IR 05000250/2011008

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IR 05000250-11-008 and 05000251-11-008; Florida Power & Light Company; on 07/11/2011 - 08/31/2011; Turkey Point Nuclear Plant Units 3 & 4, NRC Component Bases Inspection - Inspection Report
ML112590421
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 09/16/2011
From: Binoy Desai
NRC/RGN-II/DRS/EB1
To: Nazar M
Florida Power & Light Co
References
IR-11-008
Download: ML112590421 (40)


Text

UNITED STATES mber 16, 2011

SUBJECT:

TURKEY POINT NUCLEAR PLANT - NRC COMPONENT DESIGN BASES INSPECTION - INSPECTION REPORT 05000250/2011008 AND 05000251/2011008

Dear Mr. Nazar:

On, August 31, 2011, U. S. Nuclear Regulatory Commission (NRC) completed an inspection at your Turkey point Nuclear Plant. The enclosed inspection report documents the inspection results, which were discussed on September 8, 2011, with Mr. M. Kiley and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your licenses. The team reviewed selected procedures and records, observed activities, and interviewed personnel.

This report documents five NRC identified findings of very low safety significance (Green),

which were determined to involve violations of NRC requirements. The inspectors determined that one of the issues was a Severity Level IV violation of NRC requirements. The NRC is treating these violations as non-cited violations (NCVs) consistent the NRC Enforcement Policy.

If you contest these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.:

Document Control Desk, Washington DC 20555-001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Turkey Point. Further, if you disagree with the cross-cutting aspect assigned to any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at Turkey Point. The information you provide will be considered in accordance with Inspection Manual Chapter 0305.

FP&L 2 In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Binoy Desai, Chief Engineering Branch 1 Division of Reactor Safety

Enclosure:

Inspection Report 05000250/2011008 and 05000251/2011008, w/Attachment: Supplemental Information Docket Nos.: 50-250, 50-251 License Nos.: DPR-31, DPR-41

REGION II==

Docket Nos.: 50-250, 50-251 License Nos.: DPR-31, DPR-41 Report Nos.: 05000250/2011008, 05000251/2011008 Licensee: Florida Power & Light Company (FP&L)

Facility: Turkey Point Nuclear Plant, Units 3 & 4 Location: 9760 S. W. 344th Street Homestead, FL 33035 Dates: July 11 - August 31, 2011 Inspectors: D. Jones, Senior Reactor Inspector (Lead)

R. Patterson, Reactor Inspector D. Mas Penaranda, Reactor Inspector E. Stamm, Project Engineer D. Terry-Ward, Construction Inspector (Trainee)

M. Yeminy, Contractor G. Skinner, Contractor Approved by: Binoy B. Desai, Chief Engineering Branch 1 Division of Reactor Safety Enclosure

SUMMARY OF FINDINGS

IR 05000250 & 251/2011008; 07/11/2011 - 08/31/2011; Turkey Point Nuclear Plant;

Component Design Bases Inspection.

This inspection was conducted by a team of five NRC inspectors from the Region II office, and two NRC contract inspectors. Five Green non-cited violations (NCV) were identified of which one was a Severity Level IV violation. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using the NRC Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, (ROP) Revision 4, dated December 2006.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green.

The team identified a Green non-cited violation (NCV) of 10 CFR Part 50, Appendix B, Criterion III, Design Control, for the licensees failure to verify or check the adequacy of design for with four examples. The licensee entered these issues into their corrective action program as ARs 1672459, 1676403, 1674790, 1675544 and 1679053, and performed evaluations to assure operability of components.

The licensees failure to adequately perform engineering evaluations as described in the four examples was a performance deficiency. The performance deficiency was more than minor because it adversely affected the Mitigating Systems cornerstone attribute of Design Control and adversely affected the cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences.

Specifically, the deficiencies described above, resulted in a reasonable doubt that safety-related equipment could perform their functions under the most limiting conditions. In accordance with NRC IMC 0609.04, Initial Screening and Characterization of Findings, the inspectors conducted a Phase 1 Significance Determination Process (SDP) screening and determined the finding to be of very low safety significance (Green) because it was a design deficiency confirmed not to result in the loss of operability or functionality. Specifically, the licensee performed evaluations that provided reasonable assurance that the components would perform their required functions when called upon. The team determined that no cross cutting aspect was applicable to this performance deficiency because this finding was not indicative of current licensee performance. [Section 1R21.2.2]

Green.

The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion XVII, Quality Assurance Records, for the licensees failure to maintain sufficient records to furnish evidence of activities affecting quality. Specifically, the licensee was not able to retrieve test data and calculations supporting an acceptance criterion that assures the reliability and availability of minimum MCC voltage to provide adequate voltage to MCC control circuits. The licensee entered these issues into their corrective action program as AR 1676661 and has proposed actions to (1) implement a design modification to increase the control power transformer size for three motor operated valves (MOV), (2) add the control circuits for the 3 MOVs to the sites low margin list, and (3) re-create missing analysis and test data.

The inspectors determined that the failure to have retrievable test data and calculations to support acceptance criteria for MCC control circuit voltage was a performance deficiency. The finding was more than minor because it affected the Mitigating Systems Cornerstone attribute of Design Control, and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.

Specifically, there was reasonable doubt as to whether safety-related MCC control circuits would have sufficient voltage to function during a degraded voltage condition. The finding was considered to be of very low safety significance (Green) since this was a design deficiency confirmed not to have resulted in a loss of operability or functionality. The team determined that no cross cutting aspect was applicable to this performance deficiency because this finding was not indicative of current licensee performance. [Section 1R21.2.4.b.1]

Green.

The team identified a NCV of 10 CFR Part 50, Appendix B, Criterion III,

Design Control, for the licensees failure to perform adequate voltage calculations for safety-related equipment with two examples. The licensee entered these issues into their corrective action program as ARs 1677149, 1677149-02, 1673843, 1677149-02, 1676754 and 01676641 and performed evaluations to provide reasonable assurance that components would have adequate voltage pending forma re-analysis.

The inspectors determined that the failure to perform adequate design calculations to support the setpoint of the degraded voltage relays and the failure to perform adequate design calculations for the 120Vac instrument system was a performance deficiency. The finding was more than minor because it affected the Mitigating Systems Cornerstone attribute of Design Control, and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.

Specifically, there was reasonable doubt as to whether the components would have adequate voltage to perform their safety function during a degraded voltage condition. The finding was considered to be of very low safety significance (Green) since this was a design deficiency confirmed not to have resulted in a loss of operability or functionality. The team determined that no cross cutting aspect was applicable to this performance deficiency because this finding was not indicative of current licensee performance. [Section 1R21.2.4.b.2]

Specifically, a common-mode failure method was not described in the UFSAR that required proceduralized manual actions during design bases rain events.

The licensee entered these issues into their corrective action program as AR 1679078.

The failure to update the UFSAR as required by procedure ENG Q1-3.4 and 10 CFR 50.71(e) was a performance deficiency. This performance deficiency was considered as traditional enforcement because, not having an adequately updated UFSAR hinders the licensees ability to perform adequate 10 CFR 50.59 evaluations and can impact the NRCs ability to perform its regulatory function such as, license amendment reviews and inspections. In addition, the team determined that the performance deficiency was material to safety because the modification resulted in a common-mode failure method that required proceduralized manual actions for the Unit 3 EDGs to meet their mission time during design bases rain events. This violation was determined to be a SL-IV violation using Section 6.1 of the NRCs Enforcement Policy because the erroneous information was not used to make an unacceptable change to the facility or procedures. Cross-cutting aspects are not assigned for traditional enforcement violations. [Section 1R21.2.8]

Green.

The team identified a NCV of 10 CFR 50.63 for the licensees failure to test the station blackout (SBO) cross-tie components under loaded conditions.

Since 1991, the licensee failed to verify the capability of the SBO cross-tie and associated components to carry the required amperage during post installation tests or subsequent periodic maintenance tests. The licensee entered these issues into their corrective action program as ARs 1676402 and 1680428 with an action to establish a method and frequency for loading the SBO cross-tie components.

The team determined that the licensees failure to perform adequate post installation testing and periodic testing as required by the licensees commitment to RG 1.155, Station Blackout, was a performance deficiency. This finding was more than minor because it affected the Mitigating Systems cornerstone attribute of Equipment Performance and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems and components that respond to initiating events to preclude undesirable consequences (i.e. core damage).

Specifically, since the installation of cross-tie components to meet SBO requirements, the licensee failed to test the components in a loaded condition.

The lack of testing resulted in a reduced reliability of the SBO cross-tie. In accordance with NRC IMC 0609.04, Initial Screening and Characterization of Findings, the team conducted a Phase 1 SDP screening and determined the finding to be of very low safety significance (Green) because it was not a design issue resulting in loss of function, did not represent an actual loss of a system safety function, did not result in exceeding a TS allowed outage time, and did not affect external event mitigation. The team determined that no cross cutting aspect was applicable to this performance deficiency because this finding was not indicative of current licensee performance. [Section 1R21.2.10]

Licensee-Identified Violations

None

REPORT DETAILS

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R21 Component Design Bases Inspection

.1 Inspection Sample Selection Process

The team selected risk significant components and operator actions for review using information contained in the licensees Probabilistic Risk Assessment (PRA). In general, this included components and operator actions that had a risk achievement worth factor greater than 1.3 or Birnbaum value greater than 1 X10-6. The sample included fifteen components including one associated with containment, and four operating experience (OE) items.

The team performed a margin assessment and a detailed review of the selected risk-significant components to verify that the design bases had been correctly implemented and maintained. This design margin assessment considered original design issues, margin reductions due to modifications, or margin reductions identified as a result of material condition issues. Equipment reliability issues were also considered in the selection of components for a detailed review. These reliability issues included items related to failed performance test results, significant corrective action, repeated maintenance, maintenance rule status, Regulatory Issue Summary (RIS)05-020 (formerly Generic Letter (GL) 91-18) conditions, NRC resident inspector input of problem equipment, System Health Reports, industry OE, and licensee problem equipment lists.

Consideration was also given to the uniqueness and complexity of the design, operating experience, and the available defense-in-depth margins. An overall summary of the reviews performed and the specific inspection findings identified is included in the following sections of the report.

.2 Component Reviews (15 Samples)

.2.1 Intake Cooling Water Pump (ICW) Pump 4C and Strainer

a. Inspection Scope

The team reviewed the plants Updated Final Safety Analysis Report (UFSAR), Technical Specification (TS), design bases documents (DBD), and piping and instrumentation drawings (P&ID) to establish an overall understanding of the design bases of the ICW pumps. Design calculations and site procedures were reviewed to verify the design bases and design assumptions had been appropriately translated into these documents.

Component walk downs were conducted to verify that the installed configurations would support their design bases functions under accident/event conditions and had been maintained to be consistent with design assumptions. Test procedures and recent test results were reviewed against design basis documents to verify that acceptance criteria for tested parameters were supported by calculations or other engineering documents and that individual tests and/or analyses served to validate component operation under accident/event conditions. Vendor documentation, preventive and corrective maintenance history, and corrective action system documents were reviewed to verify that potential degradation was being monitored.

b. Findings

No findings were identified.

.2.2 Auxiliary Feedwater (AFW) Pumps

a. Inspection Scope

The team reviewed the UFSAR, PI&Ds, test data, system health, vendor manual, as well as operating and surveillance procedures to identify design, maintenance, and operational requirements related to steam supply, pump flow rate, developed head, achieved system flow rate, net positive suction head (NPSH), and minimum flow requirements. These requirements were reviewed for pump operation with the source of water originating from the condensate storage tank (CST). Design calculations, as well as documentation of periodic surveillance tests, were reviewed to verify that design performance requirements were met. Maintenance, in-service testing, corrective action documents, and design change histories were reviewed to assess the potential for component degradation and the resulting impact on design margins and performance.

The team also evaluated the adequacy of the suction piping of the pump, its vulnerability to over pressurization due to back flow from a leaking discharge check valve and whether a leaking discharge check valve could cause reverse rotation of the idle pump.

The team verified the pumps capability of performing its safety function, i.e., delivering the required flow rate to the steam generators at the prescribed design pressure as well as the acceptability of AFW system operation criteria and operator action to secure pumps for minimum flow requirements. The team also reviewed off-normal and emergency operating procedures to verify that adequate guidance exists to shut down one of two AFW pumps operating on the same train. Simulator exercise performance was reviewed to confirm operators successfully perform the task within the time requirements. Additionally, the team walked down portions of the AFW system to verify that the installed configuration was consistent with design bases information and to visually inspect the material condition of the pumps.

b. Findings

Introduction:

The team identified a Green non-cited violation (NCV) of 10 CFR Part 50, Appendix B, Criterion III, Design Control, for the licensees failure to verify or check the adequacy of design for with four examples.

Description:

The team identified four examples of design control violations:

Example 1: Failure to Analyze the Most Limiting System Configuration in the Auxiliary Feedwater (AFW) Pumps NPSH Calculation Calculation PTN-BFSM-98-0010, AFW Pump Net Positive Suction Head (NPSH)

Assessment, Rev. 0 assessed worst case NPSH requirements for a single AFW pump taking suction from two condensate storage tanks (CST). The team noted that the most limiting AFW configuration described in the UFSAR was a single pump taking suction from a single CST. This configuration is more limiting because of additional line resistance losses incurred when taking suction from a single tank. The team determined that insufficient NPSH existed for this most limiting configuration. During the inspection, the licensee performed a prompt operability determination for which a new NPSH calculation was drafted to properly account for the most limiting conditions. The re-analysis resulted in a significant loss of margin. This issue was entered into the licensees corrective action program as AR 1672459.

Example 2: Failure to Translate Uncertainties into an Emergency Operating Procedure (EOP)

Procedure 3-EOP-E-0, Reactor Trip or Safety Injection, Rev. 3, states that when the water level in the CST decreases to 10%, the operators are required to line up the condensate transfer pump and transfer water from the demineralized water tank to the CST. The required increase in water level is to protect the AFW pump from the ingestion of air caused by a vortex. The team noted that the licensee failed to translate the uncertainty associated with the CST level instrument, (+3.25% and -3.1% of full scale) when developing the criteria for aligning the alternate water source to the CST.

This deficiency could result in the operators not initiating manual actions associated with re-filling the CST until the water level is at 6.9%. Waiting until 6.9% CST level would unnecessarily challenge the operators with respect to avoiding a vortex issue. This issue was entered into the licensees corrective action program as AR 1676403 and the licensee plans to increase the CST level upon which the make up process is required to commence.

Example 3: Failure to Adequately Evaluate Refueling Water Storage Tank (RWST)

Vortex Limit in Calculation Calculation M12-383-01, Vortex Design of Refueling Water Storage Tank,12/13/1991, assessed worst case flow conditions to provide assurance that air ingestion by vortexing would not occur during design bases accidents. The team identified a deficiency in the calculation that resulted in a reasonable doubt that the licensee had adequately evaluated vortexing. The team noted that the licensee used a graph created by Gould Pumps Inc. to extrapolate the minimum water height required to avoid vortex formation when two safety injection pumps, two residual heat removal pumps and two containment spray pumps all take suction from the RWST. The team determined that the licensee incorrectly extrapolated data from the graph. This error resulted in an increase (22 feet to 27 feet) of the submergence height required to avoid vortex formation. This issue was entered into the licensees corrective action program as AR 1674790 and the licensee performed engineering evaluation, PTN-ENG-SEMS-11-075, Flow Dynamics Effect on Determining RWST Submergence to recover the negative margin that resulted from the teams observation.

Example 4: Failure to Adequately Evaluate Alternate Cooling of Load Center and Switchgear Rooms The Unit 3 load center and switchgear rooms are provided with a two train air conditioning system to remove the heat dissipated by electrical safety-related equipment during normal plant operation and emergency conditions. In the event that the air conditioning system is rendered non-functional by hazards such as fire, high winds, missiles, and heavy load drops, UFSAR Section, 9.16.3 states, in part, that reliability and independence is provided by a wall-mounted cooling fan located in the west wall of the building. For the event of a total loss of air conditioning, Procedure 3-NOP-070, Vital Load Center and Switchgear Rooms Chilled Water Air Conditioning System, Rev. 3 provides guidance for operators to initiate alternate cooling by placing the exhaust fan in service which includes opening doors to the exterior of the building. The procedure states that if any room temperature approaches 95°F immediately notify the shift manager because the design limit as stated in the UFSAR is 100 ºF for the switchgear room and 104ºF for the load center room.

The team noted that Calculation JPN-PTN-SENJ-92-003, Rev. 0, Safety Assessment for Load Center and Switchgear Rooms HVAC Safety Classification, Section 2.3 states, in part, that during alternate cooling, air temperature in the rooms rises slowly and remains below the 100ºF continuous service temperature limit for more than half a day. The team determined that within the first hour following the opening of the doors, the EDG discharge air would increase the bulk ambient air temperature in the rooms well above the 100ºF continuous service temperature limit. The team reached this conclusion because the calculation states that the EDG exhaust temperature will be approximately 120ºF and a sign on a steel railing located outside the room warns Railing May Be Hot when the EDG is Operating. A flow rate of 35,000 CFM will pass two million cubic feet of hot air (much greater than the rooms volume) at a temperature significantly greater than 104ºF, in less than one hour. This will result in a quick temperature rise above the switchgear and load center rooms design temperatures of 100ºF and 104ºF respectively. Additionally, the team determined that the assessment for more than half a day was not consistent with the seven days thats mentioned in the UFSAR. The result of the deficiencies is that Procedure 3-NOP-070 provides inadequate guidance to mitigate a complete loss of air conditioning to the Unit 3 load center and switchgear rooms. This issue was entered into the licensees corrective action program as AR 1675544 and 1679053. Additionally, the licensee performed a preliminary assessment that determined the equipment in the rooms would be operable up to 135ºF.

Analysis:

The licensees failure to adequately perform engineering evaluations as described in the four examples was a performance deficiency. The performance deficiency was more than minor because it was similar to Inspection Manual Chapter (IMC) 0612, Power Reactor Inspection Reports, Appendix E, Examples of Minor Issues, Example 3.j, which states that if the engineering calculation error results in a condition where there is now a reasonable doubt on the operability of a system or component the performance deficiency is not minor. Further, the deficiencies were more than minor because the performance deficiencies adversely affected the Mitigating Systems cornerstone attribute of Design Control and adversely affected the cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the deficiencies described above, resulted in a reasonable doubt that safety-related equipment could perform their functions under the most limiting conditions. In accordance with NRC IMC 0609.04, Initial Screening and Characterization of Findings, the inspectors conducted a Phase 1 Significance Determination Process (SDP) screening and determined the finding to be of very low safety significance (Green) because it was a design deficiency confirmed not to result in the loss of operability or functionality. Specifically, for the three examples provided above, the licensee performed evaluations that provided reasonable assurance that the components would perform their required functions when called upon. The team determined that no cross cutting aspect was applicable to this performance deficiency because this finding was not indicative of current licensee performance.

Enforcement:

10 CFR Part 50, Appendix B, Criterion III, Design Control requires, in part, that design control measures provide for verifying or checking the adequacy of design. Contrary to the above, as of August 12, 2011 the licensee failed to verify the adequacy of design in calculations used to provide assurance that safety-related components would perform their functions during design bases accidents. Specifically, the licensee

(1) failed to verify that a single AFW pump would have adequate NPSH, (2)failed to verify that the uncertainties associated with CST level instrumentation were appropriately translated into an EOP,
(3) failed to adequately verify that ECCS pumps would not be affected by the formation of air vortices during the most limiting flow conditions and
(4) failed to adequately assess the capability of alternate cooling during the loss of all air conditioning to the Unit 3 switchgear and load center rooms. Because this finding is of very low safety significance and because it was entered into the licensees corrective action program as ARs 1672459, 1676403, 1674790, 1675544 and 1679053, this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy. NCV 05000250 & 251/2011008-01, Failure to Verify or Check the Adequacy of Design for with Four Examples.

.2.3 125vdc 3A Bus

a. Inspection Scope

The team reviewed loading and sizing calculations related to 125VDC 3A Bus to verify whether the bus would have sufficient capacity to support its required loads under worst case accident loading conditions. The team reviewed schematic diagrams and calculations for the breakers to determine whether equipment operation was consistent with the design bases. The team reviewed calculations for protective device settings to determine whether the breakers were subject to spurious tripping, and whether the breakers were selectively coordinated with upstream devices. Also, the team reviewed associated corrective action history to verify that degraded conditions were being appropriately addressed. In addition, the team interviewed the system engineer and performed a non-intrusive visual inspection of the bus to assess the installation configuration and verify that degraded material conditions were being appropriately addressed.

b. Findings

Introduction:

The team indentified an Unresolved Item (URI) regarding the licensees failure to establish a test program for safety-related molded case circuit breakers (MCCB) (120vac and 125vdc) to demonstrate these breakers would be able to reliably perform their intended safety functions, specifically protective tripping.

Description:

The age range of approximately 511 safety-related MCCBs at Turkey Point is twenty to forty years - some are original plant equipment, some were installed in the 1980s, and the remainder in the early 1990s. With the exception of bench testing prior to installation, no testing/maintenance has been performed on the breakers. MCCBs are susceptible to age related failures such as, overheating due to loose connections and long term grease hardening. Overheating can exceed material temperature ratings, distort motor control center case and operating mechanism tolerances, and result in hardening/baking of grease. Long term grease hardening can result in the breaker failing to open or a delay in opening during a downstream electrical fault.

NRC Information Notice (IN) 93-64, Periodic Testing and Preventive Maintenance of Molded Case Circuit Breakers, states, in part: MCCB preventive maintenance practices can mitigate the effects of aging and help ensure continued MCCB reliability, and that certain standard MCCB tests (such as individual pole resistance, 300 percent thermal overload and instantaneous magnetic trip tests) performed periodically were found effective along with the additional techniques of infrared temperature measurement and vibration testing. Also, EPRI NP-7410, Section 7.3.1, states, that ensuring that all MCBs are periodically exercised is considered a vital part of a maintenance program, applicable to all breakers regardless of their safety classification.

In addition, EPRI/NMAC NP-7410-V3, Section 7.3.1, states that safety related MCCB cycling/trip testing should be performed on a 4 to 6 year frequency.

In 2005 and 2006, during Turkey Points preventive maintenance optimization (PMO)project, the licensee identified the lack of a testing program for safety-related 120vac and 120vdc MCCBs which resulted in the creation of a preventative maintenance (PM)program for the breakers. The PMs for the 120Vac breakers were to include a periodic inspection and electrical test to verify functionality. The PMs for the 125Vdc breakers were to replace each individual breaker. However, the licensee suspended the PMs, in part, because of scheduling challenges associated with Technical Specification (TS)restrictions - the TS has a two hour action statement associated with the de-energization of the ac or dc load centers.

In 2008, in response to the cancelled PMs, CAR 08-069 was created and assigned as a Turkey Point Excellence (TPE) project. TPE considered several options, and decided on a one-time replacement of the vital 120Vac and 125Vdc breakers.

In 2010, the licensee initiated AR 1649834 because the funding for the TPE project was terminated. This AR created a new long term asset management initiative to re-target the project in future years.

In 2011, ECR 1657020 was created for a one-time replacement of the MCCBs and entered into the licensees long term asset management program (PTN-11-0177 [U3]

and PTN -11-0179[U4].

The team identified that since 2005/2006 when the lack of periodic testing of the MCCBs was identified; no interim measures were taken to correct the nonconforming condition.

Specifically, on multiple occasions since 2005, the licensee failed to take adequate actions to ensure the reliability and capability of the MCCBs to perform their design function while pursuing long term strategies. Additionally, the team identified that the licensee failed to scope the protective tripping function of the MCCBs in the Maintenance Rule program. These issues were entered into the licensees corrective action program as ARs 1675539 and 1676808 which include developing an interim strategy that is to consider visual inspections augmented by thermography, planned cycling, and testing of the MCCBs.

Summary: This issue is unresolved pending further inspection to determine the extent of condition and impact of not establishing a test program for the MCCBs. The team requires additional information from the licensee to determine if the issue is more than minor. Specifically, the team will review test results of a statistically significant amount of the approximately 511 safety-related MCCBs prior to dispositioning the issue. (URI 05000250, 251/2011008-02, Molded Case Circuit Breaker Testing)

.2.4 3A and/or 3B 4.16kv Bus

a. Inspection Scope

The team reviewed bus loading calculations to determine whether the 4160V system had sufficient capacity to support its required loads under worst case accident loading and grid voltage conditions. The team reviewed the design of the degraded voltage protection scheme to determine whether it afforded adequate voltage to safety-related devices at all voltage distribution levels. This included review of degraded voltage relay setpoint calculations, motor starting and running voltage calculations, and motor control center (MCC) control circuit voltage drop calculations. The team reviewed the overcurrent protection scheme for the 4.16kV buses including drawings and calculations to determine whether loads were adequately protected and immune from spurious tripping. The team reviewed the load shedding and load sequencing schemes to determine whether they were consistent with the design bases and design calculations.

The team reviewed the fast bus transfer scheme, including drawings and procedures, to determine whether the transfer capability described in the UFSAR could be achieved without adverse effects on equipment and systems. The team reviewed the high resistance grounding scheme of the 4.16kV buses including drawings and alarm response procedures to determine whether system operation was consistent with equipment design requirements. The team reviewed corrective action documents and maintenance records to determine whether there were any adverse operating trends. In addition, the team performed a visual inspection of the 4.16kV safety buses to assess material condition and the presence of hazards.

The inspectors also reviewed off-normal and emergency operating procedures to verify that adequate guidance exists for operators to restore power to a de-energized bus.

b.1 Findings

Introduction:

The inspectors identified a Green, NCV of 10 CFR Part 50, Appendix B, Criterion XVII, Quality Assurance Records, for the licensees failure to maintain sufficient records to furnish evidence of activities affecting quality. Specifically, the licensee was not able to retrieve test data and calculations supporting an acceptance criterion that assures the reliability and availability of minimum MCC voltage to provide adequate voltage to MCC control circuits.

Description:

Calculation PTN-3FSE-07-001, Unit 3 Safety-related AC Electrical Distribution PSB-1, Short Circuit, Voltage Drop and Bus Loading, Rev. 1 was used by the licensee to provide assurance that motor control center (MCC) had adequate voltage.

The calculation uses a May 20, 1982, letter (L-82-211) to the NRC from Florida Power &

Light (FPL) as an input into the calculation. The values provided in the letter are used as the basis for the minimum voltage required at MCCs to ensure adequate voltage to MCC contactors. These values for minimum MCC voltages ranged from 69.2% to 82.1% of 480 volts. Letter L-82-211 stated that the required MCC voltages were developed by testing contactors and control transformers, and by performing calculations for cable and control transformer voltage drop. However, the licensee was not able to retrieve test data or calculations to support the values provided in the letter.

The team noted that the licensee did not performed periodic pickup voltage testing of the contactors to demonstrate that the alternate contactor pick up voltage cited in the letter remained valid over the installed life of the contactors. Additionally, the team noted that vendor manual A0534 listed the required pickup voltage for the magnetic contactors as 85%, consistent with National Electrical Manufacturers Association (NEMA) and Underwriters Laboratories (UL) standards. The team further noted that Specification 5610-E-8 for ITE contactors required design tests in accordance with NEMA and UL standards and did not specify alternate (lower) contactor pickup voltage criteria.

In response to this concern the licensee performed preliminary calculations based on actual circuit lengths and contactor pickup criteria provided in a February 24, 1982, letter (L-82-65) to the NRC. This letter cited contactor pickup voltages ranging from 71% to 76% of 120 volts, based on data supplied by the vendor. The preliminary calculations identified control circuits for three safety-related MOVs as having low voltage under degraded voltage conditions. They included circuits for Pressurizer Relief Isolation Valves MOV-3-535 and MOV-4-535, and Steam Generator Sample Valve MOV-3-1427.

The preliminary calculations showed that these circuits would have voltage deficits of approximately 1% to 2%.

The licensee entered this item into the corrective action program as AR 1676661 and performed a prompt operability determination. The licensees proposed actions include the following:

(1) implement a design modification to increase the control power transformer size for the three MOVs,
(2) add the control circuits for the three MOVs to the sites low margin list, and
(3) recreate analysis and test data in support of letter L-82-211.

Based on the original criteria in Letter L-82-211and 2008 test data for a size 4 contactor that operated successfully at 70% voltage, the licensee concluded that there was reasonable assurance of operability for these MOVs pending final resolution.

Analysis:

The inspectors determined that the failure to have retrievable test data and calculations to support acceptance criteria for MCC control circuit voltage was a performance deficiency. The finding was more than minor because it affected the Mitigating Systems Cornerstone attribute of Design Control, and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. In addition, the finding is similar to IMC 0612 Appendix E, example 3.j because the issue resulted in a condition where there was a reasonable doubt with respect to operability of safety-related components. Specifically, there was reasonable doubt as to whether safety-related MCC control circuits would have sufficient voltage to function during a degraded voltage condition. The finding was considered to be of very low safety significance (Green) since this was a design deficiency confirmed not to have resulted in a loss of operability or functionality. The team determined that no cross cutting aspect was applicable to this performance deficiency because this finding was not indicative of current licensee performance.

Enforcement:

10 CFR 50, Appendix B, Criterion III, Criterion XVII, Quality Assurance Records, requires, in part, that sufficient records shall be maintained to furnish evidence of activities affecting quality. It also requires that inspection and test records identify the type of observation, the results, the acceptability, and the action taken in connection with any deficiencies noted, and that the records be identifiable and retrievable. Contrary to the above, on August 12, 2011 the licensee failed to maintain sufficient records to furnish evidence of activities affecting quality. Specifically, the licensee was not able to retrieve test data and calculations supporting an acceptance criterion that assures the reliability and availability of minimum MCC voltage to provide adequate voltage to MCC control circuits. Because this violation was of very low safety significance and because the issue was entered into the licensees CAP as AR 1676661, this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy and designated as NCV 05000250/2011008-03 and 05000251/2011008-03 Failure to Maintain Adequate Records to Support Acceptance Criteria in Design Calculations.

b.2 Findings

Introduction:

The inspectors identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion III, Design Control, for the licensees failure to perform adequate voltage calculations for safety-related equipment with two examples.

Description:

The team identified two examples of design control violations associated with electrical calculations. The issues discussed below are applicable to both units.

Example 1: Inadequate calculations to support basis for degraded voltage relay setpoint Staff positions defined in NRC Generic Letter to FPL dated June 3, 1977 states that the selection of voltage and time delay setpoints for the degraded voltage relays shall be determined from an analysis of the voltage requirements of the safety-related loads at all on-site system distribution levels. The team noted that the voltage requirements for some safety-related loads were not properly considered in the calculation that determined the degraded voltage relay setpoints for Unit 3.

Calculation PTN-3FSE-07-001, Unit 3 Safety-related AC electrical distribution PSB-1, Short Circuit, Voltage Drop and Bus Loading contained the following errors:

  • Calculations for motor starting voltage during load sequencing assumed a minimum administratively controlled switchyard voltage of 233kV instead of the lower voltage afforded by the degraded voltage relays. In response to this concern, the licensee initiated AR 1677149 and performed preliminary calculations for load sequencing based on degraded voltage relay setpoints defined in Technical Specifications. These calculations showed that the safety buses could remain connected to the offsite power with switchyard voltage as low as approximately 220kV for train A and 224kV for train B.

These calculations showed that all motors met their specified starting voltage criteria of 80% of rated voltage except for the containment spray pumps, 3P214A (78.19%) and 3P214B (76.82%). The licensee noted that Calculation 21701-523-E-02, Voltage Drop for A.C. & D.C. Control Circuits for Unit 3 [Plant Change/Modification (PC/M) 83-154], Rev. 1 showed that the motors were able to accelerate with 70.7% voltage without tripping their overcurrent protection.

  • No calculations were available to start individual motors during degraded voltage conditions. In response to this concern, the licensee initiated AR 1677149-02 and performed preliminary calculations for starting individual motors with the safety buses near the degraded voltage relay setpoint defined in Technical Specifications. These calculations again showed that the containment spray pumps did not meet their 80% starting voltage specification; 3P214A (77.82%) and 3P214B (76.5%), but were still acceptable as noted above. In addition, two emergency containment cooler fans exhibited voltages below their 80% starting voltage specification; 3V30B (78.87%) and 3V30C (79.86%). The licensee concluded that these motors would not stall or trip their overcurrent protection during degraded voltage based on evaluations in Calculation 21701-523-E-02.
  • Degraded voltage calculations did not address voltage requirements for non-motor loads such as the constant voltage transformer (CVT). In response to this concern, the licensee initiated AR 1677149-02 and evaluated voltage available to the CVTs. This evaluation determined that the voltage at the terminals of the CVTs under degraded voltage conditions would be below the 432V (90%) minimum voltage specified. The vendor indicated that reduced input voltage could degrade the tolerance of the output voltage from its specified +/- 2% to approximately +/- 3%. This effect was considered by the licensee to be within the available voltage margin of the affected 120Vac instrument panel circuits.
  • Calculation PTN-3FSE-07-001 provided inputs to Calculation PTN-BFSE-90-006, Motor Operated Valve Voltage Drop Calculations, Rev. 26 for calculating voltage to Generic Letter 89-10 motor operated valves (MOV). The inputs from Calculation PTN-3FSE-07-001 used the minimum administratively controlled switchyard voltage 233kV instead of the degraded voltage relay setpoints defined in Technical Specifications. In response to this concern, the licensee initiated AR 1673843 and evaluated available torque using the worst case voltages at MCCs from the preliminary load sequencing calculations described for the motors above. The licensee concluded that by using these conservatively bounding voltages, all safety-related MOVs would still have sufficient available torque to start and run. Based on the above evaluations, the team concluded that there was reasonable expectation of operability for the affected circuits, pending formal re-analysis.

Example 2: Lack of analysis to ensure adequate voltage for safety-related loads supplied by 120 Vac vital buses The safety-related 120Vac instrument panels can be supplied from their primary source consisting of a battery supplied 120Vac inverter, or an alternate source consisting of a Constant Voltage Transformer (CVT) that is supplied by a 480 volt vital MCC. Although the output voltage of both sources is regulated to within +/-2%, variables such as circuit length and loading must be controlled to ensure adequate voltage at safety-related loads under accident loading conditions.

The team learned through interviews that voltage calculations were not available for the original installation. However, for recent modifications to the 120vac system (Panel 3P08) the licensee has analyzed the effect of loading changes (including the effect on voltage drop). The team reviewed selected modifications and noted that the voltage drop evaluations were either qualitative, or non-conservative. For example, PCMs04-112 and 04-113 evaluated load additions to various non-safety and safety-related 120Vac circuits and assumed a voltage drop of approximately 1 volt from the inverter to the distribution panel. PCM 07-055 concluded that the additional voltage drop of approximately 1% due to new equipment was negligible. The evaluation in PCM 08-025 concluded that the load remained within the ratings of the inverters and circuit breakers and that no adverse voltage drop effects were anticipated.

As a result of the teams review, the licensee performed preliminary calculations for Panel 3P23 which determined that actual voltage drop from Inverter 3Y02 to Panel 3P23 was 2.97V and from CVT 3Y02A to Panel 3P23 the voltage drop was 5.37V. These voltage drops were considerably larger than the 1V assumed for the circuits evaluated in PCMs04-112 and 04-113 R1.

The team noted that voltage requirements for electrical loads are typically +/-10% of rated voltage. Considering the +/-2% voltage regulation of the power source and >4% voltage drop from the worst case source (the CVT), the team concluded that for 120V rated equipment there was less than 4% margin for voltage drop for the rest of the circuit.

As a result of the low margin, the team concluded that the lack of initial calculations for the 120Vac panels adversely affected the ability of the licensee to evaluate 120Vac system changes that could adversely affect the operability of safety-related loads.

Additionally, the team noted that the licensees maintenance procedure that periodically measures the output voltage of the CVT did not have proper acceptance criteria because it only required the voltage to be approximately 120 volts and did not require the voltage to be within the design requirement of +/-2%. The combination of the lack of calculations, and the lack of proper acceptance criteria resulted in a reasonable doubt that the CVT could not perform its design bases function.

In response the teams concern, the licensee initiated ARs 01676754 and 01676641, and provided a more detailed preliminary analysis of loads supplied by Instrument Panel 3P23. The analysis noted that output voltage measurements for the CVTs over the last 3 years have been >120VAC and that some equipment such as the Hagan instrument modules are rated less than 120VAC (117V+/-10%), thus providing reasonable assurance that adequate voltage would be supplied by the alternate CVT source until a formal evaluation is performed.

Analysis:

The inspectors determined that the failure to perform adequate design calculations to support the setpoint of the degraded voltage relays and the failure to perform adequate design calculations for the 120Vac instrument system was a performance deficiency. The finding was more than minor because it affected the Mitigating Systems Cornerstone attribute of Design Control, and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. In addition the finding is similar to IMC 0612 Appendix E, example 3.j because the issue resulted in a condition where there was a reasonable doubt with respect to operability of safety-related components. Specifically, there was reasonable doubt as to whether the components would have adequate voltage to perform their safety function during a degraded voltage condition. The finding was considered to be of very low safety significance (Green) since this was a design deficiency confirmed not to have resulted in a loss of operability or functionality. The team determined that no cross cutting aspect was applicable to this performance deficiency because this finding was not indicative of current licensee performance.

Enforcement:

10 CFR 50, Appendix B, Criterion III, Design Control, requires, in part, that design control measures provide for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program.

Contrary to the above, as of August 12, 2011 the licensees design control measures failed to check the adequacy of design for the degraded voltage relay setpoint and the adequacy of design for the voltage to the 120VAC Instrument AC system. Specifically, the licensees degraded voltage analyses failed to properly consider the voltage requirements of starting motors, MOVs and the CVTs; and did not have adequate calculations to enable proper evaluation of changes to the 120Vac system. Because this violation was of very low safety significance and because the issue was entered into the licensees CAP as ARs 1677149, 1677149-02, 1673843, 1677149-02, 1676754 and 01676641 this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy and designated as NCV 05000250/2011008-04 and 05000251/2011008-04 Inadequate Voltage Calculations.

.2.5 Unit 4 MOV 843A/B, HHSI Pump to Cold Leg Injection Valves

a. Inspection Scope

The team reviewed the plants TS, UFSAR, DBDs, and P&IDs to establish an overall understanding of the design bases of valves 843A and 843B. The team reviewed records of surveillance testing, maintenance activities, and applicable corrective actions to verify that potential degradation was being monitored and prevented or corrected.

The team also conducted interviews with plant personnel to discuss the history of the valve testing, maintenance, and details of the corrective actions that had been completed. The team also conducted a visual inspection of both valves to verify that any degraded material conditions were being appropriately addressed. In addition, the team verified that the power demand requirements for the valves were captured in electrical load and degraded voltage calculations. The team also verified that the worst case/highest differential pressure was used to determine the maximum valve opening and/or closing requirements to ensure that the valve would perform its intended safety-related design basis function. A review was conducted of the licensees testing procedures and a review of results from diagnostic valve testing was performed to verify that both MOVs were tested in a manner that would detect a malfunctioning valve and verify compliance with Generic Letter (GL) 89-10 program plan requirements.

b. Findings

No findings were identified.

.2.6 120Vac Instrument Bus 3P08/3P27

a. Inspection Scope

The team reviewed 120Vac Instrument System load lists, design calculations, and modification packages to determine whether inverters were applied within their specified ratings, and whether system voltage drop had been adequately evaluated. The team reviewed system arrangement drawings, DBD and TS to determine whether the system design was consistent with its design and licensing bases. The team reviewed maintenance procedures, technical manuals, schedules and completed work orders to determine whether the 120 Vac instrument system was being properly maintained. The team reviewed maintenance rule scoping criteria for the 120 Vac instrument system to determine whether the system and components were being properly tracked. The team reviewed maintenance records and corrective action history for 120 Vac instrument system components to determine whether there had been any adverse operating trends.

In addition, the team performed a visual inspection of the components to assess material condition and the presence of hazards.

b. Findings

See Section 1R21.2.3 and 2.4

.2.7 Unit 4 Motor Operated Valve (MOV) 626 and Check Valves 4-721A/B/C (Containment

Related Sample)

a. Inspection Scope

The inspectors reviewed applicable portions of the plants TS, UFSAR, DBDs, system descriptions, and system lesson plans to identify design basis requirements for MOV 4-626 and check valves 4-721A/B/C. Component walkdown of MOV 4-626 was conducted to verify that the installed configurations would support the design basis function under accident conditions and had been maintained to be consistent with design assumptions.

The inspectors conducted a non-intrusive visual inspection of MOV 4-626 to verify that potentially degraded material conditions were being appropriately addressed. The inspectors compared valve testing data with the design requirements to verify that valve performance was adequate. The inspectors reviewed calculations that determined required valve actuator torque and thrust limits and traced these requirements to the vendor-supplied data. The inspectors interviewed the system engineer and MOV engineer to discuss the valve analysis as well as operational and maintenance history to verify that potentially degraded conditions were being appropriately addressed. Control logic diagrams were reviewed to verify that controls and interlocks were consistent with the design-basis performance requirements and operating procedures. The inspectors reviewed system modifications to verify that modifications did not degrade the performance capability of the valves and were appropriately incorporated into relevant drawings and procedures. Control panel indicators were observed and operating procedures reviewed to verify that component operation and alignments were consistent with design and licensing bases assumptions. Test procedures and recent test results were reviewed against design bases documents to verify that acceptance criteria for tested parameters were supported by calculations or other engineering documents and that individual tests and analyses served to validate component operation under accident conditions. The inspectors examined maintenance rule documentation to verify that the valves were properly scoped, and monitored. Vendor documentation, system health reports, preventive and corrective maintenance history, and corrective action system documents were reviewed in order to verify that potential degradation was monitored or prevented and that scheduled component replacements were consistent with vendor recommendations and equipment qualification life. Additionally, associated electrical calculations were reviewed to confirm that the design basis minimum voltage at the MOV motor terminals was consistent with the design inputs used in the MOV thrust calculations, and that the thermal overload heaters protecting the motors would not prematurely trip. The team verified by review of control diagrams, that the operation of the MOV is consistent with the design basis and operational requirements. Also, the team verified testing and calibration of instruments related to the valve.

b. Findings

No findings were identified.

.2.8 Emergency Diesel Generator (EDG) 3A and 3B Fuel Oil Supply

a. Inspection Scope

The team reviewed the UFSAR, TS, DBD, and P&IDs to establish an overall understanding of the design bases of the EDG with special emphasis on the fuel oil supply and delivery system. Design calculations and site procedures were reviewed to verify that the design bases and design assumptions had been appropriately translated into these documents. The team reviewed system modifications to verify that the modifications did not degrade the components performance capability and were appropriately incorporated into relevant drawings and procedures. The team focused on vulnerability to flooding. Component walkdowns were conducted to verify that the installed configurations would support their design bases function under accident, flood, and loss of offsite power conditions and had been maintained to be consistent with design assumptions. Operating procedures were reviewed to verify that component operation and alignments were consistent with design and licensing bases assumptions.

Test procedures and results were reviewed against the design bases to verify that acceptance criteria for tested parameters were supported by calculations or other engineering documents and that tests and analyses served to validate component operation under accident and loss of offsite power conditions. Vendor documentation, preventive and corrective maintenance history, and corrective action system documents were reviewed to ascertain that potential degradation was monitored or prevented and that component rework and replacement was consistent with equipment qualification life.

b. Findings

Introduction:

The team identified a SL-IV NCV for the licensees failure to update the Updated Final Safety Analysis Report (UFSAR) for a modification affecting the Unit 3 emergency diesel generator fuel oil storage tank. Specifically, a common-mode failure method was not described in the UFSAR that required proceduralized manual actions during design bases rain events.

Description:

The EDG fuel oil storage and transfer system is credited in the UFSAR, Section 9.15.1.1, for providing a storage capacity of fuel oil for seven days and maintaining that fuel supply to at least one Unit 3 EDG. In addition, UFSAR, Section 9.15.1.2, states that diesel oil is normally transferred from the diesel oil storage tank automatically to maintain diesel oil day tank level. In April 2005, Plant Change/Modification 04-036 was approved to replace the existing aggregate base surrounding the Unit 3 EDG fuel oil storage tank with an impervious surface of concrete.

The berm and associated ramps were installed in order to ensure compliance with new oil pollution prevention requirements by capturing any oil spills. The licensee conducted a 10 CFR 50.59 evaluation to review potential flooding of the Unit 3 EDG fuel oil storage tank area due to the modification. The evaluation identified that the modification presented a new common-mode failure method (design basis rain event) for the EDG fuel oil storage tank isolation valves (solenoid valves SV-3-2051A & B), which, during a design basis rainfall, would become submerged, fail closed, and prevent the flow of diesel fuel oil from the storage tank to the day tanks. The licensee installed reach rods onto manual bypass valves 3-70-010A & B and implemented procedural guidance to manually open the bypass valves as part of hurricane preparations and to implement operator actions during rounds to drain any standing water in the tank area.

The licensees procedure for updating the UFSAR, ENG Q1-3.4, UFSAR Updating, Rev.5 contained guidance which stated the existing level of detail typically provides a sufficient basis for determining whether an UFSAR change is required. The version of the UFSAR in effect at the time of the modification referenced downstream air-operated valves and other solenoid valves in the diesel fuel oil flow path as well as their associated manual actions. ENG Q1-3.4 also stated, that new or revised restrictions on facility operation should be included in the UFSAR. The inspectors determined that although the licensees evaluation concluded that prior NRC approval was not required for the modification, the licensee failed to translate a description of the new common-mode failure (design basis rain event) of the solenoid valves and the alternate use of the manual valves into the UFSAR. Failure to update the UFSAR to include this new information resulted in erroneous information being contained in the current version of the UFSAR. Specifically, for design bases rain events, the operation of the fuel oil transfer system was not automatic as described in the UFSAR. This issue was entered into the licensees corrective action program as AR 1679078.

Analysis:

The failure to update the UFSAR as required by procedure ENG Q1-3.4 and 10 CFR 50.71(e) was a performance deficiency. This performance deficiency was considered as traditional enforcement because, not having an adequately updated UFSAR hinders the licensees ability to perform adequate 10 CFR 50.59 evaluations and can impact the NRCs ability to perform its regulatory function such as, license amendment reviews and inspections. In addition, the team determined that the performance deficiency was material to safety because the modification resulted in a common-mode failure method that required proceduralized manual actions for the Unit 3 EDGs to meet their mission time during design bases rain events. This violation was determined to be a SL-IV violation using Section 6.1 of the NRCs Enforcement Policy because the erroneous information was not used to make an unacceptable change to the facility or procedures. Cross-cutting aspects are not assigned for traditional enforcement violations.

Enforcement:

10 CFR 50.71(e) requires, in part, that the licensee shall update periodically, the final safety analysis report originally submitted as part of the application for the license, to assure that the information included in the report contains the latest information developed. The submittal shall include the effects of all changes made in the facility or procedures as described in the final safety analysis report and all safety analyses and evaluations performed by the licensee in support of conclusions that changes did not require a license amendment in accordance with 10 CFR 50.59(c)(2).

Contrary to the above, from April 2005, to August 12, 2011, the licensee did not update the UFSAR to include the effects of changes made to the facility and procedures as part of the modification that affected the Unit 3 fuel oil storage tank. Specifically, a common-mode failure method was not described in the UFSAR that required proceduralized manual actions during design bases rain events because this violation was determined to be a SL-IV violation and was entered into the licensees corrective action program as AR 1679078, it is being treated as an NCV in accordance with Section 2.3.2 of the NRC Enforcement Policy. The violation is identified as: NCV 05000250, 251/2011008-05, Failure to Update the UFSAR to Reflect Changes to the Unit 3 Fuel Oil Storage and Transfer System.

.2.9 Cross-tie Breakers 3AD07,4AD07 and Associated Components

a. Inspection Scope

The team reviewed load flow calculations to verify that the cross-tie components were assessed within their specified capacity ratings under worst case accident loading. The team reviewed EDG loading calculations to verify that loads do not exceed EDG capacity and that the licensee properly accounted for frequency changes. Also, the team reviewed design bases documents and operation procedures to verify that the EDG loading calculation accounted for all accident loads. In addition, the team reviewed short circuit calculations to verify that the duty cycle does not exceed the equipment protection ratings. The team reviewed calculations for protective device settings to determine whether the breakers were subject to spurious tripping, and whether the breakers were selectively coordinated with upstream devices. The team reviewed completed test procedures for the cross-tie breakers to verify the trip accuracy of breakers. One-line and schematic diagrams were reviewed to verify proper configuration of the electrical distribution system. The team performed a walkdown to verify material condition of the cross-tie equipment and reviewed a sample of corrective action system documents to confirm that the licensee adequately identified, evaluated, and dispositioned adverse conditions. The team also reviewed off-normal and emergency operating procedures to verify that adequate guidance exists for operators to perform the 4KV cross-tie during a station blackout event.

b. Findings

No findings were identified.

.2.10 Unit 3 Switchyard Breakers for Start-up Transformers

a. Inspection Scope

The team reviewed battery sizing calculations to verify that loads do not exceed battery bank capacity. For station blackout event and loss of coolant accident scenarios, the team verified that all control circuit breaker loads were accounted for in the loading calculation. Also, a review of the battery service test was performed to verify that for the required current, the battery can provide the adequate voltage during an accident. One-line and schematic diagrams were reviewed to verify proper configuration of the electrical controls. The team performed a walkdown to verify material condition of the switchyard batteries and start-up transformers.

Also, the team reviewed bus load flow, short-circuit and voltage drop calculations to determine whether the start-up transformers were applied within their specified capacity ratings under worst case accident loading and grid voltage conditions. The team reviewed schematic diagrams and calculations for the transformer to determine whether equipment operation was consistent with the design basis. The team reviewed calculations for protective device settings to determine whether the feeder breakers were subject to spurious tripping, and whether the protective devices were selectively coordinated with upstream devices. The team reviewed maintenance schedules, vendor data, and procedures for breaker routine maintenance and overhauls to determine whether scheduled maintenance activities were consistent with vendor recommendations.

The team reviewed recent corrective action documents and completed maintenance and testing records to determine whether there were any adverse operating trends. In addition, the team performed a visual inspection of the breaker to assess observable material condition and the presence of hazards.

b. Findings

Introduction:

The team identified a Green NCV of 10 CFR 50.63, for the licensees failure to test the station blackout (SBO) cross-tie components under loaded conditions. Since 1991, the licensee failed to verify the capability of the SBO crosstie and associated components to carry the required amperage during post installation tests or subsequent periodic maintenance tests.

Description:

In 1991, Turkey Point installed a unit crosstie at the 4.16 kV level to comply with the SBO Rule (10 CFR 50.63). UFSAR, Section 8.2.2.2, states, in part, that the ability to align an alternate source of electrical power in 10 minutes during a station blackout event is provided by a cross-tie which allows the 4.16 kV switchgear of each unit to be connected together. The cross-tie is sized to carry 500 amperes which is the continuous Unit 4 EDGs' rated capacity. The 4.16 kV system has the capability via the cross-tie and the swing switchgear to connect any EDG with either the "A" or "B" switchgear of the opposite unit. The design provides the capability to perform this function from within the Control Room.

The licensees periodic maintenance program for the cross-tie components included breaker functionality testing on an eighteen month frequency, and included an inspection of the breaker connections and a meggar check of the cross-tie cable on a fifty-four month frequency.

The team noted that the licensee did not apply an electrical load to the SBO components during post installation testing that was performed in 1991. Additionally, the team noted that since 1991, the licensees periodic maintenance program does not apply an electrical load to confirm the capability of the cross-tie components to carry the required load during an SBO event. The team determined that the licensees failure to load the components since 1991 is a failure to provide reasonable assurance that the components are capable of fulfilling their safety function during a SBO event. Loading the SBO cross-tie is the most effective method to demonstrate that the system (terminations, breakers, cable, etc.) will be able to perform their design basis function.

This issue was entered into the licensees corrective action program as AR 1676402 and 1680428 to establish a method and frequency for loading the SBO cross-tie cable.

Additionally, during the inspection the licensee performed resistance checks of the cable with favorable results.

Analysis:

The team determined that the licensees failure to perform adequate post installation testing and periodic testing as required by the licensees commitment to RG 1.155, Station Blackout, was a performance deficiency. This finding was more than minor because it affected the Mitigating Systems cornerstone attribute of Equipment Performance and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems and components that respond to initiating events to preclude undesirable consequences (i.e. core damage). Specifically, since the installation of cross-tie components to meet SBO requirements, the licensee failed to test the components in a loaded condition. The lack of testing resulted in a reduced reliability of the SBO cross-tie. In accordance with NRC IMC 0609.04, Initial Screening and Characterization of Findings, the team conducted a Phase 1 SDP screening and determined the finding to be of very low safety significance (Green) because it was not a design issue resulting in loss of function, did not represent an actual loss of a system safety function, did not result in exceeding a TS allowed outage time, and did not affect external event mitigation. The team determined that no cross cutting aspect was applicable to this performance deficiency because this finding was not indicative of current licensee performance.

Enforcement:

10 CFR 50.63, states, in part, that nuclear power plants must be able to withstand for a specified duration and recover from a station blackout. RG 1.155, Sections 3.3.6 states, in part, that a system or component added specifically for a SBO event that initial tests should be performed to verify that modifications were performed properly. RG 1.155, Sections 3.3.7 states, in part, that a system or component added specifically for a SBO event, should be inspected, maintained, and tested periodically to demonstrate equipment operability and reliability.

Contrary to the above, since 1991, the licensee failed to perform appropriate initial tests and periodic tests to demonstrate equipment operability and reliability to withstand and recover from a station blackout. Specifically, the licensee has not verified the capability of the cross-tie components to carry the required amperage via SBO cross-tie components. Because this finding was of very low safety significance and because it was entered into the licensees CAP as AR 1676402 and AR 1680428, this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy and is being designated as NCV 05000250, 251/2011008-06, Failure to Test the SBO Cross-Tie under Loaded Conditions

.2.11 Refueling Water Storage Tank (RWST) Valves 870A and B

a. Inspection Scope

The inspectors reviewed applicable portions of the plant TS, UFSAR, DBDs, system descriptions, and system lesson plans to identify design basis requirements for manual RWST cross-tie valves 870A and 870B. Component walkdown of valves 870A&B were conducted to verify that the installed configurations would support the design basis function under accident conditions and had been maintained to be consistent with design assumptions. The inspectors conducted a non-intrusive visual inspection of valves 870A&B to verify that potentially degraded material conditions were being appropriately addressed. The inspectors reviewed operational and maintenance history to verify that potentially degraded conditions were being appropriately addressed. Operating procedures were reviewed to verify that component operation and alignments were consistent with design and licensing basis assumptions. The inspectors examined maintenance rule documentation to verify that the valves were properly scoped, and monitored. Vendor documentation, system health reports, preventive and corrective maintenance history, and corrective action system documents were reviewed in order to verify that potential degradation was monitored or prevented.

b. Findings

No findings were identified.

.2.12 3A HHSI Pump

a. Inspection Scope

The team reviewed the plants TS, UFSAR, DBDs, and P&IDs to establish an overall understanding of the design bases of the pumps. Design calculations and site procedures were reviewed to verify that the design bases and design assumptions had been appropriately translated into these documents. Component walk downs were conducted to verify that the installed configurations would support their design bases function under accident/event conditions and had been maintained to be consistent with design assumptions. Test procedures and recent test results were reviewed against design basis documents to verify that acceptance criteria for tested parameters were supported by calculations or other engineering documents and that individual tests and/or analyses validated component operation under accident/event conditions. Vendor documentation, preventive and corrective maintenance history, and corrective action system documents were reviewed to verify that potential degradation was being monitored.

b. Findings

See Section 1R21.2.2

.2.13 Turbine Plant Cooling Water Isolation Valves (TPCW) - 4882/4883

a. Inspection Scope

The team reviewed the plant TS, UFSAR, DBDs, and P&IDs to establish an overall understanding of the design bases of pneumatically operated valves (POV) 4882 &

4883. The team reviewed records of surveillance testing, maintenance activities, and applicable corrective actions to verify that potential degradation was being monitored and prevented or corrected. The team also conducted interviews with plant personnel to discuss the history of valve testing, maintenance, and corrective actions that had been completed. The team also conducted a visual inspection of all valves to verify that any degraded material conditions were being appropriately addressed. The team also examined documentation to verify that the valves were properly scoped, and monitored in the maintenance rule program.

b. Findings

.2.14 Emergency Diesel Generator (EDG) 4A and 4B Fuel Oil Supply

a. Inspection Scope

The team reviewed the UFSAR, TS, DBD, and P&IDs to establish an overall understanding of the design bases of the EDG with special emphasis on the fuel oil supply and delivery system. Design calculations and site procedures were reviewed to verify that the design bases and design assumptions had been appropriately translated into these documents. The team reviewed system modifications to verify that the modifications did not degrade the components performance capability and were appropriately incorporated into relevant drawings and procedures. The team focused on vulnerability to flooding. Component walkdowns were conducted to verify that the installed configurations would support their design bases function under accident, flood, and loss of offsite power conditions and had been maintained to be consistent with design assumptions. Operating procedures were reviewed to verify that component operation and alignments were consistent with design and licensing bases assumptions.

Test procedures and results were reviewed against the design bases to verify that acceptance criteria for tested parameters were supported by calculations or other engineering documents and that tests and analyses served to validate component operation under accident and loss of offsite power conditions. Vendor documentation, preventive and corrective maintenance history, and corrective action system documents were reviewed to ascertain that potential degradation was monitored or prevented and that component rework and replacement was consistent with equipment qualification life.

b. Findings

No findings were identified.

.2.15 Unit 3 Load Center and Switchgear Rooms - Alternate Cooling Function

a. Inspection Scope

The team reviewed the UFSAR, PI&Ds, design specifications and design basis temperature limits for electrical components in the load center and switchgear room to establish an overall understanding of the alternate cooling function. The team reviewed calculations, analyses, and modifications to verify the capability of the alternate cooling function to remove the required heat loads during postulated events. The team reviewed the operating procedure to verify the adequacy of guidance for manual operator actions.

Additionally, the team performed a walkdown to verify the feasibility of implementing the alternate cooling strategy.

b. Findings

See Section 1R21.2.2

.3 Operating Experience (4 Samples)

a. Inspection Scope

The team reviewed four operating experience issues for applicability at the Turkey Point Nuclear Plant. The team performed an independent applicability review for these issues and where applicable, assessed the licensees evaluation and dispositioning of each item. The issues that received a detailed review by the team included:

[General Electric HFA and HGA Relays]

  • H. B. Robinson, LER 2010-005-00: EDG Inoperable Due to Inverter Failure
  • NRC Information Notice IN 2010-09, Importance of Understanding Circuit Breaker Control Power Indications

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA6 Meetings, Including Exit

On September 8, 2011, the team presented the inspection results to Mr. M. Kiley and other members of the licensees staff. Proprietary information that was reviewed during the inspection was returned to the licensee.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

S. Bell, Mechanical Design Engineer
S. Chaviano, Design Engineering Supervisor
J. Garcia, Engineering Manager
R. Everett, Licensing
R. Tomonto, Licensing Manager

NRC personnel

B. Desai, Chief, Engineering Branch Chief 1, Division of Reactor Safety, RII
S. Stewart, Senior Resident Inspector, Turkey Point

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Opened and Closed

05000250 & 251/2011008-01 NCV Failure to Verify or Check the Adequacy of Design for Safety-Related Components with Four Examples (Section 1R21.2.2)
05000250 & 251/2011008-03 NCV Failure to Maintain Adequate Records to Support Acceptance Criteria in Design Calculations (Section 1R21.2.4.b.1)
05000250 & 251/2011008-04 NCV Inadequate Voltage Calculations (Section 1R21.2.4.b.2)
05000250 & 251/2011008-05 SL-IV Failure to Update the UFSAR to Reflect Changes to the Unit 3 Fuel Oil Storage and Transfer System (Section 1R21.2.8)
05000250 & 251/2011008-06 NCV Failure to Test the SBO Cross-Tie under Loaded Conditions (Section 1R21.2.10)

Opened

05000250 & 251/2011008-02 URI Molded Case Circuit Breaker Testing (Section 1R21.2. 3)

LIST OF DOCUMENTS REVIEWED