IR 05000259/2012002

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IR 05000259-12-002, 05000260-12-002, 05000296-12-002, 07200052-12-001, on 01/01/2012 -03/31/2012, Browns Ferry Nuclear Plant, Units 1, 2 and 3, Fire Protection, Event Follow-up, Other Activities
ML12121A507
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 04/27/2012
From: Eugene Guthrie
Division Reactor Projects II
To: James Shea
Tennessee Valley Authority
References
IR-12-001, IR-12-002
Download: ML12121A507 (54)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION ril 27, 2012

SUBJECT:

BROWNS FERRY NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT 05000259/2012002, 05000260/2012002, 05000296/2012002 and 07200052/2012001

Dear Mr. Shea:

On March 31, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Browns Ferry Nuclear Plant, Units 1, 2, and 3. The enclosed inspection report documents the inspection results which were discussed on April 6, 2012, with Mr. Lang Hughes and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations, orders, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Three NRC identified findings of very low safety significance (Green) were identified during this inspection. These findings were determined to involve violations of NRC requirements.

Additionally, the NRC has determined that a traditional enforcement Severity Level IV violation occurred. Furthermore, a licensee-identified violation which was determined to be of very low safety significance is listed in this report. The NRC is treating the violations as non-cited violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy. If you contest these non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001, with copies to: (1) the Regional Administrator, Region II; (2) the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and (3) the NRC Resident Inspector at the Browns Ferry Nuclear Plant.

In addition, if you disagree with any cross-cutting aspect assignment in the report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the Browns Ferry Nuclear Plant.

TVA 2 In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any), will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Eugene F. Guthrie, Chief Special Project, Browns Ferry Division of Reactor Projects Docket Nos.: 50-259, 50-260, 50-296,72-052 License Nos.: DPR-33, DPR-52, DPR-68

Enclosure:

NRC Integrated Inspection Report 05000259/2012002, 05000260/2012002, 05000296/2012002, and 07200052/2012001

REGION II==

Docket Nos.: 50-259, 50-260, 50-296, 072-052 License Nos.: DPR-33, DPR-52, DPR-68 Report No.: 05000259/2012002, 05000260/2012002, 05000296/2012002, and 07200052/2012001 Licensee: Tennessee Valley Authority (TVA)

Facility: Browns Ferry Nuclear Plant, Units 1, 2, and 3 Location: Corner of Shaw and Nuclear Plant Roads Athens, AL 35611 Dates: January 1, 2012, through March 31, 2012 Inspectors: C. Stancil, Resident Inspector P. Niebaum, Resident Inspector L. Pressley, Resident Inspector K. Korth, Senior Training Instructor (1R04, 1R12, 1R13)

R. Carrion, Senior Reactor Inspector (4OA5.2)

C. Fletcher, Senior Reactor Inspector (4OA5.2)

Approved by: Eugene F. Guthrie, Chief Reactor Projects Special Branch Division of Reactor Projects Enclosure

SUMMARY OF FINDINGS

IR 05000259/2012002, 05000260/2012002, 05000296/2012002, 07200052/2012001; 01/01/2012 -03/31/2012; Browns Ferry Nuclear Plant, Units 1, 2 and 3; Fire Protection, Event Follow-up, Other Activities The report covered a three month period of inspection by resident and regional inspectors.

Three non-cited violations (NCVs) were identified. The significance of most findings is identified by their color (Green, White, Yellow, and Red) using Inspection Manual Chapter (IMC) 0609,

Significance Determination Process (SDP); and, the cross-cutting aspects were determined using IMC 0310, Components Within the Cross-Cutting Areas. Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review.

The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process Revision 4, dated December 2006.

NRC Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green.

The NRC identified a non-cited violation of Technical Specification 5.4.1.d,

Fire Protection Program, for the licensees failure to adequately implement Limiting Conditions For Operation in accordance with Fire Protection Report Volume 1, Fire Protection Plan. Specifically, the licensee failed to adequately implement impaired fire barrier and detector controls which resulted in the failure to establish a continuous fire watch for an impaired fire barrier having smoke detection identified as unavailable to protect either side of the inoperable barrier. The licensee subsequently returned the impaired fire door and smoke detection to service. The licensee entered this event into their corrective action program as PERs 529543 and 527311.

The finding was determined to be more than minor because it was associated with the Mitigating Systems cornerstone attribute of Protection Against External Events, and adversely affected the cornerstone objective to ensure the availability of systems that respond to initiating events to prevent undesirable consequences (i.e. core damage). Specifically, inadequate implementation of the licensees FPIP and LCO processes resulted in the licensee missing a LCO entry condition and not establishing a continuous fire watch for an impaired fire door. The significance of this finding was evaluated in accordance with the IMC 0609 Appendix F, Attachment 01, Part 1, Fire Protection SDP Phase 1 Worksheet. The finding was determined to be of very low safety significance (Green) because the condition represented a low degradation of fire prevention and administrative controls. Specifically, a smoke detection system on one side of the impaired fire door was discovered functional.

The cause of this finding was directly related to the cross cutting aspect of Procedural Compliance in the Work Practices component of the Human Performance area, because licensee expectations were ineffectively communicated and fire protection procedures inadequately implemented to maintain a site understanding of fire barrier and detector configuration H.4(b). (Section 1RO5)

Cornerstone: Initiating Events

Green.

The NRC identified a non-cited violation of Technical Specification 5.4.1.d,

Fire Protection Program implementation associated with the licensees failure to report a fire in the Unit 1 Turbine Building to the main control room (MCR).

Specifically, the failure to report a plant fire resulted in a failure of the MCR operators to implement Emergency Plan Implementing Procedure EPIP-17, Fire Emergency Response. Following the event, plant staff performed additional inspections of plant areas and either removed electrical extension cords or ensured each cord had a required GFCI and was not overloaded. Expectations for plant employees discovering and responding to fires were reinforced by plant management. The licensee entered this event into their corrective action program as PER 527090.

The performance deficiency was determined to be more than minor because if left uncorrected, the failure to notify the MCR of plant fire events would have the potential to lead to a more significant safety concern. Specifically, emergency response procedures for plant fires would not be entered and implemented and the Fire Brigade response would be delayed. The significance of this finding was evaluated in accordance with the IMC 0609, Appendix F, Attachment 1, Part 1, Fire Protection SDP Phase 1 Worksheet. The inspectors concluded that the significance of this finding was Green due to a low degradation rating for this fire event because it was a small electrical fire with no combustible material within the vicinity of the fire.

The cause of this finding was directly related to the cross cutting aspect of Procedural Compliance in the Work Practices component of the Human Performance area, because the licensee failed to recognize the requirement to immediately report a fire and enter the appropriate fire emergency response procedures H.4(b).

(Section 4OA3.4)

Cornerstone: Barrier Integrity

  • Green: The NRC identified a Green non-cited violation of 10CFR 50.46, Acceptance criteria for emergency core cooling systems for light-water nuclear power reactors, for the licensees failure to ensure that the ECCS was satisfactorily designed such that the maximum fuel element cladding temperature specified in 10 CFR 50.46(b)(1)would not be exceeded. On May 29, 2011, operating limitations were implemented to account for the error in calculations. This violation has been entered into the licensees CAP as PER 372764.

This performance deficiency was considered greater than minor because it was associated with the Design Control attribute of the Barrier Integrity Cornerstone and adversely affected the cornerstone objective of providing reasonable assurance that the physical design barriers protect the public from radionuclide releases caused by accidents. The inspectors determined the finding to not be greater than green based on the remaining barriers to fission product release were unaffected. The cause of this finding was directly related to the cross-cutting aspect of Issue Identification in the Corrective Action Program component of the Problem Identification and Resolution area because the licensee failed to completely, accurately, and in a timely manner identify the errors with the ECCS evaluation model [P.1.(a)]. (4OA5.3)

Licensee Identified Violations

One violation of very low safety significance, which was identified by the licensee, has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. The violation and the corrective action program tracking number are listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Unit 1 operated at essentially full Rated Thermal Power (RTP) for the report period.

Unit 2 operated at essentially full RTP for most of the report period except for a planned downpower on March 8 to 92 percent RTP power to remove the C1 and C2 high pressure feedwater heaters from service to facilitate downstream piping repairs. The unit returned to full RTP the same day.

Unit 3 operated at essentially full RTP for most of the report period except for two unplanned downpowers. On January 21, the unit performed an unplanned downpower to 80 percent RTP due to false temperature indications on the main generators stator cooling water system. The unit returned to full RTP on January 22. On February 24, the unit performed an unplanned downpower to 43 percent RTP because the 3A condenser circulating water (CCW) pump tripped while the 3C CCW pump was out of service for planned maintenance. Unit 3 returned to full RTP on February

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

.1 Tornado Warning

a. Inspection Scope

On March 2, a Tornado Warning was issued for adjacent counties. The inspectors reviewed the licensee=s overall preparations/protection for the expected weather conditions and observed the licensees implementation of abnormal operating instruction 0-AOI-100-7, Severe Weather. The inspectors also reviewed and discussed the implementation of 0-AOI-100-7 with the responsible Unit Supervisors (US) and Shift Manager. Furthermore, the inspectors witnessed the licensees execution of evacuation orders of vulnerable areas and buildings outside the power block, and the termination of work and evacuation of the turbine and refueling floors. The inspectors also toured the plant grounds for loose debris, which could become missiles during a tornado, and ascertained operator staffing and if they could access controls and indications for those systems required for safe control of the plant. This activity constituted one inspection sample.

b. Findings

No findings were identified.

1R04 Equipment Alignment

.1 Partial Walkdown

a. Inspection Scope

The inspectors conducted three partial equipment alignment walkdowns to evaluate the operability of selected redundant trains or backup systems, listed below, while the other train or subsystem was inoperable or out of service. The inspectors reviewed the functional systems descriptions, Updated Final Safety Analysis Report (UFSAR), system operating procedures, and Technical Specifications (TS) to determine correct system lineups for the current plant conditions. The inspectors performed walkdowns of the systems to verify that critical components were properly aligned and to identify any discrepancies which could affect operability of the redundant train or backup system.

This activity constituted three inspection samples.

  • Unit 3 Qualified Alternate Offsite Power Sources (161 kV) with Athens 161 kV Line Out of Service

b. Findings

No findings were identified.

.2 Complete Walkdown

a. Inspection Scope

The inspectors completed a detailed alignment verification of the Unit 1/2 C EDG, using the applicable P&ID flow diagrams, 0-47E861-3, 0-47E861-7, and 0-47E840-2, along with the relevant operating instructions, 0-OI-82, to verify equipment availability and operability. The inspectors reviewed relevant portions of the UFSAR and TS. This detailed walkdown also verified electrical power alignment, the condition of applicable system instrumentation and controls, component labeling, pipe hangers and support installation, and associated support systems status. Furthermore, the inspectors examined applicable System Health Reports, open Work Orders, and any previous Problem Evaluation Reports (PERs) that could affect system alignment and operability.

This activity constituted one inspection sample.

b. Findings

No findings were identified.

1R05 Fire Protection

.1 Fire Protection Tours

a. Inspection Scope

The inspectors reviewed licensee procedures, Nuclear Power Group Standard Programs and Processes NPG-SPP-18.4.7, Control of Transient Combustibles, and NPG-SPP-18.4.6, Control of Fire Protection Impairments, and conducted a walkdown of the six fire areas (FA) and fire zones (FZ) listed below. Selected FAs/FZs were examined in order to verify licensee control of transient combustibles and ignition sources; the material condition of fire protection equipment and fire barriers; and operational lineup and operational condition of fire protection features or measures. Furthermore, the inspectors reviewed applicable portions of the Fire Protection Report, Volumes 1 and 2, including the applicable Fire Hazards Analysis, and Pre-Fire Plan drawings, to verify that the necessary firefighting equipment, such as fire extinguishers, hose stations, ladders, and communications equipment, was in place. This activity constituted six inspection samples.

  • Fire Area (FA) 5: Unit 1 Reactor Building, Electrical Board Room 1A and 250V Battery Room, EL 621
  • FA 17: Unit 1 Control Building EL 593 Battery and Battery Board Rooms
  • Fire Zone (FZ) 2-3: Unit 2 Reactor Building, EL 593 and the RHR HX Room
  • FZ 2-4: Unit 2 Reactor Building, EL 593 and the RHR HX Room
  • FZ 2-5: Unit 2 Reactor Building, EL 621 and EL 639 North of Column Line R
  • FA 25-1: Cable Tunnel to Intake Pumping Station and Fire Door 440

b. Findings

One finding was identified.

Introduction:

The NRC identified a Green, non-cited violation of Technical Specification 5.4.1.d, Fire Protection Program, for the licensees failure to adequately implement Limiting Conditions For Operation in accordance with Fire Protection Report Volume 1, Fire Protection Plan. Specifically, the licensee failed to adequately implement impaired fire barrier and detector controls which resulted in the failure to establish a continuous fire watch for an impaired fire barrier having smoke detection identified as unavailable to protect either side of the inoperable barrier.

Description:

During a walk down of the intake pumping station cable tunnel on March 22, 2012, inspectors observed that Fire Door (FD)-440 was blocked with a scaffold board and temporary sump pump discharge hose protruding through the door opening.

This blockage would have prevented the fusible link closure assembly from automatically closing the door during a fire event. FD-440 was a recent fire barrier modification implemented as a result of Browns Ferrys transition to NFPA 805 fire protection program. This fire door separated the turbine building fire area from the intake pumping station fire areas. The inspectors determined that the licensee initiated Fire Protection Impairment Permits (FPIPs) 12-3398 and 12-3394 for FD-440 and the local linear beam smoke detectors respectively, as a result of ongoing replacement of condenser circulating water pump power supply cables on Feb 27, 2012. In addition, the inspectors determined that the licensee implemented FPIP 11-2888 for the system of smoke detectors (separate from the linear beam detectors) on both sides of FD-440, due to a licensee determination that associated fire protection control panel 297 was OOS on March 1, 2011. The inspectors concluded that, based on the fire protection equipment status, the cable tunnel to the intake pumping station was without an adequate fire barrier or detection and in accordance with Fire Protection Report Volume 1, Section 9.3, Fire Protection Systems Limiting Condition for Operating, the licensee should have established a continuous fire watch in the cable tunnel beginning February 27, 2012.

After this issue was brought to the licensees attention by the inspectors, and the determination that no work requiring the impairments was in progress, FPIP 12-3394 was restored to operation on March 23, 2012, and FPIP 12-3398 was restored to operation on March 22, 2012.

Upon follow-up functional testing, the licensee determined that fire panel 297 could respond to at least one system of tunnel smoke detectors and that the panel had been improperly designated OOS for over a year as a result of operators misunderstanding the panel functions. Also, even though the 297 panel was declared OOS, the limiting condition for operating (LCO) was never administratively entered on the FPIP and in the LCO log in accordance with Fire Protection Report, Section 9.3.11.G, which contributed to not establishing a continuous fire watch. In addition, operators exceeded the monthly surveillance grace period for fire panel 297, 1-SI-4.11.A.3, Monthly Functional Test of Non-Supervised Alarm Circuits, because operators had erroneously determined the panel as OOS. FPIP 11-2888 was restored to operation on March 28, 2012.

Furthermore, inspectors observed that site sensitivity to fire protection equipment availability was not consistent with minimizing OOS time as required by Fire Protection Report Volume 1, Fire Protection Plan, Section 7.4, Control of Fire Protection Impairments. All three FPIPs above were past their restoration dates, in one case, by almost a year. The inspectors also observed that the licensee procedure FP-0-000-INS019, Fire Protection Weekly Inspection, which required inspection of the impaired equipment to ensure accurate status, was ineffective in maximizing availability.

The licensee immediately restored the fire barrier and an associated detection system, and added senior licensed operator review of all fire impairments. In addition, the licensee plans to evaluate their FPIP and fire protection LCO programs to identify potential program improvements. The licensee entered this event into their corrective action program as PERs 529543 and 527311.

Analysis:

The licensees failure to adequately implement impaired fire barrier and detector controls in accordance with the fire protection program was a performance deficiency. The inspectors determined this finding to be more than minor because it was associated with the Mitigating Systems cornerstone attribute of Protection Against External Events, and adversely affected the cornerstone objective to ensure the availability of systems that respond to initiating events to prevent undesirable consequences (i.e. core damage). Specifically, inadequate implementation of the licensees FPIP and LCO processes resulted in the licensee missing a LCO entry condition and not establishing a continuous fire watch for an impaired fire door.

The significance of this finding was evaluated in accordance with the IMC 0609 4, Phase 1- Initial Screening and Characterization of Findings, which required further evaluation in accordance with Appendix F, Attachment 01, Part 1, Fire Protection SDP Phase 1 Worksheet. The finding was determined to be of very low safety significance (Green) because the condition represented a low degradation of fire prevention and administrative controls. Specifically, a smoke detection system on one side of the impaired fire door was discovered functional.

The cause of this finding was directly related to the cross cutting aspect of Procedural Compliance in the Work Practices component of the Human Performance area, because licensee expectations were ineffectively communicated and fire protection procedures inadequately implemented to maintain an adequate site understanding of fire barrier and detector configuration H.4(b).

Enforcement:

Technical Specification 5.4.1.d required that written procedures shall be established, implemented, and maintained for Fire Protection Program implementation.

Fire Protection Report Volume 1, Fire Protection Plan, Section 9.3.11.G, LCO for Fire Rated Assemblies, required that with FD-440 inoperable, a continuous fire watch on one side of the fire door was required to be established within one hour if no fire detection was available to protect either side of the inoperable fire door. Contrary to this requirement, the licensee failed to establish a continuous fire watch on one side of the door when no fire detection was available to protect either side of the inoperable fire door. Specifically, from February 27, to March 23, 2012, the licensee failed to enter an LCO entry condition which resulted in the failure to establish a continuous fire watch for impaired fire door, FD-440. The licensee immediately restored the fire barrier and an associated detection system. Because the finding was of very low safety significance and has been entered into the licensees CAP as PERs 529543 and 527311, this violation is being treated as an NCV consistent with the NRC Enforcement Policy. This NCV is identified as NCV 05000259, 260, 296/2012002-01, Failure to Adequately Implement Impaired Fire Barrier and Detector Controls.

.2 Annual Fire Brigade Drill

a. Inspection Scope

On February 8, 2012, the inspectors witnessed an unannounced fire drill in the Unit 1 Control Bay Elevation 593 at the Unit 1 Computer Room. The inspectors assessed fire alarm effectiveness; response time for notifying and assembling the fire brigade; the selection, placement, and use of firefighting equipment; use of personnel fire protective clothing and equipment (e.g., turnout gear, self-contained breathing apparatus);communications; incident command and control; teamwork; and fire fighting strategies.

The inspectors also attended the post-drill critique to assess the licensees ability to review fire brigade performance and identify areas for improvement. Following the critique, the inspectors compared their findings with the licensees observations and to the requirements specified in the licensees Fire Protection report. This activity constituted one inspection sample.

b. Findings

No findings were identified

1R06 Internal Flood Protection Measures

.1 Review of Areas Susceptible to Internal Flooding

a. Inspection Scope

The inspectors performed walkdowns of the internal flood protection features of three risk-significant areas in the Units 1, 2 and 3 Reactor Buildings (519 elevation) with susceptible systems and equipment, which included; Residual Heat Removal (RHR) and Core Spray (CS) pump rooms, High Pressure Coolant Injection (HPCI) pump rooms and Under-Torus areas. The inspectors reviewed selected licensee documents including:

the UFSAR and design criteria; technical drawings; and procedures for mitigating and responding to flooding events, maintenance, testing, and annunciation response to verify that licensee actions were consistent with the plants licensing and design basis.

The inspectors specifically examined plant design features and measures intended to protect the plant from an internal flooding event in any Reactor Building, such as Reactor Building bulkhead watertight doors, curbing, wall penetrations, and flood level and floor drain instrumentation. The inspectors also reviewed selected completed preventive maintenance procedures, work orders, and surveillance procedures to verify that actions were completed within the specified frequency and in accordance with design basis documents. Furthermore, the inspectors reviewed the PERs initiated for the previous 12 months with respect to flood-related items and to verify that problems were being identified and entered into the corrective action program. This activity constituted one inspection sample.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification

.1 Resident Inspector Quarterly Review

a. Inspection Scope

On February 6, 2012, the inspectors observed a licensed operator requalification simulator training session for an operating crew according to Unit 2 Simulator Exercise Guide OPL177.041, H2 Supply Alarm, HPCI Pressure Switch Failure, Condenser Tube Leak, Fuel Failure, Main Steam Line leak, Unisolable RCIC Steam Line Break, HPCI Failure, 2 Area Rad Levels Above Max Safe. Additionally, on February 19, 2012, the inspectors observed licensed operator requalification classroom and simulator sessions for an operating crew validating recently changed Safe Shutdown Instruction (SSI) 0-SSI-26, Turbine Bldg, Turbine Bldg Side of Cable Tunnel to Door 440, and Radwaste Building.

The inspectors specifically evaluated the following attributes related to the operating crews performance:

  • Clarity and formality of communication
  • Ability to take timely action to safely control the unit
  • Prioritization, interpretation, and verification of alarms
  • Correct use and implementation of Abnormal Operating Instructions (AOIs), and Emergency Operating Instructions (EOIs)
  • Timely and appropriate Emergency Action Level declarations per Emergency Plan Implementing Procedures (EPIP)
  • Control board operation and manipulation, including high-risk operator actions
  • Command and Control provided by the Unit Supervisor and Shift Manager The inspectors attended the post-examination critique to assess the effectiveness of the licensee evaluators, and to verify that licensee-identified issues were comparable to issues identified by the inspector. The inspectors also reviewed simulator physical fidelity (i.e., the degree of similarity between the simulator and the reference plant control room, such as physical location of panels, equipment, instruments, controls, labels, and related form and function). This activity constituted one inspection sample.

b. Findings

No findings were identified.

.2 Control Room Observations

a. Inspection Scope

Inspectors observed and assessed licensed operator performance in the plant and main control room, particularly during periods of heightened activity or risk and where the activities could affect plant safety. Inspectors reviewed various licensee policies and procedures such as OPDP-1, Conduct of Operations, NPG-SPP-10.0, Plant Operations and GOI-100-12, Power Maneuvering.

Inspectors utilized activities such as post maintenance testing, surveillance testing and refueling and other outage activities to focus on the following conduct of operations as appropriate;

  • Operator compliance and use of procedures.
  • Control board manipulations.
  • Communication between crew members.
  • Use and interpretation of plant instruments, indications and alarms.
  • Use of human error prevention techniques.
  • Documentation of activities, including initials and sign-offs in procedures.
  • Supervision of activities, including risk and reactivity management.
  • Pre-job briefs.

This activity constituted one inspection sample.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

.1 Routine

a. Inspection Scope

The inspectors reviewed the two specific structures, systems and components (SSC)within the scope of the Maintenance Rule (MR) (10CFR50.65) with regard to some or all of the following attributes, as applicable:

(1) Appropriate work practices;
(2) Identifying and addressing common cause failures;
(3) Scoping in accordance with 10 CFR 50.65(b) of the MR;
(4) Characterizing reliability issues for performance monitoring;
(5) Tracking unavailability for performance monitoring;
(6) Balancing reliability and unavailability;
(7) Trending key parameters for condition monitoring;
(8) System classification and reclassification in accordance with 10 CFR 50.65(a)(1) or (a)(2);
(9) Appropriateness of performance criteria in accordance with 10 CFR 50.65(a)(2); and
(10) Appropriateness and adequacy of 10 CFR 50.65 (a)(1) goals, monitoring and corrective actions (i.e., Ten Point Plan). The inspectors also compared the licensees performance against site procedure NPG-SPP-3.4, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting; Technical Instruction 0-TI-346, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting; and NPG-SPP-03.1, Corrective Action Program. The inspectors also reviewed, as applicable, work orders, surveillance records, PERs, system health reports, engineering evaluations, and MR expert panel minutes; and attended MR expert panel meetings to verify that regulatory and procedural requirements were met. This activity constituted two inspection samples.
  • Unit 1 HPCI System Exceeded Unreliability Performance Criteria

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation

a. Inspection Scope

For planned online work and/or emergent work that affected the combinations of risk significant systems listed below, the inspectors examined five on-line maintenance risk assessments, and actions taken to plan and/or control work activities to effectively manage and minimize risk. The inspectors verified that risk assessments and applicable risk management actions (RMAs) were conducted as required by 10 CFR 50.65(a)(4)and applicable plant procedures such as NPG-SPP-7.0, Work Management; NPG-SPP-7.1, On-Line Work Management; 0-TI-367, BFN Equipment to Plant Risk Matrix; NPG-SPP-7.3, Work Activity Risk Management Process; and NPG-SPP-7.2, Outage Management. Furthermore, as applicable, the inspectors verified the actual in-plant configurations to ensure accuracy of the licensees risk assessments and adequacy of RMA implementation. This activity constituted five inspection samples.

  • Unit 1/2 C EDG and common B Control Bay Chiller out of service (OOS)
  • 250 VDC Shutdown Board A Battery, B Control Bay Chiller, B Control Air Compressor, 3A Control Bay Chiller, 3B RCW Pump, 3B1 Shutdown Board Room Chiller OOS
  • Unit 1 HPCI OOS, B Control Air Compressor, 1A Raw Cooling Water Pump, work in the switchyard, Trinity 161kV line switching
  • South EECW Header, Main Bank 4 Battery and Charger OOS, Switchyard high risk for 500 kV (Pre-Outage Work) and 161 kV (PCB 928)

b. Findings

No findings were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the six operability/functional evaluations listed below to verify technical adequacy and ensure that the licensee had adequately assessed TS operability. The inspectors also reviewed applicable sections of the UFSAR to verify that the system or component remained available to perform its intended function. In addition, where appropriate, the inspectors reviewed licensee procedure NEDP-22, Functional Evaluations, to ensure that the licensees evaluation met procedure requirements. Furthermore, where applicable, inspectors examined the implementation of compensatory measures to verify that they achieved the intended purpose and that the measures were adequately controlled. The inspectors also reviewed PERs on a daily basis to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. This activity constituted six inspection samples.

  • C EDG Overload Condition (PER 493979)
  • Unit 2 RCIC 2-FCV-71-2, Inboard Isolation Valve electric backseat evaluation (PER 447881)
  • C EDG Hole Drilled in Day Tank During Performance of DCN 69454 (PER 486972)
  • 3C EDG Shorted Rotor Pole (PER 480886)

b. Findings

No findings were identified.

1R18 Plant Modifications

a. Inspection Scope

The inspectors reviewed the modifications listed below to verify regulatory requirements were met, along with procedures, as applicable, such as NPG-SPP-9.3, Plant Modifications and Engineering Change Control; NPG-SPP-9.5, Temporary Alterations; and NPG-SPP-6.9.3, Post-Modification Testing. The inspectors also reviewed the associated 10 CFR 50.59 screenings and evaluations and compared each against the UFSAR and TS to verify that the modifications did not affect operability or availability of the affected systems. Furthermore, the inspectors walked down each modification to ensure that it was installed in accordance with the modification documents and reviewed post-installation and removal testing to verify that the actual impact on permanent systems was adequately verified by the tests. This activity constituted two inspection samples.

  • TACF-3-10-010-210, Revision 1, Replacement of One OOS Standby Emergency Diesel Generator (DG) with Two Temporary Standby DGs and Associated Circuits to Tie into the Bus-Tie Board

b. Findings

No findings were identified.

1R19 Post Maintenance Testing

a. Inspection Scope

The inspectors witnessed and reviewed the six post-maintenance tests (PMT) listed below to verify that procedures and test activities confirmed SSC operability and functional capability following the described maintenance. The inspectors reviewed the licensees completed test procedures to ensure any of the SSC safety function(s) that may have been affected were adequately tested, that the acceptance criteria were consistent with information in the applicable licensing basis and/or design basis documents, and that the procedure had been properly reviewed and approved. The inspectors also reviewed the test data, to verify that test results adequately demonstrated restoration of the affected safety function(s). The inspectors verified that PMT activities were conducted in accordance with applicable WO instructions, or procedural requirements, including NPG-SPP-06.3, Pre-/Post-Maintenance Testing, and MMDP-1, Maintenance Management System. Furthermore, the inspectors verified that problems associated with PMTs were identified and entered into the CAP. This activity constituted six inspection samples.

  • Unit 1/2 C EDG per PMTI-69454-STG003, Post Modification Test Instruction for DCN 69454
  • Unit 1 HPCI 1-FCV-073-0016 HPCI steam supply valve repairs per WOs 112347282, 112692321 and 113272032 and 1-SR-3.6.1.3.5(HPCI), HPCI System Motor Operated Valve
  • Unit 2 Replacement of 2B Reactor Feed Pump Controller 2-SIC-046-0009 per WO 113144298
  • Unit 3 3C EDG AC Pole Drop and Impedance Testing per WOs 112486450 and 112486454 and 3-SR-3.8.1.1(3C), Diesel Generator 3C Monthly Operability Test
  • Unit 3 HPCI system outage per WO 111847024 and 3-SR-3.5.1.7, HPCI Main and Booster Pump Set Developed Head and Flow Rate Test at Rated Reactor Pressure

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors witnessed portions of, and/or reviewed completed test data for the following five surveillance tests of risk-significant and/or safety-related systems to verify that the tests met TS surveillance requirements, UFSAR commitments, and in-service testing and licensee procedure requirements. The inspectors review confirmed whether the testing effectively demonstrated that the SSCs were operationally capable of performing their intended safety functions and fulfilled the intent of the associated surveillance requirement. This activity constituted five inspection samples.

In-Service Tests:

  • 1-SR-3.5.1.6(CS 1), Unit 1 Core Spray Flow Rate Loop 1 Routine Surveillance Tests:
  • 0-SR-3.8.1.1(C), Diesel Generator C Monthly Operability Test
  • 0-SR-3.8.1.1(D), Diesel Generator D Monthly Operability Test
  • 1/2/3-SR-3.4.6.1, Dose Equivalent Iodine 131 Concentration
  • 2-SR-3.5.3.3, RCIC System Rated Flow at Normal Operating Pressure

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

a. Inspection Scope

During the report period, the inspectors observed an Emergency Preparedness (EP)

Severe Accident Management Guidelines (SAMG) training drill that contributed to the licensees Drill/Exercise Performance (DEP) and Emergency Response Organization (ERO) performance indicator (PI) measures on March 14, 2012. This drill was intended to identify any licensee weaknesses and deficiencies in classification, notification, dose assessment and protective action recommendation (PAR) development activities. The inspectors observed emergency response operations in the simulated control room, Technical Support Center, and Operations Support Center to verify that event classification and notifications were done in accordance with EPIP-1, Emergency Classification Procedure, and licensee conformance with other applicable Emergency Plan Implementing Procedures. The inspectors also attended the post-drill critiques to compare any inspector-observed weaknesses with those identified by the licensee in order to verify whether the licensee was properly identifying EP related issues and entering them in to the CAP, as appropriate. This activity constituted one inspection sample.

b. Findings

No findings were identified.

OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness

4OA1 Performance Indicator (PI) Verification

.1 Reactor Coolant System (RCS) Activity and RCS Leakage

a. Inspection Scope

The inspectors reviewed the licensees procedures and methods for compiling and reporting the following Performance Indicators (PIs), including procedure NPG-SPP-2.2, Performance Indicator Program. The inspectors examined the licensees PI data for the specific PIs listed below for the first through fourth quarters of 2011. The inspectors reviewed the licensees data and graphical representations as reported to the NRC to verify that the data was correctly reported. The inspectors also validated this data against relevant licensee records (e.g., PERs, Daily Operator Logs, Plan of the Day, Licensee Event Reports, etc.), and assessed any reported problems regarding implementation of the PI program. Furthermore, the inspectors met with responsible plant personnel to discuss and go over licensee records to verify that the PI data was appropriately captured, calculated correctly, and discrepancies resolved. The inspectors also used the Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, to ensure that industry reporting guidelines were appropriately applied. This activity constituted six inspection samples.

  • Unit 1 RCS Activity
  • Unit 1 RCS Leakage
  • Unit 2 RCS Activity
  • Unit 2 RCS Leakage
  • Unit 3 RCS Activity
  • Unit 3 RCS Leakage

b. Findings

No findings were identified.

4OA2 Identification and Resolution of Problems

.1 Review of items entered into the Corrective Action Program:

As required by Inspection Procedure 71152, Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees CAP. This review was accomplished by reviewing daily PER and Service Request (SR) reports, and periodically attending Corrective Action Review Board (CARB) and PER Screening Committee (PSC) meetings. This activity constituted one inspection sample.

.2 Annual Follow-up of Selected Issues - Root Cause Report for Unit 1 FCV-74-52 Valve

Failure Inspection Scope The inspectors reviewed the details surrounding PER 410394 which documented the failure of the Unit 1 Low Pressure Coolant Injection (LPCI) valve 74-52 on August 2, 2011, due to its Limitorque actuator failing. Specifically, the inspectors confirmed that this issue was classified as the highest priority A level PER requiring a root cause report in accordance with licensee procedures. The inspectors evaluated the thoroughness of the root cause report, the corrective actions and corrective actions to prevent recurrence (CAPRs) associated with this PER with a specific focus on corrective action and CAPR extensions. Additionally, the inspectors evaluated the licensees extent of condition review and observed the inspections and reassembly of five other LPCI injection valves. No additional valve failures were observed during these inspections. However during the inspection of the Unit 1 74-66 valve actuator, indications of abnormal wear were observed on specific parts of the clutch assembly.

These parts were replaced and the valve tested satisfactorily before returning the valve to service. This activity constituted one inspection sample.

Findings and Observations No findings were identified. The inspector observed weaknesses associated with management involvement in the CAP extension approval process.

4OA3 Event Follow-up

.1 (Closed) Licensee Event Reports (LERs) 05000259/2011-009-00 and -01, As-Found

Undervoltage Trip for the Reactor Protection System 1A1 Relay that Did Not Meet Acceptance Criteria During Several Surveillances

a. Inspection Scope

The inspectors reviewed LER 05000259/2011-009-00 dated December 5, 2011, the revised LER 05000259/2011-009-01 dated January 31, 2012, and PERs 413140 and 442914, including the associated root cause analysis, operability determination, and corrective action plans. On October 6, 2011, while performing an operability determination for the Unit 1 reactor protection system (RPS) 1A1 relay undervoltage trips, the licensee determined that the as-found undervoltage trip for the RPS 1A1 relay was less than the required acceptance criteria during several TS surveillances performed between April 2007 and August 2011. Six of the last nine surveillance test results were below the TS acceptance criteria. Therefore, based on performance history, the RPS 1A1 relay was determined to be inoperable from April 30, 2007 to October 5, 2011, when the relay was replaced. The licensee determined the root cause to be lack of specific instructions in the surveillance test program for past operability reviews when out of TS conditions were corrected during surveillances.

b. Findings

The enforcement aspects of this finding are discussed in Section 4OA7. These LERs are considered closed.

.2 (Closed) LERs 05000259/2010-003-00, -01 and -02, Failure of a Low Pressure Coolant

Injection Flow Control Valve

a. Inspection Scope

The inspectors reviewed LER 05000259/2010-003-00 dated December 22, 2010, and the revised LERs 05000259/2010-003-01 and 05000259/2010-003-02 dated April 1, 2011 and February 10, 2012 respectively. The inspectors reviewed PERs 271338 and 369800 to validate the accuracy of the reported root causes and the corrective actions.

On October 23, 2010, during a refueling outage for Unit 1, the licensee discovered that a Residual Heat Removal (RHR) Loop II low pressure coolant injection (LPCI) flow control valve (74-66) failed to open when attempting to establish shutdown cooling while in Mode 3, Hot Shutdown. Additionally, LER revisions 01 and 02 described a Part 21 report corresponding to the first root cause which was an undersized thread barrel due to a manufacturing defect. When subjected to a system differential pressure greater than the capacity of the reduced thread engagement, the valve skirt could separate from the disc. The licensee also discovered two additional root causes during the investigation of this event. The lack of requirements for verification of thread dimensions resulted in failure to identify the undersized thread barrel during reassembly of the new valve disc with the old valve skirt in 1983. Also, the mischaracterization of the active/passive safety function for valve 74-66 resulted in the inappropriate classification and removal from the Generic Letter (GL) 89-10 program. GL 89-10 describes a program to ensure valve motor-operator switch settings (torque, torque bypass, position limit, overload) for motor-operated valves (MOVs) in several specified systems are selected, set, and maintained so that the MOVs will operate under design-basis conditions for the life of the plant.

b. Findings

The enforcement aspects of this issue were discussed in NRC Inspection Report 05000259/2011-008. No additional findings were identified regarding the original or revised LERs. The NRC is conducting supplemental inspections in accordance with Inspection Procedure 95003, Supplemental Inspection for Repetitive Degraded Cornerstones, Multiple Degraded Cornerstones, Multiple Yellow Inputs or One Red Input. These LERs are considered closed.

.3 (Closed) LERs 05000259/2011-008-00, and -01, High Vibrations on High Pressure

Coolant Injection Booster Pump Thrust Bearings.

a. Inspection Scope

The inspectors reviewed LER 05000259/2011-008-00 and LER 05000259/2011-008-01 dated September 19, 2011 and January 31, 2012, respectively. Inspectors reviewed PERs 408067 and 405165 related to this event. The HPCI booster pump exhibited increased vibration and the licensee made the initial conservative determination that the condition affected the mission time and operability of the HPCI system for an unknown period. The initial LER stated that a supplement was forthcoming following further analysis. The revised LER provided further event analysis including; event causes, a timeline of significant system events and, extent of condition which included verification of correct installation on other similar bearings. In addition, the licensees analysis concluded that, given the as-found condition of the thrust bearings, the HPCI booster pump would not have been able to meet its mission time from May 20, 2011 until successful repairs on July 27, 2011.

b. Findings

One finding of significance related to the original LER 05000259/2011-008-00 was documented in IR 05000259/2011005 (see Licensee Identified Violations Section 4OA7).

No additional findings were identified regarding the original or revised LER. These LERs are considered closed.

.4 Fire Event in the Turbine Building

a. Inspection Scope

On March 21, 2012, a fire occurred in the Unit 1 Turbine Building due to an overloaded 120 VAC circuit that was powering three submersible pumps. The inspectors performed an event follow up inspection of this fire to gather details surrounding this event. The inspectors reviewed the Main Control Room logs and interviewed Fire Operations and Operations on-shift personnel and verified no spurious alarms or spurious safety-related equipment operation. The inspectors performed a walkdown of the 557 elevation of the Turbine Building where the fire occurred to verify the extent of fire damage. It was determined that three extension cords were placed in series to achieve the length necessary to support the work. A ground fault circuit interrupter (GFCI) device was connected at the end of these extension cords, not at the electrical outlet. The three submersible pumps were plugged into the GFCI. Each submersible pump was rated for 9 amps. The 120 VAC outlet that the three submersible pumps were being powered from was rated for 20 amps. The licensee determined that the circuit breaker for this power outlet tripped four separate times and was reset each time until a fault occurred at the plugs connecting the two extension cords. These actions resulted in a small electrical fire. The licensee performed additional inspections of the plant and either removed extension cords where not in use or verified each extension cord had a GFCI as required. The inspectors performed walkdowns of additional plant areas for proper extension cord use.

b. Findings

One finding was identified.

Introduction:

The NRC identified a Green NCV of Technical Specifications 5.4.1.d, Fire Protection Program implementation associated with the licensees failure to report a fire in the Unit 1 Turbine Building to the main control room (MCR). Specifically, the failure to report a plant fire resulted in a failure of the MCR operators to implement Emergency Plan Implementing Procedure EPIP-17, Fire Emergency Response.

Description:

On March 21, 2012, a plant worker discovered an electrical extension cord on fire on the 557 elevation of the Unit 1 Turbine Building. The worker contacted a member of Fire Operations who was in the vicinity performing inspections of fire protection equipment. The Fire Operations member immediately acted to put out the fire by unplugging the burning extension cord and extinguished the fire with a carbon dioxide (CO2) extinguisher. The turbine building auxiliary unit operator (AUO) was contacted to unplug the remaining extension cord from the power outlet. The Fire Operations Dispatch Report stated the fire was extinguished within 1 minute upon notification to a member of the Fire Operations staff. After the fire was extinguished, the Fire Operations member contacted the Unit 1 Unit Supervisor in an attempt to locate the Shift Manager.

The Shift Manager was touring the Turbine Building around the same time and was notified of the fire. The Shift Manager went to the scene of the fire and concurred the fire was out and determined the scene where the fire occurred was safe. The Fire Operations Shift Captain was also notified of the fire and arrived at the scene to document the fire event and extension cord damage. The licensee determined that the cause of the extension cord fire was an overloaded circuit. Specifically, a ground fault circuit interrupter (CFGI) device was improperly connected at the end of these extension cords and three submersible pumps were plugged into the GFCI. Each submersible pump was rated for nine

(9) amps. The 120VAC outlet that the three submersible pumps were being powered from was rated for twenty
(20) amps. The licensee determined that the circuit breaker for this power outlet tripped four times and was reset each time until a fault occurred at the plugs connecting two extension cords and resulted in a small electrical fire.

The inspectors challenged the licensees response to the fire and questioned why the personnel involved did not immediately report the fire to the MCR using the phone number for plant emergencies. The sites Plant Access Training (PAT000) instructed all plant personnel to report fires immediately by dialing 3911 on an installed plant phone and to alert others in the area. Emergency Plan Implementing Procedure EPIP-17, Fire Emergency Response, required the MCR to initiate the Fire Alarm bell, announce the fire location over the plants public address system and notify the Fire Protection personnel and the Shift Manager of the fire. Because the MCR was not immediately notified of the fire in the Unit 1 Turbine Building, EPIP-17, was not entered, the Fire Alarm bell was not initiated, and the Fire Brigade was not contacted to respond to the fire. The licensee entered this event into their corrective action program as PER 527090.

Analysis:

Failure to immediately report a fire in the Unit 1 Turbine Building was a performance deficiency. As a result, the MCR was not immediately notified of a plant fire and EPIP-17, Fire Emergency Response, was not implemented. The performance deficiency was determined to be more than minor because if left uncorrected, the failure to notify the MCR of plant fire events would have the potential to lead to a more significant safety concern. Specifically, emergency response procedures for plant fires would not be implemented and Fire Brigade response would be delayed. The finding was associated with the Initiating Events Cornerstone and initially characterized according to IMC 0609, Significance Determination Process (SDP), Attachment 4, Phase 1 - Initial Screening and Characterization of Findings. The results of this analysis required an evaluation in accordance with IMC 0609, Appendix F, Attachment 1, Part 1, Fire Protection SDP Phase 1 Worksheet. For the SDP Phase 1 evaluation a low degradation rating was assigned for this fire event because it was a small electrical fire with no combustible material within the vicinity of the fire. Additionally, the licensee had previously established one-hour roving fire watches in place throughout the plant to meet other requirements with specific training to immediately report fires to the MCR. The finding was determined to be of very low safety significance (Green). The cause of this finding was directly related to the cross cutting aspect of Procedural Compliance in the Work Practices component of the Human Performance area, because the licensee failed to recognize the requirement to immediately report a fire and enter the appropriate fire emergency response procedures H.4(b).

Enforcement:

Technical Specifications 5.4.1.d, Fire Protection Program implementation requires in part that the licensee will establish, implement and maintain written procedures covering implementation of the Fire Protection Program. Contrary to this requirement, licensee personnel failed to implement EPIP-17, Fire Emergency Response, for a fire in the Unit 1 Turbine Building, on March 21, 2012. Following the event, plant staff performed additional inspections of plant areas and either removed electrical extension cords or ensured each cord had a required GFCI and was not overloaded. Expectations for plant employees discovering and responding to fires were reinforced by plant management. Because the violation was of very low safety significance and has been entered into the licensees CAP as PER 527090, this violation is being treated as an NCV consistent with the NRC Enforcement Policy. This NCV is identified as NCV 05000259, 260, 296/2012002-02, Failure to Implement Fire Protection Program Procedures.

4OA5 Other Activities

.1 Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope

During the inspection period, the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status reviews and inspection activities.

b. Findings

No findings were identified.

.2 Operation of an Independent Spent Fuel Storage Installation (ISFSI)

a. Inspection Scope

The inspectors observed operations involving independent spent fuel storage installation-related activities, interviewed personnel, and reviewed licensee documentation to verify that the ISFSI-related programs and procedures fulfilled the commitments and requirements specified in the Safety Analysis Report (SAR); the Certificate of Compliance (CoC), including the technical specifications (TSs); and 10 CFR Part 72, including 10 CFR 72.48 evaluations and 10 CFR 72.212(b) evaluations for general licensed ISFSIs. In addition, the inspectors observed selected ISFSI-related activities and conducted independent evaluations to ensure that the licensee performed spent fuel loading and transport in a safe manner and in compliance with approved procedures.

The inspectors reviewed six 10 CFR 72.48 Screening Reviews for several ISFSI procedures and verified that all changes were consistent with the license and CoC, and did not reduce program effectiveness.

The inspectors attended a pre-job briefing and observed operations in the field including overall supervisory involvement, coordination, and oversight of ISFSI-related work activities. The inspectors observed lifting of a loaded HI-TRAC cask and the transfer of the multi-purpose canister (MPC) into the HI-STORM cask via the stack up configuration. The inspectors noted that the field supervisor maintained strict control of the work package and continually verified that procedural steps were followed and completed as required. The inspectors reviewed the fuel loading plan for MPC-0237 (the MPC being transported to the ISFSI pad during this inspection) and verified that the fuel assemblies identified were properly selected and loaded in accordance with characterization documents and approved procedures. The inspectors also reviewed the fuel loading plans for selected other MPCs which had been previously loaded and transported to the ISFSI pad and verified that the fuel assemblies identified were properly selected and loaded.

The inspectors verified that selected individuals had received the necessary training in accordance with approved procedures for their ISFSI-related job duties.

The inspectors reviewed a self-assessment report, two QA audits, and a benchmarking report conducted by the licensee to evaluate the effectiveness of the licensees management oversight and QA assessments of ISFSI activities.

The inspectors reviewed the Dry Cask Radiological Work Permit, the As Low As Reasonably Achievable (ALARA) Planning Report, and dose estimates for the current ISFSI campaign. The inspectors noted that the ALARA plan was comprehensive with appropriate radiological controls established to minimize personnel exposures. The inspectors observed effective contamination control techniques and dose control measure implementation in the field. Radiological conditions were effectively communicated to individuals throughout the task. Radiological surveys of the loaded cask were obtained to ensure that radiation levels and contamination levels met the requirements of the CoC for safe storage of the HI-STORM cask at the ISFSI. The inspectors discussed the retention and maintenance of ISFSI-related records with station personnel and noted that appropriate arrangements had been made to maintain these records. The inspectors also reviewed the special nuclear material (SNM) inventory forms of SPP-5.8, Special Nuclear Material Control, for MPC-0234 and two others from previously loaded HI-STORM casks on the ISFSI pad.

The inspectors walked down the transfer path from the truck bay, where the MPC is loaded into the HI-STORM, to the ISFSI pad to verify that fire and explosive controls were being implemented in accordance with CoC surveillance requirements.

The inspectors determined that the licensee had established, maintained, and implemented adequate control of dry cask processing operations, including loading, transportation, and storage per approved procedures and that technical specification requirements and acceptance criteria as outlined in the Final Safety Analysis Report were followed appropriately. Records of spent fuel stored at the facility were properly maintained. The inspectors verified that changes to the design and operation were appropriately evaluated under 10 CFR 72.48. The inspectors determined that radiation protection controls were adequately established and implemented.

b. Findings

No findings were identified.

.3 (Closed) Unresolved Item (URI) 05000259, 260 and 296/2011003-03, Use of

Inappropriately Qualified Methods to Evaluate Emergency Core Cooling During Accident Mitigation

a. Inspection Scope

The NRC inspection staff reviewed the licensee actions taken as a result of the failure to maintain an error in the ECCS Evaluation Model ECCS Evaluation Model described in EMF-2361(P)(A), EXEM BWR-2000 ECCS Evaluation Model.

b. Findings

This URI is considered closed with one NRC identified findings and one NRC identified Violation.

(1)

Introduction:

The NRC identified a Green non-cited violation of 10CFR 50.46, Acceptance criteria for emergency core cooling systems for light-water nuclear power reactors, for the licensees failure to ensure that the ECCS was satisfactorily designed such that the maximum fuel element cladding temperature specified in 10 CFR 50.46(b)would not be exceeded.

Description:

During discussions between the NRC staff, the fuel vendor, and the licensee starting in April 2010, the NRC staff questioned the appropriateness of the application of credit for spray cooling in the Units 2 and 3 ECCS evaluation and the effect non-single failure proof ADS would have on the ECCS evaluation model for the BFN units.

In a letter dated April 30, 2010 the licensee acknowledged the single failure issue and committed to modify the ADS to provide a single failure proof automatic initiation capability of 4 ADS valves. The licensee also outlined the compensatory measures intended to address the identified degraded/nonconforming condition. Additionally, the licensee committed to bring the ADS into compliance on Unit 3, during the spring 2012 outage and to Unit 2, during the spring 2013 outage.

In Inspection Report 0500259,260, 296/2011003, the inspectors reviewed Calculation ANP-2908(P), Browns Ferry Units 1, 2, and 3 105% OLTP [loss of coolant accident]

LOCA Break Spectrum

Analysis.

The inspectors determined that the analysis, which used the ECCS Evaluation Model described in EMF-2361(P)(A) was not an adequate evaluation for application at Browns Ferry. The Browns Ferry ECCS evaluation was unique for two reasons:

(1) in most BWR cases, the ADS was single failure-proof; however, for Browns Ferry it was not, and
(2) the most severe postulated LOCA were those arising from small breaks, rather than a large break. Therefore, certain aspects of the approved evaluation model were not applicable to the unique plant configuration at Browns Ferry. The unique plant configuration was associated with an error made by the fuel vendor regarding the proper application of credit for spray cooling of fuel bundles during a small break LOCA. The NRC staffs observation was documented by the licensee in PER 372764 on May 21, 2011. This error was only applicable to Units 2 and 3, as Unit 1 operated with a different fuel type.,

Because of the misapplication of spray cooling, the evaluation model described in EMF-2361(P)(A) was not entirely applicable to Units 2 and 3 while the ADS system design was considered to be non-single-failure-proof. The single failure issue involved a loss of the 250 volts- direct current (VDC) battery supplying power to Reactor Motor Operated Valve (RMOV) Board B. Both logic trains of automatic ADS initiation instrumentation were powered from RMOV Board B; consequently, loss of power to the board resulted in the loss of all automatic ADS function.

When the error was evaluated by the NRC staff consistent with Appendix K to 10 CFR 50 requirements, as illustrated in the Figure 6.19, of ANP-2908(P), the NRC staff determined that the fuel cladding temperature increase would continue until the time of rated core spray (CS) flow. At 500 seconds, the calculated peak cladding temperature would exceed 2200 degrees Fahrenheit, resulting in a high possibility of fuel failure.

The licensee entered the issue into the CAP as PER 372764 and instituted reactor protection system thermal limit compensatory measures on May 29, 2011.

Analysis:

The inspectors determined that the licensees failure to ensure that the ECCS was satisfactorily designed such that the maximum fuel element cladding temperature would not be exceeded was a performance deficiency. Specifically, the licensee failed to accurately maintain design control regarding single-failure assumptions for the ECCS and perform sufficiently bounding analyses to ensure that the calculated maximum fuel element cladding temperature of 2200 degrees Fahrenheit was not exceeded.. This performance deficiency was considered greater than minor because it was associated with the Design Control attribute of the Barrier Integrity Cornerstone and adversely affected the cornerstone objective of providing reasonable assurance that the physical design barriers protect the public from radionuclide releases caused by accidents.

Specifically, the failure to maintain the ADS single-failure proof, coupled with an ECCS modeling error, resulted in the failure of the design of the ECCS to ensure that the calculated maximum fuel element cladding temperature would not be exceeded in the event of a small break LOCA. The inspectors assessed the finding using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP), Attachment 4, and was determined to be of very low safety significance (Green), based on the remaining barriers to fission product release were unaffected.

The cause of this finding was directly related to the cross-cutting aspect of Issue Identification in the Corrective Action Program component of the Problem Identification and Resolution area because the licensee failed to completely, accurately, and in a timely manner identify the errors with the ECCS evaluation model [P.1.(a)].

Enforcement:

10 CFR Section 50.46 (a)(1)(i), requires, in part, that each boiling water nuclear power reactor be provided with an ECCS that is designed to ensure that the calculated cooling performance following postulated LOCAs does not exceed a calculated maximum fuel element cladding temperature of 2200 degrees Fahrenheit.

Contrary to the above, from April 16, 2010 to May 29, 2011, the BFN Units 2 and 3 ECCS evaluation model, EMF-2361(P)(A), EXEM BWR 2000 ECCS Evaluation Model, the implementation and results for which are provided in ANP-2908(P), Browns Ferry Units 1, 2, and 3 105% OLTP [Original Licensed Thermal Power] LOCA Break Spectrum Analysis, failed to ensure that the ECCS was satisfactorily designed such that the maximum fuel element cladding temperature of 2200F would not be exceeded in the event of a small break LOCA. On May 29, 2011, operating limitations were implemented to account for the error in calculations. Because the finding was determined to be of very low safety significance (Green) and has been entered into the licensees CAP as PER 372764, this violation is being treated as an NCV consistent with the Enforcement Policy. This NCV is identified as NCV 05000260(296)/2012002-03, Failure to Ensure ECCS Design Calculation Does Not Exceed Maximum Clad Temperature.

(2)

Introduction:

The NRC identified a SL-IV NCV of 10 CFR 50.46, Acceptance criteria for emergency core cooling systems for light-water nuclear power reactors, for the licensees failure to report a significant error discovered in their application of the ECCS model that affected the peak cladding temperature calculation.

Description:

During discussions between the NRC staff, the fuel vendor, and the licensee starting in April 2010, the NRC staff questioned the appropriateness of the application of credit for spray cooling in the Units 2 and 3 ECCS evaluation, and the effect non-single failure proof ADS would have on the ECCS evaluation model for the BFN units.

In a letter dated April 30, 2010 the licensee acknowledged the single failure issue with ADS and indicated that the estimated effect of the change or error on peak clad temperature (PCT) was not significant (greater than 50 degrees Fahrenheit). TVA committed to modify the ADS to provide a single failure proof automatic initiation capability of 4 ADS valves. The licensee also outlined the compensatory measures intended to address the identified degraded/nonconforming condition. Subsequently, on June 30, 2011, TVA submitted the annual ECCS evaluation model report and indicated a minor change to the radiative heat transfer model which resulted in a minor change in PCT for Units 2 and 3. On October 7, 2011, TVA submitted a revised ECCS analysis in support of a Unit 1 fuel transition request. This analysis provided a methodology change to address the evaluation model error associated with spray cooling, which had been identified by the NRC staff, and for which the licensee implemented operating restrictions to ensure that the effects of the error would not cause the predicted PCTs at Units 2 and 3 to exceed 2200F.. This analysis was also applicable for current operating conditions for Units 2 and 3 and was not previously reported to the NRC. NRC review identified that the effect of the evaluation model error would have resulted in greater than a 50 degree increase in predicted PCT for Units 2 and 3.

On February 29, 2012, TVA initiated Service Request 514121 which recognized that a 30-day report for a significant change in peak clad temperature consistent with 10 CFR 50.46 had not been submitted. As of March 30, 2012, TVA had not submitted the required 30-day report for a significant change in peak clad temperature consistent with 10 CFR 50.46 which was identified on February 29, 2012. Following the end of the reporting period, TVA submitted the required report per 10 CFR 50.46 on April 18, 2012.

Analysis:

The inspectors determined that the licensees repeated failure to report changes or errors in the ECCS analyses was a performance deficiency. The inspectors reviewed this issue in accordance with IMC 0612, Appendix B, and determined the performance deficiency did not constitute a Finding, but the failure to report impacted the regulatory process and was subject to traditional enforcement consistent with the discussion for Block 7, Figure 2, Paragraph 2.a.v. The violation was determined to be more than minor per the NRC Enforcement Manual, Section 2.10.F, since the NRC has evidence that this failure to report has occurred repeatedly. This violation was determined to be a Severity Level IV violation based on section 6.9 of the NRC Enforcement Policy.

Enforcement:

10 CFR 50.46 (a)(3)(ii), requires for each change to or error discovered in an acceptable evaluation model or in the application of such a model that affects the temperature calculation, the licensee shall report the nature of the change or error and its estimated effect on the limiting ECCS analysis to the Commission at least annually. If the change or error is significant, the applicant or licensee shall provide this report within 30 days and include with the report a proposed schedule for providing a reanalysis or taking other action as may be needed to show compliance with 10 CFR 50.46 requirements.

Contrary to the above, the licensee failed to report each change or error discovered in an acceptable evaluation model or in the application of such a model that affects the temperature calculation for Units 2 and 3. Specifically, from May 29, 2011 to April 18, 2012, the licensee failed to report a significant change in peak clad temperature associated with an error related to spray cooling to the NRC within 30 days, and include with the report a proposed schedule for providing reanalysis or taking other action as may be needed to show compliance. The licensee subsequently submitted the required report per 10 CFR 50.46. Because this violation was determined to be a Severity Level IV violation and was entered into the licensees CAP as PER 531752, this violation is being treated as an NCV consistent with the Enforcement Policy. This NCV is identified as NCV 05000260(296)/2012002-04, Repeated Failure to Report ECCS Analyses Methodology Change or Errors.

4OA6 Meetings, Including Exit

.1 Exit Meeting Summary

On March 30, 2012, regional inspectors presented the inspection results specifically associated with ISFSI activities via telephone with Michael Durr, Director of Engineering, and other members of the licensees staff.

On April 6, 2012, the resident inspectors presented the inspection results to Mr. Lang Hughes, Operations Manager, and other members of the licensees staff, who acknowledged the findings.

On April 13, 2012, the resident inspectors presented the inspection results specifically associated with closure of unresolved item (URI) 2011-003-03, Use of Inappropriately Qualified Methods to Evaluate Emergency Core Cooling System During Accident Mitigation, to Mr. Lang Hughes, Operations Manager, and other members of the licensees staff, who acknowledged the findings.

All proprietary information reviewed by the inspectors as part of routine inspection activities were properly controlled, and subsequently returned to the licensee or disposed of appropriately.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the licensee and was a violation of NRC requirements which met the criteria of the NRC Enforcement Policy for being dispositioned as a Non-Cited Violation.

  • Unit 1 Technical Specification 3.3.8.2, Reactor Protection System (RPS) Electric Power Monitoring, required that, for each in-service RPS motor generator set or alternate power supply, two RPS electric power monitoring assemblies be operable in Modes 1, 2, and 3; and in Modes 4 and 5 with any control rod withdrawn from a core cell containing one or more fuel assemblies. With one electric power monitoring assembly inoperable for one or both in-service power supplies, the associated in-service power supply(s) were required to be removed from service in 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in Mode 4 within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. In addition, TS 3.0.4 prohibited Mode changes with TS 3.3.8.2 not met. Contrary to this, on October 6, 2011, while performing an operability determination for the channel A RPS power monitoring system undervoltage trips, the licensee determined that the as-found undervoltage trip for the RPS 1A1 relay was less than the required TS acceptance criteria during multiple previous TS surveillances and that the RPS 1A1 relay was inoperable from April 30, 2007 to October 5, 2011. This TS violation was entered into the licensees CAP as PERs 413140 and 442914. The finding was determined to be of very low safety significance because the finding does not represent an actual loss of the RPS safety function in that the remaining operable channel A RPS electric power monitoring assembly still provided protection to the RPS bus powered components under degraded voltage conditions.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

K. Polson, Site Vice President
S. Bono, Plant General Manager
D. Hughes, Operations Manager
M. Durr, Director of Engineering
J. Boyer, Acting Assistant Director of Engineering
B. Bruce, Acting Systems Engineering Manager
D. Carter, TVA QA Program Manager
J. Emens, Nuclear Site Licensing Manager
A. Feltman, Emergency Preparedness Manager
J. Ferguson, Radiation Protection Support Superintendent
M. Hydas, Project Manager, Sequoyah Dry Cask Project
S. Kelly, Work Control Manager
D. Kettering, Electrical Systems Engineering Manager
R. King, Design Engineering Manager
P. Summers, Director of Safety and Licensing
Z. Martin, Corporate Nuclear Fuels
B. McNutt, Shift Manager
R. Norris, Radiation Protection Manager
S. Norris, Engineering Supervisor
P. Parker, Site Security Manager
E. Quidley, EDG Project Manager
R. Kerving, Performance Improvement Manager
M. Rasmussen, Operations Superintendent
H. Smith, Fire Protection Supervisor
J. Underwood, Chemistry Manager
C. Vaughn, Operations Superintendent
S. Walton, Electrical Maintenance Superintendent
M. Wilson, Director of Training
A. Yarbrough, BOP System Engineering Supervisor

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Opened and Closed

05000259, 260, 296/2012002-01 NCV Failure to Adequately Implement Impaired Fire Barrier and Detector Controls (Section 1R05)
05000259, 260, 296/2012002-02 NCV Failure to Immediately Report a Plant Fire (Section 4OA3.4)
05000260, 296/2012002-03 NCV Failure to Ensure ECCS Design Calculation Does Not Exceed Maximum Clad Temperature (Section 4OA5.3)
05000260, 296/2012002-04 NCV Repeated Failure to Report ECCS Analyses Methodology Change or Errors (Section 4OA5.3)

Closed

05000259/2011-009-00 LER As-Found Undervoltage Trip for the Reactor Protection System 1A1 Relay that Did Not Meet Acceptance Criteria During Several Surveillances (Section 4OA3.1)
05000259/2011-009-01 LER As-Found Undervoltage Trip for the Reactor Protection System 1A1 Relay that Did Not Meet Acceptance Criteria During Several Surveillances (Section 4OA3.1)
05000259/2010-003-00 LER Failure of a Low Pressure Coolant Injection Flow Control Valve (Section 4OA3.2)
05000259/2010-003-01 LER Failure of a Low Pressure Coolant Injection Flow Control Valve (Section 4OA3.2)
05000259/2010-003-02 LER Failure of a Low Pressure Coolant Injection Flow Control Valve (Section 4OA3.2)
05000259/2011-008-00 LER High Vibrations on High Pressure Coolant Injection Booster Pump Thrust Bearings (Section 4OA3.3)
05000259/2011-008-01 LER High Vibrations on High Pressure Coolant Injection Booster Pump Thrust Bearings (Section 4OA3.3)
05000259, 260, 296/2011-003-03 URI Use of Inappropriately Qualified Methods to Evaluate the Emergency Core Cooling System

Discussed

None

LIST OF DOCUMENTS REVIEWED