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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B1481993-07-30030 July 1993 LER 93-012-00:on 930702,reactor Core Isolation Cooling Sys Declared Inoperable Due to Associated Bus Voltage Dropping Below TS Limits.Sent Operator to Cycle Timer Which Caused Affected Contact to reclose.W/930730 Ltr ML20045D9331993-07-0202 July 1993 LER 93-004-00:on 930604,unexpected CRD Low Charging Water Header Scram Received Followed by Charging Water Header A2/B2 Alarm.Caused by Crud or Foreign Matl Passing Through Suction Filter.Filters Cleaned & reused.W/930702 ML20045D7501993-06-23023 June 1993 LER 93-003-00:on 930524,Div 1 ECCS Initiation Signal Received & LPCS Pump,Lpci Pump 2A & EDG Unit 0 Automatically Started.Caused by Personnel Error.Pumps Secured & Event Documented in Personnel file.W/930623 Ltr ML20044E4161993-05-28028 May 1993 LER 92-009-01:on 920923,spurious Auto Start of CR Ventilation Emergency make-up Train Occurred Due to High Radiation Spike.Radiation Monitor Circuit modified.W/930528 Ltr ML20044E4191993-05-21021 May 1993 LER 93-011-00:on 930423,manual Scram Initiated.Caused by Disconnected Linkage on Valve Positioner on Heater Drain Valve Due to Loose Jam Nut.Tailgate Session Will Be Held W/ Instrument Maint Dept Re Jam nuts.W/930521 Ltr ML20044D5161993-05-15015 May 1993 LER 92-007-01:on 920613,high Radiation Spike Received from CR Ventilation Process Radiation Monitor,Initiating Emergency Makeup Train B.Caused by Normal Variations in Radiation Readings.Spike modified.W/930515 Ltr ML20044D5571993-05-14014 May 1993 LER 93-010-00:on 930414,DG Cooling Water Pump Automatically Tripped on Magnetic Overload.Caused by Inexperienced Trainee in Operation of Control Lever.Lesson Plans & Training Programs for Operators to Be reviewed.W/930514 Ltr ML20044C9801993-05-0707 May 1993 LER 91-010-01:on 910719 & 0805,CR a Ventilation Emergency Makeup Fan auto-started on Spurious Trip of CR Air Intake Process Radiation Monitor.Caused by Normal Variations in Background Radiation.Supply Board replaced.W/930507 Ltr ML20044B6161993-02-25025 February 1993 LER 93-002-00:on 930126,Unit 1 Manual Scram Due to a SRV Being Stuck Open Due to Duct Tape Being Over Actuators Air Valve Manifold Exhaust Port.Maint Procedures That Involve Cleanliness reviewed.W/930225 Ltr ML20024G9771991-05-10010 May 1991 LER 91-005-00:on 910410,determined That Tech Spec Required Surveillance of Suppression Chamber Oxygen Sampling Missed. Caused by Inadequate Review of Tech Spec Change.Drywell & Suppression Chamber Checked for oxygen.W/910510 Ltr ML20044A3851990-06-25025 June 1990 LER 90-008-00:on 900525,Tech Spec Hourly Fire Watch Missed Due to Miscommunications Between Security Personnel & Radiation Protection Personnel.Fire Watch re-established & Memo issued.W/900625 Ltr ML20043F1721990-06-0505 June 1990 LER 90-009-00:on 900510,RWCU Outboard Suction Isolation Valve 2G33-F004 Auto Closed Which Tripped RWCU Pump B. Caused by Procedure Deficiency.Procedure LTS-500-209 Will Be revised.W/900605 Ltr ML20043F1281990-06-0101 June 1990 LER 90-009-00:on 900511,apparent Ruptured Diaphragm Found on Pressure Differential Switch in RCIC Steam Line.Caused by Torn Diaphragm Inside Switch.Replacement Switch Installed, Calibr & Functionally Tested satisfactorily.W/900608 Ltr ML20043B5681990-05-23023 May 1990 LER 89-027-01:on 891113,primary Containment Isolation Sys Group 1 Isolation Occurred During Surveillance Testing. Caused by Burnt Out Window Light Bulbs on Alarm Window. Light Bulbs Replaced & Jumpers installed.W/900523 Ltr ML20043A7721990-05-18018 May 1990 LER 90-007-00:on 900421,reactor Protection Sys Bus a Transfer & Reactor Recirculation Hydraulic Power Unit a Inboard Isolation Valves Closed,Causing Partial Group II isolation.Out-of-svc Procedure revised.W/900518 Ltr ML20043D0591990-05-18018 May 1990 LER 90-008-00:on 900502,ESF Actuation of Control Room B Emergency Ctk Ventilation Makeup Fan Occurred.Caused by Procedure deficiency.LTS-800-205 & Similar Procedures Will Be revised.W/900601 Ltr ML20042H0211990-05-10010 May 1990 LER 90-006-00:on 900412,loop a Primary Containment Chilled Water Sys Inboard Isolation Valves & Reactor Bldg Closed Cooling Water Sys Inboard Isolation Valve Went Closed.Caused by Inadequate Procedure.Procedures revised.W/900510 Ltr ML20042F9001990-05-0404 May 1990 LER 90-005-00:on 900411,experienced Loss of Dc Power to Portion of Div I Primary Containment Isolation Sys Logic Which Resulted in Isolation Signal & Actuation.Caused by Failure to Update Drawings & procedures.W/900504 Ltr ML20042F1941990-04-30030 April 1990 LER 89-025-01:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Door Containing Undervoltage Relays Closed.Caused by Misalignment of Door.Door Repaired. W/900430 Ltr ML20012D5341990-03-16016 March 1990 LER 90-003-01:on 900201,RCIC Isolation Signal Occurred During Warmup.Caused by Spurious High Steam Flow Signal.Rcic Sys Piping Integrity Verified & Isolation Logic Reset.W/ 900316 Ltr ML20012D5371990-03-16016 March 1990 LER 90-002-01:on 900129,oil in Diesel Generator Governor 1A Found to Be Low & Could Not Be Seen in Sight Glass.Caused by Slow Leak from Compensation Needle Valve Plug.Proper Amount of Oil Added & Operability Test performed.W/900316 Ltr ML20012C4931990-03-15015 March 1990 LER 90-004-00:on 900213,control Room B HVAC Intake Radiation Monitor Lost Power Causing auto-start of Emergency make-up Train B.Caused by Blown Fuses.Fuses Replaced.Logic Revs for Radiation Monitors Will Be installed.W/900315 Ltr ML20012B6501990-03-0909 March 1990 LER 90-002-00:on 900209,Operating Surveillance LOS-TG-W1 Determined to Have Exceeded Required Testing Interval,Per Tech Spec 3/4.7.10.Caused by Personnel Error.Personnel Counseled & Ref Procedures Will Be revised.W/900309 Ltr ML20012B5521990-03-0808 March 1990 LER 90-001-00:on 900206,full Reactor Scram Occurred During Instrument Surveillance Testing.Caused by Actuation of APRM E Trip Circuitry.Shutdown Margin Revised & Caution Card Placed on Control Room Bench board.W/900308 Ltr ML20011F8251990-03-0202 March 1990 LER 90-003-00:on 900201,RCIC Received Div 2 Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal Generated When Steam/Water Mixture Admitted to RCIC Steam Line.Isolation Logic reset.W/900302 Ltr ML20011F5551990-02-28028 February 1990 LER 90-002-00:on 900129,after Filling Diesel Generator 1A Governor W/Oil,Generator Started & Declared Inoperable. Caused by Slow Leak Coming from Compensation Needle Valve Plug.Oil Added & Plug Washer replaced.W/900228 Ltr ML20006F5951990-02-21021 February 1990 LER 90-001-00:on 900122,RWCU Sys Received Div 1 Leakage Detection Ambient Temp High Isolation Signal,Causing Trips of RWCU Pumps a & C.Caused by Broken Thermocouple Input Lead.Lead Wire Reconnected & Isolation reset.W/900221 Ltr ML20011F4921990-02-16016 February 1990 LER 89-013-01:on 890907,Group I Isolation Received During Performance of Instrument Surveillance LIS-MS-401.Caused by Depressurization of Main Steam Line Low Pressure Switch. Surveillance Revised to Split Into Two parts.W/900216 Ltr ML20006E4501990-02-15015 February 1990 LER 89-010-01:on 890715 & 17,voltage Oscillations Noted on Div II Battery Charger,Resulting in Inoperability of HPCS Sys.Caused by Failure of Charger in High Voltage Shutdown Relay.Charger Energized & Relay replaced.W/900215 Ltr ML20006E4451990-02-14014 February 1990 LER 89-009-01:on 890619,diaphragm Leak Discovered in RCIC Steam Line High Flow Isolation Switch.Caused by 1 & 1/2-inch Tear in Diaphragm.Pressure Differential Switch Replaced & Calibr.Reported Per NRC Bulletin 86-002.W/900214 Ltr ML20006E3981990-02-14014 February 1990 LER 89-008-01:on 890228,reactor Vessel Low Water Level 2 Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.Channel Placed in Tripped Condition & All Static-O-Ring Pressure Switches to Be replaced.W/900214 Ltr ML20006E3951990-02-14014 February 1990 LER 89-010-01:on 890303,automatic Depressurization Sys Permissive Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.All Static-O-Ring Reactor Vessel Level Switches Will Be replaced.W/900214 Ltr ML19354D8361990-01-15015 January 1990 LER 89-018-00:on 891216,plant 250-volt Battery & RCIC Sys Declared Inoperable Due to Low Battery Electrolyte Temps. Caused by Failure of Div I Switchgear Heat Removal Sys Damper Actuators.Air Intake Dampers closed.W/900115 Ltr ML20042D3921990-01-0404 January 1990 LER 89-011-01:on 890826,spurious Reactor Protection Sys Actuation Occurred.Definite Cause of Trip Not Determined. Brief Disturbance in Reactor Protection Sys Allowed Some Contactors to Trip.Procedure revised.W/900104 Ltr ML20005E2741989-12-22022 December 1989 LER 89-028-00:on 891204,RHR Shutdown Cooling Suction Header Outboard Isolation Valve Automatically Isolated.Caused by Miscommunication Between Technician & Station Operator.Task Force Developed to Review event.W/891222 Ltr ML19351A6301989-12-15015 December 1989 LER 89-006-01:on 890214,reactor Vessel Low Water Level 3 Switch Setpoint Found Out of Tolerance.Caused by Setpoint Drift.Level Switch to Be Replaced by Analog Trip Sys During First Quarter 1990.W/891215 Ltr ML20011D1341989-12-14014 December 1989 LER 89-017-00:on 891117,flow Switch FS-2E22-N006 Found W/ Setpoint Out of Tolerance Above Reject Limit.Caused by Setpoint Drift.Work Request Written to Replace Flow Switch. W/891214 Ltr ML19351A6751989-12-12012 December 1989 LER 89-027-00:on 891113,primary Containment Isolation Sys Group I Isolation Occurred While Performing Instrument Surveillance.Caused by Loss of Power to Leak Detection Sys Logic.Isolation reset.W/891213 Ltr ML19332F0081989-12-0808 December 1989 LER 89-016-00:on 891109,RWCU Isolation Occurred While Instrument Surveillance on Ventilation Differential Temp Isolation Functional Test in Progress.Caused by Faulty Thermocouple.Thermocouple repaired.W/891208 Ltr ML20005D6621989-12-0606 December 1989 LER 89-026-00:on 891106,inadvertent Primary Containment Isolation Actuation Occurred While Clearing out-of-svc. Caused by Inadequate Logic Setup During Mod Installation. Trip Status & Output Switches repositioned.W/891206 Ltr ML19332F2431989-12-0101 December 1989 LER 89-025-00:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Equipment Operator Closed Door Containing Relays.Caused by Misalignment of Door.Isolations Reset,Bus Energized & Circuit Logic tested.W/891201 Ltr ML19332E6581989-11-29029 November 1989 LER 89-015-00:on 891030,shift Control Room Engineer Noted That Quarterly Standby Liquid Control Operating Surveillance LOS-SC-Q1 Was Past Critical Date.Caused by Clerical Data Entry Error.Missed Surveillance performed.W/891129 Ltr ML19332D5181989-11-22022 November 1989 LER 89-018-01:on 890515,RCIC Received Div I & Div II Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal When Steam Added to RCIC Steam Line. Special Test Initiated.Isolation Logic reset.W/891122 Ltr ML19327C2601989-11-17017 November 1989 LER 89-014-00:on 891020,primary Containment Isolation Sys Group 4 Isolation Occurred Causing Isolation Dampers to Close.Caused by Opening of Div 2 125-volt Dc Breaker.Power Supply replaced.W/891117 Ltr ML19325F3411989-11-13013 November 1989 LER 89-024-00:on 891013 & 30,unsealed Openings in Main Control Room Floor & Main Control Room West Wall Discovered. Caused by Wide Gap Between Structural Beam & Cable Tray. Openings Sealed & Fire Watch established.W/891113 Ltr ML19324C1751989-11-0808 November 1989 LER 89-012-01:on 890309,diaphragm Leak Found in Pressure Differential Switch 1E31-N013BB.Caused by Tear Found in Diaphragm.Replacement Switch Installed,Calibr & Functionally Tested satisfactorily.W/891108 Ltr ML20024E9121983-08-26026 August 1983 LER 83-093/03L-0:on 830801,discovered full-in Indication on Core Display for Control Rod 34-47 Inoperable.Caused by Failed Switching Transistor on Data Memory Board 19.Data Memory Board replaced.W/830826 Ltr ML20024B8381983-07-0505 July 1983 LER 83-060/03L-0:on 830606,following Turbine Trip & Scram Due to High Vibration on Main Turbine,Reactor Recirculation Breaker 4B Closed.Cause Undetermined.Auxiliary Contacts cleaned.W/830705 Ltr ML20024B0721983-06-16016 June 1983 Updated LER 83-012/03X-1:on 830210,w/reactor in Cold Shutdown,Setpoints for Switches 1E31-N612A/B Found Above Tech Spec Limits.Cause Unknown.Switches calibr.W/830616 Ltr ML20024A6961983-06-14014 June 1983 LER 83-051/03L-0:on 830516,reactor Protection Sys Trip Channel H2 Limit Switch Failed to Operate Properly.Cause Unknown.Limit Switch readjusted.W/830614 Ltr 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046B1481993-07-30030 July 1993 LER 93-012-00:on 930702,reactor Core Isolation Cooling Sys Declared Inoperable Due to Associated Bus Voltage Dropping Below TS Limits.Sent Operator to Cycle Timer Which Caused Affected Contact to reclose.W/930730 Ltr ML20045D9331993-07-0202 July 1993 LER 93-004-00:on 930604,unexpected CRD Low Charging Water Header Scram Received Followed by Charging Water Header A2/B2 Alarm.Caused by Crud or Foreign Matl Passing Through Suction Filter.Filters Cleaned & reused.W/930702 ML20045D7501993-06-23023 June 1993 LER 93-003-00:on 930524,Div 1 ECCS Initiation Signal Received & LPCS Pump,Lpci Pump 2A & EDG Unit 0 Automatically Started.Caused by Personnel Error.Pumps Secured & Event Documented in Personnel file.W/930623 Ltr ML20044E4161993-05-28028 May 1993 LER 92-009-01:on 920923,spurious Auto Start of CR Ventilation Emergency make-up Train Occurred Due to High Radiation Spike.Radiation Monitor Circuit modified.W/930528 Ltr ML20044E4191993-05-21021 May 1993 LER 93-011-00:on 930423,manual Scram Initiated.Caused by Disconnected Linkage on Valve Positioner on Heater Drain Valve Due to Loose Jam Nut.Tailgate Session Will Be Held W/ Instrument Maint Dept Re Jam nuts.W/930521 Ltr ML20044D5161993-05-15015 May 1993 LER 92-007-01:on 920613,high Radiation Spike Received from CR Ventilation Process Radiation Monitor,Initiating Emergency Makeup Train B.Caused by Normal Variations in Radiation Readings.Spike modified.W/930515 Ltr ML20044D5571993-05-14014 May 1993 LER 93-010-00:on 930414,DG Cooling Water Pump Automatically Tripped on Magnetic Overload.Caused by Inexperienced Trainee in Operation of Control Lever.Lesson Plans & Training Programs for Operators to Be reviewed.W/930514 Ltr ML20044C9801993-05-0707 May 1993 LER 91-010-01:on 910719 & 0805,CR a Ventilation Emergency Makeup Fan auto-started on Spurious Trip of CR Air Intake Process Radiation Monitor.Caused by Normal Variations in Background Radiation.Supply Board replaced.W/930507 Ltr ML20044B6161993-02-25025 February 1993 LER 93-002-00:on 930126,Unit 1 Manual Scram Due to a SRV Being Stuck Open Due to Duct Tape Being Over Actuators Air Valve Manifold Exhaust Port.Maint Procedures That Involve Cleanliness reviewed.W/930225 Ltr ML20024G9771991-05-10010 May 1991 LER 91-005-00:on 910410,determined That Tech Spec Required Surveillance of Suppression Chamber Oxygen Sampling Missed. Caused by Inadequate Review of Tech Spec Change.Drywell & Suppression Chamber Checked for oxygen.W/910510 Ltr ML20044A3851990-06-25025 June 1990 LER 90-008-00:on 900525,Tech Spec Hourly Fire Watch Missed Due to Miscommunications Between Security Personnel & Radiation Protection Personnel.Fire Watch re-established & Memo issued.W/900625 Ltr ML20043F1721990-06-0505 June 1990 LER 90-009-00:on 900510,RWCU Outboard Suction Isolation Valve 2G33-F004 Auto Closed Which Tripped RWCU Pump B. Caused by Procedure Deficiency.Procedure LTS-500-209 Will Be revised.W/900605 Ltr ML20043F1281990-06-0101 June 1990 LER 90-009-00:on 900511,apparent Ruptured Diaphragm Found on Pressure Differential Switch in RCIC Steam Line.Caused by Torn Diaphragm Inside Switch.Replacement Switch Installed, Calibr & Functionally Tested satisfactorily.W/900608 Ltr ML20043B5681990-05-23023 May 1990 LER 89-027-01:on 891113,primary Containment Isolation Sys Group 1 Isolation Occurred During Surveillance Testing. Caused by Burnt Out Window Light Bulbs on Alarm Window. Light Bulbs Replaced & Jumpers installed.W/900523 Ltr ML20043A7721990-05-18018 May 1990 LER 90-007-00:on 900421,reactor Protection Sys Bus a Transfer & Reactor Recirculation Hydraulic Power Unit a Inboard Isolation Valves Closed,Causing Partial Group II isolation.Out-of-svc Procedure revised.W/900518 Ltr ML20043D0591990-05-18018 May 1990 LER 90-008-00:on 900502,ESF Actuation of Control Room B Emergency Ctk Ventilation Makeup Fan Occurred.Caused by Procedure deficiency.LTS-800-205 & Similar Procedures Will Be revised.W/900601 Ltr ML20042H0211990-05-10010 May 1990 LER 90-006-00:on 900412,loop a Primary Containment Chilled Water Sys Inboard Isolation Valves & Reactor Bldg Closed Cooling Water Sys Inboard Isolation Valve Went Closed.Caused by Inadequate Procedure.Procedures revised.W/900510 Ltr ML20042F9001990-05-0404 May 1990 LER 90-005-00:on 900411,experienced Loss of Dc Power to Portion of Div I Primary Containment Isolation Sys Logic Which Resulted in Isolation Signal & Actuation.Caused by Failure to Update Drawings & procedures.W/900504 Ltr ML20042F1941990-04-30030 April 1990 LER 89-025-01:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Door Containing Undervoltage Relays Closed.Caused by Misalignment of Door.Door Repaired. W/900430 Ltr ML20012D5341990-03-16016 March 1990 LER 90-003-01:on 900201,RCIC Isolation Signal Occurred During Warmup.Caused by Spurious High Steam Flow Signal.Rcic Sys Piping Integrity Verified & Isolation Logic Reset.W/ 900316 Ltr ML20012D5371990-03-16016 March 1990 LER 90-002-01:on 900129,oil in Diesel Generator Governor 1A Found to Be Low & Could Not Be Seen in Sight Glass.Caused by Slow Leak from Compensation Needle Valve Plug.Proper Amount of Oil Added & Operability Test performed.W/900316 Ltr ML20012C4931990-03-15015 March 1990 LER 90-004-00:on 900213,control Room B HVAC Intake Radiation Monitor Lost Power Causing auto-start of Emergency make-up Train B.Caused by Blown Fuses.Fuses Replaced.Logic Revs for Radiation Monitors Will Be installed.W/900315 Ltr ML20012B6501990-03-0909 March 1990 LER 90-002-00:on 900209,Operating Surveillance LOS-TG-W1 Determined to Have Exceeded Required Testing Interval,Per Tech Spec 3/4.7.10.Caused by Personnel Error.Personnel Counseled & Ref Procedures Will Be revised.W/900309 Ltr ML20012B5521990-03-0808 March 1990 LER 90-001-00:on 900206,full Reactor Scram Occurred During Instrument Surveillance Testing.Caused by Actuation of APRM E Trip Circuitry.Shutdown Margin Revised & Caution Card Placed on Control Room Bench board.W/900308 Ltr ML20011F8251990-03-0202 March 1990 LER 90-003-00:on 900201,RCIC Received Div 2 Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal Generated When Steam/Water Mixture Admitted to RCIC Steam Line.Isolation Logic reset.W/900302 Ltr ML20011F5551990-02-28028 February 1990 LER 90-002-00:on 900129,after Filling Diesel Generator 1A Governor W/Oil,Generator Started & Declared Inoperable. Caused by Slow Leak Coming from Compensation Needle Valve Plug.Oil Added & Plug Washer replaced.W/900228 Ltr ML20006F5951990-02-21021 February 1990 LER 90-001-00:on 900122,RWCU Sys Received Div 1 Leakage Detection Ambient Temp High Isolation Signal,Causing Trips of RWCU Pumps a & C.Caused by Broken Thermocouple Input Lead.Lead Wire Reconnected & Isolation reset.W/900221 Ltr ML20011F4921990-02-16016 February 1990 LER 89-013-01:on 890907,Group I Isolation Received During Performance of Instrument Surveillance LIS-MS-401.Caused by Depressurization of Main Steam Line Low Pressure Switch. Surveillance Revised to Split Into Two parts.W/900216 Ltr ML20006E4501990-02-15015 February 1990 LER 89-010-01:on 890715 & 17,voltage Oscillations Noted on Div II Battery Charger,Resulting in Inoperability of HPCS Sys.Caused by Failure of Charger in High Voltage Shutdown Relay.Charger Energized & Relay replaced.W/900215 Ltr ML20006E4451990-02-14014 February 1990 LER 89-009-01:on 890619,diaphragm Leak Discovered in RCIC Steam Line High Flow Isolation Switch.Caused by 1 & 1/2-inch Tear in Diaphragm.Pressure Differential Switch Replaced & Calibr.Reported Per NRC Bulletin 86-002.W/900214 Ltr ML20006E3981990-02-14014 February 1990 LER 89-008-01:on 890228,reactor Vessel Low Water Level 2 Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.Channel Placed in Tripped Condition & All Static-O-Ring Pressure Switches to Be replaced.W/900214 Ltr ML20006E3951990-02-14014 February 1990 LER 89-010-01:on 890303,automatic Depressurization Sys Permissive Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.All Static-O-Ring Reactor Vessel Level Switches Will Be replaced.W/900214 Ltr ML19354D8361990-01-15015 January 1990 LER 89-018-00:on 891216,plant 250-volt Battery & RCIC Sys Declared Inoperable Due to Low Battery Electrolyte Temps. Caused by Failure of Div I Switchgear Heat Removal Sys Damper Actuators.Air Intake Dampers closed.W/900115 Ltr ML20042D3921990-01-0404 January 1990 LER 89-011-01:on 890826,spurious Reactor Protection Sys Actuation Occurred.Definite Cause of Trip Not Determined. Brief Disturbance in Reactor Protection Sys Allowed Some Contactors to Trip.Procedure revised.W/900104 Ltr ML20005E2741989-12-22022 December 1989 LER 89-028-00:on 891204,RHR Shutdown Cooling Suction Header Outboard Isolation Valve Automatically Isolated.Caused by Miscommunication Between Technician & Station Operator.Task Force Developed to Review event.W/891222 Ltr ML19351A6301989-12-15015 December 1989 LER 89-006-01:on 890214,reactor Vessel Low Water Level 3 Switch Setpoint Found Out of Tolerance.Caused by Setpoint Drift.Level Switch to Be Replaced by Analog Trip Sys During First Quarter 1990.W/891215 Ltr ML20011D1341989-12-14014 December 1989 LER 89-017-00:on 891117,flow Switch FS-2E22-N006 Found W/ Setpoint Out of Tolerance Above Reject Limit.Caused by Setpoint Drift.Work Request Written to Replace Flow Switch. W/891214 Ltr ML19351A6751989-12-12012 December 1989 LER 89-027-00:on 891113,primary Containment Isolation Sys Group I Isolation Occurred While Performing Instrument Surveillance.Caused by Loss of Power to Leak Detection Sys Logic.Isolation reset.W/891213 Ltr ML19332F0081989-12-0808 December 1989 LER 89-016-00:on 891109,RWCU Isolation Occurred While Instrument Surveillance on Ventilation Differential Temp Isolation Functional Test in Progress.Caused by Faulty Thermocouple.Thermocouple repaired.W/891208 Ltr ML20005D6621989-12-0606 December 1989 LER 89-026-00:on 891106,inadvertent Primary Containment Isolation Actuation Occurred While Clearing out-of-svc. Caused by Inadequate Logic Setup During Mod Installation. Trip Status & Output Switches repositioned.W/891206 Ltr ML19332F2431989-12-0101 December 1989 LER 89-025-00:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Equipment Operator Closed Door Containing Relays.Caused by Misalignment of Door.Isolations Reset,Bus Energized & Circuit Logic tested.W/891201 Ltr ML19332E6581989-11-29029 November 1989 LER 89-015-00:on 891030,shift Control Room Engineer Noted That Quarterly Standby Liquid Control Operating Surveillance LOS-SC-Q1 Was Past Critical Date.Caused by Clerical Data Entry Error.Missed Surveillance performed.W/891129 Ltr ML19332D5181989-11-22022 November 1989 LER 89-018-01:on 890515,RCIC Received Div I & Div II Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal When Steam Added to RCIC Steam Line. Special Test Initiated.Isolation Logic reset.W/891122 Ltr ML19327C2601989-11-17017 November 1989 LER 89-014-00:on 891020,primary Containment Isolation Sys Group 4 Isolation Occurred Causing Isolation Dampers to Close.Caused by Opening of Div 2 125-volt Dc Breaker.Power Supply replaced.W/891117 Ltr ML19325F3411989-11-13013 November 1989 LER 89-024-00:on 891013 & 30,unsealed Openings in Main Control Room Floor & Main Control Room West Wall Discovered. Caused by Wide Gap Between Structural Beam & Cable Tray. Openings Sealed & Fire Watch established.W/891113 Ltr ML19324C1751989-11-0808 November 1989 LER 89-012-01:on 890309,diaphragm Leak Found in Pressure Differential Switch 1E31-N013BB.Caused by Tear Found in Diaphragm.Replacement Switch Installed,Calibr & Functionally Tested satisfactorily.W/891108 Ltr ML20024E9121983-08-26026 August 1983 LER 83-093/03L-0:on 830801,discovered full-in Indication on Core Display for Control Rod 34-47 Inoperable.Caused by Failed Switching Transistor on Data Memory Board 19.Data Memory Board replaced.W/830826 Ltr ML20024B8381983-07-0505 July 1983 LER 83-060/03L-0:on 830606,following Turbine Trip & Scram Due to High Vibration on Main Turbine,Reactor Recirculation Breaker 4B Closed.Cause Undetermined.Auxiliary Contacts cleaned.W/830705 Ltr ML20024B0721983-06-16016 June 1983 Updated LER 83-012/03X-1:on 830210,w/reactor in Cold Shutdown,Setpoints for Switches 1E31-N612A/B Found Above Tech Spec Limits.Cause Unknown.Switches calibr.W/830616 Ltr ML20024A6961983-06-14014 June 1983 LER 83-051/03L-0:on 830516,reactor Protection Sys Trip Channel H2 Limit Switch Failed to Operate Properly.Cause Unknown.Limit Switch readjusted.W/830614 Ltr 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217C9121999-10-12012 October 1999 SER Input Authorizing Licensee Proposed Request to Modify Definition of Core Alteration in Section 1.0 of TS & Update Sections 3/4.1,3.4.3 & 3/4.9 to Reflect Proposed Definition Change ML20217F9091999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for LaSalle County Stations,Units 1 & 2.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212C4501999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for LaSalle County Station,Units 1 & 2.With ML20210R0671999-07-31031 July 1999 Monthly Operating Repts for July 1999 for LaSalle County Station,Units 1 & 2.With ML20210C1681999-07-0909 July 1999 Seventh Refueling Outage ASME Section XI Summary Rept ML20209H1501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for LaSalle County Station,Units 1 & 2.With ML20195J7871999-05-31031 May 1999 Monthly Operating Repts for May 1999 for LaSalle County Station,Units 1 & 2.With ML20209E1431999-05-31031 May 1999 Cycle 8 COLR, for May 1999 ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations ML20206N2071999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for LaSalle County Station,Units 1 & 2.With ML20205L8421999-03-31031 March 1999 Rev 2 to EMF-96-125, LaSalle Unit 2 Cycle 8 Reload Analysis ML20205L8301999-03-31031 March 1999 Administrative Technical Requirements App B (Amend 26) LaSalle Unit 2 Cycle 8 COLR & Reload Transient Analysis Results, for Mar 1999 ML20205R2721999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for LaSalle County Station,Units 1 & 2.With ML20205L8391999-03-22022 March 1999 Rev 2 to 960103, Neutronics Licensing Rept for LaSalle Unit 2,Cycle 8 ML20204C8141999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for LaSalle County Station,Units 1 & 2.With ML20199E4601998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for LaSalle County Station,Units 1 & 2.With ML20207C7371998-12-31031 December 1998 Annual Rept for LaSalle County Station for Jan 1998 Through Dec 1998 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20198B3801998-12-14014 December 1998 SER Accepting one-time Request for Relief from Certain Provisions of Section XI of ASME Boiler & Pressure Vessel Code,Per 10CFR50.55a for Certain Plant Safety/Relief Valves ML20206N2261998-12-0909 December 1998 LER 98-S03-00:on 981116,protected Area Was Entered Without Current Authorization for Unescorted Access Due to Programmatic Deficiency Error.Changed Badge Control Process ML20197K0981998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for LaSalle County Station,Unts 1 & 2.With ML20196B1441998-11-23023 November 1998 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Bindings of Safety-Related Power-Operated Gate Valves ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195D3191998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for LaSalle County Station.With ML20154H6781998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20153D0191998-09-18018 September 1998 Part 21 Rept Re Defect in Gap Conductance Analyses for co- Resident BWR Fuel.Initially Reported on 980917.Corrective Analyses Performed Demonstrating That Current Operating Limits Bounding from BOC to Cycle Exposure of 8 Gwd/Mtu ML20153C7621998-09-18018 September 1998 Safety Evaluation Acceping NRC Bulletin 95-002, Unexpected Clogging of RHR Pump Strainer While Operating in Suppression Pool Cooling Mode ML20153C6771998-09-17017 September 1998 Part 21 Rept Re Defect Relative to MCPR Operating Limits as Impacted by Gap Conductance of co-resident BWR Fuel at Facilities.Operating Limit for LaSalle Unit 2 & Quad Cities Unit 2 Will Be Revised as Listed ML20151W0241998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for LaSalle County Station.With ML20237E2921998-08-21021 August 1998 Special Rept:On 980811,channel 5 of Lpms Became Inoperable. Caused by Channel Failed pre-amplifier Located Inside Primary Containment at Inboard Side of Electrical Penetration E-19.Initiated Repairs of Channel ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237B4861998-07-31031 July 1998 Monthly Operating Repts for July 1998 for LaSalle County Nuclear Power Station Units 1 & 2 ML20236V7701998-07-31031 July 1998 Revised LaSalle Unit 1 Cycle 8 COLR & Reload Transient Analysis Results ML20236P8231998-07-14014 July 1998 Special Rept:From 980614-17,various Fire Rated Assemblies Were Inoperable for Period Greater than Seven Days.Caused by Test Equipment Being Routed Through Fire Doors.Established Fire Watches & on 980619 Assemblies Were Declared Operable ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20236L8041998-07-0606 July 1998 Safety Evaluation Granting Licensee 980304 Request for Second 10-yr Interval Pump & Valve IST Program Plan,Rev 2, Including Changes to 2 ASME Boiler & Pressure Vessel Code Relief Requests Previously Submitted in Rev 1 ML20236P3611998-06-30030 June 1998 Monthly Operating Repts for June 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20249C4891998-06-22022 June 1998 Special Rept:On 980522,Fire Detection Zone 1-31 Was Noted out-of-service for More than 14 Days.Detection Sys Was Taken out-of-service on 980508 to Prevent False Alarms During Hot Work Activities.Sys Was Returned to Operable Status 980528 ML20248M3101998-05-31031 May 1998 Monthly Operating Repts for May 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20236V7771998-05-31031 May 1998 Rev 1 to 24A5180, Supplemental Reload Licensing Rept for LaSalle County Station Unit 1 Reload 7 Cycle 8 ML20217Q7041998-05-0404 May 1998 Safety Evaluation Accepting Util Request to Leave Leak Chase Channels Plugged During Performance of Containment ILRT ML20247M4491998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for LaSalle County Station ML20216F4941998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for LaSalle County Station,Units 1 & 2 ML20217N6581998-03-30030 March 1998 Special Rept on Fire Detection,Deluge Sys & Fire Rated Assemblies During Period of 980303-25.Established Fire Watches Until Affected Equipment Is Returned to Operable Status ML20216D9511998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for LaSalle County Station,Units 1 & 2 ML20247M4631998-02-28028 February 1998 Rev Monthly Operating Rept for Feb 1998 for LaSalle County Station ML20203D7241998-02-20020 February 1998 Special Rept:On 980118,Fire Detection Zones 1-18 & 2-18 Taken out-of-svc to Prevent False Alarms During Hot Work Activities on Auxiliary Electric Equipment Room Ventilation Sys.Fire Watches Will Remain in Place ML20202G9851998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for LaSalle County Station,Units 1 & 2 ML20199K1651998-01-23023 January 1998 Rev 65h to Topical Rept CE-1-A, Comm Ed QA Tr 1999-09-30
[Table view] |
Text
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a Commonweshh Edison W .- 'L[/,
LaSt11e County N;.c!nr Station
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~ Rura' Route #1, Box 220 Marseilles, Illinois 61341 ]
'x Telephone 615/357 6701
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- 4. g December 13, 1989 p
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Director of Nuclear Reactor Regulation
' U.S. Nuclear Regulatory Comunission . l Mail Station P1-137 Washington, D.C. 20555
Dear Sir:
1 Licensee avant Report #89-027-00, Docket #050-373 is being
- 4 submitted to your office in accordance with ,
10CFit50.73(a)(2)(iv) .
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ch h(G.J.Diede Station Manager t,aSalle County Station ,
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xc: Nuclear Licensing Administrator NRC Resident Inspector h NRC Region III Administrator P'@h INPo '- Records Center
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LICENSEE EVEN1 REPC31 (LER) , p Docket Nunt>cr (2) Pace (3)
F6cility me (1) 1loF!0l6 LaSalle County Station Unit 1 0]$101010131713 Title (4) Primary Containment Isolation During Surveillance Testing Due to Burned Out Annunciator Wii./e.i Licht Bulbs Other Facilities involved,_(8)
Eeent Date (5) LER_N atper (6? Reoort Date (7)
Sequential /// Revision Month Day Year Facility W mes Docket Nat>er(s) t Month Day Year Year ///
fff fff Nuntper
/// Nuntper ///
01 51 01 01 of I i el 9 el 9
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THis RCMT 15 $USMITTED PURSUANT TO THE REQUIREMENTS OF 10CFR (Check one or is re of the followinn) til)
" 0 20.402(b) _ 20.405(c) .X,_ 50.73(a)(2)(lv) ,,,_,
73.7)(b) 20.40i(a)(1)(l) 50.36(c)(1) 50.73(a)(2)(v) ,,,,,_ 73.7t(c)
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,,,,_.0ther (Specify LEVEL , 20.40S(a)(1)(ll) _
50.36(c)(2) ,, 50.73(a)(2)(vil) g ,_,_
20.40$(a)(1)(111) 50.73(a)(2)(l) 50.73(a)(2)(vill)(A) in Abstract (10) 01 01 0 ,,,,,,, _ __,,
below and in
/// // / u ///,/,/,/,/// , / ,,,,,, 20.405(a)(1)(lv) ,,,,_
50.73(a)(2)(ll) __ 50.73(a)(2)(vill)(B)
/'/'/ 20.405(a)(1)(v) 50.73(a)(2)(lii). _ 50.73(a)(2)(x) Text)
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f f LICENSEE CONTACT FOR THis LER (12)
TELEPHONE NUSER Name AREA CODE Don Crowl. Reaulatory Assurance. extension 2860 8 l 1 15 31 Sl 71 -l 61 71 61 I werLETE ONE LINE FOR EACH wrivuiNT FAILURE DESCRIBED IN THis REPORT (13) 7 CAUSE SYSTEM C0fr0NENT MANUFAC- REPORTABLE CAUSE SYSTEM COPPOWENT MRNUFAC- REPORTABLE TURl!R TO NPRDS TURER TO NPRDS i i i N i l i l i l
- 0 l i I I l l l l l l l l l l I i l l Expected Month l Day l Year SUPPLEENTAL REPORT EXPECTED (14) ,,,_
Sutunission
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lves (if ves, co olete EXPECTED SU8 MIS $10N DATE) ,__
YlNO ! ll ll ABSTRACT (Limit to 1400 spaces, i.e, approximately fifteen single-space typewritten lines) (16)
On Noventier 13, 1989 at 1823 hours0.0211 days <br />0.506 hours <br />0.00301 weeks <br />6.936515e-4 months <br /> with Unit I defueled, a Primary Containment Isolation System (PCIS) Group 1 isolation occurred while perfoming LaSalle Instrument Surveillance LIS-MS-1078, " Unit 1 Reactor Vessel Low
- Water Level I and Level 2 1 solation Instrument channels 8 and D Refuel Calibration." A full PCIS Group 1 lsolation occurred because the other half of the isolation logic was tripped due to the loss of leak l
detection power from the AC electrical bus 135X and 135Y outage. No valve movement occurred because all the l
Main Steam system isolation valves were previourly deenergized due to other scheduled refuel outage work.
The alarm windows were extinguished and the light bulbs for alam windows F504, "CHAN Al/A2 MSIV ISOL TRIP,"
and E504, "CHAN 81/82 MSly ISOL TRIP." on the Control Room panel 1H13-P601 were later detemined to be burnt out when testing was done. This prevented both the Unit 1 Nuclear Station Operator (PSO, licensed Reactor Operator) and the Instrument Maintenance Technician from detecting that half of the isolation logic was initiated when the AC electrical bus 135X was deenergized.
A review of the guidance for what an alam window test requires will be performed.
This event is being submitted pursuant to the requirements of 10CFR50.73(ah2)tiv) due to the actuation of an l
Engineered Safety Feature System.
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tlCENSEE EVENT REPORT (LER) itXT COWilWuAtl0W _ Fom Rev 2.0
, LtR WuegER (6) Page (3)
.(p ' PACllllY NAME (1) 00CKLI NUagER (2)
Year fj// Sequential ///
/ Revision f fff
/// Nmber /// thster L W lle County Station unit 1 0 1 5 1 0 1 0 1 0 1 31 71 3 e19 - 012I7 - 0I o of 2 0F of 6 TEXT ' Energy Industry identification System (Elis) codes are identified in the text as [XX)
~ PLANT AIS $1 STEM IDENilflCATION
+
General Electric - Dolling Water Reactor Energy Industry Identification System (Ells) codes are identified in the text as (XX).
p A. CONDITION PRIOR TO EVENT Event Date: 11/13/09 Event fles: 1823 Hours Unit (s):' 1 Reactor Mode (s): Defueled Mode (s) Name: Defueled Wr MO: 1 l l
1
- 8. . OESCRiffl0N OF EVENT on llovember 13,1989 at 1823 hours0.0211 days <br />0.506 hours <br />0.00301 weeks <br />6.936515e-4 months <br /> with Unit I defueled, a Primary Contalmuent Isolation System (PCis, PC) [JM) Group i isolation occurred while performing LaSalle lastrument Surveillance LIS 4tS-1078, " Unit i
- 1 Reactor vessel low Water Level 1 and Level 21 solation Instrement Channels 8 and 0 Refuel Calibration." Both Inboard'and Outboard Maln Steam Line Isolation valves (MS!V, MS) [$9] and Maln Steam les valve line drain valves were deenergized prior to the isolation due to planned refuel outage work.
motion took place during this event. The PCIS Group 1 isolation only resulted in relay and alam actions.
At 0715 hours0.00828 days <br />0.199 hours <br />0.00118 weeks <br />2.720575e-4 months <br /> on November 13,1989.the "A" channel calibration was completed in acconiance with LaSalle '
instrument Surveillance L15-4tS-107A, " Unit 1 Reactor Vessel Low Water Level I and Level 2 Isolation l Instrissent Channels A and C Refuel Calibration." .
L At 0725 hours0.00839 days <br />0.201 hours <br />0.0012 weeks <br />2.758625e-4 months <br /> "C" channel callbration was started in accordance with LIS-MS-107A.
i At 1305 hours0.0151 days <br />0.363 hours <br />0.00216 weeks <br />4.965525e-4 months <br /> the Division 1 AC Electrical Olstribution Duses 135X and 135Y (AP) [ED) were deenergized J and taken out-of-service in accordance with LaSalle Aeninistrative Procedure LAP-900-4, " Equipment Out-of-Service Procedure," for scheduled refuel outage work. The bus 135X and 135Y outage deenergized the Olvision I Leak Detection logic (LD/E31) (lJ). (Relays.1E31A43A and IE31A43C doenergized.)
Relays' IE31A43A and IE31A43C cause relays 1821H47A and 1821H47C to deenergize on loss of powe
. area dublent temperature or high differential temperature signal. When relays 1821H47A and 1821H-47C This occurred during the day shift and doenergize, a channel Al and A2 MSIV isolation signa) occurs. +
caused no consequence to testing the Olvision I logic per LIS-MS-107A. (only half of the isolation logic was made up at this time.)
I At 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br /> the calibration of the "C" channel per LIS-StS.107A was stopped for the shift to allow s
shift turnovers (the exchange of day shift personns) with afternoon shift personnel) to take place.
- At 1540 hours0.0178 days <br />0.428 hours <br />0.00255 weeks <br />5.8597e-4 months <br /> the calibration of the "C" channel was resisned per L15-MS-107A.
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i Fonn Rev 2.0
- llCENSEE FVENT REPORT (LER) TEXT COWilNuATION Page (3)
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DOCKET NUMBER (2) LER WU9ER (6)
IACIL11Y NAME (1)
Year ffj/
/ Sequential /// Revision j fff !
/// Nweer /// Nweer ,
01 0 01 3 01 6 LaSalle County Station unit 1 015101010131713 819 - 01217 - 0F TEXT Energy Industry Identification System (Ells) codes are identified in the text as [XX) ,
- 5. DESCRIPil0N OF EVENT (Continued)
At 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br /> the Instrument Maintenance (IM) personnel coupleted the calibration of the "C" channel per LIS-Jis-107A.
At 1630 hours0.0189 days <br />0.453 hours <br />0.0027 weeks <br />6.20215e-4 months <br /> the calibration of *t" channel was started in accordance with LIS4tS-1078. The surveillance test was authorized by the Shift Engineer (SE, licensed Senior Reactor Operator), Shift Control Roam Engineer (SCRE, licensed Senior Reactor Operator) and Unit 1 Nuclear Station operator (WSO, licensed Reactor Operator) prior to beginning the surveillance test.
At the beginning of the surveillance test, the computer points (CX/C91) [LD) were verlfled to indicate as follows:
- a. 0997, "LO L0 RX WTR LVL OlV 81 -N-LO"
- b. C500. "VERY L0 RX WTR LVL DIV ll - N-LO"
- c. C581, "RPS CH B1 INSTR GROSS Fall - AVAIL"
- d. C582, "RPS CH S1 INSTR POER LOSS - AVAIL"
- e. C564, "RPS CH B2 INSTR OROSS Fall - AVAIL"
- f. C505, "RPS CH B2 INSTR POER LOSS - AVAIL" t At the Control Rown panel IH13-P603 the following alems (AN) (18) were verifled reset or clear (slow l
flash or extinguished):
- a. B401, "DIV 1 RX VESSEL WIR LVL 2 LO"
- b. 8412. "DIV 2 RX VESSEL WTR LVL 2 LO"
- c. 6405, "CHAN A1/91 PRI CNMT PRESS HI"
- d. 1)a09, "CHAN A2/82 PRI CNMT PRESS Hi*
- e. A210. "CHAN A1/81 RX VESSEL WTR LYL 1 LO-LO-LO" At the Contro) Room panel 1Hl3-P601 alam E504, "CHAN B1/82 MSIV ISOL TRIP " was verified reset or clear (slow flash or extinguished).
LIS-MS-1078 did not require the IM's to check the Auxillary Electric Room panels 1H13-P622 and IH13-P623 The Malp Stem isolation Valve (MSIV, MS) solenold valve status lights if the MSIV's were closed. ,.
solenoid status lights are nonnally energized when no isolation signal is present.
The alam windows were extinguished and the light bulbs for alann windows F504, "CHAN A1/A2 MSIV ISOL TRIP." and E504, "CHAN 81/82 MSiv 150L TRIP," on the Control Room panel 1H13-P601 were later detem to be burnt out when testing was done, n#ien the test switch 1821-5208, "MSL DRN ISOL LOGIC," was turned to test in accordance with LIS-MS-1078 a full PCIS Group 1 isolation occurred because the other half of the isolation logic was tripped due to the loss of leak detection power from the AC electrical bus 135X and 135Y outage. No valve movement occurred because all the Main Stean system isolation valves were previously closed due to other scheduled refuel outage work. Both the Unit 1 NSO and the IM did not realize a full Group 1 1 solation had occurred at this time because the annunciator light bulbs were burnt out for alann windows- E504 --
and F504, and no valve motion took place.
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rom Rev 2.0
- LICENSEE [ VENT REPORT (LER) IIx1 CONTINUATION LER NUMBER (6) Pace (3)
FACllliY NAME (1) 00CKLI NUMBER (2)
Year #// Sequential M Revision ,
Eff Net >er fff Net >er 01217 01 o 01 4 0F 01 6 0 l S 1 0 1 0 1 0 1 31 71 1 81g
- - f LaSalle County Station Unit 1 TEK1 Energy Industry identification System (Ells) codes are identified in the text as (XX) l B. DESCRIPTION OF EVENT (Continued)
The Instr aent Maintenance personnel proceeded to the fleid and isolated 1821 4 4028 Division 11 reactor When level transmitter and attached the test equipment to simulate lowering reactor water vessel level.
the trip setpoint was reached, the Olvision 11 reactor water level trip unit opened contacts in the logic which deenergized the It21H-478 relay. The Olvision 11 reactor vessel water level trip indicator t unit trip light and alam window A210 "A1/81 LYL 2 LO LVL," lilminated. The alam window E504 did not 111 minate at this point. The IM's stopped testing to investigate why the alam window E504. "CHAN 81/82 MSly !$0L TRIP," did not 111uminate. The IM's r4 quested the NSO to make an annunciator check and it was discovered that both alam window E504 and F504 had no indication because the window light bulbs were burnt out. At this point the IM's notified the IM foreman of the probism. ,
The IM personnel were requested to return reactor level transmitter 1821-N4022 to service and the ;
Division 11 isolation was reset. The light bulbs were replaced for alam windows E504 and f 504 and the operatingDepartmentrequestedtheIM'stojupertheIE31A-K3AandIE31A-K3CrelaysforOlvisionIto allow testing of Division 11 logic to continue. This was done in accordance with LaSalle Aeninistrative Procedure LAP-240-4, " Temporary System Change," and testing was completed without any further event.
this event is being submitted pursuant to the requirements of 10CFR50.73(a)(2)(lv) due to the actuation of an Engineered Safety Feature System.
C. APPARENT CAUSE OF EVENT l
l toth alam windows E504, "CHAN 81/82 MSIV ISOL TRIP " and F504, "CHAN A1/A2 MSIV ISOL TRIP " had no indication because the window light bulbs were burnt out. This caused both the Unit 1 NSO and th* IM to When the proceed with LIS-MS-1078 believing that no other isolation signal was present at this time.
test switch 1821-5208, "MSL DRN ISOL LOGIC," was turned to test in accordance with LIS-MS-1078, a full PCIS Group 1 Isolation occurred.
When AC electrical bus 135X was deenergized for planned outage work, a Division 1 PCIS Group 1 i signal resulted (only half of the isolation logic was made up at this time.) due to the loss of power to the Leak Detection system logic which inputs to the PCIS Cogic. This was done during the day shift (0700-1500 hours). After shift change the afternoon shift (1500-2300 hours) Unit 1 NSO checked Control Room panel alams per LaSalle Operating Surveillance LOS-AA-SI, "Shiftly Surveillance," and not notice any extinguished alam window light bulbs. The Unit 1 NSO demanded an alam suunary to out on the Sequential Event Recorder typer (alann typer, AN) [lQ). A detailed review of the printout wasn't perfomed due to the work load during the shift and the neerous amount of clanns Insted on the
- typer. Many alanas were caused from the amount of work requiring systems to be in an off-nomal condition during a refueling outa08.
The LaSalle Instrument Surveillance procedure did not require verification of the alanns printed out by the Sequential Event Recorder suunary. This procedure also did not require the IM to verify the MSly The MSIV's solenoid status lights energized in the Auxiliary Electric Room if the MSIV's are closed. Checking were closed due to planned refuel outage work and were deenergized to allow work to continue.
the alann summary printout may have allowed the WSO or IM to identify that an isolation signal was present. Checking the solenoid status lights for the M51V's would not have helped in this event-because the MSIV's were out of service and the solenoids deenergized to support planned outage work.
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' , f om Rev 2.0_ i LICfW5it EVlWT REPORT (LtR) itXT CONilWUATI E k' age (3) 00CKli WUMBER (2) _ t[R WOMB (R (3)
F ACllliY NAML (1) Revision j/j/j/ Sequential Year //
/// Wunt>er
/j/j f
// Nweer__ .
01217 01 0i015 0F 01 6 0 l $ 1 0 1 0 1 0 l 31 71 3 9l9 LaSalle County Station Unit 1 Energy industry identification System (Ell 5) codes are identified in the text as [XX) l 1 EXT I
C. APPARENT CAUSE OF EVENT (Contir9ed)
When AC electrical bus 135X was deenergized the Unit i N50 on the afternoon shift did not realize th power was also lost to the Olvision I Leak Detection system which inputs to the PC15 syste isolations. Mores 11y the M50 would be aware of the condition of the system by the indication of C Room alarus.
There are no specific procedures or lists (outside design drawings) which leentify every effect a bus outage has.
The SCRE who prepared and reviewed the AC electrical bus 135X and 135Y outage knew that the valv associated with the FC15 Group 1 Isolation logic were all out of service closed or in their isola Rd position. The SCRE felt that it would not be a concern during subsequent testing that would cause an The SCRE used isolation because no actual valve rovement would take place, only relay actuation.
LaSalle Emergency Plan laplementing procedure LIP-1310-1, " Notifications," as a reference for ma this interpretation. This evaluation was not connunicated to af ternoon shift personnel.
D. SAFETY ANALYSIS OF EVENT A loss of power to the Bus outages are performed for modification work during planned unit outages.
Leak Detection system provided a Olvision I primary containment isolation system actuatlon as des The safety significance of this event is mirilmal since the unit was defueled and the valves that w have isolated were already in the closed position due to planned outage work.
E. CORPICTIVE ACT3DNS At 1945 hours0.0225 days <br />0.54 hours <br />0.00322 weeks <br />7.400725e-4 months <br /> the IH personnel wre requested to return reactor level transmitter 1821-N4028 to se and the Division 11 isolation was reset, f
1 The light bulbs were replaced for alarm windows E504, "CHAN 81/82 MSIV 150L TRIP," and F l M51V 15CL TRIP."
On Notenber ad,1989 at 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> the IM's installed jumpers in accordance with LaSalle Acalnistl Procedure LAP-240-4, "Tauporary System Change," (TSC 1-983-89) to prevent Main Steem isolation l
(M51V) Group i PC15 lse sation frtun occurring while a half isolation signal is present due to AC '
electrical bus 135X/Y outage. This was done to a. low testing of Olvision 11 logic to contin 9e.
At 1240 hours0.0144 days <br />0.344 hours <br />0.00205 weeks <br />4.7182e-4 months <br /> on Novsaber 14, 1999, L15-MS-107B was conpletes satisfactorily without any further etent.
All alarm windows for both Unit I and 2 main Control Room have been checked to verify both light bul in each window are working properly.
1 The Operating Department will review the need to revise procedures to provide more guidance on wh alars window test regulres, such as checking each wladow to determine if both bulbs are working pro ,
when tested. Action item Record (AIR) 373-200-89-11201 will track this correct;ve action, ..
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1
' Forn Rev 2.0 l tlCtW5tE EVtWT REPOR? (tfR) ItXT 00NilWUA110W __
,__ Page (3) l F ACILITY WAME (1) 00CKEl NUMBER (2) _ llR WVMRtR (0)
Year // 5equential // Revision l j/j/j
// Wueer /j/j f
// Wueer !
01 0 01 6 01 6 C l 5 1 0 1 0 1 0 l 31 71 3 8I9 -f01217
- 0F Le411e County Station Unit I
- TEXT Energy industry identific?llon System (Ells) codes are identi(led in the text as (XX.]
, E. CORRf;.'TIVE ACTIONS (Continued) ,
AC electrical but outant procedures will be developed to assist the Operating personnel in identifying AIR potential probisms which will arise due to doenergizing equipment or logic system power supplies.
373-200-49-11202 will track these procedures.
The Trainir.g Department will review this event to determine if additional training is required to insure i
proper turntsver information that could effect Engineered safety Featured system actuation reportability is discussed. AIR 373-200-09-11203 will track the completion of this review.
A General Inforination Motificatloa (GIN) wl11 be developed to review inis event with Operating,
! Melntenance and Technical Staff personnrI asphasizing the luportance of verifying or reverifying the I
required initial conditions just prior to performing a test or surveillance to prevent inadvertent Engineer # Safety Featured System acts.ations. AIR 373-200-49-11204 will track the coupktion of this GIN..
F. PREVIOUS EVENTS LER Nunber Title 373/8444940 Secondary contaltunent isolation During Testing 373/84-074-00 Reactor Water Cleanup Isolation 373/07-009-00 Group IV isolation During Survrillance Test Due to Instrassent Maintenance Procedure inadequacy 373/8743040 Reactor Scram telle Shutdown During Surveillance Due to Casananication Error 374/98-U17-00 Reactor Water Cleanup Isolation During Modification Test Due to inadequate Reset 374/99-003 4 1 Engineered Safety Feature Actuation During Perforiaance of Instrument Maintenance Functloral Tests Due to Personnel Error 374/09-013 4 0 Primary Corn:sinment Isolation During Instrument Surveillance Testing of LIS-MS-401 G. COMPONEN1 fAlLURE DATA Not applicable, i
4
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i t
form Rev 2.0
.. QCf 45f E IVlWT REPORT (llR) itti COWilNUA110N Pagej3) .;
DOCKL1 WOMBfR (2) I(R WU8e(R (6)
' F ACitIIY NAME (1) Revision g/j/ Sequential j////jj/
Year / /
, T// Wueer Wuee,r, ,
0l217 01 0, 01 6 01 6 l 0 1.5 l 0 1 0.1 0 1 31 il 3 819 - - 0F LaSalleCountySuggnUnit1 1EX1 Energy Industry Identification System (Ells) codes are Identified in the text as (XX]
}
L. CORRECTIVE ACil0NS (Continued)
AC electrical bus outage procedures will be developed to assist the Operatteg personnel in identifying AIR potential problems which will arise due to deenergizing equipment or logic system power supplies. :
373-200-89-11202 will track these procedures. i The Training Department wlli review this event to dete mine if additional training is required to lasure proper turnover information that could effect Engineered Safety featured system actuation reportability is discussed. AIR 373-200-89-11203 will track the completion of this review.
A General Information Notification (ClN) will be developed to review this event with Operating, Maintenance and Techalcal Staff personnel suphasizing the leportance of verifying or reverifying the requiredinitialconditionsjustpriortoperformingatestorsurveillancetopreventinadvertent Engineered Safety featured System actuations. AIR 373-200-89-11204 will track the completion of this GIN.
4 F. PREVIOUS EVENTS LER Nuntper Title
(
373/84 4 49-00 secondary Containment isolation During Testing 373/84-014-00 Reactor Eater Cleanup Isolation t
(
373/87-009-00 Group IV isolation During Surveillance Test Due to Instrument Maintenance "
l Procedure Inadequacy 373/87-030-00 Reactor Scram While Shutdown During Surveillance Due to Connunication Error 374/98-017-00 Reactor Water Cleanup Isolation During Modification Test Due to inadequate Reset 374/09-003-01 Engineered Safety feature Actuation During Performance of Instrument Maintenance functional Tests Due to Personnel Error 374/09-013-00 Primary Containment isolation During Instrument Surveillance Testing of LIS-MS-401 j
1 O. COMPONENT FAILURE DATA Not applicable.
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