IR 05000259/2012005

From kanterella
Jump to navigation Jump to search
IR 05000259-12-005, 05000260-12-005, 05000296-12-005; on 10/01/2012 - 12/31/2012; Browns Ferry Nuclear Plant, Units 1, 2 and 3; Amended Integrated Report
ML14160B041
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 06/09/2014
From: Bartley J
Reactor Projects Region 2 Branch 6
To: James Shea
Tennessee Valley Authority
References
IR-12-005
Download: ML14160B041 (50)


Text

UNITED STATES une 9, 2014

SUBJECT:

BROWNS FERRY NUCLEAR PLANT - AMMENDED NRC INTEGRATED INSPECTION REPORT 05000259/2012005, 05000260/2012005, AND 05000296/2012005

Dear Mr. Shea:

This letter reissues Inspection Report 05000259/2012005, 05000260/2012005, and 05000296/2012005 (ADAMS Accession number ML13039A321) with an amendment to Section 4OA5.3. This amendment adds the independent inspection portion of Temporary Instruction (TI) 2515/188 - Inspection of Near-Term Task Force Recommendation 2.3 Seismic Walkdowns, that was performed by the NRC staff. This revision also identifies TI 2515/188 as Closed in the List of Items Opened, Closed and Discussed.

On December 31, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Browns Ferry Nuclear Plant, Units 1, 2, and 3. The enclosed inspection report documents the inspection results which were discussed on January 11, 2013, with Mr.

Steve Bono, General Manager Site Operations, and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations, orders, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Two licensee-identified violations of very low safety significance (Green) were identified during the inspection. The NRC is treating the violations as a non-cited violations (NCV) consistent with Section 2.3.2 of the Enforcement Policy. If you contest this non-cited violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001, with copies to: (1) the Regional Administrator, Region II; (2) the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and (3) the NRC Resident Inspector at the Browns Ferry Nuclear Plant. In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any), will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html.

Sincerely,

/RA/

Jonathan H. Bartley, Chief Reactor Projects Branch 6 Division of Reactor Projects Docket Nos.: 50-259, 50-260, 50-296 License Nos.: DPR-33, DPR-52, DPR-68

Enclosure:

NRC Integrated Inspection Report 05000259/2012005, 05000260/2012005, and 05000296/2012005

REGION II==

Docket Nos.: 50-259, 50-260, 50-296 License Nos.: DPR-33, DPR-52, DPR-68 Report No.: 05000259/2012005, 05000260/2012005, 05000296/2012005 Licensee: Tennessee Valley Authority (TVA)

Facility: Browns Ferry Nuclear Plant, Units 1, 2, and 3 Location: Corner of Shaw and Nuclear Plant Roads Athens, AL 35611 Dates: October 1, 2012, through December 31, 2012 Inspectors: D. Dumbacher, Senior Resident Inspector C. Stancil, Resident Inspector P. Niebaum, Resident Inspector L. Pressley, Resident Inspector T. Stephen, Resident Inspector D. Hardage, Resident Inspector L. Suggs, Senior Construction Project Inspector (4OA2.5)

A. Sengupta, Reactor Inspector (1R08, 4OA5.3)

J. Laughlin, Emergency Preparedness Inspector (1EP4)

C. Kontz, Senior Project Engineer (4OA5.4)

G. Laska, Senior Operations Engineer (1R11.3)

K. Schaaf, Operations Engineer (1R11.3)

R. Baldwin, Senior Operations Engineer (1R11.4)

Approved by: Eugene F. Guthrie, Chief Reactor Projects Special Branch Division of Reactor Projects Enclosure

SUMMARY

IR 05000259/2012005, 05000260/2012005, 05000296/2012005; 10/01/2012-12/31/2012;

Browns Ferry Nuclear Plant, Units 1, 2 and 3; Event Follow-up and Identification and Resolution of Problems The report covered a three month period of inspection by the resident inspectors, three regional inspectors, and one headquarters inspector. Two licensee-identified violations of very low safety significance (Green) were identified. The significance of most findings is identified by their color (Green, White, Yellow, and Red) using Inspection Manual Chapter (IMC) 0609,

Significance Determination Process (SDP). The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process Revision 4, dated December 2006.

NRC Identified and Self-Revealing Findings

None

Licensee Identified Violations

Two violations of very low safety significance, which were identified by the licensee, have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. This violations and the corrective action program tracking numbers are described in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Unit 1 operated at full Rated Thermal Power (RTP) except for one planned downpower to support the refueling outage (U1R9). On October 20, 2012 the unit was shutdown for a scheduled refueling outage that lasted 45 days. The unit was restarted on December 4, 2012 and returned to full power on December 7, 2012. The unit remained at near full power the remainder of the quarter.

Unit 2 operated at full RTP except for 3 planned downpowers and 1 unplanned SCRAM. On October 26, 2012, a planned downpower to 70 percent power was made for one day to complete Control Rod Sequence Exchange and SCRAM Time Testing. On November 23, 2012, a planned downpower to 95 percent power was made for Control Rod Sequence Exchange. On December 12, 2012, a planned downpower to 45 percent power was performed to enable maintenance on 2B recirculation pump Variable Frequency Drive, steam leak repairs to the 73-3 line, and repairs to 2B cond. booster pump. The plant returned to 100 percent power on December 14, 2012. On December 22, 2012, Unit 2 reactor automatically scrammed due to a post maintenance test failure associated with 3D emergency diesel and a wrong-train human performance error, respectively causing a loss of the 2B reactor protection subsystem and the 2A reactor protection subsystem. Unit 2 was restarted on December 25, 2012, and synchronized to the electrical grid on December 26, 2012. The unit remained at near full power the remainder of the quarter.

Unit 3 operated at full RTP power except for 3 planned downpowers. On October 15, 2012, a planned downpower to 60 percent power for one day to repair a steam leak on the 3A Feedwater drain line. On November 19, 2012, a planned downpower to 95 percent power for one day to repair a steam leak on 3C1/3C2 High Pressure Heaters. On December 14, 2012, a planned downpower to 60 percent power for control rod sequence exchange and turbine control valve testing. The unit remained at full power the remainder of the quarter.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01 Adverse Weather Protection

.1 Evaluate Readiness to Cope with External Flooding

a. Inspection Scope

The Inspectors reviewed licensee flood protection barriers and procedures for coping with external flooding. The inspection covered the FSAR and related flood analysis documents to identify those areas that can be affected by external flooding and seasonal susceptibilities such as floods caused by hurricanes, heavy rains and flash floods. The review covered design flood level documentation and corrective actions for safety related areas. The inspectors conducted a walkdown of the Unit Common intake structure Residual Heat Removal Service Water (RHRSW) pump rooms. Specific focus addressed: sealing of equipment below the flood line, such as electrical conduits; sealing of equipment floor plugs, holes or penetrations in floors and walls between flood areas; and adequacy of watertight doors between flood areas. This activity constitutes two External Flood Protection samples.

  • Common Intake Structure RHRSW pump room hatches and vents as part of Temporary Instruction (TI) -187, Independent Flooding Walkdowns
  • Licensee walkdown packages associated with RHRSW pump room and Diesel Generator building CO2 room watertight doors as part of Temporary Instruction (TI) -

187, Flooding Walkdowns

b. Findings

No findings were identified.

.2 Readiness for Seasonal Extreme Weather Conditions

a. Inspection Scope

Prior to and during the onset of cold weather conditions, the inspectors reviewed the licensees implementation of 0-GOI-200-1, Freeze Protection Inspection, including applicable checklists: Attachment 1, Freeze Protection Annual Checklist; Attachment 2, Freeze Protection Operational Checklist; and as applicable, Attachments 3 through 12, Freeze Protection Daily Log Sheets for individual watch stations. The inspectors also reviewed the list of open FZ-coded Work Orders and Problem Evaluation Reports (PERs) to verify that the licensee was identifying and correcting potential problems relating to cold weather operations. In addition, the inspectors reviewed procedure requirements and walked down selected areas of the plant, which included the main control rooms, Residual Heat Removal Service Water (RHRSW) and Emergency Equipment Cooling Water (EECW) pump rooms, and all units Emergency Diesel Generator (EDG) buildings, to verify that affected systems and components were properly configured and protected as specified by the procedure. The inspectors discussed cold weather conditions with Operations personnel to assess plant equipment conditions and personnel sensitivity to upcoming cold weather conditions. This constitutes one Readiness for Seasonal Extreme Weather sample.

b. Findings

No findings were identified.

1R04 Equipment Alignment

.1 Partial Walkdown

a. Inspection Scope

The inspectors conducted three partial equipment alignment walkdowns to evaluate the operability of selected redundant trains or backup systems, listed below, while the other train or subsystem was inoperable or out of service. The inspectors reviewed the functional systems descriptions, Updated Final Safety Analysis Report (UFSAR), system operating procedures, and Technical Specifications (TS) to determine correct system lineups for the current plant conditions. The inspectors performed walkdowns of the systems to verify that critical components were properly aligned and to identify any discrepancies which could affect operability of the redundant train or backup system.

This activity constituted three Equipment Alignment inspection samples.

b. Findings

No findings were identified.

1R05 Fire Protection

.1 Fire Protection Tours

a. Inspection Scope

The inspectors reviewed licensee procedures, Nuclear Power Group Standard Programs and Processes (NPG-SPP)-18.4.7, Control of Transient Combustibles, and NPG-SPP-18.4.6, Control of Fire Protection Impairments, and conducted a walkdown of five fire areas (FA) and fire zones (FZ) listed below. Selected FAs/FZs were examined in order to verify licensee control of transient combustibles and ignition sources; the material condition of fire protection equipment and fire barriers; and operational lineup and operational condition of fire protection features or measures. Also, the inspectors verified that selected fire protection impairments were identified and controlled in accordance with procedure NPG-SPP-18.4.6. Furthermore, the inspectors reviewed applicable portions of the Fire Protection Report, Volumes 1 and 2, including the applicable Fire Hazards Analysis, and Pre-Fire Plan drawings, to verify that the necessary firefighting equipment, such as fire extinguishers, hose stations, ladders, and communications equipment, was in place. This activity constituted five Fire Protection inspection samples.

  • Unit 1 Reactor Building, EL 593 1B Electrical Board Room (Fire Area 4)
  • Unit 2 Reactor Building, EL 593 2B Electrical Board Room (Fire Area 8)
  • Unit 3 Reactor Building, EL 519 through 639 (Fire Zone 3-1)
  • Unit 3 Reactor Building, EL 621 3A Electric Board Room (Fire Area 13)
  • Unit 3 Reactor Building, EL 621 3A 480 Shutdown Board Room, (Fire Area 14)

b. Findings

No findings were identified.

1R08 Inservice Inspection Activities

a. Inspection Scope

Non-Destructive Examination Activities and Welding Activities: From October 29, 2012, through November 1, 2012, the inspector conducted a review of the implementation of the licensees In-service Inspection (ISI) Program for monitoring degradation of the reactor coolant system, emergency feedwater systems, risk-significant piping and components, and containment systems. The inspectors reviewed the implementation of the licensees Risk Informed ISI program for monitoring degradation of the reactor coolant system (RCS) boundary and risk significant piping boundaries. The inspectors activities consisted of an on-site review of NDE and welding activities to evaluate compliance with the applicable edition of the ASME Boiler and Pressure Vessel Code (BPVC),Section XI (Code of record: 2001 Edition through 2003 Addendum) and that indications and defects (if present) were appropriately evaluated, and dispositioned in accordance with the requirements of the ASME Code,Section XI acceptance standards or NRC approved alternative requirement.

The inspectors directly observed or reviewed records of the following NDE mandated by the ASME Code to evaluate compliance with the ASME Code Section XI and Section V requirements, and if any indications or defects were detected, to evaluate if they were dispositioned in accordance with the ASME Code or an NRC-approved alternative requirement.

  • Directly observed:

o Work Order # 112507860, Ultrasonic examination (UT) (manual) of Instrument Nozzle Safe End Welds in Feedwater System

  • Reviewed records:

o Work Order # 114009989, UT of HPCI System, pipe to flange o Work Order # 1-SI-4.6.G, Visual Examination of RHR System of Weld # 1-47B452H0158 o Work Order # 1-SI-4.6.g, Magnetic particle Testing (MT) of RHR System of Weld

  1. 1-47B452H0158-IA o Work Order # 114009989, Radiography Examination of HPCI system, Turbine Steam Supply Valve During non-destructive surface and volumetric examinations performed since the previous refuelling outage, the licensee did not identify any recordable indications that required acceptance for continued service, therefore, no NRC review was required for this inspection procedure attribute.

The inspectors reviewed documentation for the repair/replacement of the following pressure boundary welds. The inspectors evaluated if the licensee applied the pre-service non-destructive examinations and acceptance criteria required by the construction Code. In addition, the inspectors reviewed the welding procedure specifications, welder qualifications, welding material certifications, and supporting weld procedure qualification records to evaluate if the weld procedures were qualified in accordance with the requirements of the Construction Code and the ASME Code Section IX.

Identification and Resolution of Problems: The inspectors performed a review of ISI-related problems, including welding that were identified by the licensee and entered into the Corrective Action Program (CAP) as Condition Report (CRs). The inspectors reviewed the CRs to confirm that the licensee had appropriately described the scope of the problem, description of the evaluation and had identified appropriate corrective actions. The review also included the review of the licensees use, consideration and assessment of operating experience events applicable to the plant. The inspectors performed this review to ensure compliance with 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requirements. Document reviewed are listed in the Attachment.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification

.1 Resident Inspector Quarterly Review

a. Inspection Scope

On October 17, 2012, the inspectors observed a licensed operator requalification simulator examination for an operating crew according to a Unit 2 Simulator Exercise Guide, (SEG), scenario which contained at a minimum the following attributes; main generator hydrogen leak, loss of offsite power (LOOP), inadvertent pump start, failure to scram, unisolable reactor core isolation cooling (RCIC) system leak, fuel element failure.

The inspectors specifically evaluated the following attributes related to the operating crews performance:

  • Clarity and formality of communication
  • Ability to take timely action to safely control the unit
  • Prioritization, interpretation, and verification of alarms
  • Correct use and implementation of procedures including Abnormal Operating Instructions (AOIs), and Emergency Operating Instructions (EOIs)
  • Timely control board operation and manipulation, including high-risk operator actions
  • Timely oversight and direction provided by the shift supervisor, including ability to identify and implement appropriate technical specifications actions such as reporting and emergency plan actions and notifications
  • Group dynamics involved in crew performance The inspectors assessed the licensees ability to administer testing and assess the performance of their licensed operators. The inspectors attended the post-examination critique performed by the licensee evaluators, and verified that licensee-identified issues were comparable to issues identified by the inspector. The inspectors also reviewed simulator physical fidelity (i.e., the degree of similarity between the simulator and the reference plant control room, such as physical location of panels, equipment, instruments, controls, labels, and related form and function). This activity constitutes one Resident Inspector quarterly review of Licensed Operator requalification inspection sample.

b. Findings

No findings were identified.

.2 Control Room Observations

a. Inspection Scope

Inspectors observed and assessed licensed operator performance in the plant and main control room, particularly during periods of heightened activity or risk and where the activities could affect plant safety. Inspectors reviewed various licensee policies and procedures such as OPDP-1, Conduct of Operations, NPG-SPP-10.0, Plant Operations and GOI-100-12, Power Maneuvering.

Inspectors utilized activities such as post maintenance testing, surveillance testing and refueling and other outage activities to focus on the following conduct of operations as appropriate;

  • Operator compliance and use of procedures.
  • Control board manipulations.
  • Communication between crew members.
  • Use and interpretation of plant instruments, indications and alarms.
  • Use of human error prevention techniques.
  • Documentation of activities, including initials and sign-offs in procedures.
  • Supervision of activities, including risk and reactivity management.
  • Pre-job briefs.

This activity constituted one Control Room Observation inspection sample.

b. Findings

No findings were identified.

.3 Biennial Licensed Operator Requalification

a. Inspection Scope

The inspectors reviewed the facility operating history and associated documents in preparation for this inspection. During the week of October, 8-11, 2012, the inspectors reviewed documentation, interviewed licensee personnel, and observed the administration of operating tests associated with the licensees operator requalification program. Each of the activities performed by the inspectors was done to assess the effectiveness of the facility licensee in implementing requalification requirements identified in 10 CFR Part 55, Operators Licenses. The evaluations were also performed to determine if the licensee effectively implemented operator requalification guidelines established in NUREG-1021, Operator Licensing Examination Standards for Power Reactors, and Inspection Procedure 71111.11, Licensed Operator Requalification Program. The inspectors also evaluated the licensees simulation facility for adequacy for use in operator licensing examinations using ANSI/ANS-3.5-1985, American National Standard for Nuclear Power Plant Simulators for use in Operator Training and Examination. The inspectors observed two shift crews during the performance of the operating tests. Documentation reviewed included written examinations, Job Performance Measures (JPMs), simulator scenarios, licensee procedures, on-shift records, simulator modification request records, simulator performance test records, operator feedback records, licensed operator qualification records, remediation plans, watchstanding records, and medical records. The records were inspected using the criteria listed in Inspection Procedure 71111.11. Documents reviewed are listed in the Attachment.

The inspectors selected PER 245312 Reactivity Management [Control] Plan (RCP)requires improvement for a detailed review. PER 245312 states: Review of a completed RCP for the Unit 3 down power and shutdown and other RCPs indicated a lack of rigor in the execution of some of the RCP steps. Incomplete guidance on a number of the RCP steps, and some knowledge discrepancies exist. The Quality Assurance group recommended that additional training be developed for operators and to improve implementing reactivity management plans. The training department developed training on reactivity management plans that was delivered to the operations, group. The reactor engineering group was invited to attend these training sessions to add additional technical knowledge. Inspectors reviewed the training presentations developed for the additional training. It appears this training was effective.

b. Findings

No findings were identified.

.4 Annual Review of Licensee Requalification Examination Results

a. Inspection Scope

On December 12, 2012, the licensee completed the annual requalification operating examinations required to be administered to all licensed operators in accordance with 10 CFR 55.59(a)(2). The inspectors performed an in-office review of the overall pass/fail results of the individual operating examinations and the crew simulator operating examinations in accordance with Inspection Procedure (IP) 71111.11, Licensed Operator Requalification Program. These results were compared to the thresholds established in Inspection Manual Chapter (IMC) 0609, Significance Determination Process, Appendix I, Operator Requalification Human Performance Significance Determination Process.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

.1 Routine

a. Inspection Scope

The inspectors reviewed the two specific structures, systems and components (SSC)within the scope of the Maintenance Rule (MR) (10 CFR 50.65) with regard to some or all of the following attributes, as applicable:

(1) Appropriate work practices;
(2) Identifying and addressing common cause failures;
(3) Scoping in accordance with 10 CFR 50.65(b) of the MR;
(4) Characterizing reliability issues for performance monitoring;
(5) Tracking unavailability for performance monitoring;
(6) Balancing reliability and unavailability;
(7) Trending key parameters for condition monitoring;
(8) System classification and reclassification in accordance with 10 CFR 50.65(a)(1) or (a)(2);
(9) Appropriateness of performance criteria in accordance with 10 CFR 50.65(a)(2); and
(10) Appropriateness and adequacy of 10 CFR 50.65 (a)(1) goals, monitoring and corrective actions (i.e., Ten Point Plan). The inspectors also compared the licensees performance against site procedure NPG-SPP-3.4, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting; Technical Instruction 0-TI-346, Maintenance Rule Performance Indicator Monitoring, Trending and Reporting; and NPG-SPP 3.1, Corrective Action Program. The inspectors also reviewed, as applicable, work orders, surveillance records, PERs, system health reports, engineering evaluations, and MR expert panel minutes; and attended MR expert panel meetings to verify that regulatory and procedural requirements were met. This activity constituted two Maintenance Effectiveness inspection samples.
  • Browns Ferry Valve Stem Packing Program

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation

a. Inspection Scope

For planned online work and/or emergent work that affected the combinations of risk significant systems listed below, the inspectors examined four on-line maintenance risk assessments, and actions taken to plan and/or control work activities to effectively manage and minimize risk. The inspectors verified that risk assessments and applicable risk management actions (RMA) were conducted as required by 10 CFR 50.65(a)(4)applicable plant procedures, and BFN Equipment to Plant Risk Matrix. Furthermore, as applicable, the inspectors verified the actual in-plant configurations to ensure accuracy of the licensees risk assessments and adequacy of RMA implementations. This activity constituted four Maintenance Risk Assessment inspection samples.

  • October 19, 2012, Unit 3 RPS 3A Motor Generator Set Failure with 3E Raw Cooling Water Pump and G Control and F Service Air Compressors Out of Service (OOS)
  • October 25, 2012, Units 1 and 2, C Shutdown Board, C EDG and RHRSW Pumps B2 and B3 OOS, 2B CCW Pump OOS, Unit 1 ORAM Yellow
  • November 1, 2012, Unit 1 Orange planned outage risk associated with local leak rate test of valve 74-68 (Operation with Potential to Drain the Reactor Vessel, OPDRV)
  • December 13, 2012, Unit 2 elevated Green risk for Single Loop Operations

b. Findings

No findings were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the operability/functional evaluations listed below to verify technical adequacy and ensure that the licensee had adequately assessed Technical Specification operability. The inspectors also reviewed applicable sections of the UFSAR to verify that the system or component remained available to perform its intended function. In addition, where appropriate, the inspectors reviewed licensee procedure NEDP-22, Functional Evaluations, and NEDP-27, Past Operability Evaluations, to ensure that the licensees evaluation met procedure requirements.

Furthermore, where applicable, inspectors examined the implementation of compensatory measures to verify that they achieved the intended purpose and that the measures were adequately controlled. The inspectors also reviewed PERs on a daily basis to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. This activity constituted six Operability Evaluation inspection samples.

  • Reactor Building South Access Watertight Door Broken Frame Weld (PER 623264)
  • Unit Common Standby Gas Treatment Train C Inoperable longer than allowed by Technical Specification (PERs 590208 and 604350)

b. Findings

No findings were identified.

1R18 Plant Modifications

.1 Permanent Plant Modifications

a. Inspection Scope

The inspectors reviewed the Design Change Notice (DCN) and completed work package (WO 113086731) for DCN 70488, Replace Unit 1 HPCI 73-16 gate valve with a different design gate valve, including related documents and procedures. The inspectors reviewed licensee procedures NPG-SPP-9.3, Plant Modifications and Engineering Change Control, and NPG-SPP-6.9.3, Post-Modification Testing, and observed part of the licensee=s activities to implement this design change made while the unit was online.

The inspectors reviewed the associated 10 CFR 50.59 screening against the system design bases documentation to verify that the modifications had not affected system operability/availability. The inspectors reviewed selected ongoing and completed work activities to verify that installation was consistent with the design control documents.

b. Findings

No findings were identified.

1R19 Post Maintenance Testing

a. Inspection Scope

The inspectors witnessed and reviewed the four post-maintenance tests (PMT) listed below to verify that procedures and test activities confirmed SSC operability and functional capability following the described maintenance. The inspectors reviewed the licensees completed test procedures to ensure any of the SSC safety function(s) that may have been affected were adequately tested, that the acceptance criteria were consistent with information in the applicable licensing basis and/or design basis documents, and that the procedure had been properly reviewed and approved. The inspectors also witnessed and/or reviewed the test data, to verify that test results adequately demonstrated restoration of the affected safety function(s). The inspectors verified that PMT activities were conducted in accordance with applicable WO instructions, or licensee procedural requirements. Furthermore, the inspectors verified that problems associated with PMTs were identified and entered into the CAP. This activity constituted four Post Maintenance Test inspection samples.

Diesel Generator 3C Monthly Operability Test

b. Findings

No findings were identified.

1R20 Refueling and Other Outage Activities

.1 Unit 1 Scheduled Refueling Outage (U1R9)

a. Inspection Scope

From October 20, 2012, through December 4, 2012, the inspectors examined critical outage activities to verify that they were conducted in accordance with Technical Specifications, applicable plant procedures, and the licensees outage risk assessment and management plans. The inspectors also monitored critical plant parameters, and observed operator control of plant conditions, during Cold Shutdown (Mode 4), Startup (Mode 2), and Power Operation (Mode 1). Some of the significant outage activities specifically reviewed and/or witnessed by the inspectors were as follows:

Outage Risk Assessment Prior to the U1R9 refueling outage that began on October 20, the inspectors attended outage risk assessment team meetings and reviewed the Outage Risk Assessment Report to verify that the licensee had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing an outage plan that assured defense-in-depth of safety functions were maintained. The inspectors also reviewed the daily U1R9 Refueling Outage Reports, including the Outage Risk Assessment Management (ORAM) Safety Function Status, and regularly attended the twice a day outage status meetings. These reviews were compared to the requirements in licensee procedure SPP-7.2, Outage Management, and TS. These reviews were also done to verify that for identified high risk significant conditions, due to equipment availability and/or system configurations, contingency measures were identified and incorporated into the overall outage and contingency response plan. Furthermore, the inspectors frequently discussed risk conditions and designated protected equipment with Operations and outage management personnel to assess licensee awareness of actual risk conditions and mitigation strategies.

Shutdown and Cooldown Process The inspectors witnessed the shutdown and cooldown of Unit 1 in accordance with licensee procedures OPDP-1, Conduct of Operations; 1-GOI-100-12A, Unit Shutdown from Power Operations to Cold Shutdown and Reduction in Power During Power Operations; and 1-SR-3.4.9.1(1), Reactor Heatup or Cooldown Rate Monitoring.

Decay Heat Removal The inspectors reviewed licensee procedures 1-OI-74, Residual Heat Removal System (RHR); 1-OI-78, Fuel Pool Cooling and Cleanup System; and Abnormal Operating Instruction 0-AOI-72-1, Alternate Decay Heat Removal System Failures; and conducted a main control room panel and in-plant walkdowns of system and components to verify correct system alignment. During planned evolutions that resulted in increased outage risk conditions for shutdown cooling, inspectors verified that the plant conditions and systems identified in the risk mitigation strategy were available. In addition, the inspectors reviewed controls implemented to ensure that outage work was not impacting the ability of operators to operate spent fuel pool cooling, RHR shutdown cooling, and/or Alternate Decay Heat Removal (ADHR) system. Furthermore, the inspectors conducted several walkdowns of the ADHR system during operation with the fuel pool gates removed.

Critical Outage Activities The inspectors examined outage activities to verify that they were conducted in accordance with TS, licensee procedures, and the licensees outage risk control plan.

Some of the more significant inspection activities accomplished by the inspectors were as follows:

  • Walked down selected safety-related equipment clearance orders (i.e., tag order 1-TO-2012-0003, sections 1-074-0016 and 1-074-0017A for 1D RHR Pump motor and rotating element replacements
  • Verified electrical systems availability and alignment
  • Monitored important control room plant parameters (e.g., RCS pressure, level, flow, and temperature) and TS compliance during the various shutdown modes of operation, and mode transitions
  • Evaluated implementation of reactivity controls
  • Reviewed control of containment penetrations and overall integrity
  • Examined foreign material exclusion controls particularly in proximity to and around the reactor cavity, equipment pit, and spent fuel pool
  • Routine tours of the control room, reactor building, refueling floor and drywell
  • Verified the licensee was managing fatigue by review of fatigue assessments and review of certain outage and non-outage workers schedules and work hours (There were no waiver requests or self declarations.)

Reactor Vessel Disassembly and Refueling Activities The inspectors witnessed selected activities associated with reactor vessel disassembly, and reactor cavity flood-up and drain down in accordance with 1-GOI-100-3A, Refueling Operations (Reactor Vessel Disassembly and Floodup). Also, on numerous occasions, the inspectors witnessed fuel handling operations during the two Unit 1 reactor core fuel shuffles performed in accordance with TS and applicable operating procedures, such as 0-GOI-100-3A, Refueling Operations (In Vessel), 0-GOI-100-3B, Operations in the Spent Fuel Pool, and 0-GOI-100-3C, Fuel Movement Operations During Refueling. The inspectors verified specific fuel movements as delineated by the Fuel Assembly Transfer Sheets (FATF). Furthermore, the inspectors also witnessed and examined the video verification of the final completed reactor core conducted per Attachment 6, of 0-GOI-100-3C.

Torus Closeout On November 24, 2012, the inspectors reviewed the licensees conduct of 1-GOI-200-2, Torus Closeout, and performed an independent detailed closeout inspection of the Unit 1 Torus.

Drywell Closeout On November 27, 2012, the inspectors reviewed the licensees conduct of 1-GOI-200-2, Drywell Closeout, and performed an independent detailed closeout inspection of the Unit 1 drywell.

Restart Activities The inspectors specifically conducted the following:

  • Evaluated licensee actions and response to reactor vessel inner o-ring leakage.
  • Witnessed Unit 1 approach to criticality and power ascension per 1-GOI-100-1A, Unit Startup, and 1-GOI-100-12, Power Maneuvering
  • Reactor Coolant Heatup/Pressurization to Rated Temperature and Pressure per 1-SR-3.4.9.1, Reactor Heatup and Cooldown Rate Monitoring
  • Evaluated licensee decision (December 2, 2012,ODMI/PER 651334) to perform plant startup and operate plant with an existing reactor vessel inner o-ring leak Corrective Action Program The inspectors reviewed PERs generated during U1R9 and attended management review committee (MRC) meetings to verify that initiation thresholds, priorities, mode holds, operability concerns and significance levels were adequately addressed.

Resolution and implementation of corrective actions of several PERs were also reviewed for completeness.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors witnessed portions of, and/or reviewed completed test data for the following surveillance tests of risk-significant and/or safety-related systems to verify that the tests met TS surveillance requirements, UFSAR commitments, and in-service testing and licensee procedure requirements. The inspectors review confirmed whether the testing effectively demonstrated that the SSCs were operationally capable of performing their intended safety functions and fulfilled the intent of the associated surveillance requirement. This activity constituted five Surveillance Testing inspection samples, one in-service, two routine tests, one containment isolation test, and one reactor coolant system leak detection test.

In-Service Tests:

  • November 28, 2012, 1-SR-3.5.1.8, HPCI Main and Booster Pump Set Developed Head and Flow Rate Test at 150 psig Reactor Pressure Containment Isolation Valve Tests:
  • December 6, 2012, 3-SI-4.2.E-1(B), Drywell Equipment Drain Sump Flow Integrator Calibration

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP4 Emergency Action Level and Emergency Plan Changes

a. Inspection Scope

The NSIR headquarters staff performed an in-office review of the latest revisions of various Emergency Plan Implementing Procedures (EPIPs) and the Emergency Plan located under ADAMS accession numbers ML12296A649, ML12307A285, and ML12199A022 as listed in the Attachment.

The licensee determined that in accordance with 10 CFR 50.54(q), the changes made in the revisions resulted in no reduction in the effectiveness of the Plan, and that the revised Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. The NRC review was not documented in a safety evaluation report and did not constitute approval of licensee-generated changes; therefore, these revisions are subject to future inspection. Documents reviewed are listed in the Attachment. This inspection activity satisfied one inspection sample for the emergency action level and emergency plan changes on an annual basis.

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification

.1 Cornerstone: Initiating Events

a. Inspection Scope

The inspectors reviewed the licensees procedures and methods for compiling and reporting the PIs listed below, including procedure NPG-SPP-02.2. The inspectors examined the licensees PI data for the specific PIs listed below for the fourth quarter of 2011 through the third quarter of 2012. The inspectors compared the licensees raw data against graphical representations and specific values reported to the NRC for the third quarter of 2012 to verify that the data was correctly reflected in the report.

Furthermore, the inspectors validated this data against relevant licensee records (e.g.,

PERs, Daily Operator Logs, Plan of the Day, LERs, etc.), and assessed any reported problems regarding implementation of the PI program. Furthermore, the inspectors met with responsible plant personnel to discuss and go over licensee records to verify that the PI data was appropriately captured, calculated correctly, and discrepancies resolved.

The inspectors also used the Nuclear Energy Institute (NEI) 99-02, to ensure that industry reporting guidelines were appropriately applied. This activity constituted nine Performance Indicator Verification inspection samples; three unplanned scrams, three Unplanned Scrams with Complications, and three Unplanned Power Changes.

  • Unit 1 Unplanned Scrams with Complications
  • Unit 2 Unplanned Scrams with Complications
  • Unit 3 Unplanned Scrams with Complications

b. Findings

No findings were identified.

4OA2 Identification and Resolution of Problems

.1 Review of items entered into the Corrective Action Program:

As required by Inspection Procedure 71152, Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees CAP. This review was accomplished by reviewing daily PER and Service Request (SR) reports, and periodically attending Corrective Action Review Board (CARB) and PER Screening Committee (PSC) meetings.

.2 Annual Follow-up of Selected Issues

a. Inspection Scope

The inspectors reviewed the specific corrective actions associated with failed GE HFA Relays on Unit 2 (PER 618132) and Unit 3 (PER 571080).

b. Assessment and Observations The inspectors had the following observations:

The inspectors reviewed the impact, causal analysis, and corrective actions for five AC HFA relay failures that resulted in half-scrams from 2003 to 2012. The licensees apparent cause analysis for the failures concluded the relays were an older style and had thus failed due to insulation breakdowns. After the inspectors questioned this conclusion, the licensee determined that the glass enclosure for the relays which retained heat generated had not been factored into their life expectancy. Additionally, the inspectors questioned the licensees application of previous guidance related to replacement of HFA relays. Licensee follow-up identified that additional inspections were needed to ensure installed HFA relays were of a type capable of operating in the enclosure device.

Browns Ferry conducted walkdowns of approximately 2275 HFA relays on the three units to determine whether relays required replacement. Forty Four relays had to be replaced.

c. Findings

No findings were identified.

.3 Semiannual Review to Identify Trends

a. Inspection Scope

As required by Inspection Procedure 71152, the inspectors performed a review of the licensees CAP implementation and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review included the results from daily screening of individual PERs (see Section 4OA2.1 above),licensee trend reports and trending efforts, and independent searches of the PER database and WO history. The inspectors review nominally considered the six-month period of July 2012 through December 2012, although some searches expanded beyond these dates. Additionally, the inspectors review also included the Integrated Trend Reports (ITR) from the third and fourth quarters of fiscal year 2012. The licensee reports covered the period of April 1, 2012 to September 30, 2012. Furthermore, the inspectors verified that adverse or negative trends identified in the licensees PERs, periodic reports and trending efforts were entered into the CAP. Inspectors interviewed the appropriate licensee staff and also reviewed procedures, NPG-SPP-02.8, Integrated Trend Review and NPG-SPP-02.7, PER Trending.

The purpose of the licensees integrated trend reviews was to identify the top site and departmental issues (gaps to excellence) requiring management attention. Other objectives were to provide status of the top issues and their progress to resolution, identify continuing issues, emerging trends and issues to be monitored, review progress towards resolving past top issues, review issues identified by external organizations such as the NRC, INPO, Nuclear Safety Review Board (NSRB), QA, etc., and determine why they were not identified by line organizations.

b. Findings and Observations

No findings were identified. However, the inspectors had the following observations discussed below:

Inspectors noted that licensee-identified third and fourth quarter Corrective Action Program (CAP) and Human Performance issues continued from the first and second quarter 2012 trend reports. These issues were also identified as Fleet and Site top priorities. The majority of the key actions to resolve the gaps for these issues were still in progress. Trending information provided in the fourth quarter fiscal year 2012 report showed evidence of improvement in the CAP and Human Performance metrics. The sites Human Performance error rate metrics were indicating the best of the last two years.

In addition to reviewing the sites progress on the above issues, the inspectors conducted an independent review of the licensees CAP to identify potential adverse trends.

.4 Focused Annual Sample Review - Operator Workarounds

a. Inspection Scope

The inspectors conducted a review of existing Operator Workarounds (OWA) to verify that the licensee was identifying OWAs at an appropriate threshold, entering them into the corrective action program, establishing adequate compensatory measures, prioritizing resolution of the problem, and implementing appropriate corrective actions in a timely manner commensurate with its safety significance. The inspectors examined all active OWAs listed in the Limiting Condition of Operation Tracking (LCOTR) Log, and reviewed them against the guidance in BFN-ODM-4.16, Operator Workarounds/

Burdens/Challenges. The inspectors also discussed these OWAs in detail with on shift operators to assess their familiarity with the degraded conditions and knowledge of required compensatory actions. Furthermore, the inspector walked down selected OWAs, and verified the ongoing performance, and/or feasibility of, the required actions.

Lastly, for selected OWAs, the inspector reviewed the applicable PER, including the associated functional evaluation and corrective action plans (both interim and long term).

b. Findings and Observations

No findings were identified. However, the inspectors had the following observations which were discussed with the licensee:

Inspectors determined that, in general, Browns Ferry adequately tracks and trends all operator workarounds, burdens and challenges. This includes estimating, tracking and compiling the aggregate impact of the workarounds, burdens and challenges.

Inspectors identified multiple occasions where operations staff had routinely updated the progress of corrective actions within the confines of the software program designed to track OWAs (eSOMS). The licensee did self-identify that workarounds from equipment failures have adversely affected the time available for operators to perform their normal duties.

Inspectors reviewed trending information on workarounds, burdens and challenges which was reported weekly within the Browns Ferry Plan of the Day. Unit 1 and unit common systems both had 2 OWAs and were well above the goal for the majority of the year. Unit 3, however, spent the majority of the year with a high number of operator burdens. Common unit burdens also finished the year well above the stations goals.

Inspectors noted that workarounds, burdens, and challenges were existing beyond one operating cycle on a unit. There were examples of multiple burdens and challenges that were not driven to conclusion prior to plant restart and were allowed to remain outstanding following refueling outages. Inspectors determined that the site often fails to adequately address and drive to resolution lower level operator issues when the opportunity is available to do so.

The licensee entered all the above issues into the CAP as SR 665557.

.5 Focused Annual Sample Review - Environmental Qualification (EQ)

a. Inspection Scope

Inspectors conducted a review of the licensees EQ program to verify that the licensee was identifying and resolving problems associated with EQ equipment at an appropriate threshold, entering them into the corrective action program, establishing adequate compensatory measures, prioritizing resolution of the problems, and implementing appropriate corrective actions in a timely manner commensurate with its safety significance. During the week of December 17, the inspectors interviewed engineering personnel and reviewed a sample of the licensees electronic EQ binders, EQ program assessments, health reports, environmental qualification information releases (EQIRs)and EQ related problem evaluation reports (PERs) to ensure general EQ program and 10 CFR 50.49 adherence. Inspectors also conducted walkdowns of a sample of accessible EQ equipment to ensure configuration control was being maintained and that equipment was installed in accordance with the tested configuration.

b. Findings

A violation of very low safety significance, which was identified by the licensee, has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. This violation and the corrective action program tracking number are described in Section 4OA7 of this report.

4OA3 Event Follow-up

.1 (Closed) Licensee Event Reports (LERs) 05000259, 260, and 296/2012-008-00 and -01,

Standby Gas Treatment System Train C Inoperable Longer Than Allowed by Technical Specifications

a. Inspection Scope

On August 2, 2012, the licensee placed the common Standby Gas Treatment (SGT)

Train C relative humidity heater into service which resulted in an annunciator alarm indicating power was lost to the SGT Train C filter bank heater element. Licensee troubleshooting identified that the motor control center (MCC) bucket containing the associated breaker was misaligned due to a missing retaining device. The licensee concluded that the SGT Train C had been inoperable since preventive maintenance performed in September, 2011, as the result of an inadequate maintenance instruction which allowed installation of a breaker bucket with a single retaining device. The inspectors reviewed the initial LER issued on October 1, 2012, the LER revision issued on December 14, 2012, and associated Problem Evaluation Report (PER) 604350, which included the cause determination and corrective action plans. These licensee evaluations concluded that the relative humidity heater was not required for the SGT Train C to perform accident required functions.

b. Findings

No findings were identified. This LER is closed.

.2 (Closed) Licensee Event Report (LER) 05000296/2012-004-00, Manual Reactor Scram

During Startup Due to Multiple Control Rod Insertion

a. Inspection Scope

The inspectors reviewed the LER for potential performance deficiencies and/or violations of regulatory requirements. The LER was associated with the Unit 3 manual reactor scram that occurred during a reactor startup on May 24, 2012. The inspectors reviewed the root cause report associated with this event and discussed the issue with appropriate members of plant staff. The cause of the scram was attributed to Unit Operator error combined with IRM signal spikes associated with manipulation of the scram reset switch and a degraded IRM High Voltage coaxial cable connector on the 3A IRM. This condition was documented in the licensees corrective action program as PER 558437.

Additional documents reviewed are listed in the Attachment. This LER is closed.

b. Findings

No findings were identified. This LER is closed

.3 (Closed) Licensee Event Reports (LER) 05000296/2012-006-00; 05000296/2012-006-

01, Main Steam Relief Valves Lift Settings Outside Technical Specification Required Setpoint

a. Inspection Scope

The inspectors reviewed LER 05000296/2012-006-00 and 05000296/2012-006-01 dated July 24, 2012, and August 31, 2012, and the applicable PER 558488. On May 25, 2012, two of thirteen Browns Ferry Nuclear Plant Unit 3 main steam relief valves, during testing, had mechanically actuated at pressures outside the allowed +/- percent tolerance per Technical Specification 3.4.3 setpoint. One relief valve lifted high at + 3.98 percent and the other low at negative 3.1 percent. This Technical Specification Limiting Condition for Operation required 12 of the S/RVs to be capable to mechanically open to relieve excess pressure when the lift setpoint is exceeded (safety function). The licensees analysis concluded that the variations in lift setting pressures did not prohibit the ability of the MSRVs to perform the function to open in order to provide over pressure protection. Twelve S/RVs were available to relieve excess pressure if the setpoint had been exceeded. However, contrary to the technical specifications surveillance requirement, only 11 operable main steam relief valves passed the licensee lift test procedure. The root cause was determined by the Tennessee Valley Authority to be that the valve design does not make allowances for corrosion bonding. Browns Ferry captured the corrective actions in PER 558488.

b. Findings

A violation of very low safety significance, which was identified by the licensee, has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. This violation and the corrective action program tracking number are described in Section 4OA7 of this report.

This LER is closed.

4OA5 Other Activities

.1 Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope

During the inspection period, the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status reviews and inspection activities.

b. Findings

No findings were identified.

.2 (Discussed) NRC Temporary Instruction (TI) 2515/187, Inspection of Near-Term Task

Force Recommendation 2.3 Flooding Walkdowns

a. Inspection Scope

Inspectors conducted independent walkdowns to verify that the licensee completed the actions associated with the flood protection feature specified in paragraph 03.02.a.2 of this TI. Inspectors are performing walkdowns at all sites in response to a letter from the NRC to licensees, entitled Request for Information Pursuant to Title 10 of the Code of Federal Regulations 50.54(f) Regarding Recommendations 2.1, 2.3, and 9.3, of the Near-Term Task Force Review of Insights from the Fukushima Dai-Ichi Accident, dated March 12, 2012 (ADAMS Accession No. ML12053A340).

4 of the letter requested licensees to perform external flooding walkdowns using an NRC-endorsed walkdown methodology (ADAMS Accession No.

ML12056A050). Nuclear Energy Industry (NEI) document 12-07 titled, Guidelines for Performing Verification Walkdowns of Plant Protection Features, (ADAMS Accession No. ML12173A215) provided the NRC-endorsed methodology for assessing external flood protection and mitigation capabilities to verify that plant features, credited in the CLB for protection and mitigation from external flood events, and are available, functional, and properly maintained.

b. Findings

Findings or violations associated with the flooding, if any, will be documented in the 1st quarter integrated inspection report of 2013.

.3 (Closed) Temporary Instruction 2515/188 - Inspection of Near-Term Task Force

Recommendation 2.3 Seismic Walkdowns

a. Inspection Scope

The inspectors accompanied the licensee on their seismic walkdowns of Unit 1 HPCI, Unit 2 D Shutdown Board Room and Unit 3 Core Spray Loop I on August 8, 2012, and verified that the licensee confirmed that the following seismic features associated with Unit 1 HPCI, Unit 2 D 4kV shutdown board, 2B 250VDC RMOV board, 2B 480V RMOV board and Unit 3 A and C Core Spray Pumps were free of potential adverse seismic conditions.

The inspectors also verified that the licensee confirmed that the following seismic features associated with the above components were free of potential adverse seismic conditions:

  • Anchorage was free of bent, broken, missing or loose hardware
  • Anchorage was free of corrosion that is more than mild surface oxidation
  • Anchorage was free of visible cracks in the concrete near the anchors
  • Anchorage configuration was consistent with plant documentation.
  • SSCs will not be damaged from impact by nearby equipment or structures.
  • Overhead equipment, distribution systems, ceiling tiles and lighting, and masonry block walls are secure and not likely to collapse onto the equipment.
  • Attached lines have adequate flexibility to avoid damage.
  • The area appears to be free of potentially adverse seismic interactions that could cause flooding or spray in the area.
  • The area appears to be free of potentially adverse seismic interactions that could cause a fire in the area.
  • The area appears to be free of potentially adverse seismic interactions associated with housekeeping practices, storage of portable equipment, and temporary installations (e.g., scaffolding, lead shielding).

On October 17 - 19, 2012, the inspectors independently performed their walkdown of Unit 3 Diesel Generator A, B, Units 1, 2 Residual Heat Exchanger Pumps, Units 1, 2 Residual Heat Exchangers, Unit 3 Control Room CR Water Chiller, Unit 1 Service Water Pump.

The inspectors also verified that the licensee confirmed that the following seismic features associated with the above components were free of potential adverse seismic conditions:

  • Anchorage was free of bent, broken, missing or loose hardware
  • Anchorage was free of corrosion that is more than mild surface oxidation
  • Anchorage was free of visible cracks in the concrete near the anchors
  • Anchorage configuration was consistent with plant documentation.
  • SSCs will not be damaged from impact by nearby equipment or structures.
  • Overhead equipment, distribution systems, ceiling tiles and lighting, and masonry block walls are secure and not likely to collapse onto the equipment.
  • Attached lines have adequate flexibility to avoid damage.
  • The area appears to be free of potentially adverse seismic interactions that could cause flooding or spray in the area.
  • The area appears to be free of potentially adverse seismic interactions that could cause a fire in the area.
  • The area appears to be free of potentially adverse seismic interactions associated with housekeeping practices, storage of portable equipment, and temporary installations (e.g., scaffolding, lead shielding).

The inspectors also looked at the items from the Area Walk By (AWB) list:

  • Unit 3 Diesel Generator A, B
  • Unit 3 Control Room Water Chiller
  • Unit 1 Service Water Pump Observations made during the walkdown that could not be determined to be acceptable were entered into the licensees corrective action program for evaluation.

Additionally, inspectors verified that items that could allow the spent fuel pool to drain down rapidly were added to the SWEL and these items were walked down by the licensee. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

.4 Follow-up On Alternative Dispute Resolution Confirmatory Orders (IP 92702)

a. Inspection Scope

During the inspection period the inspectors performed a follow-up review of TVAs implementation of Confirmatory Order for Office of Investigation Report Nos. 2-2006-025

& 2-2009-003, item number 1. This item is closed.

1. By no later than ninety

(90) calendar days after the issuance of this Confirmatory Order, TVA shall implement a process to review proposed licensee adverse employment actions at TVAs nuclear plant sites before actions are taken to determine whether the proposed action comports with employee protection regulations, and whether the proposed actions could negatively impact the SCWE.

During the inspection period the inspectors performed a follow-up review of TVAs implementation of Confirmatory Order for Office of Investigation Report Nos. 2-2006-025

& 2-2009-003, item numbers 4, 6, and 10. These items are not closed.

4. Through the end of calendar year 2013 and on approximately a quarterly basis, TVA shall continue to analyze SCWE trends and develop planned actions, as appropriate 6. Through calendar year 2013, TVA shall conduct Town Hall-type meetings at least annually at its nuclear power plants and corporate office with TVA and contractor employees which address topics of interest, including a discussion on TVAs policy regarding fostering a SCWE.

10. TVAs annual online computer-based training course initiative, which discusses the components of a nuclear safety culture, what is meant by a SCWE, and the avenues available to raise concerns, shall be maintained through calendar year 2013.

b. Findings and Observations

No findings were identified.

4OA6 Meetings, Including Exit

.1 Exit Meeting Summary

On January 11, 2013, the resident inspectors presented the quarterly inspection results to Mr. S. Bono, General Plant Manager, Site Operations, and other members of the licensees staff, who acknowledged the findings. All proprietary information reviewed by the inspectors as part of routine inspection activities were properly controlled, and subsequently returned to the licensee or disposed of appropriately.

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by the licensee and are violations of NRC requirements which meet the criteria of the NRC Enforcement Policy, for being dispositioned as a Non-Cited Violation.

Specifically, the licensee failed to take timely corrective actions to address an extensive backlog of EQ information releases which resulted in not meeting their environmental qualification program and the 10CFR 50.49 auditability requirements.

Contrary to this requirement, since January of 2010, the licensee failed to take prompt and appropriate corrective actions to evaluate and correct an extensive backlog of EQIRs, which resulted in 81 of the licensees 99 required Environmental Qualification equipment files not being updated to reflect the as-installed specifications and configuration of EQ equipment. The licensee entered this issue into their corrective action program as PERs 238931 and 624137. The finding was determined to be of very low safety significance (Green) using Attachment 4 to IMC 0609, Significance Determination Process, because the incomplete corrective actions did not result in an actual loss of safety function.

  • Unit 3 Technical Specification 3.4.3, Safety/Relief Valves, required that twelve of thirteen main steam safety relief valves (MSRVs) lift at a setpoint within plus or minus three percent of a specified value. Contrary to this, during TS required surveillance testing following the Unit 3 Cycle 9 refueling outage, the licensee discovered that the lift setpoints of two MSRVs exceeded the plus or minus three percent TS allowed pressure band. This TS violation was entered into the licensees CAP as PER 558488. The finding was determined to be of very low safety significance because the as-found lift setpoint conditions of the Unit 3 MSRVs were evaluated and determined to meet the design basis criteria for the most limiting reactor pressure vessel over-pressurization events.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

S. Bono, General Manager Site Ops
J. Boyer, Assistant Director of Engineering
E. Cobey, Licensing
J. Davenport, Licensing
G. Dudley, Site Welding/Repair & Replacement
M. Ellet, Maintenance Rule Coordinator
J. Emens, Nuclear Site Licensing Manager
F. Froscello, ISI Program
W. Hayes, Reactor Engineering Manager
M. Henderson, Vessel Internals Program
H. Higgins, LOR Supervisor (Acting)
L. Hughes, Operations Manger
M. Hunter, Mechanical Maintenance Manager
D. Kettering, Electrical Systems Engineering Manager
T. McCaney, Operations
B. McCreary, Senior Program Manager, Employee Concerns
J. McCormack, Ventilation Systems Engineer
F. Nielson, IWE/IWL Programs
M. Oliver, Site Licensing
K. Polson, Site Vice President
M. Rasmussen, W.C. Manager
T. Scott, PI Manager
R. Stowe, Equipment Reliability Manager
J. Shea, Vice President Nuclear Licensing
P. Summers, DSL
C. Vaughn, Operations Training Manager
M. Webb, Site Licensing
M. Wilson, Site Training Direct

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Closed

05000259, 260, and 296/2012-008-00 LER Standby Gas Treatment System Train C Inoperable Longer Than Allowed by Technical Specifications (Section 4OA3.1)
05000259, 260, and 296/2012-008-01 LER Standby Gas Treatment System Train C Inoperable Longer Than Allowed by Technical Specifications (Section 4OA3.1)
05000296/2012-004-00 LER Manual Reactor Scram During Startup Due to Multiple Control Rod Insertion (Section 4OA3.2)
05000296/2012-006-00 LER Main Steam Relief Valves Lift Settings Outside Technical Specification Required Setpoint (Section 4OA3.3)
05000296/2012-006-01 LER Main Steam Relief Valves Lift Settings Outside Technical Specification Required Setpoint (Section 4OA3.3)
05000259, 260, 296- 00 ORD 12/29/2009 Confirmatory Order Action 1 (Section 4OA5.4)

2515/188 TI Inspection of Near-Term Task Force Recommendation 2.3 Seismic Walkdowns (Section 4OA5.3)

Discussed

2515/187 TI Inspection of Near-Term Task Force Recommendation 2.3 Flooding Walkdowns (Section 4OA5.2)

05000259, 260, 296- 00 ORD 12/29/2009 Confirmatory Order Action 4 (Section 4OA5.4)
05000259, 260, 296- 00 ORD 12/29/2009 Confirmatory Order Action 6 (Section 4OA5.4)
05000259, 260, 296- 00 ORD 12/29/2009 Confirmatory Order Action 10 (Section 4OA5.4)

LIST OF DOCUMENTS REVIEWED