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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B1481993-07-30030 July 1993 LER 93-012-00:on 930702,reactor Core Isolation Cooling Sys Declared Inoperable Due to Associated Bus Voltage Dropping Below TS Limits.Sent Operator to Cycle Timer Which Caused Affected Contact to reclose.W/930730 Ltr ML20045D9331993-07-0202 July 1993 LER 93-004-00:on 930604,unexpected CRD Low Charging Water Header Scram Received Followed by Charging Water Header A2/B2 Alarm.Caused by Crud or Foreign Matl Passing Through Suction Filter.Filters Cleaned & reused.W/930702 ML20045D7501993-06-23023 June 1993 LER 93-003-00:on 930524,Div 1 ECCS Initiation Signal Received & LPCS Pump,Lpci Pump 2A & EDG Unit 0 Automatically Started.Caused by Personnel Error.Pumps Secured & Event Documented in Personnel file.W/930623 Ltr ML20044E4161993-05-28028 May 1993 LER 92-009-01:on 920923,spurious Auto Start of CR Ventilation Emergency make-up Train Occurred Due to High Radiation Spike.Radiation Monitor Circuit modified.W/930528 Ltr ML20044E4191993-05-21021 May 1993 LER 93-011-00:on 930423,manual Scram Initiated.Caused by Disconnected Linkage on Valve Positioner on Heater Drain Valve Due to Loose Jam Nut.Tailgate Session Will Be Held W/ Instrument Maint Dept Re Jam nuts.W/930521 Ltr ML20044D5161993-05-15015 May 1993 LER 92-007-01:on 920613,high Radiation Spike Received from CR Ventilation Process Radiation Monitor,Initiating Emergency Makeup Train B.Caused by Normal Variations in Radiation Readings.Spike modified.W/930515 Ltr ML20044D5571993-05-14014 May 1993 LER 93-010-00:on 930414,DG Cooling Water Pump Automatically Tripped on Magnetic Overload.Caused by Inexperienced Trainee in Operation of Control Lever.Lesson Plans & Training Programs for Operators to Be reviewed.W/930514 Ltr ML20044C9801993-05-0707 May 1993 LER 91-010-01:on 910719 & 0805,CR a Ventilation Emergency Makeup Fan auto-started on Spurious Trip of CR Air Intake Process Radiation Monitor.Caused by Normal Variations in Background Radiation.Supply Board replaced.W/930507 Ltr ML20044B6161993-02-25025 February 1993 LER 93-002-00:on 930126,Unit 1 Manual Scram Due to a SRV Being Stuck Open Due to Duct Tape Being Over Actuators Air Valve Manifold Exhaust Port.Maint Procedures That Involve Cleanliness reviewed.W/930225 Ltr ML20024G9771991-05-10010 May 1991 LER 91-005-00:on 910410,determined That Tech Spec Required Surveillance of Suppression Chamber Oxygen Sampling Missed. Caused by Inadequate Review of Tech Spec Change.Drywell & Suppression Chamber Checked for oxygen.W/910510 Ltr ML20044A3851990-06-25025 June 1990 LER 90-008-00:on 900525,Tech Spec Hourly Fire Watch Missed Due to Miscommunications Between Security Personnel & Radiation Protection Personnel.Fire Watch re-established & Memo issued.W/900625 Ltr ML20043F1721990-06-0505 June 1990 LER 90-009-00:on 900510,RWCU Outboard Suction Isolation Valve 2G33-F004 Auto Closed Which Tripped RWCU Pump B. Caused by Procedure Deficiency.Procedure LTS-500-209 Will Be revised.W/900605 Ltr ML20043F1281990-06-0101 June 1990 LER 90-009-00:on 900511,apparent Ruptured Diaphragm Found on Pressure Differential Switch in RCIC Steam Line.Caused by Torn Diaphragm Inside Switch.Replacement Switch Installed, Calibr & Functionally Tested satisfactorily.W/900608 Ltr ML20043B5681990-05-23023 May 1990 LER 89-027-01:on 891113,primary Containment Isolation Sys Group 1 Isolation Occurred During Surveillance Testing. Caused by Burnt Out Window Light Bulbs on Alarm Window. Light Bulbs Replaced & Jumpers installed.W/900523 Ltr ML20043A7721990-05-18018 May 1990 LER 90-007-00:on 900421,reactor Protection Sys Bus a Transfer & Reactor Recirculation Hydraulic Power Unit a Inboard Isolation Valves Closed,Causing Partial Group II isolation.Out-of-svc Procedure revised.W/900518 Ltr ML20043D0591990-05-18018 May 1990 LER 90-008-00:on 900502,ESF Actuation of Control Room B Emergency Ctk Ventilation Makeup Fan Occurred.Caused by Procedure deficiency.LTS-800-205 & Similar Procedures Will Be revised.W/900601 Ltr ML20042H0211990-05-10010 May 1990 LER 90-006-00:on 900412,loop a Primary Containment Chilled Water Sys Inboard Isolation Valves & Reactor Bldg Closed Cooling Water Sys Inboard Isolation Valve Went Closed.Caused by Inadequate Procedure.Procedures revised.W/900510 Ltr ML20042F9001990-05-0404 May 1990 LER 90-005-00:on 900411,experienced Loss of Dc Power to Portion of Div I Primary Containment Isolation Sys Logic Which Resulted in Isolation Signal & Actuation.Caused by Failure to Update Drawings & procedures.W/900504 Ltr ML20042F1941990-04-30030 April 1990 LER 89-025-01:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Door Containing Undervoltage Relays Closed.Caused by Misalignment of Door.Door Repaired. W/900430 Ltr ML20012D5341990-03-16016 March 1990 LER 90-003-01:on 900201,RCIC Isolation Signal Occurred During Warmup.Caused by Spurious High Steam Flow Signal.Rcic Sys Piping Integrity Verified & Isolation Logic Reset.W/ 900316 Ltr ML20012D5371990-03-16016 March 1990 LER 90-002-01:on 900129,oil in Diesel Generator Governor 1A Found to Be Low & Could Not Be Seen in Sight Glass.Caused by Slow Leak from Compensation Needle Valve Plug.Proper Amount of Oil Added & Operability Test performed.W/900316 Ltr ML20012C4931990-03-15015 March 1990 LER 90-004-00:on 900213,control Room B HVAC Intake Radiation Monitor Lost Power Causing auto-start of Emergency make-up Train B.Caused by Blown Fuses.Fuses Replaced.Logic Revs for Radiation Monitors Will Be installed.W/900315 Ltr ML20012B6501990-03-0909 March 1990 LER 90-002-00:on 900209,Operating Surveillance LOS-TG-W1 Determined to Have Exceeded Required Testing Interval,Per Tech Spec 3/4.7.10.Caused by Personnel Error.Personnel Counseled & Ref Procedures Will Be revised.W/900309 Ltr ML20012B5521990-03-0808 March 1990 LER 90-001-00:on 900206,full Reactor Scram Occurred During Instrument Surveillance Testing.Caused by Actuation of APRM E Trip Circuitry.Shutdown Margin Revised & Caution Card Placed on Control Room Bench board.W/900308 Ltr ML20011F8251990-03-0202 March 1990 LER 90-003-00:on 900201,RCIC Received Div 2 Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal Generated When Steam/Water Mixture Admitted to RCIC Steam Line.Isolation Logic reset.W/900302 Ltr ML20011F5551990-02-28028 February 1990 LER 90-002-00:on 900129,after Filling Diesel Generator 1A Governor W/Oil,Generator Started & Declared Inoperable. Caused by Slow Leak Coming from Compensation Needle Valve Plug.Oil Added & Plug Washer replaced.W/900228 Ltr ML20006F5951990-02-21021 February 1990 LER 90-001-00:on 900122,RWCU Sys Received Div 1 Leakage Detection Ambient Temp High Isolation Signal,Causing Trips of RWCU Pumps a & C.Caused by Broken Thermocouple Input Lead.Lead Wire Reconnected & Isolation reset.W/900221 Ltr ML20011F4921990-02-16016 February 1990 LER 89-013-01:on 890907,Group I Isolation Received During Performance of Instrument Surveillance LIS-MS-401.Caused by Depressurization of Main Steam Line Low Pressure Switch. Surveillance Revised to Split Into Two parts.W/900216 Ltr ML20006E4501990-02-15015 February 1990 LER 89-010-01:on 890715 & 17,voltage Oscillations Noted on Div II Battery Charger,Resulting in Inoperability of HPCS Sys.Caused by Failure of Charger in High Voltage Shutdown Relay.Charger Energized & Relay replaced.W/900215 Ltr ML20006E4451990-02-14014 February 1990 LER 89-009-01:on 890619,diaphragm Leak Discovered in RCIC Steam Line High Flow Isolation Switch.Caused by 1 & 1/2-inch Tear in Diaphragm.Pressure Differential Switch Replaced & Calibr.Reported Per NRC Bulletin 86-002.W/900214 Ltr ML20006E3981990-02-14014 February 1990 LER 89-008-01:on 890228,reactor Vessel Low Water Level 2 Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.Channel Placed in Tripped Condition & All Static-O-Ring Pressure Switches to Be replaced.W/900214 Ltr ML20006E3951990-02-14014 February 1990 LER 89-010-01:on 890303,automatic Depressurization Sys Permissive Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.All Static-O-Ring Reactor Vessel Level Switches Will Be replaced.W/900214 Ltr ML19354D8361990-01-15015 January 1990 LER 89-018-00:on 891216,plant 250-volt Battery & RCIC Sys Declared Inoperable Due to Low Battery Electrolyte Temps. Caused by Failure of Div I Switchgear Heat Removal Sys Damper Actuators.Air Intake Dampers closed.W/900115 Ltr ML20042D3921990-01-0404 January 1990 LER 89-011-01:on 890826,spurious Reactor Protection Sys Actuation Occurred.Definite Cause of Trip Not Determined. Brief Disturbance in Reactor Protection Sys Allowed Some Contactors to Trip.Procedure revised.W/900104 Ltr ML20005E2741989-12-22022 December 1989 LER 89-028-00:on 891204,RHR Shutdown Cooling Suction Header Outboard Isolation Valve Automatically Isolated.Caused by Miscommunication Between Technician & Station Operator.Task Force Developed to Review event.W/891222 Ltr ML19351A6301989-12-15015 December 1989 LER 89-006-01:on 890214,reactor Vessel Low Water Level 3 Switch Setpoint Found Out of Tolerance.Caused by Setpoint Drift.Level Switch to Be Replaced by Analog Trip Sys During First Quarter 1990.W/891215 Ltr ML20011D1341989-12-14014 December 1989 LER 89-017-00:on 891117,flow Switch FS-2E22-N006 Found W/ Setpoint Out of Tolerance Above Reject Limit.Caused by Setpoint Drift.Work Request Written to Replace Flow Switch. W/891214 Ltr ML19351A6751989-12-12012 December 1989 LER 89-027-00:on 891113,primary Containment Isolation Sys Group I Isolation Occurred While Performing Instrument Surveillance.Caused by Loss of Power to Leak Detection Sys Logic.Isolation reset.W/891213 Ltr ML19332F0081989-12-0808 December 1989 LER 89-016-00:on 891109,RWCU Isolation Occurred While Instrument Surveillance on Ventilation Differential Temp Isolation Functional Test in Progress.Caused by Faulty Thermocouple.Thermocouple repaired.W/891208 Ltr ML20005D6621989-12-0606 December 1989 LER 89-026-00:on 891106,inadvertent Primary Containment Isolation Actuation Occurred While Clearing out-of-svc. Caused by Inadequate Logic Setup During Mod Installation. Trip Status & Output Switches repositioned.W/891206 Ltr ML19332F2431989-12-0101 December 1989 LER 89-025-00:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Equipment Operator Closed Door Containing Relays.Caused by Misalignment of Door.Isolations Reset,Bus Energized & Circuit Logic tested.W/891201 Ltr ML19332E6581989-11-29029 November 1989 LER 89-015-00:on 891030,shift Control Room Engineer Noted That Quarterly Standby Liquid Control Operating Surveillance LOS-SC-Q1 Was Past Critical Date.Caused by Clerical Data Entry Error.Missed Surveillance performed.W/891129 Ltr ML19332D5181989-11-22022 November 1989 LER 89-018-01:on 890515,RCIC Received Div I & Div II Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal When Steam Added to RCIC Steam Line. Special Test Initiated.Isolation Logic reset.W/891122 Ltr ML19327C2601989-11-17017 November 1989 LER 89-014-00:on 891020,primary Containment Isolation Sys Group 4 Isolation Occurred Causing Isolation Dampers to Close.Caused by Opening of Div 2 125-volt Dc Breaker.Power Supply replaced.W/891117 Ltr ML19325F3411989-11-13013 November 1989 LER 89-024-00:on 891013 & 30,unsealed Openings in Main Control Room Floor & Main Control Room West Wall Discovered. Caused by Wide Gap Between Structural Beam & Cable Tray. Openings Sealed & Fire Watch established.W/891113 Ltr ML19324C1751989-11-0808 November 1989 LER 89-012-01:on 890309,diaphragm Leak Found in Pressure Differential Switch 1E31-N013BB.Caused by Tear Found in Diaphragm.Replacement Switch Installed,Calibr & Functionally Tested satisfactorily.W/891108 Ltr ML20024E9121983-08-26026 August 1983 LER 83-093/03L-0:on 830801,discovered full-in Indication on Core Display for Control Rod 34-47 Inoperable.Caused by Failed Switching Transistor on Data Memory Board 19.Data Memory Board replaced.W/830826 Ltr ML20024B8381983-07-0505 July 1983 LER 83-060/03L-0:on 830606,following Turbine Trip & Scram Due to High Vibration on Main Turbine,Reactor Recirculation Breaker 4B Closed.Cause Undetermined.Auxiliary Contacts cleaned.W/830705 Ltr ML20024B0721983-06-16016 June 1983 Updated LER 83-012/03X-1:on 830210,w/reactor in Cold Shutdown,Setpoints for Switches 1E31-N612A/B Found Above Tech Spec Limits.Cause Unknown.Switches calibr.W/830616 Ltr ML20024A6961983-06-14014 June 1983 LER 83-051/03L-0:on 830516,reactor Protection Sys Trip Channel H2 Limit Switch Failed to Operate Properly.Cause Unknown.Limit Switch readjusted.W/830614 Ltr 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046B1481993-07-30030 July 1993 LER 93-012-00:on 930702,reactor Core Isolation Cooling Sys Declared Inoperable Due to Associated Bus Voltage Dropping Below TS Limits.Sent Operator to Cycle Timer Which Caused Affected Contact to reclose.W/930730 Ltr ML20045D9331993-07-0202 July 1993 LER 93-004-00:on 930604,unexpected CRD Low Charging Water Header Scram Received Followed by Charging Water Header A2/B2 Alarm.Caused by Crud or Foreign Matl Passing Through Suction Filter.Filters Cleaned & reused.W/930702 ML20045D7501993-06-23023 June 1993 LER 93-003-00:on 930524,Div 1 ECCS Initiation Signal Received & LPCS Pump,Lpci Pump 2A & EDG Unit 0 Automatically Started.Caused by Personnel Error.Pumps Secured & Event Documented in Personnel file.W/930623 Ltr ML20044E4161993-05-28028 May 1993 LER 92-009-01:on 920923,spurious Auto Start of CR Ventilation Emergency make-up Train Occurred Due to High Radiation Spike.Radiation Monitor Circuit modified.W/930528 Ltr ML20044E4191993-05-21021 May 1993 LER 93-011-00:on 930423,manual Scram Initiated.Caused by Disconnected Linkage on Valve Positioner on Heater Drain Valve Due to Loose Jam Nut.Tailgate Session Will Be Held W/ Instrument Maint Dept Re Jam nuts.W/930521 Ltr ML20044D5161993-05-15015 May 1993 LER 92-007-01:on 920613,high Radiation Spike Received from CR Ventilation Process Radiation Monitor,Initiating Emergency Makeup Train B.Caused by Normal Variations in Radiation Readings.Spike modified.W/930515 Ltr ML20044D5571993-05-14014 May 1993 LER 93-010-00:on 930414,DG Cooling Water Pump Automatically Tripped on Magnetic Overload.Caused by Inexperienced Trainee in Operation of Control Lever.Lesson Plans & Training Programs for Operators to Be reviewed.W/930514 Ltr ML20044C9801993-05-0707 May 1993 LER 91-010-01:on 910719 & 0805,CR a Ventilation Emergency Makeup Fan auto-started on Spurious Trip of CR Air Intake Process Radiation Monitor.Caused by Normal Variations in Background Radiation.Supply Board replaced.W/930507 Ltr ML20044B6161993-02-25025 February 1993 LER 93-002-00:on 930126,Unit 1 Manual Scram Due to a SRV Being Stuck Open Due to Duct Tape Being Over Actuators Air Valve Manifold Exhaust Port.Maint Procedures That Involve Cleanliness reviewed.W/930225 Ltr ML20024G9771991-05-10010 May 1991 LER 91-005-00:on 910410,determined That Tech Spec Required Surveillance of Suppression Chamber Oxygen Sampling Missed. Caused by Inadequate Review of Tech Spec Change.Drywell & Suppression Chamber Checked for oxygen.W/910510 Ltr ML20044A3851990-06-25025 June 1990 LER 90-008-00:on 900525,Tech Spec Hourly Fire Watch Missed Due to Miscommunications Between Security Personnel & Radiation Protection Personnel.Fire Watch re-established & Memo issued.W/900625 Ltr ML20043F1721990-06-0505 June 1990 LER 90-009-00:on 900510,RWCU Outboard Suction Isolation Valve 2G33-F004 Auto Closed Which Tripped RWCU Pump B. Caused by Procedure Deficiency.Procedure LTS-500-209 Will Be revised.W/900605 Ltr ML20043F1281990-06-0101 June 1990 LER 90-009-00:on 900511,apparent Ruptured Diaphragm Found on Pressure Differential Switch in RCIC Steam Line.Caused by Torn Diaphragm Inside Switch.Replacement Switch Installed, Calibr & Functionally Tested satisfactorily.W/900608 Ltr ML20043B5681990-05-23023 May 1990 LER 89-027-01:on 891113,primary Containment Isolation Sys Group 1 Isolation Occurred During Surveillance Testing. Caused by Burnt Out Window Light Bulbs on Alarm Window. Light Bulbs Replaced & Jumpers installed.W/900523 Ltr ML20043A7721990-05-18018 May 1990 LER 90-007-00:on 900421,reactor Protection Sys Bus a Transfer & Reactor Recirculation Hydraulic Power Unit a Inboard Isolation Valves Closed,Causing Partial Group II isolation.Out-of-svc Procedure revised.W/900518 Ltr ML20043D0591990-05-18018 May 1990 LER 90-008-00:on 900502,ESF Actuation of Control Room B Emergency Ctk Ventilation Makeup Fan Occurred.Caused by Procedure deficiency.LTS-800-205 & Similar Procedures Will Be revised.W/900601 Ltr ML20042H0211990-05-10010 May 1990 LER 90-006-00:on 900412,loop a Primary Containment Chilled Water Sys Inboard Isolation Valves & Reactor Bldg Closed Cooling Water Sys Inboard Isolation Valve Went Closed.Caused by Inadequate Procedure.Procedures revised.W/900510 Ltr ML20042F9001990-05-0404 May 1990 LER 90-005-00:on 900411,experienced Loss of Dc Power to Portion of Div I Primary Containment Isolation Sys Logic Which Resulted in Isolation Signal & Actuation.Caused by Failure to Update Drawings & procedures.W/900504 Ltr ML20042F1941990-04-30030 April 1990 LER 89-025-01:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Door Containing Undervoltage Relays Closed.Caused by Misalignment of Door.Door Repaired. W/900430 Ltr ML20012D5341990-03-16016 March 1990 LER 90-003-01:on 900201,RCIC Isolation Signal Occurred During Warmup.Caused by Spurious High Steam Flow Signal.Rcic Sys Piping Integrity Verified & Isolation Logic Reset.W/ 900316 Ltr ML20012D5371990-03-16016 March 1990 LER 90-002-01:on 900129,oil in Diesel Generator Governor 1A Found to Be Low & Could Not Be Seen in Sight Glass.Caused by Slow Leak from Compensation Needle Valve Plug.Proper Amount of Oil Added & Operability Test performed.W/900316 Ltr ML20012C4931990-03-15015 March 1990 LER 90-004-00:on 900213,control Room B HVAC Intake Radiation Monitor Lost Power Causing auto-start of Emergency make-up Train B.Caused by Blown Fuses.Fuses Replaced.Logic Revs for Radiation Monitors Will Be installed.W/900315 Ltr ML20012B6501990-03-0909 March 1990 LER 90-002-00:on 900209,Operating Surveillance LOS-TG-W1 Determined to Have Exceeded Required Testing Interval,Per Tech Spec 3/4.7.10.Caused by Personnel Error.Personnel Counseled & Ref Procedures Will Be revised.W/900309 Ltr ML20012B5521990-03-0808 March 1990 LER 90-001-00:on 900206,full Reactor Scram Occurred During Instrument Surveillance Testing.Caused by Actuation of APRM E Trip Circuitry.Shutdown Margin Revised & Caution Card Placed on Control Room Bench board.W/900308 Ltr ML20011F8251990-03-0202 March 1990 LER 90-003-00:on 900201,RCIC Received Div 2 Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal Generated When Steam/Water Mixture Admitted to RCIC Steam Line.Isolation Logic reset.W/900302 Ltr ML20011F5551990-02-28028 February 1990 LER 90-002-00:on 900129,after Filling Diesel Generator 1A Governor W/Oil,Generator Started & Declared Inoperable. Caused by Slow Leak Coming from Compensation Needle Valve Plug.Oil Added & Plug Washer replaced.W/900228 Ltr ML20006F5951990-02-21021 February 1990 LER 90-001-00:on 900122,RWCU Sys Received Div 1 Leakage Detection Ambient Temp High Isolation Signal,Causing Trips of RWCU Pumps a & C.Caused by Broken Thermocouple Input Lead.Lead Wire Reconnected & Isolation reset.W/900221 Ltr ML20011F4921990-02-16016 February 1990 LER 89-013-01:on 890907,Group I Isolation Received During Performance of Instrument Surveillance LIS-MS-401.Caused by Depressurization of Main Steam Line Low Pressure Switch. Surveillance Revised to Split Into Two parts.W/900216 Ltr ML20006E4501990-02-15015 February 1990 LER 89-010-01:on 890715 & 17,voltage Oscillations Noted on Div II Battery Charger,Resulting in Inoperability of HPCS Sys.Caused by Failure of Charger in High Voltage Shutdown Relay.Charger Energized & Relay replaced.W/900215 Ltr ML20006E4451990-02-14014 February 1990 LER 89-009-01:on 890619,diaphragm Leak Discovered in RCIC Steam Line High Flow Isolation Switch.Caused by 1 & 1/2-inch Tear in Diaphragm.Pressure Differential Switch Replaced & Calibr.Reported Per NRC Bulletin 86-002.W/900214 Ltr ML20006E3981990-02-14014 February 1990 LER 89-008-01:on 890228,reactor Vessel Low Water Level 2 Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.Channel Placed in Tripped Condition & All Static-O-Ring Pressure Switches to Be replaced.W/900214 Ltr ML20006E3951990-02-14014 February 1990 LER 89-010-01:on 890303,automatic Depressurization Sys Permissive Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.All Static-O-Ring Reactor Vessel Level Switches Will Be replaced.W/900214 Ltr ML19354D8361990-01-15015 January 1990 LER 89-018-00:on 891216,plant 250-volt Battery & RCIC Sys Declared Inoperable Due to Low Battery Electrolyte Temps. Caused by Failure of Div I Switchgear Heat Removal Sys Damper Actuators.Air Intake Dampers closed.W/900115 Ltr ML20042D3921990-01-0404 January 1990 LER 89-011-01:on 890826,spurious Reactor Protection Sys Actuation Occurred.Definite Cause of Trip Not Determined. Brief Disturbance in Reactor Protection Sys Allowed Some Contactors to Trip.Procedure revised.W/900104 Ltr ML20005E2741989-12-22022 December 1989 LER 89-028-00:on 891204,RHR Shutdown Cooling Suction Header Outboard Isolation Valve Automatically Isolated.Caused by Miscommunication Between Technician & Station Operator.Task Force Developed to Review event.W/891222 Ltr ML19351A6301989-12-15015 December 1989 LER 89-006-01:on 890214,reactor Vessel Low Water Level 3 Switch Setpoint Found Out of Tolerance.Caused by Setpoint Drift.Level Switch to Be Replaced by Analog Trip Sys During First Quarter 1990.W/891215 Ltr ML20011D1341989-12-14014 December 1989 LER 89-017-00:on 891117,flow Switch FS-2E22-N006 Found W/ Setpoint Out of Tolerance Above Reject Limit.Caused by Setpoint Drift.Work Request Written to Replace Flow Switch. W/891214 Ltr ML19351A6751989-12-12012 December 1989 LER 89-027-00:on 891113,primary Containment Isolation Sys Group I Isolation Occurred While Performing Instrument Surveillance.Caused by Loss of Power to Leak Detection Sys Logic.Isolation reset.W/891213 Ltr ML19332F0081989-12-0808 December 1989 LER 89-016-00:on 891109,RWCU Isolation Occurred While Instrument Surveillance on Ventilation Differential Temp Isolation Functional Test in Progress.Caused by Faulty Thermocouple.Thermocouple repaired.W/891208 Ltr ML20005D6621989-12-0606 December 1989 LER 89-026-00:on 891106,inadvertent Primary Containment Isolation Actuation Occurred While Clearing out-of-svc. Caused by Inadequate Logic Setup During Mod Installation. Trip Status & Output Switches repositioned.W/891206 Ltr ML19332F2431989-12-0101 December 1989 LER 89-025-00:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Equipment Operator Closed Door Containing Relays.Caused by Misalignment of Door.Isolations Reset,Bus Energized & Circuit Logic tested.W/891201 Ltr ML19332E6581989-11-29029 November 1989 LER 89-015-00:on 891030,shift Control Room Engineer Noted That Quarterly Standby Liquid Control Operating Surveillance LOS-SC-Q1 Was Past Critical Date.Caused by Clerical Data Entry Error.Missed Surveillance performed.W/891129 Ltr ML19332D5181989-11-22022 November 1989 LER 89-018-01:on 890515,RCIC Received Div I & Div II Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal When Steam Added to RCIC Steam Line. Special Test Initiated.Isolation Logic reset.W/891122 Ltr ML19327C2601989-11-17017 November 1989 LER 89-014-00:on 891020,primary Containment Isolation Sys Group 4 Isolation Occurred Causing Isolation Dampers to Close.Caused by Opening of Div 2 125-volt Dc Breaker.Power Supply replaced.W/891117 Ltr ML19325F3411989-11-13013 November 1989 LER 89-024-00:on 891013 & 30,unsealed Openings in Main Control Room Floor & Main Control Room West Wall Discovered. Caused by Wide Gap Between Structural Beam & Cable Tray. Openings Sealed & Fire Watch established.W/891113 Ltr ML19324C1751989-11-0808 November 1989 LER 89-012-01:on 890309,diaphragm Leak Found in Pressure Differential Switch 1E31-N013BB.Caused by Tear Found in Diaphragm.Replacement Switch Installed,Calibr & Functionally Tested satisfactorily.W/891108 Ltr ML20024E9121983-08-26026 August 1983 LER 83-093/03L-0:on 830801,discovered full-in Indication on Core Display for Control Rod 34-47 Inoperable.Caused by Failed Switching Transistor on Data Memory Board 19.Data Memory Board replaced.W/830826 Ltr ML20024B8381983-07-0505 July 1983 LER 83-060/03L-0:on 830606,following Turbine Trip & Scram Due to High Vibration on Main Turbine,Reactor Recirculation Breaker 4B Closed.Cause Undetermined.Auxiliary Contacts cleaned.W/830705 Ltr ML20024B0721983-06-16016 June 1983 Updated LER 83-012/03X-1:on 830210,w/reactor in Cold Shutdown,Setpoints for Switches 1E31-N612A/B Found Above Tech Spec Limits.Cause Unknown.Switches calibr.W/830616 Ltr ML20024A6961983-06-14014 June 1983 LER 83-051/03L-0:on 830516,reactor Protection Sys Trip Channel H2 Limit Switch Failed to Operate Properly.Cause Unknown.Limit Switch readjusted.W/830614 Ltr 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217C9121999-10-12012 October 1999 SER Input Authorizing Licensee Proposed Request to Modify Definition of Core Alteration in Section 1.0 of TS & Update Sections 3/4.1,3.4.3 & 3/4.9 to Reflect Proposed Definition Change ML20217F9091999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for LaSalle County Stations,Units 1 & 2.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212C4501999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for LaSalle County Station,Units 1 & 2.With ML20210R0671999-07-31031 July 1999 Monthly Operating Repts for July 1999 for LaSalle County Station,Units 1 & 2.With ML20210C1681999-07-0909 July 1999 Seventh Refueling Outage ASME Section XI Summary Rept ML20209H1501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for LaSalle County Station,Units 1 & 2.With ML20195J7871999-05-31031 May 1999 Monthly Operating Repts for May 1999 for LaSalle County Station,Units 1 & 2.With ML20209E1431999-05-31031 May 1999 Cycle 8 COLR, for May 1999 ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations ML20206N2071999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for LaSalle County Station,Units 1 & 2.With ML20205L8421999-03-31031 March 1999 Rev 2 to EMF-96-125, LaSalle Unit 2 Cycle 8 Reload Analysis ML20205L8301999-03-31031 March 1999 Administrative Technical Requirements App B (Amend 26) LaSalle Unit 2 Cycle 8 COLR & Reload Transient Analysis Results, for Mar 1999 ML20205R2721999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for LaSalle County Station,Units 1 & 2.With ML20205L8391999-03-22022 March 1999 Rev 2 to 960103, Neutronics Licensing Rept for LaSalle Unit 2,Cycle 8 ML20204C8141999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for LaSalle County Station,Units 1 & 2.With ML20199E4601998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for LaSalle County Station,Units 1 & 2.With ML20207C7371998-12-31031 December 1998 Annual Rept for LaSalle County Station for Jan 1998 Through Dec 1998 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20198B3801998-12-14014 December 1998 SER Accepting one-time Request for Relief from Certain Provisions of Section XI of ASME Boiler & Pressure Vessel Code,Per 10CFR50.55a for Certain Plant Safety/Relief Valves ML20206N2261998-12-0909 December 1998 LER 98-S03-00:on 981116,protected Area Was Entered Without Current Authorization for Unescorted Access Due to Programmatic Deficiency Error.Changed Badge Control Process ML20197K0981998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for LaSalle County Station,Unts 1 & 2.With ML20196B1441998-11-23023 November 1998 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Bindings of Safety-Related Power-Operated Gate Valves ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195D3191998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for LaSalle County Station.With ML20154H6781998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20153D0191998-09-18018 September 1998 Part 21 Rept Re Defect in Gap Conductance Analyses for co- Resident BWR Fuel.Initially Reported on 980917.Corrective Analyses Performed Demonstrating That Current Operating Limits Bounding from BOC to Cycle Exposure of 8 Gwd/Mtu ML20153C7621998-09-18018 September 1998 Safety Evaluation Acceping NRC Bulletin 95-002, Unexpected Clogging of RHR Pump Strainer While Operating in Suppression Pool Cooling Mode ML20153C6771998-09-17017 September 1998 Part 21 Rept Re Defect Relative to MCPR Operating Limits as Impacted by Gap Conductance of co-resident BWR Fuel at Facilities.Operating Limit for LaSalle Unit 2 & Quad Cities Unit 2 Will Be Revised as Listed ML20151W0241998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for LaSalle County Station.With ML20237E2921998-08-21021 August 1998 Special Rept:On 980811,channel 5 of Lpms Became Inoperable. Caused by Channel Failed pre-amplifier Located Inside Primary Containment at Inboard Side of Electrical Penetration E-19.Initiated Repairs of Channel ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237B4861998-07-31031 July 1998 Monthly Operating Repts for July 1998 for LaSalle County Nuclear Power Station Units 1 & 2 ML20236V7701998-07-31031 July 1998 Revised LaSalle Unit 1 Cycle 8 COLR & Reload Transient Analysis Results ML20236P8231998-07-14014 July 1998 Special Rept:From 980614-17,various Fire Rated Assemblies Were Inoperable for Period Greater than Seven Days.Caused by Test Equipment Being Routed Through Fire Doors.Established Fire Watches & on 980619 Assemblies Were Declared Operable ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20236L8041998-07-0606 July 1998 Safety Evaluation Granting Licensee 980304 Request for Second 10-yr Interval Pump & Valve IST Program Plan,Rev 2, Including Changes to 2 ASME Boiler & Pressure Vessel Code Relief Requests Previously Submitted in Rev 1 ML20236P3611998-06-30030 June 1998 Monthly Operating Repts for June 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20249C4891998-06-22022 June 1998 Special Rept:On 980522,Fire Detection Zone 1-31 Was Noted out-of-service for More than 14 Days.Detection Sys Was Taken out-of-service on 980508 to Prevent False Alarms During Hot Work Activities.Sys Was Returned to Operable Status 980528 ML20248M3101998-05-31031 May 1998 Monthly Operating Repts for May 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20236V7771998-05-31031 May 1998 Rev 1 to 24A5180, Supplemental Reload Licensing Rept for LaSalle County Station Unit 1 Reload 7 Cycle 8 ML20217Q7041998-05-0404 May 1998 Safety Evaluation Accepting Util Request to Leave Leak Chase Channels Plugged During Performance of Containment ILRT ML20247M4491998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for LaSalle County Station ML20216F4941998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for LaSalle County Station,Units 1 & 2 ML20217N6581998-03-30030 March 1998 Special Rept on Fire Detection,Deluge Sys & Fire Rated Assemblies During Period of 980303-25.Established Fire Watches Until Affected Equipment Is Returned to Operable Status ML20216D9511998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for LaSalle County Station,Units 1 & 2 ML20247M4631998-02-28028 February 1998 Rev Monthly Operating Rept for Feb 1998 for LaSalle County Station ML20203D7241998-02-20020 February 1998 Special Rept:On 980118,Fire Detection Zones 1-18 & 2-18 Taken out-of-svc to Prevent False Alarms During Hot Work Activities on Auxiliary Electric Equipment Room Ventilation Sys.Fire Watches Will Remain in Place ML20202G9851998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for LaSalle County Station,Units 1 & 2 ML20199K1651998-01-23023 January 1998 Rev 65h to Topical Rept CE-1-A, Comm Ed QA Tr 1999-09-30
[Table view] |
Text
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' Commonwealth Edison LaSalliCountyNuclear Station
.4i 4i Rural Route #1, Box 220 Marsellies,lilinois 61341
, Telephone 815/357-6761 November 22, 1989 i
Director of Nuclear Reactor Regulation !
' U.S. Nuclear Regulatory Commission ;
Mail Station F1-137 3 P Washington, D.C.-20555
Dear Sir :
Licensee tvent Report #89-018-01, Docket #050-373 is being s,ubmitted to your office to supercede previously submitted Licensee Event Report 89-018-00. .
7 NO f G. J. Died rich (Station Manager LaSalle County Station GJD/99tT/kg 3 Enclosure 1
xc: Nuclear Licensing Administrator
' NRC Resident Inspector l NRC Region III Administrator INPO - Records Center
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LICENSEE EVENT REPORT (LER) , g Docket thster (2) Pane (3)
Facility Name (1)
%11e County Sutton Unit 1 01 51 01 01 01 31 71 3 1lofl0l6 ,
i Title (4)
Reactor Core Isolation Coolina isolation Durina Wamue Out to Spurious Hloh 5 tem Flow Sienal nacart Dato (T) Other Facilities involved (8) )
j- Event Date (5) LIR thseer (6)
Year /// Sequential / Revision Month Day Year Facillty Names Docket thster(s)
Month Day Year l ffj
/// thster l//j/
ff
// thster I
01 51 01 01 01 I I 01 5 11 5 81 9 81 9 01118 01 1 111 21 2 61 9 01510101of I I l; l
THIS REPORT 15 $UBMITTED PURSUANT TO THE REQUIREMENTS OF 10CFR '
(Check one or wwe of the followine) (11) )
MODE N 1 20.402(b) _
20.405(c) .jL 50.73(a)(2)(lv; _ 73.71(b)
J 20.405(a)(1)(1) 50.36(c)(1) ,,,,,, 50.73(a)(2)(v) _ 73.71(c)
PONER _
50.36(c)(2) 50.73(a)(2)(vil) Other (Specify LEVEL i 20.405(a)(1)(li) _ ,,,,, _
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20.405(a)(1)(lii) 50.73(a)(2)(1) 50.73(a)(2)(vill)(A) in Abstract (10) 0I 8I 9 ,,,_ _ _
,_,20.405(a)(1)(iv) 50.73(a)(2)(ll) 50.73(a)(2)(vill)(8) below and in
/,/ /,/,/,/,/,/,/,/,/,/,/,/,/,/ /,/,/,/,/,/,/,/,/,/ ,,,,, ,,,,,,
50.73(a)(2)(lii) 50.73(a)(2)(x) Text) f
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I LICENSEE CONTACT FOR THIS LER (12)
TELEPHONE NUpBER Name AREA CODE Michael Tennyson. Technical Staff Ennineer. entension 2704 81115 31 51 71 -l 61 71 61 1 werLETE ONE L!NE FOR EACH CurrussE FAILURE DESCRIBED IN TH15 REPORT (13)
CAUSE SYSTEM COMPONENT MANUFAC- REPORTABLE CAUSE SYSTEM COMPONENT MANUFAC- REPORTABLE TURER TO NPRDS TURTR TOWPRR,,,
1 I I I I I N I I i l I l l X Bl N 1 I I I I I I I I I l l l 1 Expected Month l Day l Year SUPPLEMENTAL REPORT EXPECTED (14)
Submission
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lyes (If ves. complete EXPECTED SugMISSION DATE) YlNO I l ABSTRACT (Limit to 1400 spaces, i.e. approximately fifteen single-space typewritten lines) (16) on May 15, 1989, at 2156 hours0.025 days <br />0.599 hours <br />0.00356 weeks <br />8.20358e-4 months <br />, the Reactor Core Isolation Cooling System (RCIC) received a Division I and Division 11 (outboard and inboard) isolation on NCIC high steam line flow. Unit I was in Operational Condition 1 (Run) at 89% power.
At the time of the event, RCIC steam line was being womed up following the conpletion of L15-RI-301, " Unit 1 Steam Line High Flow RCIC ! solation Functional Test." RCIC was being returned to standby per procedure, LOP-RI-05, Preparation for Standby of the RCIC system," when the outboard isolation valve (IE51.F008), and inboard isolation valves (IE51-F0b and IE51-F063) Isolated due to a spurious high steam flow signal.
The RCIC steam line isolation was not a valid high steam flow signal. Steam trapped between the inboard valves and the outboard valve was released into the piping downstream of the outboard valve when it was opened. The surge from this release was sufficient to exceed the trip setpoint of the high flow isolation switches.
When the isolation signal was received, the outboard isolation valve closed satisfactorily, RCIC system piping integrity was verified and the isolation logic was reset. Wanning up of the RCic system proceeded with no further incidents.
This event is reportable to the Nuclear Regulatory Comnission as a Licensee Event Report in accordance with 10CFR$0.73(a)(2)(iv) due to an Engineered Safety Feature actuation.
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' L78mt8F WJ;T REPORT (LER) TEXT OWiltalAT13 Fem Rev 2.0
FACILITY Igut (1) DOCKET IRNGER (2)
Year /// 5equential f/j/j/ Revision fff
/// louder /// Ilumber oI1le o! 1 of 2 0F 01 6 l wgnecanniv$tationunit1 o l's I o I o I o 1 31 71 3 e19 - -
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t TEXT- Energy Industry identification System (E!!5) codes are identified in the test as (IK)
. PLANT AllD ST5 TEM IDENTIFICATION General Electric - telling Water Reactor
! Energy Industry identification System (Ell 5) codes are identified in the text as (KX). ,
A. CONDITION PRIOR 70 EVENT.
Event Date: 5/15/09 Event ilme: 2156 Hours
~ Unit (s): 1 t
Mode (s) Name: Run Power Level (s): 895 Reactor Mode (s): 1 l S. DESCRIPTION OF EVENT
. On May 15,1989, at 2156 hours0.025 days <br />0.599 hours <br />0.00356 weeks <br />8.20358e-4 months <br /> the Reactor Core Isolation' Cooling System (RCIC, ON) received a Division I
I. I and Division 11 (inboard and outboard) isolation signal on RCIC high steam line flow. This event occurred while Unit 1 was in operational condition 1 (Run) at 895 power.
l At the time of the event, RCic stem line was being wamed up following the completion of LaSalle f' Instro ent Surveillance, L15-RI-301, " Unit 1 Steam Line Flow RCIC isolation Functional Test." During i this surveillance, the outboard RCIC steam isolation valve (1E51-F008) and the inboard steam isolation vaires (IE51-F063 and IE51-F076) were closed. Upon coupletion of the survelliance, RCIC was being returned to standby per LaSalle operating Procedure, LOP-RI-05, " Preparation for Standby of RCIC System."' The Control Room operator attempted several times to crack open the outboard isolation valve (1E51-F000), with the inboard valves closed.
[
Shortly after the outboard valve apparently lifted off of its seat, the Operator noticed a step increase
. In RCIC stem line pressure downstream of the outboard isolation valve and lamediately closed the
. outboard valve. Within 3 seconds of the pressure increase the Olvision 1 outboard RCIC stem isolation valve (1E51-F006), and the olvision 11 inboard RCic stem isolation valves (IE51-F076 and IE51-F063) received an isolation signal due to a high stem flow signal from the pressure differential switches IE3141013AA and IE31-410130A.
l The inboard isolation valves were closed at the time of the isolation signal, and the outboard Isolation 1- valve had already closed due to the Operator's response. Subsequent to the isolation, the outboard
. valve was re-opened and the RCic steam line was wanned in accordance with the same procedure, this ' time l ;
without incident.
L The relays that isolate the inboard and outboard isolation valves for the RCIC ste m line are time delayed to energire. The isolation time for each relay was checked and it was detennined that they functioned satisfactorily.
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LICENSEE EVENT REPORT (LER) TEXT *;0NTIWuATION _ _
Forn Rev 2.0 LER BRptER (6) Pace (3)
FACILITY MUE (1) DOCKET NuPSER (2)
Year // Sequential // Revision ,
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// thatner
/j/j f
// thsuber ]
ol1Ie oI ) of 3 0F ol_1 l i % 11e County station unit 1 oI5ioIoIo 1 31 71 3 sI9 - -
Energy Inoustry identification System (Ells) codes are identified in the text as (KK) l TEXT 1
- g. OESCRIPTION OF EVENT (Continued) l The water which acc oulated in the RCIC steam Ilne piping between the inboard and outboard isolation
- valves during the surveillance appears to affect the differential pressure instroents when it is pushed The flow elbow cannot accurately measure flow in ,
past one tap of the flow elbow by the trapped steam.
these circ ostances due to the difference of fluid density between the taps. ,
C. APPARENT CAUSE OF EVENT !
The cause of the RCIC steam line isolation was a spurious high stem flow signal generated when steam j was admitted to the RCIC steam line. Apparently steam was trapped downstream of the inboorti isolation valves (1E51 F076 and 1E51-F063) and upstream of the outboard isolation vatte (1E51-F008). -l Upon re-opening of the outboard isolation valve, the trapped steam expanded into the downstream piping The isolation logic for high kCIC causing a surge of the steamfwater mixture and isolated the system.
steam line flow has a three second time delay built in it to prevent spurious isolation when fast l
. starting RCIC. Howev*r, the basis for the flow measurements used in the isolation logic is that the elbows would sense steam, not a steam / water mixture. The isolation was reset satisfactorily after it occurred.
O. SAFETY ANALYSIS OF EVENT
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Upon receiving the high steam Inne flow isolation signal, the RCIC steam line inboard and outboard !
isolation valves isolated satisfactorily. This action was conservative from the standpoint of Primary Contaimment(PC)(NH] integrity.
All the valves were already closed. (IE51-F008 was closed due to Operator action prior to the automatic closure signal.) Therefore the isolation function of these valves had been met.
' Since the valves were already closed, the isolation signal did not cause any challenges to the valves or motor operators. RCIC was already inoperable due to surveillance testing. Satisfactory operation of the high flow differential pressure switches was observed during subsequent testing which showed that the pressure pulse (s) did not damage the switch diaphragras. -
Consequences of this event were minimal since the High Pressure Core Spray (HP) (BG) and other emergexy core coeling systems were fully operable.
E. CORRECTIVE ACTIONS RCIC system piping integrity was verifled and the isolation logic was reset. Warning up of the RCIC systam proceeded with no further incidents, and RCIC was returned to standby per procedure LOP-RI-05, "Proparation for Standby of the RCIC System," at 2245 hours0.026 days <br />0.624 hours <br />0.00371 weeks <br />8.542225e-4 months <br /> on May 15, 1989.
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LICEMEE EVENT REPORT (LER) TEXT CONTINuATimi Fore Rev 2.0 FACILITY NRpE (1) DOCKET NupSER (2) LER tRDSER (6) P ee (3)
Year /
fj/j/ Sequential ff//j/ Revision
/// Weber /// Neber o I 5 I o I o I o i 31 113 e19 - ol1Ie - oi1 01 4 0F of s l Lasalle County Station unit 1
. TEXT Energy industry identification System (E!!S) codes are identified in the text as (xx]
E.- CORRECTIVE ACTIONS (Continued)
LaSalle special Test, LST-89-019 was written to slaulate the act ul conditions for a RCIC isolation during warm up. The test was perfomed to detemine a course of action to prevent the occurrence of similar isolations. Actuation of one isolation switch was observed, but it was not of sufficient duration to energize the 3 second time delay required for isolation.
Several courses of action for prevention of RCic isolation were discussed at a meeting held on May 24, 1999. The following actions were agreed to be laplemented:
- 1. During the next required isolation for maintenance of the PCIC high stem flow instruments, a special test would be perfomed in conjunction with the instraent survel11ance. The pressure differential switches IE31-m013AA/Aa/DA/te, the time delay relays associated with these switches, and the RCic steam header pressure indicator 1E51-N001 downstro m of outboard isolation valve 1E51-F000, would all be monitored during system isolation, upon closure of inboard isolation valve IE51-F063, outboard isolation valve IE51-F008 would be closed after the RCIC steam Inne isolation valve 1E51-N007 reached 400 psig. At the completion of the RCic instrument maintenance, monitoring of the instroents would continue until RCIC was returned to standby.
- 2. LaSalle Onsite Review (LD5R)09-434 would be written to place the pressure differential switches IE31-N007AS/st and IE31-#013AB/88 out of service untti they are permanently removed by modification M01-1-40-052. These switches are piped "in reverse" and cannot sense a legitimate high steam flow condition.
- 3. LaSalle Operating procedures and LaSalle Instraent Survelliances would be revised as appropriate, following the evaluation of all Special Tests.
LaSalle Special Test, LST 99-059,
- Pressure / Differential Pressure Observation of RCIC Ste m Line Hi-Flow l= Isolation Switches 1(2)E31-4013AA and 1(2)E31-N0138A,* was perfomed on June 9,1989. Due to the indeterminate results during the test, a new test LaSalle Special Test 89-062 was written and perfomed the following day.
During the RCIC system return to standby, there was no RCIC isolation. The test equipment remained connected and was monitored for three weeks to determine the possible drift that would occur to the pressure differential switches while RCIC was in service. it was determined that the drift in the switches was not sufficient to contribute to a RCIC system isolation during return to a standby condition.
LaSalle Special Test, LST 99-062 was performed a second time on July 11, 1999 inconjunctionwithaRCIC instrument surveillance. Following the closure of inboard isolation valve (IE51-F063), the RCIC steam Ilne pressure was reduced to 400 psig before the outboard isolation valve IE51-F008 was closed. Upon l-l RCIC return to service there was no RCIC isolation.
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- Foria Rev 2.0 LICENSEE EVENT REMIRT (LER) TEXT CONiluuhTION 00CEtt NupSER (2) LER 8eptER (6) Pm Cl)
PACILITY NRpE (1)
Tear fj// Sequential
/ / Revision
///
f Neauber
/j/j/
f
// Nisuber
% )1e County Statten unit 1 015 10 1010131113 e19 - 011Ie - 01 1 01 5 0F 016 TIXT Energy Industry Identification System (Ell 5) codes are identified in the test as (KK) f E. CORRECTIVE ACTIONS (Continued)
After evaluation of the tests, it was decided that LA5alle Operating Procedure. LOP-RI-43
- Shutdown of the RCIC System," would be revised. The revision was1d instruct the Control Room Operators to reduce the steam line pressure downstream of inboar11 isolation valve IE51-F063 to 400 psig before closing outboard isolation valve 1E51-F008. The pressure reduction in the steaminne would be accomplished by waiting a period of 45 to 50 minutes after closure of the inboar11 isolation valve. The revision of LaSalle Operating Precedure LOP 41-03, was completed on October 10, 1989.
All LaSalle Instroent Survel11ances that require the isolation of the RCIC system will a150 be revised to reflect that system isolation would be perforned in accordance with the specific operating precedure that is discussed in the above paragraph.
The following LaSalle Instrument Surveillances will be revised:
L1541-101, "Unnt 1 Steam Line High Flow RCIC lsolation Calibration.'
L1541-201, " Unit 2 Steam Line High Flow RCIC inciation Calibration.'
L15-RI-301, " Unit 1 Steam Line High Flow RCIC lsolation Functional fest."
L1541-401, " Unit 2 Steam Line High flow RCIC 1501stion f unctional Test.'
The change states that the RCIC system will be isolated in accordance with the revised LaSalle Operating Procedure, LDP-RI-03.
LaSalle Onsite Review, LOSR 99-034 was written on June 5, 1999 and approval to remove the switches from i
service was given on August 4, 1999.
On August 11, 1989, following a second RCIC system high steam flow isolation, a meeting was held and it was decided that the following additional corrective action would also be laplemented:
A revision to the LaSalle Electrical Surveillancee for setting the RCIC high flow isolatloa time delay relay. The setpoint for the time delay relays would be increased to 4 seconds from 3 seconds. The Technical Specification setpoint ilmit is 5 seconds.
LaSalle Setpoint Change Request SPCR 99-039/09-040 was initiated on August 31, 1989. LaSalle Electrical Surveillance LES-RI-1018 has been revised to reflect the 4 second setpoint change. The setpoint for the time delay relays on Unit 1 RCic system was changed on Septenber 28, 1999, during the refuel outage.
The setpoint change for Unit 2 RCIC system will be perforned during the next refuel outage.
The following LaSalle operating procedures and survelliance will be revised to reflect the 4 second change:
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- Fem Rev 2.0 i LhtMf EVENT REPORT (LER) TEXT Ctaff1NuAf ttaf Paas (3)
PACILITY NepE (l) DOCKET NupeER (2) AP__:: (6) Sequential Revision i Year ///
fff
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/// Wimber /// thaber ,
011ie 01 1 01 6 Or 01 6 t I m ile County statlan unit 1 0 i $ 1 0 1 0 1 0 1 31 71 3 sIe - -
Energy industry identification System (Ell 5) codes are identified in the text as (KK) l TEXT l
i E. C(MRECTIVE ACTIONS (Continued) ,
LOP-RI42, " Starting and Operation of the RCic System." i LOP 4144,
LOP 4145, " Preparation for the Standby of the RCic System.' '
LOS4143, *RCIC Sysiten Pep Operability Test.'
The fc110 wing LaSalle Operating Abnormals w'.11 be revised to reflect the 4 second change r
LOA 1(2)H13-P6010201, *RCIC Channel A Stem Line Olfferential Pressure High."
LOA 1(2)H13-P6018309, *RCic Channel S Stem Line Olfferential Pressure High."
The fo)1owing LaSalle schematic drawings will be revised to reflect the 4 second change:
IE-1-4226AD/AF ll-2-4226AD/AF p l
The pressure differentla) switches 2E314007AS/88 and 2E314013AS/es were taken out of service November l
3, 1989. The switches for the Unit 1 RCic system will be taken out of service during the startup sequence fc11owing the refuel outage.
All LaSalle Operating procedures Operating survel11ances, instroent surveillances, Operating
- Abnormal Electrical survel11ances and schematic drawings will be tracked by Action item Record i
(AIR) 373-200-8947202.
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- F. PREVIOUS EVENTS l
LER Number Title 373/85-022-00 RCIC Stem Line High Flow Isolation During Warsup "
373/84 460-00 RCIC Ste m Line Olfferential Pressure High 1so14 tion 373/83-122/03L Reit Stem Line Isolation During Warmup G.. COMPONENT FAlLURE DATA None.
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