ML101470607

From kanterella
Jump to navigation Jump to search
IR 05000282-10-010, 05000306-10-010 on 04/29/10 - 05/03/10 for Prairie Island, Units 1 and 2, Inspection of Turbine Building Internal Flooding Vulnerability
ML101470607
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 05/27/2010
From: Khadijah West
Division Reactor Projects III
To: Schimmel M
Northern States Power Co
References
EA-10-070 IR-10-010
Download: ML101470607 (23)


See also: IR 05000282/2010010

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

May 27, 2010

EA-10-070

Mr. Mark A. Schimmel

Prairie Island Nuclear Generating Plant

Northern States Power Company, Minnesota

1717 Wakonade Drive East

Welch, MN 55089

SUBJECT: PRAIRIE ISLAND NUCLEAR GENERATING PLANT, UNITS 1 AND 2

NRC INSPECTION REPORT 05000282/2010010; 05000306/2010010

PRELIMINARY GREATER THAN GREEN FINDING

Dear Mr. Schimmel:

On May 3, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your Prairie Island Nuclear Generating Plant, Units 1 and 2. The enclosed report documents

the inspection findings, which were discussed on May 3, 2010, with you and other members of

your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report discusses a finding that has preliminarily been determined to be Greater than Green

- a finding of greater than very low safety significance resulting in the need for further evaluation

to determine significance and therefore the need for additional NRC action. As documented in

Section 4OA5 of this report, the emergency diesel generators, the auxiliary feedwater system,

and the safety-related batteries were not protected from a loss of safety function following an

internal flooding event, a licensing basis event, in the Unit 1 or Unit 2 turbine building. This

finding was assessed based on the best available information, including influential assumptions,

using the applicable Significance Determination Process (SDP). The results of the SDP were

determined to be sensitive to several analysis assumptions which could be improved with

additional information. Specifically, the NRC is interested in further refining (1) the population of

high energy line break piping that can realistically interact with cooling water or fire protection

piping, and (2) the likelihood of a consequential pipe failure given that a defined interaction

occurs. For this second item, the NRC is seeking an engineering justification from you

regarding the low or high likelihood of consequential pipe failure.

M. Schimmel -2-

Upon identification of this issue, your staff performed an operability evaluation and determined

that the operability of the safety-related equipment mentioned above could not be assured with

the turbine building roll up doors in the closed position. As a result, a compensatory measure

was established to ensure that the doors were maintained at least 16 inches open such that the

flood waters could flow out the doors. Several other compensatory measures were also

implemented. These compensatory measures would prevent a loss of safety function from

occurring during a turbine building internal flooding event.

This finding is also an apparent violation of NRC requirements and is being considered

for escalated enforcement action in accordance with the NRC Enforcement Policy.

The current Enforcement Policy can be found at the NRCs Web site at

http://www.nrc.gov/reading-rm/doc-collections/enforcement.

In accordance with Inspection Manual Chapter (IMC) 0609, we intend to complete our

evaluation using the best available information and issue our final determination of safety

significance within 90 days of the date of this letter. The SDP encourages an open dialogue

between the staff and the licensee; however, the dialogue should not impact the timeliness of

the staffs final determination.

Before the NRC makes its enforcement decision, we are providing you an opportunity to either:

(1) present to the NRC your perspectives on the facts and assumptions used by the NRC to

arrive at the finding and its significance at a Regulatory Conference, or (2) submit your position

on the finding to the NRC in writing. If you request a Regulatory Conference, it should be held

within 30 days of the receipt of this letter and we encourage you to submit supporting

documentation at least 1 week prior to the conference in an effort to make the conference more

efficient and effective. If a conference is held, it will be open for public observation. The NRC

will also issue a press release to announce the conference. If you decide to submit only a

written response, such submittal should be sent to the NRC within 30 days of the receipt of this

letter. If you decline to request a Regulatory Conference or to submit a written response, you

relinquish your right to appeal the final SDP determination; in that, by not doing either you fail to

meet the appeal requirements stated in the Prerequisite and Limitation Sections of Attachment 2

of IMC 0609.

Please contact John Giessner at (630) 829-9619 in writing within 10 days of the date of this

letter to notify the NRC of your intended response. If we have not heard from you within

10 days, we will continue with our significance determination and enforcement decision. The

final resolution of this matter will be conveyed in separate correspondence.

Since the NRC has not made a final determination in this matter, no Notice of Violation is

being issued for this inspection finding at this time. Please be advised that the number and

characterization of the apparent violation described in the enclosed inspection report may

change as a result of further NRC review.

M. Schimmel -3-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document system

(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the

Public Electronic Reading Room).

Sincerely,

/RA by Gary L. Shear for/

Steven West, Director

Division of Reactor Projects

Docket Nos. 50-282; 50-306

License Nos. DPR-42; DPR-60

Enclosure: Inspection Report 05000282/2010010; 05000306/2010010

w/Attachment: Supplemental Information

cc w/encl: Distribution via ListServ

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos: 50-282; 50-306

License Nos: DPR-42; DPR-60

Report No: 05000282/2010010; 05000306/2010010

Licensee: Northern States Power Company, Minnesota

Facility: Prairie Island Nuclear Generating Plant, Units 1 and 2

Location: Welch, MN

Dates: April 29 through May 3, 2010

Inspectors: K. Stoedter, Senior Resident Inspector

P. Zurawski, Resident Inspector

L. Kozak, Senior Reactor Analyst

Approved by: John B. Giessner, Chief

Branch 4

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS .................................................................................................... 1

REPORT DETAILS ................................................................................................................ 2

4. OTHER ACTIVITIES .......................................................................................................... 2

4OA5 Other Activities ............................................................................................ 2

4OA6 Management Meetings .............................................................................. 10

SUPPLEMENTAL INFORMATION ............................................................................................... 1

Key Points of Contact ................................................................................................................... 1

List of Items Opened, Closed and Discussed ............................................................................... 1

List of Documents Reviewed ........................................................................................................ 2

List of Acronyms Used .................................................................................................................. 4

Enclosure

SUMMARY OF FINDINGS

IR 05000282/2010010, 05000306/2010010; 04/29/10 - 05/03/10; Prairie Island Nuclear

Generating Plant, Units 1 and 2; Inspection of turbine building internal flooding vulnerability.

This report covers the review of a design deficiency associated with the failure to protect several

safety-related systems from a loss of safety function following a turbine building internal flooding

event. The inspectors identified one apparent violation (AV) with a preliminary significance of

Greater than Green. The significance of most findings is indicated by their color (Green, White,

Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination

Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a

severity level after NRC management review. The NRCs program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 4, dated December 2006.

A. NRC-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

Criterion III, Design Control, was identified by the inspectors due to the licensees

failure to establish measures to ensure that engineered safety features such as the

emergency diesel generators, the auxiliary feedwater system, and the safety-related

batteries were not adversely affected by events that cause turbine building flooding. As

a result, flooding from these events would cause a loss of safety function for these

systems. This issue was entered into the licensees corrective action program (CAP) as

CAP 1178236. Upon identifying this issue, the licensee implemented compensatory

measures to ensure that the systems listed above were not adversely impacted following

a turbine building internal flood.

This finding was determined to be more than minor because it impacted the design

control and external events attributes of the Mitigating Systems cornerstone. The finding

also impacted the Mitigating Systems cornerstone objective of ensuring the availability,

reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. The inspectors performed a Phase 1 SDP evaluation and

determined that a Phase 3 evaluation was required because the finding represented a

loss of safety function of multiple mitigating systems. A Phase 2 SDP evaluation was

not performed because the Phase 2 SDP worksheets do not apply to internal flooding

events. The results of the Phase 3 SDP assessment showed that this finding was

potentially Greater than Green. No cross-cutting aspect was assigned to this finding

because licensee decisions made in regard to evaluating the susceptibility of mitigating

systems equipment to turbine building internal flooding events were made more than

3 years ago and therefore, not reflective of current plant performance. (Section 4OA5.1)

B. Licensee-Identified Violations

No violations of significance were identified.

1 Enclosure

REPORT DETAILS

4. OTHER ACTIVITIES

4OA5 Other Activities

.1 (Closed) Unresolved Item 05000282/2009003-01; 05000306/2009003-01: Potential

Turbine Building Flooding Issues

a. Inspection Scope

The inspectors reviewed the circumstances surrounding the licensees failure to protect

the emergency diesel generators, the auxiliary feedwater system and the safety-related

batteries from a loss of safety function following an internal flooding event in the Unit 1 or

Unit 2 turbine building.

b. Findings

Introduction: An apparent violation (AV) of 10 CFR Part 50, Appendix B, Criterion III,

Design Control, was identified by the inspectors due to the licensees failure to

establish measures to ensure that engineered safety features such as the emergency

diesel generators (EDGs), the auxiliary feedwater system and the safety-related

batteries were not adversely affected following a turbine building internal flooding event.

Description: In late 2009, the NRC issued a Green finding for Unit 1 and a White finding

for Unit 2 due to the discovery that a high energy line break (HELB) in the turbine

building could result in a loss of safety function for the component cooling water system.

As part of the extent of condition review for this issue, the licensee identified that a

turbine building HELB could result in the subsequent failure of cooling water piping and

the actuation of fire protection sprinklers such that a large supply of water could be

introduced into the turbine building. This large supply of water could have resulted in an

internal flooding condition that impacted the safety function of the EDGs, the auxiliary

feedwater pumps and the safety-related batteries. The licensee also identified that a

turbine building internal flooding analysis had not been performed. These issues were

documented in corrective action program document (CAP) 1178236 dated April 15,

2009. These issues were also documented as an unresolved item in NRC Inspection

Report 05000282/2009003; 05000306/2009003.

Turbine Building Design

The Unit 1 and Unit 2 turbine buildings at Prairie Island consist of multiple elevations.

The condenser pits (one per unit) were located below grade and had the ability to hold

approximately 750,000 gallons of water. The first floor of the turbine building (commonly

referred to as the 695-foot elevation) was located at grade level. The 695-foot elevation

of the Unit 1 and Unit 2 turbine buildings also provided access to rooms/buildings

containing the EDGs, the auxiliary feedwater system (for both units) and the

safety-related batteries.

2 Enclosure

Design and Licensing Basis Information

The inspectors reviewed the licensees licensing and design bases and found the

following:

On August 3, 1972, the Atomic Energy Commission (AEC) (the former name of the

Nuclear Regulatory Commission) issued a letter to Northern States Power Company

(the licensee) requesting that the Prairie Island plant design be reviewed to determine

whether the failure of any non-seismic-Class I equipment, particularly the circulating

water system, could cause flooding sufficient to adversely affect the performance of

engineered safety systems. The licensee was also required to determine whether the

failure of any equipment could cause flooding such that common mode failure of

redundant safety-related equipment would result.

To address this request, the licensee asked the plants architect engineer, Pioneer

Service and Engineering Company, to review the Prairie Island design. The results of

this review were transmitted from the architect engineer to the licensee on

September 21, 1972. The inspectors reviewed this letter and found that Pioneers

review was focused on the adequacy of the plant design to cope with a failure of the

circulating water system, flooding of the condenser pit, and flooding the turbine building.

The results of this review showed that a failure of the circulating water system would

result in filling the condenser pit in 2.5 minutes. After filling the condenser pit, the

cooling air ducts used to ventilate the D1 and D2 EDG rooms during engine operation

would fill with water causing a loss of safety function. The rate of water level rise on the

695-foot elevation of the turbine building was estimated to be 1 inch every 15 seconds.

Pioneer concluded that the 2.5 minutes available from the time the circulating water

system failed until the water reached the EDG cooling air ducts was sufficient for the

control room to dispatch a non-licensed operator to perform a visual inspection of the

condenser pit, report back to the control room, and manually shut down the circulating

water system.

On September 26, 1972, the licensee received an additional letter from the AEC.

This letter requested that the licensee review the plant design to determine whether

the failure of any non-seismic equipment, particularly in the circulating water and fire

protection systems, could result in a condition, such as flooding or the release of

chemicals, that might potentially adversely affect the performance of safety-related

equipment required for safe shutdown of the facility or to limit the consequences of an

accident. This letter became known as the DeYoung letter.

Northern States Power responded to the DeYoung letter on October 23, 1972. In this

letter, the licensee concluded that where the potential of flooding engineered safety

features exist, the operator is provided with sufficient information and means to take

corrective action in a timely manner. There was no discussion regarding the term

sufficient information or how timely the actions needed to be. However, the inspectors

believed that the time referred to in this letter was the 2.5 minutes discussed in the

September 26, 1972, letter. The licensee further described that level switches located in

the condenser pit would provide a control room alarm to alert operations personnel that

water was accumulating inside the condenser pit. The licensee stated that since all

safety-related mechanical/electrical components are on or above floor elevation 695

when the condenser pit high-high-high water level annunciates, there will still be ample

time for visual operator inspection of the situation and initiation of corrective actions.

3 Enclosure

There is no further danger of loss of safeguards by flooding after shut down of the

circulating water pumps. The licensee concluded their response by stating that any

potential failure of non-Class I equipment does not pose a threat to the overall plant

safety, either by impeding safeguard performance or by causing common mode failure of

redundant safeguard related equipment. No safety evaluation report could be located

to determine whether the AEC viewed the licensees response as adequate.

Conversely, no records could be located to indicate the response was inadequate.

On December 12, 1972, the licensee received a letter from the AEC regarding

postulated steam pipe breaks outside of containment. This letter required that the

Prairie Island Nuclear Generating Plant be designed such that the following statements

were true:

  • Failure of any structure, including seismic Class II or Class III structures, caused

by the accident should not cause failure of any other structure, system or

component in a manner to adversely affect the mitigation of the consequences of

the accident and the capability to bring the units to a cold shutdown condition;

  • Rupture of a pipe carrying high energy fluid, including a steam line rupture,

should not directly or indirectly result in the loss of required redundancy in any

portion of the protection system, Class 1E electric system, engineered safety

feature equipment, cable penetration, or their interconnecting cables required to

mitigate the consequences of that event and place the reactors in cold shutdown

condition; and

  • A discussion should be provided of the potential for flooding safety-related

equipment in the event of failure of a feedwater line or any other high energy

fluid line.

This letter became known as the Giambusso letter. The licensees responses to this

letter appeared to be focused on events occurring in the auxiliary building. There is

currently no information contained in the Updated Safety Analysis Report (USAR)

regarding HELBs in the turbine building.

On January 3, 1986, the licensee sent a letter to the NRC regarding the resolution of

Generic Issue No. 77, Flooding of Safety Equipment Compartments by Backflow

Through Floor Drains. The letter contained the following statement about water flow

in the turbine buildings:

Once the water goes above Elevation 695 - 0 the water storage capacity

increases greatly such that, with the exception of the EDG room cooling air

ducts, it would take about 3 more minutes to reach Elevation 695 - 10 whereby

the flooding would affect safety-related equipment.

To address this statement, the licensee implemented a permanent modification to

ensure that the circulating water pumps tripped due to high water level in the condenser

pit. The inspectors determined that although the EDG room cooling air duct flooding

vulnerability was identified in 1972, the modifications implemented to address this

vulnerability were not installed until 1988 and 1989. The inspectors also found that the

licensee had failed to consider other flooding scenarios (such as HELB induced flooding

4 Enclosure

or flooding due to random pipe breaks) as part of addressing any of the previous letters

sent by the AEC or the NRC.

As discussed above, on April 15, 2009, the licensee initiated a CAP to document that a

turbine building HELB could result in an internal flooding condition that impacted the

safety function of the EDGs, the auxiliary feedwater pumps and the safety-related

batteries. The licensee performed an operability review and determined that operability

of these safety-related systems could not be assured. To remedy this immediate

concern, the licensee opened both turbine building roll up doors to prevent water from

accumulating on the 695-foot elevation of the turbine building if an internal flooding event

occurred.

The same day, the inspectors reviewed the licensees corrective action system to

determine how the licensee had evaluated and addressed industry internal flooding

operating experience (OE) from 2005. The inspectors found that the licensee had

conducted an OE review, determined that the OE was applicable to Prairie Island, and

assigned several actions to evaluate specific portions of the turbine building (including

the battery rooms, the auxiliary feedwater pump room and the EDG rooms). However,

no work had been performed on these reviews as of April 2009. In summary, the

inspectors concluded that the failure to adequately protect the safety related

components from the affects of license basis events was within their ability to foresee

and correct, and is, therefore, a performance deficiency.

Since April 2009, the licensee has initiated additional CAPs and operability evaluations

associated with internal flooding of the Unit 1 or Unit 2 turbine building. The licensee

found that based upon the best available information, the pre-April 2009 plant

configuration was not adequate to ensure that operations personnel could take

appropriate actions following a turbine building internal flood to protect safety-related

equipment prior to the equipment (both trains) being impacted by the flood water. The

licensee took the following actions to ensure that safety-related equipment was

protected:

  • The turbine building roll up doors were opened (as the seasons permit) to allow

the flood waters to exit the turbine building;

  • The bottom of the roll up doors were modified to allow the doors to stay partially

open during the fall and winter;

  • Approximately 18-inch flood walls were constructed to protect the Unit 1 and

Unit 2 EDGs;

pump room were secured with fasteners to prevent additional water intrusion;

and

  • All doors leading from the turbine building into rooms housing safety-related

equipment were inspected. Repairs were made to the door from the Unit 2

turbine building into the safety-related battery room to lessen the rate of water

intrusion into the room.

Analysis: The inspectors determined that the licensees failure to establish measures to

ensure that the EDGs, the auxiliary feedwater system and the safety-related batteries

were protected from a loss of safety function following an internal flood was a

performance deficiency that required an evaluation using the Significance Determination

Process (SDP) described in NRC Inspection Manual Chapter (IMC) 0609. The

5 Enclosure

inspectors also determined that this finding should be assigned to the Mitigating

Systems cornerstone because it impacted systems used in short term and long term

heat removal.

The inspectors performed a Phase 1 SDP analysis and concluded that the finding

represented a loss of safety function of several mitigating systems including the EDGs,

the auxiliary feedwater system and the safety-related batteries (direct current power).

A Phase 2 SDP analysis was not performed because the Phase 2 process was not

applicable for internal flooding scenarios. As a result, the inspectors requested that a

regional senior reactor analyst (SRA) perform a preliminary SDP phase 3 analysis.

The SRA used spreadsheet calculations to estimate the risk from the internal flooding

scenarios affected by this finding. The Standardized Plant Analysis Risk (SPAR) model

for Prairie Island (Revision 3.45) and the Prairie Island Phase 2 SDP worksheets were

used to determine the success criteria for loss of main feedwater events and to

determine system functional requirements for auxiliary feedwater, feed and bleed, and

high pressure recirculation.

The baseline core damage frequency (CDF) for the internal flooding scenarios related to

the performance deficiency was assumed to be much lower than the CDF estimated for

the plant in the pre-April 2009 configuration. Therefore, the CDF calculated in this SDP

Phase 3 analysis was assumed to represent the delta CDF due to the performance

deficiency.

As part of this SDP Phase 3 evaluation, the following three flooding scenarios were

evaluated:

  • High Energy Line Break-induced flooding and consequential failure of other

piping;

  • Random failure of a cooling water (CL) pipe; and
  • Seismically-induced pipe failures.

HELB-induced Flooding and Consequential Failure of Cooling Water Pipe and/or Fire

Protection Piping

The SRA conducted a plant tour to observe piping arrangements and the overall layout

of the Unit 1 and Unit 2 turbine buildings. Plant general arrangement drawings and

piping and instrumentation drawings were also reviewed. Based upon this information,

the SRA assumed that the turbine building HELB could result in the consequential failure

of CL or fire protection system piping such that an unlimited supply of water from the

Mississippi River could be introduced into the turbine building causing an internal flood.

The SRA assumed that the postulated HELB resulted in a loss of main feedwater event.

If the CL and/or fire protection (FP) piping also failed as a consequence of the HELB,

and the CL and/or FP piping was not isolated by the operator, the auxiliary feedwater,

instrument air, high pressure recirculation, and direct current power functions could be

impacted. This would lead to core damage. Information provided by the licensee

showed that if the HELB resulted in the consequential failure of the largest nonsafety-

related CL pipe, the functions listed above could fail in approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> due to the

amount of water flowing into the turbine building. The amount of time available prior to

6 Enclosure

the function failing increased as the amount of water flowing into the turbine building

dropped.

The inspectors and the SRA discussed the postulated HELB and turbine building

flooding sequence of events with operations, engineering and licensee risk personnel.

The inspectors also reviewed operating procedures and simulator training associated

with HELBs and turbine building flooding. The SRA determined that isolating the flood

sources required the operators to diagnose which system(s) were causing the flooding

after the postulated HELB event. If the cause was diagnosed as a CL pipe failure,

actions could be taken in the control room to stop the flow of water from the CL system

using established procedures. If the diagnosis determined that the FP system was also

introducing water into the turbine building due to a pipe break, sprinkler actuation or

deluge system actuation, the operators would need to perform manual actions in the

turbine building or plant screenhouse to stop the flow of water.

To simplify this portion of the SDP Phase 3 analysis, two categories of HELB-induced

flooding events were analyzed. Category 1 was defined as HELB-induced flooding

events that resulted in flow rates greater than 18,000 gallons per minute (gpm) (including

any fire sprinkler flow). Category 2 was defined as HELB-induced flooding events

resulting in flow rates between 10,000 gpm and 18,000 gpm for Unit 1 and between

7800 gpm and 18,000 gpm for Unit 2. These categories were selected after considering

the results of Engineering Change EC 15656, Evaluation of flooding times and flow

rates associated with Unit 1 and Unit 2 TB [turbine building] for significance

determination, and Calculation ENG-ME-759, Gothic Internal Flooding Calculation for

the Turbine Building. These documents showed that a loss of safety function would not

occur if operator action was successful within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> for 18,000 gpm floods and within

2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> for Unit 1 10,000 gpm floods or Unit 2 7800 gpm floods. The length of HELB

piping that could interact with the CL and FP piping was estimated by the licensee and

resulting CL and/or FP flow rates were calculated. These assumptions were used in this

preliminary SDP evaluation.

The SRA estimated the frequency of HELB events that interact with CL and/or FP piping

by determining the pipe failure frequency for pressurized water reactor feedwater and

condensate piping for Major Flooding using Electric Power Research Institute (EPRI)

Document 1013141, Revision 1, Pipe Rupture Frequencies for Internal Flooding PRAs,

Table A-51, and the pipe lengths provided by the licensee. The HELB pipe was

assumed to interact with a target pipe (the non-safety-related CL and/or FP piping) and

result in the failure of that target pipe.

Due to the complexity of responding to the postulated event, it was assumed that

operator actions required at least 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to detect and isolate the flood source. As a

result, for the largest flood rates, the event could not be mitigated and core damage was

assumed to occur. If the flooding flow rate resulted in the operators having between

1 and 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> to respond, a human error probability (HEP) for operator action was

estimated using NUREG/CR-6883, The SPAR-H Human Reliability Analysis Method.

The SRA calculated a HEP associated with failing to isolate flood sources of 0.33

assuming that the actions were performed under high stress, were of moderate

complexity, and consisted of poor ergonomics for both diagnosis and action.

7 Enclosure

Random Failure of Non-safety-Related Cooling Water Piping

A failure of non-safety-related CL piping in the turbine building would initially result in

filling up the condenser pit. When the water in the condenser pit was 5 feet deep, the

circulating water pumps would trip resulting in a subsequent reactor trip. As water from

the broken CL pipe continued to enter the turbine building, it would reach a level where it

would impact the normal feedwater and condensate systems. Depending on the

location and size of the pipe failure, operators may receive low cooling water pressure or

high cooling water flow alarms in the control room. Similar to the HELB scenario,

operators would need to diagnose the source of the flood and identify the failed pipe.

After identification, the flood could be stopped by operator action within the control room.

Similar to the HELB-induced flooding information discussed previously, two categories of

flooding were defined for this event. Category 1 was defined as random CL pipe breaks

that resulted in flooding flow rates greater than 18,000 gpm. The second category was

defined as CL pipe breaks that resulted in flow rates between 12,500 gpm and

18,000 gpm. Flood rates of less than 12,500 gpm would take greater than 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to fill

the condenser pit. Operator action to isolate the flood source after 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> was assumed

to be reliable. For category 1 events, it was assumed that operators would not be able

to take action to stop the water flow before both trains of mitigating equipment would be

impacted. This was assumed to result in core damage. For the second category it was

assumed that at least 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> was available for operator action.

The pipe failure frequency for Pressurized Water Reactor Service Water - River Water

piping for Major Flooding from EPRI 1013141, Revision 1, Pipe Rupture Frequencies

for Internal Flooding PRAs, Table A-20, was used with the turbine building pipe lengths

of non-safety-related CL piping provided by the licensee to estimate the frequency of

random CL pipe failures that could result in flooding impacts to mitigating systems.

Operator response to this postulated event was assumed to be less complicated than

the response to a HELB-induced consequential failure of CL. For category 2 events, a

HEP for operator action to isolate flooding before mitigating system damage was

estimated to be 0.2. This estimate assumed high stress and poor ergonomics for

diagnosis and high stress for action execution.

Seismically-Induced Failure of Non-safety- Related Turbine Building Piping

A seismic event can result in the failure of one or more non-safety-related pipes resulting

in turbine building flooding. A loss of offsite power event may occur as a result of the

seismic event. Since loss of offsite power was a consequence of the seismic event, the

SRA concluded that the EDG function was required in the SDP evaluation. If flood

sources were not isolated before the EDG function was lost (for Unit 1) or before other

mitigating functions were lost, core damage was assumed.

Using guidance from the Risk Assessment of Operation Events (RASP) handbook,

Volume 2 - External Events, only the Bin 2 seismic events were assumed to represent

a delta CDF. Bin 2 was defined in the RASP handbook as seismic events with

intensities greater then 0.3g but less than 0.5g. Earthquakes of lesser severity were

unlikely to result in large pipe failures and earthquakes of a larger magnitude could result

in major structural damage throughout the plant. The frequency of an earthquake in

Bin 2 was estimated to be 1.4E-5 per year. A high confidence low probability of failure

8 Enclosure

of 0.3g was assigned to the most susceptible component in the non-safety-related

portion of the CL system based on preliminary information obtained by the licensee on

the seismic fragility of CL system components. This value was used to estimate a pipe

failure probability using an average bin acceleration of 0.38g. A 0.5 probability was then

assigned using engineering judgment for the likelihood that the flood was large enough

that operator action was not possible before damage to EDG, auxiliary feedwater, or

direct current power systems occurred. This judgment was based on the conditional

probability of large pipe rupture in large diameter piping in Table 3A-2-2 of the RASP

Handbook, Volume 2.

Preliminary Significance Determination Process Phase 3 Conclusions

The total delta CDF calculated for Unit 1 and Unit 2 was greater than 1E-6 per year,

which was determined to be greater than very low safety significance (Green). The

dominant scenario was a HELB which interacted with non-safety-related CL and/or

FP piping, causing the failure of that pipe and subsequent flooding. In this scenario, the

operator fails to isolate the flooding prior to the flood damaging the auxiliary feedwater,

instrument air and high pressure recirculation functions or prior to the flood damaging

both trains of direct current power. If either of these flood impacts occurred, no

mitigation was available and core damage was assumed.

The results of the SDP were determined to be sensitive to several analysis assumptions

which could be improved with additional information. Specifically, the NRC is interested

in further refining (1) the population of HELB piping that can realistically interact with CL

and FP piping, and (2) the likelihood of a consequential pipe failure given that a defined

interaction occurs. For this second item, the NRC is seeking engineering justification

from the licensee for a low or high likelihood of consequential pipe failure in the identified

pipe interactions rather than a probabilistic estimate of consequential pipe failure.

No cross-cutting aspect was assigned to this finding as the decision regarding the

completion of reviews assigned as part of the OE evaluation were made greater than

3 years ago.

Old Design Issue Review

NRC IMC 0305, Operating Reactor Assessment Program, Section 04.11 defines an

old design issue as an inspection finding involving a past design-related problem in the

engineering calculations or analyses, the associated operating procedure, or installation

of plant equipment that does not reflect a performance deficiency associated with

existing licensee programs, policy, or procedures. Section 12.01(a) of IMC 0305 states

that the NRC may refrain from considering safety significant inspection findings in the

assessment program for a design-related finding in the engineering calculations or

analysis, associated operating procedure, or installation of plant equipment if the

following statements were true:

  • The issue was licensee-identified as a result of a voluntary initiative such as a

design basis reconstitution;

  • The performance issue was or will be corrected within a reasonable period of

time following identification;

  • The issue was not likely to have been previously identified by routine efforts such

as normal surveillance or quality assurance activities; and

9 Enclosure

  • The issue does not reflect a current performance deficiency associated with

existing licensee programs, policy or procedures.

The inspectors determined that this issue did not qualify as an old design issue.

Specifically, the issue was not licensee-identified as part of a voluntary initiative. It was

identified as part of an extent of condition review for a previous NRC-identified issue.

Had the licensee taken appropriate actions following their review of the 2005 OE, the

issue would have likely been identified. Lastly, no actions had been taken after

identifying that the plant was susceptible to turbine building flooding in 2005. As a result,

the issue was not corrected within a reasonable period of time.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires,

in part, that measures be established to assure that applicable regulatory requirements

and the design basis, as defined in Section 50.2, and as specified in the license

application, for those structures, systems and components to which this appendix

applies are correctly translated into specifications, drawings, procedures, and

instructions. Further, Criterion III requires that the design control measures shall provide

for verifying or checking the adequacy of designs.

Title 10 CFR 50.2 defines design basis as that information which identifies the specific

functions to be performed by a structure, system, or component of a facility.

USAR Section 6.1.2.8 states, in part, that internal flooding which could be postulated to

adversely affect the performance of engineered safety features was a part of the original

plant design criteria. As such, the turbine building was designed to have the capacity to

accommodate large internal floods since it takes time to increase the water levels to an

elevation where nuclear safety-related equipment is located.

Section 6.1.1 of the USAR stated that the EDGs, the auxiliary feedwater system, and the

safety-related batteries were engineered safety features of the Prairie Island Nuclear

Generating Plant.

Contrary to the above, prior to January 29, 2010, the licensee failed to establish

measures to assure that the applicable regulatory requirements and the design basis for

the EDGs, the auxiliary feedwater system, and the safety-related batteries were correctly

translated into specifications, drawings, procedures, and instructions. Specifically, the

licensee failed to assure that a turbine building internal flooding event would not

adversely affect the performance of multiple engineered safety features. This is an

apparent violation of 10 CFR Part 50, Appendix B, Criterion III pending the completion of

the final significance determination (AV 05000282/2010010-01; 05000306/2010010-01,

Failure to Ensure Design Measures Were Appropriately Established for the

Emergency Diesel Generator, Auxiliary Feedwater, and Safety-Related Battery

Systems).

4OA6 Management Meetings

.1 Exit Meeting Summary

On May 3, 2010, the inspectors presented the inspection results to M. Schimmel and

other members of the licensee staff. The licensee acknowledged the issues presented.

10 Enclosure

The inspectors confirmed that none of the potential report input discussed was

considered proprietary.

ATTACHMENT: SUPPLEMENTAL INFORMATION

11 Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

M. Schimmel, Site Vice President

B. Sawatzke, Director Site Operations

K. Ryan, Plant Manager

J. Anderson, Regulatory Affairs Manager

C. England, Radiation Protection General Supervisor

D. Kettering, Site Engineering Director

J. Lash, Operations Manager

R. Madjerich, Production Planning Manager

M. Milly, Maintenance Manager

J. Muth, Nuclear Oversight Manager

S. Northard, Performance Improvement Manager

K. Peterson, Business Support Manager

J. Sternisha, Training Manager

Nuclear Regulatory Commission

J. Giessner, Chief, Reactor Projects Branch 4

T. Wengert, Project Manager, Office of Nuclear Reactor Regulation

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened

05000282/2010010-01; AV Failure to Ensure Design Measures Were Appropriately

05000306/2010010-01 Established for the Emergency Diesel Generator, Auxiliary

Feedwater, and Safety-Related Battery Systems

(Section 4OA5.1)

Closed

05000282/2009003-01; URI Potential Turbine Building Flooding Issues05000306/2009003-01

1 Attachment

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

Section 4OA5

- 10 CFR 50.59 Screening 3188; OPR 1178239 Compensatory Measures; Revision 0

- 5AWI 8.9.0; Internal Flooding Drainage Control; Revision 4

- 5AWI 8.9.0; Internal Flooding Drainage Control; Revision 4

- Abnormal Operating Procedure 2C3 AOP2; Loss of RCP Seal Cooling; Revision 6

- Abnormal Operating Procedure 2C35 AOP2; Loss of Pumping Capacity or Supply Header

Without SI; Revision 11

- C31 AOP1; Fire Protection Line Break; Revision 0

- C35 AOP2; Loss of Pumping Capacity or Supply Header Without SI; Revision 11

- C47022-0104; Turbine Building Steam Exclusion Actuated; Revision 45

- C47022-0307; Fire Header Lo Pressure; Revision 44

- C47520-0103; Loop A Cooling Water Hi Flow; Revision 32

- C47520-0201; 21 Cooling Water Pump Overload; Revision 32

- C47520-0202; 22 Cooling Water Pump Running; Revision 34

- C47520-0203; Loop A Cooling Water Lo Pressure; Revision 32

- CAP 1178236; No HELB Flooding Calculation for Turbine Building; April 15, 2009

- CAP 1179019; Actions from OEER 888906 Have Not Been Completed; April 21, 2009

- CAP 1179979; Unit 2 Turbine Roll Up Door Found at 14 Inches Open; April 28, 2009

- CAP 1192814; Turbine Building HELB Analysis Not Completed by INPO Date; August 7, 2009

- CAP 1199492; OPR 1174113 Conclusions Not Appropriate for CAP 1199165;

September 24, 2009

- CAP 1202820; Potential Concern Raised for a HELB in the Turbine Building; October 16, 2009

- CAP 1203173; Potential Concern Raised Related to a HELB in the Turbine Building;

October 19, 2009

- CAP 1203370; OPR 1178236-04 Did Not Consider Time to Enter AOP in Evaluation;

October 20, 2009

- CAP 1206060; Potential CL System Unanalyzed Condition During HELB; November 6, 2009

- CAP 1208131; Insufficient Time for Operator Response in Certain Turbine Building HELBs;

November 24, 2009

- CAP 1213357; Potential HELB Pipe Whip Impact on Doors 42 and 43; January 12, 2010

- CAP 1213638; Dumpster in Front of the West Turbine Roll Up Door; January 14, 2010

- CAP 1215137; Forklift Parked in Unit 1 Turbine Building Truck Aisle; January 25, 2010

- CAP 1218454; Cooldown to Cold-Shutdown After a HELB; February 16, 2010

- CAP 781440; Evaluate D1/D2 Compartments for Internal Flooding; November 20, 2004

- CAP 830732; Determine the Effects of Potential Flooding in the Turbine Building; April 8, 2005

- Internal Flooding - Accident Sequence Analysis for Turbine Building Floods; March 2010

- LER 2009-006-00; Unanalyzed Condition Due to Potential Safety System Susceptibility to

Turbine Building Flooding Due to a Postulated High Energy Line Break; December 17, 2009

- Licensing and Design Bases for Prairie Island Nuclear Generating Plant Turbine Building

Internal Flooding; January 29, 2010

- NRC Information Notice 2005-30; Safe Shutdown Potentially Challenged by Unanalyzed

Internal Flooding Events and Inadequate Design; November 7, 2005

2 Attachment

- OPR 1178236-04; Operability of Safety-Related Equipment Following Turbine Building

Flooding; Multiple Revisions

- OPR 1203173-01; Impact of Turbine Building HELB on Auxiliary Feedwater Pump Room Heat

Up; Revisions 0 and 1

- OPR 1206060-01; Evaluation of HELB Induced Flood, Loss of Offsite Power and Single

Failure; Revisions 0 and 1

- PINGP Calculation ENG-ME-586; Effects of Flooding in the AFW Pump Room from a

Postulated Pipe Rupture; Revision 0

- Plant Safety Procedure F9; High Energy Line Break/Leak; Revision 8

- Procedure H36; Plant Flooding; Revision 1

- Significance Determination Input Information for PINGP Turbine Building Internal Flooding;

February 19, 2010

- Simulator Exercise Guide P9110SE-CLHELB-2; High Energy Line Break with Loss of Offsite

Power - Cooling Water and Fire Protection Response; Revision 0

- Special Test Procedure TP 1398; Verify Physical Inputs to Internal Flooding Evaluations;

Revision 1

3 Attachment

LIST OF ACRONYMS USED

ADAMS Agencywide Document Access Management System

AEC Atomic Energy Commission

AV Apparent Violation

CAP Correction Action Program

CDF Core Damage Frequency

CFR Code of Federal Regulations

CL Cooling Water

EDG Emergency Diesel Generator

EPRI Electric Power Research Institute

FP Fire Protection

gpm Gallons Per Minute

HELB High Energy Line Break

HEP Human Error Probability

IMC Inspection Manual Chapter

NRC Nuclear Regulatory Commission

OE Operating Experience

PARS Publicly Available Records System

RASP Risk Assessment of Operational Events

SDP Significance Determination Process

SPAR Standardized Plant Analysis Risk

SRA Senior Reactor Analyst

USAR Updated Safety Analysis Report

4 Attachment

M. Schimmel -3-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document system

(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the

Public Electronic Reading Room).

Sincerely,

/RA by Gary L. Shear for/

Steven West, Director

Division of Reactor Projects

Docket Nos. 50-282; 50-306

License Nos. DPR-42; DPR-60

Enclosure: Inspection Report 05000282/2010010; 05000306/2010010

w/Attachment: Supplemental Information

cc w/encl: Distribution via ListServ

DOCUMENT NAME: G:\PRAI\Prai 2010 010.doc

Publicly Available Non-Publicly Available Sensitive Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl

"E" = Copy with attach/encl "N" = No copy

OFFICE RIII RIII RIII NRR OE RIII

NAME JGiessner:dtp LKozak SOrth LJames*via GGulla via SWest

RLerch for on *PPelke for Email from email *GLS for

5/20/2010 GGulla

DATE 05/25/2010 05/20/2010 05/25/2010 05/25/2010 05/25/2010 05/26/2010

JAG

OFFICIAL RECORD COPY

Letter to M. Schimmel from S. West dated May 27, 2010.

SUBJECT: PRAIRIE ISLAND NUCLEAR GENERATING PLANT, UNITS 1 AND 2

NRC INSPECTION REPORT 05000282/2010010; 05000306/2010010

PRELIMINARY GREATER THAN GREEN FINDING

DISTRIBUTION:

Susan Bagley

RidsNrrPMPrairieIsland

RidsNrrDorlLpl3-1 Resource

RidsNrrDirsIrib Resource

Cynthia Pederson

Steven Orth

Jared Heck

Allan Barker

Carole Ariano

Linda Linn

DRPIII

DRSIII

Patricia Buckley

Tammy Tomczak

ROPreports Resource

ADAMS (PARS)

RidsSecyMailCenter Resource

OCADistribution

Bill Borchardt

Bruce Mallett

Roy Zimmerman

James Wiggins

Nick Hilton

Steve West

Gary Shear

Anne Boland

Kenneth OBrien

John Giessner

Rani Franovitch

Paul Bonnett

Jeff Circle

Laura Kozak

Jeff Mitman

Suni Weerakkody

Harral Logaras

Marvin Itzkowitz

Catherine Scott

Eric Leeds

Bruce Boger

Daniel Holody

Carolyn Evans

William Jones

Gerald Gulla

MaryAnn Ashley

Holly Harrington

Hubert Bell

Guy Caputo

Mona Williams

James Lynch

Viktoria Mitlyng

Prema Chandrathil

Paul Pelke

Sarah Bakhsh

Magdalena Gryglak

OEMAIL Resource

OEWEB Resource