IR 05000424/2016002

From kanterella
Revision as of 05:17, 30 June 2018 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
Jump to navigation Jump to search
Vogtle Electric Generating Plant - NRC Integrated Inspection Report 05000424/2016002 and 05000425/2016002
ML16215A106
Person / Time
Site: Vogtle  Southern Nuclear icon.png
Issue date: 07/29/2016
From: Shane Sandal
NRC/RGN-II/DRP/RPB2
To: Taber K
Southern Nuclear Operating Co
References
IR 2016002
Download: ML16215A106 (24)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION REGION II 245 PEACHTREE CENTER AVENUE NE, SUITE 1200 ATLANTA, GEORGIA 30303-1257 July 29, 2016 Mr. Keith Taber Vice President

Southern Nuclear Operating Company, Inc.

Vogtle Electric Generating Plant

7821 River Road Waynesboro, GA 30830

SUBJECT: VOGTLE ELECTRIC GENERATING PLANT - NRC INTEGRATED INSPECTION REPORT 05000424/2016002 AND 05000425/2016002

Dear Mr. Taber:

On June 30, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your Vogtle Electric Generating Plant, Units 1 and 2. On July 14, 2016, the NRC inspectors discussed the results of this inspection with Mr. Darin Myers and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.

NRC inspectors documented one finding of very low safety significance (Green) in this report which involved a violation of NRC requirements. The NRC is treating this violation as a noncited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy. If you contest the violation or significance of this NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, U.S.

Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident inspector

at Vogtle.

If you disagree with the cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region II; and the NRC resident inspector at

Vogtle. In accordance with Title 10 of the Code of Federal Regulations 2.390, "Public Inspections, Exemptions, Requests for Withholding," of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC's Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Managem ent System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/ Shane Sandal, Chief Reactor Projects Branch 2 Division of Reactor Projects

Docket Nos.: 50-424, 50-425 License Nos.: NPF-68 and NPF-81

Enclosures:

IR 05000424/2016002; 05000425/2016002

w/Attachment:

Supplemental Information

cc: Distribution via ListServ

____ ML16215A106__________ SUNSI REVIEW COMPLETE FORM 665 ATTACHED OFFICE RII:DRP RII:DRP RII:DRP RII: DRP SIGNATURE VIA E-MAIL-TAS1 VIA E-MAIL VIA E-MAIL NAME T. Stephen A. Alen-AXA1 W. Deschaine-WXD1S. Sandal-SRS5 DATE 7/ /2016 7/ /2016 7/ /2016 7/ /2016 8/ /2016 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO Letter to B. Keith Taber from Shane Sandal dated July 29, 2016

SUBJECT: VOGTLE ELECTRIC GENERATING PLANT - NRC INTEGRATED INSPECTION REPORT 05000424/2016002 AND 05000425/2016002

Distribution w/encl: D. Gamberoni, RII

L. Gibson, RII OE Mail RIDSNRRDIRS

PUBLIC RidsNrrPMVogtle Resource Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION II

Docket Nos.: 50-424, 50-425

License Nos.: NPF-68, NFP-81

Report No.: 05000424/2016002; and 05000425/2016002

Licensee: Southern Nuclear Operating Company, Inc.

Facility: Vogtle Electric Generating Plant, Units 1 and 2

Location: Waynesboro, GA 30830

Dates: April 1, 2016 through June 30, 2016

Inspectors: T. Stephen, Senior Resident Inspector (Acting) W. Deschaine, Senior Resident Inspector (Acting)

A. Alen, Resident Inspector Approved by: Shane Sandal, Chief Reactor Projects Branch 2 Division of Reactor Projects

SUMMARY OF FINDINGS

IR 05000424/2016002; and 05000425/2016002, April 1, 2016, through June 30, 2016; Vogtle

Electric Generating Plant, Units 1 and 2, Follow-up of Events and Notices of Enforcement Discretion

The report covered a 3-month period of inspection by resident inspectors. One self-revealing non-cited violation was identified. The significance of inspection findings are indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP) dated April 29, 2015. The cross-cutting aspects are determined using IMC 0310, "Aspects within the Cross-Cutting Areas" dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRC's Enforcement Policy dated February 4, 2015. The NRC's program for overseeing the safe operations of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 5. Documents reviewed by the inspectors which are not identified in the Report Details are identified in the List of Documents Reviewed section of the Attachment.

Cornerstone: Initiating Events

  • (Green) A self-revealing non-cited violation (NCV) of Technical Specifications (TS) 5.4.1.a, Procedures, was identified for the licensee's failure to properly implement procedure 24750-2, "Steam Generator Level (Narrow Range) Protection Channel II 2L-519 Channel Operational Test and Channel Calibration." During testing of Unit 2 loop 1 steam generator (S/G) narrow range channel 2L-519 the channel was not removed from scan resulting in a reactor trip. The licensee's immediate corrective actions were to remove the technicians performing the calibration from maintenance duties for formal remediation. The licensee documented this condition in CR 10230073.

The performance deficiency (PD) was more than minor because it adversely affected the Initiating Events cornerstone objective in that the failure to properly remove channel 2L-519 from scan resulted in a reactor trip. The finding was determined to be Green because the PD did not result in a loss of mitigation equipment used to transition the reactor to a stable shutdown condition. The finding was assigned a cross cutting aspect of Avoid Complacency because maintenance technicians failed to implement appropriate error reduction tools to verify that the correct channel was removed from scan for testing. (H.12) (4OA3)

REPORT DETAILS

Summary of Plant Status

Unit 1 operated at or near full rated thermal power (RTP) for the entire inspection period.

Unit 2 began the report period at full RTP. The unit experienced an unplanned automatic trip on May 25, 2016 due to a low loop 1 steam generator water level (SGWL) condition. The unit returned full power on May 27, 2016, and operated at or near full RTP for the remainder of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

a. Inspection Scope

Summer Readiness of Offsite and Alternate AC Power System: The inspectors reviewed the licensee's procedures for operation and continued availability of offsite and onsite alternate AC power systems. The inspectors also reviewed the communications protocols between the transmission system operator and the licensee to verify that the appropriate information is exchanged when issues arise that could affect the offsite power system.

The inspectors reviewed the material condition of offsite and onsite alternate AC power

systems (including switchyard and transformers) by performing a walkdown of the switchyard. The inspectors reviewed outstanding work orders and assessed corrective actions for degraded conditions that impacted plant risk or required compensatory actions.

b. Findings

No findings were identified.

1R04 Equipment Alignment

a. Inspection Scope

Partial Walkdown: The inspectors verified that critical portions of the following systems were correctly aligned by performing partial walkdowns. The inspectors determined the correct system lineup by reviewing plant procedures and drawings listed in the

.

  • Unit 2, chemical volume control system (CVCS) centrifugal charging pump (CCP) 'A' train standby readiness alignment following restoration from planned maintenance
  • Unit 1, essential chiller water system 'B' train while the 'A' train was out of service (OOS) for planned maintenance
  • Diesel driven fire pumps following planned maintenance outage Complete Walkdown: The inspectors verified the alignment of the Unit 2 residual heat removal (RHR) system by reviewing plant procedures, drawings, the updated final safety analysis report, and other documents. The inspectors also reviewed records related to the system outstanding design issues, maintenance work requests, and deficiencies.

The inspectors reviewed corrective action documents, including condition reports and outstanding work orders, to verify the licensee was identifying and resolving equipment alignment discrepancies. The inspectors also reviewed periodic reports containing information on the status of risk-significant systems, including maintenance rule reports and system health reports.

b. Findings

No findings were identified.

1R05 Fire Protection

a. Inspection Scope

Quarterly Inspection: The inspectors evaluated the adequacy of fire plans by comparing the fire plans to the defined hazards and defense-in-depth features specified in the fire protection program the following fire areas.

  • Unit 1, control building level A east and west penetration rooms, fire zones 89, 90, 159, 87, 88, 93, 102, and 158
  • Unit 2, component cooling water (CCW) pump rooms, fire zones 36 and 37
  • Main control room and technical support center, including battery room, fire zones 105, 106, 183A, 601, 602, 603, 604, and 605
  • Spent fuel pool floor, fire zone 139 The inspectors assessed the following:
  • control of transient combustibles and ignition sources
  • fire detection systems
  • water-based fire suppression systems
  • gaseous fire suppression systems
  • manual firefighting equipment and capability
  • passive fire protection features
  • compensatory measures and fire watches
  • issues related to fire protection contained in the licensee's corrective action program
  • material condition and operational status of fire protection equipment

Fire Drill Observation: The inspectors observed the licensee's fire brigade performance during a fire drill on April 25, 2016 and assessed the brigade's capability to meet fire protection licensing basis requirements. The inspectors observed the following aspects of fire brigade performance:

  • capability of fire brigade members
  • leadership ability of the brigade leader
  • proper use of turnout gear and fire-fighting equipment
  • team effectiveness
  • compliance with site procedures The inspectors also assessed the ability of control room operators to combat potential fires including identifying the location of the fire, dispatching the fire brigade, and

sounding alarms.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

(71111.11)

a. Inspection Scope

Resident Inspector Quarterly Review of Licensed Operator Requalification:

The inspectors observed training simulator scenario, V-RQ-SE-14203, administered to a licensed operating crew, on May 4, 2016, in accordance with the licensee's accredited requalification training program. The inspectors assessed the following attributes:

  • licensed operator performance
  • the ability of the licensee to administer the scenario and evaluate the operators
  • the quality of the post-scenario critique
  • simulator performance Resident Inspector Quarterly Review of Licensed Operator Performance: The inspectors observed licensed operator performance in the main control room during the May 26, 2016 restart of Unit 2 following an unplanned reactor trip. The inspectors assessed the

following:

  • use of plant procedures
  • control board manipulations
  • communications between crew members
  • use and interpretation of instruments, indications, and alarms
  • use of human error prevention techniques
  • documentation of activities
  • management and supervision

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

Regular Maintenance Effectiveness: The inspectors assessed the licensee's change from a biennial assessment to an ongoing assessment of their maintenance rule program. The maintenance rule program assessment is required by 10 CFR 50.65(a)(3). The inspectors reviewed the licensee's implementation of the change and their assessment tools. The inspectors reviewed the licensee's assessment of several systems covered by the maintenance rule. The inspectors interviewed the maintenance rule coordinator to review the programs adherence to the guidance in NUMARC 93-01 "Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants", Rev. 4A for an ongoing assessment.

Quality Control Maintenance Effectiveness: The inspectors reviewed the licensee's control of quality in accordance with their Quality Assurance Program during work on several maintenance rule scoped components. The following work packages were reviewed for proper quality controls:

  • SNC 539529, S/G 1 main feedwater regulating valve air operated valve rebuild
  • SNC 539528, S/G 1 main feedwater regulating valve air operated valve maintenance
  • SNC 539516, S S/G 1 main feedwater regulating valve repacking
  • SNC 795249, Foreign material retrieval for the Unit 2 6A feedwater heater
  • SNC 777525, Unit 2 loop 1 atmospheric relief valve actuator repair

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the maintenance activities listed below to verify that the licensee assessed and managed plant risk as required by 10 CFR 50.65(a)(4) and licensee procedures. The inspectors assessed the adequacy of the licensee's risk assessments and implementation of risk management actions. The inspectors also verified that the licensee was identifying and resolving problems with assessing and managing maintenance-related risk using the corrective action program. Additionally, for maintenance resulting from unforeseen situations, the inspectors assessed the effectiveness of the licensee's planning and control of emergent work activities.

  • Unit 1, May 2, 2016, 'GREEN' equipment out of service (EOOS) risk profile following the failure of station air compressor no. 1 in conjunction with degraded conditions on air compressors no. 2 and no. 4
  • Unit 2, week of May 2, 2016, 'GREEN' EOOS risk profile due to nuclear service cooling water (NSCW) pump no. 1 being out of service (OOS) for planned maintenance along with service testing of 'A' and 'C' trains battery charges
  • Unit 2, May 17, 2016, 'GREEN' EOOS risk profile due to 'B' train NSCW pump no. 2 and 'B' train emergency safety features (ESF) chiller OOS
  • Unit 2, May 27, 2016, 'GREEN' EOOS risk profile due to unplanned maintenance on the 6A feedwater heater

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

The inspectors selected the operability determinations or functionality evaluations listed below for review based on the risk-significance of the associated components and systems. The inspectors reviewed the technical adequacy of the determinations to ensure that technical specification operability was properly justified and the components or systems remained capable of performing their design functions. To verify whether components or systems were operable, the inspectors compared the operability and design criteria in the appropriate sections of the technical specification and updated final safety analysis report to the licensee's evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with operability evaluations.

  • Functionality assessment (FA) for a non-functional engine block heater on the diesel fire pump no. 1, condition report (CR) 10229293 (FA #1-15-001)
  • Unit 1, immediate determination of operability (IDO) for missing hold down bolts on the ventilation cooling air supply ducts access covers of the 'A' train EDG building, CR10206003
  • Unit 2, 'A' train EDG control power 'A' failure, CR10229803
  • Unit 2, IDO for blocking open temperature control valve, 2TV-11675, which controls NSCW flow to the chiller condenser of the 'B' train essential chilled water system, CR10224020
  • Unit 2, IDO for low flow conditions in the 'B' train of the NSCW, CR10227263
  • Unit 2, prompt determination of operability (PDO) for oil content increase in the jacket water subsystem of the 'B' train EDG, CR10207224 (PDO #2-16-002)

b. Findings

No findings were identified.

1R18 Plant Modifications

a. Inspection Scope

The inspectors reviewed licensing document change request (LDCR), i.e. Plant modification, No. 2013017, "VEGP TR 13.13.1 Functionality Temperature Guidance,"

version 1.0, which changed the technical support center heating, ventilating, and air conditioning (HVAC) cooling function requirements. The inspectors assessed the

following:

  • verified that the modifications did not affect the safety functions of important safety systems
  • confirmed the modifications did not degrade the design bases, licensing bases, and performance capability of risk significant structures, systems and components
  • evaluated whether system operability and availability, configuration control, post-installation test activities, and changes to documents, such as drawings, procedures, and operator training materials, complied with licensee standards and NRC

requirements

  • reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with modifications

b. Findings

No additional findings were identified. Findings and associated enforcement aspects of this plant modification review were documented in inspection report 05000424, 425/2016502 (Section 1EP4).

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors either observed post-maintenance testing or reviewed the test results for the maintenance activities listed below to verify the work performed was completed correctly and the test activities were adequate to verify system operability and functional capability.

  • SNC539528, S/G 1 main feedwater regulating valve air operated valve maintenance, March 13, 2016
  • SNC777525, Unit 2 loop 1 atmospheric relief valve Actuator repair, April 3, 2016
  • SNC779920, 1N41 power range instrument J352 connector repair, April 5, 2016
  • SNC 480312, Nitrogen charging and air pump regulator adjustment of main feed isolation valve, 1HV-5228, May 6, 2016
  • SNC 541720, 36-Month NSCW-ESF water chiller flow channel, 2F-1803, May 17, 2016 The inspectors evaluated these activities for the following:
  • Acceptance criteria were clear and demonstrated operational readiness
  • Effects of testing on the plant were adequately addressed
  • Test instrumentation was appropriate
  • Tests were performed in accordance with approved procedures
  • Equipment was returned to its operational status following testing
  • Test documentation was properly evaluated Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with post-maintenance testing.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the surveillance tests listed below. The surveillance test was either observed directly or test results were reviewed to verify testing activities and results provide objective evidence that the affected equipment remain capable of performing their intended safety functions and maintain their operational readiness consistent with the facility's current licensing basis. The inspectors evaluated the test activities to assess for:

  • preconditioning of equipment,
  • appropriate acceptance criteria,
  • calibration and appropriateness of measuring and test equipment,
  • procedure adherence, and
  • equipment alignment following completion of the surveillance Additionally, the inspectors reviewed a sample of significant surveillance testing problems documented in the licensee's corrective action program to verify the licensee was identifying and correcting any testing problems associated with surveillance testing.

Routine Surveillance Tests

  • 14951-C, Fire Suppression System Operability Tests (Section 1.3 - Diesel Fire Pump #2 C-2301-P4-003) Monthly Test, version 32
  • 14721C-2, ECCS subsystem flow balance, version 5 In-Service Tests (IST)
  • 14825-2, Quarterly In-service Valve Test, version 94.2 (procedure section for steam generator no. 2 atmospheric relief valve PV-3010)

b. Findings

No findings were identified.

Cornerstone:

Emergency Preparedness

1EP6 Drill Evaluation

a. Inspection Scope

The inspectors observed training evolution V-RQ-SE-16202, designated as an emergency preparedness performance indicator data collection exercise (i.e. DEP and ERO), conducted on May 9, 2016. The inspectors observed licensee activities in the simulator to evaluate implementation of the emergency plan, including event classification and notification. The inspectors evaluated the licensee's performance against criteria established in the licensee's procedures. Additionally, the inspectors attended the post-exercise critique to assess the licensee's effectiveness in identifying emergency preparedness weaknesses and verified the identified weaknesses were entered in the corrective action program.

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a. Inspection Scope

The inspectors verified that the PI data complied with guidance contained in Nuclear Energy Institute 99-02, "Regulatory Assessment Performance Indicator Guideline," and licensee procedures. The inspectors verified the accuracy of reported data that were used to calculate the value of each PI.

Cornerstone:

Barrier Integrity

The inspectors reviewed a sample of the performance indicator (PI) data, submitted by the licensee, for these PIs. The inspectors reviewed plant records compiled between April 2015 and March 2016 to verify the accuracy and completeness of the data reported for the station. In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with PI data.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review

The inspectors screened items entered into the licensee's corrective action program in order to identify repetitive equipment failures or specific human performance issues for follow-up. The inspectors reviewed condition reports, attended screening meetings, or accessed the licensee's computerized corrective action database.

.2 Semi-Annual Trend Review

a. Inspection Scope

The inspectors reviewed issues entered in the licensee's corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors focused their review on the increasing trends of oil/grease in the jacket water system of the Unit 2 'B' train EDG, but also considered the results of inspector daily condition report screenings, licensee trending efforts, and licensee human performance results. The review nominally considered the 6-month period of either January 2016 through June 2016, although some examples extended beyond those dates when the scope of the trend warranted. The inspectors compared their results with the licensee's analysis of trends. Additionally, the inspectors reviewed the adequacy of corrective actions associated with a sample of the issues identified in the licensee's trend reports. The inspectors also reviewed corrective action documents that were processed by the licensee to identify potential adverse trends in the condition of structures, systems, and/or components as evidenced by acceptance of long-standing non-conforming or degraded conditions.

b. Findings and Observations

No findings were identified.

.3 Annual Follow-Up of Selected Issues

a. Inspection Scope

The inspectors conducted a detailed review of corrective action report (CAR)264166,"Improper Steam Dump Operation during the Unit 2 startup on March 28, 2016."

The inspectors evaluated the following attributes of the licensee's actions:

  • complete and accurate identification of the problem in a timely manner
  • evaluation and disposition of operability and reportability issues
  • consideration of extent of condition, generic implications, common cause, and previous occurrences
  • classification and prioritization of the problem
  • identification of root and contributing causes of the problem
  • identification of any additional condition reports
  • completion of corrective actions in a timely manner

b. Findings

No findings were identified.

4OA3 Follow-Up of Events and Notices of Enforcement Discretion

Unit 2 Automatic Reactor Trip

a. Inspection Scope

The licensee experienced an unplanned automatic reactor trip of Unit 2 on May 25, 2016. The automatic reactor trip was caused by low water level condition on the loop 1 S/G. The inspectors verified the licensee's trip response actions were in accordance with procedures. The inspectors reviewed the unit's response to the low water level condition to verify it was consistent to that described in the licensee's safety analysis.

The inspectors attended the licensee's restart Plant Review Board that was conducted to verify the unit would be allowed to be restarted in accordance with procedures. The inspectors reviewed the licensee's Human Performance Review Board results and the Reactor Trip Review report.

b. Findings

Introduction:

A Green self-revealing non-cited violation (NCV) of TS 5.4.1.a, Procedures, was identified for the licensee's failure to properly implement procedure 24750-2, "Steam Generator Level (Narrow Range) Protection Channel II 2L-519 Channel Operational Test and Channel Calibration", Ver. 23, during testing of the Unit 2 loop 1 S/G narrow range channel 2L-519.

Description:

The licensee was performing a planned Unit 2 Loop 1 S/G narrow range protection channel operational test and calibration using procedure 24750-2 "Steam Generator Level (Narrow Range) Protection Channel II 2L-519 Channel Operational test and Channel Calibration", Ver. 23. The channel being tested would be "removed from scan" which locked the steam generator water level at the current water level value regardless of the test or actual input. However, the averaging circuit was removed from scan instead of the channel being tested. This error locked in a S/G water level that was above the program level causing a reduction in main feedwater flow to the S/G. S/G water level decreased until it reached the low water level reactor trip setpoint. The licensee responded per their reactor trip procedures and stabilized the plant.

Analysis:

The failure to properly implement procedure 24750-2 as required by TS 5.4.1.a. is a performance deficiency (PD). The performance deficiency was more than minor because it adversely affected the Initiating Events cornerstone objective in that failure to properly remove channel 2L-519 resulted in a reactor trip. The finding was screened using IMC 0609, Appendix A, dated June 19, 2012. The finding was determined to be Green using Exhibit 1, Initiating Events, Transient Initiators, because the PD did not result in a loss of mitigation equipment used to transition the reactor to a stable shutdown condition. The finding was assigned a cross cutting aspect of Avoid Complacency because maintenance technicians failed to implement appropriate error reduction tools to verify that the correct channel was removed from scan for testing.

(H.12)

Enforcement:

Technical Specification 5.4.1.a required, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulation Guide 1.33, Rev. 2, Appendix A, February 1978.

Regulation Guide 1.33, Appendix A, Section 9.a. recommended written procedures for performing maintenance that can affect the performance of safety-related equipment. Procedure 24750-2 "Steam Generator Level (Narrow Range) Protection Channel II 2L-519 Channel Operational test and Channel Calibration" for the testing of the Unit 2 Loop 1 Steam Generator (S/G) narrow range channel 2L-519" required, in part, that point LY-519 be removed from scan. Contrary to the above, on May 25, 2016, licensee removed the Unit 2 Loop 1 averaging circuit from scan instead of channel 2L-519, resulting in a reactor trip. The licensee's immediate corrective actions were to remove the technicians performing the calibration from maintenance duties for formal remediation. The licensee documented this condition and the corrective actions in CR 10230073. This violation is being treated as an NCV in accordance with section 2.3.2.a of the Enforcement policy:

NCV 05000425/2016002-01, "Failure to properly implement a maintenance procedure caused a reactor trip."

4OA5 Other Activities

Operation of an Independent Spent Fuel Storage Installation (ISFSI) (60855.1)

a. Inspection Scope

The inspectors performed a walkdown of the onsite ISFSI. The inspectors reviewed surveillance records to verify that daily surveillance requirements were performed as required by technical specifications.

b. Findings

No findings were identified.

4OA6 Meetings, Including Exit On July 14, 2016, the resident inspectors presented the inspection results to Darin Myers and other members of the licensee's staff.

The inspectors confirmed that proprietary information was not provided or examined during the inspection period.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

T. Baker, Security Manager
S. Briggs, Operations Director
J. Crites, Maintenance Rule Coordinator
J. Dixon, Radiation Protection Manager
T. Fowler, Chemistry Manager
G. Gunn, Licensing Manager
S. Harris, Operations Manager
D. Komm, Work Management Director
D. Myers, Plant Manager
D. Stiles, Training Director
T. Baker, Security Manager
J. Summy, Engineering Director
D. Myers, Plant Manager
K. Taber, Site Vice-President
K. Walden, Licensing Engineer
I. White, Licensing Engineer

LIST OF REPORT ITEMS

Opened and Closed NCV

05000425/2016002-01 Failure to properly implement a maintenance procedure caused a Reactor Trip (Section 4OA3)

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection Procedures 10029-C,

NERC/SERC Standards for Generator Operators, Ver. 3 18017-C, Abnormal Grid Disturbances/Loss of Grid, Ver. 9.6
NMP-AD-014-GL01, Guidelines for Compliance with NERC Standards, Ver. 6.0
NMP-AD-014-002,
NUC-001 Nuclear Plant Interface Coordination for Southern Nuclear Company, Ver. 4.0 14230-1, Offsite A.C. Circuit Verification and Capacity/Capability Evaluation, Ver. 26
Other Site Certification Letter for Summer Readiness dated May 9, 2016
CRs 749961, 780387

Section 1R04: Equipment Alignment

Drawings

2X4DB122 Rev. 54.0, P&I Residual Heat Removal System, System No. 1205 1X4DB116-2 Ver. 37.0, P&I Diagram - Chemical & Volume Control System, System No. 1208

Procedures

13744B-1 Ver. 12.2, Train B Essential Chilled Water System
13903-C, Fire Protection System Operation
Other Tagout: 1-DT-16-1208-00064 Clearance: 1-DT-16: Tagout: 1-DT-16-1592-00094 System Description - Fire Protection dated 9/11/2015
System Health Report: Vogtle Residual Heat Removal System No. 1205: 2015 QTRs 1 - 4 and 2016 QTR 1 Corrosion Assessment No. 1205-2010-006, Ver. 2.0 Corrosion Assessment No. 1205-2013-002, Ver. 2.0
CR list for RHR System (System No. 1205) ranging from 1/1/15 thru 6/20/16

Section 1R05: Fire Protection Annual/Quarterly

Procedures

92789-1 Rev. 2.1, Zone 89 - Control Building Level A Fire Fighting Preplan 92790-1 Rev. 2.2, Zone 90 - Control Building Level A Fire Fighting Preplan
2859-1 Rev. 2.2, Zone 159 - Control Building Level A Fire Fighting Preplan
2787-1 Rev. 2.2, Zone 87 - Control Building Level A Fire Fighting Preplan
2788-1 Rev. 2.2, Zone 88 - Control Building Level A Fire Fighting Preplan
2793-1 Rev. 3.2, Zone 93 - Control Building Level A 92802-1 Rev. 1.2, Zone 102 - Control Building - Level A Fire Fighting Preplan 92858-1 Rev. 2.2, Zone 158 - Control Building Level A Fire Fighting Preplan 92737-2 Rev. 3.0, Zone 37 - Auxiliary Building - Level A, CCW Pumps, Train "B" Fire Fighting Plan 92736-2 Rev. 5.0, Zone 36 - Auxiliary Building - Level A, CCW Pumps, Train A Fire Fighting Plan 92805-2 Rev. 5, Zone 105 - Control Building - Level 1 Fire Fighting Preplan 92806-1 Rev. 2.2, Zone 106 - Control Building - Level 1 Fire Fighting Preplan
2883A-1 Rev. 1.2, Zone 183A - Control Building - Level 1 Fire Fighting Preplan
2921-1 Rev. 2.2, Zone 601 - Technical Support Center Fire Fighting Preplan
2922-1 Rev. 3.1, Zone 602 Technical Support Center Fire Fighting Preplan 92923-1 Rev. 1.2, Zone 603 Technical Support Center Electrical Equipment Room Fire Fighting Preplan 92924-1 Rev. 2.2, Zone 604 Technical Support Center Battery Room Fire Fighting Preplan 92925-1 Rev. 2.2, Zone 605 TSC Control Building Level 1 Fire Fighting Preplan
92704-2 Rev. 2.0, Zone 4 - Auxiliary Building - Level D, Containment Spray Pump "A" Fire Fighting Preplan 92705-2 Rev. 3.0, Zone 5 - Auxiliary Building - Level D, Containment Spray Pump "B" Fire Fighting Preplan 92709-2 Rev. 2.2, Zone 9 - Auxiliary Building - Level D Fire Fighting Preplan 92839-1 Rev. 3.0, Zone 139 - Fuel Handling Building - Level 1 Fire Fighting Preplan
Other
NMP-TR-425-F02, Drill Exercise Completion Sheet dated 4/25/2016

Section 1R11: Licensed Operator Requalification Program and Licensed Operator Performance

Procedures

NMP-EP-110 Ver. 8.1, Emergency Classification Determination and Initial Action
NMP-EP-110-GL03 Ver. 5.2, VEGP EALs - ICs, Thresholds Values and Basis
NMP-EP-111 Ver. 11.0, Emergency Notifications

Section 1R12: Maintenance Effectiveness

Work Orders

SNC 539529 S/G 1 Main Feedwater Regulating Valve Air Operated Valve rebuild
SNC 539528 S/G 1 Main Feedwater Regulating Valve Air Operated Valve maintenance
SNC 539516 S/G 1 Main Feedwater Regulating Valve repacking
SNC 795249 Foreign Material Retrieval for the Unit 2 6A Feedwater Heater
SNC 777525 Unit 2 Loop 1 Atmospheric Relief Valve actuator repair Other NUMARC 93-01, Rev. 4A, Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants Maintenance Rule Expert Panel Meeting Minutes from April 26, 2016
NMP-ES-027, Ver. 4.0, Maintenance Rule Program Vogtle Quality Assurance Technical Report (QATR), Rev. 12
CR 10202079,
10203906,
10236360,
10202092,
10202097,
10202669, 10205164

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Procedures

NMP-GM-31-001, Ver. 3.0, Online Maintenance Rule (a)(4) Risk Calculations
NMP-DP-001-GL01, Ver. 9.4, Risk Assessment Worksheets
Other Unit 2 Narrative Logs for the week of May 2, 2016; May 17, 2016; May 23, 2016; June 6, 2016 and June 13, 2016
Unit 2 EOOS profile for the week of May 2, 2016; May 17, 2016; May 23, 2016; June 6, 2016 and June 13, 2016 Unit 1 EOOS risk profile for week of May 2, 2016
CRs 10216596,
10217069,
10227263
CAR 265365
Work week plan for the week of May 23, 2016

Section 1R15: Operability Determination and Functionality Assessments Procedures 13744B-2, Ver. 12, Train B Essential Chilled Water System 17035-2, Ver. 34, Annunciator Response Procedures for

ALB 35 on EAB Panel

Drawings

2X4DB135-2, Rev. XX, PI&D - Nuclear Service Water System - System No. 1202
1X4AK01-046-18, Rev. W, Unit 2 EDG A Engine Control Panel Schematic 2X3D-BH-G03C, Ver. 7.0, Elementary Diagram Diesel Engine Control - Generator DG2A 2X3D-BH-G03D, Ver. 8.0, Elementary Diagram Diesel Engine Control - Generator DG2A
2X4AK01-00361, Ver. 12.0, Engine Control Panel Schematic Sheet 1 of 13
2X4AK01-00362, Rev. 13, Engine Control Panel Schematic
2X4AK01-00364, Ver. 17.0, Engine Control Panel Schematic
2X4AK01-00363, Ver. 17.0, Engine Control Panel Schematic Other UFSAR Section 9.2.9.1, Essential Chilled Water System Anton, Brandt, NALCO Water Co., letter to Jeff Waites and Nin Travljanin, Southern Nuclear Plant Vogtle, May 24, 2016 Functionality Assessment #1-15-001 VTM CX4AF14-00019, Ver. 10, Fire Protection Pump Drive Industrial Engines - Operation, Maintenance Manual, and Parts Catalog VTM AX4AJ04-20000, Ver. 7.0, Installation, Operation and Maintenance - Manual ESF Chillers
CRs 10224020,
10227263,
10229803,
10229821,
10206003,
10207224, 10229293

Section 1R19: Post Maintenance Testing

Work Orders

SNC 539528, S/G 1 Main Feedwater Regulating Valve Air Operated Valve maintenance
SNC 777525, Unit 2 Loop 1 Atmospheric Relief Valve actuator repair
SNC 541720, 36 Month
NSCW-ESF Water Chiller Flow Channel (2F-1803), May 17, 2016
SNC396950, Check valve from reactor makeup water to boric acid blend (CVCS), March 16,
2016 SNC779920, 1N41 power range instrument J352 connector repair, April 5, 2016 SNC752096, 12-week calibration of 1N41, April 7, 2016
SNC 480312, Nitrogen charging and air pump regulator adjustment for main feed isolation valve, 1HV-5228, May 6, 2016

Procedures

26852-C, Ver. 17, Main Feedwater Isolation Valve Nitrogen Charge and Oil Level Checks
24361-2, NSCW, ESF Water Chiller 2F-1803 Channel Calibration, Rev, 11.1
24700-1, Ver. 60, Nuclear Instrumentation System Power Range Channel 1N41 Channel Calibration

Drawings

AX4AR19-00037, Ver. 1.0, Schematic for Anchor/Darling Self-Contained Hydraulic Actuator
CRs 10224223,
10206098, 10218905

Section 1R22: Surveillance Testing

Completed Procedures 14460-2, Ver. 38.1, ECCS Flow Path Verification
14721C-2, ECCS subsystem flow balance, Completed on March 11, 2016 14825-2, Quarterly Inservice Valve Test, Version 94.2
14951-C, Ver. 32, Fire Suppression System Operability Tests (Section 1.3 - Diesel Fire Pump #2
C-2301-P4-003) Monthly Test, Completed on April 18, 2016

Procedures

24306-2, Ver. 7, Safety Injection Pump
2-1204-P6-003 Discharge Flow 2F-918 Channel Calibration 24307-2, Ver. 7, Safety Injection Pump
2-1204-P6-004 Discharge Flow 2F-922 Channel Calibration 24328-2, Ver. 20, Low Head Safety Injection Flow 2F-618 Channel Calibration Work Order SNC609420, ECCS flow balance, March 10, 2016

Drawings

1X4DB159-2, Ver. 33.0 P&I Diagram Main Steam System, System No. 1301
2X4DB116-1, Rev. 49, P&I Diagram - Chemical & Control Volume System - System 1208
2X4DB119, Rev. 27, P&I Diagram - Safety Injection System - System 1204
2X4DB120, Rev. 29, P&I Diagram - Safety Injection System - System 1204
2X4DB121, Rev. 50, P&I Diagram - Safety Injection System - System 1204
2X4DB122, Rev. 54, P&I Diagram - Residual Heat Removal System - System 1205
AX3D-AA-F06B, One Line Diagram - 480V MCC ANBK - A-1805-S3-NBG, Ver. 5.0 AX3D-AA-F10A, One Line Diagram - 480V MCC ANBK - A-1805-S3-NBK, Ver. 15.0 CX3D-CE-887D, Wiring Diagram - Aux Sys Fire Prot. Water Sys
C-2301-P5-FP2, Rev. 5.0
CX4DB713-1, P&I Diagram - Fire Protection Pump House No. 1 and 2, System 2301, Ver. 43.0
Other 2X5DZ000618, Ver. 1.0, Low Head Safety Injection Flow Train A 2F-618 Scaling Document 2X5DZ000619, Ver. 1.0, Low Head Safety Injection Flow Train A 2F-619 Scaling Document
2X5DZ000918, Ver. 1.0, Safety Injection Pump Train A Discharge Flow 2F-918 Scaling Document 2X5DZ000922, Ver. 1.0, Safety Injection Pump Train B Discharge Flow 2F-922 Scaling Document ASME OM Code-2001, Code for Operation and Maintenance of Nuclear Power Plants B. J. George, Southern Nuclear Plant Vogtle, letter to U. S. Nuclear Regulatory Commission, "Vogtle Electric Generating Plant Third Interval Inservice Testing (IST) Program Update," April 16, 2007 Clearance: 1-DT-16 : Tagout: 1-DT-16-2301-00068 U.S. Nuclear Regulatory Commission, "Guidelines for Inservice Testing at Nuclear Power Plants: Inservice Testing of Pumps and Valves and Inservice Examination and Testing of Dynamic Restraints (Snubbers) at Nuclear Power Plants - Final Report,"
NUREG-1482, Revision 2, October 2013
CR 10210388
Section 1EP06:
Drill Evaluation

Procedures

NMP-EP-110, Ver. 8.1, Emergency Classification Determination and Initial Action
NMP-EP-110-GL03, Ver. 5.2, VEGP EALs - ICs, Thresholds Values and Basis
NMP-EP-111, Ver. 11.0, Emergency Notifications
Other V-RQ-SE-16202, Simulator Exercise Guide

Section 4OA1: Problem Identification and Resolution

Procedures

00163-C, Rev. 14.6, NRC Performance Indicator and Monthly Operating Report Preparation and Submittal Other
NEI 99-02, Rev. 7, Regulatory Assessment Indicator Guideline

Section 4OA2: Problem Identification and Resolution

Apparent Cause Determination Report for
CAR 264166, Ver. 1.0
T.S. 3.4.1, Amendment 74, RCS Pressure, Temperature, and flow; Departure from Nucleate Boiling (DNB) Limits T.S. 3.4.1, Basis, Amendment 74; RCS Pressure, Temperature, and flow; Departure from Nucleate Boiling (DNB) Limits
CR 10161039,
10178099,
10154763,
10177067,
10176964,
10231698,
10238423 TE949569, Track and trend of 2B EDG oil and grease content in jacket water

Section 4OA2: Follow-Up of Events and Notices of Enforcement Discretion Procedures 24750-2, Ver. 23, Steam Generator Level (Narrow Range) Protection Channel

II 2L-519 Channel Operational Test and Channel Calibration 23505-C, Ver. 3, Ovation Digital Feed Water System Maintenance 17013-2, Ver. 29.4, Annunciator Response Procedures for
ALB 13 on Panel 2B1 on
MCB 18016-C, Ver. 30, Condensate and F/W Malfunction 18001-C, Ver. 36, Systems Instrumentation Malfunction
2003-C, Ver. 59, Reactor Startup (Mode 3 to Mode 2)
NMP-OS-007, Ver. 11, Conduct of Operations
Other 10006-C, Ver. 29.2, Reactor Trip Review for the Unit 2 Trip that occurred on May 25, 2016 Operator logs from May 24-26, 2016 Root Cause Charter for
CAR 265328
Human Performance Review Board Summary for
CR 10227856
CR 10227856
NMP-GM-009-F01, Ver. 6.0, Restart PRB Review for the Unit 2 Trip that occurred on May 25,
2016

Section 4OA5: Other Activities

Other VEGP 10
CFR 72.212 Report, Version 2 VEGP Certificate of Compliance, Amendment 9
VEGP ISFSI FSAR, Rev. 12