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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20196H0111997-07-11011 July 1997 Special Rept 97-001:on 970620,removed High Range Radioactive Noble Gas Effluent Monitor (Stack Ragems) from Service to Allow Secondary Calibr IAW Master Surveillance Schedule. Completed Calibr on 970628 & Returned Stack Ragems to Svc ML20129A3401996-10-15015 October 1996 Special Rept 96-001,rev 1:on 960806,stack Ragems High Range Monitor Was Removed from Svc & Not Restored to Svc in Seven Days.Caused by Malfunction of Interlock on Source. Interlock Components Replaced ML20117K5931996-09-0505 September 1996 Special Rept SR 96-001:on 960806,declared Stack Ragems High Range Monitor Inoperable.Caused by Difficulties Requiring Component Replacement.Developed Course of Action for Returning Stack Ragems Instrument ML20116B7521992-10-27027 October 1992 Special Rept 92-08:on 920929,Turbine Building High Radiation Noble Gas Monitor Declared Inoperable for Greater than Seven Days.Alternate Testing Performed Throughout Period of Inoperability ML20115G6461992-10-22022 October 1992 Special Rept 92-07:on 921015,determined That Stem & Disc Separated on Discharge Valve V-9-004 for Diesel Fire Pump P-9-102A.On 921021,fire Pumps Isolated.Redundant Fire Pump Secured & Valves Replaced ML20105A5121992-09-10010 September 1992 Special Rept 92-06:on 920807,fire Diesel Pump 1 Declared Inoperable for More than 7 Days to Perform Preventive Maint.On 920811,diesel Engine Overheated.Solenoid Valve Replaced & New Cooling Water Strainers Installed ML20104B6081992-09-10010 September 1992 Special Rept 92-05:on 920727,condenser Bay Sprinkler Sys 2 Removed from Svc After Spurious Actuation of Sprinkler Head. Hourly Fire Watch Established While Sys Out of Svc.Sprinkler Head Replaced & Sys Returned to Svc on 920814 ML20114C5191992-08-26026 August 1992 Special Rept 92-03:on 920705,electromatic Relief Valve C Inadvertently Opened While Testing Pressure Switch of Valve A.Caused by Personnel Error.Training Session Will Be Held & Engineering Work Request Submitted Re Switch Terminal Point ML20114A9701992-08-17017 August 1992 Special Rept 92-04:on 920724,fire Diesel Pump 2 Removed from Svc to Replace Battery Cables & Solenoid Valve.Correct 24 Volt Dc Coil Obtained from Mfg & Pump Returned to Svc on 920806 ML20096D4711992-05-0101 May 1992 Special Rept 92-02:on 920327,fire Diesel Pump 1 Out of Svc for More than 7 Days to Replace Pump Due to Marginal Discharge Pressure.Caused by Valve Seating Problem.Pump Replacement Expected to Be Completed by 920504 ML20100R7411992-04-10010 April 1992 Special Rept 92-01:on 920227,CO2 Fire Suppression Sys for 4,160-volt Switchgear Inoperable for More than 14 Days When Leaking Valve Stem Repaired on 920226.Possibly Caused by Moisture Intrusion.Corroded Components Replaced ML20087B8431992-01-0303 January 1992 Special Rept 91-09:on 911115,fire Diesel Pump 1-2 Failed to Meet Required Acceptance Criteria During Functional Test. Caused by Cloth Rag Becoming Lodged Inside Pump.Fire Diesel Pump 1-2 Rebuilt & Reinstalled on 911208 ML20076E2641991-08-13013 August 1991 Special Rept 91-08:on 910717,coolant Found Leaking from Cap on Heat Exchanger of Engine of Fire Diesel Pump 1-1.Caused by Wearing on HX Neck,Resulting in HX Failing to Hold Normal Pressure.Engine Secured & Work Request Initiated ML20076E3001991-08-12012 August 1991 Special Rept 91-07:on 910709,nonfunctional Fire Barrier Doors Between Fire Zones OB-FA-6 & TZ-FZ-11B Not Restored to Operable Status within 7 Days.Caused by Ventilation Flow Preventing Door from Closing.Fire Patrol Established ML20077K2271991-07-31031 July 1991 Special Rept 91-06 Re Nonfunctional Fire Barrier Door Not Repaired within 7 Days as Required by Tech Spec 3.12.E. Caused by Broken Door Closure Mechanism.Hourly Fire Watch Initiated.Door Mechanism Repaired on 910704 ML20082E1411991-07-23023 July 1991 Special Rept:On 910702,non-functional Fire Barrier Door Not Repaired within Seven Days as Required by Tech Specs. Caused by Faulty Door Closing Mechanisms.Util Evaluating Alternate Door Closing Mechanisms ML20073C9381991-04-18018 April 1991 Special Rept 91-04:on 910309,fire Detection Sys on Elevations 75' & 95' of Reactor Bldg Made Inoperable to Facilitate Maint Activities.Fire Watch Patrol Has Been Established to Compensate for Detection Sys ML20070T5341991-03-28028 March 1991 Special Rept:On 910222,inoperable Fire Hose Station 33 Not Restored to Operable Status within 14 Days as Required by Tech Specs.Caused by Maint to Angle Valve.Valve Reopened on 910312,restoring Hose Station 33 to Operability ML20070M5181991-03-14014 March 1991 Special Rept 91-02:on 901117,discovered That Fire Barrier Door Between 480-volt Switchgear Rooms a & B Nonfunctional Since 901110 & Not Repaired within 7 Days.Caused by Faulty Door Latching Mechanism.Fire Watch Established ML20058A7441990-10-16016 October 1990 Special Rept 90-04:on 900921,nonfunctional Fire Barrier Door Not Repaired within 7 Days.Fire Watch Established ML20245E7541989-06-0909 June 1989 Special Rept 89-02:on 890526,declared Fire Pump/Diesels 1-1 & 1-2 Inoperable.Caused by Loss of Fire Suppression Water. Pressure Switch & Associated Recorder for 1-2 Diesel Recalibrated Along W/Pump Discharge Pressure Gauge ML20247J2081989-05-22022 May 1989 Special Rept 89-01:on 890422,nonfunctional Fire Barrier Not Repaired within 7 Days as Required by Tech Spec 3.12.E. Fire Watch Established.Nonfunctional Fire Barrier Seal Plannned to Be Restored to Operable Status by 890523 ML20237C6711987-12-11011 December 1987 Special Rept 87-08:on 871112,fire Diesel Pump 1-2 Not Restored to Functional Status within 7 Days.Caused by Constraints Imposed by Increased outage-related Maint Activities.Fire Diesel Pump Restored to Functional Status ML20236S5201987-11-19019 November 1987 Special Rept 87-07:on 871020,nonfunctional Thermo Lag Fire Barrier Not Restored to Functional Status within 7 Days Per Tech Spec 3.12.E.Caused by Constraints Imposed by Increased Maint Activities.Fire Watch Established ML20236L3711987-10-29029 October 1987 Special Rept 87-06:on 870928-30,fire Barrier Penetration Seals Identified as Not Meeting Acceptance Criteria.Cause Not Stated.Fire Watch Established Immediately.Fire Barrier Seals Will Be Restored to Functional Status by 871030 ML20235B4411987-09-22022 September 1987 Ro:On 870811,spill of Reactor Bldg Closed Cooling Water Occurred.Caused by Failure to Follow Instructions on Switching & Tagging Request Form Re Valve Backseating. Procedures Will Be Revised & Training Provided ML20235G2151987-09-20020 September 1987 Ro:On 870911,w/reactor in Cold Shutdown Mode,Tech Spec Safety Limit 2.1.E Exceeded.Caused by Operator Error. Operators Received Training on Safety Limit,Applicable Procedures & Relevant Control Room Indications ML20214H9801987-05-0707 May 1987 Ro:On 870424,operator Personnel Blocked Open Two Torus to Drywell Vacuum Breaker Valves at Time When Primary Containment Integrity Was Required.Caused by Cognitive Personnel Error.Procedures Revised ML20215H3621987-04-0909 April 1987 Special Rept 87-02:on 870214,turbine Trip & Reactor Scram Occurred.Caused by Loose Wire Causing Loss of Feedwater Flow Signal.Following Reduction in Reactor Pressure All Electromatic Relief Valves Reseated Properly ML20206E3931987-04-0101 April 1987 Special Rept 87-01:on 870302,inoperable Fire Suppression Water Deluge Sys Not Restored to Functional Status within 14 Days from Time of Discovery.Caused by Long Lead Time for Procurement of Replacement Parts ML20209H2501987-01-23023 January 1987 Special Rept 86-017:on 861228,nonfunctional Fire Barrier Not Returned to Functional Status within 7 Days from Discovery.Hourly Fire Watch Established.Repairs Completed & Penetration Seal Restored to Functional Status on 870112 ML20207J2981986-12-17017 December 1986 Special Rept 86-16:on 861121,fire Barrier Door Between Monitor & Control Area Stairwell & Hallway Outside Cable Spreading Room Found Nonfunctional.Hourly Fire Watch Patrol Established.Door to Be Restored as Functional on 861222 ML20207J2821986-12-16016 December 1986 Special Rept 86-15:on 861110,penetrations Through Floor of 4160 Volt Switchgear 1D Vault & Floor of Motor Generator Set Room Found Degraded.As of 861117,penetrations Not Restored to Functional Condition.Hourly Fire Watch Patrol Initiated ML20197B1471986-10-0909 October 1986 Special Rept 86-14:on 860922 & 27,nonfunctional Fire Barrier Penetration Seals Not Restored to Functional Status within 7 Days.Hourly Fire Watch Patrol Established within 1 H. Restoration Expected by 861130 ML20212D6251986-07-10010 July 1986 Special Rept 86-03:on 860616,two Hangers Supporting Ofc Bldg Fire Water Supply Riser Found to Need Repair.Riser Consequently Isolated,Rendering Sprinkler Sys 4 & 12 & Deluge Sys 4 Inoperable.Hangers Repaired & Sys Restored ML20137U7031986-01-20020 January 1986 Fire Protection Special Rept 85-03:on 851216,insp of 14 Fire Dampers Identified Design or Installation Deficiencies Resulting in Dampers Being Determined Inoperable.Caused by Nonconforming as-found Fire Damper Configuration ML20117C7451985-04-25025 April 1985 Special Rept 85-02:on 850225,electromatic Relief Valves NR-108B,NR-108C & NR-108D Failed to Fully Reseat After Initial Actuation,Per Tech Spec 6.9.3.f.Caused by Valve Design Deficiency.Design Change Considered ML20102B8671985-02-21021 February 1985 Special Rept 85-01:on 850207,leakage Observed Around post-indication Valve V-9-13.Fire Suppression Water Sys Isolated on 850211 to Facilitate Valve Repair.Caused by Crack in Valve Body.Valve Replaced ML20092N6351984-06-15015 June 1984 Special Rept 84-01:on 840606,post-indicating Valve V-9-12 Branching Off 14-inch Fire Water Main Damaged by Maint Vehicle,Resulting in Loss of Fire Suppression Water Sys. Caused by Lack of Protection Against Physical Damage ML20083C6451983-12-0808 December 1983 RO 83-02T:on 831119,w/fire Pump 1-1 Out of Svc,Fire Pump 1-2 Failed to Start on Low Sys Pressure.Caused by Impeller Wear Rings Out of Tolerance on High End of Clearance Limits. Overspeed Trip Reset ML20082R6551983-11-21021 November 1983 RO 83-02:on 831119,fire Pump 1-2 Failed to Start on Low Sys Pressure During Demand for Fire Water to Fill Isolated Portion of Underground Fire Suppression Pool.Caused Suspected to Be Faulty Overspeed Trip Switch.Switch Tested ML20082L1491983-11-18018 November 1983 Followup RO 83-01:on 831103,fire Suppression Water Sys Declared Inoperable After Pump 1-1 Failed Testing.Mod Underway to Install New Pressure Relief Valves on Both Fire Pumps ML20082B7921983-11-0404 November 1983 RO 83-01:on 831103,fire Suppression Water Sys Declared Inoperable Due to Smoke Emitting from Under Fire Pump 1-2 Pumphead During post-maint Inservice Test & Failed Design Rated Curve for Pump 1-1.Caused by Misadjusted Impeller ML20082L5721983-09-15015 September 1983 Advises That Followup to RO 83-17 Re Diesel Generator Fast Start Surveillance Will Be Forwarded by 830921 ML20073A7071983-03-23023 March 1983 RO 83-4:on 830211,during Controlled Reactor Shutdown,One Dilution Pump Remained in Svc When Intake Canal Water Below Tech Spec Limit.Caused by Personnel Error.Procedures Will Be Revised to Provide More Explicit Directions ML20071B0911983-02-14014 February 1983 RO 83-1-1:on 830113,dilution Pump 1-2 Removed from Svc. Caused by Insufficient Seal Water flow.Long-term Corrective Action Includes Program Designed to Improve Pump Reliability ML20071B0951983-02-14014 February 1983 RO 83-2-1:on 830118,dilution Pump 1-1 Removed from Svc Due to Steam Around Flax Packing Gland.Caused by Wearing in of New packing.Long-term Corrective Actions Include Upgrading Dilution Pump Seal ML20071B1021983-02-14014 February 1983 RO 83-3-1:on 830123,dilution Pumps 1-2 & 1-3 Tripped Off. Caused by Failed Electrical Terminations (Stress Cones). Terminations Replaced ML20070P8361983-01-11011 January 1983 RO 82-8-2:on 821205,dilution Pump 1-3 Tripped,Leaving Dilution Pump 1-2 in Operation.Seal Water Pump Failed & Ambient Water Temp Fell Below Tech Spec Limit.Cause Unknown. Total Dilution Pump Refurbishment Program Initiated ML20064E7271982-12-21021 December 1982 RO 82-7:on 821201,dilution Pump 1-3 Removed from Svc.Caused by Mud & Debris Clogging Grates,Blocking Water Flow to Dilution Pump.Mud & Debris Removed.Total Dilution Pump Refurbishment Program Planned 1997-07-11
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4451999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Oyster Creek Nuclear Generating Station.With ML20211P6731999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Oyster Creek Nuclear Generating Station.With ML20211A7051999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Oyster Creek Nuclear Station.With ML20209G0631999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Oyster Creek Nuclear Generating Station.With ML20212H5491999-06-18018 June 1999 Non-proprietary Rev 4 to HI-981983, Licensing Rept for Storage Capacity Expansion of Oyster Creek Spent Fuel Pool ML20195E7961999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Oyster Creek Nuclear Generating Station.With ML20206N7431999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Oyster Creek Nuclear Generating Station.With ML20205P5401999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Oyster Creek Nuclear Generating Station.With ML20204C8201999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Oyster Creek Nuclear Generating Station.With ML20199E4671998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Oyster Creek Nuclear Generating Station.With ML20195E8321998-12-31031 December 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Sys & Procedures, for Period of June 1997 to Dec 1998.With ML20198D2091998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Oyster Creek Nuclear Generating Station.With ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20155J3021998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Oyster Creek Nuclear Generating Station.With ML20154R4981998-10-20020 October 1998 Core Spray Sys Insp Program - 17R ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20154Q3371998-09-30030 September 1998 Rev 8 to Oyster Creek Cycle 17,COLR ML20154L5571998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Oyster Creek Nuclear Generating Station.With ML20151V6311998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Oyster Creek Nuclear Generating Station.With ML20237D5691998-08-31031 August 1998 Rev 0 to MPR-1957, Design Submittal for Oyster Creek Core Plate Wedge Modification ML20237D5711998-08-18018 August 1998 Rev 0 to SE-000222-002, Core Plate Wedge Installation ML20237B0131998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Oyster Creek Nuclear Generating Station ML20236R0511998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Oyster Creek Nuclear Generating Station ML20249B2981998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Oyster Creek Nuclear Station ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20247F1891998-05-0505 May 1998 Risk Evaluation of Post-LOCA Containment Overpressure Request ML20247G0581998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Oyster Creek Nuclear Generating Station ML20216K0341998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Oyster Creek Nuclear Generating Station ML20151Y4651998-03-31031 March 1998 Non-proprietary Version of Rev 1 to GENE-E21-00143, ECCS Suction Strainer Hydraulic Sizing Rept ML20217A4631998-03-23023 March 1998 Safety Evaluation Accepting Use of Three Heats/Lots of Hot Rolled XM-19 Matl in Core Shroud Repair Assemblies Re Licenses DPR-16 & DPR-59,respectively ML20212E2291998-03-0404 March 1998 Rev 11 to 1000-PLN-7200,01, Gpu Nuclear Operational QAP, Consisting of Revised Pages & Pages for Which Pagination Affected ML20216J0841998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Oyster Creek Nuclear Generating Station ML20203B2781998-02-16016 February 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Systems & Procedures ML20203A3801998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Oyster Creek Nuclear Generation Station ML20198P1791997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Oyster Creek Nuclear Station ML20217C7591997-12-31031 December 1997 1997 Annual Environmental Operating Rept for Oyster Creek Nuclear Generating Station ML20197E9131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Oyster Creek Nuclear Station ML20199E4561997-11-13013 November 1997 Safety Evaluation Accepting Ampacity Derating Analysis in Response to NRC RAI Re GL-92-08, Thermo-Lag 330-1 Fire Barriers, for Plant ML20199D4381997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Oyster Creek Nuclear Station ML20202E8511997-10-21021 October 1997 Rev 0 to Scenario 47, Gpu Nuclear Oyster Creek Nuclear Generating Station Emergency Preparedness (Nrc/Fema Evaluated) 1997 Biennial Exercise. Pages 49 & 59 of Incoming Submittal Were Not Included ML20211M9481997-10-0303 October 1997 Supplemental Part 21 Rept Re Condition Effected Emergency Svc Water Pumps Supplied by Bw/Ip Intl Inc to Gpu Nuclear, Oyster Creek Nuclear Generation Station.No Other Nuclear Generating Stations Effected by Notification ML20198J7361997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Oyster Creek Nuclear Generating Station ML20211B7461997-09-24024 September 1997 Part 21 Rept Re Failure of Emergency Service Water Pump Due to Threaded Flange Attaching Column to Top Series Case Failure.Caused by Dissimilar Metals.Pumps in High Ion Svc Will Be Upgraded to 316 Stainless Steel Matl ML20210V0181997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Oyster Creek Nuclear Generating Station ML20210L2961997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Oyster Creek Nuclear Station ML20149F9961997-07-18018 July 1997 Safety Evaluation Re Gpu Nuclear Operational Quality Assurance Plan,Rev 10 for Three Mile Island Nuclear Generating Station,Unit 1 & Oyster Creek Nuclear Generating Station ML20196H0111997-07-11011 July 1997 Special Rept 97-001:on 970620,removed High Range Radioactive Noble Gas Effluent Monitor (Stack Ragems) from Service to Allow Secondary Calibr IAW Master Surveillance Schedule. Completed Calibr on 970628 & Returned Stack Ragems to Svc ML20210L3081997-06-30030 June 1997 Corrected Page to MOR for June 1997 for Oyster Creek Nuclear Generating Station ML20141H2051997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Oyster Creek Nuclear Station 1999-09-30
[Table view] |
Text
oVV W l UVO1 C' 0~ i~ M:M GPJ 0:t tH L ! :E' tc,003 7,, ;
Auccwmea 3r OPU Nuclear Corporation y NUCISar m',,o"gy "
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$c9 971 O:o sene.s c e n a v :er Mr. Wfiliam Russell, Administrator May 7, 1937 Regfon !
U.S. Nuclear Regulatory Comf ssion 631 Park Avenue King of Prussia, PA 19406
Dear Mr. Russell:
Subject:
Oyster Creek Nuclear Generating Station Docket No. 50-219 Torus to Drywell Yacuum Breakers During a reactor shutdown on April 24, 1987, Operations personnel blocked open two (2) Torus to Drywell vacuum breaker valves at a time when Primary l Containment Integrity was required. This occurred as a result of a cognf ttve l error on the part of two key control recen individuals. The purpose of the action taken was to asstst N deinerting the containment in preparation for l entering and performing maintenance within containment. This action was in I
violation of Technical Spectfications, Section 3.5.A.5 which requires operability of the Torus to Orywell vacuum breakers when primary containte9t is required. One of the individuals involved in the decision to block open the vacuum breaker valves recognized his error approximately four (4) hours af ter blocking the valves open and imediate actions were taken to restore the valves to operable status. The NRC restdent inspector was nottfled of thf s occurrence and subsequently the required nottfication was made to the NR0 Operations Center. The latter nottf f cation, however, was not made in a tfrrely manner in accordance wtth 10 CFR 50.72 In rece;nition of the serious nature of this occurrence, CPUN upper level managemnt initiated an (mediate investigation of this event concurrent with the NRC Re)fon I fnspection.
Altnuugh this event was a cognitive error by on shif t personnel, investigations by GPUN and NRC Inspectors identifled problems associated with the Temporary Varf ation Program and the implementation of the associated ufety review process. GPUN had previously identf fle t problems with reve:t to the i. Liementation of the $dfety review process at the Oyster Creck Station, Oelcar Assurance (Quality Assurance Departmnt) had performed i review t a deterrit ne the implementation aco@acy and interface ef fect1. nes o' the Temporary Varf ation Program (Station Procedure 108). Subsequent to the revision to the safety review process in Septaber of 1986, the Nuclear Safety Assessmnt Ocpartnwnt had planneif a review to assess the effectiveness of stition Proced;re 130 (Conduct of Independent Safety Reviews and Raven f ble Technical Revivas by the Plant Review Group). This assessfnent was conducted in January 1987 Doth of these assessments identified required fmpenvemants 0705270573 070515 PDH ADOCK 05000219 o PDH
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. . 05'07<87 16:17 CPUN OCNGS LICEN NO.000 003 Mr. William Russell, Administrator US NRC Page 2 in implementation. At the time of this event, actions were in progross to correct these deficiencies (Plant Procedure 108 " Equipment Control had been significantly revised and is currently in the review stage; and needed changes to the training program and Station Procedure 130 had been identified).
Based on the above, GPUN upper level management has directed that, prior to restart from the current outage, the following shall be completed:
1 All personnel (Responsible Technical Reviewers and Independent Safety Reviewers) involved in the safety , review process for temporary variations will be retrained prior to performing any reviews.
- 2. The documentation for all current outstanding temporary variations will be reviewed and revised, if required, by the Temporary Yariation Task Force. Safety evaluations will be prepared where appropriate and for those that are identified as not requiring a safety evaluation, a documented justification for the determination will be provided.
- 3. Procedure No.108 (Equipment Control) will be changed as follows:
- a. All future temporary variations will be reviewed prior to installation of a temporary variation by at least one qualified individual, who is not assigned to Control Room shift duties,
- b. Procedure No.100 (l'quipment Control) will be revised to be compatible with Procedure 130 (Conduct of Independent safety Reviews and Responsible Technical Reviews by Plant Review Group).
- c. Additional guidance will be placed in the 108 procedure to prohibit the use of a temporary variation when a procedure change is more appropriate,
- d. The temporary variation fonn will be revised to explicitly require a technical review of the temporary verf ation packaga including the >rocudure 130 "Nucicar Safety Environmental Determination leview" (NSEDR) form, which identifies the safety significance, and the written Safety Evaluation (SC) when one is required.
4 Frxedure No.130 (conduct of Independent Cafety Revim and
? vicniible Technical Reviews by Plant Roview Group) will t>e chinyd
- t. o.v'; i ' t tten justifl;ation f cr "W aWel given tu qu.istfons 3 through 6 on the NSEDR.
- 5. Procedure No. 312 (Reactor Containment Integrity and Atmosphere O ntrol) will be changed to preclude opening of roactor batiding to torus vacuun breaker valva's while primary conttin9ent integrity is required.
r M 1 0
. 05'07 87 16:18 CPUH CO65 LICEN NO.008 004 Mro William Russell, Administrator US NRC Page 3 I
- 6. Percef ved technical problems regarding torus to drywell vacuum breaker valve position indication, required maintenance, and degradation of the torus deinerting rate will be thoroughly investigated and resolved. (With regard to the torus to drywell vacuum breaker position indication concern, operability surveillance (procedure 604.4.006) was performed on all torus to drywell vacuum breakers on May 3,1987 which verified proper operation of the valves and their associated position alarms, A compartson was made between past and present torus deinerting rates. The results of the investigation show no appreciable
, increase in the time required to deinert the torus and, therefore, there is no basis for suspecting any degradation in the operation of any torus vent valves.)
GPUN has recognized a needed improvement in the review of temporary variations (TV) and TV associated safety reviews by procedurally responsible management personnel. It was found that better understanding was needed with i
regard to what was expected of them in their review of temporary variations and associated safety reviews, All management personnel procedurally responsible for reviews have been or will be retrained as to what is expected and what their responsibilities include. Examples are being provided illustrating a lack of pertinent information and, in some cases, incorrect detenninations on documentation associated with temporary variations and their associated safety reviews. These personnel are responding well in recognizing their responsibility to provide greater attention to documentation to assure
, proper content, control of interim measures with regard to testing and recovery, and to assure accurate determinations regarding safety. These personnel were directed to review, prior to restart, all currently outstanding temporary variations, In order to verify proper performance and review of these activities, the Nuclear Assurance Division will Institute increased oversight of thf s process for the next two to three months, with particular attention to temporary varf ations and associated safety determinations / evaluations. Ocf fciencies identified from this review will oc addressed promptly, In the longer term, a vacuum breaker incident investigation team has i been created and staffed by the Nuclear $afety Assessment Department to
! continue the CPUN investfgation and identify other long term actions that may i
be required or desirable. The scope and depth of this review will be guided by the Managemont Oversight and Risk Tree (M0iti) process, this process will '
examine the controls and barriers (personnel, procedurvs. and equipment) in place which should haw
- prevented this event. It will ersmine the need for improve m nts in those barriers such that greater ass panot is obtained to preclude events of this natura in the future, The management system factors will also be investigated to ascertain any other contributors to this event.
As a result, improvements in our abfilty to prevent occurrence of oversights or omissions will be made, included in the rovfew will be an examination of the Temporary Variation Program, implementation of the ssfsty review process, augmented shf f t staffing during unusually busy periods, the influence of schedular requiremnts, and contributors to personnel error.
- . vus si a vsva
. . 05 07/87 16:19 GFui OCtGS LICEt1 to.008 005 Mr. Willfaa Russell, Administrator ,
US NRC Page 4 The ongoing Perfonnance Assessment Task Force had previously identifled time delays in the disposition of technical concerns. While all final recomendations of the task force are not complete, it is believed that these delay problems will be reduced by effective adoption of a system working group concept whereby individuals from Plant Engineering, Operations, and Maintenance take responsibilf / for the status of a particular plant system and/or component. Recently, the company has achieved excellent results by utf1f zing a task force approach to problem resolutfon of particularly broad scope or technical dif ficulty. It is reasonable to assume this process will be utilized in the future, As a follow up to the procedure 108 and 130 trafning of key individuals before restart, all other Oyster Creek personnel previously qualified as Responsible Technical Reviewers and/or Independent Safety Reviewers will recefve addftional training on these procedures subsequent, wtthin a month, to plant startup.
Other concerns have been identified by GPUN and NRC inspection personno). These concerns and the associated GpVN actions are as follows:
- 1. Untimely reporting of events in accordance with 10 CFR 50.72 has been noted especially in the area of events resulting from human e rror. Strict guidance has been given to operations management to be more aggressive in strictly interpreting the reporting reg!remer.t: cf 10 CTR 50.72, i.e., when in doubt report.
- 2. The Vacuum Breaker System, both Reactor Duf1 ding to Torus check valves and the Drywc11 to Torus check valves, are princfpally passive systems. Due to a number of identiffed discrepancies over the past 8 to 10 years, it appears that some lack of sonsttivity may extSt with respect to the safety function of these valves.
Therefore, a memo will be developed and circulated to all personnel reiterating the purpose of these valves and their importance to plant safety. Additionally, the training program for those systems will be revised to include a discussion of past occurrences with regard to operation and maintenance of these systems and components.
- 3. CpuN recognitos the continuing need to reduce the number of operator and technician errors. By GPUN standards, an undue number of errors has been tiuted in several fnternal evaluations prevfously per fonned. In addition to those actions described in our $ Alp responta of April 28, 1987, corrective measures which are greently in progress or are planned include the following:
- a. ?ne feedwater system f s recognired as a complicated system to operate; therefore, the training module is botng revised to emphastre proper control and operation.
. . 05 07 8a 16:19 CFUti OCNGS L!CEN NO.008 006 Mr. William Russell, Administrator US NRC Page 5
- b. In the past, the need for strict procedural compliance has been emphasized and disciplinary action has been administered where appropriate. Continued emphasis is this area will be stressed.
- c. Where spectfic personnel related deficiencies are observed, retraining of personnel is conducted,
- d. The Performance Assessment Task Force is evaluating potential actions to reduce challenges to the operators.
- e. Improved formality and profes'stonalism is one of our top goals.
In summary, those actions being taken in the short term, prior to startup, will significantly improve operator and responsible management perfomance with regard to temporary variations and their safety reviews. The effectiveness of these actions will be monitored to assure continued visibility until substantial improvement is vertfled. The application of the MORT process which has been initiated will provide an integrated overview of personnel interfaces, responsibillties, and management system factors. Deficient areas resulting from this review will be corrected. The need for additional training in deffcfent areas will be identified and given to all involved personnel.
GPUN not only recognizes the seriousness of this event, but also the importance of addresstng all of the factors which may have contributed to tnts event as well as any other deficiencies identiffed. We have initiated those actions discussed above in order to verify acceptability of currently installed temporary variations and signtficantly improve performance in the near term and will followup our investigation to assure that pertinent problems have been identf fied and properly resolved in the long tem.
Very truly yours, P
t edTer b))
Yte.e President and Director Oyster Crook P8F/MWL/ded (0664A) cc: Mr. Aleiander W. Dromrick, Project Manager U,$. Nuclear Regulatory Comission 01vf sf sn of Roctor Projects I/II 7920 Norfolk Avenue, Phillips 01dg.
Bethesda, MD 20014 NRC Resident inspector Oyster Creek Nuclear Generating Station