|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B1481993-07-30030 July 1993 LER 93-012-00:on 930702,reactor Core Isolation Cooling Sys Declared Inoperable Due to Associated Bus Voltage Dropping Below TS Limits.Sent Operator to Cycle Timer Which Caused Affected Contact to reclose.W/930730 Ltr ML20045D9331993-07-0202 July 1993 LER 93-004-00:on 930604,unexpected CRD Low Charging Water Header Scram Received Followed by Charging Water Header A2/B2 Alarm.Caused by Crud or Foreign Matl Passing Through Suction Filter.Filters Cleaned & reused.W/930702 ML20045D7501993-06-23023 June 1993 LER 93-003-00:on 930524,Div 1 ECCS Initiation Signal Received & LPCS Pump,Lpci Pump 2A & EDG Unit 0 Automatically Started.Caused by Personnel Error.Pumps Secured & Event Documented in Personnel file.W/930623 Ltr ML20044E4161993-05-28028 May 1993 LER 92-009-01:on 920923,spurious Auto Start of CR Ventilation Emergency make-up Train Occurred Due to High Radiation Spike.Radiation Monitor Circuit modified.W/930528 Ltr ML20044E4191993-05-21021 May 1993 LER 93-011-00:on 930423,manual Scram Initiated.Caused by Disconnected Linkage on Valve Positioner on Heater Drain Valve Due to Loose Jam Nut.Tailgate Session Will Be Held W/ Instrument Maint Dept Re Jam nuts.W/930521 Ltr ML20044D5161993-05-15015 May 1993 LER 92-007-01:on 920613,high Radiation Spike Received from CR Ventilation Process Radiation Monitor,Initiating Emergency Makeup Train B.Caused by Normal Variations in Radiation Readings.Spike modified.W/930515 Ltr ML20044D5571993-05-14014 May 1993 LER 93-010-00:on 930414,DG Cooling Water Pump Automatically Tripped on Magnetic Overload.Caused by Inexperienced Trainee in Operation of Control Lever.Lesson Plans & Training Programs for Operators to Be reviewed.W/930514 Ltr ML20044C9801993-05-0707 May 1993 LER 91-010-01:on 910719 & 0805,CR a Ventilation Emergency Makeup Fan auto-started on Spurious Trip of CR Air Intake Process Radiation Monitor.Caused by Normal Variations in Background Radiation.Supply Board replaced.W/930507 Ltr ML20044B6161993-02-25025 February 1993 LER 93-002-00:on 930126,Unit 1 Manual Scram Due to a SRV Being Stuck Open Due to Duct Tape Being Over Actuators Air Valve Manifold Exhaust Port.Maint Procedures That Involve Cleanliness reviewed.W/930225 Ltr ML20024G9771991-05-10010 May 1991 LER 91-005-00:on 910410,determined That Tech Spec Required Surveillance of Suppression Chamber Oxygen Sampling Missed. Caused by Inadequate Review of Tech Spec Change.Drywell & Suppression Chamber Checked for oxygen.W/910510 Ltr ML20044A3851990-06-25025 June 1990 LER 90-008-00:on 900525,Tech Spec Hourly Fire Watch Missed Due to Miscommunications Between Security Personnel & Radiation Protection Personnel.Fire Watch re-established & Memo issued.W/900625 Ltr ML20043F1721990-06-0505 June 1990 LER 90-009-00:on 900510,RWCU Outboard Suction Isolation Valve 2G33-F004 Auto Closed Which Tripped RWCU Pump B. Caused by Procedure Deficiency.Procedure LTS-500-209 Will Be revised.W/900605 Ltr ML20043F1281990-06-0101 June 1990 LER 90-009-00:on 900511,apparent Ruptured Diaphragm Found on Pressure Differential Switch in RCIC Steam Line.Caused by Torn Diaphragm Inside Switch.Replacement Switch Installed, Calibr & Functionally Tested satisfactorily.W/900608 Ltr ML20043B5681990-05-23023 May 1990 LER 89-027-01:on 891113,primary Containment Isolation Sys Group 1 Isolation Occurred During Surveillance Testing. Caused by Burnt Out Window Light Bulbs on Alarm Window. Light Bulbs Replaced & Jumpers installed.W/900523 Ltr ML20043A7721990-05-18018 May 1990 LER 90-007-00:on 900421,reactor Protection Sys Bus a Transfer & Reactor Recirculation Hydraulic Power Unit a Inboard Isolation Valves Closed,Causing Partial Group II isolation.Out-of-svc Procedure revised.W/900518 Ltr ML20043D0591990-05-18018 May 1990 LER 90-008-00:on 900502,ESF Actuation of Control Room B Emergency Ctk Ventilation Makeup Fan Occurred.Caused by Procedure deficiency.LTS-800-205 & Similar Procedures Will Be revised.W/900601 Ltr ML20042H0211990-05-10010 May 1990 LER 90-006-00:on 900412,loop a Primary Containment Chilled Water Sys Inboard Isolation Valves & Reactor Bldg Closed Cooling Water Sys Inboard Isolation Valve Went Closed.Caused by Inadequate Procedure.Procedures revised.W/900510 Ltr ML20042F9001990-05-0404 May 1990 LER 90-005-00:on 900411,experienced Loss of Dc Power to Portion of Div I Primary Containment Isolation Sys Logic Which Resulted in Isolation Signal & Actuation.Caused by Failure to Update Drawings & procedures.W/900504 Ltr ML20042F1941990-04-30030 April 1990 LER 89-025-01:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Door Containing Undervoltage Relays Closed.Caused by Misalignment of Door.Door Repaired. W/900430 Ltr ML20012D5341990-03-16016 March 1990 LER 90-003-01:on 900201,RCIC Isolation Signal Occurred During Warmup.Caused by Spurious High Steam Flow Signal.Rcic Sys Piping Integrity Verified & Isolation Logic Reset.W/ 900316 Ltr ML20012D5371990-03-16016 March 1990 LER 90-002-01:on 900129,oil in Diesel Generator Governor 1A Found to Be Low & Could Not Be Seen in Sight Glass.Caused by Slow Leak from Compensation Needle Valve Plug.Proper Amount of Oil Added & Operability Test performed.W/900316 Ltr ML20012C4931990-03-15015 March 1990 LER 90-004-00:on 900213,control Room B HVAC Intake Radiation Monitor Lost Power Causing auto-start of Emergency make-up Train B.Caused by Blown Fuses.Fuses Replaced.Logic Revs for Radiation Monitors Will Be installed.W/900315 Ltr ML20012B6501990-03-0909 March 1990 LER 90-002-00:on 900209,Operating Surveillance LOS-TG-W1 Determined to Have Exceeded Required Testing Interval,Per Tech Spec 3/4.7.10.Caused by Personnel Error.Personnel Counseled & Ref Procedures Will Be revised.W/900309 Ltr ML20012B5521990-03-0808 March 1990 LER 90-001-00:on 900206,full Reactor Scram Occurred During Instrument Surveillance Testing.Caused by Actuation of APRM E Trip Circuitry.Shutdown Margin Revised & Caution Card Placed on Control Room Bench board.W/900308 Ltr ML20011F8251990-03-0202 March 1990 LER 90-003-00:on 900201,RCIC Received Div 2 Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal Generated When Steam/Water Mixture Admitted to RCIC Steam Line.Isolation Logic reset.W/900302 Ltr ML20011F5551990-02-28028 February 1990 LER 90-002-00:on 900129,after Filling Diesel Generator 1A Governor W/Oil,Generator Started & Declared Inoperable. Caused by Slow Leak Coming from Compensation Needle Valve Plug.Oil Added & Plug Washer replaced.W/900228 Ltr ML20006F5951990-02-21021 February 1990 LER 90-001-00:on 900122,RWCU Sys Received Div 1 Leakage Detection Ambient Temp High Isolation Signal,Causing Trips of RWCU Pumps a & C.Caused by Broken Thermocouple Input Lead.Lead Wire Reconnected & Isolation reset.W/900221 Ltr ML20011F4921990-02-16016 February 1990 LER 89-013-01:on 890907,Group I Isolation Received During Performance of Instrument Surveillance LIS-MS-401.Caused by Depressurization of Main Steam Line Low Pressure Switch. Surveillance Revised to Split Into Two parts.W/900216 Ltr ML20006E4501990-02-15015 February 1990 LER 89-010-01:on 890715 & 17,voltage Oscillations Noted on Div II Battery Charger,Resulting in Inoperability of HPCS Sys.Caused by Failure of Charger in High Voltage Shutdown Relay.Charger Energized & Relay replaced.W/900215 Ltr ML20006E4451990-02-14014 February 1990 LER 89-009-01:on 890619,diaphragm Leak Discovered in RCIC Steam Line High Flow Isolation Switch.Caused by 1 & 1/2-inch Tear in Diaphragm.Pressure Differential Switch Replaced & Calibr.Reported Per NRC Bulletin 86-002.W/900214 Ltr ML20006E3981990-02-14014 February 1990 LER 89-008-01:on 890228,reactor Vessel Low Water Level 2 Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.Channel Placed in Tripped Condition & All Static-O-Ring Pressure Switches to Be replaced.W/900214 Ltr ML20006E3951990-02-14014 February 1990 LER 89-010-01:on 890303,automatic Depressurization Sys Permissive Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.All Static-O-Ring Reactor Vessel Level Switches Will Be replaced.W/900214 Ltr ML19354D8361990-01-15015 January 1990 LER 89-018-00:on 891216,plant 250-volt Battery & RCIC Sys Declared Inoperable Due to Low Battery Electrolyte Temps. Caused by Failure of Div I Switchgear Heat Removal Sys Damper Actuators.Air Intake Dampers closed.W/900115 Ltr ML20042D3921990-01-0404 January 1990 LER 89-011-01:on 890826,spurious Reactor Protection Sys Actuation Occurred.Definite Cause of Trip Not Determined. Brief Disturbance in Reactor Protection Sys Allowed Some Contactors to Trip.Procedure revised.W/900104 Ltr ML20005E2741989-12-22022 December 1989 LER 89-028-00:on 891204,RHR Shutdown Cooling Suction Header Outboard Isolation Valve Automatically Isolated.Caused by Miscommunication Between Technician & Station Operator.Task Force Developed to Review event.W/891222 Ltr ML19351A6301989-12-15015 December 1989 LER 89-006-01:on 890214,reactor Vessel Low Water Level 3 Switch Setpoint Found Out of Tolerance.Caused by Setpoint Drift.Level Switch to Be Replaced by Analog Trip Sys During First Quarter 1990.W/891215 Ltr ML20011D1341989-12-14014 December 1989 LER 89-017-00:on 891117,flow Switch FS-2E22-N006 Found W/ Setpoint Out of Tolerance Above Reject Limit.Caused by Setpoint Drift.Work Request Written to Replace Flow Switch. W/891214 Ltr ML19351A6751989-12-12012 December 1989 LER 89-027-00:on 891113,primary Containment Isolation Sys Group I Isolation Occurred While Performing Instrument Surveillance.Caused by Loss of Power to Leak Detection Sys Logic.Isolation reset.W/891213 Ltr ML19332F0081989-12-0808 December 1989 LER 89-016-00:on 891109,RWCU Isolation Occurred While Instrument Surveillance on Ventilation Differential Temp Isolation Functional Test in Progress.Caused by Faulty Thermocouple.Thermocouple repaired.W/891208 Ltr ML20005D6621989-12-0606 December 1989 LER 89-026-00:on 891106,inadvertent Primary Containment Isolation Actuation Occurred While Clearing out-of-svc. Caused by Inadequate Logic Setup During Mod Installation. Trip Status & Output Switches repositioned.W/891206 Ltr ML19332F2431989-12-0101 December 1989 LER 89-025-00:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Equipment Operator Closed Door Containing Relays.Caused by Misalignment of Door.Isolations Reset,Bus Energized & Circuit Logic tested.W/891201 Ltr ML19332E6581989-11-29029 November 1989 LER 89-015-00:on 891030,shift Control Room Engineer Noted That Quarterly Standby Liquid Control Operating Surveillance LOS-SC-Q1 Was Past Critical Date.Caused by Clerical Data Entry Error.Missed Surveillance performed.W/891129 Ltr ML19332D5181989-11-22022 November 1989 LER 89-018-01:on 890515,RCIC Received Div I & Div II Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal When Steam Added to RCIC Steam Line. Special Test Initiated.Isolation Logic reset.W/891122 Ltr ML19327C2601989-11-17017 November 1989 LER 89-014-00:on 891020,primary Containment Isolation Sys Group 4 Isolation Occurred Causing Isolation Dampers to Close.Caused by Opening of Div 2 125-volt Dc Breaker.Power Supply replaced.W/891117 Ltr ML19325F3411989-11-13013 November 1989 LER 89-024-00:on 891013 & 30,unsealed Openings in Main Control Room Floor & Main Control Room West Wall Discovered. Caused by Wide Gap Between Structural Beam & Cable Tray. Openings Sealed & Fire Watch established.W/891113 Ltr ML19324C1751989-11-0808 November 1989 LER 89-012-01:on 890309,diaphragm Leak Found in Pressure Differential Switch 1E31-N013BB.Caused by Tear Found in Diaphragm.Replacement Switch Installed,Calibr & Functionally Tested satisfactorily.W/891108 Ltr ML20024E9121983-08-26026 August 1983 LER 83-093/03L-0:on 830801,discovered full-in Indication on Core Display for Control Rod 34-47 Inoperable.Caused by Failed Switching Transistor on Data Memory Board 19.Data Memory Board replaced.W/830826 Ltr ML20024B8381983-07-0505 July 1983 LER 83-060/03L-0:on 830606,following Turbine Trip & Scram Due to High Vibration on Main Turbine,Reactor Recirculation Breaker 4B Closed.Cause Undetermined.Auxiliary Contacts cleaned.W/830705 Ltr ML20024B0721983-06-16016 June 1983 Updated LER 83-012/03X-1:on 830210,w/reactor in Cold Shutdown,Setpoints for Switches 1E31-N612A/B Found Above Tech Spec Limits.Cause Unknown.Switches calibr.W/830616 Ltr ML20024A6961983-06-14014 June 1983 LER 83-051/03L-0:on 830516,reactor Protection Sys Trip Channel H2 Limit Switch Failed to Operate Properly.Cause Unknown.Limit Switch readjusted.W/830614 Ltr 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046B1481993-07-30030 July 1993 LER 93-012-00:on 930702,reactor Core Isolation Cooling Sys Declared Inoperable Due to Associated Bus Voltage Dropping Below TS Limits.Sent Operator to Cycle Timer Which Caused Affected Contact to reclose.W/930730 Ltr ML20045D9331993-07-0202 July 1993 LER 93-004-00:on 930604,unexpected CRD Low Charging Water Header Scram Received Followed by Charging Water Header A2/B2 Alarm.Caused by Crud or Foreign Matl Passing Through Suction Filter.Filters Cleaned & reused.W/930702 ML20045D7501993-06-23023 June 1993 LER 93-003-00:on 930524,Div 1 ECCS Initiation Signal Received & LPCS Pump,Lpci Pump 2A & EDG Unit 0 Automatically Started.Caused by Personnel Error.Pumps Secured & Event Documented in Personnel file.W/930623 Ltr ML20044E4161993-05-28028 May 1993 LER 92-009-01:on 920923,spurious Auto Start of CR Ventilation Emergency make-up Train Occurred Due to High Radiation Spike.Radiation Monitor Circuit modified.W/930528 Ltr ML20044E4191993-05-21021 May 1993 LER 93-011-00:on 930423,manual Scram Initiated.Caused by Disconnected Linkage on Valve Positioner on Heater Drain Valve Due to Loose Jam Nut.Tailgate Session Will Be Held W/ Instrument Maint Dept Re Jam nuts.W/930521 Ltr ML20044D5161993-05-15015 May 1993 LER 92-007-01:on 920613,high Radiation Spike Received from CR Ventilation Process Radiation Monitor,Initiating Emergency Makeup Train B.Caused by Normal Variations in Radiation Readings.Spike modified.W/930515 Ltr ML20044D5571993-05-14014 May 1993 LER 93-010-00:on 930414,DG Cooling Water Pump Automatically Tripped on Magnetic Overload.Caused by Inexperienced Trainee in Operation of Control Lever.Lesson Plans & Training Programs for Operators to Be reviewed.W/930514 Ltr ML20044C9801993-05-0707 May 1993 LER 91-010-01:on 910719 & 0805,CR a Ventilation Emergency Makeup Fan auto-started on Spurious Trip of CR Air Intake Process Radiation Monitor.Caused by Normal Variations in Background Radiation.Supply Board replaced.W/930507 Ltr ML20044B6161993-02-25025 February 1993 LER 93-002-00:on 930126,Unit 1 Manual Scram Due to a SRV Being Stuck Open Due to Duct Tape Being Over Actuators Air Valve Manifold Exhaust Port.Maint Procedures That Involve Cleanliness reviewed.W/930225 Ltr ML20024G9771991-05-10010 May 1991 LER 91-005-00:on 910410,determined That Tech Spec Required Surveillance of Suppression Chamber Oxygen Sampling Missed. Caused by Inadequate Review of Tech Spec Change.Drywell & Suppression Chamber Checked for oxygen.W/910510 Ltr ML20044A3851990-06-25025 June 1990 LER 90-008-00:on 900525,Tech Spec Hourly Fire Watch Missed Due to Miscommunications Between Security Personnel & Radiation Protection Personnel.Fire Watch re-established & Memo issued.W/900625 Ltr ML20043F1721990-06-0505 June 1990 LER 90-009-00:on 900510,RWCU Outboard Suction Isolation Valve 2G33-F004 Auto Closed Which Tripped RWCU Pump B. Caused by Procedure Deficiency.Procedure LTS-500-209 Will Be revised.W/900605 Ltr ML20043F1281990-06-0101 June 1990 LER 90-009-00:on 900511,apparent Ruptured Diaphragm Found on Pressure Differential Switch in RCIC Steam Line.Caused by Torn Diaphragm Inside Switch.Replacement Switch Installed, Calibr & Functionally Tested satisfactorily.W/900608 Ltr ML20043B5681990-05-23023 May 1990 LER 89-027-01:on 891113,primary Containment Isolation Sys Group 1 Isolation Occurred During Surveillance Testing. Caused by Burnt Out Window Light Bulbs on Alarm Window. Light Bulbs Replaced & Jumpers installed.W/900523 Ltr ML20043A7721990-05-18018 May 1990 LER 90-007-00:on 900421,reactor Protection Sys Bus a Transfer & Reactor Recirculation Hydraulic Power Unit a Inboard Isolation Valves Closed,Causing Partial Group II isolation.Out-of-svc Procedure revised.W/900518 Ltr ML20043D0591990-05-18018 May 1990 LER 90-008-00:on 900502,ESF Actuation of Control Room B Emergency Ctk Ventilation Makeup Fan Occurred.Caused by Procedure deficiency.LTS-800-205 & Similar Procedures Will Be revised.W/900601 Ltr ML20042H0211990-05-10010 May 1990 LER 90-006-00:on 900412,loop a Primary Containment Chilled Water Sys Inboard Isolation Valves & Reactor Bldg Closed Cooling Water Sys Inboard Isolation Valve Went Closed.Caused by Inadequate Procedure.Procedures revised.W/900510 Ltr ML20042F9001990-05-0404 May 1990 LER 90-005-00:on 900411,experienced Loss of Dc Power to Portion of Div I Primary Containment Isolation Sys Logic Which Resulted in Isolation Signal & Actuation.Caused by Failure to Update Drawings & procedures.W/900504 Ltr ML20042F1941990-04-30030 April 1990 LER 89-025-01:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Door Containing Undervoltage Relays Closed.Caused by Misalignment of Door.Door Repaired. W/900430 Ltr ML20012D5341990-03-16016 March 1990 LER 90-003-01:on 900201,RCIC Isolation Signal Occurred During Warmup.Caused by Spurious High Steam Flow Signal.Rcic Sys Piping Integrity Verified & Isolation Logic Reset.W/ 900316 Ltr ML20012D5371990-03-16016 March 1990 LER 90-002-01:on 900129,oil in Diesel Generator Governor 1A Found to Be Low & Could Not Be Seen in Sight Glass.Caused by Slow Leak from Compensation Needle Valve Plug.Proper Amount of Oil Added & Operability Test performed.W/900316 Ltr ML20012C4931990-03-15015 March 1990 LER 90-004-00:on 900213,control Room B HVAC Intake Radiation Monitor Lost Power Causing auto-start of Emergency make-up Train B.Caused by Blown Fuses.Fuses Replaced.Logic Revs for Radiation Monitors Will Be installed.W/900315 Ltr ML20012B6501990-03-0909 March 1990 LER 90-002-00:on 900209,Operating Surveillance LOS-TG-W1 Determined to Have Exceeded Required Testing Interval,Per Tech Spec 3/4.7.10.Caused by Personnel Error.Personnel Counseled & Ref Procedures Will Be revised.W/900309 Ltr ML20012B5521990-03-0808 March 1990 LER 90-001-00:on 900206,full Reactor Scram Occurred During Instrument Surveillance Testing.Caused by Actuation of APRM E Trip Circuitry.Shutdown Margin Revised & Caution Card Placed on Control Room Bench board.W/900308 Ltr ML20011F8251990-03-0202 March 1990 LER 90-003-00:on 900201,RCIC Received Div 2 Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal Generated When Steam/Water Mixture Admitted to RCIC Steam Line.Isolation Logic reset.W/900302 Ltr ML20011F5551990-02-28028 February 1990 LER 90-002-00:on 900129,after Filling Diesel Generator 1A Governor W/Oil,Generator Started & Declared Inoperable. Caused by Slow Leak Coming from Compensation Needle Valve Plug.Oil Added & Plug Washer replaced.W/900228 Ltr ML20006F5951990-02-21021 February 1990 LER 90-001-00:on 900122,RWCU Sys Received Div 1 Leakage Detection Ambient Temp High Isolation Signal,Causing Trips of RWCU Pumps a & C.Caused by Broken Thermocouple Input Lead.Lead Wire Reconnected & Isolation reset.W/900221 Ltr ML20011F4921990-02-16016 February 1990 LER 89-013-01:on 890907,Group I Isolation Received During Performance of Instrument Surveillance LIS-MS-401.Caused by Depressurization of Main Steam Line Low Pressure Switch. Surveillance Revised to Split Into Two parts.W/900216 Ltr ML20006E4501990-02-15015 February 1990 LER 89-010-01:on 890715 & 17,voltage Oscillations Noted on Div II Battery Charger,Resulting in Inoperability of HPCS Sys.Caused by Failure of Charger in High Voltage Shutdown Relay.Charger Energized & Relay replaced.W/900215 Ltr ML20006E4451990-02-14014 February 1990 LER 89-009-01:on 890619,diaphragm Leak Discovered in RCIC Steam Line High Flow Isolation Switch.Caused by 1 & 1/2-inch Tear in Diaphragm.Pressure Differential Switch Replaced & Calibr.Reported Per NRC Bulletin 86-002.W/900214 Ltr ML20006E3981990-02-14014 February 1990 LER 89-008-01:on 890228,reactor Vessel Low Water Level 2 Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.Channel Placed in Tripped Condition & All Static-O-Ring Pressure Switches to Be replaced.W/900214 Ltr ML20006E3951990-02-14014 February 1990 LER 89-010-01:on 890303,automatic Depressurization Sys Permissive Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.All Static-O-Ring Reactor Vessel Level Switches Will Be replaced.W/900214 Ltr ML19354D8361990-01-15015 January 1990 LER 89-018-00:on 891216,plant 250-volt Battery & RCIC Sys Declared Inoperable Due to Low Battery Electrolyte Temps. Caused by Failure of Div I Switchgear Heat Removal Sys Damper Actuators.Air Intake Dampers closed.W/900115 Ltr ML20042D3921990-01-0404 January 1990 LER 89-011-01:on 890826,spurious Reactor Protection Sys Actuation Occurred.Definite Cause of Trip Not Determined. Brief Disturbance in Reactor Protection Sys Allowed Some Contactors to Trip.Procedure revised.W/900104 Ltr ML20005E2741989-12-22022 December 1989 LER 89-028-00:on 891204,RHR Shutdown Cooling Suction Header Outboard Isolation Valve Automatically Isolated.Caused by Miscommunication Between Technician & Station Operator.Task Force Developed to Review event.W/891222 Ltr ML19351A6301989-12-15015 December 1989 LER 89-006-01:on 890214,reactor Vessel Low Water Level 3 Switch Setpoint Found Out of Tolerance.Caused by Setpoint Drift.Level Switch to Be Replaced by Analog Trip Sys During First Quarter 1990.W/891215 Ltr ML20011D1341989-12-14014 December 1989 LER 89-017-00:on 891117,flow Switch FS-2E22-N006 Found W/ Setpoint Out of Tolerance Above Reject Limit.Caused by Setpoint Drift.Work Request Written to Replace Flow Switch. W/891214 Ltr ML19351A6751989-12-12012 December 1989 LER 89-027-00:on 891113,primary Containment Isolation Sys Group I Isolation Occurred While Performing Instrument Surveillance.Caused by Loss of Power to Leak Detection Sys Logic.Isolation reset.W/891213 Ltr ML19332F0081989-12-0808 December 1989 LER 89-016-00:on 891109,RWCU Isolation Occurred While Instrument Surveillance on Ventilation Differential Temp Isolation Functional Test in Progress.Caused by Faulty Thermocouple.Thermocouple repaired.W/891208 Ltr ML20005D6621989-12-0606 December 1989 LER 89-026-00:on 891106,inadvertent Primary Containment Isolation Actuation Occurred While Clearing out-of-svc. Caused by Inadequate Logic Setup During Mod Installation. Trip Status & Output Switches repositioned.W/891206 Ltr ML19332F2431989-12-0101 December 1989 LER 89-025-00:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Equipment Operator Closed Door Containing Relays.Caused by Misalignment of Door.Isolations Reset,Bus Energized & Circuit Logic tested.W/891201 Ltr ML19332E6581989-11-29029 November 1989 LER 89-015-00:on 891030,shift Control Room Engineer Noted That Quarterly Standby Liquid Control Operating Surveillance LOS-SC-Q1 Was Past Critical Date.Caused by Clerical Data Entry Error.Missed Surveillance performed.W/891129 Ltr ML19332D5181989-11-22022 November 1989 LER 89-018-01:on 890515,RCIC Received Div I & Div II Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal When Steam Added to RCIC Steam Line. Special Test Initiated.Isolation Logic reset.W/891122 Ltr ML19327C2601989-11-17017 November 1989 LER 89-014-00:on 891020,primary Containment Isolation Sys Group 4 Isolation Occurred Causing Isolation Dampers to Close.Caused by Opening of Div 2 125-volt Dc Breaker.Power Supply replaced.W/891117 Ltr ML19325F3411989-11-13013 November 1989 LER 89-024-00:on 891013 & 30,unsealed Openings in Main Control Room Floor & Main Control Room West Wall Discovered. Caused by Wide Gap Between Structural Beam & Cable Tray. Openings Sealed & Fire Watch established.W/891113 Ltr ML19324C1751989-11-0808 November 1989 LER 89-012-01:on 890309,diaphragm Leak Found in Pressure Differential Switch 1E31-N013BB.Caused by Tear Found in Diaphragm.Replacement Switch Installed,Calibr & Functionally Tested satisfactorily.W/891108 Ltr ML20024E9121983-08-26026 August 1983 LER 83-093/03L-0:on 830801,discovered full-in Indication on Core Display for Control Rod 34-47 Inoperable.Caused by Failed Switching Transistor on Data Memory Board 19.Data Memory Board replaced.W/830826 Ltr ML20024B8381983-07-0505 July 1983 LER 83-060/03L-0:on 830606,following Turbine Trip & Scram Due to High Vibration on Main Turbine,Reactor Recirculation Breaker 4B Closed.Cause Undetermined.Auxiliary Contacts cleaned.W/830705 Ltr ML20024B0721983-06-16016 June 1983 Updated LER 83-012/03X-1:on 830210,w/reactor in Cold Shutdown,Setpoints for Switches 1E31-N612A/B Found Above Tech Spec Limits.Cause Unknown.Switches calibr.W/830616 Ltr ML20024A6961983-06-14014 June 1983 LER 83-051/03L-0:on 830516,reactor Protection Sys Trip Channel H2 Limit Switch Failed to Operate Properly.Cause Unknown.Limit Switch readjusted.W/830614 Ltr 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217C9121999-10-12012 October 1999 SER Input Authorizing Licensee Proposed Request to Modify Definition of Core Alteration in Section 1.0 of TS & Update Sections 3/4.1,3.4.3 & 3/4.9 to Reflect Proposed Definition Change ML20217F9091999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for LaSalle County Stations,Units 1 & 2.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212C4501999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for LaSalle County Station,Units 1 & 2.With ML20210R0671999-07-31031 July 1999 Monthly Operating Repts for July 1999 for LaSalle County Station,Units 1 & 2.With ML20210C1681999-07-0909 July 1999 Seventh Refueling Outage ASME Section XI Summary Rept ML20209H1501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for LaSalle County Station,Units 1 & 2.With ML20195J7871999-05-31031 May 1999 Monthly Operating Repts for May 1999 for LaSalle County Station,Units 1 & 2.With ML20209E1431999-05-31031 May 1999 Cycle 8 COLR, for May 1999 ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations ML20206N2071999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for LaSalle County Station,Units 1 & 2.With ML20205L8421999-03-31031 March 1999 Rev 2 to EMF-96-125, LaSalle Unit 2 Cycle 8 Reload Analysis ML20205L8301999-03-31031 March 1999 Administrative Technical Requirements App B (Amend 26) LaSalle Unit 2 Cycle 8 COLR & Reload Transient Analysis Results, for Mar 1999 ML20205R2721999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for LaSalle County Station,Units 1 & 2.With ML20205L8391999-03-22022 March 1999 Rev 2 to 960103, Neutronics Licensing Rept for LaSalle Unit 2,Cycle 8 ML20204C8141999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for LaSalle County Station,Units 1 & 2.With ML20199E4601998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for LaSalle County Station,Units 1 & 2.With ML20207C7371998-12-31031 December 1998 Annual Rept for LaSalle County Station for Jan 1998 Through Dec 1998 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20198B3801998-12-14014 December 1998 SER Accepting one-time Request for Relief from Certain Provisions of Section XI of ASME Boiler & Pressure Vessel Code,Per 10CFR50.55a for Certain Plant Safety/Relief Valves ML20206N2261998-12-0909 December 1998 LER 98-S03-00:on 981116,protected Area Was Entered Without Current Authorization for Unescorted Access Due to Programmatic Deficiency Error.Changed Badge Control Process ML20197K0981998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for LaSalle County Station,Unts 1 & 2.With ML20196B1441998-11-23023 November 1998 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Bindings of Safety-Related Power-Operated Gate Valves ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195D3191998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for LaSalle County Station.With ML20154H6781998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20153D0191998-09-18018 September 1998 Part 21 Rept Re Defect in Gap Conductance Analyses for co- Resident BWR Fuel.Initially Reported on 980917.Corrective Analyses Performed Demonstrating That Current Operating Limits Bounding from BOC to Cycle Exposure of 8 Gwd/Mtu ML20153C7621998-09-18018 September 1998 Safety Evaluation Acceping NRC Bulletin 95-002, Unexpected Clogging of RHR Pump Strainer While Operating in Suppression Pool Cooling Mode ML20153C6771998-09-17017 September 1998 Part 21 Rept Re Defect Relative to MCPR Operating Limits as Impacted by Gap Conductance of co-resident BWR Fuel at Facilities.Operating Limit for LaSalle Unit 2 & Quad Cities Unit 2 Will Be Revised as Listed ML20151W0241998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for LaSalle County Station.With ML20237E2921998-08-21021 August 1998 Special Rept:On 980811,channel 5 of Lpms Became Inoperable. Caused by Channel Failed pre-amplifier Located Inside Primary Containment at Inboard Side of Electrical Penetration E-19.Initiated Repairs of Channel ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237B4861998-07-31031 July 1998 Monthly Operating Repts for July 1998 for LaSalle County Nuclear Power Station Units 1 & 2 ML20236V7701998-07-31031 July 1998 Revised LaSalle Unit 1 Cycle 8 COLR & Reload Transient Analysis Results ML20236P8231998-07-14014 July 1998 Special Rept:From 980614-17,various Fire Rated Assemblies Were Inoperable for Period Greater than Seven Days.Caused by Test Equipment Being Routed Through Fire Doors.Established Fire Watches & on 980619 Assemblies Were Declared Operable ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20236L8041998-07-0606 July 1998 Safety Evaluation Granting Licensee 980304 Request for Second 10-yr Interval Pump & Valve IST Program Plan,Rev 2, Including Changes to 2 ASME Boiler & Pressure Vessel Code Relief Requests Previously Submitted in Rev 1 ML20236P3611998-06-30030 June 1998 Monthly Operating Repts for June 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20249C4891998-06-22022 June 1998 Special Rept:On 980522,Fire Detection Zone 1-31 Was Noted out-of-service for More than 14 Days.Detection Sys Was Taken out-of-service on 980508 to Prevent False Alarms During Hot Work Activities.Sys Was Returned to Operable Status 980528 ML20248M3101998-05-31031 May 1998 Monthly Operating Repts for May 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20236V7771998-05-31031 May 1998 Rev 1 to 24A5180, Supplemental Reload Licensing Rept for LaSalle County Station Unit 1 Reload 7 Cycle 8 ML20217Q7041998-05-0404 May 1998 Safety Evaluation Accepting Util Request to Leave Leak Chase Channels Plugged During Performance of Containment ILRT ML20247M4491998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for LaSalle County Station ML20216F4941998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for LaSalle County Station,Units 1 & 2 ML20217N6581998-03-30030 March 1998 Special Rept on Fire Detection,Deluge Sys & Fire Rated Assemblies During Period of 980303-25.Established Fire Watches Until Affected Equipment Is Returned to Operable Status ML20216D9511998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for LaSalle County Station,Units 1 & 2 ML20247M4631998-02-28028 February 1998 Rev Monthly Operating Rept for Feb 1998 for LaSalle County Station ML20203D7241998-02-20020 February 1998 Special Rept:On 980118,Fire Detection Zones 1-18 & 2-18 Taken out-of-svc to Prevent False Alarms During Hot Work Activities on Auxiliary Electric Equipment Room Ventilation Sys.Fire Watches Will Remain in Place ML20202G9851998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for LaSalle County Station,Units 1 & 2 ML20199K1651998-01-23023 January 1998 Rev 65h to Topical Rept CE-1-A, Comm Ed QA Tr 1999-09-30
[Table view] |
Text
_
Commonw:alth Edison
,/ LaSalle County Nuclear Station 2S01 N. 21st. Rd.
Marsei!!es, Illinois 61341 Telephone 815/357-6761 February 25, 1993 Director of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission Mail Station Pl-137 Hashington, D.C. 20555 P
Dear Sir:
Licensee Event Report #93-002-00, Docket #050-373 is being submitted to your office in accordance with 10CFR50.73(a)(2)(iv) and
G. F. Spedi Station Manager ("
LaSalle County Station ;
GFS/MWH/mk1 Enclosure xc: Nuclear Licensing Administrator NRC Resident Inspector NRC Region III Administrator INPO - Records Center IDNS Resident Inspector i
240045 ,pk g2250210930225 / '
S ADOCK 05000373 \
PDR '
1
- LICENSEE EVENT REPORT (LER) l Fnan Fev UL ,
Fotiitty Name (1) Docket Number (2) Pace (3)
LaSalle County Station Unit 1 0 15 10 10 10 1 31 71 3 1lof!0l5 Title (4) Unit 1 Manual Scram Due To 'A' SRV Being Stuck Open Due To Doct Tape Being Over The Actuator's Air Valve l
Manifold Enhaust Port ,
Event Date (5) LER Nsmber (6) Report Date (7) Other Facilities Involved (8)
Month Cay Year Year fjj/ Sequential
// / Revision Month Day Year Facility Names Docket Number (s)
/// Number
/jj/j/
// Number 0 15 10 10 10 I I I ;
01 1 2 16 9I3 91 3 01012 010 012 21 5 91 3 0 15 10 10 10 l l l i
THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10CFR PODE (9) 1 20.402(b) _._ 20.405(c) _x_ 50.73(a)(2)(iv) _ 73.71(b)
POWER _ 20.405(a)(1)(i) __ 50.36(c)(1) _ 50.73(a)(2)(v) _ 73.71(c) !
LEVEL 20.405(a)(1)(ii) _ 50.36(c)(2) ._,_ 50.73(a)(2)(vii) _
Other (Specify ;
0 l1 lB (10) __ 20.405(a)(1)(iii) _X.L 50.73(a)(2)(i) _, 50.73(a)(2)(viii)(A) in Abstract
'///////////////////////// _ 20.405(a)(1)(iv) _ 50.73(a)(2)(ii) __ 50.73(a)(2)(viii)(B) below and in (
/ /
LICENSEE CONTACT FOR THIS LER (12)
Name TELEPHONE NUMBER _
AREA CODE Michael W. Metain. Svstems Enaineerina Department. Extension 2576 811 l5 3 15 17 1 -16 17 16 1 ;
COMPLETE ONE LINE FOR EACH COMPO FAllORE DESCRIBED IN THIS REPORT (13) l CAUSE SYSTEM COMPONENT P%NUFAC- REPORTABLE CAUSE SYSTEM COMPONENT t%NUFAC- REPORTABLE TURER TO NPRDS TURER TO NPRDS f A SIB l l l l l l Yes l I l l l l I r l I I I I I l . I I I I I I I ,
SUPPLEMENTAL REPORT EXPECTED (14) Expected Month I Day I Year l Submission !
lyes (If ves, complete EXPECTED SUBMISSION DATE) X l NO i !l !I ABSTRACT (Limit to 1400 spaces, i.e. approximately fif teen single-space typewritten lines) (16) i
[
On January 26,1993 Unit 1 was in Operational Mode 1 (Run) at 18 percent power.
During the performance of LaSalle Operating Department Surveillance, LOS-MS-R2, Main Steam Safety Relief Valve Manual Cycling Test f or Conditions 1, 2 or 3", Unit 1 Safety Relief Valve (SRV) 'A' (EPN 1B21-F013A) failed to close when operated by the Nuclear Station Operator (NS0). Several attempts were made to close the SRV but were unsuccessful. Upon the Shift Engineer's authorization, the reactor was manually scranned, per ;
LaSalle Operating Abnormal Procedure LOA-NB-02, at 2320 hours0.0269 days <br />0.644 hours <br />0.00384 weeks <br />8.8276e-4 months <br />. The reactor mode switch was placed into the Shutdown position and scram recovery actions were initiated. 'A' SRV closed at 2334 hours0.027 days <br />0.648 hours <br />0.00386 weeks <br />8.88087e-4 months <br />, with no !
deliberate NSO action. Reactor pressure, at this point, had decreased to 340 psig. Other procedural actions were then taken to place the reactor into a Cold Shutdown condition.
Subsequent investigations revealed that 'A' SRV was pneumatically locked into a partially open position. ,
This was caused by duct tape blocking the pneumatic operator's Air Valve Manifold Exhaust Port. The SRV was !
able to open but air was not allowed to exhaust and therefore the SRV would not fully close. The duct tape eventually ripped away from the port, allowing air to exhaust and thus closing the SRV.
This event is reportable to the Nuclear Regulatory Ccanission per the requirements of 10CFR50.73(a)(2)(lv) any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF)
' and 10CFR50.73(a)(2)(1)(A) completion of any Nuclear Plant Shutdown required by Technical Specification.
5
LICENSEE EVENT RRPfmT (LER1 TEXV CONTI4JAVION Form Rev 2.0 DOCKET NUMBER (2) LER MJMBER (61 Paoe (31 JACILITY NAME (1)
Year /// Sequential //
/jj Revision fjj
/// Namber j/// Number Lgjalle County Station Unit 1 015101010131713 913 - Ol012 - O l0 01 2 0F 01 5 VEXT Energy Industry Identification System (EIIS) codes are identified in the text as (XX)
PLANT AND SYSTEM IDENTIFICATION:
General Electric - Boiling Water Reactor Energy Industry Identification System (EIIS) codes are identified in the text as [XX).
I A. CONDITION PRIOR TO EVENT Unit (s): 1 Fvent Date: 1/76/93 Event Time: 2315 Hours Reactor Mode (s): 1 Mode (s) Name: Run Power tevel(s): 18%
B. DESCRIPTION OF EVENT On .lanuary 26, 1993, at approximately 2315 hours0.0268 days <br />0.643 hours <br />0.00383 weeks <br />8.808575e-4 months <br />, Unit 1 was in Operational Condition 1 (Run) at 18%
power. At this time, LaSalle Operations Department was performing surveillance LOS-MS-R2, " Main Steam Safety Relief Valve Manual Cycling Test For Conditions 1, 2 or 3", when the Unit 1 NSO attempted to' .
cycle Main Steam (MS) ISB) Safety Relief Valve (SRV) 'A'. The ' A' SRV Control Switch (C/S) was placed into the open position and all indications showed that the SRV had opened, including MS Bypass Valve (BPV) position dropping f rom 2.5 to 0.9 BPV and 'A' SRV Tallpipe Temperature increasing. Upon placing the C/S into the auto position, the valve apparently f ailed to close. Both the open and closed indication lights were now deenergized. The NSO then checked the light indications for failed bulbs and found the bulbs were good.
Bypass valve position was now at 1.9 BPV and tailpipe temperature was still elevated. These items, 7 along with the known f act that the SRV magnetic reed switch position indicating system will exhibit dead bands or non-continuous position indication lead to the conclusion that the SRV was mid-positioned.
At 2318 hours0.0268 days <br />0.644 hours <br />0.00383 weeks <br />8.81999e-4 months <br /> on 1/26/93, the Shif t Engineer was notified of a stuck open SRV and a two minute timeclock was initiated, per LOA-NB-.02, that called for closing the SRV or scraming the reactor. The fuses for
'A' SRV,1B21C-F31 and 1821C-F32, at Panel 1M13-F628 in the Auxiliary Electric Equipment Room (AEER),
were pulled and then replaced. This resulted in no change to SRV position indication, BPV position indication or tallpipe temperature. The 'A' SRV C/S was cycled again and the OPEN indication light became energized but then deenergized when the C/S was placed into AU13. Throu;hout the C/S cycling there were no changes in BPV position indication or tailpipe temperature. The above mentioned fuses a were pulled again and then reinstalled with no changes to SRV position indication, BPV position indication, or tailpipe temperature. The C/S was cycled for the third time, with no changes to the BPV position indication or tailpipe temperature but the OPEN indication light remained energized. The Shift Engineer, at 2320 hours0.0269 days <br />0.644 hours <br />0.00384 weeks <br />8.8276e-4 months <br /> on 1/26/93, then instructed the Unit 1 NSO to manually scram the reactor.
Nonnal scram recovery actions were begun and several noteworthy conditions and indications occurred.
Following the manual scram, four control rods (CR) (CR #s 34--03, 42-39, 46-43 and 14-51) appeared to have traveled past their full-in position and then drif ted back to the zero "00" position. The last of these control rods to reach position 00 was CR #14-51, which occurred at 2325 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.846625e-4 months <br />. This type of CR drif t is an espected evolution. At 2331 hours0.027 days <br />0.648 hours <br />0.00385 weeks <br />8.869455e-4 months <br /> the Suppression Pool (SP) water level reached +4.6 inches, exceeding the +3 inch limit (Technical Specification 3.6.2.1). The SP level increased because of the SRV blowdown and corrective actions were undertaken per LaSalle General Abnormal Procedure
LIQNgf,_fVENT CtLPpH (LER1 TEXV CONTI*0ATION Fem Rev 2.0 DOCKET NUMBER (2) LER KMBER (6) Pace (3)
FACILITY NAME (1)
Year j//j/ Sequenti al /// Revision f fff
/// Number /// Number
_11alle S County Station Unit 1 015101010131713 913 -
Ol0l2 - 0 l0 01 3 0F 01 5 TEXT Energy Industry Identification System (EIIS) codes are identified in the text as [XX)
- 8. DESCRIPTION OF EVENT CONTINUED i
LGA-03, " Primary Containment Control". Nonnal pool level was restored to 2.7 inches at 0027 hours3.125e-4 days <br />0.0075 hours <br />4.464286e-5 weeks <br />1.02735e-5 months <br />, on 1/27/93, and LGA-03 was exited. At 2330 hours0.027 days <br />0.647 hours <br />0.00385 weeks <br />8.86565e-4 months <br />, on 1/26/93, the Outboard Main Steam Isolation Valves and '
associated Main Steam Line Drain Valves were closed to control the Reactor Pressure Vessel cooldown rate. The Reactor Pressure Vessel cooldown rate was limited to 96 degrees Fahrenheit (F) in a one hour period, as determined from Reactor Recirculation (RR) [AD) suction temperatures. The cooldown rate did not exceed the 100 degrees F in any one hour per Technical Specification 3.4.6.1.
At 2334 hours0.027 days <br />0.648 hours <br />0.00386 weeks <br />8.88087e-4 months <br /> on 1/26/93, 'A' SRV position indication showed that the valve had closed. This was verified by SRV Tailpipe Temperature indication. The SRV had t>een open for approximately 18 minutes and Reactor pressure during this time had decreased f rom 930 psig to 340 psig. No deliberate NSO actions were taken to close the valve.
C. APPARENT CAUSE OF EVENT The apparent cause of 'A' SRV f ailing to close is attributed to its pneumatic (or air) actuator's inability to exhaust its control air supplied by the Instrument Nitrogen, (IN) [LE) System. This was caused by duct tape found over the actuator's Air Valve Manifold Exhaust Port. The duct tape did not prevent the SRV from opening but did not allow the SRV to close. Duct tape was also found on the pneumatic air cylinder's vent.
The air valve controls the pathways for 100 psig IN that travels to the bottom side of the actuating piston, inside the air actuator cylinder. When the SRV C/S is taken to open, an associated SRV solenoid energizes and positions the air valve to port 100 psig IN to the bottom side of the air actuator's operating piston. This upward force is transferred to the SRV, via a mechanical lever or " dog" assembly, such that the main SRV spring is overcome and the SRV opens. Also, the IN above the piston, is exhausted to Drywell (DW) atmosphere through the air actuator cylinder vent. When the SRV C/S is taken back to the AUTO position, the associated solenoid de-energizes and the air valve repositions.
The 100 psig IN supply is cutoff and the volume of IN, on the unde. side of the air actuator piston, exhausts to atmosphere via the air valve manifold. Also, DW atmosphere is drawn into the air actuator, to the top side of the actuating piston, through the cylinder top vent.
With duct tape covering the exhaust port on the air valve manifold and duct tape on the actuator cylinder top vent, the air actuator will be pneumatically locked into the open condition and the SRV will be unable to close. This is caused by the 100 psig IN on the underside of the actuator piston, not being able to exhaust through the air valve manifold and therefore blocking any movement of the actuator piston. When the duct tape finally bubbled-up and ripped away from the exhaust port, the SRV closed.
It is also very likely that the duct tape on the cylinder top vent was partially blown clear when the SRV was opened and then was drawn back into the vent hole on the closing stroke of the piston. This tape may have had some affect on how the air actuator operated, in that, it may have caused a small vacuum block on the top side of the piston which added resistance to the piston movement. [
The two pieces of duct tape that were found on 'A' SRV were installed as cleanliness boundaries. 'A' SRV was reworked and tested at Wyle Labs prior to installation during LaSalle's Unit 1 Fif th Refuel Outage (L1R05) f all of 1992. The duct tape was placed on to the SRV by Vyle Lab Technicians per their QA procedures for the shipment back to LaSalle Station. LaSalle Mechanical Maintenance Department (MMD) is responsible for the SRV installation and they oversee the contractor personnel that perform the actual work. The SRV installation is governed by HMD procedure LMP-MS-06, " Removal / Installation of Main Steam Safety Relief Valves". Interviews with MMD and contractor personnel revealed that all craf t personnel were aware of
k tfCENSEE EVENT REPORT (LER1 TRXV CON 71NUAV10N Form Ree 2.0
. FACILITY NAME (1) DOCKET NUMBER (2) LER NLMER (6) Pace (3)
Year // Sequential // Revision j/g/
// Number j///g/ Number tasalle County Station Unit 1 0 l S I O I O I O I 31 71 3 913 - 01012 - 0 IO 01 4 0F Of S TEXT Energy Industry Identification System (Ells) codes are identified in the text as (XX)
C. APPARENT CAUSE OF EVENT CONTINUED the duct tape and that common cleanliness practices were followed. All procedural precautions and limitations were followed and good work practices, pre-job briefings and shif t turnovers were utilized.
No proced.sral discrepancies or abnormalities were noted during the installation process and there was adequate supervision f rom contractor management.
Also discussed during the interviews were the procedural steps that govern cleanliness control and duct tape removal. There are specific steps in LMP-MS-06 for cleanliness control and duct tape removal but only the cleanliness control step has a supervisory signoff. The cleanliness control step states the cleanliness class to be maintained during the air actuator assermbly installation but does not encompass the tape removal. The duct tape removal step clearly identifies the correct exhaust port but does not I
require any craf t or supervisory signature for step completion. Also the procedure does not identify the removal of the duct tape on the actuator cylinder top went.
Contributing factors to the root cause deterinination for this problem include the following; during the initial investigation it was noted that the duct tape found on 'A' SRV was silver colored and that the air valve, which is made of aluminum, also has a silver color. This made the tape somewhat hard to see. Also the air valve manifold exhaust port is physically located on the bottom rear portion of the j air valve assembly and once the SRV is installed, it takes some effort to locate and inspect it.
Inspection of the remaining seventeen SRVs revealed two other Srvs had duct tape on their air valve manifold exhaust ports; 'D' SRV (EPN 1821-F013D) and 'V' SRV (EPN 1B21-F013V). The duct tape on both of these valves appeared to have ripped away and were not blocking the air valve manifold exhaust ports.
Both of these SRVs had been cycled prior to 'A' SRV but it appears that their exhaust ports were cleared ,
of the duct tape during the SRV testing during Unit startup for L1R04 4th refuel Spring of 1991. A review of maintenance records revealed these two SRVs were installed during L1R04 and that the duct tape was placed on the SRVs for cleanliness purposes, the same reasocing for its use on 'A' SRV by Wyle Lab Technicians. Also both 'D' and 'V' SRV's are Automatic Depressiurisation System (ADS) SRVs and utilize 175 psig IN as control air. At this pressure the duct tape would have had additional force applied to it and may have ripped away with less resistance. Therefore, no abnormalities in their operation were noted.
The root cause for 'A' SRV failing to close is attributed to a personnel error. An unidentified contractor worker f ailed to remove the duct tape from the Air Valve Manifold Exhaust Port, even though there were procedural guidance and instructions to do so. There are several secondary and/or contributing factors as to why the tape was not remond but the final reason is unknown.
D. SAFETY ANALYSIS OF EVENT The safety consequences of this event are minimal. Compliance with all of the procedural requirements stated in LOA-NB-03, " Stuck Open Safety Relief Valve", ensured that this was true. This transient is addressed in UFSAR Chapter 15.6.1, " Inadvertent SRV Opening". In this accident analyses. It is noted -
that if the SRV cannot be closed, then reactor power should be decreased. This would mitigate the consequences of the mild depressurization event taking place. Also, UFSAR Chapter 15.6.1 states that Suppression Pool (SP) Temperature should be monitored very closely, to ensure that the reactor is shutdown when the SP temperature setpoint is reached. Technical Specifications 3.4.2 and 3.6.2 set this '
limit at a temperature of 110 degrees Fahrenheit (SP temperature increased to approximately 70 degrees Fahrenheit during this event). Suppression pool cooling was already in operation for the SRV testing.
Technical Specification 3.4.2 also sets a two minutes timeclock that gives the Unit Operators the !
opportunity to close the SRV (four attempts before a manual scram). All of these points are conservatively incorporated into LOA-NB-03, " Stuck teen SRV". This procedure was followed by the NSO and the Unit was placed into a safe condition.
j j
' - LICENSEE EVENT REPORT (LER1 TEXT CONTINUATION DOCKET Rs>EER (2) LER WJMBER (61 l Pace (31 FACILITY NAME (1)
Year //j/ Sequential /j/j
/ Revision" j//j
/ Number j/// Nyber _
tasalle County Station Unit 1 0 I $ 101010131713 913 -
0l012 -
O l0 01 5 0F 01 S i
TEXT Energy Industry Identification System (Ells) codes are identified in the test as (XX]
i E. CORREETIVE ACTIONS A troubleshooting team (MMD, Electrical Maintenance, Technical Staff, and Operations) entered the DW or 1/27/93 to perform a visual inspection on 'A' SRV. It was at this time that the duct tape was found on the Air Valve Manifold Exhaust Port and Cylinder Top Vent. The duct tape found on the Air Valve Manifold Enhaust Port exhibited evidence of bubbling and ripping. The team removed the duct tape and then began to inspect the SRV for any apparent mechanical abnormalities; none were found. Following this the team then inspected the remaining seventeen SRVs. As mentioned earlier, 'D' and 'V' SRVs also e had duct tape on their exhaust ports (but no duct tape on their cylinder top vents). This duct tape was also removed. No other abnormalities were reported by this team.
MMD procedure, LMP-MS-06, " Main Steam Safety Relief Valve Manual Cycling Test for Conditions 1, 2 or 3",
did not require any signature for step completion concerning the tape removal. MMD has submitted a procedure change that will require a supervisory sign-of f for the tape removal. This sign-of f will also encompass the tape removal f rom the Air Actuator Cylinder Top Vent, Solenoid Valve Exhaust Ports and SRV Bonnet Vent. Drawings will also be added that will specifically label all of these vents and ports. .
A review of Maintenance Procedures, that involve cleanliness requirements, will be performed.
Determination will be made as to any applicable procedures that need similar enhancement to LMP-MS-06.
These procedure reviews / revisions will be tracked by Action Item Record (AIR) 373-180-93-00901.
On 1/27/93. EMD replaced the solenoid and air valve for ' A' SRV,1821-F013A. There was no evidence of any type of damage to these components but they were replaced on the grounds of thoroughness. Both the solenoid and air valve will be tested at Wyle Labs at the next scheduled testing opportunity. These components will be installed into a spare slot on one of the non-ADS SRVs and then tested per the Wyle Labs Air Actuator Test Procedure. The testing and test results will be tracked by EMD per LaSalle (AIR) 373-180-93-00902.
The eighteen SRVs that are currently installed in LaSalle Unit 2 will be inspected for the presence of duct tape at any exhaust p;rts or vents. This will be accomplished during the next available forced or l refuel (L2R05) outage. All eighteen Unit 2 SRVs cycled satisf actorily, per LOS-MS-R2, " Main Steam .
Safety Relief Valve Manual Cycling Test for Conditions 1, 2 or 3", during Unit startup following L2R04. ;
At that time no discrepancies or abnormalities were noted. This inspection will be tracked and reported, by MMD, per AIR 373-180-93-00903. ,
On 1/28/93 Operations Department completed surveillance LOS-MS-R2,
F. PREVIOUS EVENTS None.
G. COMPONENT FAILURE DATA None.
' 58552 ' 3 VENT
SUMMARY
~
. . . i
""=bar AND "
o""-1-31-2929
- 9)
Lost generation
~
g Reactor trip i NRC violation, level ___l
~
Cost > $25,000 ESF actuation GSEP event, class ____.!
-'- ~
~
Hazard or Spill NRC reportable Tech Spec LCO
~
O Personnel injury Z LER Potential or future loss;
~
Component - PSE SALP functional area __;
Tat.,ure node r
gyp, r .
, , Dipartment
}lS NA' t.fA M' I I 4M '
i
'I I l 1 1 I I
lA l i I l 1 I I I [
Licensed? L or blank Tys.t {
Level Detall code !
hpartment f~ ;
A lua i tais- c~geez f ( l
)
A I I J A i i i i Type -
4 Detail Code
. I Dens rtment i I h l l s j l 1 I i * \
i i I I I I i l~ l l 1 1 Tyna ,Detall code i b [l l Type of deficiency i l D 'I"II * . Procedure type l)
! I I i i Iii -
- l l 1
- Detail code Type Denartment i3 : I I
! l 1 I a , , i i i
j