IR 05000250/2022004
| ML23027A096 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point |
| Issue date: | 01/27/2023 |
| From: | David Dumbacher NRC/RGN-II |
| To: | Coffey B Florida Power & Light Co |
| References | |
| IR 2022004 | |
| Download: ML23027A096 (10) | |
Text
SUBJECT:
TURKEY POINT UNITS 3 & 4 - INTEGRATED INSPECTION REPORT 05000250/2022004 AND 05000251/2022004
Dear Bob Coffey:
On December 31, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Turkey Point Units 3 & 4. On January 10, 2023, the NRC inspectors discussed the results of this inspection with Mr. Michael Pearce and other members of your staff. The results of this inspection are documented in the enclosed report.
No findings or violations of more than minor significance were identified during this inspection.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely, David E. Dumbacher, Chief Reactor Projects Branch 3 Division of Reactor Projects Docket Nos. 05000250 and 05000251 License Nos. DPR-31 and DPR-41
Enclosure:
As stated
Inspection Report
Docket Numbers:
05000250 and 05000251
License Numbers:
Report Numbers:
05000250/2022004 and 05000251/2022004
Enterprise Identifier: I-2022-004-0022
Licensee:
Florida Power & Light Company
Facility:
Turkey Point Units 3 & 4
Location:
Homestead, FL
Inspection Dates:
October 01, 2022 to December 31, 2022
Inspectors:
J. Bundy, Senior Operations Engineer
M. Endress, Senior Resident Inspector
J.R. Reyes, Resident Inspector
Approved By:
David E. Dumbacher, Chief
Reactor Projects Branch 3
Division of Reactor Projects
Enclosure
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees
performance by conducting an integrated inspection at Turkey Point Units 3 & 4, in accordance
with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for
overseeing the safe operation of commercial nuclear power reactors. Refer to
https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
No findings or violations of more than minor significance were identified.
Additional Tracking Items
Type
Issue Number
Title
Report Section
Status
LER 2021-004-00 for Turkey
Point, Unit 3, Through-Wall
Leakage from Core Exit
Thermocouple Tubing
Closed
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in
effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with
their attached revision histories are located on the public website at http://www.nrc.gov/reading-
rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared
complete when the IP requirements most appropriate to the inspection activity were met,
consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection
Program - Operations Phase. The inspectors performed activities described in IMC 2515,
Appendix DProperty "Inspection Manual Chapter" (as page type) with input value "NRC Inspection Manual 2515,</br></br>Appendix D" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process., Plant Status, observed risk-significant activities, and completed on-site portions of
IPs. The inspectors reviewed selected procedures and records, observed activities, and
interviewed personnel to assess licensee performance and compliance with Commission rules
and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Impending Severe Weather Sample (IP Section 03.02) (2 Samples)
(1)
The inspectors evaluated the adequacy of the overall preparations to protect risk-
significant systems from impending severe weather from Hurricane Nicole on
November 8, 2022.
(2)
The inspectors evaluated the adequacy of the overall preparations to protect risk-
significant systems from impending cold weather on December 23, 27, and 28, 2022.
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following
systems/trains:
(1)
Unit 4B containment spray pump (CSP) train while the 4A CSP train was out of
service (OOS) for maintenance, on October 18, 2022
(2)
Unit 3B emergency diesel generator (EDG) while the 3A EDG was OOS for
maintenance, on November 15 and 16, 2022
(3)
Unit 3B CSP while the 3A CSP was OOS for testing, on December 15, 2022
Complete Walkdown Sample (IP Section 03.02) (1 Sample)
(1)
The inspectors evaluated system configurations during a complete walkdown of the
Unit 3 and Unit 4 CSP systems, on December 13, 2022.
71111.05 - Fire Protection
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated the implementation of the fire protection program by conducting a
walkdown and performing a review to verify program compliance, equipment functionality,
material condition, and operational readiness of the following fire areas:
(1)
Unit 3 and Unit 4 component cooling water pump and heat exchanger areas in fire
zones (FZ) 054 and 047; and Unit 3 and Unit 4 CSP rooms in FZ 038 and 031, on
October 12, 2022
(2)
Cable spreading room in FZ 097 and 098, on October 16, 2022
(3)
Unit 4 4A and 4B EDG rooms in FZ 140 and FZ133, on October 19, 2022
(4)
Emergency security diesel engine room, transformer, inverter, and breaker rooms, FZ
165, on October 26, 2022
(5)
Unit 4 4KV switchgear rooms FZ 068 and 067, on December 20, 2022
71111.06 - Flood Protection Measures
Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)
The inspectors evaluated internal flooding mitigation protections in the:
(1)
Unit 3 and Unit 4 4kV switchgear rooms
71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance
Requalification Examination Results (IP Section 03.03) (1 Sample)
(1)
During the week of December 12, 2022, the inspector reviewed and evaluated the
licensed operator examination failure rates for the requalification annual operating
exam that was completed on October 28, 2022. The licensee completed the annual
requalification operating examinations required to be administered to all licensed
operators in accordance with Title 10 of the Code of Federal Regulations 55.59(a)(2),
"Requalification Requirements," of the NRC's "Operator's Licenses." The inspector
performed an in-office review of the overall pass/fail results of the individual operating
examinations and the crew simulator operating examinations in accordance with IP 71111.11, "Licensed Operator Requalification Program." These results were
compared to the thresholds established in Section 3.03, "Requalification Examination
Results," of IP 71111.11.
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1
Sample)
(1)
The inspectors observed and evaluated licensed operator performance in the Control
Room during RI-4-11 paper changeout, the 4A EDG operability run, and Unit 4
reactor startup, on October 13, October 14, and December 7, 2022, respectively.
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
(1)
The inspectors observed and evaluated a training simulator scenario administered to
an operating crew on October 25, 2022.
71111.12 - Maintenance Effectiveness
Maintenance Effectiveness (IP Section 03.01) (1 Sample)
The inspectors evaluated the effectiveness of maintenance to ensure the following
structures, systems, and components (SSCs) remain capable of performing their intended
function:
(1)
Unit 3 startup transformer exceeded maintenance rule availability
Quality Control (IP Section 03.02) (1 Sample)
The inspectors evaluated the effectiveness of maintenance and quality control activities to
ensure the following SSC remains capable of performing its intended function:
(1)
Work order (WO) #40734416, air leak in 3A EDG air start system, on October 3, 2022
Aging Management (IP Section 03.03) (1 Sample)
The inspectors evaluated the effectiveness of the aging management program for the
following SSCs that did not meet their inspection or test acceptance criteria:
(1)
Residual heat removal and seal water heat exchanger shell and cover (WO #40783649-01), and non-regenerative heat exchanger shell and charging pump oil
coolers bonnet (WO #40782723-01)
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated the accuracy and completeness of risk assessments for the
following planned and emergent work activities to ensure configuration changes and
appropriate work controls were addressed:
(1)
Unit 3 and Unit 4 online risk assessment during the risk-informed completion time
entry for the 4A CSP maintenance period, on October 20, 2022
(2)
Unit 3 and Unit 4 online risk assessment while the Unit 3A EDG was OOS for
maintenance, on November 15 and 16, 2022
(3)
Unit 3 and Unit 4 online risk assessment after securing the excess let down system
and subsequently exiting the Unit 3 unusual event, on December 8 and 9, 2022
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 03.01) (1 Sample)
The inspectors evaluated the licensee's justifications and actions associated with the
following operability determinations and functionality assessments:
(1)
Past operability determination for 4B emergency containment cooler outlet valve, on
October 18, 2022
71111.19 - Post-Maintenance Testing
Post-Maintenance Test Sample (IP Section 03.01) (2 Samples)
The inspectors evaluated the following post-maintenance testing activities to verify system
operability and/or functionality:
(1)
WO# 40734416, 3A EDG air start repair
(2)
WO# 40705909, 4A CSP motor replacement and baseplate repair
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance testing activities to verify system operability
and/or functionality:
RCS Leakage Detection Testing (IP Section 03.01) (1 Sample)
(1)
3-OSP-041.1, Reactor Coolant System Leak Rate Calculation, on December 12,
2022
71114.06 - Drill Evaluation
Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)
The inspectors performed the following:
(1)
Observed the emergency preparedness drill and evaluated the scenarios for the
control room simulator and the technical support center on November 3, 2022
OTHER ACTIVITIES - BASELINE
71151 - Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
MS06: Emergency AC Power Systems (IP Section 02.05) (2 Samples)
(1)
Unit 3 (October 1, 2021 through September 30, 2022)
(2)
Unit 4 (October 1, 2021 through September 30, 2022)
MS07: High Pressure Injection Systems (IP Section 02.06) (2 Samples)
(1)
Unit 3 (October 1, 2021 through September 30, 2022)
(2)
Unit 4 (October 1, 2021 through September 30, 2022)
MS08: Heat Removal Systems (IP Section 02.07) (2 Samples)
(1)
Unit 3 (October 1, 2021 through September 30, 2022)
(2)
Unit 4 (October 1, 2021 through September 30, 2022)
MS09: Residual Heat Removal Systems (IP Section 02.08) (2 Samples)
(1)
Unit 3 (October 1, 2021 through September 30, 2022)
(2)
Unit 4 (October 1, 2021 through September 30, 2022)
MS10: Cooling Water Support Systems (IP Section 02.09) (2 Samples)
(1)
Unit 3 (October 1, 2021 through September 30, 2022)
(2)
Unit 4 (October 1, 2021 through September 30, 2022)
71152A - Annual Follow-up Problem Identification and Resolution
Annual Follow-up of Selected Issues (Section 03.03) (1 Sample)
The inspectors reviewed the licensees implementation of its corrective action program
related to the following issues:
(1)
Action request (AR) 2445288, intake fire system piping support degradation
71152S - Semiannual Trend Problem Identification and Resolution
Semiannual Trend Review (Section 03.02) (1 Sample)
(1)
The inspectors reviewed the licensees corrective action program for potential
adverse trends in the 3A EDG air start system reliability that might be indicative of a
more significant safety issue.
71153 - Follow Up of Events and Notices of Enforcement Discretion
Event Followup (IP Section 03.01) (1 Sample)
(1)
The inspectors evaluated the licensee's declaration of a Notice of Unusual Event
(Event Notification 56264) for unidentified reactor coolant system (RCS)
leakage of greater than 10 gpm for more than 15 minutes, and the licensees
response on December 8, 2022. EN 56264 was retracted on January 9, 2023, when
the licensee obtained additional information, not available at the time of the initial
notification, which demonstrated that an actual RCS leak did not exist on December
8, 2022, therefore, the event declaration was not required. The inspectors evaluated
the licensees basis for the retraction.
Event Report (IP Section 03.02) (1 Sample)
The inspectors evaluated the following licensee event reports (LERs):
(1)
LER 05000250/2021-004-00, Through-Wall Leakage from Core Exit Thermocouple
Tubing (ADAMS Accession No. ML22006A109). This LER was submitted and
subsequently retracted by licensee correspondence titled "Cancellation of LER 2021-
004, Through-Wall Leakage from Core Exit Thermocouple Tubing," dated March 28,
2022 (ADAMS Accession No. ML22087A079).
INSPECTION RESULTS
No findings were identified.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
On January 10, 2023, the inspectors presented the integrated inspection results to Mr.
Michael Pearce and other members of the licensee staff.