ML18106A432

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Insp Repts 50-272/98-01 & 50-311/98-01 on 980202-0315.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML18106A432
Person / Time
Site: Salem  PSEG icon.png
Issue date: 04/02/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18106A426 List:
References
50-272-98-01, 50-272-98-1, 50-311-98-01, 50-311-98-1, NUDOCS 9804070157
Download: ML18106A432 (37)


See also: IR 05000272/1998001

Text

Docket Nos:

License Nos:

Report No.

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved by:

U.S. NUCLEAR REGULATORY COMMISSION

50-272 & 50-311

DPR-70 & DPR-75

REGION I

50-272/98-01 & 50-311 /98-01

Public Service Electric and Gas Company

Salem Nuclear Generating Station, Units 1 & 2

P.O. Box 236

Hancocks Bridge, New Jersey 08038

February 2, 1998 - March 15, 1998

M. G. Evans, Senior Resident Inspector

F. J. Laughlin, Resident Inspector

H. K. Nieh, Resident Inspector

E. H. Gray, Senior Reactor Engineer

L. J. Prividy, Senior Reactor Engineer

L. M. Harrison, Reactor Engineer

James C. Linville, Chief, Projects Branch 3

Division of Reactor Projects

9804070157 980402

PDR

ADOCK 05000272

G

PDR

EXECUTIVE SUMMARY -

Salem Nuclear Generating Station

NRC Inspection Report 50-272/98-01 & 50-311/98-01

This integrated inspection included aspects of licensee operations, engineering,

maintenance, and plant support. The report covers a six-week period of resident

inspection; in addition, it includes the results of announced inspections by regional

engineering inspectors of the Unit 1 motor-operated valve program and an emergency

diesel generator turbocharger failure.

Operations

In general, the conduct of operations was professional and safety-conscious.

Activities associated with the shutdown of Unit 2 on February 11 and the heatup of

Unit 1 on February 18, were performed in a deliberate manner with clear

communications.

Licensed operators' inadequate monitoring of plant parameters and maintenance of

steam generator levels, combined with inadequate communications and crew

teamwork resulted in an inadvertent automatic start of the auxiliary feedwater

pumps when the 14 steam generator level decreased to 9%. The reactor operator

did not follow procedure requirements to maintain the steam generator levels within

the required band.

The licensee's corrective actions to address the reasons for an apparently fatigued

licensed control room supervisor were acceptable. However, there were some

weaknesses identified in licensee management oversight of individµal employee

work hours which the licensee has initiated actions to address.

Maintenance-

Poor planning and inadequate maintenance practices resulted in an incorrect control

switch being installed on the 12 Diesel Fuel Oil Transfer Pump (DFOTP), which.

rendered the pump inoperable. The licensee ascended to Mode 4 on Unit 1 with

less than the required DFOTPs operable, which was a Technical Specification

violation. The licensee's immediate corrective actions for this event were weak,

including an untimely operability determination for the wrong part being installed on

the 21 DFOTP, and untimely verification of correct part numbers for similar control

switches on the four DFOTP electrical panels.

Procedural adherence for the 2A Emergency Diesel Generator (EOG) post-

maintenance testing was poor. Numerous procedural violations by maintenance and

operations personnel resulted in the improper operation of the diesel. There was

little safety significance to these violations as the diesel was out of service for

maintenance. However, they showed a lack of questioning attitude and attention to

ii

Executive Summary

detail by numerous personnel. Additionally, the engineering actiori plan utilized for

the maintenance effort was not sufficiently detailed to promote smooth transition

between the maintenance and operations procedures used.

The licensee met all Technical Specification requirements for the 2C EDG outage

and the crankcase alarm on the 28 EDG. The operator correctly followed the alarm

response procedure for the 28 alarm. The operability determination for the 28 EDG

after the cause of the alarm was determined was adequate, but the decision to run .

the 28 EDG during the 16-hour 2C EDG outage was not appropriate.

On February 11, 1998, the 2A EDG turbocharger failed during a post maintenance

test. The licensee formed a team to get the relevant facts, find the cause of the

failure, evaluate its significance to the operability of the other EDGs, and establish

corrective actions. The NRC reviewed the team activities to assess the evaluation

scope, methods and results. This NRC inspection did not identify any factors that

would provide a basis for disagreeing with the scope, method of investigation, or

with the preliminary findings.

The licensee had adequately implemented their Technical Specification Surveillance

Improvement Program to support Unit 1 restart.

Engineering

The licensee had adequately demonstrated design basis capability for Salem Unit 1

MOVs to support restart. Justifications for key program assumptions and the

applied valve factors were adequate.

The licensee continued to adequately pursue resolution of issues related to the

control area ventilation system (CAVS). However, long term corrective actions are

still necessary to eliminate the need f6r maintenance mode, a time-consuming,

resource-intensive work around which ensures adequate dp margin between the

control room and the adjacent spaces. When this mode is employed, then any

circumstance which necessitates accident pressurized mode, such as an inoperable

CAVS radiation monitor, would require a unit shutdown to Mode 5 so that the

control room emergency air conditioning system intake could be lined up to a non-

operating unit ..

Elevated grass levels in the Delaware River combined with degraded service water

strainers and lack of service water reliability program oversight resulted in

accelerated rates of service water biofouling. Weak management attention allowed

biofouling to occur at unpredictable rates. Several instances of biofouling occurred

in plant components before strainer degradation was identified and effective

corrective actions were taken. In one instance, the biofouling contributed fo the

inoperability of a Unit 2 safety related chiller. Salem staff failed to take prompt

iii

Executive Summary

corrective actions to determine and correct the cause of service water biofouling

problems. System Engineering and Operations interfaces were weak during the

analysis of those problems. The licensee did not adequately evaluate the extent of

condition at both Salem Units. The inspector also concluded that the corrective

actions taken in response to Licensee Event Report 50-272/96-34 were acceptable .

iv

TABLE OF CONTENTS

EXECUTIVE SUMMARY .............................................. ii

TABLE OF CONTENTS ................................. * ............... v

I. Operations ; . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

01

Conduct of Operations ..................................... 1

01 . 1

General Comments ....... *. . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

01.2 Unit 1 Inadvertent Automatic Actuation of an Engineered

Safeguards Feature - Auxiliary Feedwater Pumps ............. 1

04

Operator Knowledge and Performance .......................... 3

04. 1

Inattentive Control Room Supervisor ....................... 3

OB

Miscellaneous Operations Issue ............................... 4

O.B.1 (Closed) LER 50-311/9B-04 ......................... * .... 4

O.B.2 (Closed) LER 50-311/9B-05 ............................. 5

II. Maintenance .................................................... 5

M 1

Conduct of Maintenance .................................... 5

M 1 . 1 General Comments . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

M 1 .2 Wrong Control Switch Installed on 12 Diesel Fuel Oil Transfer

Pump ............................................ 6

M1 .3 Post-Maintenance Testing of 2A Emergency Diesel Generator after

Turbocharger Failure .................................. B

M2

Maintenance and Material Condition of Facilities and Equipment ........ 9

M2. 1 High Crankcase Pressure Alarm on the 2B Emergency Diesel

Generator During a Technical Specification Required Run ........ 9

MB

Miscellaneous Maintenance Issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

MB. 1 2A Emergency Diesel Generator Turbocharger Blade Failure . . . . . . 11

MB.2 (Closed) LER 50-272/96-05, Supplements 6 through 16 ........ 12

Ill. Engineering .................................................... 13

E 1

Conduct of Engineering ............... : . . . . . . . . . . . . . . . . . . . . 13

E1 .1

Generic Letter B9-10 Motor-Operated Valve Program Review and

(Closed) NRC Programmatic Restart Issue 111.a.23: Adequacy of

Motor-Operated Valve Program (Unit 1) . . . . . . . . . . . . . . . . . . . 13

E1 .2

Update on Control Area Ventilation System Issues ............ 20

E2

Engineering Support of Facilities and Equipment ................... 21

E2. 1

Service Water Biofouling and (Closed) LER 50-272/9.6-34 ....... 21

EB

Miscellaneous Engineering Issues ............................. 24

EB.1

(Closed) Violation 50-272/96-11-01 ...................... 24

EB.2

(Closed) Inspector Followup Item 50-272/96-11-02 ........... 24

EB.3

(Closed) Inspector Followup Item 50-272/96-11-03 ........... 25

EB.4

(Closed) Inspector Followup Item 50-272/96-11-04 ...... ~ .... 25

EB.5

(Closed) Violation 50-272/96-11-05 ...................... 25

EB. 6

(Closed) Inspector Followup Item 50-272/96-11-06 ........... 25

v

E8.7

E8.8

E8.9

E8.10

E8.11

E8.12

(Closed) Inspector Followup Item 50-272/96-11-07 ........... 25

(Closed) Inspector Follow Item 50-272/96-11-08 ............. 26

(Closed) Inspector Followup Item 50-272/96-11-09 ........... 26

(Closed) Unresolved Item 50-272/96-11-11 ................. 26

(Closed) Unresolved Item 50-311/96-80-01 ................. 27

(Update) Violation 50-311 /97-21-05 and (Closed) LER 50-311 I

96-07-02 ......................................... 27

V. Management Meetings ............................................ 27

X 1

Exit Meeting Summary .................................... 27

X2

Management Meeting Summary .............................. 27

vi

..

Report Details

Summary of Plant Status

Unit 1 began the period in Mode 5, Cold Shutdown. On February 18, 1998, the operators

increased the average coolant temperature above 200°F and entered Mode 4. The unit

remained in Mode 4 through the end of the inspection period.

Unit 2 began the period operating at 100% power. On February 11, 1998, the licensee

commenced a plant shut down in order to make repairs to the 2A emergency diesel

generator following a failure of the turbocharger. During the shutdown, the licensee

performed other repair activities which included replacement of two pressurizer code

safety valves and repair of the 22 steam generator steam flow transmitters. On March 3,

the NRC resident inspectors participated in the full participation exercise covered by

Inspection Report 50-272, 311, 354/98-80. On March 14, the unit was returned to

service and was operating at about 50% power at the end of the inspection period.

I. Operations

01

Conduct of Operations (71707, 92901, 93702 & 40500)

01 . 1

General Comments

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations. In general, the conduct of operations was professional

and safety-conscious. The inspectors observed activities associated with the

shutdown of Unit 2 on February 11 and the heatup of Unit 1 on February 18, and

noted that the evolutions were performed in a deliberate manner with clear

communications. These evolutions were also observed by the NRC Readiness

Assessment Team Inspection (RATI), as documented in Inspection Report 50-272 &

311 /98-81 . Additional specific events and noteworthy observations are detailed in

the sections below.

01.2 Unit 1 Inadvertent Automatic Actuation of an Engineered Safeguards Feature -

Auxiliary Feedwater Pumps

a.

Inspection Scope

On February 21, 1998, with Salem Unit 1 operating in Mode 4 (Hot Shutdown), the

11 and 12 auxiliary feedwater (AFW) pumps automatically started on Lo-Lo steam

generator level in the 14 steam generator (SG). The licensee made a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />

telephone notification to the NRC as required to document this automatic actuation

of an Engineered Safeguards Feature (ESF). The inspectors reviewed this event and

the licensee's root cause evaluation and corrective actions which are documented in

Action Request (AR) 980221128 .

.2

b.

Observations and Findings

On February 19, the operators commenced warming the main steam lines in

accordance with procedures being utilized to take the plant from Cold Shutdown to

Hot Standby. Warming the main steam lines requires opening the main steam stop

bypass valves (MS18s). In Mode 4, feedwater is manually supplied to the SGs on a

periodic basis. This is usually accomplished by maintaining operating AFW pumps

discharging against closed SG feedwater supply valves on recirculation and opening

these valves when feedwater is needed. However, in this case the AFW pumps

were cycled on and off because orie of the SG feedwater valves was leaking

through. To avoid frequent starting and stopping of the AFW pumps, the periodic

filling of the SGs was performed on a less frequent basis, and SG level was allowed

to vary over a wider range before refilling. Establishing flow through the MS18

valves increased the steaming rate of the SGs, thereby increasing the required

frequency of providing feedwater to the SGs to maintain water levels. The MS18

valves were opened approximately 1 to 2 % of valve open position. The increased

steaming rate required the starting of the AFW pumps approximately once per 12

hour shift in order to maintain SG levels.

On February 20, the night shift further opened all MS18 valves to approximately

4% valve open position. The SGs were filled to greater than 33% narrow range

level at 4:51 a.m. on the morning of February 21. The additional ste.am demand,

which caused water levels to fall at an increased rate, was not anticipated by the

on-coming day shift. In addition, prior to the event, SG water level narrow range

chart recorders and SG water level program deviation console alarms on control

console 2 were inoperable due to Advanced Ditigal Feedwater Control System

testing which was in progress. The Unit 1 reactor operator (RO) logged 14 SG

narrow range level at 32 % at 7:30 a.m. At 1 :30 p.m., while performing shiftly

logs, the RO noticed 14 SG level to be 12%. The RO was about to start the AFW

pumps and refill the SGs just as the automatic action occurred. At 1 :32 p.m., the

11 and 12 AFW pumps automatically started on Lo-Lo SG level when 14 SG water

level reached 9% narrow range level. Operators promptly established feedwater to

all SGs to restore water levels. At the time of the event, the 11, 12, and 13 SG

water levels were 21 % , 31 % , and 32% respectively. The 14 SG narrow range

. level dropped from 36% to 9% in approximately 8.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.

Licensee evaluation of the event determined that the cause was human error. The

two ROs on duty, and the control room supervisor did not adequately monitor SG

water levels nor did they anticipate the increased feedwater requirements. A

contributing cause was ineffective shift turnover and poor team communication.

Although the additional steam demand on the SGs was discussed during the

individual watch turnovers, the subject was never discussed at the pre-watch shift

brief nor did the Unit 1 control room crew discuss any increased monitoring of SG

water levels. The operating crew also did not discuss what SG water level should

be maintained. The RO was unsure as to what level range was to be maintained in

3

the SGs. Guidance provided in procedure S1 .OP-SO.AF-0001, "Auxiliary Feedwater

System Operation," and S1.0P-IO.ZZ-0002, "Cold Shutdown to Hot Standby,"

required level be maintained between 28-38%. Levels in the 11 and 14 SG were

allowed to go below this level.

The licensee's corrective actions included discussion of lessons learned lead by the

two ROs involved in this event. Also, an emphasis of responsibilities and the

importance of safe operations was reinforced by the Operations Superintendents

and reviewed with the operating crews. Also, the chart recorders and alarms were

returned to operable status on February 21 .

The inspectors discussed this event with the .individuals involved and reviewed the

licensee's corrective actions and found them acceptable. - The safety significance of

this event was minimal because the SGs were not being relied upon for decay heat

removal. At the time of the event, core cooling was being provided by the 11

residual heat removal loop. Therefore, this licensee identified and corrected

violation for failure to follow procedure.s for maintaining SG levels is being treated

as a Non:.cited Violation consistent with Section Vll.B.1 of the NRC Enforcement

Policy. (NCV 50-272/98-01-01)

c.

Conclusions

Licensed operators' inadequate monitoring of plant parameters and maintenance of

steam generator levels, combined with inadequate communications and crew

teamwork resulted in an inadvertent automatic start of the auxiliary feedwater

pumps when the 14 steam generator level decreased to 9%. The reactor operator

did not follow procedure requirements to maintain the steam generator levels within

the required band.

04

Operator Knowledge and Performance

04.1

Inattentive Control Room Supervisor

a.

Inspection Scope

b.

At about 4:30 p.m. on March 11, 1998, during observation of a Unit 2

startup/reactivity briefing which was conducted in the conference room adjacent to

the control room, the inspector noted that a control room supervisor (CRS) was

having difficulty staying awake and appeared inattentive. The inspector informed

the Operations Manager of the observed condition of the CRS. Licensee

management took actions to address this condition, as discussed below.

Observations and Findings

The Operations Manager took prompt corrective action by suspending the briefing

and initiating an investigation (AR 980311292). The CRS was relieved from his

4

duties and tested for Fitness for Duty (FFD). The test results were negative, he

was coached about the serious negative perception of his alleged actions, and

returned to work the following day. Licensee investigation did not confirm that he

was inattentive, but did determine that he was apparently tired at the briefing.

Further licensee review determined that the CRS had worked six - 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> shifts

the previous week and that March 11 was his ninth -12 hour day out of the

previous 10 days. Although, this is within the licensee's overtime guidelines

described in procedure, NC.NA-AP.ZZ-0005, "Station Operating Practices," (NAP

5), as a corrective action, licensee management stated that General Manager

approval would now be required for any individual scheduled to work greater than

60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br /> in a week and this requirement would be proceduralized in NAP 5. The

intent of these actions was to minimize the impact of working excessive hours on

employee quality of life and fitness for duty ..

The inspectors questioned the extent of other operations personnel working

excessive hours. In response, the licensee initiated an audit of operations

department personnel work hours and identified several instances since January

1998 of licensed senior reactor operator's (SRO's) gate-to-gate times exceeding 72

hours in a seven day period. In addition, long turnovers were resulting in

consecutive 13 to 14 hour1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br /> work days. NAP 5 guidance is that an individual should

not be permitted to work more than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> in any seven day period, excluding

shift turnover time. The inspector questioned the gate-to-gate times for two SROs,

whose times in a seven day period were 83 and 87 hours0.00101 days <br />0.0242 hours <br />1.438492e-4 weeks <br />3.31035e-5 months <br />. After further review,

licensee management stated that these individuals had met the requirements of

NAP 5, because they had worked 6- 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> shifts during the periods in question,

and that the hours over 72, were the result of long turnovers. The licensee initiated

AR 980318079 to document and evaluate the results of their audit and the

corrective actions taken. Licensee management strongly stated that the results of

this audit did not meet their expectations for individual work hours and that

additional audits were being conducted to further unoerstand the extent of this

condition.

c.

Conclusions

The licensee's corrective actions to address the reasons for an apparently fatigued

licensed control room supervisor were acceptable. However, there were some

weaknesses identified in licensee management oversight of individual employee

work hours which the licensee has initiated actions to address.

08

Miscellaneous Operations Issue

0.8.1. (Closed) LER 50-311 /98-04: Failure to Comply with Technical Specification

Surveillance Requirement 4.1.3.1.1.

On February 4, 1998, the rod position deviation monitor was declared inoperable

when it was determined that the Plant Processing Computer System (P250) was

f

5

not updating the. rod position deviation computer data point "RODD EV". The

"RODDEV" data point provides the input to an overhead alarm window which

automatically alarms when the rods deviate beyond the required number of steps

from the group demand counter. This computer point is the rod position deviation

monitor required by Technical Specification Surveillance Requirement 4.1.3.1.1. On

November 21., 1997, the computer point was disabled, apparently without

informing the control room personnel. Since the operators were not aware that the

rod position deviation monitor was inoperable, control rod positions were not

verified every four hours as required by Technical Specification 4.1.3.1.1, however,

they were verified once per shift. The licensee concluded that the apparent cause

of the event was attributed to human error. Corrective actions associated with this

event consisted of a lesson learned discussion and the implementation of periodic

reviews of the P250 computer points to ensure Technical Specification associated .

points are not disabled.

Based *an the minimal safety significance of this condition, the inspector performed

an in-office review of the information provided in this LER. The inspector found the

licensee's root cause and corrective actions discussed to be acceptable. Therefore,

this licensee identified and corrected violation of Technical. Specification

Surveillance Requirement 4.1.3.1.1 is being treated as a Non-Cited Violation

consistent with Section Vll.B.1 of the NRC Enforcement Policy. (NCV 50-311/98-

01-02)

0.8.2 (Closed) LER 50-311/98-05: Technical Specification Required Shutdown of Salem

Unit 2 Due to the Failure of the 2A Emergency Diesel Generator Turbocharger.

This LER documents the February 11, 1998 controlled shutdown of Salem Unit 2 as

required by Technical Specification 3.8. 1.1, following the failure of the 2A

emergency diesel generator (EOG) turbocharger. Since the licensee's root cause

analysis and corrective actions for this event were previously reviewed and

documented in Section M8.1 of this report and Section E.7.2 of NRC Inspection

Report 50-272 & 311 /98-81, the inspector performed an in-office review of this

  • LER. The inspector found that no new information was provided and that no

additional inspection effort was warranted; Therefore, this LER is closed.

II. Maintenance

M1

Conduct of Maintenance (50001, 62707, 61726, 92902, & 40500)

M 1 . 1 General Comments

The inspectors observed all or portions of the following work activities and

Technical Specification surveillance tests:

W/O 950606013:

13 AFP Overspeed Trip Test

6

W/O 970916012:

21 EDG Lube Oil Heater Clean and Inspection

W/O 971006167:

Replace 2PR3

W/O 970818068:

Replace 2PR4

. W/O 971006167:

Repair 22 SG Steam Flow Channels (2FT523

and 2FA3472)

W/O 980131065:

2C EDG Watt Meter Transducer Replacement

W/O 980205085:

2B EDG Reliability Run While 2C EDG Inoperable

W/O 970120269:

2A EDG Lube Oil Cooler Jacket Water Heat

Exchanger dp Transmitter Work

W/O 980301186:

Inspect 23 Service Water Strainer

W/O 980301188:

Inspect 21 Service Water Strainer For Possible

Bypass

S2.0P-ST.SJ-0001:

Safety Injection Pump lnservice Test

S2.0P-ST.DG-001:

2A EDG Surveillance Test

SC. CH-CA.ZZ-0325:

Boron Sample by Titration of RWST Sample

S1 .RA-ST.SJ-0002:

12 Safety Injection Pump lnservice Testing

The inspectors observed that the plant staff performed the maintenance effectively

  • within the requirements of the station maintenance program, and that the plant

staff did surveillances safely, effectively proving operability of the associated

system. Minor deficiencies noted by the inspector during .. the performance of the

refueling water storage tank boron sample and analysis were promptly corrected by

the licensee.

M1 .2 Wrong Control Switch Installed on 12 Diesel Fuel Oil Transfer Pump

a.

Inspection Scope

b.

The licensee discovered during the 31-day surveillance run of the 12 Diesel Fuel Oil

Transfer Pump (DFOTP) on February 19, 1998, that the pump would not start in

automatic when required to do so. Troubleshooting revealed that the wrong control

switch was installed on the pump. The inspector followed up on this self-revealing

event through personnel interviews and documentation review.

Observations and Findings

The licensee replaced a degraded control switch for the 12 DFOTP on January 30,

1998. .On February 19, 1998, while performing the 31-day surveillance run on the

pump, it would not start in automatic control when the fuel oil day tank dropped to

the appropriate level. Troubleshooting revealed that the wrong control switch was

installed on January 30, which prevented the automatic start of the pump,

rendering it inoperable. Unit 1 was in Mode 5 at the time the wrong switch was

installed on January 30. Technical Specification (TS) 3.8.1.2 requires one of the

two DFOTPs to be operable in Mode 5. However, the licensee entered Mode 4 on

February 18 at 8:35 a.m., and TS 3.8.1.1.b.2 requires two DFOTPs to be operable

in Mode 4. The 12 DFOTP was restored to operable status on February 20 at 2:31

c.

7

a.m. The licensee's ascension to Mode 4 with one of two DFOTPs inoperable was

a violation of TS 3.8.1.1.b.2.

(VIO 50-272/98-01-03)

The inspector determined that there were multiple failures which caused this event.

The Planning Department listed the wrong part number for the control switch on the

work order (WO) and staged it for the work. Additionally, the WO listed the wrong

print number for the electrical panel where the switch is located, and listed another

print which does not exist. The post-maintenance test (PMT) was inadequate in

that it did not test the automatic start feature of the pump. The PMT described on

the WO was not specific, and operations and maintenance personnel did not

question its adequacy.

The technician who performed the work did not verify the correct switch part

number when replacing the switch. Also, he did not recall having the appropriate

electrical drawings at the work site per management expectations, and did not

verify proper operation of electrical contacts controlled by the switch after the work

was done. Any of these actions would have revealed that the wrong control switch

was installed.

The licensee's immediate corrective actions for this event were weak. A technician

documented on February 19 that he had verified that the other three DFOTPs had

the correct control switches. However, the 2A EOG was protected at the time due .

to maintenance on another EOG, so he did not verify the 21 DFOTP .. He

remembered this omission on February 27 and checked it for the correct control

switch. He discovered that this DFOTP also had the wrong part number. This

switch had been replaced in January 1994 with the wrong part number, but had

passed all surveillance tests (STs) since then. The licensee did not know how the

21 DFOTP control switch was placed in its present configuration with the wrong

part number. However, the switch appeared to function as designed.

Initially, there was no analysis performed to verify operability of the 21 DFOTP

control switch for this abnormal configuration. Rather the licensee concluded that

the 21 DFOTP was operable since it had passed all STs. The inspector brought this

issue to management's attention on March 12, 1998. The Operations Manager

stated that the 21 DFOTP was operable and the licensee ascended to Mode 1 on

March 14 with no documented operability determination (00). Subsequently, the

licensee performed an OD on March 16, which the inspector concluded was

adequate, but not timely. Additionally, the licensee did not verify correct part

numbers for the remaining six control switches on each DFOTP electrical panel,

three of which have the same control switch as the DFOTP, until questioned by the

inspector.

Conclusions

Poor planning and inadequate maintenance practices resulted in an incorrect control

switch being installed on the 12 Diesel Fuel Oil Transfer Pump (DFOTP), which

- ----

  • -* ----------------------------------

8

rendered the 12 DFOTP inoperable. The licensee ascended to Mode 4 on Unit 1

with less than the required DFOTPs operable, which was a Technical Specification

violation. The licensee's immediate corrective actions for this event were weak,

including an untimely operability determination for the wrong part being installed on

the 21 DFOTP, and untimely verification of correct part numbers for similar control

switches on the four DFOTP electrical panels.

M1 .3 Post-Maintenance Testing of 2A Emergency Diesel Generator after Turbocharger

Failure

a.

Inspection Scope

b.

The inspector followed up on licensee post-maintenance testing (PMT) activities on

the 2A EOG following the February 11, 1998 turbocharger failure.

Observations and Findings

On Thursday, February 19, 1998~ maintenance personnel were completing

maintenance activities on the 2A EOG in accordance with procedure SC.MD-ST.DG-

0003, "Eighteen Month Diesel Engine Inspection Maintenance." The maintenance

supervisor ordered technicians to close the EOG petcocks in preparation for

returning the diesel to operation. Although the technicians stated that they closed

the petcocks, this was not documented in step 5.17.4 of the procedure, as

required.

On Friday, February 20, 1998, operations personnel barred the diesel over in

accordance with procedure SC.OP-PT.DG-0001, "Diesel Generator Manual* Barring,"

in preparation for running the engine. This procedure requires the diesel petcocks

to be open for barring and closed for running the engine. Nuclear equipment

operators signed off the procedure indicating that the petcocks were closed ~nd

independently verified (IV'd) as such. But when the diesel was subsequently

started, the petcocks were found open because the operators did not understand

how to properly position the petcocks.

On Sunday, February 22, 1998, at 1 :35 a.m. operators started the 2A EOG in

accordance with procedure S2.0P-ST.DG-0001, "2A Diesel Generator Surveillance

Test" for an operability and 24-hour surveillance run. During the run, a

maintenance engineer noted a strange sound coming from the left side of the

engine. The operator checked engine cylinder temperatures and noted that the 5-

Left cylinder temperature indicated that it was not firing. Further investigation

revealed that the 5-Left cylinder fuel pump was locked out. All other cylinders were

checked with no discrepancies noted. The 5-Left cylinder was restored and the 2A

EOG run was completed successfully.

Step 5.17 .9.M of the above mainten!3nce procedure requires that cylinder fuel pump

racks be checked unlatched (not locked out) and IV'd* as such. Procedure review

9

showed that the IV line was signed off, but not the initial check. Interviews with

the technicians revealed that ttie initial* check was completed but not signed off,

and no IV was completed, but was signed off. Additionally, the maintenance

supervisor signed the procedure without recognizing that the step 5.17.9.M initial

check was not signed off.

The licensee took immediate corrective actions for the open petcock and cylinder

lock-out issues, including stopping work to remediate personnel involved, and

reviewing lessons learned with all maintenance personnel the week following the

errors. The licensee is also planning other long-term corrective actions to address

these issues.

In the above instances, maintenance and operations personnel failed to comply with

station procedures for the control of safety-related systems. These licensee

identified failures are a violation of TS 6.8.1 which requires that written procedures

be implemented for safety-related equipment recommended in Appendix "A" of

Regulatory Guide (RG) 1.33, Revision 2, February 1978. This RG recommends that

written procedures be implemented for control of EDGs. (VIO 50-311/98-01-04)

c.

Conclusions

Procedural adherence for the 2A Emergency Diesel Generator post-maintenance

testing was poor. Numerous procedural violations by maintenance a_nd operations

personnel resulted in the improper operation of the diesel. There was little safety

significance to these violations as the diesel was out of service for maintenance.

However, they showed a lack of questioning attitude and attention to detail by

numerous personnel. Additionally, the engineering action plan utilized for the

maintenance effort was not sufficiently detailed to promote smooth transition

between the maintenance and operations procedures used.

M2

Maintenance and Material Condition of Facilities and Equipment

M2. 1 High Crankcase Pressure Alarm on the 28 Emergency Diesel Generator During a*

Technical Specification Required Run

a.

Inspection Scope

The inspector observed the February 3, 1998 run of the 28 EOG, which was *

required by TS 3.8.1.1.b due to the 2C EOG outage for maintenance. The 28 EOG

was shut down when the "Crankcase Blower Failure" alarm was received. The

inspector followed up on this shutdown, the trouble-shooting of the cause of the

alarm, and the post-maintenance EOG run after the problem was corrected ..

10

b.

Observations and Findings

On February 3, 1998, licensee operators were running the 28 EDG to satisfy TS 3.8.1.1, action b, since the 2C EDG was out of service for maintenance. The 2C

EDG maintenance placed Unit 2 in a 72-hour shutdown action statement and

required running the 2A and 28 EDGs to show reliability. Approximately 13

minutes after the diesel was fully loaded, the "Crankcase Blower Failure" alarm was

received. The operator correctly carried out the alarm response procedure and

attempted unsuccessfully to reset the alarm. Therefore, the 28 EDG was shut

down and declared inoperable by the Control Room Supervisor, who was observing.

the diesel run. This placed the plant in a two-hour shutdown action statement, due

to the inoperability of two diesels.

After the diesel was shut down, the operator again attempted to reset the alarm

and this time was successful. Subsequent investigation revealed that the three-

way root valve for the crankcase pressure switch had apparently vibrated out of

position, porting air manifold pressure to the switch instead of crankcase pressure.

Crankcase pressure is normally at vacuum, while air manifold pressure is at a

vacuum with the diesel unloaded or lightly loaded, but at pressure when the diesel

is loaded. This caused a false high crankcase pressure indication. The three-way

valve was positioned correctly, and the 28 EDG was re-started with a Heise

pressure gage connected to read crankcase pressure. This gage indicated normal

pressure (about -1.2 inches we) for the remainder of the run and no more alarms

were received. The 28 EDG was declared operable approximately 13 minutes

before the two-hour action statement expired.

The inspector questioned the Operations Superintendent concerning his operability

determination. The OS declared the diesel operable after 20 minutes of the one-

hour surveillance run after the pressure switch problem was corrected. He stated

that since the alarm was received 13 minutes after the diesel was fully loaded, and

that he was confident that the problem was corrected, he could declare the diesel

operable after a similar amount of time (20 minutes) of a loaded run, once he had

verified that the crankcase pressure was satisfactory. The Operations Manager

concurred with that decision, and further stated that if other problems arose during

the remainder of the one-hour run, that he would have used the original failure time

(not the time the diesel was declared operable) to calculate time available before

plant shutdown was necessary. The inspector concluded that these actions were

satisfactory.

The inspector also questioned the OS concerning the timing of the 28 EDG

reliability run. At the time of the run, the 2C EDG was out of service for on-line

maintenance, which placed the plant in a 72-hour action statement, and which

required the licensee to run the remaining two diesels within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of declaring

the 2C inoperable. The 2A EDG was successfully run prior to taking the 2C EDG

  • out of service. However, the 2C EDG was taken out of service at approximately

6:00 a.m. and was scheduled to be out of service for about 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />. The

11

inspector questioned why the 28 was run at 11 :00 a.m. that same morning instead

of waiting until work was completed on the 2C. The OS stated that he was fully

confident that the 28 EDG was operable and he did not anticipate any problems

with running it. The inspector concluded that, based on the intended outage time

of the 2C EDG, that it would have been more appropriate to run the 28 EDG before

the 2C was taken out of service.

The inspector asked the diesel system manager if the crankcase pressure switch

was required to be calibrated. He stated that it was calibrated every three years,

but that due to the present operational schedule, the calibration had been deferred

from November 1997 to the next refueling outage in January 1999. The system

manager stated that he intended to move the calibration of the switch up to the

summer of 1998. The inspector concluded that since the pressure switch provided

an alarm function only, and not a protective function, that the calibration deferral

was acceptable.

c.

Conclusions

The licensee met all Technical Specification requirements for the 2C emergency

diesel generator (EOG) outage and the crankcase alarm on the 28 EDG. The

operator correctly followed the alarm response procedure for the 28 EDG alarm.

The operability determination for the 28. EDG after the cause of .the alarm was

determined was adequate, but the decision to run the 28 EDG during. the 16-hour

2C EDG outage was not appropriate.

MS

Miscellaneous Maintenance Issues

MS. 1 2A Emergency Diesel Generator Turbocharger Blade Failure

a.

Inspection Scope

b.

Approximately 44 minutes into a post-maintenance test on February 11, 1998, the

Unit 2, 2A emergency diesel generator (EDG) turbocharger failed. The licensee

formed a team to get the relevant facts, find the cause of the failure, evaluate its

significance relative to the operability of the other EDGs, and establish corrective

actions. In the month after the failure, the NRC resident inspector sampled the

work of the team and a regional based engineering inspector met with team

members to review the scope of activities of the team and its conclusions.

Observations and Findings

The turbocharger failure occurred when one rotating blade on the engine exhaust

gas input side of the ~urbocharger broke loose subsequent to fatigue cracking of the

blade where it was mechanically rooted in the rotor assembly.

The team, formed

to evaluate the failure, included in its scope: an examination of the diesel engine

internals to verify that no engine components had been exhausted into the

..

12

turbocharger; review of the history of the turbochargers on each Salem EDG;

review of previous industry turbocharg*er failures; metallurgical and chemistry

analysis on the blades and debris; dynamic factors, event facts, root cause and

change analysis; and turbocharger service life. By March 12, 1998, most of the

evaluation work of the team was complete, but the analysis of the dynamic factors

that may or may not have led to the failure was in progress by an industry expert

on turbines. In summary, the team conducted an extensive evaluation of the

failure.

c.

Conclusions

On February 11, 1998, the Unit 2 emergency diesel generator (EDG) turbocharger

failed during a post-maintenance test. The licensee formed a team to get the

relevant facts, find the cause of the failure, evaluate its significance to the other

EDGs and establish corrective actions. The NRC reviewed the evaluation scope,

methods and results. This NRC inspection concluded that the preliminary root

cause evaluation of the failed turbocharger blade was thorough, detailed, and

accurate~ The inspector concluded that the licensee had properly responded to the

EDG turbocharger failure by initiating a thorough evaluation.

M8.2 (Closed) LER 50-272/96-05; Supplements 6 through 16: Technical Specification

Surveillance Requirement Implementation Deficiencies

These supplemental reports documented additional findings of the Technical

Specification Surveillance Improvement Program (TSSIP), the licensee's long-term

corrective action plan for surveillance testing deficiencies originally described in LER 96-005. The TSSIP project was initiated for Salem station as part of the corrective

actions taken by PSE&G regarding surveillance deficiencies identified at Hope Creek

(reference violation 50-354/95-11-02). Although these reports identified different

surveillance requirements that were not appropriately implemented for ensuring

technical specification requirements were met, the licensee took timely corrective

action, demonstrated operability of the required equipment in each case, and

provided adequate bases that no safety consequences resulted from the testing

inadequacies. The associated root caus'e for these supplemental reports were the

same as for supplemental reports one through five and constituted a violation of

NRC Test Control requirements per 10 CFR 50, Appendix 8, criterion XI. However,

based on licensee identification and action taken to correct these deficiencies, this

violation is being treated as a non-cited violation consistent with Section VII of the

NRC Enforcement Policy. (NCV 50-272 & 311/98-01-05)

These minor issues were closed based on an in-office review of the licensee-

provided information. However, the inspector also reviewed selected testing

procedures to verify the licensee had implemented adequate procedural changes to

address the deficiencies, as detailed in the LER. *No discrepancies were identified .

..

13

The inspector noted that PSE&G prioritized and completed their actions in response

to Generic Letter (GL) 96-01, "Testing of Safety-Related Logic Circuits" as

described in their letters to the NRC dated April 16, 1996, and January 15, 1998,

as part of the TSSIP. As the licensee stated in their letter dated January 30, 1998,

these implementing procedures related to GL 96-01 review were completed for both

Salem Units 1 and 2. Additionally, PSE&G appropriately assigned the next highest

priority to technical specification procedures associated with relatively high risk

surveillances and safety-related systems and the lowest priority to those procedures

with relatively low risk surveillances and nonsafety-related systems. Further, the

inspector noted that the licensee extended their commitment to complete their

review of the remaining procedures from December 1997 to May 1998. However,

the licensee stated that the higher priority procedures would be completed prior to

Unit 1 restart/entry into Mode 2. At the time of this inspection the licensee had

completed their review of 1, 185 of the 1,293 (92%) technical specification

implementing procedures. Based on the minor significance of all of the identified

procedural deficiencies for both Units 1 and 2 as well as those enveloped by the

Hope Creek TSSIP program, the inspector .determined that the risk associated with

restarting Unit 1 without completion of the lower priority procedure review was

minimal and acceptable.

Ill. Engineering

E1

Conduct of Engineering (Tl 2515/109, 37551, 40500 & 92903)

E1 .1

Generic Letter 89-10 Motor-Operated Valve Program Review and (Closed) NRC

Programmatic Restart Issue 111.a.23: Adequacy of Motor-Operated Valve Program

(Unit 1)

a.

Inspection Scope

On June 28, 1989, the NRC issued Generic Letter (GL) 89-10, "Safety-Related

Motor-Operated Valve Testing and Surveillance," requesting licensees to establish a

program to ensure that switch settings for safety-related motor-operated valves

(MOVs) were selected, set, and maintained properly. Seven supplements to the GL

have been issued to provide additional guidance and clarification. NRC inspections

of licensee actions implementing the provisions of the GL and its supplements have

been conducted based on the guidance provided in NRC Temporary Instruction

2515/109. The most recent inspection of MOV activities at Salem was

documented in IR 50-311/97-03, dated April 3, 1997, when the NRC's review of

the GL 89-10 program for Salem Unit 2 was closed (Unit 1 was not inspected).

The purpose of this inspection was to review the actions implemented at Salem

Unit 1 to closeout programmatic restart item 111.a.23 and determine if those actions

were sufficient to warrant closure of the NRC staff's review of the GL 89-10

program. Since the MOVs for both Salem Units are similar, the inspection focused

b.

14

on any performance differences between the Unit 1 and 2 MOVs, and included. the

review of:

1.

Specific MOV issues experienced during the Salem Unit 2 review.

2.

Load sensitive behavior, stem friction coefficient, and degradation margin.

3.

Specific MOV problems encountered at Salem Unit 1.

4.

Thrust margin improvement plans.

5.

Measures to monitor industry actions regarding operator and motor

performance.

6.

Licensee's actions regarding existing MOV open items for Salem Unit 1.

The inspectors reviewed PSE&G'S-l-VAR-NEE-1266, "Generic Letter 89-10 Closure

Summary for. the Motor Operated Valve Program As Implemented at Salem Unit 1,"

Rev. 0, and documents associated with all MOVs in the GL 89-10 program. The

closure summary document was in draft stage during the initial onsite inspection. It

was completed on February 1, 1998, and further reviewed in-office by the

inspectors. In addition to the onsite visit of January 15 and 16, 1998, comments

on the closure summary document were discussed on several instances afterwards

during a conference call on February 4, 1998, and most recently on March 4, 1998.

The findings discussed below refer to Revision 0 of the closure summary document

although PSE&G had issued Revision 1 to address the inspectors' comments. The

inspectors also referred to the similar document, S-C-VAR-NEE-1117, Revision 1,

"Generic Letter 89-10 Closure Summary for the Motor Operated Valve Program As

Implemented at Salem Unit 2," that had been used as a basis for the closeout of

the Salem Unit 2 MOV program.

Observations and Findings

Two main program documents govern MOV activities at Salem. These documents

are (1) Programmatic Standard NC.DE-PS.ZZ-0033(0) which includes many.

appendices providing details for design basis reviews, MOV capability assessments,

etc; and (2) Program Position Papers EE:A-O-ZZ-MEE-0609 which provide licensee

positions on many MOV technical issues such as temperature effects* on motor

  • performance. The inspectors confirmed that significant changes had not been made

to these MOV program documents. Essential program elements, such as the

definition of MOVs in the program scope, tracking and trending of MOV

performance, and post maintenance practices, were in place at Salem Unit 1 similar

to that observed during the Salem Unit 2 review. The inspectors verified that the

residual heat removal discharge-to-hot leg isolation valve, 1 RH-26, had been added

to the MOV program scope and had been dynamically tested. The comparable

15

valve, 2RH-26, had also been added to the GL 89-10 MOV program at Salem

Unit 2. There were no other MOV program scope changes.

PSE&G dynamically tested about 50% of the 95 MOVs in the GL 89-10 program at

Salem Unit 1 . PSE&G provided information for the 95 MOVs which were grouped

into 16 MOV families. The inspectors reviewed the following MOV families where

specific issues had been discussed during the closeout review of the Salem Unit 2

MOV program.

Specific MOV Issues Experienced During the Salem Unit 2 Review

Family 6: 14" Copes Vulcan 2500 psi Parallel Double Disk Gate Valves

This family consisted of the reactor coolant system (RCS) hot leg to residual

heat removal (RHR) suction header valves (1 RH1 and 1 RH2). The

  • comparable valves (2RH 1 and 2RH2) had been discussed during the MOV

program review at Salem Unit 2. Specifically, PSE&G revised its initial 0.55

valve factor basis for these valves to 0.61 which was based on the

maximum value of valves tested at Salem Unit 2. This was considered

acceptable for GL 89-10 program closure based on PSE&G's commitment to

pursue an improved valve factor basis for these valves as part of their

periodic verification program.

For Salem Unit 1, PSE&G continued to assume a valve factor of 0.61 for

these valves. Using a design basis differential pressure (DBDP) condition of

381 psid, a stem friction coefficient of 0.20, actuator pullout efficiency, and

a 212°F environment for the actuator temperature to determine motor

performance, PSE&G calculated a thrust margin of 16% and 11 % for 1RH1

and 1 RH2, respectively. In pursuing an improved valve factor basis as part

of the periodic verification program, PSE&G agreed to use the Electric Power

Research Institute (EPRI) Performance Prediction Methodology (PPM). Also,

efforts would continue with other reactor facilities to seek valve factor

information regarding these valves. The plan to further assess these valves

was included in the licensee's corrective action program by revising an

existing Action Request 970418119 which had been issued to address the

issues from the Salem Unit 2 MOV program review. The inspectors

considered PSE&G's actions acceptable for restart. An inspector Followup

Item (IFI 50-272/98-01-06) is opened to verify implementation of this action

for GL 89-10 program closure.

Family 9: Power Operated Relief Valve (PORV) Block Valves (1 PR6 and

1 PR7)

PSE&G modified the Salem Unit 2 PORV block valves to operate them based

on limit switch control, and thereby take advantage of full actuator motor

capability for valve closing. A similar modification has been accomplished

16

for the Salem Unit 1 valves. PSE&G calculated the thrust margin to be 19%

and 8% for 1PR6 and 1PR7, respectively, based on a DBDP of 2510 psid, a

0.61 valve factor, a 0.20 stem friction coefficient, and using actuator pullout

efficiency in demonstrating design basis capability. (Note: Similar parameters

were used during the Salem Unit 2 review.)

In following up on an issue discussed during the Salem Unit 2 review,

PSE&G acknow.ledged that they had not fully addressed the NRC request

regarding the adequacy of the valve factor basis and any non-predictability

for these valves. Internal dimensions had been taken for the Salem Unit 1

valves to assist in determining the valve predictability and thrust

requirements at both Salem Units in accordance with the EPRI PPM.

However, since this dimensional information had not yet been translated into

a calculation of a design standard valve factor according to the EPRI PPM,

PSE&G intends to complete these calculations (Action Request 970418119).

PSE&G stated preliminary calculations indicated that there were no

nonpredictability concerns for these valves. The inspectors considered

PSE&G's actions acceptable for restart. IFI 50-272/98-01-07 will include

verification of licensee completion of these calculations for GL 89-10

program closure.

Family 9: Reactor Coolant Pump (RCP) Thermal Barrier Isolation Valves

(1CC131 and 1CC190)

Both RCP thermal barrier* isolation valves reviewed during the Salem Unit 2

inspection demonstrated positive thrust margins, with valve 2CC131 the

least at 8% using torque switch control in the closed direction. While this

was considered acceptable for GL 89-10 closure, PSE&G plans to take

measures to improve the actuator capability for these MOVs. PSE&G also

plans to confirm the adequacy of the valve factor basis and to evaluate any

non-predictability for these valves as part of the Salem Unit 2 periodic

verification program.

Both RCP thermal barrier isolation valves at Salem Unit 1 were modified in

accordance with design change DCP lEE-0368 to operate under limit switch

control to improve their design basis capability. A similar modification will

be implemented at Salem Unit 2 during the next refueling outage. Based on

  • a DBDP of 2241 psid, a 0.61 valve factor, a 0.20 stem friction coefficient,

and using actuator pullout efficiency in demonstrating design basis

capability, PSE&G calculated a thrust margin of about 30% for the Salem

Unit 1 valves which was acceptable.

In following up on an issue discussed during the Salem Unit 2 review (similar

to the discussion above for 1 PR6 and 1 PR7), PSE&G acknowledged that

they had not fully addressed the NRC request regarding the adequacy of the

valve factor basis and any non-predictability concerns for these valves.

17

Accordingly, PSE&G plans to complete calculations using the EPRI PPM to

evaluate these issues (Action Request 970418119). PSE&G stated

preliminary calculations indicated that there were no non-predictability

concerns for these valves. The inspectors considered PSE&G's actions

acceptable for restart. IFI 50-272/98-01-07 wiil include verification that the

calculations were completed for GL 89-10 program closure.

Load Sensitive Behavior, Stem Friction Coefficient, and Degradation Margin

The Salem Unit 2 Closure Summary included a statistical analysis of 75 data points

and determined an average load sensitive behavior of 3. 7% with an associated

standard deviation of 9.6%. To properly account for load sensitive behavior,

PSE&G's error analysis added 4% error in thrust calculations directly as a bias

margin, and an additional 21 % error as a random value that was included with

other uncertainties using the square root sum of the squares method. Also, PSE&G

had co.mpleted a comprehensive stem friction coefficient review of the results from

in-plant testing to justify the use of a stem friction coefficient value of 0.20 and

revised their setup methods to include a 5% bias margin to account for

degradations as a part of their standard error analysis. The results of the analyses

for load sensitive behavior, stem friction coefficient, and degradation margin were

included in the Salem Unit 2 Closure Report (S-C-VAR-NEE-1117, Revision 1) as

Attachments 19, 20, and 21, respectively.

The additional data obtained from Salem Unit 1 testing done during the past year

was factored into updated analyses for load sensitive behavior, stem friction

coefficient, and degradation margin. This data supported the Salem Unit 2 data and

did not invalidate any of the conclusions. It was included in similar Attachments to

the Salem Unit 1 Closure Report (S-l-VAR-NEE-1266) where PSE&G concluded that

the margins allocated for load sensitive behavior (4% as a bias and 21 % as a

random value) and degradation (5% as a bias) and the stem friction coefficient

value of 0.20 for the Salem Unit 1 MOVs should be the same as that established

for the Salem Unit 2 MOVs. Where stem friction coefficient values just above 0.20

were experienced for 1CC118 (0.21) and 12CC3 (0.22) during recent differential

pressure testing, PSE&G plans to inspect and correct these conditions. It is noted

that these MOVs did demonstrate positive thrust margins.

The inspectors found this approach for addressing load sensitive behavior, stem

friction coefficient, and degradation margin to be acceptable for Salem Unit 1

restart. Inspector followup item (IFI 50-272/98-01-08) is opened to verify

. completion of the PSE&G actions regarding correction of the high stem friction '

coefficient values of 1 CC118 and 12CC3 as part of the licensee's MOV periodic

verification program being implemented per GL 96-05, "Periodic Verification of

Design-Basis Capability of safety-Related Motor-Operated Valves."

18

Specific MOV Problems Encountered at Salem Unit 1

Family 5: 6" Anchor Darling 150 psi Parallel Double Disk Gate Valves

The RCP bearing cooling water outlet containment isolation valves (1CC136

and 187) are six-inch Anchor Darling, double disk gate valves. (Note: During

the Salem Unit 2 review, PSE&G agreed to improve the thrust margin of

2CC136.) Both 1CC136 and 187 exhibited high closing forces during recent

dynamic testing at Salem Unit 1 .. Each valve failed to close during the initial

dynamic test on December 30, 1997, with the valves set at the as-found

torque switch settings. No similar failure-to-close problems were

experienced with the related 1 CC117 and 118 valves in this family although

1 CC117 did exhibit a higher than expected valve factor of 0.68 based on its

differential pressure test at 73% of design basis conditions. PSE&G plans to

. repeat this test during the next refueling outage.

Since the* component cooling water system had been de-chromated for an

extended period, corrosion products in the valve internals were attributed, in

part, to the poor performance. This parallel disk valve design is intended to

force the disks apart by the sliding action of angled upper (or fixed) and

lower disk (or floating) wedges (sometimes called wedge shoes). Valves

with the upper wedge located downstream of the flow (the non-preferred

direction) can require more thrust to achieve full wedging of the disk into its

seat. To enhance the valve performance, the wedge shoes for these valves

\\

in Salem Units 1 and 2 had been ~odified in the past year with stellite

hardfacing. The performance of 1CC187 was worse because its wedge

shoes were found installed in the non-preferred orientation. The wedge*

shoes for 1 CC 136 were oriented correctly.

Both valves were cleaned and installed correctly. Static and dynamic tests

were performed satisfactorily. The inspectors were concerned regarding the

long term performance of these and related (1 CC117 and 118) MOVs in this

family at Salem Units 1 and 2. To address these concerns, PSE&G plans to

do the following:

Unit 1: Issue action requests to perform differential pressure testing of

1CC117&118 at degraded voltage at the start of the next Unit 1 refueling

outage. Open and inspect the valv1es to verify correct wedge shoe

orientation. Expand the testing scope to 1CC136 and 1CC187 if there is a

significant change in valve performance.

Unit 2: Issue action requests to perform differential pressure testing of

2CC 117, 2CC 118, 2CC 136, and 2CC 187 at degraded voltage at the start of

the next Unit 2 refueling outage. Open and inspect the valves to verify

correct wedge shoe orientation if there is a significant change in valve

performance since the last differential pressure test.

. 19

The inspectors considered PSE&G's actions acceptable for restart. Inspector

followup item (IFI 50-272/98-01-09) is opened to verify completion of these

actions as part of the licensee's MOV periodic verification program being

implemented per GL 96-05.

Measures to Monitor Industry Actions Regarding Actuator Performance

The inspectors reviewed the licensee's measures taken and expected in response to

forthcoming information from Limitorque regarding the modification of previously

published actuator efficiencies. This subject had also been addressed in NRC

Information Notice 96-48, "Motor-Operated Valve Performance Issues."

As explained in Attachment 22, "Actuator Efficiency Evaluation," of the Salem

Unit 1 MOV program summary report, PSE&G has performed many differential

pressure tests at degraded voltage at Salem Units 1 and 2. This was done to better

characterize in plant motor performance under these conditions and to provide

assurance regarding their use of run efficiency in the closed direction for all torque

seated gate and globe valves. PSE&G indicated that it had reviewed the

information in NRC Information N-otice 96-48, it was monitoring industry

information for further developments, and any additional guidance issued on this

topic in the future by Limitorque would be reviewed and appropriate actions taken

in accordance with the Vendor Document and Corrective Action Programs.

Thrust Margin Improvement Plans

Inspector followup item 50-272/96-11-06 had been opened to review thrust margin

improvements needed for MOV 12CC16 (RHR heat exchanger component cooling

water outlet isolation valve) which previously evidenced a negative thrust margin at

design basis conditions. PSE&G has modified the control circuit to close this valve

under limit control. This action acceptably resolved the problem since the thrust

margin for the closing direction is currently about 17%.

The inspectors noted that several Salem Unit 1 MOVs were scheduled for margin

improvements. Although the following MOVs had adequate basis for the applied

thrust requirements, they had low thrust margins and were identified by the

inspectors to ensure that they were included in PSE&G's margin improvement

plans: 1CC118, 1 CC30, 1 PR7, and 1 SJ4.

The licensee was requested to review these MOVs and to include them as part of

their margin improvement program. PSE&G personnel agreed to conduct this

review. Closure of these MOVs under the GL 89-10 program was contingent upon

the licensee's agreement to improve the margin of these MOVs as part of Salem

Unit 1 's periodic verification program conducted per GL 96-05.

20

c.

Conclusions

PSE&G had adequately demonstrated design basis capability for Salem Unit 1

MOVs to support restart. Justifications for key program assumptions and the

applied valve factors were adequate to support closure of Restart Issue 111.a.23 for

Unit 1 . Regarding GL 89-10 program closure, PSE&G was requested to update and

clarify program summary S-l-VAR-NEE-1266, "Generic Letter 89-10 Closure

Summary for the Motor Operated Valve Program As Implemented at Salem Unit 1;"

consistent with the inspector followup items in this report.

E1 .2

Update on Control Area Ventilation System Issues

The Control Area Ventilation System (CAVS) is comprised of two subsystems: the

control area air conditioning system (CAACS) and the Control Room Emergency Air

Conditioning System (CREACS). When one train of CREACS is inoperable, the

CAVS cannot maintain the Technical Specification (TS) required 1 /8 inch water

column differential pressure (dp) between the control room and adjacent spaces.

As a compensatory measure, the licensee aligns CAVS in the "maintenance mode,"

wherein the adjacent spaces are vented* to atmosphere to maintain the required dp.

The licensee addressed two issues which prohibited two-unit operation while in the

maintenance mode. Engineering Evaluation (EE) S-C-CAV-MEE-1285, "Control

Room Ventilation-Radiological Contaminated Air Intrusion," was completed to

address the issue of a radiological cloud potentially entering the control room

adjacent spaces while in maintenance mode, which could affect control room

watchstanders. This evaluation confirmed that positive pressure in the adjacent

spaces from CAVS operation would prevent such an intrusion. Long-term

corrective actions to remove the necessity of maintenance mode are a TS change to

change the dp reference to the outside atmosphere instead of the adjacent spaces,

and ventilation equipment changes to increase the dp margin. The inspectors

concluded that the EE was adequate to address the radiological cloud issue.

The second issue concerned the Unit 2 Radiological Monitoring System (RMS)

inverter (power supply), which has a non safety-related battery backup. The CAVS

radiation monitors are powered from the inverter and would fail high if the inverter

was lost. This would open the CREACS air intakes on both Salem units, placing

control room personnel ;:it risk to adverse radiological conditions. The licensee

completed an operability determination for the inverter and is pursuing a design

change to provide a safety-related battery backup.

The inspectors concluded that these actions were adequate to address the two

issues mentioned. However, the long-term corrective actions mentioned above

were necessary to eliminate the need for maintenance mode. It is a time-

consuming, resource-intensive work around which ensures adequate dp margin

between the control room and the adjacent spaces. When this mode is employed,

then any circumstances which necessitate accident pressurized mode, such as an

21

inoperable CAVS radiation monitor, would require a unit shutdown to Mode 5 so

that the CREACS air intake could be lined up to a non-operating unit. This would

ensure that control room personnel dose limits are not exceeded during accident

conditions. The licensee stated that the TS change would be submitted to the NRC

within the next two weeks, and that ventilation equipment changes to increase the

dp margin are still under evaluation.

E2

Engineering Support of Facilities a_nd Equipment

E2.1

Service Water Biofouling and (Closed) LER 50-272/96~34

a.

Inspection Scope

b.

Several safety related and non-safety related service water (SW) cooled heat

exchangers (HX) experienced accelerated biofouling from marsh grass from the

Delaware River from January to March 1998. As a result, degraded plant.

conditions and in one instance, equipment inoperability occurred. The inspector

analyzed the events and the licensee's response to evaluate the effectiveness of

licensee controls to resolve this problem. The inspector also reviewed the

corrective actions specified for Licensee Event Report (LER) 50-272/96-34: service

water strainer design deficiency potentially outside design basis .

Observations and Findings

During the weeks of January 18 and 25, 1998, operators noted increasing

temperature trends on the Unit 2 turbine auxiliaries cooling (TAC) and main turbine

lube oil (MTLO) HXs. Operators also noted an increasing temperature trend on the

No. 3 station air compressor (SAC). Inspections cif the TAC, MTLO HXs and SAC

identified that the SW inlet tube sheets were clogged with river grass, which

resulted in degraded thermal performance.

On January 21, a differential pressure (D/P) test to monitor SW biofouling revealed

that the gear oil cooler exceeded the D/P limit across the HX for the 21 charging

pump. An internal inspection revealed that the inlet tube sheet was clogged with

river grass. However, SW flow through the HX was still above the minimum

required. The licensee initiated Action Request (AR) 980120280, and performed a

detailed self assessment to review the effectiveness of the SW reliability program.

Weaknesses in the licensee's response to this issue are discussed in NRC RATI

Inspection Report No. 50-272&311 /98-81, Section E4.

The self assessment revealed a lack of SW reliability program oversight that

resulted from the ongoing engineering department reorganization. Procedure

NC.NA-AP.ZZ-0039, Rev. 0, "Service Water Reliability Program," specifies that

Specialty Engineering is responsible for the implementation of the program, and that

a program manager is responsible for oversight, control, and technical. adequacy of

the program. Specialty Engineering no longer exists and no program manager was

22

assigned to ensure proper program implementation. PSE&G's commitments to

Generic Letter (GL) 89-13, "Service Water System Problems Affecting Safety-

Related Equipment," include a test program to verify the heat transfer capability of

all safety-related HXs cooled by SW. Temperature and pressure trending was

established for safety injection pump lube oil coolers, centrifugal charging pump

gear and lube oil coolers, SW pump motor coolers, and diesel generator jacket

water and lube oil coolers. Trending was not continued after the startup of Unit 2

in August 1997, since the SW reliability program manager assumed a new position

within the organization, and a new program manager was not assigned. The

licensee has assigned a new SW reliability program manager, and has delegated

trending responsibilities to the S~lem in-service testing program manager. In

addition to GL 89-13 commitments, the licensee established a SW biofouling D/P

test program in January 1998, based on industry guidance for monitoring of macro

biological fouling. At the time of inspection, only about. one half of the Unit 2

safety related HXs were D/P tested, and no Unit 1 HXs were tested. The licensee

determined, that the biofouling D/P monitoring program was not promptly

implemented.

On February 25, the 22 chiller tripped on high condenser pressure during

realignment of the control room ventilation system to normal operation. The

licensee initiated AR 980225270, and declared the chiller inoperable. Internal

inspection of the chiller condenser found river grass covering the inlet tube sheet.

Grass was also found in the chiller's recirculation pump discharge ch~ck valve,

22SW99, during a surveillance test performed one week earlier. As a result the

check valve failed its surveillance requirement. Further investigation revealed that

the chiller had passed its biofouling D/P test in January. Salem operations initiated

supplemental data logging of SW HX differential pressures after biofouling was

discovered in the 21 charging pump gear oil cooler. The inspector reviewed the

data logged by the equipment operators and noted that the SW inlet pressure

readings for the 22 chiller were being logged as failed due to clogging from river silt

since February 9. The inspector reported the data to system engineering, who were

unaware of the supplemental data. Although no requirement exists for .the logging

and evaluation of this data, the inspector concluded that a weakness existed in the

interface between operations and system engineering.

On March 1, the 21 charging pump gear and lube o'il coolers failed the biofouling

D/P test, after being in service for approximately 14 days following its D/P test

failure in January. Inspection of the coolers revealed that both were completely

clogged with river 'grass. The licensee initiated AR 980301138, which was

subsequently upgraded to significance level one to address all rec_ent SW biofouling

issues. On February 27, the licensee had assmbled an engineering team to

determine corrective actions and root causes. Immediate corrective actions

included additional Unit 2 HX inspections, D/P testing, SW strainer inspections, and

determining apparent causes. Testing and inspection revealed that the 21

component cooling water HX tube sheets were clogged with river grass. However,

SW flow remained above acceptable limits. No other biofouling problems were

23

identified. Each SW strainer consists of a rotating basket with approximately

eleven hundred perforated disks retained in place with a threaded plastic ring.

Strainer inspections revealed that two disks were missing from the 22 SW strainer

basket, and the 21 SW strainer basket internal clearance exceeded the maximum

tolerance.

Each of these conditions results in SW flow bypassing the strainer

media. While troubleshooting high D/P across the 25 SW strainer in January,

maintenance workers found two disk retaining rings partially backed out.

Inadequate maintenance practices were attributed to this condition.

The engineering team determined the apparent cause to be elevated river grass level

compound.ed with degraded strainer conditions, noncontinuous traveling screen

operation, and lack of appropriate HX biofouling trending. On March 12, abnormal

operating procedure SC.OP-AB.ZZ-0003, Rev. 0, "Component Biofouling," was

implemented. SC.OP-AB.ZZ-0003 specifies operator actions to be ta.ken for

excessive river grass loading, such as continuous SW traveling screen operation and

more frequent biofouling D/P testing and data logging. The licensee is also planning

to perform internal SW strainer inspections during the associated SW pump

bimonthly silt inspection. The inspector concluded that the implementation of the

abnormal operating procedure and the more frequent strainer inspections would

adequately detect any significant SW biofouling.

During the previous Unit 1 and 2 refueling outages, SW pump discharge strainers

were modified by design change packages 1 EC-3685 and 2EC-3600..

Strainer disk

hole sizes were increased from 1 /32" to 1 /16", and the backwash setpoint was

lowered from 7 psid to 5 psid. The modification was made to improve strainer

reliability, because the strainer motors were experiencing overload trips that

resulted from high D/P across the strainer disks. Additionally, design calculations

assumed that an average of one SW strainer would operate continuously in

backwash mode during accident conditions. An engineering review determined that

the disks with 1 /32" diameter holes may cause more frequent strainer backwash

cycles resulting in more than one strainer in backwash mode during accident

conditions. 1he licensee reported this condition in LER 50-272/96-034. PSE&G

attributed the cause of this reportable condition to the failure to recognize long term

clogging effects on the strainer disks. The filter disks were replaced along with a

recurring task to inspect the SW strainer disks.r The inspector reviewed the 10 CFR

50.59 applicability review for this modification and did not note any problems. This

LER is closed.

The Salem SW system is susceptible to biofouling from river grass, and

accumulation of grass in components may occur over extended periods of time.

Several indications of accelerated SW biofouling existed before the 22 chiller

tripped. However prompt management actions to determine and correct the causes

were not initiated until the after the chiller tripped. The licensee's corrective

actions were mainly focused on Unit 2 and did not include a detailed evaluation of

SW biofouling effects on Unit 1. The inspector also noted that on January 25,

maintenance identified that the 14 SW strainer had one disk missing, however no

24

AR was initiated until questioned by the inspector on March 13. Failure to promptly

identify and correct SW biofouling problems is a violation of 10 CFR 50, Appendix

8, Criterion XVI, Corrective Action (VIO 50-272 & 311/98-01-10).

c.

Conclusions

Elevated grass levels in the Delaware River combined with degraded service water

strainers and lack of service water reliability program oversight resulted in

accelerated rates of service water biofouling. Weak management attention allowed

biofouling to occur at unpredictable rates. Several instances of biofouling occurred

in plant components before strainer degradation was identified and effective

corrective actions were taken. In one instance, the biofouling contributed to the

inoperability of a Unit 2 safety related chiller. Salem staff failed to take prompt

corrective actions to determine and correct the cause of service water biofouling

problems. System Engineering and Operations interfaces were weak during the

analysis of those problen:is. The licensee did not adequately evaluate the extent of

condition at both Salem Units. The inspector also concluded that the corrective

actions taken in response to Licensee Event Report 50-272/96-34 were acceptable.

ES

Miscellaneous Engineering Issues

E8.1

(Closed) Violation 50-272/96-11-01: In NRC Inspection Report 50-272&311/96-11

violations were identified concerning inadequate test control measures during

dynamic testing conducted on valves 1 &2CV68 and 1 &2CV69 (Charging Header

Stop Valves). The inspectors determined that the differential pressures assumed by

the dynamic test analysis were uncertain because: 1) the upstream pressure

instruments did not account for the presence of pressure control valves located

between the pressure instruments and the test valves and 2) the test procedure

specified the use of a downstream pressure gage with an abnormally wide rarige

which provided insufficient sensitivity for the expected test conditions. More

importantly the questionable test data obtained was used as the valve factor basis

for the PORV block valves (1 &2PR6 and 1 &2PR7).

The inspectors had reviewed PSE&G'S corrective actions to this violation for Salem

Unit 2 and found them to be adequate as documented in IR 50-311/97-03. The

inspectors confirmed that similar corrective actions were taken for Salem Unit 1 .

For example, PSE&G reviewed other Salem Unit 1 dynamic tests to identify if

similar test control mistakes were made. No significant problems were noted.

Also, PSE&G noted that continuous pressure data acquisition was being used where

possible to enhance the accuracy of test results. This violation is now closed.

EB. 2

(Closed) Inspector Followup Item 50-272/96-11-02: Complete load sensitive

behavior study for Salem Unit 1. As documented in Section E1 .1 of this report, for

restart PSE&G _has completed an acceptable load sensitive behavior study to

establish adequate margins to account for this factor for MOVs at Salem Unit 1 .

This item is closed.

,/.

25

(Closed) Inspector Followup Item 50-272/96-11-03: Complete stem friction

coefficient study for Salem Unit1. As documented in Section E1 .1 of this report,

for restart PSE&G has completed an acceptable stem friction coefficient study for

Salem Unit 1. This item is closed ..

(Closed) Inspector Followup Item 50-272/96-11-04: Revise test feedback method

to include margin for valve degradation. As documented in Section E1 .1 of this

report, PSE&G has revised their MOV setup methodology for Salem Unit 1 to

specifically include a 5% margin for potential valve degradations. This item is

closed.

(Closed) Violation 50-272/96-11-05: Incorrect assumptions in the mechanical

design calculations for the residual heat removal suction header valves ( 1 &2RH 1

and 2) resulted in low torque switch settings. The incorrect settings for these risk

significant pressure isolation valves created the possibility that they might not close

under design-basis conditions since the torque switch was wired in series with the

limit switch for these limit-controlled MOVs. PSE&G responded to the Notice of

Violation* by letter LR-N96332 dated November 1, 1996, wherein they stated the

corrective actions to be taken to prevent recurrence for both Salem Units .1 and 2.

The inspector had reviewed PSE&G'S corrective actions to this violation for Salem

Unit 2 and found them to be adequate as documented in Inspection Report

50-311197-03. The inspector confirmed that similar corrective actions were taken

for Salem Unit 1 . For example, PSE&G had corrected the mechanical design

calculations for 1RH1 and 2 and set the torque switches to the maximum allowable

such that the torque switch settings would not prevent full closure of these MOVs.

The inspector also verified that the licensee had checked other limit controlled

MOVs, including butterfly valves, and confirmed that they were not impacted

similarly. The inspector concluded these actions to be appropriate for closing out

this item.

E8.6

(Closed) Inspector Followup Item 50-272/96-11-06: Review thrust margin

improvements needed for MOV 12CC16 (RHR heat exchanger component cooling

water outlet isolation valve) which previously evidenced a negative thrust margin at

design basis conditions. As discussed in Section E1 .1 of this report PSE&G has

modified the control circuit to close this valve under limit control. This action

acceptably resolved the problem since the thrust margin for the closing direction is

currently about 17%. Therefore, this item is closed.

E8. 7

(Closed) Inspector Followup Item 50-272/96-11-07: Request for PSE&G to

increase the capability of marginal MOVs. As discussed in Section E1 .1, PSE&G

has agreed to review measures to improve the capability of certain MOVs in

conjunction with their periodic program verification efforts. The inspectors

concluded that these actions were acceptable for closing this item .

26

.E8.8

(Closed) Inspector Follow Item 50-272/96-11-08: Verify MOV switch setting

requirements for Pratt service water system butterfly valves. Family 16 consisted

of 8" and 24" Pratt butterfly valves. Similar to the final setup of these MOVs at

Salem Unit 2, PSE&G has used the EPRI PPM butterfly model to develop the torque

requirements for the Salem Unit 1 valves. No spring pack modifications were

needed to increase the output capability as was the case at Salem Unit 2. The

inspector concluded that the methodology for setting the torque switches for these

valves was acceptable for closing this item at Salem Unit 1.

E8.9

(Closed) Inspector Followup Item 50-272/96-11-09: An independent assessment of

the Salem MOV program to evaluate its readiness for closure was conducted in

August 1995 by two individuals who were MOV project members at another

nuclear facility. The assessment appeared to be highly constructive with strengths

and weaknesses noted and various recommendations presented for assuring Salem

MOV program closure. However, PSE&G had not established firm management

controls for providing their action plans or addressing the other items in the

independent assessment report.

The inspector had reviewed PSE&G'S corrective actions regarding this issue for

Salem Unit 2 and found them to be adequate as documented in IR 50-311/97-03.

The corrective actions consisted of a formal review of the 1995 independent

assessment findings. No new issues had been identified by PSE&G then and the

licensee indicated that similarly now no new issues were developed from

subsequent reviews. The inspector concluded that this issue was resolved for

Salem Unit 1.

ES. 10 (Closed) Unresolved Item 50-272/96-11-11: PSE&G had submitted an MOV

program closure letter on June 25, 1996, for Salem Unit 1 and March 20, 1995 for

Salem Unit 2 and had not amended these letters. In light of this fact and the nature

and extent of the findings in NRC Inspection Report 50-311 /96-11, a question

regarding compliance with 10 CFR 50.9, "Completeness and Accuracy of

Information" was raised. This issue was identified as an Unresolved Item for both

Units. The issue was discussed at a public meeting held on November 12, 1996,

between PSE&G and the NRC. PSE&G indicated that engineering evaluation A-O-

ZZ-MEE-0926 served as a technical basis for the Salem Units 1 and 2 MOV

program closure letters. PSE&G maintained that there was no significant negative

information that occurred subsequent to the June 25, 1996 or March 20, 1995

letters which would have warranted an amended response. MOV changes that

were made were considered to be minor enhancements to improve performance and

were not significant deviations from the MOV program technical basis.

T_his issue was reviewed and closed out satisfactorily for Salem Unit 2 as

documented in IR 50-311/97-03. The inspector reviewed the reasons for

satisfactorily closing this issue for Salem Unit 2 and concluded that no new

significant factors developed since the Salem Unit 2 review was conducted that

should prevent closure of the issue at Salem Unit 1.

27

In summary, the inspector concluded that the question regarding compliance with

10 CFR 50.9 had been resolved in that there was not a compliance problem. This *

unresolved item is closed.

EB. 11 (Closed) Unresolved Item 50-311 /96-80-01: Single Failure Licensing Basis of Fuel

Handling Ventilation System.

This issue involved determination of the fuel handling ventilation system's original

licensing and design basis with respect to single failure. The NRC Office of Nuclear

Reactor Regulation (NRR) performed a review, and based on the research

conducted, could not conclude that the fuel handling ventilation system for Salem

Unit 2 was required to meet the single failure criterion. Therefore, no violation of

NRC requirements occurred. This item is closed.

EB.12 (Update) Violation 50-311 /97-21-05 and (Closed) LER 50-311 /96-07-02: Missed

Surveillance of Containment Penetration Overcurrent Protection Devices.

This supplement to LER 96-07 was submitted to identify that on January 30, 1998,

one additional containment protection overcurrent device for each unit was

identified as not being tested per the Technical Specification requirements. This

issue was recently discussed in Inspection Report 97-21 and Violation 50-311/97-

21-05 was issued. Therefore, the cause of the condition and the corrective actions

identified by the licensee in this LER will be reviewed as part of the licensee's

response to the violation. This LER supplement is closed.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the

conclusion of the inspection on March 24, 1998. The licensee acknowledged the findings

presented. The bases for the inspection conclusions did not involve proprietary

information, nor was any such information included in this inspection report.

X2

Management Meeting Summary

On February 27, 1998, a meeting was held between the management of PSE&G and NRC

Region I and the Office of Nuclea*r Reactor Regulation (NRR), at the Salem Units 1 & 2

  • Nuclear Generating Station. The purpose of the meeting was for the licensee to present an

assessment of their readiness to restart Salem Unit 1, as required by Confirmatory Action

Letter (CAL) 1-95-009. Overheads used in the licensee's presentation at this. meeting

were included as Attachment 1 to Readiness Assessment Team Inspection Report Nos. 50-

272,311 /98-81 .

IP 37551:

IP 40500:

IP 61726:

IP 62707:

IP 71707:

IP 71750:

IP 92901:

IP 92902:

IP 92903:

IP 92904:

IP 93702:

Tl 2515/109

Opened

/

.28

INSPECTION' PROCEDURES USED

Onsite Engineering

Effectiveness of Licensee Controls in Identifying, Resolving~ and Preventing

Problems

Surveillance Observations

Maintenance Observations

Plant Operations

Plant Support Activities

Plant Operations Followup

Maintenance Followup

Engineering Followup

Plant Support Followup

Event Followup

Inspection Requirement for Generic Letter 89-10, Safety-Related Motor-

Operated Valve Testing and Surveillance

ITEMS OPENED, CLOSED, AND DISCUSSED

50-272/98-01-03

50-311/98-01-04

50-272/98-01-06

VIO

VIO

IFI

Wrong control switch installed on 12 OF.OTP.

Failure to comply with procedures for control of EDGs.

GL 98-10; Safety-Related MOV Testing and

Surveillance Program Closure.

50-272/98-01-07

50-272/98-01-08

50-272/98-01-09

50-272&311/98-01-10

Opened/Closed

50-272/98-01-01

50-311/98-01-02

50-272&311/98-01-05

IFI

IFI

IFI

VIO

NCV

NCV

NCV

Closeout review re MOV issues of PORV block valves,

RHR/RCS isolation valves, and RCP thermal barrier

cooling valves.

Closeout review re MOV issues of stem friction

coefficient, load sensitive behavior, and stem

lubrication degradation.

Closeout review re MOV issues of RCP bearing water

cooling valves.

Failure to promptly identify and correct SW biofouling

problems.

Failure to follow procedures for maintaining SG levels.

Failure to comply with TS Surveillance Requirement 4.1.3.1.1

Test control violations related to TSSIP.

Closed

50-272/96-11-01

50-272/96-11-02

50-272/96-11-03

50-272/96-11-04

50-272/96-11-05

50-272/96-11-06

50-272/96-11-07

50-272/96-11-08

50-272/96-11-09

50-272/96-11-11

50-311/96-80-01

50-311/96-07-02

50-272/96-34

50-311 /98-04

50-311 /98-05

Discussed

50-311/97-21-05

VIO

IFI

IFI

IFI

VIO

IFI

IFI

IFI

IFI

URI

URI

LER

LER

LER

LER

29

Inadequate test control and application of MOV test

data

Basis for load sensitive behavior margin used in thrust

calculations

Basis for stem friction coefficient used in thrust

calculations

Basis for valve degradation margin used in thrust

calculations

Inadequate design control of switch settings for MOVs

2RH1 and 2

Improve thrust margin for 12CC16

Request to improve thrust margin for selected MOVs

Evaluate torque requirements for Pratt butterfly valves

PSE&G to evaluate and document response to MOV

program assessment.

Resolve question regarding Salem Unit 2 MOV program

completion in the context of 10 CFR 50.9(b)

Single failure licensing basis of fuel handling ventilation

system.

Missed surveillance of containment penetration

overcurrent protection devices.

Service Water strainer design deficiency potentially

outsid.e design basis.

Failure to comply with TS surveillance requirement 4.1.3.1.1.

TS required shutdown of Salem Unit 2 due to the failure

of the 2A EDG turbocharger.

VIO

Missed surveillance of containment penetration

overcurrent protection devices .

r'

AR

AFW

CAA CS

CAL

CAVS

CREA CS

CRS

D/P

DBDP

DFOTPs

EOG

EE

EPRI

FFD

GL

HX

IFI

IV'd

MOV

MTLO

NCV

NRC

NRR

OD

OS

PDR

PMT

PORV

PPM

PR

PSE&G

RATI

RCP

RCS

RG

RHR

RO

  • RWST

SAC

SRO

STs

SW

TAC

TS

30

LIST OF ACRONYMS USED

Action Request

Auxiliary Feedwater

Control Area Air Conditioning System

Confirmatory Action Letter

Control Area Ventilation System

Control Room Emergency Air Conditioning System

Control Room Supervisor

Differential Pressure

Design Basis Differential Pressure

Diesel Fuel Oil Transfer Pumps

Emergency Diesel Generator

Engineering Evaluation

Electric Power Research Institute

Generic Letter

Heat Exchangers

Inspector Followup Item

Independently Verified

Motor-Operated Valve

Main Turbine Lube Oil

Non-cited Violation

Nuclear Regulatory Commissio.n

Nuclear Reactor Regulation

Operability Determination

Operations Superintendent

Public Document Room

Post-Maintenance Test

Power Operated Relief Valve

Performance Prediction Methodology

Primary Relief

Public Service Electric and Gas

Readiness Assessment Team Inspection

Reactor Coolant Pump

Reiactor Coolant system

Regulatory Guide

Residual Heat Removal

Reactor Operator

Refueling Water Storage Tank

Station Air Compressor

Senior Reactor Operator

Surveillance Tests

Service Water

Turbine Auxiliaries Cooling

Technical Specification

'

TSSIP

UFSAR

URI

WO 31

Technical Specification Surveillance Improvement Program

Updated Final Safety Analysis Report

Unresolved Item

Work Order