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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B1481993-07-30030 July 1993 LER 93-012-00:on 930702,reactor Core Isolation Cooling Sys Declared Inoperable Due to Associated Bus Voltage Dropping Below TS Limits.Sent Operator to Cycle Timer Which Caused Affected Contact to reclose.W/930730 Ltr ML20045D9331993-07-0202 July 1993 LER 93-004-00:on 930604,unexpected CRD Low Charging Water Header Scram Received Followed by Charging Water Header A2/B2 Alarm.Caused by Crud or Foreign Matl Passing Through Suction Filter.Filters Cleaned & reused.W/930702 ML20045D7501993-06-23023 June 1993 LER 93-003-00:on 930524,Div 1 ECCS Initiation Signal Received & LPCS Pump,Lpci Pump 2A & EDG Unit 0 Automatically Started.Caused by Personnel Error.Pumps Secured & Event Documented in Personnel file.W/930623 Ltr ML20044E4161993-05-28028 May 1993 LER 92-009-01:on 920923,spurious Auto Start of CR Ventilation Emergency make-up Train Occurred Due to High Radiation Spike.Radiation Monitor Circuit modified.W/930528 Ltr ML20044E4191993-05-21021 May 1993 LER 93-011-00:on 930423,manual Scram Initiated.Caused by Disconnected Linkage on Valve Positioner on Heater Drain Valve Due to Loose Jam Nut.Tailgate Session Will Be Held W/ Instrument Maint Dept Re Jam nuts.W/930521 Ltr ML20044D5161993-05-15015 May 1993 LER 92-007-01:on 920613,high Radiation Spike Received from CR Ventilation Process Radiation Monitor,Initiating Emergency Makeup Train B.Caused by Normal Variations in Radiation Readings.Spike modified.W/930515 Ltr ML20044D5571993-05-14014 May 1993 LER 93-010-00:on 930414,DG Cooling Water Pump Automatically Tripped on Magnetic Overload.Caused by Inexperienced Trainee in Operation of Control Lever.Lesson Plans & Training Programs for Operators to Be reviewed.W/930514 Ltr ML20044C9801993-05-0707 May 1993 LER 91-010-01:on 910719 & 0805,CR a Ventilation Emergency Makeup Fan auto-started on Spurious Trip of CR Air Intake Process Radiation Monitor.Caused by Normal Variations in Background Radiation.Supply Board replaced.W/930507 Ltr ML20044B6161993-02-25025 February 1993 LER 93-002-00:on 930126,Unit 1 Manual Scram Due to a SRV Being Stuck Open Due to Duct Tape Being Over Actuators Air Valve Manifold Exhaust Port.Maint Procedures That Involve Cleanliness reviewed.W/930225 Ltr ML20024G9771991-05-10010 May 1991 LER 91-005-00:on 910410,determined That Tech Spec Required Surveillance of Suppression Chamber Oxygen Sampling Missed. Caused by Inadequate Review of Tech Spec Change.Drywell & Suppression Chamber Checked for oxygen.W/910510 Ltr ML20044A3851990-06-25025 June 1990 LER 90-008-00:on 900525,Tech Spec Hourly Fire Watch Missed Due to Miscommunications Between Security Personnel & Radiation Protection Personnel.Fire Watch re-established & Memo issued.W/900625 Ltr ML20043F1721990-06-0505 June 1990 LER 90-009-00:on 900510,RWCU Outboard Suction Isolation Valve 2G33-F004 Auto Closed Which Tripped RWCU Pump B. Caused by Procedure Deficiency.Procedure LTS-500-209 Will Be revised.W/900605 Ltr ML20043F1281990-06-0101 June 1990 LER 90-009-00:on 900511,apparent Ruptured Diaphragm Found on Pressure Differential Switch in RCIC Steam Line.Caused by Torn Diaphragm Inside Switch.Replacement Switch Installed, Calibr & Functionally Tested satisfactorily.W/900608 Ltr ML20043B5681990-05-23023 May 1990 LER 89-027-01:on 891113,primary Containment Isolation Sys Group 1 Isolation Occurred During Surveillance Testing. Caused by Burnt Out Window Light Bulbs on Alarm Window. Light Bulbs Replaced & Jumpers installed.W/900523 Ltr ML20043A7721990-05-18018 May 1990 LER 90-007-00:on 900421,reactor Protection Sys Bus a Transfer & Reactor Recirculation Hydraulic Power Unit a Inboard Isolation Valves Closed,Causing Partial Group II isolation.Out-of-svc Procedure revised.W/900518 Ltr ML20043D0591990-05-18018 May 1990 LER 90-008-00:on 900502,ESF Actuation of Control Room B Emergency Ctk Ventilation Makeup Fan Occurred.Caused by Procedure deficiency.LTS-800-205 & Similar Procedures Will Be revised.W/900601 Ltr ML20042H0211990-05-10010 May 1990 LER 90-006-00:on 900412,loop a Primary Containment Chilled Water Sys Inboard Isolation Valves & Reactor Bldg Closed Cooling Water Sys Inboard Isolation Valve Went Closed.Caused by Inadequate Procedure.Procedures revised.W/900510 Ltr ML20042F9001990-05-0404 May 1990 LER 90-005-00:on 900411,experienced Loss of Dc Power to Portion of Div I Primary Containment Isolation Sys Logic Which Resulted in Isolation Signal & Actuation.Caused by Failure to Update Drawings & procedures.W/900504 Ltr ML20042F1941990-04-30030 April 1990 LER 89-025-01:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Door Containing Undervoltage Relays Closed.Caused by Misalignment of Door.Door Repaired. W/900430 Ltr ML20012D5341990-03-16016 March 1990 LER 90-003-01:on 900201,RCIC Isolation Signal Occurred During Warmup.Caused by Spurious High Steam Flow Signal.Rcic Sys Piping Integrity Verified & Isolation Logic Reset.W/ 900316 Ltr ML20012D5371990-03-16016 March 1990 LER 90-002-01:on 900129,oil in Diesel Generator Governor 1A Found to Be Low & Could Not Be Seen in Sight Glass.Caused by Slow Leak from Compensation Needle Valve Plug.Proper Amount of Oil Added & Operability Test performed.W/900316 Ltr ML20012C4931990-03-15015 March 1990 LER 90-004-00:on 900213,control Room B HVAC Intake Radiation Monitor Lost Power Causing auto-start of Emergency make-up Train B.Caused by Blown Fuses.Fuses Replaced.Logic Revs for Radiation Monitors Will Be installed.W/900315 Ltr ML20012B6501990-03-0909 March 1990 LER 90-002-00:on 900209,Operating Surveillance LOS-TG-W1 Determined to Have Exceeded Required Testing Interval,Per Tech Spec 3/4.7.10.Caused by Personnel Error.Personnel Counseled & Ref Procedures Will Be revised.W/900309 Ltr ML20012B5521990-03-0808 March 1990 LER 90-001-00:on 900206,full Reactor Scram Occurred During Instrument Surveillance Testing.Caused by Actuation of APRM E Trip Circuitry.Shutdown Margin Revised & Caution Card Placed on Control Room Bench board.W/900308 Ltr ML20011F8251990-03-0202 March 1990 LER 90-003-00:on 900201,RCIC Received Div 2 Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal Generated When Steam/Water Mixture Admitted to RCIC Steam Line.Isolation Logic reset.W/900302 Ltr ML20011F5551990-02-28028 February 1990 LER 90-002-00:on 900129,after Filling Diesel Generator 1A Governor W/Oil,Generator Started & Declared Inoperable. Caused by Slow Leak Coming from Compensation Needle Valve Plug.Oil Added & Plug Washer replaced.W/900228 Ltr ML20006F5951990-02-21021 February 1990 LER 90-001-00:on 900122,RWCU Sys Received Div 1 Leakage Detection Ambient Temp High Isolation Signal,Causing Trips of RWCU Pumps a & C.Caused by Broken Thermocouple Input Lead.Lead Wire Reconnected & Isolation reset.W/900221 Ltr ML20011F4921990-02-16016 February 1990 LER 89-013-01:on 890907,Group I Isolation Received During Performance of Instrument Surveillance LIS-MS-401.Caused by Depressurization of Main Steam Line Low Pressure Switch. Surveillance Revised to Split Into Two parts.W/900216 Ltr ML20006E4501990-02-15015 February 1990 LER 89-010-01:on 890715 & 17,voltage Oscillations Noted on Div II Battery Charger,Resulting in Inoperability of HPCS Sys.Caused by Failure of Charger in High Voltage Shutdown Relay.Charger Energized & Relay replaced.W/900215 Ltr ML20006E4451990-02-14014 February 1990 LER 89-009-01:on 890619,diaphragm Leak Discovered in RCIC Steam Line High Flow Isolation Switch.Caused by 1 & 1/2-inch Tear in Diaphragm.Pressure Differential Switch Replaced & Calibr.Reported Per NRC Bulletin 86-002.W/900214 Ltr ML20006E3981990-02-14014 February 1990 LER 89-008-01:on 890228,reactor Vessel Low Water Level 2 Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.Channel Placed in Tripped Condition & All Static-O-Ring Pressure Switches to Be replaced.W/900214 Ltr ML20006E3951990-02-14014 February 1990 LER 89-010-01:on 890303,automatic Depressurization Sys Permissive Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.All Static-O-Ring Reactor Vessel Level Switches Will Be replaced.W/900214 Ltr ML19354D8361990-01-15015 January 1990 LER 89-018-00:on 891216,plant 250-volt Battery & RCIC Sys Declared Inoperable Due to Low Battery Electrolyte Temps. Caused by Failure of Div I Switchgear Heat Removal Sys Damper Actuators.Air Intake Dampers closed.W/900115 Ltr ML20042D3921990-01-0404 January 1990 LER 89-011-01:on 890826,spurious Reactor Protection Sys Actuation Occurred.Definite Cause of Trip Not Determined. Brief Disturbance in Reactor Protection Sys Allowed Some Contactors to Trip.Procedure revised.W/900104 Ltr ML20005E2741989-12-22022 December 1989 LER 89-028-00:on 891204,RHR Shutdown Cooling Suction Header Outboard Isolation Valve Automatically Isolated.Caused by Miscommunication Between Technician & Station Operator.Task Force Developed to Review event.W/891222 Ltr ML19351A6301989-12-15015 December 1989 LER 89-006-01:on 890214,reactor Vessel Low Water Level 3 Switch Setpoint Found Out of Tolerance.Caused by Setpoint Drift.Level Switch to Be Replaced by Analog Trip Sys During First Quarter 1990.W/891215 Ltr ML20011D1341989-12-14014 December 1989 LER 89-017-00:on 891117,flow Switch FS-2E22-N006 Found W/ Setpoint Out of Tolerance Above Reject Limit.Caused by Setpoint Drift.Work Request Written to Replace Flow Switch. W/891214 Ltr ML19351A6751989-12-12012 December 1989 LER 89-027-00:on 891113,primary Containment Isolation Sys Group I Isolation Occurred While Performing Instrument Surveillance.Caused by Loss of Power to Leak Detection Sys Logic.Isolation reset.W/891213 Ltr ML19332F0081989-12-0808 December 1989 LER 89-016-00:on 891109,RWCU Isolation Occurred While Instrument Surveillance on Ventilation Differential Temp Isolation Functional Test in Progress.Caused by Faulty Thermocouple.Thermocouple repaired.W/891208 Ltr ML20005D6621989-12-0606 December 1989 LER 89-026-00:on 891106,inadvertent Primary Containment Isolation Actuation Occurred While Clearing out-of-svc. Caused by Inadequate Logic Setup During Mod Installation. Trip Status & Output Switches repositioned.W/891206 Ltr ML19332F2431989-12-0101 December 1989 LER 89-025-00:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Equipment Operator Closed Door Containing Relays.Caused by Misalignment of Door.Isolations Reset,Bus Energized & Circuit Logic tested.W/891201 Ltr ML19332E6581989-11-29029 November 1989 LER 89-015-00:on 891030,shift Control Room Engineer Noted That Quarterly Standby Liquid Control Operating Surveillance LOS-SC-Q1 Was Past Critical Date.Caused by Clerical Data Entry Error.Missed Surveillance performed.W/891129 Ltr ML19332D5181989-11-22022 November 1989 LER 89-018-01:on 890515,RCIC Received Div I & Div II Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal When Steam Added to RCIC Steam Line. Special Test Initiated.Isolation Logic reset.W/891122 Ltr ML19327C2601989-11-17017 November 1989 LER 89-014-00:on 891020,primary Containment Isolation Sys Group 4 Isolation Occurred Causing Isolation Dampers to Close.Caused by Opening of Div 2 125-volt Dc Breaker.Power Supply replaced.W/891117 Ltr ML19325F3411989-11-13013 November 1989 LER 89-024-00:on 891013 & 30,unsealed Openings in Main Control Room Floor & Main Control Room West Wall Discovered. Caused by Wide Gap Between Structural Beam & Cable Tray. Openings Sealed & Fire Watch established.W/891113 Ltr ML19324C1751989-11-0808 November 1989 LER 89-012-01:on 890309,diaphragm Leak Found in Pressure Differential Switch 1E31-N013BB.Caused by Tear Found in Diaphragm.Replacement Switch Installed,Calibr & Functionally Tested satisfactorily.W/891108 Ltr ML20024E9121983-08-26026 August 1983 LER 83-093/03L-0:on 830801,discovered full-in Indication on Core Display for Control Rod 34-47 Inoperable.Caused by Failed Switching Transistor on Data Memory Board 19.Data Memory Board replaced.W/830826 Ltr ML20024B8381983-07-0505 July 1983 LER 83-060/03L-0:on 830606,following Turbine Trip & Scram Due to High Vibration on Main Turbine,Reactor Recirculation Breaker 4B Closed.Cause Undetermined.Auxiliary Contacts cleaned.W/830705 Ltr ML20024B0721983-06-16016 June 1983 Updated LER 83-012/03X-1:on 830210,w/reactor in Cold Shutdown,Setpoints for Switches 1E31-N612A/B Found Above Tech Spec Limits.Cause Unknown.Switches calibr.W/830616 Ltr ML20024A6961983-06-14014 June 1983 LER 83-051/03L-0:on 830516,reactor Protection Sys Trip Channel H2 Limit Switch Failed to Operate Properly.Cause Unknown.Limit Switch readjusted.W/830614 Ltr 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046B1481993-07-30030 July 1993 LER 93-012-00:on 930702,reactor Core Isolation Cooling Sys Declared Inoperable Due to Associated Bus Voltage Dropping Below TS Limits.Sent Operator to Cycle Timer Which Caused Affected Contact to reclose.W/930730 Ltr ML20045D9331993-07-0202 July 1993 LER 93-004-00:on 930604,unexpected CRD Low Charging Water Header Scram Received Followed by Charging Water Header A2/B2 Alarm.Caused by Crud or Foreign Matl Passing Through Suction Filter.Filters Cleaned & reused.W/930702 ML20045D7501993-06-23023 June 1993 LER 93-003-00:on 930524,Div 1 ECCS Initiation Signal Received & LPCS Pump,Lpci Pump 2A & EDG Unit 0 Automatically Started.Caused by Personnel Error.Pumps Secured & Event Documented in Personnel file.W/930623 Ltr ML20044E4161993-05-28028 May 1993 LER 92-009-01:on 920923,spurious Auto Start of CR Ventilation Emergency make-up Train Occurred Due to High Radiation Spike.Radiation Monitor Circuit modified.W/930528 Ltr ML20044E4191993-05-21021 May 1993 LER 93-011-00:on 930423,manual Scram Initiated.Caused by Disconnected Linkage on Valve Positioner on Heater Drain Valve Due to Loose Jam Nut.Tailgate Session Will Be Held W/ Instrument Maint Dept Re Jam nuts.W/930521 Ltr ML20044D5161993-05-15015 May 1993 LER 92-007-01:on 920613,high Radiation Spike Received from CR Ventilation Process Radiation Monitor,Initiating Emergency Makeup Train B.Caused by Normal Variations in Radiation Readings.Spike modified.W/930515 Ltr ML20044D5571993-05-14014 May 1993 LER 93-010-00:on 930414,DG Cooling Water Pump Automatically Tripped on Magnetic Overload.Caused by Inexperienced Trainee in Operation of Control Lever.Lesson Plans & Training Programs for Operators to Be reviewed.W/930514 Ltr ML20044C9801993-05-0707 May 1993 LER 91-010-01:on 910719 & 0805,CR a Ventilation Emergency Makeup Fan auto-started on Spurious Trip of CR Air Intake Process Radiation Monitor.Caused by Normal Variations in Background Radiation.Supply Board replaced.W/930507 Ltr ML20044B6161993-02-25025 February 1993 LER 93-002-00:on 930126,Unit 1 Manual Scram Due to a SRV Being Stuck Open Due to Duct Tape Being Over Actuators Air Valve Manifold Exhaust Port.Maint Procedures That Involve Cleanliness reviewed.W/930225 Ltr ML20024G9771991-05-10010 May 1991 LER 91-005-00:on 910410,determined That Tech Spec Required Surveillance of Suppression Chamber Oxygen Sampling Missed. Caused by Inadequate Review of Tech Spec Change.Drywell & Suppression Chamber Checked for oxygen.W/910510 Ltr ML20044A3851990-06-25025 June 1990 LER 90-008-00:on 900525,Tech Spec Hourly Fire Watch Missed Due to Miscommunications Between Security Personnel & Radiation Protection Personnel.Fire Watch re-established & Memo issued.W/900625 Ltr ML20043F1721990-06-0505 June 1990 LER 90-009-00:on 900510,RWCU Outboard Suction Isolation Valve 2G33-F004 Auto Closed Which Tripped RWCU Pump B. Caused by Procedure Deficiency.Procedure LTS-500-209 Will Be revised.W/900605 Ltr ML20043F1281990-06-0101 June 1990 LER 90-009-00:on 900511,apparent Ruptured Diaphragm Found on Pressure Differential Switch in RCIC Steam Line.Caused by Torn Diaphragm Inside Switch.Replacement Switch Installed, Calibr & Functionally Tested satisfactorily.W/900608 Ltr ML20043B5681990-05-23023 May 1990 LER 89-027-01:on 891113,primary Containment Isolation Sys Group 1 Isolation Occurred During Surveillance Testing. Caused by Burnt Out Window Light Bulbs on Alarm Window. Light Bulbs Replaced & Jumpers installed.W/900523 Ltr ML20043A7721990-05-18018 May 1990 LER 90-007-00:on 900421,reactor Protection Sys Bus a Transfer & Reactor Recirculation Hydraulic Power Unit a Inboard Isolation Valves Closed,Causing Partial Group II isolation.Out-of-svc Procedure revised.W/900518 Ltr ML20043D0591990-05-18018 May 1990 LER 90-008-00:on 900502,ESF Actuation of Control Room B Emergency Ctk Ventilation Makeup Fan Occurred.Caused by Procedure deficiency.LTS-800-205 & Similar Procedures Will Be revised.W/900601 Ltr ML20042H0211990-05-10010 May 1990 LER 90-006-00:on 900412,loop a Primary Containment Chilled Water Sys Inboard Isolation Valves & Reactor Bldg Closed Cooling Water Sys Inboard Isolation Valve Went Closed.Caused by Inadequate Procedure.Procedures revised.W/900510 Ltr ML20042F9001990-05-0404 May 1990 LER 90-005-00:on 900411,experienced Loss of Dc Power to Portion of Div I Primary Containment Isolation Sys Logic Which Resulted in Isolation Signal & Actuation.Caused by Failure to Update Drawings & procedures.W/900504 Ltr ML20042F1941990-04-30030 April 1990 LER 89-025-01:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Door Containing Undervoltage Relays Closed.Caused by Misalignment of Door.Door Repaired. W/900430 Ltr ML20012D5341990-03-16016 March 1990 LER 90-003-01:on 900201,RCIC Isolation Signal Occurred During Warmup.Caused by Spurious High Steam Flow Signal.Rcic Sys Piping Integrity Verified & Isolation Logic Reset.W/ 900316 Ltr ML20012D5371990-03-16016 March 1990 LER 90-002-01:on 900129,oil in Diesel Generator Governor 1A Found to Be Low & Could Not Be Seen in Sight Glass.Caused by Slow Leak from Compensation Needle Valve Plug.Proper Amount of Oil Added & Operability Test performed.W/900316 Ltr ML20012C4931990-03-15015 March 1990 LER 90-004-00:on 900213,control Room B HVAC Intake Radiation Monitor Lost Power Causing auto-start of Emergency make-up Train B.Caused by Blown Fuses.Fuses Replaced.Logic Revs for Radiation Monitors Will Be installed.W/900315 Ltr ML20012B6501990-03-0909 March 1990 LER 90-002-00:on 900209,Operating Surveillance LOS-TG-W1 Determined to Have Exceeded Required Testing Interval,Per Tech Spec 3/4.7.10.Caused by Personnel Error.Personnel Counseled & Ref Procedures Will Be revised.W/900309 Ltr ML20012B5521990-03-0808 March 1990 LER 90-001-00:on 900206,full Reactor Scram Occurred During Instrument Surveillance Testing.Caused by Actuation of APRM E Trip Circuitry.Shutdown Margin Revised & Caution Card Placed on Control Room Bench board.W/900308 Ltr ML20011F8251990-03-0202 March 1990 LER 90-003-00:on 900201,RCIC Received Div 2 Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal Generated When Steam/Water Mixture Admitted to RCIC Steam Line.Isolation Logic reset.W/900302 Ltr ML20011F5551990-02-28028 February 1990 LER 90-002-00:on 900129,after Filling Diesel Generator 1A Governor W/Oil,Generator Started & Declared Inoperable. Caused by Slow Leak Coming from Compensation Needle Valve Plug.Oil Added & Plug Washer replaced.W/900228 Ltr ML20006F5951990-02-21021 February 1990 LER 90-001-00:on 900122,RWCU Sys Received Div 1 Leakage Detection Ambient Temp High Isolation Signal,Causing Trips of RWCU Pumps a & C.Caused by Broken Thermocouple Input Lead.Lead Wire Reconnected & Isolation reset.W/900221 Ltr ML20011F4921990-02-16016 February 1990 LER 89-013-01:on 890907,Group I Isolation Received During Performance of Instrument Surveillance LIS-MS-401.Caused by Depressurization of Main Steam Line Low Pressure Switch. Surveillance Revised to Split Into Two parts.W/900216 Ltr ML20006E4501990-02-15015 February 1990 LER 89-010-01:on 890715 & 17,voltage Oscillations Noted on Div II Battery Charger,Resulting in Inoperability of HPCS Sys.Caused by Failure of Charger in High Voltage Shutdown Relay.Charger Energized & Relay replaced.W/900215 Ltr ML20006E4451990-02-14014 February 1990 LER 89-009-01:on 890619,diaphragm Leak Discovered in RCIC Steam Line High Flow Isolation Switch.Caused by 1 & 1/2-inch Tear in Diaphragm.Pressure Differential Switch Replaced & Calibr.Reported Per NRC Bulletin 86-002.W/900214 Ltr ML20006E3981990-02-14014 February 1990 LER 89-008-01:on 890228,reactor Vessel Low Water Level 2 Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.Channel Placed in Tripped Condition & All Static-O-Ring Pressure Switches to Be replaced.W/900214 Ltr ML20006E3951990-02-14014 February 1990 LER 89-010-01:on 890303,automatic Depressurization Sys Permissive Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.All Static-O-Ring Reactor Vessel Level Switches Will Be replaced.W/900214 Ltr ML19354D8361990-01-15015 January 1990 LER 89-018-00:on 891216,plant 250-volt Battery & RCIC Sys Declared Inoperable Due to Low Battery Electrolyte Temps. Caused by Failure of Div I Switchgear Heat Removal Sys Damper Actuators.Air Intake Dampers closed.W/900115 Ltr ML20042D3921990-01-0404 January 1990 LER 89-011-01:on 890826,spurious Reactor Protection Sys Actuation Occurred.Definite Cause of Trip Not Determined. Brief Disturbance in Reactor Protection Sys Allowed Some Contactors to Trip.Procedure revised.W/900104 Ltr ML20005E2741989-12-22022 December 1989 LER 89-028-00:on 891204,RHR Shutdown Cooling Suction Header Outboard Isolation Valve Automatically Isolated.Caused by Miscommunication Between Technician & Station Operator.Task Force Developed to Review event.W/891222 Ltr ML19351A6301989-12-15015 December 1989 LER 89-006-01:on 890214,reactor Vessel Low Water Level 3 Switch Setpoint Found Out of Tolerance.Caused by Setpoint Drift.Level Switch to Be Replaced by Analog Trip Sys During First Quarter 1990.W/891215 Ltr ML20011D1341989-12-14014 December 1989 LER 89-017-00:on 891117,flow Switch FS-2E22-N006 Found W/ Setpoint Out of Tolerance Above Reject Limit.Caused by Setpoint Drift.Work Request Written to Replace Flow Switch. W/891214 Ltr ML19351A6751989-12-12012 December 1989 LER 89-027-00:on 891113,primary Containment Isolation Sys Group I Isolation Occurred While Performing Instrument Surveillance.Caused by Loss of Power to Leak Detection Sys Logic.Isolation reset.W/891213 Ltr ML19332F0081989-12-0808 December 1989 LER 89-016-00:on 891109,RWCU Isolation Occurred While Instrument Surveillance on Ventilation Differential Temp Isolation Functional Test in Progress.Caused by Faulty Thermocouple.Thermocouple repaired.W/891208 Ltr ML20005D6621989-12-0606 December 1989 LER 89-026-00:on 891106,inadvertent Primary Containment Isolation Actuation Occurred While Clearing out-of-svc. Caused by Inadequate Logic Setup During Mod Installation. Trip Status & Output Switches repositioned.W/891206 Ltr ML19332F2431989-12-0101 December 1989 LER 89-025-00:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Equipment Operator Closed Door Containing Relays.Caused by Misalignment of Door.Isolations Reset,Bus Energized & Circuit Logic tested.W/891201 Ltr ML19332E6581989-11-29029 November 1989 LER 89-015-00:on 891030,shift Control Room Engineer Noted That Quarterly Standby Liquid Control Operating Surveillance LOS-SC-Q1 Was Past Critical Date.Caused by Clerical Data Entry Error.Missed Surveillance performed.W/891129 Ltr ML19332D5181989-11-22022 November 1989 LER 89-018-01:on 890515,RCIC Received Div I & Div II Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal When Steam Added to RCIC Steam Line. Special Test Initiated.Isolation Logic reset.W/891122 Ltr ML19327C2601989-11-17017 November 1989 LER 89-014-00:on 891020,primary Containment Isolation Sys Group 4 Isolation Occurred Causing Isolation Dampers to Close.Caused by Opening of Div 2 125-volt Dc Breaker.Power Supply replaced.W/891117 Ltr ML19325F3411989-11-13013 November 1989 LER 89-024-00:on 891013 & 30,unsealed Openings in Main Control Room Floor & Main Control Room West Wall Discovered. Caused by Wide Gap Between Structural Beam & Cable Tray. Openings Sealed & Fire Watch established.W/891113 Ltr ML19324C1751989-11-0808 November 1989 LER 89-012-01:on 890309,diaphragm Leak Found in Pressure Differential Switch 1E31-N013BB.Caused by Tear Found in Diaphragm.Replacement Switch Installed,Calibr & Functionally Tested satisfactorily.W/891108 Ltr ML20024E9121983-08-26026 August 1983 LER 83-093/03L-0:on 830801,discovered full-in Indication on Core Display for Control Rod 34-47 Inoperable.Caused by Failed Switching Transistor on Data Memory Board 19.Data Memory Board replaced.W/830826 Ltr ML20024B8381983-07-0505 July 1983 LER 83-060/03L-0:on 830606,following Turbine Trip & Scram Due to High Vibration on Main Turbine,Reactor Recirculation Breaker 4B Closed.Cause Undetermined.Auxiliary Contacts cleaned.W/830705 Ltr ML20024B0721983-06-16016 June 1983 Updated LER 83-012/03X-1:on 830210,w/reactor in Cold Shutdown,Setpoints for Switches 1E31-N612A/B Found Above Tech Spec Limits.Cause Unknown.Switches calibr.W/830616 Ltr ML20024A6961983-06-14014 June 1983 LER 83-051/03L-0:on 830516,reactor Protection Sys Trip Channel H2 Limit Switch Failed to Operate Properly.Cause Unknown.Limit Switch readjusted.W/830614 Ltr 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217C9121999-10-12012 October 1999 SER Input Authorizing Licensee Proposed Request to Modify Definition of Core Alteration in Section 1.0 of TS & Update Sections 3/4.1,3.4.3 & 3/4.9 to Reflect Proposed Definition Change ML20217F9091999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for LaSalle County Stations,Units 1 & 2.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212C4501999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for LaSalle County Station,Units 1 & 2.With ML20210R0671999-07-31031 July 1999 Monthly Operating Repts for July 1999 for LaSalle County Station,Units 1 & 2.With ML20210C1681999-07-0909 July 1999 Seventh Refueling Outage ASME Section XI Summary Rept ML20209H1501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for LaSalle County Station,Units 1 & 2.With ML20195J7871999-05-31031 May 1999 Monthly Operating Repts for May 1999 for LaSalle County Station,Units 1 & 2.With ML20209E1431999-05-31031 May 1999 Cycle 8 COLR, for May 1999 ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations ML20206N2071999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for LaSalle County Station,Units 1 & 2.With ML20205L8421999-03-31031 March 1999 Rev 2 to EMF-96-125, LaSalle Unit 2 Cycle 8 Reload Analysis ML20205L8301999-03-31031 March 1999 Administrative Technical Requirements App B (Amend 26) LaSalle Unit 2 Cycle 8 COLR & Reload Transient Analysis Results, for Mar 1999 ML20205R2721999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for LaSalle County Station,Units 1 & 2.With ML20205L8391999-03-22022 March 1999 Rev 2 to 960103, Neutronics Licensing Rept for LaSalle Unit 2,Cycle 8 ML20204C8141999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for LaSalle County Station,Units 1 & 2.With ML20199E4601998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for LaSalle County Station,Units 1 & 2.With ML20207C7371998-12-31031 December 1998 Annual Rept for LaSalle County Station for Jan 1998 Through Dec 1998 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20198B3801998-12-14014 December 1998 SER Accepting one-time Request for Relief from Certain Provisions of Section XI of ASME Boiler & Pressure Vessel Code,Per 10CFR50.55a for Certain Plant Safety/Relief Valves ML20206N2261998-12-0909 December 1998 LER 98-S03-00:on 981116,protected Area Was Entered Without Current Authorization for Unescorted Access Due to Programmatic Deficiency Error.Changed Badge Control Process ML20197K0981998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for LaSalle County Station,Unts 1 & 2.With ML20196B1441998-11-23023 November 1998 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Bindings of Safety-Related Power-Operated Gate Valves ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195D3191998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for LaSalle County Station.With ML20154H6781998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20153D0191998-09-18018 September 1998 Part 21 Rept Re Defect in Gap Conductance Analyses for co- Resident BWR Fuel.Initially Reported on 980917.Corrective Analyses Performed Demonstrating That Current Operating Limits Bounding from BOC to Cycle Exposure of 8 Gwd/Mtu ML20153C7621998-09-18018 September 1998 Safety Evaluation Acceping NRC Bulletin 95-002, Unexpected Clogging of RHR Pump Strainer While Operating in Suppression Pool Cooling Mode ML20153C6771998-09-17017 September 1998 Part 21 Rept Re Defect Relative to MCPR Operating Limits as Impacted by Gap Conductance of co-resident BWR Fuel at Facilities.Operating Limit for LaSalle Unit 2 & Quad Cities Unit 2 Will Be Revised as Listed ML20151W0241998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for LaSalle County Station.With ML20237E2921998-08-21021 August 1998 Special Rept:On 980811,channel 5 of Lpms Became Inoperable. Caused by Channel Failed pre-amplifier Located Inside Primary Containment at Inboard Side of Electrical Penetration E-19.Initiated Repairs of Channel ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237B4861998-07-31031 July 1998 Monthly Operating Repts for July 1998 for LaSalle County Nuclear Power Station Units 1 & 2 ML20236V7701998-07-31031 July 1998 Revised LaSalle Unit 1 Cycle 8 COLR & Reload Transient Analysis Results ML20236P8231998-07-14014 July 1998 Special Rept:From 980614-17,various Fire Rated Assemblies Were Inoperable for Period Greater than Seven Days.Caused by Test Equipment Being Routed Through Fire Doors.Established Fire Watches & on 980619 Assemblies Were Declared Operable ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20236L8041998-07-0606 July 1998 Safety Evaluation Granting Licensee 980304 Request for Second 10-yr Interval Pump & Valve IST Program Plan,Rev 2, Including Changes to 2 ASME Boiler & Pressure Vessel Code Relief Requests Previously Submitted in Rev 1 ML20236P3611998-06-30030 June 1998 Monthly Operating Repts for June 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20249C4891998-06-22022 June 1998 Special Rept:On 980522,Fire Detection Zone 1-31 Was Noted out-of-service for More than 14 Days.Detection Sys Was Taken out-of-service on 980508 to Prevent False Alarms During Hot Work Activities.Sys Was Returned to Operable Status 980528 ML20248M3101998-05-31031 May 1998 Monthly Operating Repts for May 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20236V7771998-05-31031 May 1998 Rev 1 to 24A5180, Supplemental Reload Licensing Rept for LaSalle County Station Unit 1 Reload 7 Cycle 8 ML20217Q7041998-05-0404 May 1998 Safety Evaluation Accepting Util Request to Leave Leak Chase Channels Plugged During Performance of Containment ILRT ML20247M4491998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for LaSalle County Station ML20216F4941998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for LaSalle County Station,Units 1 & 2 ML20217N6581998-03-30030 March 1998 Special Rept on Fire Detection,Deluge Sys & Fire Rated Assemblies During Period of 980303-25.Established Fire Watches Until Affected Equipment Is Returned to Operable Status ML20216D9511998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for LaSalle County Station,Units 1 & 2 ML20247M4631998-02-28028 February 1998 Rev Monthly Operating Rept for Feb 1998 for LaSalle County Station ML20203D7241998-02-20020 February 1998 Special Rept:On 980118,Fire Detection Zones 1-18 & 2-18 Taken out-of-svc to Prevent False Alarms During Hot Work Activities on Auxiliary Electric Equipment Room Ventilation Sys.Fire Watches Will Remain in Place ML20202G9851998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for LaSalle County Station,Units 1 & 2 ML20199K1651998-01-23023 January 1998 Rev 65h to Topical Rept CE-1-A, Comm Ed QA Tr 1999-09-30
[Table view] |
Text
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'~ ~X Commonwoalth Edison LaSalle County Nuclear Station
- *- f -:) ' Rural Route c1, Box 220
. \ -
' Marsellies, Illinois 61341
\ Telephone B15/357 6761 l
1 i
December 22, 1989 4
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Director of Nuclear l<eactor Regulation U.S. Nuclear Regulatory Commission ;
Mail Station I'l-137 Washington, D.C. 205bS 1 i
Dear Sir:
1.icetince I?vesit Hepo: L l109 028-00, Docket 110b0 'JI3 in iming submitted to your office in accordance with 10CFR50.73(a)(2)(iv). I l
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'G.J.Diederich/2[
S ation iianager I,analle County filat lon GJD/DhC/kg Enclosure xc: Nuclear 1.icensing Administrator NRC Hentdent inspector NRC l(egion 111 Administrator INPO - Itecords Center
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laSalle County Station Unit 1 015101010131713 1lof!0l5 litle (4) Shutdown Cooling Outboard Isolation Valve Automatic Closure Due to M i s cunenu n i ca t l on,Jiror,,,. Du r i no _ i ns t rmen t su rw e l l 1 a nce twent Date (h) LtR Neber (6h ReportDate(7) Other f acilliles involved (8)
Month Day Year Year / 5equential
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I ll lL On Decenter 4,1959 with Unit 1 in the Refuel Mode (Operational Condition 5) the Ill2-IO00 Residual lleat Reeval Shutdown CoolinD Suction licader Outboard Isolation Valve autonutically isolated durin0 the 1 performance of LaSalle Instrunent Surveillance ll5-NB-lli, ' Unit 1 Reactor lingh Pressure Shutdown C001100 I Is31ation Calibration."
Th) IE12-I000 valve is normully deenergized or closed to prevent an autunatic isolation during the performance of Lis-ND-Ill, but due to a misconmnication between the Instrment Maintenante lechnician r questing the IE12-f000 valve breaker to be de-energized and the Unit 1 Nuclear Station Operator (NSO, licensed Reactor Operator), the breaker was re-energized prior to completing this surveillance.
This event had no effect on shutdown cooling because decay heat rmoval was being provided by an alternate method. Af ter the autonatic isolation of the IE12-f 000 valve, it was Icf t in the closed position and the surveillance was conpleted without any further event.
A task force was developed to review this event and similar events to deterniine what corrective actions will be inplenented to minimize recurrence of miscomnunication events.
This report is being sulnitted pursuant to the requirenents of 10CIR50.73(a)(2)(lv) due to the actuation of an Engineered Safety feature system, I
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LICtW5( L(,Vjui k[POPT (LER) TEXT CONilWUA110N fonn Rev 2.0
!. .IACllllT NAME (1) DOCKL1 NUMBLR (2) LER WUMB[R (6) P40e (3)
Year Sequential Revision *
{f{({
Net >cr _ ( Ned>cr i
LaSalle County Station Unit I .0 l 5 1 0 1 0 1 0 l 31 71 3 8l9 0l218 -
.O l 0 01 2 Or 01 5 1LX1 Energy Industry identification System (Ell 5) codes are identified in the text as (XX]
PLANT AND SYSILM 10LWillICA110N l
General Electric - Bolling Water Reactor I
- j. Energy Industry Identification System (Ell 5) codes are identified in the text as (XX).
A. COND1110N PRIOR 10 LVLNi i Unit (s): 1- Event Date: 12/04/89 Lvent line: _ 0945 llours l
Reactor Mode (s): 5 Mode (s) Nane: Refuel' Power level (s): DE
- 8. DL5CRIP110N OF LYLNi On Decent >cr 4,1909 with Unit 1 in Operational Condition 5 (Refuci Mode) the 1[12 4 000 Residual Heat Renoval (RllR, RH) (00) shutdown Cooling Suction lleader Outboard Isolation Valve autunatically 1solated during the perfonnance of LaSalle Instrunent Surveillance LIS-NU-Ill, " Unit 1 Heactor High Pressure Shutdown Cooling Isolatlun Calibration."
Af ter Shif t Engineer (50, licensed Senior Reactor Operator) approval, the Lead Instrunent Maintenance (IM) lechnician approached the Shift Control Room Engineer (SCRC, licensed Senior Reactor Operator) for approval to perfonn L1548-111. After reviewing the Shutdown Cooling system' status, the SCRC determined that the only two isolation valves that were open at the tine which were affected by this procedure were IE124008 and 1L124009 RHR Shutdown Cooling Suction Header inboard and Outboard isolation valves. The SCRE then discussed with the SE the Shutdown Cooling system status and asked if the Ill24000 and 1012 4 009 should be lef t in the open position or taken to the closed riosition to perfonn Ll$-NB-ll).
The 50 deteimined the 10124000 and IE12-F009 should remain open to maintain the shutdown Cooling suction hr.ader in the filled and vented status. The SCRE then attached a tiote to the surveillance attachment to de-energize one valve at a time (IE12-F000 or 1012-1009) when doing this surveillance in
- order to keep one isolation valve operabic in the line while perfonning the surveillance on the pressure switch which would close the other. (this is allowed by the procedure.)
The lead IM then approacteed the Unit 1 Nuclear Station Operator (N50, licensed Reactor Operator) for approval to perform this surveillance and discussed the need to have the 1012-1000 valve de-energized.
At this time the N50 Instructed an Operator to open the 1012 4 008 valve notor operator power supply breaker. -
The lead lH then proceeded to the 1A RilR Pmp Room (which is a high radiation area) at pressure switch IB33-N018A, and the other IM was positioned in the Main Control Room to instruct the NSO to acknowledge and reset alanns or isolation logic as required by the surveillance procedure.
The lead IM instructed the IM in the Main Control Room to have the N50 de-energize the Ill2-f 000 valve breaker, lhe IM in the 1A RHR Pmp Room then connected the deadweight pmp in order to proceed with the surveillance.
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llCINSLE LVIN1_ Rip 0RT (LER) IfXI CONilNILAll0N form Rev 2.0 i ACILilpHAML (1) 00CKL1 NUMBER (2) Page,,{3)
- t f R NUMBLR_{f>)__ _ _ _
Year /// Sequential /// Itevision fff f
/// Nunber ff(ff
/ Nunt>cr Lesa11e County statlpn unit i _ _
0_[ s l_0 1 0 1 0 1 31 11 3 e19 -
0 I 2 1 8- - 0I o 01 3 Or OI 5 itx1 Lnergy industry Identification System (Lil5) codes are identified in the text as [XX)
B. DL5 CHIN 10N Ol [VINI (continued) 1he IM in the Centrol Roum, not knowing the Ill2-f 008 valve was already de-energized, requested the N50 to de-energize Ill2-f008 valve. 1he lead 1H had requested that valve Ill2-f000 be de-energized previously. 1he N50 knowing the Ill?-f 000 was previously de-energired interpreted the instruction from the IM as wanting the power supply for the Ill2-f 008 valve to be re-energlied. The N50 then lustructed an fquipment Attendant (LA, non-licensed Operator) to energlie Ill2.f 000 valve notor power supply breaker.
1he Operator responded to the Unit 1 NSO by paraphrasing that he was requested to turn on the Ill2-f 000 valve breaker and the N50 confinned his response.
1he LA energized the notor operator power supply for the Ill2-f 000 valve breaker and returned to the Control Room.
When the LA returned to the Control Room, the IM responded to the LA by saying, that he had gotten that breaker pretty quickly. Ihc IM in the Control Room then questioned why the it 12-f 006 valve position Indicating Ilghts aniuined lilir:Inated all the time. Ihc LA who energized the breater Mked the SCRL why the valve lights renuin energized and SCRL replied the valve indication has a separate power supply. 1he LA who energlied the Ill2-F000 valve then relayed this infornution to the IM in the Control Roum.
1he IM in the Control Reom did not reallic the Ill2-f 000 valve was re-energlied at this tine.
The IM in the Control Room now knowing that the Ill2 f000 valve indication has a separate power supply, and believing that the Ill2-5000 valve was de-energized, instructed the IM at the IB33-N01BA pressure switch that the Ill2-f 000 was de-energized and testing could continue.
The IM at the pressure switch then pressurized the switch using the deadweight pump, When the switch setpoint isolationpressure signal. was reached the Ill2-f 008 valve autonutically closed due to a high reactor pressure C. APPARENT CAUSL OF LVENT 1he closure of the ill2-f D00 valve was caused by the motor operator power supply for the valve being re-energized prior to the conpletion of the calibration for pressure switch ID33-N010A per Ll$-NH-lli contrary to the procedure. The breaker was re-energized due to a miscunmunication between the IM in the Control Room and the Unit 1 NSO. The Unit 1 NSO misinterpreted the conmunication due to the mindset caused by expecting the next request to perform an action on valve IL12-1000 would be to re-energlie the valve (l.c., change its state). The IM had requested the breaker to be de-energlied prior to beginning the surveillance (which was performed) thus the Unit 1 NSO believed the next step would be to reset the logic and to re-energize the breaker. An hour had elapsed since the lead IM had requested the Unit 1 NSO to initially de-energlie the breaker for the Ill2-f008 valve. 1herefore, when the N50 was requested to take an action on valve Ill2-f 008, he expected it to be re-energizing the valve.
A contributing factor is that the IL12-f008 valve has a separate power supply for the valve position indication, therefore the valve notor epcrator power supply could be de-energlied and the valve position Indicating lights in the Main Control Rotrn would renuin energlied. (This is unique to this valve.)
This also led to the mindset of the IM performing the surveillance that the breaker was off following another misconmunication between the LA who energized the breaker and the IM in the Control Room. The process conputer alarm printer will print valve IL12-f 000 notor power supply breaker status when it chanDes, status, but this nethod is not currently used by the IM personnel to determine valve power supply i
LIClW5f L (VLWT REPORT (LER) 1LX1 COWLINUAll0N f orm Rev,_2,,0_
ipCIL11f NAt'l (1) I DOCKLI NOMIiLR (2) IIR NUMHf R _(6_) , Paoc,_{3)
Year / Sequential /// k#v $i "
/jj/j/
//
N/
Nunber_ , /// Nuntjel !
lasalle County Station _tkit.1 0 1 5 1 0,1 0 1 0 l 31 71 3 8IL- 0 l 2_l '8 -
,,0,( 0 01 4 or 01 5 1 EXT Enesgy Industry identification System (Lil5) codes are Identified in the text as (XX)
'C. APPARLNI CAU5L Of- EVLN1 (Continued)
Another contributin) factor was that the lead IM sild not request the N50 to log de-energizing the IL12-F'000 valve tarcaker as required by the surveillance procedure. Also this instrunent surveillance is
-not consistent with other instrunent surveillances which require initiallng procedure steps that repos'ition equipment such as valves or breakers.
An additional contributing factor is that a work practice requiring a warning of the Unit N50 prior to inillatirg a trip signal has not been established. This nuy have warned the Unit I N50 that a trip signal was goinD to be initiated with the Ill2-T000 valvo energized.
Another contributing factor is that no periodic training has been established to instruct station personnel on the requirenents of the LaSalle County Station coppany Policy Guideline for consnunication.
D. $AillY ANALYSIS OF LYLN1 1his event had no ef fect on nnderatur tenperature because the Itllit shutdown cooling systs'rii was shutdown and the Reactor Water Cleanup systen, was lined up for maximum heat renoval as an alternate riethod of decay heat renoval. 1he RitR shutdown cooling high pressure isolation is not required during the Refueling Mode with the vessel head rmoved. The concern for protecting low pressure equipnent during i this mode of operation does not exist in this operating condition.
L. CORRLCllVL ACl10NS 1he Ill24008 valve was left in the closed position and the calibration for pressure switch ID33-N0iBA was conv1rted satisfactorily at 1045 hours0.0121 days <br />0.29 hours <br />0.00173 weeks <br />3.976225e-4 months <br /> without any further event.
The individuals involved were counselled on this event.
A cormninication task force was developed to review the current station coninunication practice and develop reconinendations to inprove caninunication practices. 1he progress of the caninunication task force will be tracked by Action Itun Record (AIR) number 373-200-09-11001, r
lhe Instrisnent Maintenance Departrient will review L15-NB-III and similar procedures to detertnine the need for requiring a si noff D when log entries are required or conponents such as breakers or valves are nanipulated. Also review the need to utilize multiple indications when verifying or re-verifylng conditions prior to perforining a surveillance. AIR nmber 373-200-89-11002 will track this corrective action.
The Instrunent Maintenance Ucpartment is developing a work practice to notify the N50 prior to any 1/2
' scrivn or 1/2 isolation signal by issuing a new vialnteriance rii'ero. By providing the H50 with the warning of an incoming trip signal, the N50 nuy be able to better evaluate the consequences of receiving the trip signal knowing the status of the plant and provide another nochanism for catching an error. This corrective action is being tracked by previously issued AIR nmber 374 200-09-04901.
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7 LICEW5f L_t VJW1 HEPOR1 (LIR) 1(XI_ C_0NilNUA1_10N funn Rev,7._0_ l lACit.111 N ML (1) LKKAll wuhillR (2) (LH WlpyllH_{6) P:ge_(3}___ t Year // Sequential / Revision
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// _Nwidier laSalle Count,y sta H un Unit I_ .0 1 5 1 0 1 0 1 0 1 31 71 3 8l9 Ol_2] 8 - Oj 0 OLsJn 0L5 1LX1 Energy Industry identification System (Ells) codes are identifled in the text as [XXJ F. PRLV1005 f.VLN15 LLH Wund>cr litle 373/84-0$8-00 Inadvertent Start of VC/vE Esnergency Make-up Titter Unit 374/84-027-01 Loss of Reactor Water Cleanup Isolation Leak Detection 373/86 003-00 Missed Surveillance Reactor Water pil Due to Personnel trtor 373/86-016-00 fuel Bundle toaded Without Proper SRM Instrumentation Due to a Personnel Error 373/87-030-00 Reactor Scram While shutdown During Surveillance Due to coninunication Error 374/89-003-01 Engineered Safety f eature Actuation During Performnce of Instrunent Maintenance Iunctional lests Due to Personnel Error G. COMPONENI IAILURL DA1A Not applicable.
1