IR 05000250/2019004
| ML20030A024 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point, 07200062 |
| Issue date: | 01/30/2020 |
| From: | Randy Musser NRC/RGN-II |
| To: | Moul D Florida Power & Light Co |
| References | |
| IR 2019001, IR 2019004 | |
| Download: ML20030A024 (11) | |
Text
January 30, 2020
SUBJECT:
TURKEY POINT UNITS 3 & 4 - INTEGRATED INSPECTION REPORT 05000250/2019004 AND 05000251/2019004 AND INDEPENDENT SPENT FUEL STORAGE INSTALLATION INSPECTION (ISFSI) REPORT 07200062/2019001
Dear Mr. Moul:
On December 31, 2019, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Turkey Point Units 3 & 4. On January 16, 2020, the NRC inspectors discussed the results of this inspection with Mr. Brian Stamp, Site Director, and other members of your staff.
The results of this inspection are documented in the enclosed report.
No findings or violations of more than minor significance were identified during this inspection.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Randall A. Musser, Chief Reactor Projects Branch 3 Division of Reactor Projects
Docket Nos. 05000250, 05000251, and 07200062 License Nos. DPR-31 and DPR-41
Enclosure:
As stated
Inspection Report
Docket Numbers:
05000250, 05000251, and 07200062
License Numbers:
Report Numbers:
05000250/2019004, 05000251/2019004 and 07200062/2019001
Enterprise Identifier: I-2019-004-0020 and I-2019-001-0148
Licensee:
Florida Power & Light Company
Facility:
Turkey Point Units 3 & 4
Location:
Homestead, FL 33035
Inspection Dates:
October 01, 2019 to December 31, 2019
Inspectors:
D. Bacon, Senior Operations Engineer
M. Bates, Senior Operations Engineer
J. Orr, Senior Resident Inspector
J. Reyes, Resident Inspector
Approved By:
Randall A. Musser, Chief
Reactor Projects Branch 3
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees
performance by conducting an integrated inspection at Turkey Point Units 3 & 4, in accordance
with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for
overseeing the safe operation of commercial nuclear power reactors. Refer to
https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
No findings or violations of more than minor significance were identified.
Additional Tracking Items
None.
PLANT STATUS
Unit 3 operated at or near rated thermal power for the entire inspection period.
Unit 4 operated at or near rated thermal power for the entire inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in
effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with
their attached revision histories are located on the public website at http://www.nrc.gov/reading-
rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared
complete when the IP requirements most appropriate to the inspection activity were met
consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection
Program - Operations Phase. The inspectors performed plant status activities described in
IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem
Identification and Resolution. The inspectors reviewed selected procedures and records,
observed activities, and interviewed personnel to assess licensee performance and compliance
with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.04Q - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (2 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following
systems/trains:
(1)
Unit 3 start-up transformer (SUT) and the 4A and 4B emergency diesel generators
(EDGs) while the Unit 4 SUT was out of service (OOS) for testing on November 05,
2019
(2)
3A EDG and the 3A, 4A, and 4B safety injection pumps while the 3B EDG was OOS
for maintenance on October 09 and 12, 2019
71111.04S - Equipment Alignment
Complete Walkdown Sample (IP Section 03.02) (1 Sample)
(1)
The inspectors evaluated system configurations during a complete walkdown of the
Unit 3 and Unit 4 charging and boric acid storage tank systems on November 01, 07,
08, 12, and 13, 2019.
71111.05Q - Fire Protection
Quarterly Inspection (IP Section 03.01) (5 Samples)
The inspectors evaluated fire protection program implementation in the following selected
areas:
(1)
Fire zones (FZs) 019, 020, 026 and 027 for the Unit 3 south and west electrical
penetration rooms (EPRs) and the Unit 4 north and west EPRs on November 05,
2019
(2)
FZ 079A for the auxiliary building breezeway on November 08, 2019
(3)
FZ 010 for the auxiliary building 10-foot elevation outside of the high radiation areas
on November 12, 2019
(4)
FZs 093 and 094 for the safety-related Unit 4A/4B and 4C/4D 480-volt load centers
on December 12, 2019
(5)
FZs 067 and 068 for the safety-related 4A and 4B 4kV switchgear rooms on
December 20, 2019
71111.06 - Flood Protection Measures
Inspection Activities - Internal Flooding (IP Section 02.02a.) (1 Sample)
The inspectors evaluated internal flooding mitigation protections in the:
(1)
Units 3 and 4 residual heat removal pump and heat exchanger rooms on November 4
- 7, 2019
71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance
Requalification Examination Results (IP Section 03.03) (1 Sample)
The licensee completed the annual requalification operating examinations required to be
administered to all licensed operators in accordance with Title 10 of the Code of Federal
Regulations 55.59(a)(2), Requalification Requirements, of the NRCs Operators
Licenses. During the week of December 23, 2019, the inspector performed an in-office
review of the overall pass/fail results of the individual operating examinations, the crew
simulator operating examinations, and the biennial written examinations in accordance with
Inspection Procedure (IP) 71111.11, Licensed Operator Requalification Program. These
results were compared to the thresholds established in Section 3.02, Requalification
Examination Results, of IP 71111.11.
(1)
The inspectors reviewed and evaluated the licensed operator examination failure
rates for the requalification annual operating exam administered on December 26,
2019.
71111.11B - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Requalification Program (IP Section 03.04) (1 Sample)
The inspectors completed an inspection to verify the licensees ability to evaluate the
performance of their licensed operators during the conduct of examinations, to assess their
ability to properly develop and administer requalification annual operating tests and biennial
written examinations, to evaluate the performance of the control room simulator and their
testing and maintenance of the simulator, to ensure that licensed individuals satisfy the
conditions of their licenses, and to assess their effectiveness in ensuring that operator
license conditions are satisfied.
(1)
Biennial Requalification Written Examinations
The inspectors evaluated the quality of the licensed operator biennial requalification
written examination administered on November 18, 2019.
Annual Requalification Operating Tests
The inspectors evaluated the adequacy of the facility licensees annual requalification
operating test.
Administration of an Annual Requalification Operating Test
The inspectors evaluated the effectiveness of the facility licensee in administering
requalification operating tests required by 10 CFR 55.59(a)(2) and that the facility
licensee is effectively evaluating their licensed operators for mastery of training
objectives.
Requalification Examination Security
The inspectors evaluated the ability of the facility licensee to safeguard examination
material, such that the examination is not compromised.
Remedial Training and Re-examinations
The inspectors evaluated the effectiveness of remedial training conducted by the
licensee, and reviewed the adequacy of re-examinations for licensed operators who
did not pass a required requalification examination.
Operator License Conditions
The inspectors evaluated the licensees program for ensuring that licensed operators
meet the conditions of their licenses.
Control Room Simulator
The inspectors evaluated the adequacy of the facility licensees control room
simulator in modeling the actual plant, and for meeting the requirements contained in
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1
Sample)
(1)
The inspectors observed and evaluated licensed operator performance in the control
room during surveillance test 4-OSP-028.6, Rod Control Cluster Assembly (RCCA)
Periodic Exercise on October 17, 2019
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
(1)
The inspectors observed and evaluated a requalification training simulator scenario
administered to an operating crew on November 25, 2019
71111.12 - Maintenance Effectiveness
Routine Maintenance Effectiveness Inspection (IP Section 02.01) (2 Samples)
The inspectors evaluated the effectiveness of routine maintenance activities associated with
the following equipment and/or safety significant functions:
(1)
Action requests (ARs) 2316994, 2317227, 2317749, and 2320802, 3A intake cooling
water pump stopped due to high amps and motor overload alarm (event date was
June 5, 2019) on November 14, 25 and 26, 2019
(2)
AR 2334034, 3C charging pump seal failures (event date was November 1, 2019) on
November 26 and 27, 2019
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)
The inspectors evaluated the risk assessments for the following planned and emergent work
activities:
(1)
4B charging pump, 3B EDG, and 4B EDG control panel room air conditioning
unit 4S231B OOSs on October 4, 7, 8, and 10, 2019
(2)
4C component cooling water (CCW) pump, 4C intake cooling water (ICW) pump, 3A
safety injection pump and safety-related 4D 4kV switchgear OOSs on October 23,
2019
(3)
3C charging pump and 4C ICW pump OOSs on November 13 and 14, 2019
(4)
Unit 3 start-up transformer, auxiliary feedwater train 1, 4A ICW pump and 4A
CCW pump OOSs on November 20 and 21, 2019
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 02.02) (4 Samples)
The inspectors evaluated the following operability determinations and functionality
assessments:
(1)
AR 2331140, RD-3/4-15 Administrative limit for in-leakage found incorrect on October
23, November 05, 06 and 07, 2019
(2)
ARs 2335574, 2335576 and 2335599, Control rod drive mechanism G-3 misaligned
during RCCA drive mechanism exercising on November 14, 15 and 26, 2019
(3)
ARs 2336434, 2336438 and 2015046, Gas void identified in high head safety
injection system on November 21, 2019
(4)
AR 2338565, 3A EDG fuel oil pressure higher than acceptable criteria on December
17 and 19, 2019
71111.19 - Post-Maintenance Testing
Post-Maintenance Test Sample (IP Section 03.01) (6 Samples)
The inspectors evaluated the following post maintenance tests:
(1)
3-OSP-023.1, Diesel Generator Operability Test, after 3B EDG overhaul
maintenance, work order (WO) 40518734
(2)
4-OSP-062.2D, Safety Injection Pump 4A Comprehensive Pump Test, after
mechanical seal and oiler replacement, WO 40583620
(3)
3-OSP-055.1, Emergency Containment Cooler Operability Test, Section 4.2, after
CV-3-2908, 3A emergency containment cooler outlet air-operated valve, piston o-ring
replacement, WO 40675719
(4)
4-OSP-019.1, Intake Cooling Water Inservice Test, Section 7.6, after 4C ICW pump
discharge check valve replacement, WO 40460905
(5)
3-OSP-047.1H, Charging Pump 3C Comprehensive Pump Test, after modification
and replacement of 3C charging pump seal package, WO 40632602
(6)
4-NOP-005, 4kV Busses A, B, and D, after repairing oil leaks and replacing relays
associated with the Unit 4 startup transformer, WO 40249199
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Surveillance Tests (other) (IP Section 03.01) (1 Sample)
(1)
3-OSP-075.7, Auxiliary Feedwater Train 2 Backup Nitrogen Test on October 29, 2019
Inservice Testing (IP Section 03.01) (1 Sample)
(1)
3-OSP-062.2A, Safety Injection Pump 3A Group B Pump Test on December 20, 2019
OTHER ACTIVITIES - BASELINE
71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
MS06: Emergency AC Power Systems (IP Section 02.05) (2 Samples)
(1)
Unit 3, October 2018 through September 2019
(2)
Unit 4, October 2018 through September 2019
MS07: High Pressure Injection Systems (IP Section 02.06) (2 Samples)
(1)
Unit 3, October 2018 through September 2019
(2)
Unit 4, October 2018 through September 2019
MS08: Heat Removal Systems (IP Section 02.07) (2 Samples)
(1)
Unit 3, October 2018 through September 2019
(2)
Unit 4, October 2018 through September 2019
MS09: Residual Heat Removal Systems (IP Section 02.08) (2 Samples)
(1)
Unit 3, October 2018 through September 2019
(2)
Unit 4, October 2018 through September 2019
MS10: Cooling Water Support Systems (IP Section 02.09) (2 Samples)
(1)
Unit 3, October 2018 through September 2019
(2)
Unit 4, October 2018 through September 2019
71152 - Problem Identification and Resolution
Semiannual Trend Review (IP Section 02.02) (1 Sample)
(1)
The inspectors reviewed the licensees corrective action program for
potential trends that might be indicative of a more significant safety issue. The
following issue was reviewed in detail to verify an adverse human performance trend
did not exist during performance of in-service surveillance testing; AR 2336802,
Escalation - Organization, Preparation, Contingency, and Execution of In-service
Tests.
OTHER ACTIVITIES - TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL
60855.1 - Operation of an Independent Spent Fuel Storage Installation at Operating Plants
Operation of an Independent Spent Fuel Storage Installation at Operating Plants (1 Partial)
(1)
(Partial)
The inspectors evaluated FPL's independent spent fuel storage installation cask
loadings on October 22, 2019.
INSPECTION RESULTS
No findings were identified.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On January 16, 2020, the inspectors presented the integrated inspection results to Mr.
Brian Stamp, Site Director, and other members of the licensee staff.
On December 5, 2019, the inspectors presented the Licensed Operator Requalification
Program inspection results to E. Neville, Operations Director, and other members of the
licensee staff.
THIRD PARTY REVIEWS
The inspectors reviewed an Institute on Nuclear Power Operations report that was issued on
January 28, 2019. The inspectors reviewed the report to ensure that issues identified were
consistent with NRC perspectives of licensee performance and to determine if any safety issues
were identified that require further NRC inspection or discussion.