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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B1481993-07-30030 July 1993 LER 93-012-00:on 930702,reactor Core Isolation Cooling Sys Declared Inoperable Due to Associated Bus Voltage Dropping Below TS Limits.Sent Operator to Cycle Timer Which Caused Affected Contact to reclose.W/930730 Ltr ML20045D9331993-07-0202 July 1993 LER 93-004-00:on 930604,unexpected CRD Low Charging Water Header Scram Received Followed by Charging Water Header A2/B2 Alarm.Caused by Crud or Foreign Matl Passing Through Suction Filter.Filters Cleaned & reused.W/930702 ML20045D7501993-06-23023 June 1993 LER 93-003-00:on 930524,Div 1 ECCS Initiation Signal Received & LPCS Pump,Lpci Pump 2A & EDG Unit 0 Automatically Started.Caused by Personnel Error.Pumps Secured & Event Documented in Personnel file.W/930623 Ltr ML20044E4161993-05-28028 May 1993 LER 92-009-01:on 920923,spurious Auto Start of CR Ventilation Emergency make-up Train Occurred Due to High Radiation Spike.Radiation Monitor Circuit modified.W/930528 Ltr ML20044E4191993-05-21021 May 1993 LER 93-011-00:on 930423,manual Scram Initiated.Caused by Disconnected Linkage on Valve Positioner on Heater Drain Valve Due to Loose Jam Nut.Tailgate Session Will Be Held W/ Instrument Maint Dept Re Jam nuts.W/930521 Ltr ML20044D5161993-05-15015 May 1993 LER 92-007-01:on 920613,high Radiation Spike Received from CR Ventilation Process Radiation Monitor,Initiating Emergency Makeup Train B.Caused by Normal Variations in Radiation Readings.Spike modified.W/930515 Ltr ML20044D5571993-05-14014 May 1993 LER 93-010-00:on 930414,DG Cooling Water Pump Automatically Tripped on Magnetic Overload.Caused by Inexperienced Trainee in Operation of Control Lever.Lesson Plans & Training Programs for Operators to Be reviewed.W/930514 Ltr ML20044C9801993-05-0707 May 1993 LER 91-010-01:on 910719 & 0805,CR a Ventilation Emergency Makeup Fan auto-started on Spurious Trip of CR Air Intake Process Radiation Monitor.Caused by Normal Variations in Background Radiation.Supply Board replaced.W/930507 Ltr ML20044B6161993-02-25025 February 1993 LER 93-002-00:on 930126,Unit 1 Manual Scram Due to a SRV Being Stuck Open Due to Duct Tape Being Over Actuators Air Valve Manifold Exhaust Port.Maint Procedures That Involve Cleanliness reviewed.W/930225 Ltr ML20024G9771991-05-10010 May 1991 LER 91-005-00:on 910410,determined That Tech Spec Required Surveillance of Suppression Chamber Oxygen Sampling Missed. Caused by Inadequate Review of Tech Spec Change.Drywell & Suppression Chamber Checked for oxygen.W/910510 Ltr ML20044A3851990-06-25025 June 1990 LER 90-008-00:on 900525,Tech Spec Hourly Fire Watch Missed Due to Miscommunications Between Security Personnel & Radiation Protection Personnel.Fire Watch re-established & Memo issued.W/900625 Ltr ML20043F1721990-06-0505 June 1990 LER 90-009-00:on 900510,RWCU Outboard Suction Isolation Valve 2G33-F004 Auto Closed Which Tripped RWCU Pump B. Caused by Procedure Deficiency.Procedure LTS-500-209 Will Be revised.W/900605 Ltr ML20043F1281990-06-0101 June 1990 LER 90-009-00:on 900511,apparent Ruptured Diaphragm Found on Pressure Differential Switch in RCIC Steam Line.Caused by Torn Diaphragm Inside Switch.Replacement Switch Installed, Calibr & Functionally Tested satisfactorily.W/900608 Ltr ML20043B5681990-05-23023 May 1990 LER 89-027-01:on 891113,primary Containment Isolation Sys Group 1 Isolation Occurred During Surveillance Testing. Caused by Burnt Out Window Light Bulbs on Alarm Window. Light Bulbs Replaced & Jumpers installed.W/900523 Ltr ML20043A7721990-05-18018 May 1990 LER 90-007-00:on 900421,reactor Protection Sys Bus a Transfer & Reactor Recirculation Hydraulic Power Unit a Inboard Isolation Valves Closed,Causing Partial Group II isolation.Out-of-svc Procedure revised.W/900518 Ltr ML20043D0591990-05-18018 May 1990 LER 90-008-00:on 900502,ESF Actuation of Control Room B Emergency Ctk Ventilation Makeup Fan Occurred.Caused by Procedure deficiency.LTS-800-205 & Similar Procedures Will Be revised.W/900601 Ltr ML20042H0211990-05-10010 May 1990 LER 90-006-00:on 900412,loop a Primary Containment Chilled Water Sys Inboard Isolation Valves & Reactor Bldg Closed Cooling Water Sys Inboard Isolation Valve Went Closed.Caused by Inadequate Procedure.Procedures revised.W/900510 Ltr ML20042F9001990-05-0404 May 1990 LER 90-005-00:on 900411,experienced Loss of Dc Power to Portion of Div I Primary Containment Isolation Sys Logic Which Resulted in Isolation Signal & Actuation.Caused by Failure to Update Drawings & procedures.W/900504 Ltr ML20042F1941990-04-30030 April 1990 LER 89-025-01:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Door Containing Undervoltage Relays Closed.Caused by Misalignment of Door.Door Repaired. W/900430 Ltr ML20012D5341990-03-16016 March 1990 LER 90-003-01:on 900201,RCIC Isolation Signal Occurred During Warmup.Caused by Spurious High Steam Flow Signal.Rcic Sys Piping Integrity Verified & Isolation Logic Reset.W/ 900316 Ltr ML20012D5371990-03-16016 March 1990 LER 90-002-01:on 900129,oil in Diesel Generator Governor 1A Found to Be Low & Could Not Be Seen in Sight Glass.Caused by Slow Leak from Compensation Needle Valve Plug.Proper Amount of Oil Added & Operability Test performed.W/900316 Ltr ML20012C4931990-03-15015 March 1990 LER 90-004-00:on 900213,control Room B HVAC Intake Radiation Monitor Lost Power Causing auto-start of Emergency make-up Train B.Caused by Blown Fuses.Fuses Replaced.Logic Revs for Radiation Monitors Will Be installed.W/900315 Ltr ML20012B6501990-03-0909 March 1990 LER 90-002-00:on 900209,Operating Surveillance LOS-TG-W1 Determined to Have Exceeded Required Testing Interval,Per Tech Spec 3/4.7.10.Caused by Personnel Error.Personnel Counseled & Ref Procedures Will Be revised.W/900309 Ltr ML20012B5521990-03-0808 March 1990 LER 90-001-00:on 900206,full Reactor Scram Occurred During Instrument Surveillance Testing.Caused by Actuation of APRM E Trip Circuitry.Shutdown Margin Revised & Caution Card Placed on Control Room Bench board.W/900308 Ltr ML20011F8251990-03-0202 March 1990 LER 90-003-00:on 900201,RCIC Received Div 2 Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal Generated When Steam/Water Mixture Admitted to RCIC Steam Line.Isolation Logic reset.W/900302 Ltr ML20011F5551990-02-28028 February 1990 LER 90-002-00:on 900129,after Filling Diesel Generator 1A Governor W/Oil,Generator Started & Declared Inoperable. Caused by Slow Leak Coming from Compensation Needle Valve Plug.Oil Added & Plug Washer replaced.W/900228 Ltr ML20006F5951990-02-21021 February 1990 LER 90-001-00:on 900122,RWCU Sys Received Div 1 Leakage Detection Ambient Temp High Isolation Signal,Causing Trips of RWCU Pumps a & C.Caused by Broken Thermocouple Input Lead.Lead Wire Reconnected & Isolation reset.W/900221 Ltr ML20011F4921990-02-16016 February 1990 LER 89-013-01:on 890907,Group I Isolation Received During Performance of Instrument Surveillance LIS-MS-401.Caused by Depressurization of Main Steam Line Low Pressure Switch. Surveillance Revised to Split Into Two parts.W/900216 Ltr ML20006E4501990-02-15015 February 1990 LER 89-010-01:on 890715 & 17,voltage Oscillations Noted on Div II Battery Charger,Resulting in Inoperability of HPCS Sys.Caused by Failure of Charger in High Voltage Shutdown Relay.Charger Energized & Relay replaced.W/900215 Ltr ML20006E4451990-02-14014 February 1990 LER 89-009-01:on 890619,diaphragm Leak Discovered in RCIC Steam Line High Flow Isolation Switch.Caused by 1 & 1/2-inch Tear in Diaphragm.Pressure Differential Switch Replaced & Calibr.Reported Per NRC Bulletin 86-002.W/900214 Ltr ML20006E3981990-02-14014 February 1990 LER 89-008-01:on 890228,reactor Vessel Low Water Level 2 Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.Channel Placed in Tripped Condition & All Static-O-Ring Pressure Switches to Be replaced.W/900214 Ltr ML20006E3951990-02-14014 February 1990 LER 89-010-01:on 890303,automatic Depressurization Sys Permissive Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.All Static-O-Ring Reactor Vessel Level Switches Will Be replaced.W/900214 Ltr ML19354D8361990-01-15015 January 1990 LER 89-018-00:on 891216,plant 250-volt Battery & RCIC Sys Declared Inoperable Due to Low Battery Electrolyte Temps. Caused by Failure of Div I Switchgear Heat Removal Sys Damper Actuators.Air Intake Dampers closed.W/900115 Ltr ML20042D3921990-01-0404 January 1990 LER 89-011-01:on 890826,spurious Reactor Protection Sys Actuation Occurred.Definite Cause of Trip Not Determined. Brief Disturbance in Reactor Protection Sys Allowed Some Contactors to Trip.Procedure revised.W/900104 Ltr ML20005E2741989-12-22022 December 1989 LER 89-028-00:on 891204,RHR Shutdown Cooling Suction Header Outboard Isolation Valve Automatically Isolated.Caused by Miscommunication Between Technician & Station Operator.Task Force Developed to Review event.W/891222 Ltr ML19351A6301989-12-15015 December 1989 LER 89-006-01:on 890214,reactor Vessel Low Water Level 3 Switch Setpoint Found Out of Tolerance.Caused by Setpoint Drift.Level Switch to Be Replaced by Analog Trip Sys During First Quarter 1990.W/891215 Ltr ML20011D1341989-12-14014 December 1989 LER 89-017-00:on 891117,flow Switch FS-2E22-N006 Found W/ Setpoint Out of Tolerance Above Reject Limit.Caused by Setpoint Drift.Work Request Written to Replace Flow Switch. W/891214 Ltr ML19351A6751989-12-12012 December 1989 LER 89-027-00:on 891113,primary Containment Isolation Sys Group I Isolation Occurred While Performing Instrument Surveillance.Caused by Loss of Power to Leak Detection Sys Logic.Isolation reset.W/891213 Ltr ML19332F0081989-12-0808 December 1989 LER 89-016-00:on 891109,RWCU Isolation Occurred While Instrument Surveillance on Ventilation Differential Temp Isolation Functional Test in Progress.Caused by Faulty Thermocouple.Thermocouple repaired.W/891208 Ltr ML20005D6621989-12-0606 December 1989 LER 89-026-00:on 891106,inadvertent Primary Containment Isolation Actuation Occurred While Clearing out-of-svc. Caused by Inadequate Logic Setup During Mod Installation. Trip Status & Output Switches repositioned.W/891206 Ltr ML19332F2431989-12-0101 December 1989 LER 89-025-00:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Equipment Operator Closed Door Containing Relays.Caused by Misalignment of Door.Isolations Reset,Bus Energized & Circuit Logic tested.W/891201 Ltr ML19332E6581989-11-29029 November 1989 LER 89-015-00:on 891030,shift Control Room Engineer Noted That Quarterly Standby Liquid Control Operating Surveillance LOS-SC-Q1 Was Past Critical Date.Caused by Clerical Data Entry Error.Missed Surveillance performed.W/891129 Ltr ML19332D5181989-11-22022 November 1989 LER 89-018-01:on 890515,RCIC Received Div I & Div II Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal When Steam Added to RCIC Steam Line. Special Test Initiated.Isolation Logic reset.W/891122 Ltr ML19327C2601989-11-17017 November 1989 LER 89-014-00:on 891020,primary Containment Isolation Sys Group 4 Isolation Occurred Causing Isolation Dampers to Close.Caused by Opening of Div 2 125-volt Dc Breaker.Power Supply replaced.W/891117 Ltr ML19325F3411989-11-13013 November 1989 LER 89-024-00:on 891013 & 30,unsealed Openings in Main Control Room Floor & Main Control Room West Wall Discovered. Caused by Wide Gap Between Structural Beam & Cable Tray. Openings Sealed & Fire Watch established.W/891113 Ltr ML19324C1751989-11-0808 November 1989 LER 89-012-01:on 890309,diaphragm Leak Found in Pressure Differential Switch 1E31-N013BB.Caused by Tear Found in Diaphragm.Replacement Switch Installed,Calibr & Functionally Tested satisfactorily.W/891108 Ltr ML20024E9121983-08-26026 August 1983 LER 83-093/03L-0:on 830801,discovered full-in Indication on Core Display for Control Rod 34-47 Inoperable.Caused by Failed Switching Transistor on Data Memory Board 19.Data Memory Board replaced.W/830826 Ltr ML20024B8381983-07-0505 July 1983 LER 83-060/03L-0:on 830606,following Turbine Trip & Scram Due to High Vibration on Main Turbine,Reactor Recirculation Breaker 4B Closed.Cause Undetermined.Auxiliary Contacts cleaned.W/830705 Ltr ML20024B0721983-06-16016 June 1983 Updated LER 83-012/03X-1:on 830210,w/reactor in Cold Shutdown,Setpoints for Switches 1E31-N612A/B Found Above Tech Spec Limits.Cause Unknown.Switches calibr.W/830616 Ltr ML20024A6961983-06-14014 June 1983 LER 83-051/03L-0:on 830516,reactor Protection Sys Trip Channel H2 Limit Switch Failed to Operate Properly.Cause Unknown.Limit Switch readjusted.W/830614 Ltr 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046B1481993-07-30030 July 1993 LER 93-012-00:on 930702,reactor Core Isolation Cooling Sys Declared Inoperable Due to Associated Bus Voltage Dropping Below TS Limits.Sent Operator to Cycle Timer Which Caused Affected Contact to reclose.W/930730 Ltr ML20045D9331993-07-0202 July 1993 LER 93-004-00:on 930604,unexpected CRD Low Charging Water Header Scram Received Followed by Charging Water Header A2/B2 Alarm.Caused by Crud or Foreign Matl Passing Through Suction Filter.Filters Cleaned & reused.W/930702 ML20045D7501993-06-23023 June 1993 LER 93-003-00:on 930524,Div 1 ECCS Initiation Signal Received & LPCS Pump,Lpci Pump 2A & EDG Unit 0 Automatically Started.Caused by Personnel Error.Pumps Secured & Event Documented in Personnel file.W/930623 Ltr ML20044E4161993-05-28028 May 1993 LER 92-009-01:on 920923,spurious Auto Start of CR Ventilation Emergency make-up Train Occurred Due to High Radiation Spike.Radiation Monitor Circuit modified.W/930528 Ltr ML20044E4191993-05-21021 May 1993 LER 93-011-00:on 930423,manual Scram Initiated.Caused by Disconnected Linkage on Valve Positioner on Heater Drain Valve Due to Loose Jam Nut.Tailgate Session Will Be Held W/ Instrument Maint Dept Re Jam nuts.W/930521 Ltr ML20044D5161993-05-15015 May 1993 LER 92-007-01:on 920613,high Radiation Spike Received from CR Ventilation Process Radiation Monitor,Initiating Emergency Makeup Train B.Caused by Normal Variations in Radiation Readings.Spike modified.W/930515 Ltr ML20044D5571993-05-14014 May 1993 LER 93-010-00:on 930414,DG Cooling Water Pump Automatically Tripped on Magnetic Overload.Caused by Inexperienced Trainee in Operation of Control Lever.Lesson Plans & Training Programs for Operators to Be reviewed.W/930514 Ltr ML20044C9801993-05-0707 May 1993 LER 91-010-01:on 910719 & 0805,CR a Ventilation Emergency Makeup Fan auto-started on Spurious Trip of CR Air Intake Process Radiation Monitor.Caused by Normal Variations in Background Radiation.Supply Board replaced.W/930507 Ltr ML20044B6161993-02-25025 February 1993 LER 93-002-00:on 930126,Unit 1 Manual Scram Due to a SRV Being Stuck Open Due to Duct Tape Being Over Actuators Air Valve Manifold Exhaust Port.Maint Procedures That Involve Cleanliness reviewed.W/930225 Ltr ML20024G9771991-05-10010 May 1991 LER 91-005-00:on 910410,determined That Tech Spec Required Surveillance of Suppression Chamber Oxygen Sampling Missed. Caused by Inadequate Review of Tech Spec Change.Drywell & Suppression Chamber Checked for oxygen.W/910510 Ltr ML20044A3851990-06-25025 June 1990 LER 90-008-00:on 900525,Tech Spec Hourly Fire Watch Missed Due to Miscommunications Between Security Personnel & Radiation Protection Personnel.Fire Watch re-established & Memo issued.W/900625 Ltr ML20043F1721990-06-0505 June 1990 LER 90-009-00:on 900510,RWCU Outboard Suction Isolation Valve 2G33-F004 Auto Closed Which Tripped RWCU Pump B. Caused by Procedure Deficiency.Procedure LTS-500-209 Will Be revised.W/900605 Ltr ML20043F1281990-06-0101 June 1990 LER 90-009-00:on 900511,apparent Ruptured Diaphragm Found on Pressure Differential Switch in RCIC Steam Line.Caused by Torn Diaphragm Inside Switch.Replacement Switch Installed, Calibr & Functionally Tested satisfactorily.W/900608 Ltr ML20043B5681990-05-23023 May 1990 LER 89-027-01:on 891113,primary Containment Isolation Sys Group 1 Isolation Occurred During Surveillance Testing. Caused by Burnt Out Window Light Bulbs on Alarm Window. Light Bulbs Replaced & Jumpers installed.W/900523 Ltr ML20043A7721990-05-18018 May 1990 LER 90-007-00:on 900421,reactor Protection Sys Bus a Transfer & Reactor Recirculation Hydraulic Power Unit a Inboard Isolation Valves Closed,Causing Partial Group II isolation.Out-of-svc Procedure revised.W/900518 Ltr ML20043D0591990-05-18018 May 1990 LER 90-008-00:on 900502,ESF Actuation of Control Room B Emergency Ctk Ventilation Makeup Fan Occurred.Caused by Procedure deficiency.LTS-800-205 & Similar Procedures Will Be revised.W/900601 Ltr ML20042H0211990-05-10010 May 1990 LER 90-006-00:on 900412,loop a Primary Containment Chilled Water Sys Inboard Isolation Valves & Reactor Bldg Closed Cooling Water Sys Inboard Isolation Valve Went Closed.Caused by Inadequate Procedure.Procedures revised.W/900510 Ltr ML20042F9001990-05-0404 May 1990 LER 90-005-00:on 900411,experienced Loss of Dc Power to Portion of Div I Primary Containment Isolation Sys Logic Which Resulted in Isolation Signal & Actuation.Caused by Failure to Update Drawings & procedures.W/900504 Ltr ML20042F1941990-04-30030 April 1990 LER 89-025-01:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Door Containing Undervoltage Relays Closed.Caused by Misalignment of Door.Door Repaired. W/900430 Ltr ML20012D5341990-03-16016 March 1990 LER 90-003-01:on 900201,RCIC Isolation Signal Occurred During Warmup.Caused by Spurious High Steam Flow Signal.Rcic Sys Piping Integrity Verified & Isolation Logic Reset.W/ 900316 Ltr ML20012D5371990-03-16016 March 1990 LER 90-002-01:on 900129,oil in Diesel Generator Governor 1A Found to Be Low & Could Not Be Seen in Sight Glass.Caused by Slow Leak from Compensation Needle Valve Plug.Proper Amount of Oil Added & Operability Test performed.W/900316 Ltr ML20012C4931990-03-15015 March 1990 LER 90-004-00:on 900213,control Room B HVAC Intake Radiation Monitor Lost Power Causing auto-start of Emergency make-up Train B.Caused by Blown Fuses.Fuses Replaced.Logic Revs for Radiation Monitors Will Be installed.W/900315 Ltr ML20012B6501990-03-0909 March 1990 LER 90-002-00:on 900209,Operating Surveillance LOS-TG-W1 Determined to Have Exceeded Required Testing Interval,Per Tech Spec 3/4.7.10.Caused by Personnel Error.Personnel Counseled & Ref Procedures Will Be revised.W/900309 Ltr ML20012B5521990-03-0808 March 1990 LER 90-001-00:on 900206,full Reactor Scram Occurred During Instrument Surveillance Testing.Caused by Actuation of APRM E Trip Circuitry.Shutdown Margin Revised & Caution Card Placed on Control Room Bench board.W/900308 Ltr ML20011F8251990-03-0202 March 1990 LER 90-003-00:on 900201,RCIC Received Div 2 Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal Generated When Steam/Water Mixture Admitted to RCIC Steam Line.Isolation Logic reset.W/900302 Ltr ML20011F5551990-02-28028 February 1990 LER 90-002-00:on 900129,after Filling Diesel Generator 1A Governor W/Oil,Generator Started & Declared Inoperable. Caused by Slow Leak Coming from Compensation Needle Valve Plug.Oil Added & Plug Washer replaced.W/900228 Ltr ML20006F5951990-02-21021 February 1990 LER 90-001-00:on 900122,RWCU Sys Received Div 1 Leakage Detection Ambient Temp High Isolation Signal,Causing Trips of RWCU Pumps a & C.Caused by Broken Thermocouple Input Lead.Lead Wire Reconnected & Isolation reset.W/900221 Ltr ML20011F4921990-02-16016 February 1990 LER 89-013-01:on 890907,Group I Isolation Received During Performance of Instrument Surveillance LIS-MS-401.Caused by Depressurization of Main Steam Line Low Pressure Switch. Surveillance Revised to Split Into Two parts.W/900216 Ltr ML20006E4501990-02-15015 February 1990 LER 89-010-01:on 890715 & 17,voltage Oscillations Noted on Div II Battery Charger,Resulting in Inoperability of HPCS Sys.Caused by Failure of Charger in High Voltage Shutdown Relay.Charger Energized & Relay replaced.W/900215 Ltr ML20006E4451990-02-14014 February 1990 LER 89-009-01:on 890619,diaphragm Leak Discovered in RCIC Steam Line High Flow Isolation Switch.Caused by 1 & 1/2-inch Tear in Diaphragm.Pressure Differential Switch Replaced & Calibr.Reported Per NRC Bulletin 86-002.W/900214 Ltr ML20006E3981990-02-14014 February 1990 LER 89-008-01:on 890228,reactor Vessel Low Water Level 2 Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.Channel Placed in Tripped Condition & All Static-O-Ring Pressure Switches to Be replaced.W/900214 Ltr ML20006E3951990-02-14014 February 1990 LER 89-010-01:on 890303,automatic Depressurization Sys Permissive Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.All Static-O-Ring Reactor Vessel Level Switches Will Be replaced.W/900214 Ltr ML19354D8361990-01-15015 January 1990 LER 89-018-00:on 891216,plant 250-volt Battery & RCIC Sys Declared Inoperable Due to Low Battery Electrolyte Temps. Caused by Failure of Div I Switchgear Heat Removal Sys Damper Actuators.Air Intake Dampers closed.W/900115 Ltr ML20042D3921990-01-0404 January 1990 LER 89-011-01:on 890826,spurious Reactor Protection Sys Actuation Occurred.Definite Cause of Trip Not Determined. Brief Disturbance in Reactor Protection Sys Allowed Some Contactors to Trip.Procedure revised.W/900104 Ltr ML20005E2741989-12-22022 December 1989 LER 89-028-00:on 891204,RHR Shutdown Cooling Suction Header Outboard Isolation Valve Automatically Isolated.Caused by Miscommunication Between Technician & Station Operator.Task Force Developed to Review event.W/891222 Ltr ML19351A6301989-12-15015 December 1989 LER 89-006-01:on 890214,reactor Vessel Low Water Level 3 Switch Setpoint Found Out of Tolerance.Caused by Setpoint Drift.Level Switch to Be Replaced by Analog Trip Sys During First Quarter 1990.W/891215 Ltr ML20011D1341989-12-14014 December 1989 LER 89-017-00:on 891117,flow Switch FS-2E22-N006 Found W/ Setpoint Out of Tolerance Above Reject Limit.Caused by Setpoint Drift.Work Request Written to Replace Flow Switch. W/891214 Ltr ML19351A6751989-12-12012 December 1989 LER 89-027-00:on 891113,primary Containment Isolation Sys Group I Isolation Occurred While Performing Instrument Surveillance.Caused by Loss of Power to Leak Detection Sys Logic.Isolation reset.W/891213 Ltr ML19332F0081989-12-0808 December 1989 LER 89-016-00:on 891109,RWCU Isolation Occurred While Instrument Surveillance on Ventilation Differential Temp Isolation Functional Test in Progress.Caused by Faulty Thermocouple.Thermocouple repaired.W/891208 Ltr ML20005D6621989-12-0606 December 1989 LER 89-026-00:on 891106,inadvertent Primary Containment Isolation Actuation Occurred While Clearing out-of-svc. Caused by Inadequate Logic Setup During Mod Installation. Trip Status & Output Switches repositioned.W/891206 Ltr ML19332F2431989-12-0101 December 1989 LER 89-025-00:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Equipment Operator Closed Door Containing Relays.Caused by Misalignment of Door.Isolations Reset,Bus Energized & Circuit Logic tested.W/891201 Ltr ML19332E6581989-11-29029 November 1989 LER 89-015-00:on 891030,shift Control Room Engineer Noted That Quarterly Standby Liquid Control Operating Surveillance LOS-SC-Q1 Was Past Critical Date.Caused by Clerical Data Entry Error.Missed Surveillance performed.W/891129 Ltr ML19332D5181989-11-22022 November 1989 LER 89-018-01:on 890515,RCIC Received Div I & Div II Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal When Steam Added to RCIC Steam Line. Special Test Initiated.Isolation Logic reset.W/891122 Ltr ML19327C2601989-11-17017 November 1989 LER 89-014-00:on 891020,primary Containment Isolation Sys Group 4 Isolation Occurred Causing Isolation Dampers to Close.Caused by Opening of Div 2 125-volt Dc Breaker.Power Supply replaced.W/891117 Ltr ML19325F3411989-11-13013 November 1989 LER 89-024-00:on 891013 & 30,unsealed Openings in Main Control Room Floor & Main Control Room West Wall Discovered. Caused by Wide Gap Between Structural Beam & Cable Tray. Openings Sealed & Fire Watch established.W/891113 Ltr ML19324C1751989-11-0808 November 1989 LER 89-012-01:on 890309,diaphragm Leak Found in Pressure Differential Switch 1E31-N013BB.Caused by Tear Found in Diaphragm.Replacement Switch Installed,Calibr & Functionally Tested satisfactorily.W/891108 Ltr ML20024E9121983-08-26026 August 1983 LER 83-093/03L-0:on 830801,discovered full-in Indication on Core Display for Control Rod 34-47 Inoperable.Caused by Failed Switching Transistor on Data Memory Board 19.Data Memory Board replaced.W/830826 Ltr ML20024B8381983-07-0505 July 1983 LER 83-060/03L-0:on 830606,following Turbine Trip & Scram Due to High Vibration on Main Turbine,Reactor Recirculation Breaker 4B Closed.Cause Undetermined.Auxiliary Contacts cleaned.W/830705 Ltr ML20024B0721983-06-16016 June 1983 Updated LER 83-012/03X-1:on 830210,w/reactor in Cold Shutdown,Setpoints for Switches 1E31-N612A/B Found Above Tech Spec Limits.Cause Unknown.Switches calibr.W/830616 Ltr ML20024A6961983-06-14014 June 1983 LER 83-051/03L-0:on 830516,reactor Protection Sys Trip Channel H2 Limit Switch Failed to Operate Properly.Cause Unknown.Limit Switch readjusted.W/830614 Ltr 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217C9121999-10-12012 October 1999 SER Input Authorizing Licensee Proposed Request to Modify Definition of Core Alteration in Section 1.0 of TS & Update Sections 3/4.1,3.4.3 & 3/4.9 to Reflect Proposed Definition Change ML20217F9091999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for LaSalle County Stations,Units 1 & 2.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212C4501999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for LaSalle County Station,Units 1 & 2.With ML20210R0671999-07-31031 July 1999 Monthly Operating Repts for July 1999 for LaSalle County Station,Units 1 & 2.With ML20210C1681999-07-0909 July 1999 Seventh Refueling Outage ASME Section XI Summary Rept ML20209H1501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for LaSalle County Station,Units 1 & 2.With ML20195J7871999-05-31031 May 1999 Monthly Operating Repts for May 1999 for LaSalle County Station,Units 1 & 2.With ML20209E1431999-05-31031 May 1999 Cycle 8 COLR, for May 1999 ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations ML20206N2071999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for LaSalle County Station,Units 1 & 2.With ML20205L8421999-03-31031 March 1999 Rev 2 to EMF-96-125, LaSalle Unit 2 Cycle 8 Reload Analysis ML20205L8301999-03-31031 March 1999 Administrative Technical Requirements App B (Amend 26) LaSalle Unit 2 Cycle 8 COLR & Reload Transient Analysis Results, for Mar 1999 ML20205R2721999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for LaSalle County Station,Units 1 & 2.With ML20205L8391999-03-22022 March 1999 Rev 2 to 960103, Neutronics Licensing Rept for LaSalle Unit 2,Cycle 8 ML20204C8141999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for LaSalle County Station,Units 1 & 2.With ML20199E4601998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for LaSalle County Station,Units 1 & 2.With ML20207C7371998-12-31031 December 1998 Annual Rept for LaSalle County Station for Jan 1998 Through Dec 1998 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20198B3801998-12-14014 December 1998 SER Accepting one-time Request for Relief from Certain Provisions of Section XI of ASME Boiler & Pressure Vessel Code,Per 10CFR50.55a for Certain Plant Safety/Relief Valves ML20206N2261998-12-0909 December 1998 LER 98-S03-00:on 981116,protected Area Was Entered Without Current Authorization for Unescorted Access Due to Programmatic Deficiency Error.Changed Badge Control Process ML20197K0981998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for LaSalle County Station,Unts 1 & 2.With ML20196B1441998-11-23023 November 1998 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Bindings of Safety-Related Power-Operated Gate Valves ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195D3191998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for LaSalle County Station.With ML20154H6781998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20153D0191998-09-18018 September 1998 Part 21 Rept Re Defect in Gap Conductance Analyses for co- Resident BWR Fuel.Initially Reported on 980917.Corrective Analyses Performed Demonstrating That Current Operating Limits Bounding from BOC to Cycle Exposure of 8 Gwd/Mtu ML20153C7621998-09-18018 September 1998 Safety Evaluation Acceping NRC Bulletin 95-002, Unexpected Clogging of RHR Pump Strainer While Operating in Suppression Pool Cooling Mode ML20153C6771998-09-17017 September 1998 Part 21 Rept Re Defect Relative to MCPR Operating Limits as Impacted by Gap Conductance of co-resident BWR Fuel at Facilities.Operating Limit for LaSalle Unit 2 & Quad Cities Unit 2 Will Be Revised as Listed ML20151W0241998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for LaSalle County Station.With ML20237E2921998-08-21021 August 1998 Special Rept:On 980811,channel 5 of Lpms Became Inoperable. Caused by Channel Failed pre-amplifier Located Inside Primary Containment at Inboard Side of Electrical Penetration E-19.Initiated Repairs of Channel ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237B4861998-07-31031 July 1998 Monthly Operating Repts for July 1998 for LaSalle County Nuclear Power Station Units 1 & 2 ML20236V7701998-07-31031 July 1998 Revised LaSalle Unit 1 Cycle 8 COLR & Reload Transient Analysis Results ML20236P8231998-07-14014 July 1998 Special Rept:From 980614-17,various Fire Rated Assemblies Were Inoperable for Period Greater than Seven Days.Caused by Test Equipment Being Routed Through Fire Doors.Established Fire Watches & on 980619 Assemblies Were Declared Operable ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20236L8041998-07-0606 July 1998 Safety Evaluation Granting Licensee 980304 Request for Second 10-yr Interval Pump & Valve IST Program Plan,Rev 2, Including Changes to 2 ASME Boiler & Pressure Vessel Code Relief Requests Previously Submitted in Rev 1 ML20236P3611998-06-30030 June 1998 Monthly Operating Repts for June 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20249C4891998-06-22022 June 1998 Special Rept:On 980522,Fire Detection Zone 1-31 Was Noted out-of-service for More than 14 Days.Detection Sys Was Taken out-of-service on 980508 to Prevent False Alarms During Hot Work Activities.Sys Was Returned to Operable Status 980528 ML20248M3101998-05-31031 May 1998 Monthly Operating Repts for May 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20236V7771998-05-31031 May 1998 Rev 1 to 24A5180, Supplemental Reload Licensing Rept for LaSalle County Station Unit 1 Reload 7 Cycle 8 ML20217Q7041998-05-0404 May 1998 Safety Evaluation Accepting Util Request to Leave Leak Chase Channels Plugged During Performance of Containment ILRT ML20247M4491998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for LaSalle County Station ML20216F4941998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for LaSalle County Station,Units 1 & 2 ML20217N6581998-03-30030 March 1998 Special Rept on Fire Detection,Deluge Sys & Fire Rated Assemblies During Period of 980303-25.Established Fire Watches Until Affected Equipment Is Returned to Operable Status ML20216D9511998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for LaSalle County Station,Units 1 & 2 ML20247M4631998-02-28028 February 1998 Rev Monthly Operating Rept for Feb 1998 for LaSalle County Station ML20203D7241998-02-20020 February 1998 Special Rept:On 980118,Fire Detection Zones 1-18 & 2-18 Taken out-of-svc to Prevent False Alarms During Hot Work Activities on Auxiliary Electric Equipment Room Ventilation Sys.Fire Watches Will Remain in Place ML20202G9851998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for LaSalle County Station,Units 1 & 2 ML20199K1651998-01-23023 January 1998 Rev 65h to Topical Rept CE-1-A, Comm Ed QA Tr 1999-09-30
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s
, Commonw::lth Edison LaSalle County Nuclear Station 2601 N. 21st. Rd.
Marseilles. lllinois 61341 Telephone 815/357-6761 August 26, 1993 l
U.S. Nuclear Regulatory Commission Attention: Document Control Desk Hashington, D.C. 20555
Dear Sir:
Licensee Event Report #92-016-01, Docket #050-374 is being submitted to your office in accordance with 10CFR50.73(a)(2)(iv).
\ ~
. V. Schmeltz i Acting Station Manager LaSalle County Station JVS/DJE/lja Enclosure xc: Nuclear Licensing Administrator NRC Resident Inspector NRC Region III Administrator INPO - Records Center IDNS Resident Inspector I
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j8P 888 h R 888 6 9 d' I PDR g
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' LICENSEE EVENT REPORT (LER) [
Form Rev 2.0 ;
Facility Name (1) Docket Number (2) Pace (3) i kaSalle County Station Unit 2 O!510101Of317!4 1 lof!0l5 Title (4) [
Peactor Scram On toss Of Air Due To An Inadecuate Out of Service Review i Event Date (5) LER Number (6) Reoort Date (7) Other Facilities Involved (8)
Year Sequential /jj// Revision f j Month Day Year /j//
ff f Month Day Year Facility Names Docket Number (s) ;
/// Number /// Number ,
015101010131713 !
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l 11 1 11 6 91 2 91 2 0I1 16 011 0l8 21 6 91 3 Ol 51 O! 0101 I I I I
ONM THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10CFR [
(Check one or more of the followino) (11) 1 20.402(b) _ 20.405(c) JL, 50.73(a)(2)(iv) _ 73.71(b) i POWER _ 20.405(a)(1)(i) _ 50.36(c)(1) _ 50.73(a)(2)(v) _ 73.71(c) !
LEVEL 20.405(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vii) Other (Specify 0 l0 i
(10) 1
_ 20.405(a)(1)Oii) _ 50.73(a)(2)fi) _ 50.73(a)(2)(vHi)(A) in Abstract '
HSiliHHHSSHSHf5HSH - '5(*unod - 5 ' hu'"") - s ' (*" M'"U m "'** *"" '"
20.405an e 50.73(ax2n n o i HHHHHHHHHHHHB - _ _ 50.73(a>(2)(x) Text)
LICENSEE CONTACT FOR THIS LER (12)
Name TELEPHONE NUMBER f AREA CODE !
Daniel Enricht. Doeratino Department. Extension 2204 8 1 1 15 31 51 71 -l 61 71 61 !
COMPLETE ONE LINE FOR EACH COMPON NT FAILURE DESCRIBE 0 IN THIS REPORT (13) l CAUSE SYSTEM COMPONENT MANUFAC- REPORTABLE !
j/ CAUSE SYSTEM COMPONENT MANUFAC- REPORTABLE TURER TO NPRDS / TURER TO NPRDS A L1F l 1 l l l l N k i l i l I l l 1 I I I l l I / I I I l l 1 1 SUPPLEMENTAL REPORT EXPECTED (14) Expected Month i Day I Year !
Submission lyes (If ves. complete EXPECTED SUBMISSION DATE) X l NO D# * (15) I !l !l {
AdSTRACT (Limit to 1400 spaces, i.e. approximately fif teen single-space typewritten lines) (16) i At 0122 on November 16, 1992. LaSalle County Station's Unit 2 scrammed from approximately 80% power following a load reduction f rom 100% power as a result of a feedwater transient that was caused by a loss of all }
Station Air (SA) Compressors. !
Operating Personnel isolated cooling water to the Unit 2 SA Compressor as part of a scheduled Out of l
Service. This resulted in cooling water being isolated from the running Unit I and Common SA Compressors due '
to the Unit 2 Turbine Building Closed Cooling Water System (TBCCW) being cross-tied to the Unit 1 and Common SA Compressors while refuel outage activities were being perfonned on the Unit 1 TBCCW System.
Due to the loss of cooling water, the Unit 1 and Common SA Compressors tripped on high lube oil temperature.
This rest.lted in a reduction of Instrument Air pressure. The loss of air pressure, combined with its subsequent restoration, resulted in a feedwater transient that resulted in a Main Turbine trip due to high l reactor water level . The turbine trip caused a reactor scram.
The root cause of this event is an inadequate review of the Out of Service. A contributing factor to the !
cause of this event is a lack of c.dministrative control over the abnormal lineup of the TBCCW Systems. The l procedure used for cross-tying the SA Compressor's cooling water to the other unit did not provide provisions for positive administrative control over this abnormal lineup nor did it provide provisions for alerting operating personnel that the abnormal lineup existed.
Corrective actions include counseling the individuals involved, and revising the procedure utilized for cross-tying SA Compressor Cooling Water to the other unit to provide provisions for positive control over this abnormal lineup. In addition, engraved plaques have been placed at the applicable SA Compressor Supply, Return, and Cross-Tie Valves to instruct operators to verify cooling water will be available to the required SA Compressors prior to repositioning them.
4 LICENSEE EVENT REPORT (LER) TEXT COWINUATf0N Fom Rev 2.0 FACILITY, NAME ('1) DOCKET NUMBrR (2) tER NUMBER (6) _
Pace (31 Year / Sequential f/j/j/ Revision j/j/j/
// Number /// Number LaSalle County Station Unit 2 015101010l31714 9l2 -
0I1 I6 -
O l1 Of 2 0F 01 5 TEXT Energy Industry Identificatien System (EIIS) codes are identified in the text as [XX)
PLANT AND SYSTEM IDENTIFICATION General Electric - Boiling Water Reactor Energy Industry Identification System (EIIS) codes are identified in the text as [XX).
A. CONDITION PRIOR TO EVENT Unit (s): 2 Event Date: 11/16/92 Event Time: 0122 Hours Reactor Mode (s): 1 Mode (s) Name: Run Power Level (s): }H B. DESCRIPTION OF EVENT LaSalle County Station Unit 2 scrammed from approximately 80% power as a result of a transient that was caused by a loss of all Station Air Compressors (SA) [LF).
The following is a list of events that lead up to and resulted in the scram of Unit 2 from approximately 900 megawatts on November 16, 1992.
On October 5,1992, the Unit 2 Turbine Building Closed Cooling Water (TBCCW) (WT) [KB] System was cross-tied to the Unit 1 and Comon SA Compressors in accordance with Step F.4 of LOP-WT-02 "Startup and Operation of the Turbine Building Closed Cooling Water System". This was perfomed in order to provide cooling to the Unit I and Comon SA Compressors while the Unit : TBCCW System was shutdown for refuel outage activities. Administrative Out of Service (005) 1-0705-91 was hung at this time to provide control over the cross-tying operation, and to ensure that the Un.t 1 SA Compressor TBCCW Supply and Return Valves remained closed to prevent connecting the running Un t 2 TBCCW System to the shutdown Unit 1 TBCCW System. In addition to hanging 005 cards on the Unit 1 SA Compressor TBCCW Valves 005 cards were hung on the Unit 1 TBCCW Pump Control Switches.
On November 14, 1992, the Operating Department comenced actions to return the Unit 1 TBCCW System to operation. TBCCW System Electrical and Mechanical Lineup Checklists were started and completed on Sunday, November 15. It was noted by the Equipment Attendant (EA, non-licensed) perf oming Mechanical Checklist LOP-WT-01M, that the SA Compressor TBCCW Cross-Tie Stop Valves OWT098 and OWT099 were open, and that the Unit 1 SA Compressor TBCCW Supply and Return Valves 1WT106 and 1WT107 were 005 closed.
Administrative DOS 1-0705-92 was cleared in order to return the Unit 1 TBCCW Pumps to service for system startup. The Unit 2 TBCCW System was to be lef t cross-tied to the Unit 1 and Common SA Compressors until it could be verified that the system was operating properly, and that there were no plans to shutdown the Unit 1 TBCCW System again. The Unit 1 TBCCW System was started on Sunday, November 15.
At approximately 0015 on November 16, the Operating Shift Crew began hanging 005 2-2202-92 on the Unit 2 SA Compressor in accordance with an established schedule for planned maintenance. Although the Operating Supervisors on shift were aware that the Unit 2 TBCCW System was supplying cooling to the running Unit 1 and Comon SA Compressors, they were not aware of the fact that 005 2-2202-92 included closing Unit 2 SA Compressor TBCCW Supply and Return Valves 2WT106 and 2WT107, which would isolate cooling water to all SA Compressors due to the cross-tied lineup in place at the time.
' t LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Form Rev 2.0 i FACILITY,NAME (1) DOCKET NUMBER (2) LER NUMBER (6) Pace (3) f Year Sequential Revision j g/// Number g//
/ Number -
Ldalle County Station Unit 2 0 l S 1 O l 010131714 9I2 -
Ol1l6 -
O l1 01 3 0F 01 S TEXT Energy Industry Identification System (EIIS) codes are identified in the text as [XX] !
l i
B. DESCRIPTION OF EVENT CONTINUED i
At approximately 0115, EAs assigned to hang 005 2-2202-92 closed Unit 2 SA Compressor TBCCW Supply and l Return Valves 2WT106 and 2WT107 (located in the Unit 2 SA Compressor Room) in accordance with the 005 i checklist and proceeded to the Unit 1 SA Compressor Room to continue hanging the 005. The EAs found the [
cross-tie valves OWT098 and OWT099 open which they had not expected, and lef t to call the Control Room.
At approximately 0118, the Unit 1 SA Compressor tripped followed approximately one minute later by a trip of the Comon SA Compressor, both tripping due to high lube oil temperature. The EAs were made aware of the SA Compressor trips via a plant page made by Control Room Personnel, and imediately took actions to restore cooling to the SA Compressors and return them to operation. !
k Upon receiving the SA Comprsssor trip alarms, Control Room Personnel imediately observed indications of ?
decreasing Instrument and Service Air Pressures. The Shif t Engineer (SE, licensed SRO) and Shif t i Supervisors (SS, licensed SRO) reported to the Control Room. The Unit 2 Nuclear Station Operator (NSO, licensed RO) began reducing reactor power from 100'4 by reducing reactor recirculation (RR) [AD] flow. A reactor water level transient began due to the reduction in Instrument Air (IA) [LD) Pressure which caused: the 2B Turbine Driven Reactor Feed Pump (TDRFP) (FW) [JK), which was in manual, to stop pumping due to a loss of control air pressure; the Feedwater Minimum Flow Valves to fall open; and the Heater Drain (HD) [$M] Pump Forward Valves to fail closed. The extra NSO in the Control Room took a position !
at the Feedwater Control Panel to respond to the transient. The 'A' TDRFP, which was in three element control continued to pump water to the reactor, and the Motor Driven Reactor Feed Pump (MDRFP) was manually started due to the loss of flow from the 'B' TDRFP and the decreasing reactor water level.
Instrument Air Pressure decreased to approximately 60 psig before the SA Compressors were restarted. !
The Control Room personnel utilized LOA-IA-01 " Loss Of Instrument Air", and LOA-SA-01, " Loss Of Service !
Air", during the transient. Upon restoration of instrument air, the 'B' TDRFP began to pump to the reactor again until it was manually tripped due to increasing reactor water level. In addition, the Feed Pump Minimum Flow Valves went closed and the Heater Drain Pump Forward Valves went open due to the restoration of Instrument Air Pressure, both contributing to a high reactor water level condition. The operation of the Feedwater and Heater Drain System components was consistent with the reduction and f
restoration of air pressure.
l, At approximately 0123, the Unit 2 Main Turbine (TG) [TA] tripped due to high reactor water level (Level '
8, 45S.S" reactor water level) which resulted in a reactor scram due to Turbine Stop Valve (EH) [TG) closure. Reactor water level reached a maximum level of approximately +60", followed by a decrease of !
level to a minimum of approximately +2" caused by " shrink" during the turbine trip and scram pressure I transient. This resulted in a reactor low level scram .ignal (Level 3, +12.S"). Recovery actions from ;
the scram were nonnal and reactor parameters were stabilized.
Af ter the scram, the "U" Safety Relief Valve (SRV) (NB) [AD), which is a Group 1 Safety Relief Valve, lifted. Group 1 Safety Relief Valve's have the lowest relief pressure settings and would be 1xpected to lift first during a pressure transient. Review of the pressure transient indicates that the Safety f Relief Valve operated consistert with its design setpoint.
During the transient the Reactor Core Isolation Cooling System (RCIC) (RI) [BN] initiated due to an l instrument rack pressure spike which caused an invalid low reactor level (Level 2 - S0") to be sensed. }
The RCIC Turbine was imediately tripped by the NSO in the Control Room before the system injected into ;
the reactor vessel. The level spike resulted from pressure waves traveling from the Turbine Control and j Stop Valves up the steam lines into the Reactor Pressure Vessel Dome. General Electric, the Nuclear I Steam Supply Syste.n (NSSS) Supplier, has indicated that these spikes are expected and were present on i the initial cycle startup tests.
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_ LICENSEE EVENT REPORT (LER) TEXT CONVINUATION Fom Rev 2.0 FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) Paoe (3)
Year // Sequential /j/j/ Revision j/jj/
// Number f
/// Number LaSalle County Station Unit 2 015 i 0 l 010 l 317! 4 912 - 0I116 -
0 11 01 4 0F 01 5 TEXT Energy Industry Identificatioe System (EIIS) codes are identified in the text as [XX)
B. DESCRIPTION OF EVENT CONTINUE 0 It should be noted that Unit 1 experienced the same reduction in Instrument and Service Air Pressures ;
during the event. However, Unit I was in its fif th refuel outage with the reactor defueled at the time, ,
and experienced no adverse consequences.
This event is reportable pursuant to the requirement of 10CFRSO.73(a)(2)(iv) due to the automatic actuation of the Reactor Protection System (RPS) (RP) [JC).
C. APPARENT CAUSE OF EVENT The cause of this event was the reduction in Instrument Air pressure which caused a Feedwater transient. This resulted in a trip of the Main Turbine due to high reactor water level and a subsequent reactor scram.
The loss of, Instrument Air pressure was the result of trips of the two running SA Compressors due to high lube oil temperature as a result of the loss of all cooling water.
The loss of all cooling water to the SA Compressors was caused by the closure of the Unit 2 SA Compressor TBCCW Supply and Return Valves by Operating Personnel as part of a scheduled 005 while the Unit 2 TBCCW System vai cross-tied to supply cooling water to the Unit 1 and Coninon SA Compressors.
This was caused by a lack of realization on the part of the preparers and the personnel hanging OOS e 2-2202-92 that closing these valves would isolate cooling water to the running SA Compressors. !
The Out of Services at LaSalle Station are prepared by qualified individuals well in advance of the time they will be actually utilized. This methodology allows a thorough review, without any time pressure, :
to ensure that the equipment will be properly isolated. When the Out of Service is to be hung, the unit supervisor reviews the equipment being removed from service to ensure that it is not required for plant operations.
The root cause of this event was an inadequate review of the Out of Service. In this event, the Out of Service was written assuming a normal cooling water line-up. The preparer did not identify the possible impact of the Out of Service if the cooling water was in a non-normal configuration. When the Out of Service was hung, the unit supervisor was aware of the abnormal configuration, but not how this would be affected. Because no previous dif ficulties have been experienced as a result of the interaction between l two off normal conditions, the individuals did not put enough detail into their reviews to prevent the probl em.
D. SAFETY ANALYSIS OF EVENT Turbine trip with bypass is classified as a transient of moderate frequency in Chapter 15 of the Update ;
Final Safety Analysis Report (UFSAR). The turbine trip in this event initiated the reactor scram as required. Following the scram, reactor pressure was controlled by the Safety Relief Valve and Turbine Bypass Valves. These events are consistent with the UFSAR analysis of this event. ,
o r
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LICENSEE EVENT REPORT (LERI VEXT CONTfNUATION Form Rev 2.0 FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) Paoe t3) l Year /// Sequential /// Revision j jjj/
// Number j///
ff Number LaSelle County Station Unit 2 015101010131714 912 - 0I1I6 -
0 11 01 5 0F 01 5 i VEXT Energy Industry Identification System (EIIS) codes are identified in the text as [XXJ D. SAFETY ANALYSIS OF EVENT CONTINUED !
Safety features were initiated as designed and expected, with the exception of the RCIC System initiation which occurred due to a pressure spike sensed in the variable leg of its associated level !
instruments. ,
E. CORRECTIVE ACTIONS >
The individuals involved have been counseled on the need to thoroughly consider the effects of their actions, j All Shif t Supervisors have been briefed on the need to ensure that they have thorough understanding of (
the ef fect of Out of Services hung on their shif t. ,
All Out of Service preparers have been counselled on the need to consider the effects of boundary isolations on systems where there is more than one design configuration. Where such configurations exist, the need for a heightened level of review will be clearly identified on the Out of Service before j it is delivered to the shift supervisor. j i
LOP-WT-02 "Startup and Operation of the Turbine Building Closed Cooling Water System" will be revised to I include provisions for positive control and to alert operators of the abnormal cross-tied lineup of the SA Compressor TBCCW by means of established station administrative methcds and procedures. Action Item Reccrd (AIR) 374-180-92-08201 will track procedure revisions.
Engraved plaques have been installed at each of the applicable SA Compressor TBCCW Supply, Return, and Cross-tie Valves (lWT106,1WT107, 2WT106, 2WT107, OWT098, and OWT099) instructing operators to verify that coolirg will be available to the required SA Compressors prior to repositioning them. AIR -
374-163-92-08202 will track completion of the installation of the engraved plaques. l A letter will be sent to all Shif t Engineers with system procedure assignments asking them to review their systems for similar physical configurations that could result in inadvertent system / unit crossties. AIR 374-180-92-08233 will track completion of these reviews.
F. PREVIOUS EVENTS A search of the LER/DVR data base indicated no previous similar events.
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G. COMPONENT FAILURE DATA None.
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l CAESE CODES i
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05000374/LER-1992-016 | LER 92-016-01:on 921116,reactor Scram on Loss of Air Occurred.Caused by Inadequate Out of Svc Review & Lack of Administrative Controls.Procedures Revised & Individuals Involved counseled.W/930826 Ltr | |
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