IR 05000424/2016001

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NRC Integrated Inspection Report 05000424/2016001 and 05000425/2016001, January 1, 2016 Through March 31, 2016
ML16124A779
Person / Time
Site: Vogtle  Southern Nuclear icon.png
Issue date: 05/03/2016
From: Shane Sandal
NRC/RGN-II/DRP/RPB2
To: Taber K
Southern Nuclear Operating Co
References
IR 2016001
Download: ML16124A779 (35)


Text

UNITED STATES May 3, 2016

SUBJECT:

VOGTLE ELECTRIC GENERATING PLANT - NRC INTEGRATED INSPECTION REPORT 05000424/2016001 AND 05000425/2016001

Dear Mr. Taber:

On March 31, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Vogtle Electric Generating Plant, Units 1 and 2. On April 25, 2016, the NRC inspectors discussed the results of this inspection with you and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.

The inspections examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. No findings were identified.

In accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding, of the NRC's Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Shane Sandal, Chief Reactor Projects Branch 2 Division of Reactor Projects Docket Nos.: 50-424, 50-425 License Nos.: NPF-68 and NPF-81

Enclosures:

IR 05000424/2016001; 05000425/2016001 w/Attachment: Supplemental Information

REGION II==

Docket Nos.: 50-424, 50-425 License Nos.: NPF-68, NPF-81 Report Nos.: 05000424/2016001 and 05000425/2016001 Licensee: Southern Nuclear Operating Company, Inc. (SNC)

Facility: Vogtle Electric Generating Plant, Units 1 and 2 Location: Waynesboro, GA 30830 Dates: January 1, 2016 through March 31, 2016 Inspectors: W. Deschaine, Senior Resident Inspector A. Alen, Resident Inspector J. Rivera-Ortiz, Senior Reactor Inspector (1R08)

R. Williams, Senior Reactor Inspector (1R08)

C. Dykes, Health Physicist (2RS3, 2RS4)

R. Kellner, Senior Health Physicist (2RS1)

J. Panfel, Health Physicist (2RS2, 4OA1)

Approved by: Shane Sandal, Chief Reactor Projects Branch 2 Division of Reactor Projects Enclosure

SUMMARY OF FINDINGS

IR 05000424/2016001; and 05000425/2016001; January 1, 2016, through March 31, 2016;

Vogtle Electric Generating Plant, Units 1 and 2; Quarterly Integrated Inspection Report The report covered a 3-month period of inspection by resident inspectors and regional inspectors. The NRCs program for overseeing the safe operations of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 5.

REPORT DETAILS

Summary of Plant Status

Unit 1 operated at or near full rated thermal power for the entire inspection period.

Unit 2 began the report period at full rated thermal power. The unit was shut down for planned refueling outage cycle 18 (2R18) on March 6, 2016. The unit was restarted on March 27, 2016, and attained full power on March 31,

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

a. Inspection Scope

Impending Adverse Weather Conditions: The inspectors reviewed the licensees preparations to protect risk-significant systems from predicted severe weather conditions of sub-freezing temperatures expected on the week of January 18, 2016. The inspectors evaluated the licensees implementation of adverse weather preparation procedures and compensatory measures, including operator staffing, before the onset of and during the adverse weather conditions. The inspectors reviewed the licensees plans to address the ramifications of potentially lasting effects that may result from the sub-freezing temperatures. The inspectors verified that operator actions specified in the licensees adverse weather procedure maintain readiness of essential systems. The inspectors verified that required surveillances were current, or were scheduled and completed, if practical, before the onset of anticipated adverse weather conditions. The inspectors also verified that the licensee implemented periodic equipment walkdowns or other measures to ensure that the condition of plant equipment met operability requirements.

b. Findings

No findings were identified.

1R04 Equipment Alignment

a. Inspection Scope

Partial Walkdown: The inspectors verified that critical portions of the following systems were correctly aligned by performing partial walkdowns. The inspectors determined the correct system lineup by reviewing plant procedures and drawings listed in the

.

  • Unit 2, centrifugal charging pump B train while the A train was out of service (OOS)for planned maintenance.
  • Unit 2, safety injection B train while the A train was OOS for planned maintenance.
  • Unit 1, 1E 4160-volt electrical power bus alignment to the standby auxiliary transformer due to the qualified offsite circuit no. 2 being OOS for planned maintenance

b. Findings

No findings were identified.

1R05 Fire Protection

a. Inspection Scope

Quarterly Inspection: The inspectors evaluated the adequacy of fire plans by comparing the fire plans to the defined hazards and defense-in-depth features specified in the fire protection program for the following five fire areas.

  • Unit 1, component cooling water heat exchanger rooms, fire zones 54, 55, 148, 23, 172 and 147
  • Unit 1, component cooling water pump rooms, fire zones 36 and 37
  • Unit 2, cable spreading rooms, fire zones 94, 95, 173, 174, 107, 108, 120, and 121
  • Unit 2, containment building, fire zones 140A, 140B, 140C, and 140E
  • Unit 2, north and south main steam valve house, fire zones 99, 45 and 104 The inspectors assessed each fire area for the following attributes:
  • control of transient combustibles and ignition sources
  • fire detection systems
  • water-based fire suppression systems
  • gaseous fire suppression systems
  • manual firefighting equipment and capability
  • passive fire protection features
  • compensatory measures and fire watches
  • issues related to fire protection contained in the licensees corrective action program
  • material condition and operational status of fire protection equipment Fire Drill Observation: The inspectors observed the licensees fire brigade performance for fire drill no. 2016-Q1-03, fire in the Unit 1 train A diesel generator building, on February 10, 2016. The inspectors assessed the fire brigades capability to meet fire protection licensing basis requirements and assessed the following performance attributes:
  • capability of fire brigade members
  • leadership ability of the brigade leader
  • proper use of turnout gear and fire-fighting equipment
  • team effectiveness
  • compliance with site procedures The inspectors also assessed the ability of control room operators to combat potential fires including identifying the location of the fire, dispatching the fire brigade, and sounding alarms. The inspectors evaluated the licensees ability to declare the appropriate emergency action level and make required notifications in accordance with NUREG 0654, Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and Preparedness in Support of Nuclear Power Plants (FEMA-REP-1)and 10 CFR Part 50, Domestic Licensing of Production and Utilization Facilities.

b. Findings

No findings were identified.

1R07 Heat Sink Performance

a. Inspection Scope

Annual Review: The inspectors verified the readiness and availability of the Unit 2 A train of component cooling water heat exchanger and A train emergency diesel generator jacket water heat exchanger to perform their design functions by verifying the licensee followed periodic maintenance methods outlined in the plants specific commitments to Generic Letter 89-13, reviewing performance test results, and observing inspection and state of cleanliness of the heat exchangers. Additionally, the inspectors verified that the licensee had entered any significant heat exchanger performance problems into the corrective action program and that the licensees corrective actions were appropriate.

b. Findings

No findings were identified.

1R08 Inservice Inspection Activities

a. Inspection Scope

Non-Destructive Examination Activities and Welding Activities: The inspectors conducted an onsite review of the implementation of the licensees in-service inspection (ISI) program for monitoring degradation of the reactor coolant system boundary, risk-significant piping and component boundaries, and containment boundaries in Unit 2.

The inspectors either directly observed and/or reviewed documentation for the following non-destructive examinations (NDEs) mandated by the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (Code of Record: 2001 Edition with 2003 Addenda) or Vogtles Risk-Informed ISI Program to evaluate compliance with the applicable ASME Code requirements, and verify that indications or defects were dispositioned in accordance with the ASME Code, or an NRC-approved alternative requirement. The inspectors also reviewed the qualifications of the NDE technicians performing the examinations, to determine whether they were current and in compliance with the ASME Code requirements.

  • UT of Weld 21305-062-11-RB, Condensate and Feedwater System, ASME Class 2, Augmented/Technical Specification Exam (document review)

The inspectors reviewed final records for the welding activities listed below to evaluate compliance with procedures and the ASME Code,Section XI and Section IX requirements. Specifically, the inspectors reviewed the work order (WO), repair and replacement plan, weld data sheets, welding procedures, procedure qualification records, welder performance qualification records, and NDE reports.

  • Weld Traveler 14104, Removal and Reinstallation of Elbow to Support Mechanical Stress Improvement Process, Component 2-1201-055-1, Reactor Coolant System, ASME Class 1 During non-destructive surface and volumetric examinations performed since the previous refueling outage, the licensee did not identify any relevant indications that were analytically evaluated and accepted for continued service; therefore, no NRC review was completed for this inspection procedure attribute.

Pressurized Water Reactor Vessel Upper Head Penetration Inspection Activities: The inspectors reviewed the licensees calculation for Effective Degradation Years and Reinspection Years to verify that for the Unit 2 vessel head, a bare metal visual examination and a volumetric examination were not required during this outage, in accordance with the requirements of ASME Code Case N-729-1 and 10 CFR 50.55a(g)(6)(ii)(D). The licensee did not identify any relevant indications that were accepted for continued service. Additionally, the licensee did not perform any welding repairs to the vessel head penetrations since the beginning of the last Unit 2 refueling outage; therefore, no NRC review was completed for these inspection procedure attributes.

Boric Acid Corrosion Control Inspection Activities: The inspectors reviewed the licensees boric acid corrosion control program (BACCP) activities to determine if the activities were implemented in accordance with the commitments made in response to NRC Generic Letter 88-05, Boric Acid Corrosion of Carbon Steel Reactor Pressure Boundary Components in PWR Plants, and applicable industry guidance documents.

Specifically, the inspectors performed an onsite records review of procedures, and the results of the licensees containment walkdown inspections performed during the current refueling outage. The inspectors also interviewed the BACCP owner and conducted an independent walkdown of the reactor building containment areas listed below to evaluate compliance with licensees BACCP requirements and verified that degraded or non-conforming conditions, such as boric acid leaks, were properly identified and corrected in accordance with the licensees BACCP and the corrective action program.

  • Top of Pressurizer (Elevation 252)
  • Area Inside Bioshield, Loop 3, Reactor Coolant Pump Seal no. 3 Platform (Elevation 171)
  • Area Inside Bioshield, Loop 3, Steam Generator no. 3 Secondary Side Platform, (Elevation 171)
  • General Area Outside the Bioshield: C Level (Elevation 171), B Level (Elevation 185), Lower A Level (Elevation 195), and Upper A Level (Elevation 210)

The inspectors reviewed the following engineering evaluations, completed for evidence of boric acid leakage, to determine if the licensee properly applied applicable corrosion rates to the affected components; and properly assessed the effects of corrosion induced wastage on structural or pressure boundary integrity in accordance with the licensee procedures.

  • 1204-2008-015, Safety Injection System, Component 21204-241-3 Flange
  • 1208-2008-021, Chemical and Volume Control System, Component 21208-F4005
  • CR 864653 (WO SNC604980), Component 1208 21208X4036, Chemical and Volume Control System Charging Pump A Discharge FE-0138 Steam Generator Tube Inspection Activities: The inspectors reviewed the eddy current (EC) examination activities performed in Unit 2 steam generators (SGs) 1, 2, 3, and 4 during this current refueling outage to verify compliance with the licensees Technical Specifications, ASME BPVC Section XI, and Nuclear Energy Institute 97-06, Steam Generator Program Guidelines.

The inspectors reviewed the scope of the EC examinations, and the implementation of scope expansion criteria, to verify these were consistent with the Electric Power Research Institute (EPRI) Pressurized Water Reactor Steam Generator Examination Guidelines, Revision 7. The inspectors reviewed documentation for a sample of EC data analysts, probes, and testers to verify that personnel and equipment were qualified to detect the applicable degradation mechanisms in accordance with the EPRI Examination Guidelines. This review included a sample of site-specific Examination Technique Specification Sheets (ETSSs) to verify that their qualification and site-specific implementation were consistent with Appendix H or I of the EPRI Examination Guidelines. The inspectors also reviewed a sample of EC data for steam SG tubes 1-R12C94, 1-R12C117, 2-R35C61, 2-R21C61, 4-R57C48, and 4-R52C33 with a qualified data analyst, to confirm that data analysis and equipment configuration were performed in accordance with the applicable ETSSs and site-specific analysis guidelines. The inspectors verified that recordable indications were detected and sized in accordance with vendor procedures.

The inspectors selected a sample of degradation mechanisms from the Unit 2 Degradation Assessment report (i.e., anti-vibration bar wear and outside diameter stress corrosion cracking at Hot Leg Extensions), and verified that their respective in-situ pressure testing criteria were determined in accordance with the EPRI Steam Generator Integrity Assessment Guidelines, Revision 3. Additionally, the inspectors reviewed EC indication reports to determine whether tubes with relevant indications were appropriately screened for in-situ pressure testing. The inspectors also compared the latest EC examination results with the last Condition Monitoring and Operational Assessment report for Unit 2, to assess the licensees prediction capability for maximum tube degradation and number of tubes with indications. The inspectors verified that the licensees evaluation was conservative and that current examination results were bounded by the Operational Assessment projections.

The inspectors assessed the latest EC examination results to verify that new degradation mechanisms, if any, were identified and evaluated before plant startup.

The review of EC examination results included the disposition of potential loose part indications on the SG secondary side, to verify that corrective actions for evaluating and retrieving loose parts were consistent with the EPRI Guidelines. The inspectors also reviewed a sample of primary-to-secondary leakage data for Unit 2, to confirm that operational leakage in each SG remained below the detection or action level threshold during the previous operating cycle.

The inspectors review included the implementation of tube repair criteria and repair methods, to verify they were consistent with plant Technical Specifications and industry guidelines. The inspectors were informed that no tubes were plugged based on the EC examination results. The inspectors interviewed plant personnel and reviewed final EC examination results to verify that none of the tubes left in-service met the tube repair criteria. Furthermore, the inspectors interviewed licensee staff and reviewed a sample of inspection results for the inspection conducted in the secondary side internals of SGs 1, 2, 3, and 4 to verify that potential areas of degradation based on site-specific operating experience were inspected, and appropriate corrective actions were taken to address degradation indications. This review included the results of Foreign Object Search and Retrieval activities in all SGs.

Identification and Resolution of Problems: The inspectors reviewed a sample of ISI-related issues entered into the corrective action program as CRs to determine if the licensee had appropriately described the scope of the problem, and had initiated corrective actions. The review also included the licensees consideration and assessment of operating experience events applicable to the plant. The inspectors performed this review to ensure compliance with 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action requirements.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

a. Inspection Scope

Resident Inspector Quarterly Review of Licensed Operator Requalification: The inspectors observed one evaluated simulator scenario, V-RQ-SE-16102, and one training simulator scenario, V-RQ-SE-14302, administered to a licensed operating crew, on February 10, 2016, in accordance with the licensees accredited requalification training program. The inspectors assessed the following attributes:

  • licensed operator performance
  • the ability of the licensee to administer the scenario and evaluate the operators
  • the quality of the post-scenario critique
  • simulator performance Resident Inspector Quarterly Review of Licensed Operator Performance: The inspectors observed licensed operator performance in the main control room during the Unit 2 reactor shutdown at the beginning of the cycle 18 refueling outage. The inspectors assessed the following attributes:
  • use of plant procedures
  • control board manipulations
  • communications between crew members
  • use and interpretation of instruments, indications, and alarms
  • use of human error prevention techniques
  • documentation of activities
  • management and supervision

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors assessed the licensees treatment of the issue listed below to verify the licensee appropriately addressed equipment problems within the scope of the maintenance rule (10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants). The inspectors reviewed procedures and records to evaluate the licensees identification, assessment, and characterization of the problems as well as their corrective actions for returning the equipment to a satisfactory condition.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the four maintenance activities listed below to verify that the licensee assessed and managed plant risk as required by 10 CFR 50.65(a)(4) and licensee procedures. The inspectors assessed the adequacy of the licensees risk assessments and implementation of risk management actions. The inspectors also verified that the licensee was identifying and resolving problems with assessing and managing maintenance-related risk using the corrective action program. Additionally, for maintenance resulting from unforeseen situations, the inspectors assessed the effectiveness of the licensees planning and control of emergent work activities.

  • Unit 2, week of January 25, 2016, projected YELLOW equipment out of service (EOOS) risk profile due to scheduled maintenance on the B train of the auxiliary Feedwater system.
  • Unit 2, February 22, 2016, YELLOW EOOS risk profile due to scheduled surveillance testing on the B train control room isolation automatic actuation logic.
  • Unit 2, March 8-9, 2016, YELLOW Outage Risk Assessment Monitor (ORAM) risk condition due to core cooling and reactor coolant system inventory control.

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

Operability Determinations and Functionality Assessments Review: The inspectors selected the four operability determinations or functionality evaluations listed below for review based on the risk-significance of the associated components and systems. The inspectors reviewed the technical adequacy of the determinations to ensure that technical specification operability was properly justified and the components or systems remained capable of performing their design functions. To verify whether components or systems were operable, the inspectors compared the operability and design criteria in the appropriate sections of the Technical Specification and updated final safety analysis report to the licensees evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with operability evaluations.

  • Unit 1, solid state protection system A train logic test failure on reactor coolant pump under-frequency during operability test, condition report (CR) 10192480
  • Unit 2, immediate determination of operability (IDO) for nuclear service water system pump no. 3 with respect to a 10 CFR Part 21 issue on radiation dose qualification of the motor (Ref. ML16012A502), CR10173354
  • Unit 2, IDO for B train centrifugal charging pump outboard pump seal is leakage, CR 10008234
  • Units 1 and 2, prompt operability determination (PDO) to defend minimum required amount of trisodium phosphate for containment sump pH control due to a calculation error, PDO No. 1-16-001, CR10176879

b. Findings

No findings were identified.

1R18 Plant Modifications

a. Inspection Scope

The inspectors reviewed licensing document change request (LDCR), i.e. Plant modification, No. 2016007, 1E Battery Service Test Interval, Version 1.0. The inspectors assessed the following:

  • Verified that the modification did not affect the safety functions of important safety systems.
  • Confirmed the modification did not degrade the design bases, licensing bases, and performance capability of risk significant structures, systems and components.
  • Verified modification performed during plant configurations involving increased risk did not place the plant in an unsafe condition.
  • Evaluated whether system operability and availability, configuration control, post-installation test activities, and changes to documents, such as drawings, procedures, and operator training materials, complied with licensee standards and NRC requirements.
  • Reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with modifications.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors either observed post-maintenance testing or reviewed the test results for the eight maintenance activities listed below to verify the work performed was completed correctly and the test activities were adequate to verify system operability and functional capability.

  • SNC536447, Unit 2 A train nuclear service cooling water system spray header bypass valve control temperature element, TE-1668, 36 month calibration, 3/11/16
  • SNC756038, Unit 1 containment pressure channel IV, 1P-934, replacement of failed loop power supply (NLP) card, 1/27/16
  • SNC771837, Unit 1 B train EDG fuel oil storage tank transfer pump no. 4 functionally test of the lo-lo level switch, 1-LSLL-9021, 3/21/16
  • SNC676145, Unit 1, replacement of solenoid valve 1FY0111A for the chemical and volume control system reactor makeup water storage tank to boric acid blender flow control, 3/22/16
  • SNC123830, Unit 1 B train EDG preventive maintenance to remove, inspect and reinstall cylinder liners, 3/13/16
  • SNC380674, Unit 2 mechanical and electrical inspections of motor operated valve, 2HV8716A-MO, residual heat removal hot leg isolation, 3/11/16 The inspectors evaluated these activities for the following attributes:
  • Acceptance criteria were clear and demonstrated operational readiness.
  • Effects of testing on the plant were adequately addressed.
  • Test instrumentation was appropriate.
  • Tests were performed in accordance with approved procedures.
  • Equipment was returned to its operational status following testing.
  • Test documentation was properly evaluated.

Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with post-maintenance testing.

b. Findings

No findings were identified.

1R20 Refueling and Other Outage Activities

a. Inspection Scope

For the Unit 2 refueling outage of March 6 through March 27, 2016, the inspectors evaluated the following outage activities:

  • outage planning
  • fatigue management
  • shutdown, cooldown, refueling, heatup, and startup
  • reactivity and inventory control
  • containment closure The inspectors verified that the licensee:
  • considered risk in developing the outage schedule
  • controlled plant configuration in accordance with administrative risk reduction methodologies
  • developed work schedules to manage fatigue
  • developed mitigation strategies for loss of key safety functions
  • adhered to operating license and technical specification requirements Inspectors verified that safety-related and risk-significant structures, systems, and components not accessible during power operations were maintained in an operable condition. The inspectors also reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with outage activities.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the four surveillance tests listed below. The surveillance test was either observed directly or test results were reviewed to verify testing activities and results provide objective evidence that the affected equipment remain capable of performing their intended safety functions and maintain their operational readiness consistent with the facilitys current licensing basis. The inspectors evaluated the test activities to assess for:

  • preconditioning of equipment
  • appropriate acceptance criteria
  • calibration and appropriateness of measuring and test equipment
  • procedure adherence
  • equipment alignment following completion of the surveillance Additionally, the inspectors reviewed a sample of significant surveillance testing problems documented in the licensees corrective action program to verify the licensee was identifying and correcting any testing problems associated with surveillance testing.

Routine Surveillance Tests

  • 14666-2, Train A Diesel Generator and ESFAS Test, Version 37.1
  • 14712C-2, Turbine-Driven Auxiliary Feedwater Remote Shutdown Panel Transfer Switch and Control Circuit 18 Month Surveillance Test, Revision 2.2 Containment Isolation Valve
  • 14362-2, Containment Penetration No. 62 - PRT Sample Local Leak Rate Test, Version 9 In-Service Tests (IST)
  • 28210-C, Main Steamline Code Safety Valve Setpoint Verification, Version 23.1

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

a. Inspection Scope

The inspectors observed the emergency preparedness drill conducted on February 17, 2016. The inspectors observed licensee activities in the simulator and technical support center to evaluate implementation of the emergency plan, including event classification, notification, dose assessment, and protective action recommendations. The inspectors evaluated the licensees performance against criteria established in the licensees procedures. Additionally, the inspectors attended the post-exercise critique to assess the licensees effectiveness in identifying emergency preparedness weaknesses and verified the identified weaknesses were entered in the corrective action program.

b. Findings

No findings were identified.

RADIATION SAFETY

(RS)

2RS1 Radiological Hazard Assessment and Exposure Controls

a. Inspection Scope

Hazard Assessment and Instructions to Workers: During facility tours the inspectors directly observed labeled radioactive material and postings for radiation areas and High Radiation Areas (HRAs) established within the Radiologically Controlled Area (RCA) of Unit 1 (U1) and Unit 2 (U2) Auxiliary Buildings, radioactive waste storage and processing areas, and the Independent Spent Fuel Storage Installation (ISFSI). The inspectors independently measured radiation dose rates or directly observed conduct of licensee radiation surveys for selected RCA areas. The inspectors reviewed and verified survey records for several plant areas including surveys for alpha emitters, airborne radioactivity, and gamma surveys with a range of dose rate gradients. The inspectors reviewed several radiation work permit (RWP) details to assess communication of radiological control requirements and current radiological conditions to workers. The inspectors reviewed selected Electronic Dosimeter (ED) dose and dose rate alarms, to verify workers properly responded to the alarms and that the licensees review of the events was appropriate. The inspectors observed jobs in radiologically risk-significant areas including HRAs and areas with, or with the potential for airborne activity.

Contamination and Radioactive Material Control: The inspectors observed the release of potentially contaminated items from the RCA and from contaminated areas. The inspectors also reviewed the procedural requirements for, and equipment used to perform, the radiation surveys for release. During plant walk downs, the inspectors evaluated radioactive material storage areas and containers, including satellite RCAs and yard areas, assessing material condition, posting/labeling, and control of materials/areas. In addition, the inspectors reviewed the sealed source inventory and verified labeling, storage conditions, and leak testing of selected sources.

Radiological Hazards Control and Work Coverage: The inspectors evaluated licensee performance in controlling worker access to radiologically significant areas and monitoring jobs in-progress during the week of the onsite inspection. The inspectors also reviewed the procedural guidance for multi and extremity badging. For HRA tasks involving significant dose rate gradients, the inspectors evaluated the use and placement of whole body and extremity dosimetry to monitor worker exposure. The inspectors reviewed RWPs for use in airborne areas, ensuring the prescribed controls were appropriate for the conditions as identified in radiological surveys and air samples.

ED alarm set points and worker stay times were evaluated against area radiation survey results for containment and auxiliary building activities.

Risk Significant High Radiation Areas and Very High Radiation Area Controls: The inspectors evaluated access barrier effectiveness for selected Locked High Radiation Area (LHRA) and Very High Radiation Area (VHRA) locations. Changes to procedural guidance for LHRA and VHRA controls were discussed with Radiation Protection (RP)supervisors. During plant walk downs of the Reactor Building, the inspectors verified the posting/locking of LHRA/VHRA areas. Established radiological controls (including airborne controls) were evaluated for selected tasks including work in auxiliary building HRAs, and radwaste processing and storage. In addition, licensee controls for areas where dose rates could change significantly as a result of plant shutdown and refueling operations were reviewed and discussed.

Radiation Worker Performance and RP Technician Proficiency: The inspectors observed radiation worker performance through direct observation. Jobs observed included maintenance and refueling activities in the containment and auxiliary buildings in high radiation and contaminated areas. The inspectors also observed health physics technicians (HPTs) providing pre-job/RWP briefings, releasing material from the RCA, and providing field coverage of jobs. Occupational workers adherence to selected RWPs and HPT proficiency in providing job coverage were evaluated through direct observations and interviews with licensee staff. ED alarm set points and worker stay times were evaluated against area radiation survey results for reviewed RWPs.

Problem Identification and Resolution: Condition Reports (CR) associated with radiological hazard assessment and control were reviewed and assessed. The inspectors evaluated the licensees ability to identify, characterize, prioritize, and resolve the identified issues in accordance with procedure NMP-GM-002, Corrective Action Program, Version 13.2 and NMP-GM-002-001, Corrective Action Program Instructions, Version 34.0. The inspectors also evaluated the scope of the licensees internal audit program and reviewed recent assessment results.

RP activities were evaluated against the requirements of Updated Final Safety Analysis Report (UFSAR) Section 12; Technical Specifications (TS) Sections 5.4 and 5.7; 10 CFR Parts 19 and 20; and approved licensee procedures. Licensee programs for monitoring materials and personnel released from the RCA were evaluated against 10 CFR Part 20 and IE Circular 81-07, Control of Radioactively Contaminated Material. The inspectors completed the required seven samples specified in IP 71124.01.

b. Findings

No findings were identified.

2RS2 As Low As Reasonably Achievable (ALARA)

a. Inspection Scope

Radiological Work Planning: The inspectors reviewed planned work activities and their collective exposure estimates for the previous Unit 1 Refueling Outage 19 (1R19) and current Unit 2 Refueling Outage 18 (R218). ALARA planning packages were reviewed for the following tasks: Scaffolding Activities, Foreign Object Search and Retrieval, Reactor Head Disassembly, Sludge Lancing and Eddy Current Testing. For the selected tasks, the inspectors reviewed established dose goals and discussed assumptions regarding the bases for the current estimates with responsible ALARA planners. The inspectors evaluated the incorporation of exposure reduction initiatives and operating experience, including historical post-job reviews, into RWP requirements.

Verification of Dose Estimates and Exposure Tracking Systems: The inspectors reviewed the collective exposure three-year rolling average from 2012 - 2014. The inspectors reviewed the historical dose data and contrasted it to the current and projected future dose values. The inspectors reviewed dose reduction activities that were being pursued in the current outage and those that are being contemplated that current plant conditions preclude implementation. Day-to-day collective dose data for the selected tasks were compared with established dose estimates and evaluated against procedural criteria (trigger points) for additional ALARA review. Where applicable, changes to established estimates were discussed with ALARA planners and evaluated against work scope changes or unanticipated elevated dose rates.

Implementation of ALARA and Radiological Work Controls: The inspectors verified that ALARA planning and work controls were effectively integrated into a sample of in-plant work activities. The inspectors observed pre-job briefs and several outage activities in order to evaluate the extent ALARA concepts are involved in radiological work. The radiological results achieved from those outage activities were compared with the intended radiological and dose outcomes.

Radiation Worker Performance Radiation: worker performance was observed and evaluated as part of IP 71124.01 and is documented in section 2RS1. While observing job tasks, the inspectors evaluated the use of remote technologies to reduce dose including teledosimetry and remote visual monitoring. The inspectors also interviewed individuals, as necessary, to assess knowledge and awareness of implemented ALARA work controls.

Problem Identification and Resolution: The inspectors reviewed and discussed selected Corrective Action Program (CAP) documents associated with ALARA program implementation. The inspectors evaluated the licensees ability to identify and resolve the issues in accordance with licensee procedure NMP-GM-002, Corrective Action Program, Ver. 13.2. The inspectors also evaluated the scope and frequency of the licensees self-assessment program and reviewed recent assessment results.

ALARA program activities were evaluated against the requirements of UFSAR Section 12, TS Section 5.4; 10 CFR Part 20; and approved licensee procedures. The inspectors completed the required five samples specified in IP 71124.02.

b. Findings

No findings were identified.

2RS3 In-Plant Airborne Radioactivity Control and Mitigation

a. Inspection Scope

Engineering Controls: The inspectors reviewed the use of temporary and permanent engineering controls to mitigate airborne radioactivity during the 2R18. The inspectors observed the use of portable air filtration units for work in contaminated areas of the RCB and reviewed filtration unit testing certificates. The inspectors evaluated the effectiveness of continuous air monitors and air samplers placed in work area breathing zones to provide indication of increasing airborne levels.

Respiratory Protection Equipment: The inspectors reviewed the use of respiratory protection devices to limit the intake of radioactive material. This included review of devices used for routine tasks and devices stored for use in emergency situations. As part of IP 71124.02, the inspectors reviewed ALARA evaluations for the use of respiratory protection devices during work in the steam generator. Selected Self-Contained Breathing Apparatus (SCBA) units and negative pressure respirators (NPR)s staged for routine and emergency use in the Main Control Room (MCR) and other locations were inspected for material condition, SCBA bottle air pressure, number of units, and number of spare masks and air bottles available. The inspectors discussed SCBA repair and maintenance with licensee staff and reviewed maintenance records for selected SCBA units for the past two years. The inspectors evaluated SCBA and NPR compliance with National Institute for Occupational Safety and Health certification requirements. The inspectors also reviewed records of air quality testing for supplied-air devices and SCBA bottles.

The inspectors discussed training for various types of respiratory protection devices with HP staff and interviewed radworkers and control room operators on use of the devices including SCBA bottle change-out and use of corrective lens inserts. Respirator qualification records (including medical qualifications) were reviewed for several MCR operators and emergency responder personnel in the Maintenance and HP departments.

Problem Identification and Resolution: NCRs associated with airborne radioactivity mitigation and respiratory protection were reviewed and assessed. The inspectors evaluated the licensees ability to identify and resolve the issues in accordance with procedures NMP-GM-002 & NMP-GM-002-001, Corrective Action Program &

Corrective Action Program Instructions. The inspectors also reviewed recent self-assessment results.

Licensee activities associated with the use of engineering controls and respiratory protection equipment were reviewed against FSAR Section 12; T.S. Section 5.4; 10 CFR Part 20; RG 8.15, Acceptable Programs for Respiratory Protection; and applicable licensee procedures. The inspectors completed the required four samples specified in IP 71124.03.

b. Findings

No findings were identified.

2RS4 Occupational Dose Assessment

a. Inspection Scope

External Dosimetry: The inspectors reviewed the licensees National Voluntary Accreditation Program (NVLAP) certification data for accreditation for the current year for Ionizing Radiation Dosimetry and discussed program guidance for storage, processing, and results for active and passive personnel dosimeters currently in use. The inspectors reviewed program procedures for processing EDs and onsite storage of Optically Stimulated Luminescent Dosimeters (OSLD)s. Comparisons between ED and OSLD results, including correction factors, were discussed in detail. Licensee procedures for shallow and deep dose assessments for workers with identified skin contaminations were reviewed and discussed. In addition, inspectors evaluated the use of extremity dosimetry, multi-badging, and re-positioning of whole body dosimetry during R18 activities. The inspectors also reviewed dosimetry occurrence reports regarding alarming dosimeters.

Internal Dosimetry: Program guidance (including Derived Air Concentration (DAC)-hr tracking), instrument detection capabilities, and assessment results for internally deposited radionuclides were reviewed in detail. There were no internal dose assessments for internal exposure greater than 10 millirem committed effective dose equivalent to review. The inspectors reviewed selected routine in vivo (Whole Body Count) analyses from April 2014 to February 2016. In addition, capabilities for collection and analysis of special bioassay samples were evaluated and discussed with licensee staff.

Special Dosimetric Situations: The inspectors reviewed records for declared pregnant workers (DPW)s from April 2014 through February 2016 and discussed guidance for monitoring and instructing DPWs. The inspectors evaluated the licensees use of multi-badging, extremity dosimetry, and dosimeter relocation within non-uniform dose rate fields and discussed worker monitoring in neutron areas with licensee staff. The inspectors also reviewed the licensees use of Effective Dose Equivalent from External Exposure (EDEX) to calculate total effective dose equivalent (TEDE) for individuals performing steam generator work for the past two refueling outages. In addition, the inspectors reviewed shallow dose assessments for selected Personnel Contamination Events (PCEs) occurring between April 2014 and February 2016 were reviewed and discussed.

Problem Identification and Resolution: The inspectors reviewed and discussed selected CAP documents associated with occupational dose assessment. The inspectors evaluated the licensees ability to identify and resolve the identified issues in accordance with procedures NMP-GM-002 & NMP-GM-002-001, Corrective Action Program &

Corrective Action Program Instructions. The inspectors also discussed the scope of the licensees internal audit program and reviewed recent assessment results.

Occupational dose assessment program activities were evaluated against the requirements of FSAR Section 12; TS Sections 5.4, Procedures; 10 CFR Parts 19 and 20; RG 8.40, Methods for Measuring Effective Dose Equivalent from External Exposure; and approved licensee procedures. The inspectors completed the required five samples specified in IP 71124.04.

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a. Inspection Scope

The inspectors reviewed a sample of the performance indicator (PI) data, submitted by the licensee, for the Unit 1 and Unit 2 PIs listed below. The inspectors reviewed plant records compiled between January 2015 and December 2015 to verify the accuracy and completeness of the data reported for the station. The inspectors verified that the PI data complied with guidance contained in Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, and licensee procedures. The inspectors verified the accuracy of reported data that were used to calculate the value of each PI.

In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with PI data.

Cornerstone: Initiating Events

  • unplanned scrams per 7,000 critical hours
  • Occupational Exposure Control Effectiveness The inspectors reviewed the PI results from February 2015 through February 2016. The inspectors reviewed ED alarm logs and selected CRs related to controls for exposure significant areas. The inspectors also reviewed licensee procedural guidance for collecting and documenting PI data.

Public Radiation Safety Cornerstone

  • Radiological Control Effluent Release Occurrences The inspectors reviewed the PI results from February 2015 through February 2016. The inspectors reviewed cumulative and projected doses to the public contained in liquid and gaseous release permits and CRs related to Radiological Effluent Technical Specifications/ODCM issues.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review

The inspectors screened items entered into the licensees corrective action program in order to identify repetitive equipment failures or specific human performance issues for follow-up. The inspectors reviewed condition reports, attended screening meetings, or accessed the licensees computerized corrective action database.

.2 Annual Follow-up of Selected Issues

a. Inspection Scope

The inspectors conducted a detailed review of corrective action report (CAR) 262037, Oil Leak on Unit 1 Turbine-Driven Auxiliary Feedwater Pump Bearing sight glass. The inspectors evaluated the following attributes:

  • complete and accurate identification of the problem in a timely manner
  • evaluation and disposition of operability and reportability issues
  • consideration of extent of condition, generic implications, common cause, and previous occurrences
  • classification and prioritization of the problem
  • identification of root and contributing causes of the problem
  • identification of any additional condition reports
  • completion of corrective actions in a timely manner

b. Findings

No findings were identified.

4OA6 Meetings, Including Exit

On April 25, 2016, the resident inspectors presented the inspection results to Mr. Keith Taber and other members of the licensees staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection period.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

J. August Steam Generator Programs

T. Baker, Security Manager

C. Blackburn Engineering Programs

J. Carswell, SNC Corporate RP

J. Churchwell Engineering Programs

R. Collins, Chemistry Manager
J. Dixon, RPM
G. Gunn, Licensing Manager (interim)
M. Johnson, Health Physics Manager

K. Morrow Licensing Engineer

D. Myers, Plant Manager
C. Nesbitt, Training Manager
F. Pournia, Engineering Director
J. Robinson, Engineering Programs Manager

J. Santana Engineering Programs

G. Saxon, Plant Manager

T. Smith Engineering Programs

K. Taber, Site Vice-President
J. Thomas, Work Management Director
D. Thompson, RP Radwaste
T. Thompson, Systems Engineering Manager
K. Walden, Licensing Engineer

NRC personnel

Shane Sandal, Chief, Region II Reactor Projects Branch 2

LIST OF DOCUMENTS REVIEWED