|
---|
Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20196H0111997-07-11011 July 1997 Special Rept 97-001:on 970620,removed High Range Radioactive Noble Gas Effluent Monitor (Stack Ragems) from Service to Allow Secondary Calibr IAW Master Surveillance Schedule. Completed Calibr on 970628 & Returned Stack Ragems to Svc ML20129A3401996-10-15015 October 1996 Special Rept 96-001,rev 1:on 960806,stack Ragems High Range Monitor Was Removed from Svc & Not Restored to Svc in Seven Days.Caused by Malfunction of Interlock on Source. Interlock Components Replaced ML20117K5931996-09-0505 September 1996 Special Rept SR 96-001:on 960806,declared Stack Ragems High Range Monitor Inoperable.Caused by Difficulties Requiring Component Replacement.Developed Course of Action for Returning Stack Ragems Instrument ML20116B7521992-10-27027 October 1992 Special Rept 92-08:on 920929,Turbine Building High Radiation Noble Gas Monitor Declared Inoperable for Greater than Seven Days.Alternate Testing Performed Throughout Period of Inoperability ML20115G6461992-10-22022 October 1992 Special Rept 92-07:on 921015,determined That Stem & Disc Separated on Discharge Valve V-9-004 for Diesel Fire Pump P-9-102A.On 921021,fire Pumps Isolated.Redundant Fire Pump Secured & Valves Replaced ML20105A5121992-09-10010 September 1992 Special Rept 92-06:on 920807,fire Diesel Pump 1 Declared Inoperable for More than 7 Days to Perform Preventive Maint.On 920811,diesel Engine Overheated.Solenoid Valve Replaced & New Cooling Water Strainers Installed ML20104B6081992-09-10010 September 1992 Special Rept 92-05:on 920727,condenser Bay Sprinkler Sys 2 Removed from Svc After Spurious Actuation of Sprinkler Head. Hourly Fire Watch Established While Sys Out of Svc.Sprinkler Head Replaced & Sys Returned to Svc on 920814 ML20114C5191992-08-26026 August 1992 Special Rept 92-03:on 920705,electromatic Relief Valve C Inadvertently Opened While Testing Pressure Switch of Valve A.Caused by Personnel Error.Training Session Will Be Held & Engineering Work Request Submitted Re Switch Terminal Point ML20114A9701992-08-17017 August 1992 Special Rept 92-04:on 920724,fire Diesel Pump 2 Removed from Svc to Replace Battery Cables & Solenoid Valve.Correct 24 Volt Dc Coil Obtained from Mfg & Pump Returned to Svc on 920806 ML20096D4711992-05-0101 May 1992 Special Rept 92-02:on 920327,fire Diesel Pump 1 Out of Svc for More than 7 Days to Replace Pump Due to Marginal Discharge Pressure.Caused by Valve Seating Problem.Pump Replacement Expected to Be Completed by 920504 ML20100R7411992-04-10010 April 1992 Special Rept 92-01:on 920227,CO2 Fire Suppression Sys for 4,160-volt Switchgear Inoperable for More than 14 Days When Leaking Valve Stem Repaired on 920226.Possibly Caused by Moisture Intrusion.Corroded Components Replaced ML20087B8431992-01-0303 January 1992 Special Rept 91-09:on 911115,fire Diesel Pump 1-2 Failed to Meet Required Acceptance Criteria During Functional Test. Caused by Cloth Rag Becoming Lodged Inside Pump.Fire Diesel Pump 1-2 Rebuilt & Reinstalled on 911208 ML20076E2641991-08-13013 August 1991 Special Rept 91-08:on 910717,coolant Found Leaking from Cap on Heat Exchanger of Engine of Fire Diesel Pump 1-1.Caused by Wearing on HX Neck,Resulting in HX Failing to Hold Normal Pressure.Engine Secured & Work Request Initiated ML20076E3001991-08-12012 August 1991 Special Rept 91-07:on 910709,nonfunctional Fire Barrier Doors Between Fire Zones OB-FA-6 & TZ-FZ-11B Not Restored to Operable Status within 7 Days.Caused by Ventilation Flow Preventing Door from Closing.Fire Patrol Established ML20077K2271991-07-31031 July 1991 Special Rept 91-06 Re Nonfunctional Fire Barrier Door Not Repaired within 7 Days as Required by Tech Spec 3.12.E. Caused by Broken Door Closure Mechanism.Hourly Fire Watch Initiated.Door Mechanism Repaired on 910704 ML20082E1411991-07-23023 July 1991 Special Rept:On 910702,non-functional Fire Barrier Door Not Repaired within Seven Days as Required by Tech Specs. Caused by Faulty Door Closing Mechanisms.Util Evaluating Alternate Door Closing Mechanisms ML20073C9381991-04-18018 April 1991 Special Rept 91-04:on 910309,fire Detection Sys on Elevations 75' & 95' of Reactor Bldg Made Inoperable to Facilitate Maint Activities.Fire Watch Patrol Has Been Established to Compensate for Detection Sys ML20070T5341991-03-28028 March 1991 Special Rept:On 910222,inoperable Fire Hose Station 33 Not Restored to Operable Status within 14 Days as Required by Tech Specs.Caused by Maint to Angle Valve.Valve Reopened on 910312,restoring Hose Station 33 to Operability ML20070M5181991-03-14014 March 1991 Special Rept 91-02:on 901117,discovered That Fire Barrier Door Between 480-volt Switchgear Rooms a & B Nonfunctional Since 901110 & Not Repaired within 7 Days.Caused by Faulty Door Latching Mechanism.Fire Watch Established ML20058A7441990-10-16016 October 1990 Special Rept 90-04:on 900921,nonfunctional Fire Barrier Door Not Repaired within 7 Days.Fire Watch Established ML20245E7541989-06-0909 June 1989 Special Rept 89-02:on 890526,declared Fire Pump/Diesels 1-1 & 1-2 Inoperable.Caused by Loss of Fire Suppression Water. Pressure Switch & Associated Recorder for 1-2 Diesel Recalibrated Along W/Pump Discharge Pressure Gauge ML20247J2081989-05-22022 May 1989 Special Rept 89-01:on 890422,nonfunctional Fire Barrier Not Repaired within 7 Days as Required by Tech Spec 3.12.E. Fire Watch Established.Nonfunctional Fire Barrier Seal Plannned to Be Restored to Operable Status by 890523 ML20237C6711987-12-11011 December 1987 Special Rept 87-08:on 871112,fire Diesel Pump 1-2 Not Restored to Functional Status within 7 Days.Caused by Constraints Imposed by Increased outage-related Maint Activities.Fire Diesel Pump Restored to Functional Status ML20236S5201987-11-19019 November 1987 Special Rept 87-07:on 871020,nonfunctional Thermo Lag Fire Barrier Not Restored to Functional Status within 7 Days Per Tech Spec 3.12.E.Caused by Constraints Imposed by Increased Maint Activities.Fire Watch Established ML20236L3711987-10-29029 October 1987 Special Rept 87-06:on 870928-30,fire Barrier Penetration Seals Identified as Not Meeting Acceptance Criteria.Cause Not Stated.Fire Watch Established Immediately.Fire Barrier Seals Will Be Restored to Functional Status by 871030 ML20235B4411987-09-22022 September 1987 Ro:On 870811,spill of Reactor Bldg Closed Cooling Water Occurred.Caused by Failure to Follow Instructions on Switching & Tagging Request Form Re Valve Backseating. Procedures Will Be Revised & Training Provided ML20235G2151987-09-20020 September 1987 Ro:On 870911,w/reactor in Cold Shutdown Mode,Tech Spec Safety Limit 2.1.E Exceeded.Caused by Operator Error. Operators Received Training on Safety Limit,Applicable Procedures & Relevant Control Room Indications ML20214H9801987-05-0707 May 1987 Ro:On 870424,operator Personnel Blocked Open Two Torus to Drywell Vacuum Breaker Valves at Time When Primary Containment Integrity Was Required.Caused by Cognitive Personnel Error.Procedures Revised ML20215H3621987-04-0909 April 1987 Special Rept 87-02:on 870214,turbine Trip & Reactor Scram Occurred.Caused by Loose Wire Causing Loss of Feedwater Flow Signal.Following Reduction in Reactor Pressure All Electromatic Relief Valves Reseated Properly ML20206E3931987-04-0101 April 1987 Special Rept 87-01:on 870302,inoperable Fire Suppression Water Deluge Sys Not Restored to Functional Status within 14 Days from Time of Discovery.Caused by Long Lead Time for Procurement of Replacement Parts ML20209H2501987-01-23023 January 1987 Special Rept 86-017:on 861228,nonfunctional Fire Barrier Not Returned to Functional Status within 7 Days from Discovery.Hourly Fire Watch Established.Repairs Completed & Penetration Seal Restored to Functional Status on 870112 ML20207J2981986-12-17017 December 1986 Special Rept 86-16:on 861121,fire Barrier Door Between Monitor & Control Area Stairwell & Hallway Outside Cable Spreading Room Found Nonfunctional.Hourly Fire Watch Patrol Established.Door to Be Restored as Functional on 861222 ML20207J2821986-12-16016 December 1986 Special Rept 86-15:on 861110,penetrations Through Floor of 4160 Volt Switchgear 1D Vault & Floor of Motor Generator Set Room Found Degraded.As of 861117,penetrations Not Restored to Functional Condition.Hourly Fire Watch Patrol Initiated ML20197B1471986-10-0909 October 1986 Special Rept 86-14:on 860922 & 27,nonfunctional Fire Barrier Penetration Seals Not Restored to Functional Status within 7 Days.Hourly Fire Watch Patrol Established within 1 H. Restoration Expected by 861130 ML20212D6251986-07-10010 July 1986 Special Rept 86-03:on 860616,two Hangers Supporting Ofc Bldg Fire Water Supply Riser Found to Need Repair.Riser Consequently Isolated,Rendering Sprinkler Sys 4 & 12 & Deluge Sys 4 Inoperable.Hangers Repaired & Sys Restored ML20137U7031986-01-20020 January 1986 Fire Protection Special Rept 85-03:on 851216,insp of 14 Fire Dampers Identified Design or Installation Deficiencies Resulting in Dampers Being Determined Inoperable.Caused by Nonconforming as-found Fire Damper Configuration ML20117C7451985-04-25025 April 1985 Special Rept 85-02:on 850225,electromatic Relief Valves NR-108B,NR-108C & NR-108D Failed to Fully Reseat After Initial Actuation,Per Tech Spec 6.9.3.f.Caused by Valve Design Deficiency.Design Change Considered ML20102B8671985-02-21021 February 1985 Special Rept 85-01:on 850207,leakage Observed Around post-indication Valve V-9-13.Fire Suppression Water Sys Isolated on 850211 to Facilitate Valve Repair.Caused by Crack in Valve Body.Valve Replaced ML20092N6351984-06-15015 June 1984 Special Rept 84-01:on 840606,post-indicating Valve V-9-12 Branching Off 14-inch Fire Water Main Damaged by Maint Vehicle,Resulting in Loss of Fire Suppression Water Sys. Caused by Lack of Protection Against Physical Damage ML20083C6451983-12-0808 December 1983 RO 83-02T:on 831119,w/fire Pump 1-1 Out of Svc,Fire Pump 1-2 Failed to Start on Low Sys Pressure.Caused by Impeller Wear Rings Out of Tolerance on High End of Clearance Limits. Overspeed Trip Reset ML20082R6551983-11-21021 November 1983 RO 83-02:on 831119,fire Pump 1-2 Failed to Start on Low Sys Pressure During Demand for Fire Water to Fill Isolated Portion of Underground Fire Suppression Pool.Caused Suspected to Be Faulty Overspeed Trip Switch.Switch Tested ML20082L1491983-11-18018 November 1983 Followup RO 83-01:on 831103,fire Suppression Water Sys Declared Inoperable After Pump 1-1 Failed Testing.Mod Underway to Install New Pressure Relief Valves on Both Fire Pumps ML20082B7921983-11-0404 November 1983 RO 83-01:on 831103,fire Suppression Water Sys Declared Inoperable Due to Smoke Emitting from Under Fire Pump 1-2 Pumphead During post-maint Inservice Test & Failed Design Rated Curve for Pump 1-1.Caused by Misadjusted Impeller ML20082L5721983-09-15015 September 1983 Advises That Followup to RO 83-17 Re Diesel Generator Fast Start Surveillance Will Be Forwarded by 830921 ML20073A7071983-03-23023 March 1983 RO 83-4:on 830211,during Controlled Reactor Shutdown,One Dilution Pump Remained in Svc When Intake Canal Water Below Tech Spec Limit.Caused by Personnel Error.Procedures Will Be Revised to Provide More Explicit Directions ML20071B0911983-02-14014 February 1983 RO 83-1-1:on 830113,dilution Pump 1-2 Removed from Svc. Caused by Insufficient Seal Water flow.Long-term Corrective Action Includes Program Designed to Improve Pump Reliability ML20071B0951983-02-14014 February 1983 RO 83-2-1:on 830118,dilution Pump 1-1 Removed from Svc Due to Steam Around Flax Packing Gland.Caused by Wearing in of New packing.Long-term Corrective Actions Include Upgrading Dilution Pump Seal ML20071B1021983-02-14014 February 1983 RO 83-3-1:on 830123,dilution Pumps 1-2 & 1-3 Tripped Off. Caused by Failed Electrical Terminations (Stress Cones). Terminations Replaced ML20070P8361983-01-11011 January 1983 RO 82-8-2:on 821205,dilution Pump 1-3 Tripped,Leaving Dilution Pump 1-2 in Operation.Seal Water Pump Failed & Ambient Water Temp Fell Below Tech Spec Limit.Cause Unknown. Total Dilution Pump Refurbishment Program Initiated ML20064E7271982-12-21021 December 1982 RO 82-7:on 821201,dilution Pump 1-3 Removed from Svc.Caused by Mud & Debris Clogging Grates,Blocking Water Flow to Dilution Pump.Mud & Debris Removed.Total Dilution Pump Refurbishment Program Planned 1997-07-11
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4451999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Oyster Creek Nuclear Generating Station.With ML20211P6731999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Oyster Creek Nuclear Generating Station.With ML20211A7051999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Oyster Creek Nuclear Station.With ML20209G0631999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Oyster Creek Nuclear Generating Station.With ML20212H5491999-06-18018 June 1999 Non-proprietary Rev 4 to HI-981983, Licensing Rept for Storage Capacity Expansion of Oyster Creek Spent Fuel Pool ML20195E7961999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Oyster Creek Nuclear Generating Station.With ML20206N7431999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Oyster Creek Nuclear Generating Station.With ML20205P5401999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Oyster Creek Nuclear Generating Station.With ML20204C8201999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Oyster Creek Nuclear Generating Station.With ML20199E4671998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Oyster Creek Nuclear Generating Station.With ML20195E8321998-12-31031 December 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Sys & Procedures, for Period of June 1997 to Dec 1998.With ML20198D2091998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Oyster Creek Nuclear Generating Station.With ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20155J3021998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Oyster Creek Nuclear Generating Station.With ML20154R4981998-10-20020 October 1998 Core Spray Sys Insp Program - 17R ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20154Q3371998-09-30030 September 1998 Rev 8 to Oyster Creek Cycle 17,COLR ML20154L5571998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Oyster Creek Nuclear Generating Station.With ML20151V6311998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Oyster Creek Nuclear Generating Station.With ML20237D5691998-08-31031 August 1998 Rev 0 to MPR-1957, Design Submittal for Oyster Creek Core Plate Wedge Modification ML20237D5711998-08-18018 August 1998 Rev 0 to SE-000222-002, Core Plate Wedge Installation ML20237B0131998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Oyster Creek Nuclear Generating Station ML20236R0511998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Oyster Creek Nuclear Generating Station ML20249B2981998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Oyster Creek Nuclear Station ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20247F1891998-05-0505 May 1998 Risk Evaluation of Post-LOCA Containment Overpressure Request ML20247G0581998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Oyster Creek Nuclear Generating Station ML20216K0341998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Oyster Creek Nuclear Generating Station ML20151Y4651998-03-31031 March 1998 Non-proprietary Version of Rev 1 to GENE-E21-00143, ECCS Suction Strainer Hydraulic Sizing Rept ML20217A4631998-03-23023 March 1998 Safety Evaluation Accepting Use of Three Heats/Lots of Hot Rolled XM-19 Matl in Core Shroud Repair Assemblies Re Licenses DPR-16 & DPR-59,respectively ML20212E2291998-03-0404 March 1998 Rev 11 to 1000-PLN-7200,01, Gpu Nuclear Operational QAP, Consisting of Revised Pages & Pages for Which Pagination Affected ML20216J0841998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Oyster Creek Nuclear Generating Station ML20203B2781998-02-16016 February 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Systems & Procedures ML20203A3801998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Oyster Creek Nuclear Generation Station ML20198P1791997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Oyster Creek Nuclear Station ML20217C7591997-12-31031 December 1997 1997 Annual Environmental Operating Rept for Oyster Creek Nuclear Generating Station ML20197E9131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Oyster Creek Nuclear Station ML20199E4561997-11-13013 November 1997 Safety Evaluation Accepting Ampacity Derating Analysis in Response to NRC RAI Re GL-92-08, Thermo-Lag 330-1 Fire Barriers, for Plant ML20199D4381997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Oyster Creek Nuclear Station ML20202E8511997-10-21021 October 1997 Rev 0 to Scenario 47, Gpu Nuclear Oyster Creek Nuclear Generating Station Emergency Preparedness (Nrc/Fema Evaluated) 1997 Biennial Exercise. Pages 49 & 59 of Incoming Submittal Were Not Included ML20211M9481997-10-0303 October 1997 Supplemental Part 21 Rept Re Condition Effected Emergency Svc Water Pumps Supplied by Bw/Ip Intl Inc to Gpu Nuclear, Oyster Creek Nuclear Generation Station.No Other Nuclear Generating Stations Effected by Notification ML20198J7361997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Oyster Creek Nuclear Generating Station ML20211B7461997-09-24024 September 1997 Part 21 Rept Re Failure of Emergency Service Water Pump Due to Threaded Flange Attaching Column to Top Series Case Failure.Caused by Dissimilar Metals.Pumps in High Ion Svc Will Be Upgraded to 316 Stainless Steel Matl ML20210V0181997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Oyster Creek Nuclear Generating Station ML20210L2961997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Oyster Creek Nuclear Station ML20149F9961997-07-18018 July 1997 Safety Evaluation Re Gpu Nuclear Operational Quality Assurance Plan,Rev 10 for Three Mile Island Nuclear Generating Station,Unit 1 & Oyster Creek Nuclear Generating Station ML20196H0111997-07-11011 July 1997 Special Rept 97-001:on 970620,removed High Range Radioactive Noble Gas Effluent Monitor (Stack Ragems) from Service to Allow Secondary Calibr IAW Master Surveillance Schedule. Completed Calibr on 970628 & Returned Stack Ragems to Svc ML20210L3081997-06-30030 June 1997 Corrected Page to MOR for June 1997 for Oyster Creek Nuclear Generating Station ML20141H2051997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Oyster Creek Nuclear Station 1999-09-30
[Table view] |
Text
n. - _
I
?
GPU Nuclear Corporation -l Nuclear ::=:;388 Forked River, New Jersey 08731-0388 609 971-4000 Writer's Direct Dial Number:
Document Control Desk september 22, 1987 U.S. Nuclear Regulatory Commission Washington, DC 20555 l
Dear Sir:
Subject:
Oyster Creek Nuclear Generating Station Docket No. 50-219 Spill of Reactor Building Closed Cooling Water during Maintenance On September 11, 1987, a safety limit violation occurred at the Oyster Creek Nuclear Generating Station. An analysis of that event and GPUN's corrective action was contained in our submittal dated September 20, 1987. That letter stated that a detailed review of the maintenance activities leading to that violation would be submitted via a separate submittal. Attachment I to this letter provides the results of that review.
If any further information is required, please contact Mr. John Rogers of my staff at (609) 971 -4893.
VMtrul _
p y P te B. Fiedler V President and Director er Creek PBF/JR/dmd Attachment (0645Q) cc: Mr. William T. Russell, Administrator Mr. Lee H. Bettenhausen Region I Chief, Projects Branch No. I U.S. Nuclear Regulatory Commission US NRC 631 Park Avenue Region I King of Prussia, PA 19406 631 Park Avenue King of Prussia, PA 19406 Mr. Alexander W. Dromerick, Project Manager U.S. Nuclear Regulatory Commission Dr. Thomas E. Murley, Director Division of Reactor Projects I/II Division of Nuclear Reactor Reg.
7920 Norfolk Avenue, Phillips Bldg. US NRC Betheda, MD 20014 Washington, DC 20555 NRC Resident Inspector Oyster Creek Nuclear Generating Station 8709240105 9709g2 PDR ADOCK 05000219' S PDR GPU Nuclear Corporation is a subsidiary of the General Pubhc Utihties Corporation gh
ATTACHMENT I Title of Event:
Spill of Reactor Building Closed Cooling water containing very low levels of contamination while repacking the stem of an isolation valve in the Reactor Building Closed Cooling Water System.
Brief Description of the Event At about 0208 on September 11, 1987, a leak occurred while a mechanic from the Plant's Maintenance Department was.in the process of removing the packing from Reactor Building Closed Cooling Water (RBCCW) drywell isolation valve V-5-167. The mechanic directed the flow of water into a catch bag but the bag started to overflow and he called for help. A radiological control technician, who was stationed nearby, heard.the call for help and noticed that water was spraying down from the overhead. After checking the status of the person who was calling for help and confirming that he (the mechanic) was uninjured, the radiological control technician immediately notified the control room of the spill and requested their assistance. The mechanic who had been sprayed with water had come down from the scaffold platform and was waiting for further instructions. The Group Operating Supervisor (G0S) was immediately dispatched to the Reactor Building 23' elevation to investigate the source of the leak.
The G0S reported to the Control Room that it appeared a rupture of RBCCW piping had occurred and recommended that they isolate cooling water flow to the drywell. The RBCCW system was providing cooling water to the Drywell Equipment Drain Tank, the operating drywell recirculating fans, and the operating reactor recirculation pumps (B&C). The control room operator secured the operating reactor recirculation pumps in preparation for securing RBCCW flow to the drywell. (For discussion on the related safety limit violation, see GPUN letter, P.R. Clark to Dr. Murley dated September 20, 1987)
A few minutes later, the GOS was informed by the control room that the reactor recirculation pumps had been secured and that RBCCW flow to the drywell could be isolated. The G0S directed a nearby equipment operator to go to the reactor building 51' elevation and shut the manually operated RBCCW drywell isolation valve V-5-709. The GOS instructed the control room operator to close the motor operated drywell isolation valve (V-5-166) which is located inside the drywell. These valves were shut. The leak rate was reduced but not completely stopped. The GOS determined that the leak was from the packing on V-5-167.
About this time, the Maintenance, Construction, and Facilities (MCF) Area Supervisor arrived at the spill scene. He knew that an RBCCW valve was being repacked on the 23' elevation and thought that the spill was a result of this work. He discussed the position of the valve with the GOS and was informed that the valve had been electrically backseated. The MCF Area Supervisor thought that the leakage was too excessive for the valve to be on its backseat. The MCF area supervisor thought it would take too much time to get an electrician to verify the valve was on its backseat. He requested permission to try to manually backseat the valve. An MCF management representative, the MCF Area Supervisor, and the G0S discussed the situation
, and developed a plan by which the MCF Area Supervisor could attempt to manually backseat the valve in an attempt to isolate the leak. The MCF area
- supervisor then checked with the radiological control personnel who were in the area and was directed to don appropriate waterproof protective clothing prior to entering the area. The MCF Area Supervisor suited up and entered the area to backseat the valve. He opened the valve one additional turn of the manual handwheel onto its backseat at which point the leak stopped.
The area was immediately secured and appropriate spill response actions were taken. Both the mechanic and the MCF Area Supervisor had been sprayed with water. The MCF Area Supervisor was determined to be uncontaminated and was released from the area. Radiological control personnel determined that the mechanic's clothing was contaminated and had him undress. The mechanic was then released from the area and subsequently given a whole body count as a precautionary measure. The RBCCW system uses a corrosion inhibitor. The mechanic required some minor first aid later in the morning as the solution had caused some minor irritation to his right eye. The spill recovery actions were closely supervised by the plant's safety department.
Plant Conditions Prior to the Event The reactor was shutdown with the Mode Selector Switch locked in the Shutdown position. Reactor water temperature was 140*F and the reactor was vented.
Reactor water level was approximately 156 inches above the Top of the Active Fuel (TAF). Condensate pump "C" was operating, providing water to the reactor as necessary, and Shutdown Cooling Pumps A and B were in service. Reactor recirculation pumps B and C were in operation.
The RBCCW system was operating with A and B pumps providing 82 psig of pressure. RBCCW water temperature was 89'F. A sample of RBCCW system water taken 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> after the event contained 5.4 x 10-4 uci/ml of activity, pH was 10.19, i
l l
Actions Leading to the Event On 8-6-87, Plant Engineering initiated Maintenance Short Form No. 46069 to repack V-5-167 with live loaded packing in accordance with Procedure 700.1.030. The valve was required to be repacked to correct the root cause of a previous surveillance test failure.
A work package was developed by the MCF planning section. The maintenance supervisor assigned to the job reviewed the work package. He submitted a Switching and Tagging Request on 9-10-87 which requested that the valve be isolated and the system depressurized. This condition was specified on the tagging request as it was a prerequisite in the referenced repacking procedure.
At approximately 10:00 AM the Group Shift Supervisor (GSS) advised the maintenance supervisor that the valve could not be isolated and that the tagging request would have to be revised to repack the valve on its backseat.
The maintenance supervisor did not believe that the repacking procedure permitted repacking the valve on its backseat and advised his management. MCF management contacted Plant Engineering to determine if the valve had a backseat (it did) and question the intent of the procedure. Plant Engineering stated that the procedure was not written to repack valves on their backseat because of the uncertainty involved with isolating the stuffing box using the backseat, but it was " technically possible" to repack the valve on its '
backseat. This was construed by MCF management to mean that it was permissible to repack this valve on its backseat.
A subsequent discussion held between Plant Engineering and the MCF Job Planner identified that a procedure revision to include additional precautions and instructions should be issued to the repacking procedure to specifically permit repacking a valve on its backseat. This procedure revision was not initiated.
The switching and tagging request was revised and resubmitted on the same day (9/10/87) at approximately 1:30 p.m. specifying that the valve was to be placed on its backseat and tagged out. The GSS attempted to place the valve on its backseat using the normal control switch by giving it an additional opening signal. (This did not result in any valve motion.) The GSS incorrectly thought that a second opening signal would bypass the limit switch and the valve would "go out on its torque switch" against the backseat. The maintenance supervisor was in the control room during this evolution and was advised by the GSS that the valve was just on or very close to its backseat.
The maintenance supervisor was cautioned by the GSS to look for leakage and if excessive leakage were noted, an operator would further backseat the valve manually. The Maintenance Supervisor questioned why there wasn't an isolation boundary tag on the hand wheel. The GSS told him that this way the valve could be manually backseated if required. The GSS was very concerned about backseating the valve as previous valve failures were attributable to improper backseating techniques. Further, he preferred electrically backseating valves to manually backseating valves, because he thought that a valve backseated
backseated electrically would be protected by a torque switch. The preference to electrically backseat, vice manually backseat, was based on information presented in the operator tr aining program. No approved station procedure or method was used to backseat this valve.
Maintenance personnel were prepared to repack the valve on the 4 - 12 shift but could not because the new packing follower required machining. The repacking was subsequently started on the 12 midnight to 8:00 a.m. shift on 9/11/87. The turnover between operating shifts and maintenance shif ts stated that the valve was electrically backseated. The mechanic performing the repacking was concerned that the valve might not be backseated and reviewed the copy of the switching and tagging request. He concluded that the valve was backseated based on the switching and tagging request. The mechanic proceeded to remove the packing from the valve one ring at a time. No leakage was observed until the fif th of 8 rings was in the process of being removed, when the remaining packing blew out, causing an RBCCW 1eak, of approximately 20 to 25 gallons per minute.
Consequences of the Event
- 1. Areas Contaminated:
The east side section of the reactor building on the 23' elevation had been sprayed with water. It was subsequently secured and posted. During the spill, the water had been substantially contained by diking the area with clean, unused protective clothing. After the leak was stopped, the water was pumped to a nearby floor drain.
Surveys of the spill residual showed contamination which was not evident on readings of the RBCCW water. Apparently, the water flow had flushed over pipes and conduits on its way to the floor. The area has been cleaned up and decontaminated, l
- 2. Personnel Contaminated: j The mechanic was not contaminated, but his clothing was contaminated. He frisked out clean (less than 100 cpm) when he was !
unclothed and was released by the Radiological Control Department. J The mechanic was given a whole body count as he had been drenched and possibly ingested some liquid. His whole body count, while unclothed, read only normal levels of potassium 40.
The MCF area supervisor was not contaminated. As a result of wearing the waterproof suit the MCF area supervisor frisked out clean (less than 100 cpm). The MCF area supervisor was subsequently given a precautionary whole body count on 9/15/87. His whole body count read only normal levels of potassium 40.
l
- 3. Personnel Injured:
The mechanic came into physical contact with the RBCCW water and was instructed by the Safety and Health Engineer to shower for 15 minutes. He stated that some of this RBCCW water got into his eye.
He was instructed to flush his eye while showering. As a precautionary measure later in the morning, the mechanic was directed to report to the company doctor for an examination and any necessary treatment. His right eye had drops instilled prophylactically and he was released by the medical department.
The MCF area supervisor did not require any medical attention.
Cause of the Event Root Cause The root cause of this event was failing to properly execute the specified instructions on the switching and tagging request form by the operations department personnel.
Contributing Causes
- 1. Station administrative procedures are not clear in assigning responsibilities for Operations and Maintenance. The specific maintenance procedures used for this event were insufficient to perform the maintenance evolution as planned.
The operations and maintenance personnel involved either were not aware of the procedural limitations or did not address the inadequacies (e.g., issue a temporary change to the procedure) prior to implementation of the maintenance effort.
- 2. The operators did not comply with specific details of procedures controlling plant equipment, specifically as they relate to switching and tagging. Plant maintenance did not comply with procedural requirements to verify the safety and adequacy of the pressure boundaries established for this maintenance activity. Additionally, communication was noted to be weak during shift or personnel turnovers.
1
- 3. Training on Valve Motor Operators was misleading and incomplete in l some respects. Although the information presented was generally accurate, the emphasis placed on certain valve operator characteristics and the omission of the motor operator control l circuit opening logic contributed to the incorrect decisions reached by the GSS.
I 1
l l
Corrective Action The following corrective actions will be taken prior to restart:
- 1. Procedures for the operations / maintenance interface will be revised to more clearly assign responsibilities. Operators and maintenance personnel will have these responsibilities emphasized to them as part of a training session.
- 2. Operations and maintenance management will stress the importance of procedural compliance to their personnel. Training will be provided on switching and tagging requirements and approved valve backseating techniques to appropriate personnel. Additionally, maintenance management will issue a policy providing guidance to maintenance supervisors on proper job turnovers during shift changes.
- 3. Detailed information relating to control logic of the valve motor operator and a copy of the critique of this event will be placed in the required reading programs for appropriate personnel.
The following corrective actions will be completed prior to December 31, 1987:
- 1. Specific procedures relating to backseating and unbackseating of valves will be combined into a single procedure under the control of the Operations department. The maintenance procedure which was applicable to repacking the valve during this event, will be revised to identify prerequisites, precautions, and limitations which will allow safely repacking this valve on its backseat.
- 2. Maintenance department will issue a procedure to formalize its policy on proper job turnover during maintenance.
- 3. Formal training will be provided to appropriate personnel on specific details of valve motor opertor control logic.
- 4. A Management Oversight and Risk Tree (MORT) analysis will be performed on this event to ensure that no additional attributing causes were omitted.
1
__