ML20210V018

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Monthly Operating Rept for Aug 1997 for Oyster Creek Nuclear Generating Station
ML20210V018
Person / Time
Site: Oyster Creek
Issue date: 08/31/1997
From: Nash R, Roche M
GENERAL PUBLIC UTILITIES CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
6730-97-2233, NUDOCS 9709220221
Download: ML20210V018 (3)


Text

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GPU Nuclear ine.

g U S. Route #9 south NUCLEAR  ;,*l',*$,l u"ls*m mes Tel 609 9714000 September 15, 1997 6730-97-2233 U. S, Nuclear Regulatory Commission Attention: Document Control Desk Washington, DC 20555

Dear Sir:

SUBJECT:

Oyster Creek Nuclear Generating Station Docket No. 50-219 Monthly Operating Report - August,1997 Enclosed are two copies of the August,1997 Monthly Operating Report for Oyster Creek Nuclear Station. The content and format ofinformation submitted in this report is in accordance with the guidance provided by Generic Letter 97-02.

If you should have any questions, please contact Ms. Brenda DeMerchant, Oyster Creek Regulatory AtTairs Engineer, at 609-971-4692.

Very truly yours, c

g Michael B. Roche Vice President & Director Oyster Creek MBR/DDeM/gl Enclosures \

cc: Administrator, Region I (2 copies)

NRC Project Manager NRC Sr. Resident inspector E

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APPENDlX A Operating Datalspm1 Docket Nt: 50 219 Date: September 13,1997 Compleicd]y: Rick Nash Icicphone: (609) 971-4851 REPORTING PERIOD: August,1997 MONTH YEAR TO DATE CUMULATIVE 1.

DESIGN ELECTRICAL RATING (MWe NET).

The nominal net electrical output of the unit specilled by 650 *

  • the utility aux! insed for the purpose of plant design.
2. MAXIMUM DEPENDABLE C APACITY (MWe NET).

1he gross electrical output as measured at the output 619 *

  • terminals of the turbine gencrutor during the most restrictive seasonal conditions mmus the normal station wtvice louds.
3. NUMBER OF HOURS REACTOR WAS CRITICAL.

1he total numher of hours during the gross hours of the 489.1 **5328.0 **166,916.8-reporting period that the reactor was critical.

4. HOURS GENERATOR ON LINE.

(Senice llours) The total numtwr of hours dunng the gross 445.8 5236.3 -163,154.1 hours1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> of the reporting period that the unit operated with the breakers ekml to the station bus. Tiie sum of the hours that the generator was on line plus the total outage hours in the reporting period.

5. UNIT RESERVE SHUTDOWN HOURS.

The total numhet of hours during the grop hours of the 0 reporting penod that the unit was removeu irom service for 0 0 economic or similar reasons but was available for operation.

6. NET ELECTRICAL ENERGY (MWH).

The gross electncal output of the unit measured at the 264,57 3,222,525 95,230,112 output tenninals of the turbine generator minus the imrmal station service kmds during the gross hours of the reportmg period, expressed in magawatt hours. Negative quantities should not he used

  • Design values have no " Year to Date" or " Cumulative" significance.

" April,1997," Hours Critical" reported as 535.9, should have been 539.4. Difference of 3.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.

E Appendix B -

Unit Shutdowns ,

Docket No. 50-219 Date: 09/08/97

' Conipleted Bv: Rick Nash Telephone: (609)971-4851 Reportina Period: . August 1997 No. Date Type

  • Duration Reason'. Method of . Cause & Corrective Action to (Hours) Shutting Down Prevent Recurrence 2

Reactor 4 970801 F- 298.2 H 2 Oyster Creek Nuclear Generating Station was manually scrammed at 1340 on August 1,1997, due to a reported fire in the generator exciter. The plant was restarted on August 10, 1997, but due to an isolation condenser shell temperature approaching saturation conditions (during plant heatup); the plant was shut down on August i1,1997, for isolation condenser valve diagnostics. The plant was restarted on August 12,1997, and the generator synchronized to the grid on August 13,1997.

  • I 2 F Forced Reasim: . hiestud S Saeduled A-E9ipment Failure (Eglain) 3-Manual B-Maintenance er Test 2-Manual Scram C.Refuelmg 3-Ausomanc Scram D-Regulatory Reerictkwa 40ther(Eglain)

FAWor Training & 11renung E- -

F-Admanstrative GOperational Error (Explain)

H4)ther (Explam)

Summary: Oyster Creek generated 264,579 MWH net electric during August which was 57.4% ofits MDC rated capacity.

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