ML22118A936

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Integrated Inspection Report 05000275/2022001 and 05000323/2022001
ML22118A936
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 05/05/2022
From: Jason Kozal
NRC/RGN-IV/DORS/PBA
To: Gerfen P
Pacific Gas & Electric Co
References
IR 2022001
Download: ML22118A936 (23)


See also: IR 05000275/2022001

Text

May 05, 2022

Ms. Paula A. Gerfen, Senior Vice President,

and Chief Nuclear Officer

Pacific Gas and Electric Company

P.O. Box 56

Mail Code 104/6

Avila Beach, CA 93424

SUBJECT: DIABLO CANYON POWER PLANT, UNITS 1 AND 2 - INTEGRATED

INSPECTION REPORT 05000275/2022001 AND 05000323/2022001

Dear Ms. Gerfen:

On March 31, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at Diablo Canyon Power Plant, Units 1 and 2. On April 7, 2022, the NRC inspectors discussed

the results of this inspection with you and other members of your staff. The results of this

inspection are documented in the enclosed report.

Three findings of very low safety significance (Green) are documented in this report. All of

these findings involved violations of NRC requirements. We are treating these violations as

non-cited violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violations or the significance of the violations documented in this inspection

report, you should provide a response within 30 days of the date of this inspection report, with

the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document

Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator,

Region IV; the Director, Office of Enforcement; and the NRC Resident Inspector at Diablo

Canyon Power Plant, Units 1 and 2.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; and the

NRC Resident Inspector at Diablo Canyon Power Plant, Units 1 and 2.

P. Gerfen 2

This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document

Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public

Inspections, Exemptions, Requests for Withholding.

Sincerely,

Jason W. Kozal, Chief

Projects Branch A

Division of Operating Reactor Safety

Docket Nos. 05000275 and 05000323

License Nos. DPR-80 and DPR-82

Enclosure:

As stated

cc w/ encl: Distribution via LISTSERV

Signed by Kozal, Jason

on 05/05/22

ML22118A936 KEYWORD- NRC-002

SUNSI Review X Non-Sensitive X Publicly Available

X PVossmar Sensitive Non-Publicly Available

OFFICE ASRI:DORS/A RI:DORS/A ASRI:DORS/A ASRI:DORS/A BC:DORS/EB1

NAME NHernandez /RA/AAthar AA NDay NHD JDrake /RA/ VGaddy /RA/

DATE 4/28/2022 5/2/2022 04/29/2022 5/2/2022 5/2/2022

OFFICE BC:DORS/EB2 BC:DORS/OB BC:DRSS/RCB TL:DORS/IPAT BC:DRSS/RxIB

NAME NTaylor /RA/ HGepford /RA/ MHaire MSH AAgrawal /RA/ GWarnick /RA/

DATE 5/2/2022 4/29/2022 04/28/2022 4/29/2022 5/2/2022

OFFICE SPE:DORS/A BC:DORS/A

NAME PVossmar /RA/ JKozal /RA/

DATE 4/25/2022

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Numbers: 05000275 and 05000323

License Numbers: DPR-80 and DPR-82

Report Numbers: 05000275/2022001 and 05000323/2022001

Enterprise Identifier: I-2022-001-0013

Licensee: Pacific Gas and Electric Company

Facility: Diablo Canyon Power Plant, Units 1 and 2

Location: Avila Beach, CA

Inspection Dates: January 1, 2022, to March 31, 2022

Inspectors: A. Athar, Resident Inspector

N. Day, Acting Senior Resident Inspector

M. Doyle, Operations Engineer

J. Drake, Acting Senior Resident Inspector

N. Hernandez, Acting Senior Resident Inspector

Approved By: Jason W. Kozal, Chief

Projects Branch A

Division of Operating Reactor Safety

Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at Diablo Canyon Power Plant, Units 1

and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is

the NRCs program for overseeing the safe operation of commercial nuclear power reactors.

Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Promptly Correct a Condition Adverse to Quality which Resulted in an Inoperable

Auxiliary Saltwater Pump

Cornerstone Significance Cross-Cutting Report

Aspect Section

Mitigating Green [H.6] - Design 71152A

Systems NCV 05000275,05000323/2022001-02 Margins

Open/Closed

A self-revealed Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, was

identified when the licensee failed to promptly identify and correct a condition adverse to

quality. Specifically, excessive moisture and debris on the Unit 1 auxiliary saltwater pump 1-1

caused a ground on the motor that challenged the presumption of operability, and the system

was required to be declared inoperable and removed from service for troubleshooting and

corrective maintenance.

Failure to Follow Procedures Results in Inoperable Emergency Diesel Generator

Cornerstone Significance Cross-Cutting Report

Aspect Section

Mitigating Green [H.5] - Work 71153

Systems NCV 05000323/2022001-01 Management

Open/Closed

A self-revealed Green, non-cited violation of Technical Specification 5.4.1.a, was identified for

the licensees failure to implement adequate work instructions for post-maintenance testing of

the emergency diesel generator following tuning of the governor. Specifically, following

corrective maintenance for governor troubleshooting, the licensee utilized an informal work

instruction to perform tuning of the electric governor and failed to ensure that all testing

described in Procedure MP E-21.6, Diesel Generator Electrical Governor and Voltage

Regulator Adjustments, Revision 22, was identified and performed, to ensure that the

emergency diesel generator 2-3 would be able to perform its specified safety function.

Inadequate Alarm Response Procedure

Cornerstone Significance Cross-Cutting Report

Aspect Section

Initiating Events Green None (NPP) 71153

NCV 05000275,05000323/2022001-03

Open/Closed

The inspectors identified a Green, non-cited violation of Technical Specification 5.4.1.a, for

the licensee's failure to establish an adequate procedure for responding to the "FDWTR

HTRS LEVEL HI" alarm, as recommended by Section 5 of Regulatory Guide 1.33, Revision 2,

Appendix A, dated February 1978.

2

Specifically, step 2.3.6 of Annunciator Response Procedure AR PK10-16, FDWTR HTRS

LEVEL HI, Revision 8A, directed the control room crew to obtain management advice before

taking certain actions to mitigate a feedwater heater tube leak, which could result in undue

delay.

Additional Tracking Items

None.

3

PLANT STATUS

Unit 1 began the inspection period at rated thermal power. On February 23, 2022, Unit 1

reduced power to approximately 50 percent for planned condenser cleaning. Unit 1 returned to

rated thermal power on February 25, 2022. On March 6, 2022, Unit 1 entered end-of-fuel-cycle

coast-down in preparation for a planned refueling outage. On March 26, 2022, the unit was shut

down to enter planned Refueling Outage 23 and remained shut down for the remainder of the

inspection period.

Unit 2 operated at or near rated thermal power for the entire inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed activities described in IMC 2515,

Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of

IPs. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel to assess licensee performance and compliance with Commission rules

and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President

of the United States on the public health risks of the coronavirus (COVID-19), resident and

regional inspectors were directed to begin telework and to remotely access licensee information

using available technology. During this time, the resident inspectors performed periodic site

visits each week, increasing the amount of time on site as local COVID-19 conditions permitted.

As part of their onsite activities, resident inspectors conducted plant status activities as

described in IMC 2515, Appendix D; observed risk-significant activities; and completed on site

portions of IPs. In addition, resident and regional baseline inspections were evaluated to

determine if all or a portion of the objectives and requirements stated in the IP could be

performed remotely. If the inspections could be performed remotely, they were conducted per

the applicable IP. In some cases, portions of an IP were completed remotely and on site. The

inspections documented below met the objectives and requirements for completion of the IP.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

External Flooding Sample (IP Section 03.03) (1 Sample)

(1) The inspectors evaluated that flood protection barriers, mitigation plans, procedures,

and equipment are consistent with the licensees design requirements and risk

analysis assumptions for coping with external flooding on March 22, 2022.

4

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1) Unit 1 residual heat removal pump 1-2 on January 24, 2022

(2) Unit 1 emergency diesel generator 1-1 starting air system on February 25, 2022

(3) Unit 2 residual heat removal pump 2-1 on March 14, 2022

(4) Unit 1 reactor vessel refueling level indication system on March 28, 2022

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire areas:

(1) Fire on owner controlled area near 500 kV offsite line on February 2, 2022

(2) Unit 1 turbine building component cooling water heat exchanger room, 85-foot

elevation, on February 16, 2022

(3) Unit 2 turbine building component cooling water heat exchanger room, 85-foot

elevation, on March 15, 2022

(4) Unit 1 emergency diesel generator 1-1, 1-2, and 1-3 rooms, 85-foot elevation, on

March 16, 2022

(5) Unit 1 turbine building on the 119-foot elevation 4 kV rooms on March 27, 2022

Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the onsite fire brigade training and performance during an

unannounced fire drill on January 30, 2022.

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (1 Partial)

(1) (Partial)

The inspectors evaluated internal flooding mitigation protections in the Unit 2

emergency diesel generator 2-3 room on March 2, 2022. The inspectors completed

inspection procedure Sections 03.01.1 and 03.01.2.

71111.07A - Heat Exchanger/Sink Performance

Annual Review (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated readiness and performance of the Unit 1 component

cooling water heat exchangers 1-1 and 1-2 thermal performance testing on

March 1, 2022.

5

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

(1) The inspectors reviewed and evaluated the licensed operator examination failure

rates for the requalification annual operating exam administered on March 29, 2022.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

(1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control

room during the Unit 1 shutdown for Refueling Outage 1R23 on March 27, 2022.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated licensed operator annual exams on

February 9, 2022.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (1 Partial)

(1) (Partial)

The inspectors evaluated the effectiveness of maintenance to ensure the Unit 2

condensate system remained capable of performing its intended function. The

inspectors completed inspection procedure Sections 03.01.1, 03.01.2, and 03.01.4.

Quality Control (IP Section 03.02) (1 Sample)

The inspectors evaluated the effectiveness of maintenance and quality control activities to

ensure the following structure, system, or component remains capable of performing its

intended function:

(1) Emergency diesel generator lube oil storage on January 7, 2022

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed:

(1) Unit 1 emergency diesel generator 1-1 major maintenance outage window on

January 12, 2022

(2) Unit 2 concurrently exercising boration pathway valves on February 15, 2022

(3) Unit 1 condenser differential pressure emergent trend on February 15, 2022

(4) Unit 1 emergency diesel generator 1-2 major maintenance outage window on

February 24, 2022

6

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (4 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1) Unit 1 emergency diesel generator 1-2 lube oil heat exchanger leak on

January 25, 2022

(2) Emergency plan equipment discussed in Notification 51143190 and 51143191 on

February 9, 2022

(3) Operability of concurrent outage of containment fan cooler unit 1-4 and emergency

diesel generator 1-2 on February 18, 2022

(4) Unit 1 residual heat removal valve RHR-1-8072 following discovery of through wall

leak on leak-off line RHR-Line-2524 on March 31, 2022

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)

(1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) Installation of a sixth emergency diesel generator on February 17, 2022

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the following post-maintenance testing activities to verify system

operability and/or functionality:

(1) Unit 1 emergency diesel generator 1-1 major maintenance outage window on

January 14, 2022

(2) Unit 2 component cooling water pump 2-3 maintenance outage window on

January 18, 2022

(3) Unit 2 component cooling water heat exchanger 2-1 and auxiliary saltwater pump 2-1

maintenance outage window on January 31, 2022

(4) Unit 1 control room ventilation maintenance outage window on February 9, 2022

(5) Unit 1 emergency diesel generator 1-2 major maintenance outage window on

February 26, 2022

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Partial)

(1) (Partial)

The inspectors evaluated Refueling Outage 1R23 activities from March 26, 2022, to

March 31, 2022. The inspectors completed inspection procedure Sections 3.01.a

and 3.01.b..

7

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities to verify system operability

and/or functionality:

Surveillance Tests (other) (IP Section 03.01) (5 Samples)

(1) Unit 2 emergency diesel generator 2-2 routine surveillance test on January 20, 2022

(2) Observation of operator rounds on February 3, 2022

(3) Unit 1 safety bus G 4 kV under voltage testing per Work Order 64219827 on

February 22, 2022

(4) Unit 1, Work Order 64253229, I-7-P456. A pressurizer power-operated relief valve

calibration on February 28, 2022

(5) Unit 1, 4 kV, bus G non-safety injection auto-transfer test on March 27, 2022

Inservice Testing (IP Section 03.01) (1 Sample)

(1) Unit 1 containment spray pump 1-1 routine surveillance test on January 28, 2022

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01)

(1 Sample)

(1) The inspectors evaluated a tabletop emergency preparedness drill in the Emergency

Operation Facility on January 25, 2022.

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicator submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01) (2 Samples)

(1) Unit 1 (January 1, 2021, through December 31, 2021)

(2) Unit 2 (January 1, 2021, through December 31, 2021)

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02)

(2 Samples)

(1) Unit 1 (January 1, 2021, through December 31, 2021)

(2) Unit 2 (January 1, 2021, through December 31, 2021)

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2 Samples)

(1) Unit 1 (January 1, 2021, through December 31, 2021)

(2) Unit 2 (January 1, 2021, through December 31, 2021)

8

71152A - Annual Follow-up Problem Identification and Resolution

Annual Follow-up of Selected Issues (Section 03.03) (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program

related to the following issues:

(1) Unit 1 auxiliary saltwater pump 1-1 multiple ground alarms on March 10, 2022. The

inspector completed Section 3.0.3. This completes the sample that was partially

completed and documented in Integrated Inspection Report 05000275/2021004 and

05000323/2021004 (ADAMS Accession No. ML22024A495).

71153 - Follow Up of Events and Notices of Enforcement Discretion

Event Report (IP Section 03.02) (2 Samples)

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 05000323/2021-001-00, Diesel Engine Generator (DEG) Declared lnoperable

due to Low Frequency Condition Discovery during Routine Surveillance (ADAMS

Accession No. ML21263A062). The inspection conclusions associated with this LER

are documented in this report under Inspection Results Section 71153.

(2) LER 05000323/2021-002-00, Unit 2 Manual Reactor Trip Due to Increased Water

Level in Feedwater Heater (ADAMS Accession No. ML21348A112). The inspection

conclusions associated with this LER are documented under Inspection Results

Section 71153.

INSPECTION RESULTS

Failure to Promptly Correct a Condition Adverse to Quality which Resulted in an Inoperable

Auxiliary Saltwater Pump

Cornerstone Significance Cross-Cutting Report

Aspect Section

Mitigating Green [H.6] - Design 71152A

Systems NCV 05000275,05000323/2022001-02 Margins

Open/Closed

A self-revealed Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, was

identified when the licensee failed to promptly identify and correct a condition adverse to

quality. Specifically, excessive moisture and debris on the Unit 1 auxiliary saltwater pump 1-1

caused a ground on the motor that challenged the presumption of operability, and the system

was required to be declared inoperable and removed from service for troubleshooting and

corrective maintenance.

Description: The auxiliary salt water (ASW) system design includes two safety-related motor

driven pumps that draw water from the Pacific Ocean to provide safety-related cooling water

for heat removal. The pump motors are housed in an enclosed vault adjacent to the Pacific

Ocean that includes forced ventilation through a raised snorkel/intake riser. Through the

inherent design of the vault, the ventilation introduces salty air into the environment where the

motor is housed on top of the auxiliary saltwater pump.

During normal operations, Diablo Canyon Power Plant does not need to operate both

auxiliary saltwater pumps. In order to perform scheduled work and minimize runtime wear,

9

the auxiliary saltwater pumps are swapped between a standby and running pump as

appropriate (typically each week). While in the standby (non-running) state, forced air is still

provided into the room for appropriate environmental temperatures. To support readiness

and long-term reliability, large motors typically have nonsafety-related components. A typical

component that supports the readiness in moisture environments is a motor heater. The

inspectors note that, although the heater itself is not safety-related, the motor is. In the case

of standby operations (nonrunning no heat/drying for moisture removal), excessive moisture

builds up that challenges the motor, which is a safety-related component and can affect the

reliability and operability of the ASW system.

In September 2019, during routine maintenance, Diablo Canyon identified that the motor

heater for ASW pump 1-1 was degraded. In January 2020, the station established a monthly

monitoring plan to observe the temperature difference between the stator and the lower

bearing; ultimately this monitoring strategy was ineffective due to the relatively long time

between evaluations of these parameters. The heater continued to degrade and completely

failed July 1, 2021. The degradation of the motor heater allowed elevated levels of

contamination and moisture buildup on the Auxiliary Saltwater Pump 1-1 motor windings,

which went undetected by the monthly monitoring plan. Over time, the contamination and

moisture accumulated enough to cause a ground fault in the Auxiliary Saltwater Pump 1-1

motor.

On July 5, 2021, the scheduled train swap occurred, with a routine start of the ASW

pump 1-1. The pump started and ran; however, almost immediately, unexpected main

control room ground detection system annunciators alarmed, and the operators were required

to secure the running pump due to a detected ground. Operators declared the pump

inoperable, and troubleshooting commenced. Insulation performance testing revealed

excessive moisture and debris on the pump motor, which spectroscopy confirmed to be sea

salt debris. The pump motor was replaced with a spare motor and the licensee performed

post-service analysis on the motor that was removed from service. The licensees analysis

determined that if the motor was needed in an accident scenario, the motor ground would

have cleared due to self-heating and moisture removal; nonetheless, this issue rendered the

system inoperable and unavailable for 75 hours8.680556e-4 days <br />0.0208 hours <br />1.240079e-4 weeks <br />2.85375e-5 months <br />.

Corrective Actions: Diablo Canyon Power Plant replaced the motor with a spare auxiliary

saltwater pump motor and declared ASW pump 1-1 operable on July 8, 2021, performed a

root cause analysis, revised equipment reliability process procedures to drive management

review of risk, created plant computer monitoring points for auxiliary saltwater pump motor

heaters, and revised the conduct of engineering and technical evaluation procedures to add

specific guidance to improve adverse condition monitoring.

Corrective Action References: Notification 5114756

Performance Assessment:

Performance Deficiency: Diablo Canyon Power Plant Unit 1 failed to promptly identify and

correct moisture and debris build up on the Unit 1 ASW pump 1-1 motor internal windings

which is a condition adverse to quality. Failing to identify and correct a condition adverse to

quality is a performance deficiency that was within the licensees ability to foresee and

correct.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Equipment Performance attribute of the Mitigating

10

Systems cornerstone and adversely affected the cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. Specifically, the licensees failure to promptly identify and correct

moisture and debris build up on the Unit 1 ASW pump 1-1 motor internal windings caused 75

hours of unavailability of the ASW pump 1-1.

Significance: The inspectors assessed the significance of the finding using Inspection

Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for

Findings At-Power. Using Exhibit 2, Mitigating System Screening Questions, the finding

was screened as having very low safety significance (Green) because it was not a design

deficiency; did not represent a loss of system function; did not represent an actual loss of

function of at least a single train for longer than its technical specification allowed outage

time; and did not result in the loss of a high safety-significant nontechnical specification train.

Cross-Cutting Aspect: H.6 - Design Margins: The organization operates and maintains

equipment within design margins. Margins are carefully guarded and changed only through a

systematic and rigorous process. Special attention is placed on maintaining fission product

barriers, defense-in-depth, and safety related equipment. The inspectors noted that Diablo

Canyon found degraded current on the auxiliary saltwater pump motor heater in

September 2019. However, the licensee failed to replace the motor heater before it failed in

July 2021, even when presented with opportunities to replace it during a refuel outage.

During this time, the station justified not replacing the heater and failed to maintain plant

equipment with appropriate design margin.

Enforcement:

Violation: Title 10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, conditions

adverse to quality are promptly identified and corrected.

Contrary to the above, on July 5, 2021, Diablo Canyon Power Plant failed to promptly identify

and correct a condition adverse to quality. Specifically, the excessive moisture and debris on

the Unit 1 auxiliary saltwater pump 1-1, a condition adverse to quality, caused a ground on

the motor that challenged the presumption of operability and required the system to be

declared inoperable and removed from service for troubleshooting and corrective

maintenance.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

11

Failure to Follow Procedures Results in Inoperable Emergency Diesel Generator

Cornerstone Significance Cross-Cutting Report

Aspect Section

Mitigating Green [H.5] - Work 71153

Systems NCV 05000323/2022001-01 Management

Open/Closed

A self-revealed Green, non-cited violation of Technical Specification 5.4.1.a, Procedures,

was identified for the licensees failure to establish and implement adequate work instructions

for post-maintenance testing of the emergency diesel generator (EDG) following tuning of the

governor. Specifically, following corrective maintenance for governor troubleshooting, the

licensee utilized an informal work instruction to perform tuning of the electric governor and

failed to ensure that all testing described in Procedure MP E-21.6, Diesel Generator

Electrical Governor and Voltage Regulator Adjustments, Revision 22, was identified and

performed, to ensure that the EDG 2-3 would be able to perform its specified safety function.

Description: On June 28, 2021, EDG 2-3 was removed from service for governor tuning.

EDG 2-3 had been experiencing load and frequency oscillations during its last two

surveillances, and the licensee had determined that the governor control system had been

impacted by fuel rack resistance changes from previous fuel system maintenance. The

personnel scheduled to perform the governor tuning had not previously performed this work.

However, only an informal work instruction was prepared to provide guidance for the tuning

and post-maintenance testing. Due to the complex nature of the governor tuning work scope,

the work order instructions were left vague with detailed actions contained in an informal

guidance document. The maintenance work order instructions were to adjust the governor

controls "per Engineering direction."

Since the document providing direction was an informal work plan, it was not required to be

place kept, and place keeping was not performed. Governor tuning maintenance was

completed on June 29, 2021; however, a fuel oil leak developed and testing was delayed until

the next shift. The maintenance verification testing was scoped, but due to insufficient detail

and lack of place keeping, the as-left isochronous (ISOC) frequency set-point on the governor

was not verified. EDG 2-3 was declared operable and placed in standby.

On July 21, 2021, EDG 2-3 was started on a simulated undervoltage signal for routine

monthly surveillance testing per Procedure STP M-9A3. The EDG was started with the mode

select switch in the "AUTO" position which indicated the diesel was aligned for dedicated

supply to its associated 4 kV vital electrical bus. Upon starting, the as-read steady-state

frequency was 58.9 Hz which was outside of the required technical specification acceptance

criteria of 59.2 Hz to 60.8 Hz. This resulted in a failed surveillance and the EDG being

declared inoperable since June 28, 2021. Engineering determined that the governor as-left

ISOC frequency set-point was the problem. The EDG 2-3 ISOC frequency set-point was

restored within limits per Procedure MP E-21.6. The EDG 2-3 passed all post-maintenance

testing requirements and was declared operable on July 22, 2021, at 10:55 p.m.

Corrective Actions: The licensee restored the correct governor settings, issued licensee

event report (LER) 05000323/2021-001-00, "Emergency Diesel Generator Declared

Inoperable due to Low Frequency Condition Discovery during Routine Surveillance," (ADAMS

Accession No. ML21263A062), updated Maintenance Procedure MP E-21.6 to include a note

about partial procedure use and impacts on ISOC frequency to ensure sufficient maintenance

verification testing, and initiated action to provide EDG governor control system training for

select system material experts.

12

Corrective Action References: Notification 51113496

Performance Assessment:

Performance Deficiency: The inspectors determined that the licensees failure to provide

adequate work instructions and follow procedures related to tuning and testing the EDG 2-3

governor was a performance deficiency that was reasonably within the licensees ability to

foresee and should have been prevented. Specifically, use of an informal work instruction to

perform complex corrective maintenance on the governor resulted in EDG 2-3 being

inoperable for greater than the technical specification allowed outage time.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Equipment Performance attribute of the Mitigating

Systems cornerstone and adversely affected the cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. Specifically, the failure to provide adequate guidance for work on

the tuning and post maintenance testing of the governor resulted in EDG 2-3 being

inoperable for 25 days.

Significance: The inspectors assessed the significance of the finding using Inspection

Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for

Findings At-Power. Using Exhibit 2, Mitigating System Screening Questions, the finding

was screened as having very low safety significance (Green) because it was not a design

deficiency; did not represent a loss of system and/or train function; did not represent an

actual loss of function of at least a single train for longer than its technical specification

allowed outage time; and did not result in the loss of a high safety-significant nontechnical

specification train. EDG 2-3 maintained its ability to perform its safety function.

Cross-Cutting Aspect: H.5 - Work Management: The organization implements a process of

planning, controlling, and executing work activities such that nuclear safety is the overriding

priority. The work process includes the identification and management of risk commensurate

to the work and the need for coordination with different groups or job activities. Specifically,

the licensee used an informal work instruction rather than developing a formalized

procedure/guidance for the operators to complete the complex task of tuning and testing the

EDG 2-3 governor.

Enforcement:

Violation: Technical Specification Section 5.4.1.a states, in part, that written procedures

shall be established, implemented, and maintained covering the applicable procedures

recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. NRC

Regulatory Guide 1.33, Appendix A, Section 9.a, recommends that maintenance that can

affect the performance of safety-related equipment should be properly preplanned and

performed in accordance with written procedures, documented instructions, or drawings

appropriate to the circumstances.

Contrary to the above, on June 28, 2021, the licensee failed to ensure that maintenance that

could affect the performance of safety-related equipment was properly preplanned and

performed in accordance with written procedures, documented instructions, or drawings

appropriate to the circumstances. Specifically, the licensee utilized an informal work

instruction to perform the complex task of tuning and testing the electric governor for EDG 2-3

and failed to complete all required post-maintenance testing required to demonstrate that

13

structures, systems, and components will perform satisfactorily in service. As a result,

EDG 2-3 was inoperable for approximately 25 days.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

Inadequate Alarm Response Procedure

Cornerstone Significance Cross-Cutting Report

Aspect Section

Initiating Events Green None (NPP) 71153

NCV 05000275,05000323/2022001-03

Open/Closed

The inspectors identified a Green, non-cited violation of Technical Specification 5.4.1.a, for

the licensee's failure to establish an adequate procedure for responding to the "FDWTR

HTRS LEVEL HI" alarm, as recommended by Section 5 of Regulatory Guide 1.33,

Revision 2, Appendix A, dated February 1978. Specifically, step 2.3.6 of Annunciator

Response Procedure AR PK10-16, FDWTR HTRS LEVEL HI, Revision 8A, directed the

control room crew to obtain management advice before taking certain actions to mitigate a

feedwater heater tube leak, which could result in undue delay.

Description: On October 15, 2021, at 8:49 a.m., the Unit 2 feedwater heaters high level

(FDWTR HTRS LEVEL HI) annunciator alarmed in the control room. Based on multiple

diverse indications, station personnel verified excessive condensate water on the shell side of

feedwater heater 2-5B.

The station entered Annunciator Response Procedure AR PK10-16, FDWTR HTRS LEVEL

HI, Revision 8A, upon receiving the alarm in the control room. Step 2.2.3 of Procedure AR

PK 10-16 outlines a methodology to determine whether the high level condition is the result of

a level control system malfunction or a feedwater heater tube leak. By 12:26 p.m. that day,

operations personnel had completed this step and had determined that there was no

malfunction of the level control system, indicating the presence of a tube leak in the

feedwater heater 2-5B. At 12:33 p.m., the instrumentation and controls maintenance

supervisor had concurred that there was no malfunction of the level control system. Thus,

the station had strong evidence at 12:33 p.m. that there was a tube leak in feedwater

heater 2-5B.

Step 2.3.6 of Procedure AR PK 10-16 provides instructions in the event that a tube leak has

been diagnosed. This step directs the station to perform either or both of the following, as

deemed advisable by plant management after an assessment of event severity:

Conduct an orderly plant shutdown

Dispatch an operator to isolate the affected feedwater heater

This step was entered at 12:33 p.m., and a plant management meeting occurred at 3:00 p.m.

to discuss the options listed. The station ultimately decided to dispatch an operator to isolate

feedwater heater 2-5B, which first required a downpower to 90 percent due to thermodynamic

considerations of taking a feedwater heater out of service. The inspectors noted that the

downpower began at 4:09 p.m.almost 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> after the tube leak was initially diagnosed.

The downpower was completed at 5:12 p.m., and an operator was then dispatched to isolate

feedwater heater 2-5B.

14

While the operator was attempting the close the condensate outlet isolation valve, the level in

the sight glass for feedwater heater 2-5B continued to rise, until it was off-scale (out of sight)

high. As required by procedure, the control room crew manually tripped the Unit 2 reactor

due to the feedwater heater 2-5B being off-scale high. Immediately following the trip, the

crew closed the main steam isolation valves (MSIVs) per Procedure AR PK 10-16. This

action also isolated the main feedwater pumps, which are steam-driven.

The inspectors noted that step 2.3.6 of Procedure AR PK 10-16 directs the station to obtain

management advice before taking action to mitigate the feedwater heater tube leak. On

October 15, the station gathered a senior management meeting to complete this step, before

taking action to mitigate the feedwater heater tube leak. After the downpower was completed

and an operator was dispatched to isolate the affected feedwater heater, the operator was

unable to complete the isolation of feedwater heater 2-5B before the feedwater heater level

went off-scale (out of sight) high and the control room crew had to manually trip the reactor.

During the inspection, the licensee provided additional information including timelines

describing activities occurring in parallel with plant management meeting preparations,

evidence that a plant trip was unavoidable due to the extensive FWH damage in this case,

and operating experience suggesting this event progressed significantly more rapidly than

past events. Upon review of this information, the inspectors concluded that there was not

sufficient basis to conclude the performance deficiency caused the October 15 plant trip and

loss of the condenser and feedwater pumps. However, the inspectors concluded that

Procedure AR PK 10-16 was inadequate because step 2.3.6 directed control room operators

to gain management input before taking action to mitigate the feedwater heater tube leak,

which could take the decision-making out of the control room and incur an undue delay.

Corrective Actions: The licensee removed the statement "as deemed advisable by plant

management," from step 2.3.6 of Procedure AR PK 10-16, and instead directed the control

room operators to take action to mitigate a feedwater heater tube leak as directed by the shift

manager.

Corrective Action References: Notifications 51148759 and 51145638

Performance Assessment:

Performance Deficiency: The failure to establish an adequate procedure for responding to

the "FDWTR HTRS LEVEL HI" alarm in accordance with the requirements of plant technical

specifications was a performance deficiency that was within the licensee's ability to foresee

and correct.

Screening: The inspectors determined the performance deficiency was more than minor

because if left uncorrected, it would have the potential to lead to a more significant safety

concern. Specifically, the undue delay caused by convening a management meeting may

lead to a more significant safety concern while implementing this procedure.

Significance: The inspectors assessed the significance of the finding using Inspection

Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for

Findings At-Power. Using Exhibit 1, Initiating Events Screening Questions, the finding was

screened as having very low safety significance (Green) because it did not cause a reactor

trip.

15

Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to

this finding because the inspectors determined the finding did not reflect present licensee

performance. Specifically, the latest revision of Annunciator Response Procedure AR PK10-

16, FDWTR HTRS LEVEL HI, Revision 8A, was issued on October 12, 2016, which was

outside the 3-year window normally considered to be present performance.

Enforcement:

Violation: Technical Specification 5.4.1.a requires, in part, that written procedures shall be

established, implemented, and maintained covering the applicable procedures recommended

in Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Regulatory

Guide 1.33, Revision 2, Appendix A, Section 5, identifies procedures pertaining to alarm

conditions as recommended procedures.

Contrary to the above, prior to October 15, 2021, the licensee failed to establish adequate

written procedures to respond to the FDWTR HTRS LEVEL HI alarm. Specifically,

Annunciator Response Procedure AR PK10-16, FDWTR HTRS LEVEL HI, Revision 8A,

Step 2.3.6, directed control room operators to gain management input before taking action to

mitigate a feedwater heater tube leak, which could take the decision-making out of the control

room and incur an undue delay.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On April 7, 2022, the inspectors presented the integrated inspection results to

Ms. P. Gerfen, Senior Vice President, Generation and Chief Nuclear Officer, and other

members of the licensee staff.

16

DOCUMENTS REVIEWED Chief Nuclear Officer

Inspection Type Designation Description or Title Revision or

Procedure Date

71111.01 Procedures CP M-16 Severe Weather 20

71111.04 Corrective Action Notifications 51141818, 51141819, 51141871, 51141890

Documents

71111.04 Procedures OP A-2:X RVRLIS Alignments for Refueling Outages 10

71111.04 Procedures OP B-2:I RHR System Alignment Verification for Plant Startup 26

71111.05 Corrective Action Notifications 51142578

Documents

71111.05 Corrective Action Notifications 51071040, 51094718, 51132042

Documents

71111.05 Drawings 111805-49 Fire Preplan Turbine Building Elevation 85' 3

71111.05 Drawings 11805-54 Fire Preplan Turbine Building Elevation 119' 3

71111.05 Miscellaneous Generic Safety

Plan GPAAHHR

and GPAASITE

71111.05 Procedures Generic Hot Work Fire Lesson Plan 4

71111.07A Corrective Action Notifications 51144881, 51144943, 51144976

Documents

71111.07A Procedures PEP M-234 CCW Heat Exchanger Performance Test 21

71111.07A Work Orders WO 64187929, 64187939

71111.11A Miscellaneous ARQ results ARQ Results 03/28/2022

71111.11Q Procedures E-0 Reactor Trip or Safety Injection 45D

71111.11Q Procedures E-0.1 Reactor Trip Response 43

71111.11Q Procedures OP L-4 Normal Operation at Power 103

71111.12 Miscellaneous PG&E Letter No. Diablo Canyon Units 1 and 2 License Amendment Request 02/14/1992

DCL 92-036, 92-03, Revision of Technical Specifications 3/4.8.1 and

Docket No. 50- 3/4.8.2 Increase Emergency Diesel Generator Fuel Oil

275, OL-DPR-80, Storage Requirements

Docket No. 50-

323, OL-DPR-82

71111.12 Miscellaneous PG&E Letter No. Diablo Canyon Units 1 and 2 Response to NRC Questions 06/05/1992

DCL 92-131 on License Amendment Request 92-03, Revision of

Docket No. 50- Technical Specifications 3/4.8.1 and 3/4.8.2 Increase

17

Inspection Type Designation Description or Title Revision or

Procedure Date

275, OL-DPR-80, Emergency Diesel Generator Fuel Oil Storage Requirements

Docket No. 50-

323, OL-DPR-82

71111.12 Miscellaneous SISI Manual Seismically Induced Systems Interaction Manual 13

71111.12 Miscellaneous STP M-9G Diesel Generator 24 Hour Load Test and Hot Restart Test 04/22/2017

Completed

Surveillance

Results

71111.12 Miscellaneous STP M-9G Diesel Generator 24 Hour Load Test and Hot Restart Test 04/19/2019

Completed

Surveillance

Results

71111.12 Miscellaneous STP M-9G Diesel Generator 24 Hour Load Test and Hot Restart Test 05/14/2021

Completed for 4-22-2017, 4-19-2019, 5-14-21

Surveillance

Results

71111.12 Procedures Behavior Of Loose Equipment In A Seismic Event 06/1985

71111.12 Procedures STP M-9G Diesel Generator 24 Hour Load Test and Hot Restart Test 59

71111.13 Corrective Action Notifications 51139208, 51140737, 51140750, 51140937, 51140954,

Documents 51141885

71111.13 Miscellaneous Unit 1 Condenser Station Prediction of Condenser DP 02/15/2022

DP Trends

71111.13 Procedures AD7.ID14 Assessment of Integrated Risk 29

71111.13 Procedures OM7.ID7 Emerging Issue and Event Investigations

71111.13 Procedures OP O-36 Protected Equipment Postings 27

71111.13 Procedures OP1.DC10 Conduct of Operations 65

71111.13 Procedures OP1.ID3 Reactivity Management Program 18

71111.13 Procedures STP V-3E1 Exercising Valve FCV-110A Boric Acid to Blender 22

71111.13 Procedures STP V-3E2 Exercising Valve FCV-110B Blender to Charging Header 10

71111.15 Corrective Action Notifications 50985660, 51123152, 51131514, 51135585, 51147276

Documents

71111.15 Drawings 102010-3 Residual Heat Removal System 52

71111.15 Drawings 102028-20 ASME Code Boundary 53

71111.15 Drawings 224757-1 Residual Heat Removal System Suction Loop 4 V-8702 3

18

Inspection Type Designation Description or Title Revision or

Procedure Date

Leak-off & Thermal Expansion

71111.15 Miscellaneous 9000039632 Emergency Diesel Generator Fuel Oil Storage 0

71111.15 Procedures EP MT-21 Emergency Kits 19

71111.15 Procedures MP M-21-HX.2 Diesel Generator Lube Oil Heat Exchanger Maintenance 8

71111.18 Calculations Calc M-786 Determine Required Diesel Fuel Oil Storage to Meet DCPP 6

Licensing Basis of Operating "Minimum ESF Loads"

71111.18 Calculations Calc M-786 Determine Required Diesel Fuel Oil Storage to Meet DCPP 8

Licensing Basis of Operating "Minimum ESF Loads"

71111.18 Engineering DCN DC2-EM- Install sixth Diesel Engine Generator 1

Changes 44405

71111.18 Engineering DCN DC2-EM- Diesel Engine Generator 2-3 0

Changes 46476

71111.18 Engineering DCP M-44405 Install sixth Diesel Engine Generator 3

Changes

71111.19 Corrective Action Notifications 51140355, 51140689, 51140691, 51140700, 51140702,

Documents 51140708, 51140711, 51140724, 51140732, 51140733,

51140734, 51140735, 51140736, 51140738, 51140739,

51140780, 51140784, 51140793, 51140818, 51140856,

51140857, 51140870, 51140882, 51140883, 51141044,

51141058, 51141062, 51141078, 51141379, 51142497,

51142521, 51142533

71111.19 Work Orders WO 60130870, 64131387, 64131388, 64132042, 64132052,

64174747, 64213744, 64222825, 64238407

71111.20 Procedures OP B-1A CVCS Borate the RCS to Refuel 3

71111.20 Procedures OP B-9:I Primary Sampling - Make System Available 13

71111.20 Procedures OP L-5 Plant Cooldown from Minimum Load to Cold Shutdown 110

71111.20 Procedures OP L-6 Cold Shutdown Refueling 88

71111.22 Corrective Action Notifications 51141538, 51142224, 51147252, 51147253, 51147446

Documents

71111.22 Miscellaneous U1 Auxiliary Building Round for February 03, 2022, and U2

Turbine Building Rounds for February 04, 2022

71111.22 Procedures STP M-13G 4 kV Bus G Non-SI Auto-Transfer Test 61

71111.22 Procedures STP M-16A Slave Relay Test of Trains A and B K603 (Safety Injection)30

71111.22 Procedures STP M-9A2 Diesel Engine Generator 2-2 Routine Surveillance Test 13

19

Inspection Type Designation Description or Title Revision or

Procedure Date

71111.22 Procedures STP P-CSP-11 Routine Surveillance Test of Containment Spray Pump 1-1 21A

71111.22 Procedures STP V-3I3A Full Stroke Exercise of Containment Spray Valve CS-9001A 8

71111.22 Work Orders WO 64172567, 64218102, 64252011, 64252019, 64253229,

64261233

71114.06 Corrective Action Notifications 51141937

Documents

71151 Corrective Action Notifications 51142375

Documents

71152A Corrective Action Notification and 5114756

Documents Causal

Evaluation

71153 Corrective Action Notifications 51088141, 51115230, 51117574, 51126031, 51126111,

Documents 51133450, 51133724

71153 Procedures AD13.ID4 Post Maintenance Testing 37

71153 Procedures AR PK 10-16 FDWTR HTRS LEVEL HI Annunciator Response Procedure 8A

71153 Procedures MP M-21.8 Diesel Engine Governor Actuator Maintenance 26

71153 Procedures MP_E-21.6 Diesel Generator Electrical Governor and Voltage Regulator 22

Adjustments

71153 Procedures MP_E-21.GOV Emergency Diesel Generator Electrical Governor 4

Maintenance

71153 Procedures OP C-7:IV Condensate System - Feedwater Heaters Remove from 11

Service

71153 Work Orders 60131137, 60136440, 60136888, 60138461, 60138932

20