable.

The problem had minor safety significance as a result of Unit 2 plant status

(shutdown for 22 months) and the operator's ability to maintain the facility in the

shutdown condition for an extended time period. The inspector concluded that

failure to establish containment integrity within eight hours with *only one operable

4

AC electrical bus train while in mode 5 (Cold Shutdown) is a violation of TS 3.8.2.2. (50-311 /97-07-01)

Subsequent to the event, the inspector identified that S2.0P-S0.115-0013,

Revision 5, 2C 115V Vital Instrument Bus UPS System Operation, Section 5.9.4 did

not contain adequate guidance to ensure TS 3.8.2.2 compliance when operating the

inverter on DC only. Operators initiated action to revise S2.0P-S0-115-0013. In

addition, the Operations Technical Support Superintendent identified that S2.0P-

ST.4KV-0002, Revision 7, Electrical Power Systems AC Distribution, did not check

Vital instrument bus inverter alignment to its AC supply in mode 5 or 6. Thus,

procedure S2.0P-ST.4KV-0002 did not satisfy the surveillance requirements of TS 4.8.2.2. The operations staff revised the procedure and satisfactorily performed the

surveillance within the 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> allowed by TS Section 4.0.3. The operations staff

initiated CR 970410123 to evaluate -the apparent cause for the inadequate

surveillance and to determine why the Technical Specification Surveillance

Improvement Project (TSSIP) phase one did not identify and correct_ the deficiency.

This licensee-identified and corrected violation of failing to properly test the vital

instrument bus inverter as required by TS 4.8.2.2 is being treated as a non-cited

violation, consistent with Section Vll.B.1 of the NRC Enforcement Policy.

c.

Conclusions

  • Less than adequate technical specification tracking, knowledge deficiencies

concerning vital instrument bus inverter operation, and poor operator turnover

resulted in an NRC-identified violation of technical specifications concerning

electrical bus train operability. The operators and plant management they took

prompt and appropriate action to restore the. correct electrical configuration, identify

the cause, and prevent recurrence.

02.2 Operator Workarounds and Control Room Deficiencies

a.

Inspection Scope (92901 l

The inspector' assessed the effectiveness of continued implementation of SC.OP-

AP .ZZ-0030, Operator Workaround Program.

b.

Observations and Findings

Salem procedure SC.OP-AP.ZZ-0030 established the Operations Manager's

expectations concerning the identification, tracking, and management of operator

workarounds and burdens. The inspector identified that the operations staff failed

to meet these expectations in the following areas:

The operations work control superintendent did not maintain an updated

workaround listing available to the operating shifts. (A 10-week old listing

was available in front of narrative log.)

5

The operations shift support superintendent did not ensure that operating

shifts were knowledgeable of operator workarounds and burdens.

The operations work control superintendent did not perform a quarterly

assessment to determine the aggregate impact of workarounds on the plant

and operator capabilities.

The operations work control superintendent did not coordinate effectively

with the maintenance department to remove operator workarounds and

operator burdens.

The operations work control superintendent promptly initiated actions to improve

operator awareness (including an updated listing in the control room) and to assess,

manage, and coordinate the removal of operator workarounds and burdens. The

inspector noted that the recent turnover of work control superintendents and

licensed operators directly responsible for the program contributed to the observed

weakness in this area.

c.

Conclusions

Operations management did not ensure proper implementation of the operator

workaround program. The existing operator workarounds did not adversely impact

plant safety, however, continued inattention to underlying deficient conditions could

prevent the normal operation of structures, systems and components. The

operations work control superintendent initiated corrective actions to improve

performance in this area.

03

Operations Procedures and Documentation

03.1

Operator Questioning Attitude (71707)

07

07.1

a.

Reactor operators demonstrated good questioning attitudes and a willingness to

improve technical specification surveillance procedures. Operators identified and

documented questions conc;:erning potential diesel generator preconditioning (AR

97040908), potential operation of pressurizer overpressure protection system

(POPS) outside the design basis (AR 97042114 7), and diesel generator hot restart

testing enhancements (AR 970424061 ). The inspector concluded that operators

demonstrated a safety-conscious questioning attitude to ensure appropriate

management review of potentially safety significant technical issues.

Quality Assurance in Operations

Self Assessment Capability, NRC Restart Item 111.21 (Closed) and Salem Restart

Assessment Plan (Closed)

Inspection Scope

The inspectors reviewed the licensee's self assessment program consisting of work

packages and associated procedures prepared by the licensee to satisfy the Salem

6

Self Assessment Restart Action Plan as defined in the licensee's letter of March 26,

1996, to determine whether the actions within the plan that are needed for restart

have been completed. The inspection also reviewed the implementation and

effectiveness of the program to meet the expected results cited in the plan through

audits of self assessment reports in the areas of maintenance, operations and

planning, and areas that needed significant improvement at the time of plant

shutdown. Interviews were conducted with the Supervisor, Salem Station Projects;

the Salem Self Assessment Coordinator;. and several members of the Quality

Assurance organization. The inspection was conducted followir.g the guidance for

self assessment inspections that was included in Inspection Procedure 40500.

b.

Observations and Findings

From July 9 through July 11, 1996, and from January 6 through January 9, 1997,

NRR inspectors performed an inspection of the Salem Self Assessment Restart

Action Plan. The inspectors reviewed the actions that the licensee had taken to

satisfy the items in the plan, Revision 8, dated July 16, 1996. The objective of the

plan was to develop the capability and acceptance of the Salem organization such

that self assessment is used effectively and routinely to improve performance

continually. The plan consists of two Problem Statements needing resolution to

achieve an acceptable self assessment program. Problem Statement . No. 1 stated

that the existing *self assessment program was limited in scope and that the results

did not accurately identify the root causes of performance weaknesses. Problem

Statement No. 2. stated that the Salem work force, in general, rarely performed self

assessments, and when they were performed, they were done so inconsistently:

The licensee expected to establish a new culture that encouraged self assessment is

an automatic and explicit step' of every action by each employee; established

procedures to improve the use and effectiveness of self assessment; conducted

comprehensive organization self assessments that document its major performance

weaknesses and the completed actions that address these weaknesses; and

demonstrated an inc.reased trend in the percenta~e of self identified issues.

Revision 8 to the plan indicated that all restart actions needed to address each of

the Problem Statements have been completed. The inspectors audited (or reviewed)*

all of the backup files for the Problem Statement actions to review the bases for

licensee's findings.

Following are some of the items reviewed by the inspectors: ( 1) the Self

_ Assessment procedure for routine operations, SC.SA-AP.ZZ-0034(0), Revision 1,

  • (2) the Self Assessment procedure for restart following outages,-SC.SA-SD.ZZ-

0035(0), Revision 0, (3) the qualifications of the Salem Self Assessment

Coordinator, (4) Self Assessments of Maintenance (for the periods of October 5-20,

1995, February 20 -23, * 1996, and December 3 - 13, 1996), Radiation Protection

(for the period of June 1 through June 29, 1996), Operations (December, 1996),

and Planning (December 18, 1996), and (5) Self Assessment of the Self

Assessment Program (for the perioc.i of May 22 - June 15, 1996) .

7

In addition, the inspectors reviewed the closure documents for Problem Statement

No. 1, dated February 15, 1996, and Problem Statement No. 2, dated July 8,

1996. The inspectors verified completion of all the actions in the plan required prior

to restart.

Problem Statement No. 1 stated that the existing self assessment program was

limited in scope and the results did not accurately identify the root causes of Salem

performance weaknesses. To assess the actions taken to address Problem

Statsment No. 1, the inspectors reviewed 3everal of the Self Assessment

procedures, interviewed the Station Self Assessment Coordinator, and reviewed his

qualifications. The inspectors considered the self assessment program broad in

scope and effectively managed, and able to effectively identify performance

weaknesses. These weaknesses are then handled by the Corrective Action

Program, discussed in NRC Inspection Report 50-272/311, 96-18. This Inspection

Report notes improvement in root cause analysis skills and concludes that the

-

actions taken to improve the Corrective Action Program supported restart. Thus,

the inspectors concluded that the objectives of Problem Statement No. 1 of the

Self Assessment Restart Action Plan had been met.

Problem Statement No. 2 stated that, in general, the Salem work force rarely

performed self assessments, and when they were performed, they were done

inconsistently .

_With regard to the frequency of performing self assessments, the inspectors noted

that the Self Assessment procedure for routine operations stated that the frequency

should be based on the inputs from the preceding self assessments, but that at

least four per year should be performed. It also stated that at least one assessment

per year should address the department's performance in the area of Corrective

Actions. The Self Assessment Coordinator stated that the four self assessments

per year do not have to be assessments of the entire department, but rather of a*

particular departmental function.

The Self Assessment procedure for restart following outages required a full

department Self Assessment prior to restart from a refueling outage or extended

outage of approximately four weeks. The Self Assessment Coordinator informed

the inspectors that this procedure will be changed to require that a self assessment

be performed prior to restart from any outage, reactor trip or inadvertent safety

injection actuation and that the scope of that self assessment will be determined

based on the cause of the outage.

_The inspectors concluded that the frequency of self assessments required by these _

two procedures has been met and satisfies the part of Problem Statement No. 2

that states that the Salem work force rarely performed self assessments.

In order to assess the progress the licensee has made in meeting the inconsistency

statement of Problem Statement No. 2, the inspectors reviewed self assessment

reports in the areas of maintenance, operations, planning, and radiation protection .

The inspectors found that the comprehensive Self Assessments effectively identified


8

areas that needed improvement. For example, the Self Assessment of the

Maintenance Department for the period of October 5-20, 1995, concluded that

there were weaknesses that needed to be resolved before the Maintenance

Department would be ready to safely and reliably support restart of Salem and

continued safe full power operation. The Self Assessment was a contributing factor

in management's decision to impose the Maintenance Intervention and provide

training for department personnel. The Self Assessment for the period of December

  • 3 - 13, 1996, noted improvements in the maintenance area, but stated that

sustained performance in this area will be required to determine the effectiveness of

the Maintenance Intervention. The Self Assessment stated that several of the

people that were interviewed thought that they had learned a lot from the

Maintenance Intervention and that it will help them perform their job in a more

professional manner. Furthermore, the NRC Resident Inspector staff noted

improvement in the performance *of the Maintenance Department as noted in

Inspection Report 50-272/311, 97-03, dated April 3, 1997.

The recent self assessments of operations and planning concluded that both areas

were ready for restart, but noted areas that needed additional attention. These

areas, which will. be handled by the Corrective Action Program, include procedure

use and adherence, management presence in the field, and tagging.

The percentage of self-identified problems improved from about 60 per cent in

November, 1995, to about 90 per cent in June, 1996. This percentage remained

between 80 and 90 per cent, with several short-duration drops due to increased

outside inspections. This is an indication of the effectiveness of the Self

Assessment program.

The implementation of the management and peer observer program has shown

improvement. A new process instituted pre-printed index cards used to provide

field observation comments. This has increased the number of management

observations being reported. Peer observations are being done by supervisors,

rather than peers, because of objections by the union. The inspectors concluded

that this is an acceptable alternative and has been effective in identifying concerns.

Based on their review of several key self assessments, and noting the increase in

the percentage of problems that are self-identified and the improvements in

performance in the areas of operations and maintenance, the inspectors. concluded

that the inconsistency part of Problem Statement No. 2 has been adequately

corrected.

c.

Conclusions

Effective implementation of the Salem Assessment Restart Action Plan re_sulted in

establishment of a new self assessment, development of procedures to improve the

use and effectiveness of self assessment, conduct of comprehensive self

assessments that documented weaknesses, and an increased percentage of self-

identified issues. The inspectors concluded that the area of self assessment is

ready for restart.

9

07.2 Salem Human Performance Restart Plan (Closed)

a.

Inspection Scope

The inspectors reviewed the Salem Human Performance Restart Action Plan,

Revision 6, dated December 3, 1996, to determine whether actions within the plan

needed for restart had been completed. - The inspection also reviewed the

implementation and effectiveness of the program, as documented in audits of

human performance, in meeting the expected results cited in the plan. Inspectors

interviewed the Supervisor, Salem Station Projects; Planning and Development

Manager, Human Resources; the Project Manag'er, Restart Plan Coordinator; the

Manager, Corrective Actions and Quality Services; the Supervisor, Corrective

Actions; several members of the Quality Assurance organization; and a random

selection of plant personnel.

b.

Observations and Findings

From July 9 through July 11, 1996, arid from January- 6 through January 9, 1997,

NRR inspectors performed an inspection of the Human Performance Restart Plan.

The plan consists of six Problem Statements needing resolution to achieve an

acceptable Human Performance Program. The Expected Results in the plan are that

the management and supervisory positions are filled with the right people; that high

standards are established, communicated, understood and demonstrated by the

employees; that leaders are working together; t_hat there is ari increased number of

people on Performance Improvement Plans; and that the 11umber of incident reports

due to human error show a consistent decreasing trend.

Revision 6 of the plan, dated December 3, 1996, indicates that all of the restart

actions needed to address each of the Problem* Statemen_ts have been completed.

The inspectors audited the backup files for selected actions to review the bases for

the licensee's findings regarding supervisory performance improvement (Actions 1 e,

1 g, and 1 h); expectations, work processes, performance indicators (2b, 2c, 2g, 2j,

21); leadership training and self assessment skills (3c, 3e); communications (4c, 4e,

4g); teamwork and management presence in the field (5.1, 5.3); human

performance trending and causes (6.1, 6.2).

In addition, the inspection also reviewed the closure inputs for: Problem Statement

No. 1, dated October 3, 1996; Problem Statement No. 2, dated October 2, 1996;

Problem Statement No. 3, dated October 3, 1996; Problem Statement No. 4, dated

June 19, 1996; Problem Statement No. 5, dated November 13, 1996; and Problem

Statement. No. 6,.dated November 15, 1996.

As part of Problem Statement No. 1, the performance of the managers and

supervisors was evaluated. As a result, many personnel changes were made. The

inspectors, based on- interviews with the licensee's staff and discussions with the

NRC Resident Inspectors, concluded that the changes have resulted in a stronger

management team at the station. The inspectors concluded that the objectives of

Problem Statement No. 1 have been met.

,.

10

As part of Problem Statement No. 2, the licensee has instituted a program known

as Breakthrough FOCUS in which selected personnel are sent offsite for five days of

training intended to change the culture at the station and lead to improvements in

work practices. Approximately 400 people have received this training.

Based on the results of the Culture Index Survey, improvement is taking place in all

of the five key characteristics known to be present in high performing organizations:

missions and goals, knowledge and skills, lateral integration, simple work processes,

and self improvement culture. The inspectors concluded that the objectives of

Problem Statement No.2 have been met. *

As part of Problem Statement No. 3, the licensee offers, on a voluntary basis, a

Dale Carnegie personal development course which been taken by approximately 350-

people. All supervisors have taken MARC training which involves the appropriate

use of direction and discipline in the workplace. The inspectors conciude that the

leadership training and self assessment objectives of Problem Statement No. 3 have

been met.

As part of Problem Statement No. 4, to improve communications the licensee

started conducting meetings on a regular basis to keep staff informed of key issues

and hear feedback from their management. Use was made of a publication called

"Nuclear Today" to communicate key items of progress and key issues regarding

Salem Restart Plans. The Communications Exchange Process was started in late

1995 to communicate key messages from the Salem management team and the

departments through face-to-face weekly meetings. Feedback was requested and

communicated to the Salem management team. Face-to-face meetings were

initiated to increase department manager/supervisor field presence. The licensee

also conducted audits through questioning of Salem employees regarding the

effectiveness of the Communications Exchange Process. Although the licensee

concludes that improvement in the quality of communications has occurred, the

face-to-face mode is lagging with respect to other modes of communication.

The inspectors observed the Management Meeting that was held on July 10, 1996,

where management goals, schedules, performance indicators and key plant and

licensing issues were discussed. The Chief Nuclear Officer/President of the Nuclear

Business Unit to first level supervision attended the meeting. It began with a

statement from someone who had recently completed the Breakthrough training.

He appeared to be satisfied with the training. The inspectors found that the

meeting was effective in improving communications at the site.

The inspectors agree that_communications has inJp(oved as evidenc~d by pul;>li_sh_ed

information placed on bulletin boards throughout the plant and a sampling of staff

meetings. The inspectors conclude that the. objectives of Problem Statement No. 4

have been met.

One of the actions in Problem Statement No. 5 is to increase manager/supervisor

presence in the field. The licensee stated that is not able to verify the time spent in

the field by managers and supervisors, but believes it is improving. The inspectors,

11

based on random discussions with plant personnel and discussions with the

Resident Inspectors, agree that manager/supervisor presence in the field has

improved, but improvement in this area is still needed.

Another objective of Problem Statement No. 5 was to improve teamwork in the

Salem management group. The regularly scheduled Management Meetings

previously discussed under Problem Statement No. 4 have been effective in

improving teamwork at the site. Thus, the inspectors conclude that the objectives

of Problem Statement No. 5 have been met.

As a result of comments from an independent assessment team, the licensee added

Problem Statement No. 6 dealing with trending of human performance. The

trending of human performance, using methodology developed by FPI International,

entails the classification of human error events as either breakthrough events, near

misses, or precursors. The number of occurrences is then calculated per 10,000

person-hours and plotted month-to-month. The inspectors reviewed the results for

the period of August through November of 1996 and noted a slight decrease in the

number of human error events. The inspectors concluded that the process is a

good method for trending human error events, but it has not been in place long

enough to determine the actual human error trend at the station. *

c.

Conclusions

Implementation of the Salem Human Performance Management Restart Action Plan

resulted in significant improvement in the quality of oversight, teamwork; and

assessment of worker performance. The inspectors concluded that it is too early to

judge the effectiveness of the trending results of the human performance errors.

The inspectors noted increased supervisory presence in the field, however, station

management does not have an effective tool for monitoring these observations.

However, on balance, the inspectors concluded that the improvements in human

performance management were adequate to support restart.

08

Miscellaneous Operations Issue

08.1

(Closed) Inspector Follow-up Item 50-272&311 /96-16-02: improperly coded

corrective action documents. Salem staff corrected the significance coding on

several corrective action documents that an NRC inspector identified as incorrect.

Salem staff also determined that the mis-coding was not a generic issue. This item

is closed.

08. 2

(Closed) Violation 50-27 2&311/94-24-01 : failure to ensure containment integrity.

Technical Specification 3.9.4 requires containment integrity during core alterations.

The loss of integrity that occurred in October 1994, resulted from open service

water vent valves inside containment thus providing a release path to open service

water drain valves outside containment. Corrective actions to this violation were

inadequate as indicated by a similar event the inspectors documented as a violation

in NRC Report 50-272&311/96-18 (VIO 96-18-02). In this more recent event,

operators lost containment integrity when mechanics removed a service water valve


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12

in piping outside containment at a time when service water*vents for the piping

were open inside containment. For administrative purposes, item 94-24-01 is

I

closed and corrective action adequacy will be tracked under iter:n number 96-18-02.

08.3

(Closed) Violation 50-272&311 /96-07-02: violation of Technical Specification 6.8.1

requirements. An equipment operator failed to perform a procedure step to close

the control power breaker after racking up a 13kV breaker and subsequent failure of

the responsible senior reactor operator to initiate appropriate action. The inspector

concluded PSE&G staff's response 'to the violation was adequate. Also, the NRC

staff determined the Corrective Action Restart Plan appropriately addressed generic

corrective action issues. This violation is closed.

08.4

(Closed) Violation 50-272&311/96-15-01: corrective action for op~rator

performance problems. This violation identified that Operations staff inadequately

investigated an instance where operators inadvertently operated an emergency

control air compressor without service water cooling being supplied to the

compressor. Operations management developed procedure SC.OP-AP.ZZ-0114(Z),

Event Identification and Investigation. The procedure provides guidance to

operators for initial shift investigations of events. The inspector determined the

procedure was adequate and confirmed Operations staff trained the operators on

the new procedure. Also, NRC staff concluded Salem staff adequately addressed

the generic issue of corrective action through the Corrective Action Restart Plan.

This violation is closed.

08.5 (Closed) Violations 50-272&311/EA94-239-01012. 50-272&311/EA96-177-01012,

and 50-272&311/EA96-177-01022: discrimination against employees engaged in

protected activities as defined in 10 CFR 50. 7 (a)( 1). A brief summary of each

event follows:

Violation EA94-239-01012

In December 1992, two Safety Review Group (SRG) engineers attempted to

document a safety concern on a corrective action document, however, the then-

General Manager - Salem Operations tried to dissuade them from issuing the

document. When they suggested that they may need to file a safety concern he

told them to get out of his office.

Violation EA96-177-01012

In 1993 and 1994, an Onsite Safety Review (OSR) engineer received negative

performance reviews from the matrager-Nuclear Safety Review because the OSR

engineer supported the two engineers, mentioned above, regarding their roles in

the December 1992 event.

Violation EA96-177-01022

In August 1994, PSE&G management transferred an SRG engineer, against his will,

from the Salem organization to the Hope Creek organization because of his role in

the December 1992 event.

13

The inspector reviewed the responses to these violations and examined a number of

supporting documentation such as corporate memos, training material, station

procedures, and interviewed members of the Employee Concerns Program. The

corrective actions for these violations was comprehensive. They include:

Since 1994, senior PSE&G management made significant personnel changes

throughout the Salem and Hope Creek organizations. The managers involved

in the above events are no longer at Salem or Hope Creek.

PSE&G management communicated, and continues to emphasize, company

policy regarding safety concerns. The policy is that expressing a concern

about safety is not only acceptable, it is a professional responsibility.

Management training and General Employee Training emphasii;es handling of

safety concerns.

-

A formal Employee Concerns Program is in place with dedicated staff.

Employees have access to this program via an office visit, mail, drop box,

phone, or exit interview.

Additionally, based on observations made over the past eight months during plant

inspection activities, the inspector has noted significant improvement in company

environment regarding openness toward safety concerns. Management has also

improved the corrective action programs that address those concerns. The

inspector concluded senior PSE&G management took comprehensive and effective

corrective actions in response to the discrimination events. These violations are

closed.

08.6 (Closed) LER 50-272/96-041 - missed surveillance for radiation monitors

source check. This LER was a minor issue and was closed.

08. 7

(Closed) LER 50-311 /96-011 - missed surveillance for sampling boron concentration

of refueling canal. The inspectors discussed the subject of this LER in NRC Report

No. 50-272&311 /96-12. The LER did not reveal any new issues. This LER is

closed.

08.8 (Closed) LER 50-311 /96-013 - missed surveillance for performing *tritium grab

samples when the refueling canal was flooded. This event occurred due to a

misinterpretation of the technical specification requirement to sample within twenty-

four _hours of flooding the refueling canal. Operators thought the twenty-four hour

interval began at the- completion -of the flooding. Salem staff later concluded the

interval started at the initiation of flooding and revised the appropriate procedure

accordingly. The inspector verified Salem staff revised the procedure. This LER is

closed.

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14

II. Maintenance

M 1

Conduct of Maintenance

M 1 . 1 General Comments

a.

Inspection Scope* (62707)

The inspectors observed all or portions of the following work activities:

  • * * *

970224263:

970117323:

961227217:

970209046:

steam generator primary manway leak repair

28 EOG exhaust manifold leak repair

CFCU SW piping modification

no. 21 RHR pump casing flange gasket leak repair

The inspectors observed that the plant staff performed the maintenance effectively

within the requirements of the station maintenance program.

b.

Inspection Scope (61726)

The inspectors observed all or portions* of the following surveillances:

  • * * * * * *

S2.0P-ST.DG-0002:

S2.RE-ST.ZZ-0002:

S2.0P-ST.DG-0001:

S2.0P-ST.DG-0019:

S2.0P-ST.CAN-0007:

S2.0P-ST .4KV-0002:

S2.0P-ST .PZR-0002:

28 diesel generator surveillance test

shutdown margin calculation

2A diesel generator surveillance test

2A diesel generator hot restart test

refueling operations - containment closure

electrical power systems AC distribution

inservice testing PORV and PORV block valves

modes 1-6

The inspectors observed that plant staff did the surveillance safely, effectively

proving operability of the associated system.

M1 .2 Adequacy of the Foreign Material Exclusion (FMEl Program, NRC Restart Inspection

Item 111.5 (Closed)

a.

Inspection Scope

Inspection Rep9rt 50-272,311 /96-08 documented an inspection performed in

August 1996 for this restart item. The inspector concluded at that time that

although much had been done to improve the FME program, problems still existed

with implementation of the program. Since then, the inspector made several field

tours for' the purpose of rr0nitoring FME compliance and reviewed the corrective

action for problems identified in the previous inspection report.

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15

b.

Observations and Findings

The inspector found that since the August inspection, implementation of the FME

program has improved. When violations of the program have been found, Salem

staff has documented these in the corrective action program and in their trending

program. Also, Salem management has responded to these violations with pre-job

briefings with emphasis on FME practices, with follow up observations, and with

additional FME training for Salem maintenance personnel. During plant tours, the

inspector found that when required, FME areas have been posted and adequate

precautions have been taken to prevent introduction of foreign material into systems

and components. Numerous examples of good FME practices have been witnessed

during these plant tours.

c.

Conclusions

The inspector concluded that PSE&G has made significant improvement since the

shutdown of the Salem units in mid 1995. In addition, management continues to

respond to problems and continues to make progress in improving overall FME

compliance. This issue is adequate to support the restart of Salem Units 1 and 2.

M1 .3 Tagging. NRC Restart Item 111.3 (Closed)

a.

Inspection Scope

In response to numerous tagging errors, Salem management established an

improved Safety Tagging Program. The inspectors assessed the adequacy of the

revised program.

b.

Observations and Findings

Salem staff analyzed a data base of approximately 100 tagging issues, covering .the

period November 1994 through January 1996. Their analysis showed tagging

errors had root causes in inadequate program design, inadequate training,

inadequate supervisory methods, and inadequate work practice. In response, the

Operations staff: sharply reduced the number of people authorized to perform

tagging evolutions; performed a job task analysis and issued qualification cards for

. tagging; re-qualified personnel according to their tagging responsibilities; filled

positions in the work control center only with individuals qualified to new tagging

standards; and issued a significant revision to the tagging procedure, NC.NA-AP.ZZ-

0015(0), Safety Tagging on January 15, 1997.

The inspector reviewed performance indicators for the month following

implementation of the revised tagging procedure to determine whether the new

program was effective. The inspector noted three relatively minor errors. Also, the

rate of tagging errors was the lowest in over a year, even though during this recent

interval plant personnel performed many more evolutions (445) than during a similar

interval in 1996 (341 ). The inspector also assessed the significance of the errors

and noted that no event was a breakthrough event (defined as an event where

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16

process barriers failed, with potential or actual personnel injury or equipment

damage). Historically, there was at least one breakthrough event a month from

August 1 996 to January 1 997. The inspector attributed the favorable performance

in tagging to operators adequately implementing the improved procedure.

The inspector also noted that management added a self-assessment element to the

tagging program. Senior reactor operators evaluate one out of every five tagging

evolutions and each maintenance supervisor conducts three job evaluations per

week. Salem staff initiated condition r~solution reports to address deficiencies

identified as a result of these assessments.

c.

Conclusions

The inspector concluded that PSE&G has made significant improvement since the

shutdown of the Salem units in mid 1995.. In addition, management continues to

respond to problems and continues to make progress in improving overall FME

compliance. This issue. is adequate to support the restart of Salem Units 1 and 2.

M7

Quality Assurance in Maintenance Activities

M7. 1 Work Control

a.

Observations and Findings

During the inspection period plant managers noted continued difficulty in completing

daily work as planned and scheduled .. In particular~ the managers noted that plant

staff continued to distract control room operators with requests for authorization of

work not previously. planned for that day. The requests caused operators and shift

technical advisors to spend time reviewing the potential impact of the requested *

activities on plant conditions and already ongoing activities. The review provided

the potential to distract control room staff from their normal duties.

As a result of their concern about scheduling effectiveness, the plant managers

decided to direct operators to refuse to authorize work not previously scheduled,

unless the operators concluded that failure to perform the work would have an

adverse impact on safety. In addition, the managers implemented the twelve-week

work schedule for Salem Unit 2, starting with the activities for week five of the

twelve week schedule. The managers expect that the twelve week schedule will

improve the ability of plant staff to plan and control the daily work.

b.

Conclusions

The ability to plan and schedule work, then accomplish the work according to the

schedule and plan has been a long-standing weakness at Salem. The Salem

management and f:taff made significant improvement in the effectiveness of

planning and scheduling during the current shut down. During the current

inspection period, plant management implemented the twelve week work

' '

MS

MS.1

17

schedule to further improve the effectiveness of planning and scheduling, and to

reduce distractions and potential challenges to control room staff.

Miscellaneous Maintenance Issues

(Closed) Unresolved Item 50-272 & 311/94-01-01: control of maintenance

troubleshooting. In February 1994, maintenance technicians inadvertently caused

the opening of the main steam dump valves to the condenser. This item was

opened pending the investigation of the event. Salem staff determined that the root

cause was inadequate pre-job planning.

Since that time, maintenance personnel

have been through a significant training program to strengthen technical skills and

to emphasize attention to detail. The inspector found this training appropriate to

address this event. This item is closed.

MS.2 (Closed) Preventive Maintenance Change Request Backlog

a.

Inspection Scope

The inspector reviewed the Salem maintenance program relative to the outstanding

backlog of requests for changes. Specifically, the inspector held discussions with

Preventive Maintenance Group staff members, reviewed the list of outstanding

Preventive Maintenance Change Requests (PMCRs), reviewed a sample of PMCRs,

and reviewed procedures in place to control the processing of PMCRs.

b.

Observations and Findings

From discussions with the Preventive Maintenance Group staff, the inspector

learned that there were 249 outstanding PMCRs for Salem Unit 2 .. They expect that

this backlog will be reduced by a factor of eight to about thirty by the end of 1997.

Although the group is short of staff, recruiting is in progress to obtain additional

personnel. The inspector obtained a list of all 249 outstanding PMCRs and

reviewed it to select a sample of those that by the description appeared to have a

potential for safety impact (i.e., due to a safety function of the component and the

age of the PMCR). The inspector selected fifteen and then reviewed the details of

the PMCR documentation for those sampled. None were found which the inspector

believed would present a safety impact even if delayed until years' end.

From the review of the administrative procedures, the inspector found that the

procedures provide guidance for processing of PMCRs from initiation until closure.

From a discussion and demonstration regarding the computerized database, the

inspector *found that it contained pertinent data related to the PMCRs such as

description, reason for initiation, and due date. The data was also easily retrieved.

The inspector also learned that PSE&G actively monitors the size of the backlog via

a PMCR "Burn-Off" curve. Also, PSE&G staff screen PMCRs and assign due dates

to ensure that they make changes in sufficient time to support the next performance

of the task.

18

c.

Conclusions

From the inspection observations, the inspector found it reasonable to concluoe

that the backlog of PMCRs, although sizable, does not represent an impact to the

safe operation of Salem Unit 2. The administrative control of the PMCRs is

appropriate and effective. PSE&G staff is aware of the size of the backlog and is

working to reduce it.

M8.3 (Closed) Violation 50-272&31 'I /95-12-01: inadequate corrective action for ITE

circuit breaker problems. During the period from December 4, 1989, to March 29,

1995, Salem staff documented thirteen failures of safety related ITE breakers.

During this time, management failed to perform a timely root cause analysis and

failed to implement corrective action to prevent repetitive failures; inspectors

identified two significant concerns with this issue: the technical issue of correcting

the hardware problem, and the programmatic problem of lack of rigor and timeliness

in PSE&G staff determining the root cause.

Regarding the first concern, PSE&G staff, with the aid of the breaker manufacturer,

determined the route cause to be less than adequate preventive maintenance.

PSE&G engineers enhanced the preventive maintenance procedure and performed

the procedure on suspect ITE breakers (i.e., those with sluggish closing times). The

engineers later decided to perform an extensive overhaul on all ITE breakers. The

inspector confirmed that Salem staff completed this overhaul for Unit 2 and that

plant staff is tracking overhaul tasks for Unit 1 breakers. The inspector's review of

the recent performance history revealed no examples of breaker failure following

overhaul. Also, during an interview with the system engineer, the inspector learned

that a newly approved preventive maintenance procedure provides for in place in-

place breaker timing tests every 18 months. These tests detect degradation in

breaker performance.

Regarding the programmatic issue, PSE&G management implemented extensive

changes to improve the corrective action program. Management documented those

changes in their response to NRC Restart Issue 111.a.10, Corrective Action Program.

NRC staff reviewed the program, concluded the improvements *have been effective,

and documented closure of that restart issue in NRG Report 50-272&311 /97-03.

Based on that review and on the information in the previous paragraph, this

violation is closed.

M8.4 (Closed) LER 50-311196-014 - emergency diesel generator automatic start - ESF

actuation. The EDG automatically started during a manual transfer of one off-site

power supply to another. Salem staff determined the cause to be a defective relav

in a vital supply breaker. The corr.active actions included replacing the breaker,

notifying the manufacturer, and revising the breaker inspection procedure to include

details for inspecting the relay. Additionally, Salem staff identified other relays

susceptible to the defect and found that the relays operated satisfactorily. The

inspector considers this LER closed.

'

'

19

MS. 5 (Closed) LER 50-311/96-01 2 - engineered safety feature actuation, 2A 4kv vital bus

undervoltage. While performing an electrical test of the service water pump motor,

two potential transformer fuses opened causing one *of three undervoltage relays to

trip. When operators tried to measure phase to phase voltages using a local panel

voltmeter, a second undervoltage relay tripped causing initiation of the Safeguards

Equipment Controller. This started the 2A EOG. There was little safety significance

since the EOG started and loaded the bus as designed and the plant was already

shutdown and defueled.

Salem engineers performed a formal root cause analysis of the event. They

attributed the cause of the first incident, the blown fuses, to lack of attention to

detail during testing. The cause of the second undervoltage relay tripping was a

design deficiency which is only present when one of the two potential transformers

has open fuses.

The inspector reviewed the corrective actions and determined

they were adequate.

MS.6 (Closed) LER 50-311 /96-015 - breach of containment closure during core reload.

Inspectors documented this issue in NRC Inspection Report 50-272&311 /96-1 S. As

a result of this event, the NRC staff issued violation 50-311 /96-1 S-02.

MS. 7 {Closed) LER 50-311/96-016 - missed surveillance for determining response time of

high containment gaseous radioactivity ESF actuation. Technical specifications

require a verification of this ESF actuation response time every eighteen months.

The maintenance dep,artment tracks this surveill.ance requirement using a

proceduralized computer search of required recurring tasks. The database

incorrectly indicated'that the surveillance was applicable in modes 1 through 5. The

technical specification requirement is applicable in modes 1 through 6.

The inspector reviewed the cofrective action as detailed in Salem's root cause

analysis of the event and concluded that it was satisfactory. In addition, Salem

staff addressed the generic issue of technical specification problems with the

Technical Specification Surveillance Improvement Program (TSSIP).

MS.S (Closed) LER 50-272/96-021 - potential common mode failure for 2SV DC battery

chargers due to molded case circuit breaker damage. During a review of

maintenance inspections, Salem staff determined that circuit breakers within the

2SV DC battery chargers experienced common mode failure of the terminals

involving cracked terminal blocks. In response to this finding, Salem staff revised

maintenance inspection procedures to require inspection specifically for the cracking

which precedes this failure mode. In addition, PSE&G staff investigated whether

similar breakers were in use in other applications at Salem and Hope Creek.

Although PSE&G staff did locate other applications, none was configured in the

manner which induced the cracking. The inspector concluded that the corrective

action for this event was .:;;atisfactory.

MS.9 {Closed) LER 50-272/96-025 - inadequate calibration of overpower delta

temperature protection channels. While performing the calibration of a turbine first

stage impulse pressure channel, the technicicm noticed that the output of the Hagan

'

'

20

lead/lag module was higher than expected. Subsequent testing revealed that the

method used to calibrate the modules was inadequate. The method yielded a non-

conservative output. The inspector learned that this was reportable because these

modules provide output which is used to shutdown the reactor to protect against

excessive power.

The inspector reviewed the corrective action for this problem and learned Salem

staff corrected calibration procedures and then properly calibrated the units. Also,

the investigation determined that other modules in the plant were also being

improperly calibrated so PSE&G staff applied corrective actions to these as well.

This licensee-identified and corrected violation is being treated as a Non-Cited

Violation, consistent with Sec.tion Vll.B.1 of the NRC Enforcement Manual.

M8.10 (Closed) LER 50-272/96-027 - diesel watt meter inaccuracies not accounted for in

surveillance testing. There are three technical specification requirements to perform

EOG testing with the diesels loaded to 2500 - 2600 kw. In October 1996, Salem

staff determined tt)at the diesel watt meter inaccuracy was actually +/- 65 kw. This

meant that even if the testing were performed with a meter indication of exactly

2550 kw, the actual foad could be 15 kw above or below the prescribed load band.

The inspector considered the safety significance of this event to be minimal since

the EDGs were still capable of performing their intended function. Salem staff

revised the surveillance procedures to utilize more accurate test equipment and *

retested the Salem Unit 2 EDGs. There is also a corrective action tracking

document to assure Salem staff applies the corrective action for Salem Unit 1 EDGs

as well.

MS.11 (Closed) LER 50-272/96~029 - surveillance test did not meet technical specification

surveillance requirement. During a recent 18 month surveillance test on a hydrogen

recombiner, *a measurement of the heater and neutral to ground resistance indicated

values below the acceptance criteria. The technicians questioned the test results

because the recombiner had performed well during an operability test. An

investigation revealed two things: 1) Technicians were not taking readings properly

because of procedure inadequacies and, 2) Technicians took previous readings with

a digital volt/ohm meter (DVOM) instead of with a meggar. The surveillance

procedure does not direct using the DVOM, which if used may provide incorrect

data.

The corrective action included a revision to the surveillance procedure to provide

details for attaching test equipment, and general counseling of personnel to strictly

follow procedures. The hydrogen recombiners were retested using the re.vised

method and met the surveillance requirement.

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21

Ill. Engineering

E2

Engineering Support of Facilities and Equipment

E2.1

Generic Letter 96-06 (GL 96-06) Modifications

a.

Inspection Scope (37551)

Design engineering began installation of design change package (DCP) 2EC-3590 to

address saf.ety issues identified in GL 96-06 as they impacted the Salem Unit 2

containment fan cooler units (CFCUs) and attached service water system piping.

The inspector evaluated the engineering organization's involvement in the

installation of DCP 2EC-3590.

b.

Observations and Findings

Design engineering did not allow sufficient time in the schedule for installation and

testing of the CFCU modification. Despite schedule pressure, contract maintenance

supervisors provided continuous and focused oversight of ongoing SW piping

modifications to ensure personal safety and minimal impact of SW system

operation. Salem maintenance supervisors, by contrast, provided little oversight of

field installation .

Contract maintenance supervisors identified that technicians attached a portion of

the new SW piping to the no. 21 SW header prior to proper hanger installation.

Plant management promptly declared the associated SW header inoperable and

disconnected the new section of piping .. Maintenance supervision initiated a

significance level 2 condition resolution report (970404205) to evaluate the cause

and potential adverse affects of this problem .

. The inspector observed that design engineers provided frequent engineering

oversight at the job site, and quality assurance inspectors and operations senior

nuclear shift supervisors conducted regulator field observations of the SW piping

modifications.

c.

Conclusions

Design engineering did not allow sufficient time for installation arid testing of the*

CFCU modifications without adversely affecting the outage plan. Design engineers,

quality assurance inspectors and senior nuclear shift supervisors provided frequent

oversight of the installation.

E7

Quality Assurance in Engineering Activities

E7 .1

Technical Specification Surveillance Improvement Program (TSSIP)

In NRC Inspection 50-272&311 /96-15, the NRC requested that PSE&G provide

justification for not completing TSSIP, Phase 2, prior to restart of Salem Unit 2. In

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'

22

a letter to the NRC dated April 10, 1997, PSE&G provided a discussion of the TSSIP

process, the accomplishments of Phase 1, and the results of FSAR, LER, and

additional technical reviews. In the letter, PSE&G concluded that the multiple

reviews and the corrective actions stemming from the reviews provided reasonable

assurance the Salem Technical Specification Surveillances and implementing

procedures are adequate to support restart. The inspectors concluded that PSE&G

provided reasonable assurance the Technical Specifications and implementing

procedures are adequate to support restart of Salem Unit 2.

ES

Miscellaneous Engineering Issues

E8. l

(Closed) Violation *50-272&311 /96-117-03013 and -04013: inappropriate corrective

action. The technical issue involved the dete.rmination and resolution of

noncpnservative setpoint methodology with regard to the POPS. The programmatic

issue involved the general failure of Salem staff's corrective action program.

Together, these violations represented examples where management failed to

implement timely corrective action, failed to promptly issue a Licensee Event Report

for an operating condition outside the licensing basis, took credit in a calculation for

an operating configuration outside the design basis, and took credit for an American

Society of Mechanical Engineers (ASME) Code Case that the NRC had not yet

approved for use. These violations were significant and resulted in civil penalties.

E8.2

The NRC staff documented the review of the technical issue regarding* acceptable

POPS design basis in NRC Report 50-272&311 /96-07, .Section E8.4. Following

NRR review and approval of proposed new limits, NRC staff closed the issue in NRC

Report 50-272&311 /97-02! Section EB.6.

Salem management addressed the programmatic issues regarding the corrective

action program in the response to NRC R'estart Issue 111.a.10, Corrective Action

Program. NRC staff documented the review and acceptance of the Corrective

Action Program in NRC Report 50-272&311 /97~03. Based on acceptable closure of

the technical and programmatic issues related to these violations, the two violations

are closed.

(Closed) Violation 50-272&311 /96-117-06013: valve not properly positioned

following a plant modification. In May 1993, plant personnel added drain lines and

a drain valve to Pressurizer Overpressure Protection system piping. The installation

process, however, did not ensure that operators properly positioned the drain valve

following the modification. As a result, the valve remained closed (instead of open)

from May 1993 until October 1994.

The inspector determined that operators have correctly positioned the valve and

that Salem staff reviewed the valve alignment database to assure themselves no

other similar examples e"'.isted. The inspector also verified that Salem staff revised

SC.OP-AP.ZZ-0103(0), TRIS Configuration Control, to address proper system

alignment following design changes. The inspector reviewed this procedure and

considered the process adequate. This violation is closed .

' .

23

E8.3

(Closed) LER 50-272/96-019 - misclassification of blowdown sample valves. In July

1996, while performing a review of 10 CFR 50 Appendix J valves, Salem staff

identified four valves in the steam generator blow down sample system which were

not included in the leak rate test program. A 1985 Licensing Change Request

deleted the valves from the technical specifications and from the leak rate test

program. Salem staff requested the change because they believed the valves were

part of a closed system within containment and were therefore not required to be in

the test program. However, during the July 1996 review, Salem staff determined

that because the system was seismic Category II rather that Category I, the system

is not a closed system.

The inspector reviewed the corrective action plan and found it adequate to address

the issue. Also, this corrective action is documented in the Salem corrective action

tracking system to assure completion. This licensee identified violation is being

treated as a Non-Cited Violation consistent with Section Vll.B.I of the NRC

Enforcement Policy.

E8.4

(Closed) Violation 50-311 /96-13-02: failure to follow procedures. During a recent

inspection, an inspector found two examples where Salem staff failed to adhere to

approved procedures. One example involved a field discrepancy that an operator

identified and corrected, but did not result in anybody initiating a corrective action

document. Another example involved a change made to a safety evaluation after

Salem staff had approved the evaluation. The inspector reviewed the corrective

action for the violation and found it to be satisfactory. In addition,* the inspector

noted that the generic issue of procedure compliance was addressed in the

licensee's response to NRC Restart Item 111.3, Procedure Use and Adequacy.

Inspection Report 50-272&311 /97-03 documented closure of that issue. This

violation is closed.

E8.5. (Closed) Violation 50-272&311/E94-112-01013: failure to promptly identify and

correct the cause of spurious high steam flow signals. The spurious signals

occurred during reactor/turbine trips on June 10, 1989, July 11, 1993, February

10, 1994 and on April 7, 1994.

There were two issues of concern regarding this violation. One was the technical

issue of understanding the cause and implementing corrective action to resolve the

spurious signal problem. Salem staff specifically addressed that issue in PSE&G's

response to NRC Restart Issue 11.38, Spurious High Steam Flow Signals Causing SI.

The NRC staff is reviewing that information for acceptability. The second concern

was the broader programmatic issue of timely and adequate corrective action and

the general application of that program by PSE&G staff. Salem staff addressed that

issue in PSE&G's response to NRC Restart Issue 111.10, Corrective Action Program.

NRC Inspection Report 50-272&311 /97-03 documented the NRC review and

closure of that issue and documented that the corrective action plans are adequate

to support Salem restart. Since the NRC tracked the technical concern as a restart

issu*e and has closed and documented the programmatic issue, this violation is

closed.

- '

'

24

E8.6

(Closed) Violation 50-272&311 /96-08-04: failure of Salem staff to initiate a

corrective action document in a timely manner. A team that reviewed temporary

and permanent modifications installed at Salem identified conditions potentially

adverse to quality. Salem staff, however, did not write a condition report to

address the conditions until a month after the audit team exited. PSE&G staff

addressed the broad issue of the corrective action program, including the prompt

initiation of corrective action documents, in the response to NRC Restart Issue

111.10, Corrective Action Program. NRC Inspection Report 50-272&311 /97-03

documented NRC review and closure of that issue. Based on that closure, this

violation is closed.

E8.7

(Closed) Violation 50-272&311/E95-117-02013: inadequate corrective action for

No. 12 switchgear fan failure. In December 1994, No. 12 switchgear penetration

area ventilation (SPAV) fan failed. In May 1995, No. 13 SPAV fan failed, resulting

in the SPAV system being unable to perform its design function of cooling safety

related switchgear. In the response to the violation, Salem management identified

several contributing factors, including operator and engineering staff lack of

knowledge of the SPAV system design basis.

E8.8

For corrective actions, Salem staff repaired the fans; created additional preventive

maintenance tasks for the fans; revised the Operability Determination procedure and

the nuclear safety equipment and surveillance tracking procedure, and revised the

.

.

.

corrective action program. The inspector reviewed the revised documents,

including those that track surveillances for non Technical Specification equipment

important to safety. This element of corrective action was satisfactory. Other

elements of the violation response are satisfactory based on prior NRC closure of

restart items that addressed the Corrective Action Program, Operability

Determinations, and Operator Performance. This violation is closed.

(Closed) Violation 50-272 & 311/E95-117-05013: Salem staff did not promptly

identify and correct miscellaneous conditions adverse to quality. The violation

identified nine examples where PSE&G failed to take appropriate corrective action

for conditions adverse to quality. The conditions occurred during the period from

1990 until 1995.

The inspector reviewed PSE&G' s response to this violation and found that for each

example, PSE&G had implemented corrective action to resolve each condition.

These examples represented failures of the Salem corrective action program, failures

of operations operability determinations, and one failure to install a safety classified

part. Since mid 1995, PSE&G has made significant improvements in plant programs

as part of resolving NRC Restart Issues. Specifically, PSE&G has responded to NRC

Restart Issue 111.a.10, Corrective Action Program, Restart Issue 111.6, Operability

Determinations, and Restart Issue 111.18, Parts Availability and Accuracy of Bill of

Material. The NRC has reviewed PSE&G's response to these issues and has found

the corrective actions adequate. The NRC has documented this in Inspection

Reports 50- 272 & 311 /96-08, /97-03, and /97-02, respectively. The inspector

has reviewed the scope of those restart issues and found that they envelop the

generic corrective action requirements for the nine examples of this violation.

' .

25

Based on the review of the violation response, and the three closed restart issues,

this violation is closed.

IV. Plant Support

R1

Radiological Protection and Chemistry (RP&C) Controls

R 1. 1

External Exposure Controls

a.

Scope (83750)

The inspector reviewed facility postings and high radiation area controls, reviewed

RP instrument and respiratory protection controls, and reviewed dosimetry vendor*

changes during this inspection period. Tours of the facility, review of documents

and interviews with licensee personnel were conducted.

b.

Observations and Findings

The inspector verified that selected locked high radiation areas were locked as

required and verified that the high radiation area key controls were in place and all

keys were accountable. RP oversight of the primary RCA access control point was

excellent. RP instrument and respiratory protection issue was provided through RP

technicians utilizing computer review of qualifications for equipment issuance and

accountability for the equipment issued. All RP equipment available for issuance

was appropriately calibrated and source-checke*d as reqL::~ed.

Both Units _1 and 2 containments were well posted and radiologically controlled.

The auxiliary buildings were, in general, appropriately posted and controlled. The

inspector observed some discrepancies in the solid radwaste "hot" machine shop

area, in that some lexan tent areas were posted in excess of actual radiological

conditions. Tent number 1 had a shielded component on the floor with a radiation

area posting on the door, but no other indication of the radiological hazard in the

tent from the shielded component. Tents 2 and 3 were both posted as radiation

areas, while a current survey indicated dose rates of less than 1 mR/hr. Further

review indicated that the shielded component in Tent number 1 was an SJ valve

that was last worked in June 1996. The licensee determined that the valve was

waste material and was disposed of during the inspection. All three lexan tent

areas were deposted in accordance with survey results.

Radiation Work Permits (RWPs) were written with an emphasis on restricting

individual doses per entry with very low dose alarm set points used on electronic

dosimetry. Typical values* of 3-15 mr'em alarm setpoints were used. Higher

expected doses per entry involve ALARA prejob discussions prior to er.1:ry,. resulting

in customized setpoints based on specific work requirements.

Beginning April 1, 1997, the licensee b~gan utilizing Pennsylvania Power and Light

(PP&L) as a TLD processing vendor. The inspector verified that PSE&G had

26

conducted a QA audit prior to accepting the new vendor and that PP&L was a

NVLAP-accredited laboratory in categories I-VIII. PSE&G continues to conduct a

blind spike program by exposing 15 TLDs to a known exposure and submitting them

to PP&L with each batch of personnel badges for quality assurance purposes.

PSE&G continues to maintain responsibility and cognizance for personnel dosimetry

processing and record dose determination processes.

c.

Conclusions

The licensee provided excellent oversight of the RCA access control point and

provides very effective exposure controls, limiting individual exposures to only

necessary and expected values. Continued diligence is necessary to ensure

accurate postings reflect survey results and for the timely removai of unnecessary

radiological hazards. TLD vendor processing was properly reviewed by the licensee

with appropriate quality control procedures implemented.

R1 .2

Internal Exposure Controls

a.

Scope (83750)

The inspector reviewed the bioassay measurement facility, reviewed applicable

calibration and source check records, reviewed current internal exposure

assessment results, licensee procedures, and interviewed licensee personnel.

Over the past 3 years, the licensee has maintained one whole body counter that

utilizes sodium-iodide detectors for conducting bioassay measurements. Previous

inspection reports have documented the complex of radionuclides present at both

Salem and Hope Creek stations and questioned the capability of the sodium-iodide

counter to accurately discriminate between these radionuclides. There have not

been any recorded internal exposures during that time period, however, the

capability for providing accurate measurements has been in question.

b.

Observations and Findings

During this inspection, the inspector verified that the licensee's germanium detector

whole body counter had been calibrated on March 13, 1997, sufficient to provide

the radionuclide discrimination capability. The inspector observed that since vendor

calibration in March 1997, daily source check counts of the germanium whole body

counter had not been successfully obtained and, therefore, the instrument had not

yet been put into service. The inspector determined that the whole body counter

operator did not have the skills required to effect a successful fine gain adjustment

on the germanium whole body counter.

The inspect:Jr reviewed whole body count records since the previous RP inspection

in December 1996. Four positive whole body counts were documented, of which,

only one reached an 'a,ction level requiring repeat measurements and exposure

assessment. Rapid radionuclide clearance from the body was appropriately

assessed by the licensee as a gastro-intestinal deposition resulting in less than 1 0

'

'

27

mrem CEDE (procedures require recording at 50 mrem or greater). The inspector

noted that the subject investigational whole body count was not recorded in the

licensee's PREMS database system as required by procedure ND.RS-Tl.ZZ-0403(0),

Rev. 3. When this discrepancy was identified, the licensee initiated an action report

to evaluate and correct this issue. The inspector determined that since there was

no exposure significance to this omission that this met the criteria for a non-cited

violation.

The inspector reviewed the above mentioned procedure, "Evaluation of Bioassay

Data," and observed that very limited guidance was provided for conducting an

internal exposure assessment and no requirement for a peer review to verify

calculations was provided.

c.

Conclusions

The inspector determined that the licensee at both Salem and Hope Creek stations

continues to conduct RP programs resulting in no recorded internal exposures. A 3-

year issue regarding calibration of the licensee's investigational whole body counter

has been .recently resolved. Although recently calibrated, the investigational whole

body counter has not been in service due to limitations in training of the operator.

The Radiation Protection services supervisor stated that additional whole body

counter trainina on the investigational whole body counter would be provided during

1997. The inspector also noted t~at the internal exposure assessment procedure

lacked sufficient guidance relative to the conduct of internal exposure assessments.

The Radiation Protection services staff indicated that procedure development was

underway. The internal exposure assessment program is improving but some

weaknesses in staff training and procedure adequacy remain.

R1 .3

As Low As Is Reasonably Achievable. (ALARA)

The inspector discussed with the licensee collective occupational exposure results

for 1996 at Salem Station. A Salem Station exposure goal of 208 person-rem was

established in late 1995 based on both units being returned to operation in February

and June of 1996, as originally scheduled and without anticipating the replacement

of steam generators in Unit 1. The licensee reported 209 person-re*m for 1996

withoL1t including the Unit 1 steam generator replacement exposures. Inclusion of

the 1996 Unit 1 steam generator replacement exposure (130.8 person-rem) resulted

in a total of 340.3 person-rem for Salem station 1996 exposures. The steam

generator replacement project was originally estimated to cost 166.5 person-rem,

however, the estimate was revised upward to 232.9 person-rem in early 1997 due

to additional steam generator support modifications, steam generator removal

equipment modifications and outage schedule delays. Salem Station exposure

estimates for 1997 are projected to be 30 person-rem plus 102.1 person-rem for

completion of the Unit 1 steam generator replacement project. Current (as of April

21, 1 997) 1997 exposure results are tracking within the goal at 17.7 person-rem

and 85.6, respectively. In light of the short duration of planning the steam

generator replacement project, exposures were well managed and controlled. The

. ' '

R6

R6.1

a.

28

Salem Station ALARA program for 1 996 through this inspection period was found

to be effective.

RP&C Organization and Administration

RP Organization Changes

Scope (83750)

The inspector reviewed the current RP staffing level of Salem Station commensurate.

with both units in extended outage conditions.

  • b.

Observations and Findings

Individual reactor unit RP oversight was provided by specifically assigned RP

supervisors. The 35 permanent RP technician workforce was expanded by 30

additional contractor RP technicians that were appropriately trained and qualified to

provide the necessary radiological safety coverage. Inspector outage observations

indicated adequate personnel resources were provided.

c.

Conclusions

Salem Station RP staffing resources were appropriate during extended outage

conditions of both Units ..

R7

Quality Assurance in RP&C Activities

R7. 1

RP Program. Oversight

a.

Scope (83750)

The licensee's QA organization was beginning a biennial RP program audit during

this inspection arid was, therefore, not reviewed. During this inspection, additional

review of the RP corrective action process for identified problems was conducted,

the program oversight provided by RP services (Section R8.1, UFSAR review) was

reviewed, and the RP self-assessment program was reviewed. This review

consisted of examination of selected licensee documents and interviews with

applicable licensee personnel.

b.

Observations and Findings

During a previous inspection\\ significant weakness was reported with respect to

providing effective corrective actions for licensee-identified radiological problems.

PSE&G correspondence to the NRC, dated February 6, 1997, addressed these

concerns. The licensee indicated that a root cause manual was enhanced and that

. 1 Inspection Report Nos. 50-272/96-17 and 50-311/96-17

c.

29

the program now requires identification o"f a corrective action for each root cause or

causal factor, or a justification when a corrective action is not specified for each

root cause or causal factor. The licensee indicated that the improved corrective

action process was implemented January 1, 1997, and indicated that an RP

corrective action desk guide would be developed by March 31 , 1 997.

The inspector reviewed the following station corrective action program procedures:

"Action Request Process," NC.NA-AP.ZZ-OOOO(Q), Rev. 1

"Corrective Action Program," NC.NA-AP.ZZ-0006(0), Rev. 14

"Radiological Occurrence Investigations," NC.RP-Tl.ZZ-1001 (Q), Rev. 0

"Salem Radiation Protection Department Self Assessment/Corrective Action

Program Desk Guide," Rev. 0

The licensee indicated that the improved corrective action program in the RP

department was fully implemented by mid-February 1997, with some changes

added in March 1997 to improve the thoroughness of handling radiological

incidents. The inspector noted that while the program was implemented,

insufficient information was available to assess effectiveness.

The* action request process procedure designated level 1 events as:. severe or

unusual plant transients, safety system malfunction or improper operations,

radiation in excess of limits( or severe injury. The corrective action program

procedure provides root cause analyses for only Level 1 events with corrective

actions associated with each cause to prevent recurrence of the event. Level 2

events were defined as conditions that do not have a significant impact on plant or

personnel safety. The Level 2 events are assigned apparent causes and corrective

action is assigned to resolve the conditions. For Level 2 events, assigning actions

to prevent recurrence or to verify effectiveness was optional. In practice, Sale.m

RORs are all designated as level 2 or 3 events, not requiring the identification of

root causes and with no requirement for assigning corrective actions to each

identified cause. In practice, however, the RP department has shown in recent

results, that level 2 events are carefully considered with all causes identified and

corrective actions assigned to each. Additional program guidance was contained in

an RP department desk guide, which required a peer review and RPM review for

each level 1 and level 2 event and specified that a corrective action be identified for

each identified cause. The desk guide provided the additional program guidance

necessary to effectively resolve radiological incidents.

The RP department has been conducting self-assessments since October 1995.

The inspector reviewed RP self-assessment reports for the last 6 months. The

inspector noted variable quality and value of these self-assessments.

Conclusions

The licensee's corrective action response letter of February 2, 1997 described

actions taken for Level 1 events. RP incidents that do not result in exceeding

  • i'

30

exposure limits (Level 2 and 3 events), do not require a root cause or corrective

action review. The RP department has developed a desk guide to accomplish an

improved review of level 2 events.

The RP department self-assessment program is beginning to provide some value,

although the assessments continue to be of variable quality.

RS

Miscellaneous RP&C Issues

RS.1

Review of Updated Final Safety Analysis Report (UFSARl Comr-:-:itments

a.

Scope (83750)

The inspector reviewed current Salem Station practices with respect to Section

12.4 of the UFSAR.

b.

Observations and Findings

While performing the inspections discussed in this report, the inspector reviewed

Section 12.4 of the UFSAR that related to the areas inspected. The following

inconsistency was noted between the wording of the UFSAR and the plant practices

and procedures observed by the inspector .

Within Section 12.4 entitled, "ALARA Program," the UFSAR lists the functions to

be provided by the Principal Health Physicist-Radiological Safety, which include:

ensuring periodic reviews of the ALARA program are conducted and providing

periodic assessments of the station RP program.

The inspector reviewed documented results of the RP services group efforts over

the last several years, and did not find significant evidence of periodic reviews of

the ALARA program scheduled by RP services that were conducted, nor any

evidence of periodic assessments of the Salem s'f:ation RP program provided by RP

services. *Documents reviewed indicated that in late 1995, RP and ALARA program

elements were scheduled for assessment by the RP services group over a 4-year

time period, however, none of the subject assessments were conducted.

c.

Conclusions

The UFSAR commitment discussed above is specified in licensee procedure NC.NA-

AP.ZZ-0024(0), Rev. 7, which states in Section 3.6 that, the Principal Health

Physicist-Radiological Safety is responsible for ensuring periodic reviews of the

ALARA program are conducted and is responsible for periodic, scheduled

assessments of the station RP program with a frequency such that all functional

activities are assessed at least every 4 years.

Contrary to the above, the Principal Health Physicist-Radiological Safety has not

scheduled or provided periodic ALARA program reviews, nor RP program

assessments for the past 4 years. The Principal Health Physicist-Radiological Safety

31

documented a business process action report on April 14, 1 997, indicating that

assessments of the RP program have not been systematically performed, however,

.no corrective actions had been taken at the time of this inspection. Considering the

time period of omission and lack of results reviewed, this is considered a violation

of RP procedures (50-272/97-07-02, 50-311/97-07-02).

S 1

Conduct of Security and Safeguards Activities

a.

Inspection Scope

Determine whether the security program, as implemented, met the licensee's

commitments in the NRC-approved security plan (the Plan) and NRC regulatory

requirements. The security program was inspected during the period of

March 17-21rand April 14-17, 1997. Areas ins.pected included: previously

identified items; protected area barriers and detection aids; alarm stations and

communications; testing, maintenance and compensatory measures; training *and

qualification; organization and administration; quality assurance; and security and

safeguards activities.

b.

Observations and Findings

Appropriate corrective actions have been implemented to address previously

identified weaknesses in the program. The alarm station operators were

knowledgeable of their duties and responsibilities, and security training was being

performed in accordance with the NRC-approved training and qualification plan ..

Protected area detection equipment satisfied the NRC-approved Physical Security

Plan (the Plan) commitments, security equipment testing was being performed as

required by the Plan, and maintenance of security equipment was being performed

in a timely manner. Based on observations and discussions with security officers,

the inspectors determined that they possessed the requisite knowledge to carry out

their assigned duties and that the training program was effective.

c.

Conclusions

The inspectors determined that the licensee was conducting its security and

safeguards activities in a manner that protected public health and safety:

S2

Status of Security Facilities and Equipment

S2.1

Protected Area Barrier (PABl and Detection Aids

a.

Inspection Scope

Conduct a physical inspection of the PAB and intrusion detection systems (IDSs) to

verify that the PAB satisfied the requirements of the Plan and the IDSs were

functional, effective, and met licensee commitments .

._:

'

32

b.

Observations and Findings

On March 19, 1997, the inspectors observed the testing of the IDSs. However, the

inspectors noted, during a walkdown of the PAB, that in several areas, the height of

the PAB was below the requirements noted in the Plan. The inspectors determined,

based on observations and discussions with security management, that the

discrepancy was caused by gravel within the PAB washing against the fence during

heavy rains. To correct the concern, the licensee committed to rake out all areas

along the PAB where a height discrepancy was identified and include surveillance of

the PAB as part of routine patrols.

c.

Conclusion

On April 16, 1997, the inspectors determined by observation, that the actions taken

by the licensee to correct the concern were adequate. The inspectors determined

that the height of the PAB satisfied the requirements of the Plan and that the IDSs

were functional and effective, and were installed and maintained as described in the

Plan.

S2.2

Alarm Stations and Communications

a.

Inspection Scope

Determine whether the Central Alarm Station (CAS) and Secondary Alarm Station

(SAS): (1) are equipped with appropriate alarm, surveillance and communication

capability; (2) are continuously manned by operators; and (3) include independent

and diverse systems so that no single act can remove the capability for detecting a

threat and calling for assistance, or otherwise responding to the threat, as required *

by NRC regulations.

b.

Observations and Findings

Observations of CAS and SAS operations verified that the alarm stations were

equipped with the appropriate alarm, surveillance, and communication capabilities.

Interviews with CAS and SAS operators found them generally knowledgeable of

their duties and responsibilities. However, on March 19, 1997, the inspectors

noted during interviews that there was some confusion on the part of several of the

CAS/SAS operators regarding when it was necessary to dispatch a responder to

assess an alarm; however, the inspectors did not observe any problems with actual

alarm responses. The concern was discussed with security management by the

inspectors. To address the concern, the licensee agreed to reiterate the expectation

concerning appropriate alarm assessment with all CAS/SAS operators during shift

briefings. Additionally, the inspectors also verified through observations and

interviews that the CAS and SAS operators were not required to engage in activities

that would interfere with the assessment and response functions, and that the

licensee had exercised communication methods with the local law enforcement

agencies as committed to in the Plan.

'

33

c.

Conclusion

The inspectors determined by discussions with the CAS/SAS operators on

April 16, 1 997, that the actions taken by the iicensee to reiterate expectations

concerning alarm assessment were effective. T~e determination was based on the

CAS/SAS operators' responses to the inspectors' questioning. The CAS/SAS

operators were knowledgeable of their alarm assessment responsibilities and the

alarm stations and communications met the licensee's Plan commitments and NRC

requirements.

52.3

Testing, Maintenance and Compensatory Measures

a.

Inspection Scope

Determine whether programs are implemented that will ensure the reliability of

security-related equipment, including proper installation, testing and maintenance to

replace defective or marginally effective equipment. Additionally, determine that

when security-related equipment fails, the compensatory measures put in place are

comparable to the effectiveness of the security system that existed prior to the

failure.

b.

Observations and Findings

The inspectors reviewed testing and maintenance records for security-related

equipment and found that documentation was on file to demonstrate that the

licensee was testing and maintaining systems <,lnd equipment as committed to in the

Plan. However, the inspectors noted that the testing re ... ords of the access control

search equipment did not indicate any equipment failures. On March 20, 1997, the

inspectors observed testing of the metal detectors and noted that three of eight

metal detectors failed the testing criteria. When questioning security management

about the failures and lack of failures annotated on the equipment test records, the

inspectors were informed that failures were not annotated on the test records for

the access control equipment because normal practice was to have the

instrumentation and calibration (l&Cl department make the necessary repairs

immediately upon notification of equipment failures. The inspectors stated that

even though such a practice ensures timely repairs of the equipment, the lack of

failures annotated on the test records eliminates the possibility of trending

equipment reliability. The licensee agreed with the inspectors' rationale and stated

that future equipment testing documentation would capture equipment failures. The

inspectors noted that a priority status was being assigned to each work request and

repairs were normally being completed th.e same day a work request necessitating

compensatory measures was generated. The inspectors also noted that the*

working relationship between security, maintenance and the l&C departments was

excellent as evidenced by the low number of open work requests related to security

equipment during the review of maintenance records .

c.

34

Conclusions

Documentation on file, reviewed April 16, 1997, confirmed that security equipment

was being tested and maintained as required; however, failures of search equipment

were not being documented in the test records. The licensee agreed to change its

practice to allow for tracking and trending of equipment failures found during

testing. Repair work was timely and the use of compensatory measures was found

to be appropriate and minimal.

S5

Security and Safeguar~s Staff Training and Qualification

a.

Inspection Scope

Determine whether members of the security organization are trained and qualified to

perform each assigned security-related job task or duty ln accordance with the NRC-

approved Training and Qualification (T&Q) Plan.

b.

Observations and Findings

On March 17, 1997, the inspectors met with *the security training staff and*

discussed training initiatives associated with enhanced contingency response drills

and tactical response training. The inspectors also observed classroom re-

qualification training addressing the use of force, and determined that the

instructor's presentation was good and that all course material was properly

covered.

The inspectors randomly selected and reviewed T&Q records for fifteen security

force members (SFMs) on April 15, 1997. Physical and firearms re-qualification

records were inspected for armed and unarmed SFMs and security supervisors. The

irispectors found that the training had been conducted in accordance with the T&Q

Plan and was properly documented. Additionally, the inspectors observed weapons

requalification training and determined that the training was conducted in

accordance with the T&Q Plan and that the range was.controlled in a safe manner.

Throughout the inspection,* the inspectors interviewed a number of SFMs to

determine if they possessed the requisite knowledge and ability to carry out their

assigned duties.

c.

Conclusions

The inspectors determined that training had been conducted in accordance with the

T&Q Plan. Based on the SFMs' responses to the inspectors' questions and the

inspectors' observations, the training provided by the security training staff was

considered effective.

"

I

..

35

S6

Security Organization and Administration

a.

Inspection Scope

Conduct a review of the level of management support for the licensee's physical

security program.

b.

Observations and Findings

The inspectors reviewed various program enhancements made since the last

program inspection, which was conducted in August 1996. These enhancements

included the procurement of new weapons to enhance tactical response capabilities,

new uniforms and web gear for the security officers, and the procurement of 17

new radios for communication enhancement. The inspectors reviewed the Manager

- Nuclear Security's position in the organizational struc;:ture and reporting chair.. The

Manager - Nuclear Security reports to the Director - Nuclear Operations Services,

who reports directly to the Senior Vice President - Nuclear Operations, who reports

directly to the Chief Nuclear Officer and President - Nuclear Business Unit.

c.

Conclusions

Management support for the physical security program was determined to be

adequate. No problems with the organizational structure that would be detrimental

to the effective implementation of the security and safeguards programs were

observed or reported.

S7

Quality Assurance in Security and Safeguards Activities

S7. 1

Effectiveness of Management Controls

a.

Inspection Scope

Determine if the licensee has controls for identifying, resolving and preventing

programmatic problems.

b.

Observations and Findings

The inspectors reviewed the licensee controls for identifying, resolving and

preventing security program problems. These controls included departmental self-

assessments and the performance of the NRC-required annual quality assurance

(QA) audits. The licensee also utilizes industry data, such as violations of

regulatory requirements identified by the NRC at other facilities, as criteria for self-

assessment. The inspectors reviewed documentation applicable to the performance

of the self-assessment program and noted that the self-assessment program was

limited in scope. Specifically, 13 of 14 tasks developed to implement the program

have been performe~ repeatedly for the past four years. Additionally, the results of

the performed tasks have not been trended since October 1995. Even though self-

assessment tasks are assigned and performed by security supervision on a weekly

..

c

\\ ....

  • c.

36

basis, the inspectors questioned the effectiveness of the program with security

management. The inspectors were informed by security management that a new

self-assessment program was being developed and would be implemented in the

near future.

Conclusions

The inspectors concluded that the self-assessment program in place to identify,

prevent and resolve potential problems was weak and an improved self-assessment

program would enhance program effectiveness.

S7.2

Audits

a.

Inspection Scope

Review the licensee's QA report of the NRC-required security program audit to

determine if the licensee's commitments as contained in the Plan were being

satisfied.

Observations and Findings

The inspectors reviewed the 1996 QA audit of the security program, conducted

May 6-17, 1996, (Audit No.96-031 ). The audit was found to have been

conducted in accordance with the Plan. To enhance the effectiveness of the audit,

the audit team included two independent technical specialists .. The audit report

identified four weaknesses. The weaknesses were in the areas of vital area

documentation, preventive maintenance for security equipment, closed circuit

television improvements, and the identification of contraband by the security force

member, during an audit drill. The weaknesses were not indicative of programmatic

weaknesses but, if corrected, would enhance program effectiveness. The audit

results had been disseminated to the appropriate levels of management. The

inspectors determined, based on discussions with security management and a

review of the responses to the weaknesses, that the corrective actions were

effective.

c.

Conclusions

The review concluded that the audit was comprehensive in scope and depth, that

the findings were appropriately distributed and addressed and that the audit

program was being properly administered.

S7 .3

Adequacy of Security, NRC Restart Inspection Item 111.24 (Closed)

All open items identified in previous inspection reports were reviewed and corrective

actions were verified to be reasonable, complete and properly implemented.* Security

program implementation has been determined to be adequate to support restart.

37

SS

Miscellaneous Security and Safeguards Issues

S8.1

Review of Updated Final Safety Analysis Report (UFSAR)

. A recent discovery of a licensee operating its facility in a manner contrary to the

UFSAR description highlighted the need for a special focused review that compares

plant practices, procedures, and parameters to the UFSAR description. Since the

UFSAR does not specifically include security program requirements, the inspectors

compared licensee activities to the NRC-approved physical security plan, which is

the applicable document. While performing the inspection discussed in this report,

the inspectors reviewed Section 4.2.2 of the Plan, titled "Vehicle and Cargo

Control," the inspectors determined, based on discussions with security supervision

and reviews of applicable procedures and records, that vehicles were being

searched and controlled prior to entry into the protected area as described in the

Plan a_nd applicable procedures. *

S8.2

(Closed) Inspection Followup Item 50-272, 50-311, 50-354/93-28-01 - Review the

effectiveness of assessment aids after upgrade is complete. The program to

upgrade the assessment aids has been completed and the assessment aids were

. determined to be adequate to perform their intended function.

S8.3

(Closed) Violation 50-272, 50-311/96-18-01, 50-354/96-10-03- Failure to control

badge/keycards and failure to display photo badges in the protected area. The

inspectors verified the corrective actions described in the licensee's response letter,

dated February 26, 1997, to be reasonable and complete and they were found to be

properly implemented. No similar problems were identified.

S8.4

(Closed) Violation 50-272, 50-311, 50-354/EA96-344-01013 - Failure to exercise

positive access control over photo badge keycards thereby creating the opportunity

for unauthorized access to the vital areas. The inspectors verified that corrective

actions described in the licensee's response to letter, dated January 10, 1997, to

be reasonable and complete and they were found to be properly implemented. No

similar problems were identified ..

S8.5

(Closed) Violation 50-272, 50-311, 50-/EA96-344-02013 - Failure to conduct a

physical pat-down search of a contractor that had caused two portal metal

detecto.rs to alarm on three different attempts to pass through them, although these

alarms provided reasonable cause to suspect that the contractor was attempting to

introduce firearms, explosives, incendiary devices, or other unauthorized material

into the protected area, before issuing him a photo badge keycard, and allowing him

to enter the protected area. The inspectors verified the corrective actions described

in the licensee's response letter dated January 10, 1997, to be reasonable.

and complete and properly implemented. No similar problems were identified.

S8.6

(Closed) Violation 50-272, 50-311, 50-354/EA 96-344-02023 - Failure to notify the

senior nuclear shift supervisor (SNSS) of a security threat when a contractor that

should have received a pat-down search entered the protected* area without a pat-

down search. The failure to notify the SNSS resulted in the event not being

58.7

58.8

38

classified per Event Classification Guide 16. The inspectors verified the corrective

actions described in the licensee's response letter, dated January 10, 1997, to be

reasonable and complete and properly implemented. No similar problems were

identified.

(Closed) Violation 50-272, 50-311, 50-354/EA96-344-03014 - Failure to inactivate

the security photo badges and personnel access clearance for 1 2 employees

terminated in June and July 1996 within two working days of termination of

employment. The inspectors verified the corrective actions described in the

licensee's-response letter, dated January 10, 1997, to be rea~rrnable and complete

and properly implemented.

(Closedl°Violation 50-272, 50-311, 50-354/EA96-344-04014 - Failure of two

security supervisors to qualify in all required crit.ical security tasks prior to being

assigned field operations supervisor duties. The inspectors verified the corrective

actions described in the licensee's response letter, dated January 10, 1997, to be

reasonable and complete and properly implemented. No similar problems were

identified.

58.9

(Closed) Violation 50-272, 50-311, 50-354/EA96-344-05014 - Failure to complete

all required tests of an alarm zone prior to releasing the security force member

posted at the alarm zone. The inspectors verified the corrective actions described

int he licensee's response letter, dated January 10, 1997, to be reasonable and

complete and properly implemented. No similar problems were identified.

V. Management Meetings

X1

Exit Meeting Summary

Security inspectors met with licensee representatives at the conclusion of the inspection

on April 17, 1997. At that time, the inspectors reviewed the purpose and scope of the

inspection and presented the preliminary findings. The licensee acknowledged the

preliminary inspection findings.

The inspectors presented the inspection results to members of licensee management at the

conclusion of the inspection on May 7, 1 997. The licensee acknowledged the findings

presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified .

'

v'.,

  • , -

..

INSPECTION PROCEDURES USED

IP37751:

IP 61726:

IP 62707:

IP 71707:

Onsite Engineering

Surveillance Observations

Maintenance Observations

Plant Operations

IP 71750:

Plant Support

IP 81700:

IP 83750:

Physical Security Program

Occupational Radiation Exposure

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-311/97-07-01

50-272,311 /97-07-02

Closed

50-272&311/EA94-239-01012,

EA96-177-01012 & 50-272&

VIO

failure to establish containment integrity within

eight hours with only one operable AC electrical

bus train while in mode 5 (Cold Shutdown)

VIO

Failure of RP Services to provide periodic RP

program and ALARA program assessments.

311/EA96-177-01022

VIO

discrimination against employees engaged in *

protected activities as designed in 10 CFR 50.7

(a)(1)

50-272&311/EA94-112-01013

.VIO

50-272&311/94-01-01

URI

50-27 2&311/94-24-01

VIO

50-272&311 /95-12-01

VIO

50-272&311 /EA95-117-02013

VIO

50-272&311 /EA95-117-05013

VIO

50-27 2&311/EA96-117-03013&

04013

VIO

50-272&311 /EA96-117-06013

VIO

50-272&311 /96-07-02

VIO

50-272&311 /96-08-04

VIO

50-311 /96-13-02

VIO

50-272&311/96-15-01

VIO

failure to promptly identify and correct the cause

of spurious high steam flow signals

control of maintenance troubleshooting

failure to ensure containment integrity *

inadequate corrective action for ITE circuit

breaker problems

inadequate corrective action for #12 switchgear

fan failure

Salem staff did not promptly identify and correct

miscellaneous conditions adverse to quality

  • inappropriate corrective action

valve not properly positioned following a plant

modification

violation of TS 6.8.1 requirements

failure of Salem staff to initiate a corrective

action document in a timely manner

failure to follow procedures

corrective action for operator performance

problems

...

' . .

50-272&311/96-16-02

50-272/96-019 '

50-272/96-021

50-272/96-025

50-272/9.6-027

50-272/96-029

50-272/96-041

50-311 /96-011

50-311/96-01 2

50-311/96-013

50-311 /96-014

50-311/96-015

50-311/96-016

Discussed

2

IFI

improperly coded corrective action documents

LER

misclassification of blowdown sample valves

LER

potential. common mode failure for 28V DC

battery chargers due to molded case circuit

breaker damage

LER

inadequate calibration of overpower delta .

temperature protection channels

LER

diesel watt meter inaccuracies not accounted for

in surveillance testing

LER

surveillance test did not meet TS surveillance

requirement

LER

missed surveillance for radiation monitors source

check

LER

missed surveillance for sampling boron

concentration of refueling canal

LER

ESF actuation, 2A 4kv vital bus undervoltage

LER

missed surveillance for performing tritium grab

samples when the refueling canal was flooded

LER

emergency diesel generator automatic start

LER

breach of containment closure during core reload

LER

missed surveillance for determining response

time of high containment gaseous radioactivity

ESF actuation

, /

....

I

<

A LARA

ASME

CAS

CCTV

CRO

DCP

DVOM

EDG

FME

IDS

NRC

OHA

OSR

PA

PDR

PEO

PMCRs

POPS

PRE MS

PSE&G

RCA

RHR

RP

QA

SAS

SEC

SFM

SPAV

SRG

T&Q

the Plan

TLD

  • TS

TSSIP

UFSAR

LIST OF ACRONYMS USED

As low as is reasonably achievable

American Society of Mechanical Engineers

Central Alarm System

Closed Circuit Television

Control Room Operator

Design Change Package

Digital Volt/Ohm Meter

Emergency Diesel Generator

Foreign Material Exclusion

lntrusiqn Detection Systems

Nuclear Regulatory Commission

Overhead Annunciator

Onsite Safety Review

Protected Area

Public Document Room

Plant Equipment Operator

Preventive Maintenance Change Requests

Pressurizer Overpressure Protection System

Personnel Radiation Exposure Management System

Public Service Electric and Gas

Radiological controlled area

Residual Heat Removal

Radiation Protection

Quality Assurance

Secondary Alarm System

Safeguards Equipment Cabinet

Security Force Members

Switchgear Penetration Area Ventilation

Safety Review Group

Training and Qualification

NRC-approved Physical Security Plan

Thermoluminescent dosimeter

Technical Specification

Technical Specifica~ion Surveillance Improvement Program

Updated Final Safety Analysis Report