05000336/LER-1997-023, Updates NRC Staff Re Submittal of Suppl to LER 97-023-00 as Committed to by Facility for Unit 2 in LER 97-023-00.LER 50-336/97-023-00 Contained Listed Commitment for Unit 2

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Updates NRC Staff Re Submittal of Suppl to LER 97-023-00 as Committed to by Facility for Unit 2 in LER 97-023-00.LER 50-336/97-023-00 Contained Listed Commitment for Unit 2
ML20217K682
Person / Time
Site: Millstone Dominion icon.png
Issue date: 10/23/1997
From: Bowling M
NORTHEAST NUCLEAR ENERGY CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
B16821, NUDOCS 9710280373
Download: ML20217K682 (2)


LER-2097-023, Updates NRC Staff Re Submittal of Suppl to LER 97-023-00 as Committed to by Facility for Unit 2 in LER 97-023-00.LER 50-336/97-023-00 Contained Listed Commitment for Unit 2
Event date:
Report date:
3362097023R00 - NRC Website

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Docket No, 50 336 B16821 U.S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, DC 20555 l

l Millstone Nuclear Power Station Unit No. 2 Update on the Status of Licensee Event Report 97-023 Minimum HPSI flow used in FSAR Accident Analysis may be Non-conservative The purpose of this letter is to update the NRC Staff concerning our submittal of a supplement to LER 97-023-00 as committed to by Northeast Nuclear Energy Company I

(NNECO) for Millstone Unit No. 2 in LER 97-023-00.0)

LER 50-336/97-023-00 contained the following commitment for Millstone Unit No. 2:

816599-02: Investigation of this event is continuing to ensure appropriate corrective actions are identified. A supplement to this LER will be submitted by October 1,1997 to provide additional information identified as a result of this investigation.

As of October 21,1997 analyses are ongoing to determine if any changes to operational parameters are required.

Commitments:

B16821-01: Millstone Unit No. 2 will complete appropriate corrective actions and M submit a supplement to LER 97-023-00 prior to plant entry into MODE 4 /T from the current outage, jf V 9710280373h[1'lfd d gDR ADOCK 05000336 g POR "I

LER 50-336/97 023 00,' Minimum HPSI flow used in FSAR Accident Analysis may be Non-conservative,' dated July 14,1997, t

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  • U.S. Nucl::r Regul: tory Commission B16821/Page 2 Should you have any questions on the information provided, please contact Mr. R. G.

Joshi at (860) 440-2080.

Very truly yours, NORTHEAST NUCLEAR ENERGY COMPANY Nk Martin L. Bowling, Jr/

Millstone Unit No. 2 Recovery Officer I cc: H. J. Miller, Region l Administrator D. G. Mcdonald, Jr., NRC Senior Project Manager, Millstone Unit No. 2 D. P. Beaulieu, Senior Resident inspector, Millstone Unit No. 2 W. D. Travers, Ph.D., Director, Special Projects Office P. F. McKee, Deputy Director of Licensing, Special Projects Office W. D. Lanning, Deputy Director of Inspections, Special Projects Office