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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B1481993-07-30030 July 1993 LER 93-012-00:on 930702,reactor Core Isolation Cooling Sys Declared Inoperable Due to Associated Bus Voltage Dropping Below TS Limits.Sent Operator to Cycle Timer Which Caused Affected Contact to reclose.W/930730 Ltr ML20045D9331993-07-0202 July 1993 LER 93-004-00:on 930604,unexpected CRD Low Charging Water Header Scram Received Followed by Charging Water Header A2/B2 Alarm.Caused by Crud or Foreign Matl Passing Through Suction Filter.Filters Cleaned & reused.W/930702 ML20045D7501993-06-23023 June 1993 LER 93-003-00:on 930524,Div 1 ECCS Initiation Signal Received & LPCS Pump,Lpci Pump 2A & EDG Unit 0 Automatically Started.Caused by Personnel Error.Pumps Secured & Event Documented in Personnel file.W/930623 Ltr ML20044E4161993-05-28028 May 1993 LER 92-009-01:on 920923,spurious Auto Start of CR Ventilation Emergency make-up Train Occurred Due to High Radiation Spike.Radiation Monitor Circuit modified.W/930528 Ltr ML20044E4191993-05-21021 May 1993 LER 93-011-00:on 930423,manual Scram Initiated.Caused by Disconnected Linkage on Valve Positioner on Heater Drain Valve Due to Loose Jam Nut.Tailgate Session Will Be Held W/ Instrument Maint Dept Re Jam nuts.W/930521 Ltr ML20044D5161993-05-15015 May 1993 LER 92-007-01:on 920613,high Radiation Spike Received from CR Ventilation Process Radiation Monitor,Initiating Emergency Makeup Train B.Caused by Normal Variations in Radiation Readings.Spike modified.W/930515 Ltr ML20044D5571993-05-14014 May 1993 LER 93-010-00:on 930414,DG Cooling Water Pump Automatically Tripped on Magnetic Overload.Caused by Inexperienced Trainee in Operation of Control Lever.Lesson Plans & Training Programs for Operators to Be reviewed.W/930514 Ltr ML20044C9801993-05-0707 May 1993 LER 91-010-01:on 910719 & 0805,CR a Ventilation Emergency Makeup Fan auto-started on Spurious Trip of CR Air Intake Process Radiation Monitor.Caused by Normal Variations in Background Radiation.Supply Board replaced.W/930507 Ltr ML20044B6161993-02-25025 February 1993 LER 93-002-00:on 930126,Unit 1 Manual Scram Due to a SRV Being Stuck Open Due to Duct Tape Being Over Actuators Air Valve Manifold Exhaust Port.Maint Procedures That Involve Cleanliness reviewed.W/930225 Ltr ML20024G9771991-05-10010 May 1991 LER 91-005-00:on 910410,determined That Tech Spec Required Surveillance of Suppression Chamber Oxygen Sampling Missed. Caused by Inadequate Review of Tech Spec Change.Drywell & Suppression Chamber Checked for oxygen.W/910510 Ltr ML20044A3851990-06-25025 June 1990 LER 90-008-00:on 900525,Tech Spec Hourly Fire Watch Missed Due to Miscommunications Between Security Personnel & Radiation Protection Personnel.Fire Watch re-established & Memo issued.W/900625 Ltr ML20043F1721990-06-0505 June 1990 LER 90-009-00:on 900510,RWCU Outboard Suction Isolation Valve 2G33-F004 Auto Closed Which Tripped RWCU Pump B. Caused by Procedure Deficiency.Procedure LTS-500-209 Will Be revised.W/900605 Ltr ML20043F1281990-06-0101 June 1990 LER 90-009-00:on 900511,apparent Ruptured Diaphragm Found on Pressure Differential Switch in RCIC Steam Line.Caused by Torn Diaphragm Inside Switch.Replacement Switch Installed, Calibr & Functionally Tested satisfactorily.W/900608 Ltr ML20043B5681990-05-23023 May 1990 LER 89-027-01:on 891113,primary Containment Isolation Sys Group 1 Isolation Occurred During Surveillance Testing. Caused by Burnt Out Window Light Bulbs on Alarm Window. Light Bulbs Replaced & Jumpers installed.W/900523 Ltr ML20043A7721990-05-18018 May 1990 LER 90-007-00:on 900421,reactor Protection Sys Bus a Transfer & Reactor Recirculation Hydraulic Power Unit a Inboard Isolation Valves Closed,Causing Partial Group II isolation.Out-of-svc Procedure revised.W/900518 Ltr ML20043D0591990-05-18018 May 1990 LER 90-008-00:on 900502,ESF Actuation of Control Room B Emergency Ctk Ventilation Makeup Fan Occurred.Caused by Procedure deficiency.LTS-800-205 & Similar Procedures Will Be revised.W/900601 Ltr ML20042H0211990-05-10010 May 1990 LER 90-006-00:on 900412,loop a Primary Containment Chilled Water Sys Inboard Isolation Valves & Reactor Bldg Closed Cooling Water Sys Inboard Isolation Valve Went Closed.Caused by Inadequate Procedure.Procedures revised.W/900510 Ltr ML20042F9001990-05-0404 May 1990 LER 90-005-00:on 900411,experienced Loss of Dc Power to Portion of Div I Primary Containment Isolation Sys Logic Which Resulted in Isolation Signal & Actuation.Caused by Failure to Update Drawings & procedures.W/900504 Ltr ML20042F1941990-04-30030 April 1990 LER 89-025-01:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Door Containing Undervoltage Relays Closed.Caused by Misalignment of Door.Door Repaired. W/900430 Ltr ML20012D5341990-03-16016 March 1990 LER 90-003-01:on 900201,RCIC Isolation Signal Occurred During Warmup.Caused by Spurious High Steam Flow Signal.Rcic Sys Piping Integrity Verified & Isolation Logic Reset.W/ 900316 Ltr ML20012D5371990-03-16016 March 1990 LER 90-002-01:on 900129,oil in Diesel Generator Governor 1A Found to Be Low & Could Not Be Seen in Sight Glass.Caused by Slow Leak from Compensation Needle Valve Plug.Proper Amount of Oil Added & Operability Test performed.W/900316 Ltr ML20012C4931990-03-15015 March 1990 LER 90-004-00:on 900213,control Room B HVAC Intake Radiation Monitor Lost Power Causing auto-start of Emergency make-up Train B.Caused by Blown Fuses.Fuses Replaced.Logic Revs for Radiation Monitors Will Be installed.W/900315 Ltr ML20012B6501990-03-0909 March 1990 LER 90-002-00:on 900209,Operating Surveillance LOS-TG-W1 Determined to Have Exceeded Required Testing Interval,Per Tech Spec 3/4.7.10.Caused by Personnel Error.Personnel Counseled & Ref Procedures Will Be revised.W/900309 Ltr ML20012B5521990-03-0808 March 1990 LER 90-001-00:on 900206,full Reactor Scram Occurred During Instrument Surveillance Testing.Caused by Actuation of APRM E Trip Circuitry.Shutdown Margin Revised & Caution Card Placed on Control Room Bench board.W/900308 Ltr ML20011F8251990-03-0202 March 1990 LER 90-003-00:on 900201,RCIC Received Div 2 Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal Generated When Steam/Water Mixture Admitted to RCIC Steam Line.Isolation Logic reset.W/900302 Ltr ML20011F5551990-02-28028 February 1990 LER 90-002-00:on 900129,after Filling Diesel Generator 1A Governor W/Oil,Generator Started & Declared Inoperable. Caused by Slow Leak Coming from Compensation Needle Valve Plug.Oil Added & Plug Washer replaced.W/900228 Ltr ML20006F5951990-02-21021 February 1990 LER 90-001-00:on 900122,RWCU Sys Received Div 1 Leakage Detection Ambient Temp High Isolation Signal,Causing Trips of RWCU Pumps a & C.Caused by Broken Thermocouple Input Lead.Lead Wire Reconnected & Isolation reset.W/900221 Ltr ML20011F4921990-02-16016 February 1990 LER 89-013-01:on 890907,Group I Isolation Received During Performance of Instrument Surveillance LIS-MS-401.Caused by Depressurization of Main Steam Line Low Pressure Switch. Surveillance Revised to Split Into Two parts.W/900216 Ltr ML20006E4501990-02-15015 February 1990 LER 89-010-01:on 890715 & 17,voltage Oscillations Noted on Div II Battery Charger,Resulting in Inoperability of HPCS Sys.Caused by Failure of Charger in High Voltage Shutdown Relay.Charger Energized & Relay replaced.W/900215 Ltr ML20006E4451990-02-14014 February 1990 LER 89-009-01:on 890619,diaphragm Leak Discovered in RCIC Steam Line High Flow Isolation Switch.Caused by 1 & 1/2-inch Tear in Diaphragm.Pressure Differential Switch Replaced & Calibr.Reported Per NRC Bulletin 86-002.W/900214 Ltr ML20006E3981990-02-14014 February 1990 LER 89-008-01:on 890228,reactor Vessel Low Water Level 2 Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.Channel Placed in Tripped Condition & All Static-O-Ring Pressure Switches to Be replaced.W/900214 Ltr ML20006E3951990-02-14014 February 1990 LER 89-010-01:on 890303,automatic Depressurization Sys Permissive Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.All Static-O-Ring Reactor Vessel Level Switches Will Be replaced.W/900214 Ltr ML19354D8361990-01-15015 January 1990 LER 89-018-00:on 891216,plant 250-volt Battery & RCIC Sys Declared Inoperable Due to Low Battery Electrolyte Temps. Caused by Failure of Div I Switchgear Heat Removal Sys Damper Actuators.Air Intake Dampers closed.W/900115 Ltr ML20042D3921990-01-0404 January 1990 LER 89-011-01:on 890826,spurious Reactor Protection Sys Actuation Occurred.Definite Cause of Trip Not Determined. Brief Disturbance in Reactor Protection Sys Allowed Some Contactors to Trip.Procedure revised.W/900104 Ltr ML20005E2741989-12-22022 December 1989 LER 89-028-00:on 891204,RHR Shutdown Cooling Suction Header Outboard Isolation Valve Automatically Isolated.Caused by Miscommunication Between Technician & Station Operator.Task Force Developed to Review event.W/891222 Ltr ML19351A6301989-12-15015 December 1989 LER 89-006-01:on 890214,reactor Vessel Low Water Level 3 Switch Setpoint Found Out of Tolerance.Caused by Setpoint Drift.Level Switch to Be Replaced by Analog Trip Sys During First Quarter 1990.W/891215 Ltr ML20011D1341989-12-14014 December 1989 LER 89-017-00:on 891117,flow Switch FS-2E22-N006 Found W/ Setpoint Out of Tolerance Above Reject Limit.Caused by Setpoint Drift.Work Request Written to Replace Flow Switch. W/891214 Ltr ML19351A6751989-12-12012 December 1989 LER 89-027-00:on 891113,primary Containment Isolation Sys Group I Isolation Occurred While Performing Instrument Surveillance.Caused by Loss of Power to Leak Detection Sys Logic.Isolation reset.W/891213 Ltr ML19332F0081989-12-0808 December 1989 LER 89-016-00:on 891109,RWCU Isolation Occurred While Instrument Surveillance on Ventilation Differential Temp Isolation Functional Test in Progress.Caused by Faulty Thermocouple.Thermocouple repaired.W/891208 Ltr ML20005D6621989-12-0606 December 1989 LER 89-026-00:on 891106,inadvertent Primary Containment Isolation Actuation Occurred While Clearing out-of-svc. Caused by Inadequate Logic Setup During Mod Installation. Trip Status & Output Switches repositioned.W/891206 Ltr ML19332F2431989-12-0101 December 1989 LER 89-025-00:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Equipment Operator Closed Door Containing Relays.Caused by Misalignment of Door.Isolations Reset,Bus Energized & Circuit Logic tested.W/891201 Ltr ML19332E6581989-11-29029 November 1989 LER 89-015-00:on 891030,shift Control Room Engineer Noted That Quarterly Standby Liquid Control Operating Surveillance LOS-SC-Q1 Was Past Critical Date.Caused by Clerical Data Entry Error.Missed Surveillance performed.W/891129 Ltr ML19332D5181989-11-22022 November 1989 LER 89-018-01:on 890515,RCIC Received Div I & Div II Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal When Steam Added to RCIC Steam Line. Special Test Initiated.Isolation Logic reset.W/891122 Ltr ML19327C2601989-11-17017 November 1989 LER 89-014-00:on 891020,primary Containment Isolation Sys Group 4 Isolation Occurred Causing Isolation Dampers to Close.Caused by Opening of Div 2 125-volt Dc Breaker.Power Supply replaced.W/891117 Ltr ML19325F3411989-11-13013 November 1989 LER 89-024-00:on 891013 & 30,unsealed Openings in Main Control Room Floor & Main Control Room West Wall Discovered. Caused by Wide Gap Between Structural Beam & Cable Tray. Openings Sealed & Fire Watch established.W/891113 Ltr ML19324C1751989-11-0808 November 1989 LER 89-012-01:on 890309,diaphragm Leak Found in Pressure Differential Switch 1E31-N013BB.Caused by Tear Found in Diaphragm.Replacement Switch Installed,Calibr & Functionally Tested satisfactorily.W/891108 Ltr ML20024E9121983-08-26026 August 1983 LER 83-093/03L-0:on 830801,discovered full-in Indication on Core Display for Control Rod 34-47 Inoperable.Caused by Failed Switching Transistor on Data Memory Board 19.Data Memory Board replaced.W/830826 Ltr ML20024B8381983-07-0505 July 1983 LER 83-060/03L-0:on 830606,following Turbine Trip & Scram Due to High Vibration on Main Turbine,Reactor Recirculation Breaker 4B Closed.Cause Undetermined.Auxiliary Contacts cleaned.W/830705 Ltr ML20024B0721983-06-16016 June 1983 Updated LER 83-012/03X-1:on 830210,w/reactor in Cold Shutdown,Setpoints for Switches 1E31-N612A/B Found Above Tech Spec Limits.Cause Unknown.Switches calibr.W/830616 Ltr ML20024A6961983-06-14014 June 1983 LER 83-051/03L-0:on 830516,reactor Protection Sys Trip Channel H2 Limit Switch Failed to Operate Properly.Cause Unknown.Limit Switch readjusted.W/830614 Ltr 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046B1481993-07-30030 July 1993 LER 93-012-00:on 930702,reactor Core Isolation Cooling Sys Declared Inoperable Due to Associated Bus Voltage Dropping Below TS Limits.Sent Operator to Cycle Timer Which Caused Affected Contact to reclose.W/930730 Ltr ML20045D9331993-07-0202 July 1993 LER 93-004-00:on 930604,unexpected CRD Low Charging Water Header Scram Received Followed by Charging Water Header A2/B2 Alarm.Caused by Crud or Foreign Matl Passing Through Suction Filter.Filters Cleaned & reused.W/930702 ML20045D7501993-06-23023 June 1993 LER 93-003-00:on 930524,Div 1 ECCS Initiation Signal Received & LPCS Pump,Lpci Pump 2A & EDG Unit 0 Automatically Started.Caused by Personnel Error.Pumps Secured & Event Documented in Personnel file.W/930623 Ltr ML20044E4161993-05-28028 May 1993 LER 92-009-01:on 920923,spurious Auto Start of CR Ventilation Emergency make-up Train Occurred Due to High Radiation Spike.Radiation Monitor Circuit modified.W/930528 Ltr ML20044E4191993-05-21021 May 1993 LER 93-011-00:on 930423,manual Scram Initiated.Caused by Disconnected Linkage on Valve Positioner on Heater Drain Valve Due to Loose Jam Nut.Tailgate Session Will Be Held W/ Instrument Maint Dept Re Jam nuts.W/930521 Ltr ML20044D5161993-05-15015 May 1993 LER 92-007-01:on 920613,high Radiation Spike Received from CR Ventilation Process Radiation Monitor,Initiating Emergency Makeup Train B.Caused by Normal Variations in Radiation Readings.Spike modified.W/930515 Ltr ML20044D5571993-05-14014 May 1993 LER 93-010-00:on 930414,DG Cooling Water Pump Automatically Tripped on Magnetic Overload.Caused by Inexperienced Trainee in Operation of Control Lever.Lesson Plans & Training Programs for Operators to Be reviewed.W/930514 Ltr ML20044C9801993-05-0707 May 1993 LER 91-010-01:on 910719 & 0805,CR a Ventilation Emergency Makeup Fan auto-started on Spurious Trip of CR Air Intake Process Radiation Monitor.Caused by Normal Variations in Background Radiation.Supply Board replaced.W/930507 Ltr ML20044B6161993-02-25025 February 1993 LER 93-002-00:on 930126,Unit 1 Manual Scram Due to a SRV Being Stuck Open Due to Duct Tape Being Over Actuators Air Valve Manifold Exhaust Port.Maint Procedures That Involve Cleanliness reviewed.W/930225 Ltr ML20024G9771991-05-10010 May 1991 LER 91-005-00:on 910410,determined That Tech Spec Required Surveillance of Suppression Chamber Oxygen Sampling Missed. Caused by Inadequate Review of Tech Spec Change.Drywell & Suppression Chamber Checked for oxygen.W/910510 Ltr ML20044A3851990-06-25025 June 1990 LER 90-008-00:on 900525,Tech Spec Hourly Fire Watch Missed Due to Miscommunications Between Security Personnel & Radiation Protection Personnel.Fire Watch re-established & Memo issued.W/900625 Ltr ML20043F1721990-06-0505 June 1990 LER 90-009-00:on 900510,RWCU Outboard Suction Isolation Valve 2G33-F004 Auto Closed Which Tripped RWCU Pump B. Caused by Procedure Deficiency.Procedure LTS-500-209 Will Be revised.W/900605 Ltr ML20043F1281990-06-0101 June 1990 LER 90-009-00:on 900511,apparent Ruptured Diaphragm Found on Pressure Differential Switch in RCIC Steam Line.Caused by Torn Diaphragm Inside Switch.Replacement Switch Installed, Calibr & Functionally Tested satisfactorily.W/900608 Ltr ML20043B5681990-05-23023 May 1990 LER 89-027-01:on 891113,primary Containment Isolation Sys Group 1 Isolation Occurred During Surveillance Testing. Caused by Burnt Out Window Light Bulbs on Alarm Window. Light Bulbs Replaced & Jumpers installed.W/900523 Ltr ML20043A7721990-05-18018 May 1990 LER 90-007-00:on 900421,reactor Protection Sys Bus a Transfer & Reactor Recirculation Hydraulic Power Unit a Inboard Isolation Valves Closed,Causing Partial Group II isolation.Out-of-svc Procedure revised.W/900518 Ltr ML20043D0591990-05-18018 May 1990 LER 90-008-00:on 900502,ESF Actuation of Control Room B Emergency Ctk Ventilation Makeup Fan Occurred.Caused by Procedure deficiency.LTS-800-205 & Similar Procedures Will Be revised.W/900601 Ltr ML20042H0211990-05-10010 May 1990 LER 90-006-00:on 900412,loop a Primary Containment Chilled Water Sys Inboard Isolation Valves & Reactor Bldg Closed Cooling Water Sys Inboard Isolation Valve Went Closed.Caused by Inadequate Procedure.Procedures revised.W/900510 Ltr ML20042F9001990-05-0404 May 1990 LER 90-005-00:on 900411,experienced Loss of Dc Power to Portion of Div I Primary Containment Isolation Sys Logic Which Resulted in Isolation Signal & Actuation.Caused by Failure to Update Drawings & procedures.W/900504 Ltr ML20042F1941990-04-30030 April 1990 LER 89-025-01:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Door Containing Undervoltage Relays Closed.Caused by Misalignment of Door.Door Repaired. W/900430 Ltr ML20012D5341990-03-16016 March 1990 LER 90-003-01:on 900201,RCIC Isolation Signal Occurred During Warmup.Caused by Spurious High Steam Flow Signal.Rcic Sys Piping Integrity Verified & Isolation Logic Reset.W/ 900316 Ltr ML20012D5371990-03-16016 March 1990 LER 90-002-01:on 900129,oil in Diesel Generator Governor 1A Found to Be Low & Could Not Be Seen in Sight Glass.Caused by Slow Leak from Compensation Needle Valve Plug.Proper Amount of Oil Added & Operability Test performed.W/900316 Ltr ML20012C4931990-03-15015 March 1990 LER 90-004-00:on 900213,control Room B HVAC Intake Radiation Monitor Lost Power Causing auto-start of Emergency make-up Train B.Caused by Blown Fuses.Fuses Replaced.Logic Revs for Radiation Monitors Will Be installed.W/900315 Ltr ML20012B6501990-03-0909 March 1990 LER 90-002-00:on 900209,Operating Surveillance LOS-TG-W1 Determined to Have Exceeded Required Testing Interval,Per Tech Spec 3/4.7.10.Caused by Personnel Error.Personnel Counseled & Ref Procedures Will Be revised.W/900309 Ltr ML20012B5521990-03-0808 March 1990 LER 90-001-00:on 900206,full Reactor Scram Occurred During Instrument Surveillance Testing.Caused by Actuation of APRM E Trip Circuitry.Shutdown Margin Revised & Caution Card Placed on Control Room Bench board.W/900308 Ltr ML20011F8251990-03-0202 March 1990 LER 90-003-00:on 900201,RCIC Received Div 2 Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal Generated When Steam/Water Mixture Admitted to RCIC Steam Line.Isolation Logic reset.W/900302 Ltr ML20011F5551990-02-28028 February 1990 LER 90-002-00:on 900129,after Filling Diesel Generator 1A Governor W/Oil,Generator Started & Declared Inoperable. Caused by Slow Leak Coming from Compensation Needle Valve Plug.Oil Added & Plug Washer replaced.W/900228 Ltr ML20006F5951990-02-21021 February 1990 LER 90-001-00:on 900122,RWCU Sys Received Div 1 Leakage Detection Ambient Temp High Isolation Signal,Causing Trips of RWCU Pumps a & C.Caused by Broken Thermocouple Input Lead.Lead Wire Reconnected & Isolation reset.W/900221 Ltr ML20011F4921990-02-16016 February 1990 LER 89-013-01:on 890907,Group I Isolation Received During Performance of Instrument Surveillance LIS-MS-401.Caused by Depressurization of Main Steam Line Low Pressure Switch. Surveillance Revised to Split Into Two parts.W/900216 Ltr ML20006E4501990-02-15015 February 1990 LER 89-010-01:on 890715 & 17,voltage Oscillations Noted on Div II Battery Charger,Resulting in Inoperability of HPCS Sys.Caused by Failure of Charger in High Voltage Shutdown Relay.Charger Energized & Relay replaced.W/900215 Ltr ML20006E4451990-02-14014 February 1990 LER 89-009-01:on 890619,diaphragm Leak Discovered in RCIC Steam Line High Flow Isolation Switch.Caused by 1 & 1/2-inch Tear in Diaphragm.Pressure Differential Switch Replaced & Calibr.Reported Per NRC Bulletin 86-002.W/900214 Ltr ML20006E3981990-02-14014 February 1990 LER 89-008-01:on 890228,reactor Vessel Low Water Level 2 Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.Channel Placed in Tripped Condition & All Static-O-Ring Pressure Switches to Be replaced.W/900214 Ltr ML20006E3951990-02-14014 February 1990 LER 89-010-01:on 890303,automatic Depressurization Sys Permissive Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.All Static-O-Ring Reactor Vessel Level Switches Will Be replaced.W/900214 Ltr ML19354D8361990-01-15015 January 1990 LER 89-018-00:on 891216,plant 250-volt Battery & RCIC Sys Declared Inoperable Due to Low Battery Electrolyte Temps. Caused by Failure of Div I Switchgear Heat Removal Sys Damper Actuators.Air Intake Dampers closed.W/900115 Ltr ML20042D3921990-01-0404 January 1990 LER 89-011-01:on 890826,spurious Reactor Protection Sys Actuation Occurred.Definite Cause of Trip Not Determined. Brief Disturbance in Reactor Protection Sys Allowed Some Contactors to Trip.Procedure revised.W/900104 Ltr ML20005E2741989-12-22022 December 1989 LER 89-028-00:on 891204,RHR Shutdown Cooling Suction Header Outboard Isolation Valve Automatically Isolated.Caused by Miscommunication Between Technician & Station Operator.Task Force Developed to Review event.W/891222 Ltr ML19351A6301989-12-15015 December 1989 LER 89-006-01:on 890214,reactor Vessel Low Water Level 3 Switch Setpoint Found Out of Tolerance.Caused by Setpoint Drift.Level Switch to Be Replaced by Analog Trip Sys During First Quarter 1990.W/891215 Ltr ML20011D1341989-12-14014 December 1989 LER 89-017-00:on 891117,flow Switch FS-2E22-N006 Found W/ Setpoint Out of Tolerance Above Reject Limit.Caused by Setpoint Drift.Work Request Written to Replace Flow Switch. W/891214 Ltr ML19351A6751989-12-12012 December 1989 LER 89-027-00:on 891113,primary Containment Isolation Sys Group I Isolation Occurred While Performing Instrument Surveillance.Caused by Loss of Power to Leak Detection Sys Logic.Isolation reset.W/891213 Ltr ML19332F0081989-12-0808 December 1989 LER 89-016-00:on 891109,RWCU Isolation Occurred While Instrument Surveillance on Ventilation Differential Temp Isolation Functional Test in Progress.Caused by Faulty Thermocouple.Thermocouple repaired.W/891208 Ltr ML20005D6621989-12-0606 December 1989 LER 89-026-00:on 891106,inadvertent Primary Containment Isolation Actuation Occurred While Clearing out-of-svc. Caused by Inadequate Logic Setup During Mod Installation. Trip Status & Output Switches repositioned.W/891206 Ltr ML19332F2431989-12-0101 December 1989 LER 89-025-00:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Equipment Operator Closed Door Containing Relays.Caused by Misalignment of Door.Isolations Reset,Bus Energized & Circuit Logic tested.W/891201 Ltr ML19332E6581989-11-29029 November 1989 LER 89-015-00:on 891030,shift Control Room Engineer Noted That Quarterly Standby Liquid Control Operating Surveillance LOS-SC-Q1 Was Past Critical Date.Caused by Clerical Data Entry Error.Missed Surveillance performed.W/891129 Ltr ML19332D5181989-11-22022 November 1989 LER 89-018-01:on 890515,RCIC Received Div I & Div II Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal When Steam Added to RCIC Steam Line. Special Test Initiated.Isolation Logic reset.W/891122 Ltr ML19327C2601989-11-17017 November 1989 LER 89-014-00:on 891020,primary Containment Isolation Sys Group 4 Isolation Occurred Causing Isolation Dampers to Close.Caused by Opening of Div 2 125-volt Dc Breaker.Power Supply replaced.W/891117 Ltr ML19325F3411989-11-13013 November 1989 LER 89-024-00:on 891013 & 30,unsealed Openings in Main Control Room Floor & Main Control Room West Wall Discovered. Caused by Wide Gap Between Structural Beam & Cable Tray. Openings Sealed & Fire Watch established.W/891113 Ltr ML19324C1751989-11-0808 November 1989 LER 89-012-01:on 890309,diaphragm Leak Found in Pressure Differential Switch 1E31-N013BB.Caused by Tear Found in Diaphragm.Replacement Switch Installed,Calibr & Functionally Tested satisfactorily.W/891108 Ltr ML20024E9121983-08-26026 August 1983 LER 83-093/03L-0:on 830801,discovered full-in Indication on Core Display for Control Rod 34-47 Inoperable.Caused by Failed Switching Transistor on Data Memory Board 19.Data Memory Board replaced.W/830826 Ltr ML20024B8381983-07-0505 July 1983 LER 83-060/03L-0:on 830606,following Turbine Trip & Scram Due to High Vibration on Main Turbine,Reactor Recirculation Breaker 4B Closed.Cause Undetermined.Auxiliary Contacts cleaned.W/830705 Ltr ML20024B0721983-06-16016 June 1983 Updated LER 83-012/03X-1:on 830210,w/reactor in Cold Shutdown,Setpoints for Switches 1E31-N612A/B Found Above Tech Spec Limits.Cause Unknown.Switches calibr.W/830616 Ltr ML20024A6961983-06-14014 June 1983 LER 83-051/03L-0:on 830516,reactor Protection Sys Trip Channel H2 Limit Switch Failed to Operate Properly.Cause Unknown.Limit Switch readjusted.W/830614 Ltr 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217C9121999-10-12012 October 1999 SER Input Authorizing Licensee Proposed Request to Modify Definition of Core Alteration in Section 1.0 of TS & Update Sections 3/4.1,3.4.3 & 3/4.9 to Reflect Proposed Definition Change ML20217F9091999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for LaSalle County Stations,Units 1 & 2.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212C4501999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for LaSalle County Station,Units 1 & 2.With ML20210R0671999-07-31031 July 1999 Monthly Operating Repts for July 1999 for LaSalle County Station,Units 1 & 2.With ML20210C1681999-07-0909 July 1999 Seventh Refueling Outage ASME Section XI Summary Rept ML20209H1501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for LaSalle County Station,Units 1 & 2.With ML20195J7871999-05-31031 May 1999 Monthly Operating Repts for May 1999 for LaSalle County Station,Units 1 & 2.With ML20209E1431999-05-31031 May 1999 Cycle 8 COLR, for May 1999 ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations ML20206N2071999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for LaSalle County Station,Units 1 & 2.With ML20205L8421999-03-31031 March 1999 Rev 2 to EMF-96-125, LaSalle Unit 2 Cycle 8 Reload Analysis ML20205L8301999-03-31031 March 1999 Administrative Technical Requirements App B (Amend 26) LaSalle Unit 2 Cycle 8 COLR & Reload Transient Analysis Results, for Mar 1999 ML20205R2721999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for LaSalle County Station,Units 1 & 2.With ML20205L8391999-03-22022 March 1999 Rev 2 to 960103, Neutronics Licensing Rept for LaSalle Unit 2,Cycle 8 ML20204C8141999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for LaSalle County Station,Units 1 & 2.With ML20199E4601998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for LaSalle County Station,Units 1 & 2.With ML20207C7371998-12-31031 December 1998 Annual Rept for LaSalle County Station for Jan 1998 Through Dec 1998 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20198B3801998-12-14014 December 1998 SER Accepting one-time Request for Relief from Certain Provisions of Section XI of ASME Boiler & Pressure Vessel Code,Per 10CFR50.55a for Certain Plant Safety/Relief Valves ML20206N2261998-12-0909 December 1998 LER 98-S03-00:on 981116,protected Area Was Entered Without Current Authorization for Unescorted Access Due to Programmatic Deficiency Error.Changed Badge Control Process ML20197K0981998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for LaSalle County Station,Unts 1 & 2.With ML20196B1441998-11-23023 November 1998 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Bindings of Safety-Related Power-Operated Gate Valves ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195D3191998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for LaSalle County Station.With ML20154H6781998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20153D0191998-09-18018 September 1998 Part 21 Rept Re Defect in Gap Conductance Analyses for co- Resident BWR Fuel.Initially Reported on 980917.Corrective Analyses Performed Demonstrating That Current Operating Limits Bounding from BOC to Cycle Exposure of 8 Gwd/Mtu ML20153C7621998-09-18018 September 1998 Safety Evaluation Acceping NRC Bulletin 95-002, Unexpected Clogging of RHR Pump Strainer While Operating in Suppression Pool Cooling Mode ML20153C6771998-09-17017 September 1998 Part 21 Rept Re Defect Relative to MCPR Operating Limits as Impacted by Gap Conductance of co-resident BWR Fuel at Facilities.Operating Limit for LaSalle Unit 2 & Quad Cities Unit 2 Will Be Revised as Listed ML20151W0241998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for LaSalle County Station.With ML20237E2921998-08-21021 August 1998 Special Rept:On 980811,channel 5 of Lpms Became Inoperable. Caused by Channel Failed pre-amplifier Located Inside Primary Containment at Inboard Side of Electrical Penetration E-19.Initiated Repairs of Channel ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237B4861998-07-31031 July 1998 Monthly Operating Repts for July 1998 for LaSalle County Nuclear Power Station Units 1 & 2 ML20236V7701998-07-31031 July 1998 Revised LaSalle Unit 1 Cycle 8 COLR & Reload Transient Analysis Results ML20236P8231998-07-14014 July 1998 Special Rept:From 980614-17,various Fire Rated Assemblies Were Inoperable for Period Greater than Seven Days.Caused by Test Equipment Being Routed Through Fire Doors.Established Fire Watches & on 980619 Assemblies Were Declared Operable ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20236L8041998-07-0606 July 1998 Safety Evaluation Granting Licensee 980304 Request for Second 10-yr Interval Pump & Valve IST Program Plan,Rev 2, Including Changes to 2 ASME Boiler & Pressure Vessel Code Relief Requests Previously Submitted in Rev 1 ML20236P3611998-06-30030 June 1998 Monthly Operating Repts for June 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20249C4891998-06-22022 June 1998 Special Rept:On 980522,Fire Detection Zone 1-31 Was Noted out-of-service for More than 14 Days.Detection Sys Was Taken out-of-service on 980508 to Prevent False Alarms During Hot Work Activities.Sys Was Returned to Operable Status 980528 ML20248M3101998-05-31031 May 1998 Monthly Operating Repts for May 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20236V7771998-05-31031 May 1998 Rev 1 to 24A5180, Supplemental Reload Licensing Rept for LaSalle County Station Unit 1 Reload 7 Cycle 8 ML20217Q7041998-05-0404 May 1998 Safety Evaluation Accepting Util Request to Leave Leak Chase Channels Plugged During Performance of Containment ILRT ML20247M4491998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for LaSalle County Station ML20216F4941998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for LaSalle County Station,Units 1 & 2 ML20217N6581998-03-30030 March 1998 Special Rept on Fire Detection,Deluge Sys & Fire Rated Assemblies During Period of 980303-25.Established Fire Watches Until Affected Equipment Is Returned to Operable Status ML20216D9511998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for LaSalle County Station,Units 1 & 2 ML20247M4631998-02-28028 February 1998 Rev Monthly Operating Rept for Feb 1998 for LaSalle County Station ML20203D7241998-02-20020 February 1998 Special Rept:On 980118,Fire Detection Zones 1-18 & 2-18 Taken out-of-svc to Prevent False Alarms During Hot Work Activities on Auxiliary Electric Equipment Room Ventilation Sys.Fire Watches Will Remain in Place ML20202G9851998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for LaSalle County Station,Units 1 & 2 ML20199K1651998-01-23023 January 1998 Rev 65h to Topical Rept CE-1-A, Comm Ed QA Tr 1999-09-30
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Common:rith Edison
' LaSalle County Nucl(ar Station
-- Rural Route #1. Dox 220 .
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~ k v' 7 Marseilles, Illinois 61341
.K / ' . Telephone 815/357 67611 r
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March 8, 1990 Director of Nuclear Reactor Regulation U.S.' Nuclear' Regulatory Commission Mail Station Pl-137 Washington, D.C. 20555'
Dear Sir:
i Licensee Event Report #90-001-00, Docket #050-374 is being submitted to your office in accordance with 10CFR50.73(a)(2)(iv).
4 J d ic tation Manager LaSalle County Station ;
GJD/KCD/kg Enclosure xc: . Nuclear Licensing Administrator NRC Resident Inspector j NRC Region III Administrator INPO - Records Center l
l Q315A g 90030g y l S K 05000374 ( ( l PNU. \
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1 LICENSEE EVENT REPORT (LER) p 7, j Docket Neber (2) Pace (3) l Facility N me (1)
L W 11e County Stat' ion Unit 2 015101010131714 1lof!0l5 Title (4) .
Reactor Scrm durine Instroent Surveillance Testino Caused by Spurious Spike on Averace Power Ranoe Monitor 1 l
Event Date (5) LER Neber (6) Report Date (7) Other Facilities involved (8)
Sequential Revision Month Day Year Facility N aes Docket Weber (s)
Month Day Year Year ///
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01 2 01 6 91 0 91 0 01011
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THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10CFR
"^ (Check one or more of the followino) (11) i M00E N 1 20.402(b) _ 20.405(c) _X_ 50.73(a)(2)(lv) 73.71(b) l 20.405(a)(1)(l) 50.36(c)(1) 50.73(a)(2)(v) ,,,,, 73.71(c) j POWER ,,, _
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Ii 01 0 20.405(a)(1)(111) 50.73(a)(2)(l) 50.73(a)(2)(vill)(A) in Abstract (10) ,,__ ,,,,_
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LICENSEE CONTACT FOR THl5 LER (12)
I TELEPHONE NUSER Nme AREA CODE Kevin C. Oorwick. Technical Staff Enoineer, extension 2705 8 l 1 15 315171-l6171611 )
COW LETE ONE LINE FOR EACH CO WONENT FAILURE DESCRIBE 0 IN THIS REPORT (13) {
CAUSE SYSTEM COMPONENT MANUFAC- REPORTA8LE CAUSE SYSTEM COMPONENT MANUFAC. REPORTABLE TO NPRDS TURER TO NPROS TURER X tI o l l I I I I N I I I I I I I X Al A l l l Gl01810 Y l l l l l l l Expected Month l Day l Year SUPPLEENTAL REPORT EXPECTED (14)
Subalssion
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Dak ( W 016l210!910 YlYes (if ves complete EXPECTED SUBMISSION DATE) l NO A8STRACT (Limit to 1400 spaces, i.e, approximately fifteen single-space typewritten lines) (16)
On February 6,1990 at 0926 hours0.0107 days <br />0.257 hours <br />0.00153 weeks <br />3.52343e-4 months <br />, while Unit 2 was in Operational Condition 1 (Run) at 99.85 power, during the perforinance of LaSalle Instrument surveillance LIS-NR-403, " Unit 2 Average Power Range Monitor (APRM) Rod j Block and Scr m Functional lest," a full reactor scrm occurred. Morinally the surveillance only causes half-scr ms. At the time of the occurrence, F APRM was trippsd, per the procedure, which tripped Reactor Protection System (RPS) Channel A. While the RPS Channel "A" half scr m condition was in effect, E APRM spiked spuriously, causing RPS Channel B to trip and a full reactor scrm occurred.
Additionally, it was also deterinined that all other expected automatic actions occurred as expected including Primary containment isolation signals when reactor water level reached 12.5 inches decreasing.
Initiation of the event was not due to an actual transient on a parameter which is monitored to protect the reactor core but due to spurious spike of APRM E. Troubleshooting E APRM will continue under Work Request L%857 in an attenyt to deterinine the cause of the spurious spikes.
Unit I was not affected by this event.
This event is reportable pursuant to 10CFR50.73(a)(2)(lv) due to an actuation of an Engineered Safety Feature.
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- J LICENSEE EVENT REPORT (LER) TEXT CONTINUATION' Fo m Rev 2.0 Paes (3) $
. FACILITY NAfE (1) DOCKET NU SER (2) LER NUSER (6)
Year /
j/f Sequential //j/, Revision
/T/ thsiber j/
/7 Nueer !
% 11e Coucty Station unit.2~ 0 1 5 1 0 1 0 1 0 1 31 71 4 9I0 - 0 1 0 l'1 - 0I0 '01 2 0F 01 5 l Energy industry identification System (Ells) codes are identified in the text as [XX] l TEXT l' PLANT AND SYSTEM IDENTIFICATION General Electric - bolling Water Reactor 3 v ,
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.EnergyIndustryidentificationSystem(Ells)codesareidentlfledinthetextas[XX].
A.- CONDITION PRIOR TO EVENT Event Time: 0926 Hours Unit (s): 2 Event Date: 02/06/90 Reactor. Mode (s): 1 Mode (s) N ee: Run- Power Level (s): 99.85
, B. DESCRIPTION OF EVENT On February 6, 1990 at 0926 hours0.0107 days <br />0.257 hours <br />0.00153 weeks <br />3.52343e-4 months <br />, while Unit 2 was in operational condition:1 (Run) at 99.85 power,.
- during the perfomance of LaSalle Instraent Surveillance L15-NR-403, " Unit 2 Average Power Range n ~ Monitor. (APRM) Rod Block and Scrm Functional Test," a full reactor scram occurred. Nomally the surveillance only causes half-scrams. Atthetimeoftheoccurrence,FAPRM[lG)was tripped, per the
. procedure, which tripped Reactor Protection System (RPS, C71) [JC] Channel A._ While the RPS Channel "A" ,
half scrm condition was in effect, E APRM spiked spuriously, causing RPS channel B to trip and a full reactor scr m occurred.'
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- After the automatic scrm, the control Room Operator.(NS0) noticed that Control Rod Orive (CRO) (RD, ~ '
Cll) [AA] 26-47 was-latched at the."02" position. .The rod was subsequently manually inserted to the required "00" position. Subsequent testing revealed that control rod 26-47 initially,went to the full-in position. Upon resetting the automatic scr m ,' the rod drifted and latched at the "02" position.
Additionally, it was detemined that all other expected automatic actions operated correctly _ Including' .
Primary Containment Isolation signals (PCIS, PC) [JM] when reactor water level reached 12.5 inches '
decreasing.
Unit I was not affected by this event.
This event is reportable pursuant to 10CFR50.73(a)(2)(lv) due to an actuation of an Engineered Safety.
. Feature.
, C. APPARENT CAUSE OF EVENT -
L.
The cause of the reactor scram was due to an unexpected actuation of the E APRM trip circuitry. A half scram condition existed due to the perfomance of LIS-NR-403. When the E APRM trip circuitry actuated, a fu11 reactor scram occurred. The cause of the spike is unknown.
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!~ LICENSEE EVENT REPORT (LER) TEXT CONilWUATIDW Fom Rev 2.0 DDCKET NUSER (2) LER WUSER (6) Pace (3)
FACILITY NAE (1)
Year //,/ Sequential // Revision j/,/j/ Number
/j/j/j/ thauber t e lle Countv Station unit 2 0 1 5 1 0 1 0 1 0 1 31 11 4 9IO - 0I011 - 01 0 01 3 0F 01 5 TEXT Energy Industry identification System (Ells) codes are identified in the text as (XX]
.C. APPARENT CAUSE OF EVENT (Continued)
Special recorders had been installed in the RPS logic strings to attanipt to help pinpoint the source and collect data on the character of very short trip signals entered into the RPS logic (LER 314/99-011-41). The recorder on the A2 logic string recorded this scram event. This recorder trace shows that the RPS logic string was opened for slightly less than 1 AC cycie, or approximately 12 - 15 milliseconds. The RPS contactors completely de-energized as expected.. A recorder trace was also obtained from the 81 logic string recorder. It was triggered at the time of the intentional 1/2 scram-from APM F. This recorder trace does not extend in time to the APM E trip. (Due to the scan rate, a recorder trace only shows about 400 milliseconds of data - the E APM trip was 1.3 seconds after APM -j F). However, it does show that the electrical conditions in the B RPS channel were completely stable within 2 AC cycles after the F APM trip, well before the APM E trip occurred.
The RPS recorders indicate that the APRM E trip was internal to the APM drawer, and not induced by the actuation of other RPS circuitry. There appears to be no direct relationship between the survelliance in APRM F and the APRM E trip. This was verified by the testing sequence following the scram, where the functional tests for APM F,'then E, then F again were conducted, with no trip indications appearing in APM E. (Thistestsequenceisthesameasoccurredjustbeforethereactortrip.)
Troubleshooting CRD 26-47 indicated that it is runnlag " hotter" than most other CRD's. This is consistent with data collected over the past year. This data, collected previously per LaSalle Special Test, LST-89-IS1, "CRD Thenuocouple Direct Measurement at 1(2)Cll-R018 Recorder," shows CR0 26-47 running consistently at 350 - 400 degrees F. This high tanqperature condition is likely due to foreign material blockage of the CRD cooling water orifice inside the drive mechanism., This postulation is supported by the fact that the insert stall flows for this CR0 have steadily decreased over the current operating cycle indicating a restricted cooling water orifice. The CRD consistently running " hot" with a lack of coo) lng water flow is believed to have led to greatly accelerated wearing of the stop piston seals, potentially aggravated by nonnal weekly exercising of the CRD and a " hot" scram which occurred in August, 1989. This stop piston seal wearing is demonstrated by the steadily and sharply increasing withdraw stall flows observed over this operating cycle. At the start of this cycle, both the insert and withdraw stall flows were still in the nonnal range. This CR0 was installed in Unit 2 during its first refuel outage 'in the spring of 1987.
Due to the station's awareness of this CRD's high temperature and degrading stall flow trends several corrective measures were attempted during the August,1989 Unit 2 shutdown. This included flushing the CRD in accordance with LaSalle Operating Procedure, LOP-RD-19, "CRD Flushing," which involves a high pressure extended withdraw stall flow to flush collet area. Also, the CR0 cooling water orifice was back flushed through the insert line vent valve in an attempt to increase cooling water flow. Welther of the above actions proved successful for this CRD.
D. SAFETY ANALYSIS DF EVENT Initiation of the event was not due to an actual transient on a parameter which is monitored by RPS.
With the exception of Control Rod Drive 26-47, all systems required to operate functioned as designed.
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LheS""1 EVENT REPORT (LER) TEXT CONTINUATION Fom Rev 2.0 l DOCKET NupWER (2) LER tRpWER (6) Pee (3)
FACILITY NAM (1)- '
' Year /// . Sequential Revision N/ //g// Netper f
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0 l'0 l 1 0lo 0 i s 1 0 1 0 1 0 1 31~71 4 910 01 4 0F 01 5 laSalleCount'yStationunit2 - -
iEXT . Energy Industry identification System (Ells) codes are identified in the text as [XX]
D.- SAFETY ANALYSIS OF. EVENT (Continued)
A shutdown margin calculation was performed by General Electric to detennine the consequences of CRD 47 settling at position "02" lestead of "00." The results indicate that the shutdown margin was 1
. adequate with this rod at position "02" and the next strongest rod fully withdrawn.
-Based on the above, the safety consequences of this event are considered minimal. .
-E.. CORRECTIVE ACTIONS An investigation was performed following the event and the following items were noted:
No radio transmissions were noticed just prior to or during the scram. This addressed any radio frequency noise concerns which may have caused interference with the RPS or APRM drawer's trip ,
logic.
No personnel were present inside the Control Room panels which could have inadvertently bumped a cable.-
An interview of all personnel working in the Control Room area was perfomed and it was detemined '
that no work was in progress that could have resulted in a trip of APRM Channel E. It was also detemined that no one was present in the Cable Spreading Room which could have used a radio.or bumped a cable, it was detemined that no welding was in progress at the time of the event that could have resulted in the trip of APRM E.
Troubleshooting E APRM will continue under Work Request L96857 in an attempt to detennine the cause of the spurious spikes. A supplement to this report will include the results of this troubleshooting and will be tracked by Action item Record (AIR) 374-200-90-00301. ,
The entire calibration procedure for APRM E was conducted to ensure that no abnonnalities exist in the circultry, not seemingly related to the neutron flux trip circuit. -This c.alibration procedure
- completely checks the drawer, power supply ripple and regulation, and all trip functions and indications. No out of callbration conditions were found.
CRD 26-47 (S/W A994) has already been scheduled for replacement during LaSalle's Unit 2 third refueling outage (L2R03) which is scheduled to begin in March of 1990. Work Request L94782 was written previously due to the degraded stall flows and high tangeratures ou CRD 26-47.
Action item Record 374-200-90 4 0302 has been generated to track the inspection and detennination of the failure mode for CR0 26-47. This action will be coupleted once the CRD is removed during L2R03.
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Fore Rev 2.0 LICEaKEE EVENT REPORT (LER) TEXT CONTINUATION LER INSER (6) Pane (3) .]
DOCKET NU SER (2)
FACillif NRME (1) ' Year // Sequential //j/ Revision fg//
/ Number ff
/// thsiber i m 11e County Station unit 2 015 I o I o 10131714 9Io - oIoI1 - oIo 01 5 0F 01 5 TEKT Energy Industry identification System (Ells) codes are identified in the text as (XXJ E. CORRECTIVE ACTIONS (Continued)
Furthennore, as control rod 26-47 may again drift from position "00" to position "02" after a scram -
reset, the shutdown margin analysis was revised to assisme that control rod 2647 is at "02" along with the highest worth rod being fully withdrawn, prior to the startup after the scr m. A caution card was i
placed on the Control Room bench board (scrm reset switch) to lainediately select and insert CRD 2647 when resetting a full scrm. This caution card will be removed after the drive replacement is coupleted.
F. ' PREVIOUS EVENTS LER Number Title 374/89-011-00 Spurious Reactor Protection System Actuation Due to Unknown Causes G. COMPONENT fAlLURE DATA N/A ,
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