|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B1481993-07-30030 July 1993 LER 93-012-00:on 930702,reactor Core Isolation Cooling Sys Declared Inoperable Due to Associated Bus Voltage Dropping Below TS Limits.Sent Operator to Cycle Timer Which Caused Affected Contact to reclose.W/930730 Ltr ML20045D9331993-07-0202 July 1993 LER 93-004-00:on 930604,unexpected CRD Low Charging Water Header Scram Received Followed by Charging Water Header A2/B2 Alarm.Caused by Crud or Foreign Matl Passing Through Suction Filter.Filters Cleaned & reused.W/930702 ML20045D7501993-06-23023 June 1993 LER 93-003-00:on 930524,Div 1 ECCS Initiation Signal Received & LPCS Pump,Lpci Pump 2A & EDG Unit 0 Automatically Started.Caused by Personnel Error.Pumps Secured & Event Documented in Personnel file.W/930623 Ltr ML20044E4161993-05-28028 May 1993 LER 92-009-01:on 920923,spurious Auto Start of CR Ventilation Emergency make-up Train Occurred Due to High Radiation Spike.Radiation Monitor Circuit modified.W/930528 Ltr ML20044E4191993-05-21021 May 1993 LER 93-011-00:on 930423,manual Scram Initiated.Caused by Disconnected Linkage on Valve Positioner on Heater Drain Valve Due to Loose Jam Nut.Tailgate Session Will Be Held W/ Instrument Maint Dept Re Jam nuts.W/930521 Ltr ML20044D5161993-05-15015 May 1993 LER 92-007-01:on 920613,high Radiation Spike Received from CR Ventilation Process Radiation Monitor,Initiating Emergency Makeup Train B.Caused by Normal Variations in Radiation Readings.Spike modified.W/930515 Ltr ML20044D5571993-05-14014 May 1993 LER 93-010-00:on 930414,DG Cooling Water Pump Automatically Tripped on Magnetic Overload.Caused by Inexperienced Trainee in Operation of Control Lever.Lesson Plans & Training Programs for Operators to Be reviewed.W/930514 Ltr ML20044C9801993-05-0707 May 1993 LER 91-010-01:on 910719 & 0805,CR a Ventilation Emergency Makeup Fan auto-started on Spurious Trip of CR Air Intake Process Radiation Monitor.Caused by Normal Variations in Background Radiation.Supply Board replaced.W/930507 Ltr ML20044B6161993-02-25025 February 1993 LER 93-002-00:on 930126,Unit 1 Manual Scram Due to a SRV Being Stuck Open Due to Duct Tape Being Over Actuators Air Valve Manifold Exhaust Port.Maint Procedures That Involve Cleanliness reviewed.W/930225 Ltr ML20024G9771991-05-10010 May 1991 LER 91-005-00:on 910410,determined That Tech Spec Required Surveillance of Suppression Chamber Oxygen Sampling Missed. Caused by Inadequate Review of Tech Spec Change.Drywell & Suppression Chamber Checked for oxygen.W/910510 Ltr ML20044A3851990-06-25025 June 1990 LER 90-008-00:on 900525,Tech Spec Hourly Fire Watch Missed Due to Miscommunications Between Security Personnel & Radiation Protection Personnel.Fire Watch re-established & Memo issued.W/900625 Ltr ML20043F1721990-06-0505 June 1990 LER 90-009-00:on 900510,RWCU Outboard Suction Isolation Valve 2G33-F004 Auto Closed Which Tripped RWCU Pump B. Caused by Procedure Deficiency.Procedure LTS-500-209 Will Be revised.W/900605 Ltr ML20043F1281990-06-0101 June 1990 LER 90-009-00:on 900511,apparent Ruptured Diaphragm Found on Pressure Differential Switch in RCIC Steam Line.Caused by Torn Diaphragm Inside Switch.Replacement Switch Installed, Calibr & Functionally Tested satisfactorily.W/900608 Ltr ML20043B5681990-05-23023 May 1990 LER 89-027-01:on 891113,primary Containment Isolation Sys Group 1 Isolation Occurred During Surveillance Testing. Caused by Burnt Out Window Light Bulbs on Alarm Window. Light Bulbs Replaced & Jumpers installed.W/900523 Ltr ML20043A7721990-05-18018 May 1990 LER 90-007-00:on 900421,reactor Protection Sys Bus a Transfer & Reactor Recirculation Hydraulic Power Unit a Inboard Isolation Valves Closed,Causing Partial Group II isolation.Out-of-svc Procedure revised.W/900518 Ltr ML20043D0591990-05-18018 May 1990 LER 90-008-00:on 900502,ESF Actuation of Control Room B Emergency Ctk Ventilation Makeup Fan Occurred.Caused by Procedure deficiency.LTS-800-205 & Similar Procedures Will Be revised.W/900601 Ltr ML20042H0211990-05-10010 May 1990 LER 90-006-00:on 900412,loop a Primary Containment Chilled Water Sys Inboard Isolation Valves & Reactor Bldg Closed Cooling Water Sys Inboard Isolation Valve Went Closed.Caused by Inadequate Procedure.Procedures revised.W/900510 Ltr ML20042F9001990-05-0404 May 1990 LER 90-005-00:on 900411,experienced Loss of Dc Power to Portion of Div I Primary Containment Isolation Sys Logic Which Resulted in Isolation Signal & Actuation.Caused by Failure to Update Drawings & procedures.W/900504 Ltr ML20042F1941990-04-30030 April 1990 LER 89-025-01:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Door Containing Undervoltage Relays Closed.Caused by Misalignment of Door.Door Repaired. W/900430 Ltr ML20012D5341990-03-16016 March 1990 LER 90-003-01:on 900201,RCIC Isolation Signal Occurred During Warmup.Caused by Spurious High Steam Flow Signal.Rcic Sys Piping Integrity Verified & Isolation Logic Reset.W/ 900316 Ltr ML20012D5371990-03-16016 March 1990 LER 90-002-01:on 900129,oil in Diesel Generator Governor 1A Found to Be Low & Could Not Be Seen in Sight Glass.Caused by Slow Leak from Compensation Needle Valve Plug.Proper Amount of Oil Added & Operability Test performed.W/900316 Ltr ML20012C4931990-03-15015 March 1990 LER 90-004-00:on 900213,control Room B HVAC Intake Radiation Monitor Lost Power Causing auto-start of Emergency make-up Train B.Caused by Blown Fuses.Fuses Replaced.Logic Revs for Radiation Monitors Will Be installed.W/900315 Ltr ML20012B6501990-03-0909 March 1990 LER 90-002-00:on 900209,Operating Surveillance LOS-TG-W1 Determined to Have Exceeded Required Testing Interval,Per Tech Spec 3/4.7.10.Caused by Personnel Error.Personnel Counseled & Ref Procedures Will Be revised.W/900309 Ltr ML20012B5521990-03-0808 March 1990 LER 90-001-00:on 900206,full Reactor Scram Occurred During Instrument Surveillance Testing.Caused by Actuation of APRM E Trip Circuitry.Shutdown Margin Revised & Caution Card Placed on Control Room Bench board.W/900308 Ltr ML20011F8251990-03-0202 March 1990 LER 90-003-00:on 900201,RCIC Received Div 2 Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal Generated When Steam/Water Mixture Admitted to RCIC Steam Line.Isolation Logic reset.W/900302 Ltr ML20011F5551990-02-28028 February 1990 LER 90-002-00:on 900129,after Filling Diesel Generator 1A Governor W/Oil,Generator Started & Declared Inoperable. Caused by Slow Leak Coming from Compensation Needle Valve Plug.Oil Added & Plug Washer replaced.W/900228 Ltr ML20006F5951990-02-21021 February 1990 LER 90-001-00:on 900122,RWCU Sys Received Div 1 Leakage Detection Ambient Temp High Isolation Signal,Causing Trips of RWCU Pumps a & C.Caused by Broken Thermocouple Input Lead.Lead Wire Reconnected & Isolation reset.W/900221 Ltr ML20011F4921990-02-16016 February 1990 LER 89-013-01:on 890907,Group I Isolation Received During Performance of Instrument Surveillance LIS-MS-401.Caused by Depressurization of Main Steam Line Low Pressure Switch. Surveillance Revised to Split Into Two parts.W/900216 Ltr ML20006E4501990-02-15015 February 1990 LER 89-010-01:on 890715 & 17,voltage Oscillations Noted on Div II Battery Charger,Resulting in Inoperability of HPCS Sys.Caused by Failure of Charger in High Voltage Shutdown Relay.Charger Energized & Relay replaced.W/900215 Ltr ML20006E4451990-02-14014 February 1990 LER 89-009-01:on 890619,diaphragm Leak Discovered in RCIC Steam Line High Flow Isolation Switch.Caused by 1 & 1/2-inch Tear in Diaphragm.Pressure Differential Switch Replaced & Calibr.Reported Per NRC Bulletin 86-002.W/900214 Ltr ML20006E3981990-02-14014 February 1990 LER 89-008-01:on 890228,reactor Vessel Low Water Level 2 Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.Channel Placed in Tripped Condition & All Static-O-Ring Pressure Switches to Be replaced.W/900214 Ltr ML20006E3951990-02-14014 February 1990 LER 89-010-01:on 890303,automatic Depressurization Sys Permissive Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.All Static-O-Ring Reactor Vessel Level Switches Will Be replaced.W/900214 Ltr ML19354D8361990-01-15015 January 1990 LER 89-018-00:on 891216,plant 250-volt Battery & RCIC Sys Declared Inoperable Due to Low Battery Electrolyte Temps. Caused by Failure of Div I Switchgear Heat Removal Sys Damper Actuators.Air Intake Dampers closed.W/900115 Ltr ML20042D3921990-01-0404 January 1990 LER 89-011-01:on 890826,spurious Reactor Protection Sys Actuation Occurred.Definite Cause of Trip Not Determined. Brief Disturbance in Reactor Protection Sys Allowed Some Contactors to Trip.Procedure revised.W/900104 Ltr ML20005E2741989-12-22022 December 1989 LER 89-028-00:on 891204,RHR Shutdown Cooling Suction Header Outboard Isolation Valve Automatically Isolated.Caused by Miscommunication Between Technician & Station Operator.Task Force Developed to Review event.W/891222 Ltr ML19351A6301989-12-15015 December 1989 LER 89-006-01:on 890214,reactor Vessel Low Water Level 3 Switch Setpoint Found Out of Tolerance.Caused by Setpoint Drift.Level Switch to Be Replaced by Analog Trip Sys During First Quarter 1990.W/891215 Ltr ML20011D1341989-12-14014 December 1989 LER 89-017-00:on 891117,flow Switch FS-2E22-N006 Found W/ Setpoint Out of Tolerance Above Reject Limit.Caused by Setpoint Drift.Work Request Written to Replace Flow Switch. W/891214 Ltr ML19351A6751989-12-12012 December 1989 LER 89-027-00:on 891113,primary Containment Isolation Sys Group I Isolation Occurred While Performing Instrument Surveillance.Caused by Loss of Power to Leak Detection Sys Logic.Isolation reset.W/891213 Ltr ML19332F0081989-12-0808 December 1989 LER 89-016-00:on 891109,RWCU Isolation Occurred While Instrument Surveillance on Ventilation Differential Temp Isolation Functional Test in Progress.Caused by Faulty Thermocouple.Thermocouple repaired.W/891208 Ltr ML20005D6621989-12-0606 December 1989 LER 89-026-00:on 891106,inadvertent Primary Containment Isolation Actuation Occurred While Clearing out-of-svc. Caused by Inadequate Logic Setup During Mod Installation. Trip Status & Output Switches repositioned.W/891206 Ltr ML19332F2431989-12-0101 December 1989 LER 89-025-00:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Equipment Operator Closed Door Containing Relays.Caused by Misalignment of Door.Isolations Reset,Bus Energized & Circuit Logic tested.W/891201 Ltr ML19332E6581989-11-29029 November 1989 LER 89-015-00:on 891030,shift Control Room Engineer Noted That Quarterly Standby Liquid Control Operating Surveillance LOS-SC-Q1 Was Past Critical Date.Caused by Clerical Data Entry Error.Missed Surveillance performed.W/891129 Ltr ML19332D5181989-11-22022 November 1989 LER 89-018-01:on 890515,RCIC Received Div I & Div II Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal When Steam Added to RCIC Steam Line. Special Test Initiated.Isolation Logic reset.W/891122 Ltr ML19327C2601989-11-17017 November 1989 LER 89-014-00:on 891020,primary Containment Isolation Sys Group 4 Isolation Occurred Causing Isolation Dampers to Close.Caused by Opening of Div 2 125-volt Dc Breaker.Power Supply replaced.W/891117 Ltr ML19325F3411989-11-13013 November 1989 LER 89-024-00:on 891013 & 30,unsealed Openings in Main Control Room Floor & Main Control Room West Wall Discovered. Caused by Wide Gap Between Structural Beam & Cable Tray. Openings Sealed & Fire Watch established.W/891113 Ltr ML19324C1751989-11-0808 November 1989 LER 89-012-01:on 890309,diaphragm Leak Found in Pressure Differential Switch 1E31-N013BB.Caused by Tear Found in Diaphragm.Replacement Switch Installed,Calibr & Functionally Tested satisfactorily.W/891108 Ltr ML20024E9121983-08-26026 August 1983 LER 83-093/03L-0:on 830801,discovered full-in Indication on Core Display for Control Rod 34-47 Inoperable.Caused by Failed Switching Transistor on Data Memory Board 19.Data Memory Board replaced.W/830826 Ltr ML20024B8381983-07-0505 July 1983 LER 83-060/03L-0:on 830606,following Turbine Trip & Scram Due to High Vibration on Main Turbine,Reactor Recirculation Breaker 4B Closed.Cause Undetermined.Auxiliary Contacts cleaned.W/830705 Ltr ML20024B0721983-06-16016 June 1983 Updated LER 83-012/03X-1:on 830210,w/reactor in Cold Shutdown,Setpoints for Switches 1E31-N612A/B Found Above Tech Spec Limits.Cause Unknown.Switches calibr.W/830616 Ltr ML20024A6961983-06-14014 June 1983 LER 83-051/03L-0:on 830516,reactor Protection Sys Trip Channel H2 Limit Switch Failed to Operate Properly.Cause Unknown.Limit Switch readjusted.W/830614 Ltr 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046B1481993-07-30030 July 1993 LER 93-012-00:on 930702,reactor Core Isolation Cooling Sys Declared Inoperable Due to Associated Bus Voltage Dropping Below TS Limits.Sent Operator to Cycle Timer Which Caused Affected Contact to reclose.W/930730 Ltr ML20045D9331993-07-0202 July 1993 LER 93-004-00:on 930604,unexpected CRD Low Charging Water Header Scram Received Followed by Charging Water Header A2/B2 Alarm.Caused by Crud or Foreign Matl Passing Through Suction Filter.Filters Cleaned & reused.W/930702 ML20045D7501993-06-23023 June 1993 LER 93-003-00:on 930524,Div 1 ECCS Initiation Signal Received & LPCS Pump,Lpci Pump 2A & EDG Unit 0 Automatically Started.Caused by Personnel Error.Pumps Secured & Event Documented in Personnel file.W/930623 Ltr ML20044E4161993-05-28028 May 1993 LER 92-009-01:on 920923,spurious Auto Start of CR Ventilation Emergency make-up Train Occurred Due to High Radiation Spike.Radiation Monitor Circuit modified.W/930528 Ltr ML20044E4191993-05-21021 May 1993 LER 93-011-00:on 930423,manual Scram Initiated.Caused by Disconnected Linkage on Valve Positioner on Heater Drain Valve Due to Loose Jam Nut.Tailgate Session Will Be Held W/ Instrument Maint Dept Re Jam nuts.W/930521 Ltr ML20044D5161993-05-15015 May 1993 LER 92-007-01:on 920613,high Radiation Spike Received from CR Ventilation Process Radiation Monitor,Initiating Emergency Makeup Train B.Caused by Normal Variations in Radiation Readings.Spike modified.W/930515 Ltr ML20044D5571993-05-14014 May 1993 LER 93-010-00:on 930414,DG Cooling Water Pump Automatically Tripped on Magnetic Overload.Caused by Inexperienced Trainee in Operation of Control Lever.Lesson Plans & Training Programs for Operators to Be reviewed.W/930514 Ltr ML20044C9801993-05-0707 May 1993 LER 91-010-01:on 910719 & 0805,CR a Ventilation Emergency Makeup Fan auto-started on Spurious Trip of CR Air Intake Process Radiation Monitor.Caused by Normal Variations in Background Radiation.Supply Board replaced.W/930507 Ltr ML20044B6161993-02-25025 February 1993 LER 93-002-00:on 930126,Unit 1 Manual Scram Due to a SRV Being Stuck Open Due to Duct Tape Being Over Actuators Air Valve Manifold Exhaust Port.Maint Procedures That Involve Cleanliness reviewed.W/930225 Ltr ML20024G9771991-05-10010 May 1991 LER 91-005-00:on 910410,determined That Tech Spec Required Surveillance of Suppression Chamber Oxygen Sampling Missed. Caused by Inadequate Review of Tech Spec Change.Drywell & Suppression Chamber Checked for oxygen.W/910510 Ltr ML20044A3851990-06-25025 June 1990 LER 90-008-00:on 900525,Tech Spec Hourly Fire Watch Missed Due to Miscommunications Between Security Personnel & Radiation Protection Personnel.Fire Watch re-established & Memo issued.W/900625 Ltr ML20043F1721990-06-0505 June 1990 LER 90-009-00:on 900510,RWCU Outboard Suction Isolation Valve 2G33-F004 Auto Closed Which Tripped RWCU Pump B. Caused by Procedure Deficiency.Procedure LTS-500-209 Will Be revised.W/900605 Ltr ML20043F1281990-06-0101 June 1990 LER 90-009-00:on 900511,apparent Ruptured Diaphragm Found on Pressure Differential Switch in RCIC Steam Line.Caused by Torn Diaphragm Inside Switch.Replacement Switch Installed, Calibr & Functionally Tested satisfactorily.W/900608 Ltr ML20043B5681990-05-23023 May 1990 LER 89-027-01:on 891113,primary Containment Isolation Sys Group 1 Isolation Occurred During Surveillance Testing. Caused by Burnt Out Window Light Bulbs on Alarm Window. Light Bulbs Replaced & Jumpers installed.W/900523 Ltr ML20043A7721990-05-18018 May 1990 LER 90-007-00:on 900421,reactor Protection Sys Bus a Transfer & Reactor Recirculation Hydraulic Power Unit a Inboard Isolation Valves Closed,Causing Partial Group II isolation.Out-of-svc Procedure revised.W/900518 Ltr ML20043D0591990-05-18018 May 1990 LER 90-008-00:on 900502,ESF Actuation of Control Room B Emergency Ctk Ventilation Makeup Fan Occurred.Caused by Procedure deficiency.LTS-800-205 & Similar Procedures Will Be revised.W/900601 Ltr ML20042H0211990-05-10010 May 1990 LER 90-006-00:on 900412,loop a Primary Containment Chilled Water Sys Inboard Isolation Valves & Reactor Bldg Closed Cooling Water Sys Inboard Isolation Valve Went Closed.Caused by Inadequate Procedure.Procedures revised.W/900510 Ltr ML20042F9001990-05-0404 May 1990 LER 90-005-00:on 900411,experienced Loss of Dc Power to Portion of Div I Primary Containment Isolation Sys Logic Which Resulted in Isolation Signal & Actuation.Caused by Failure to Update Drawings & procedures.W/900504 Ltr ML20042F1941990-04-30030 April 1990 LER 89-025-01:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Door Containing Undervoltage Relays Closed.Caused by Misalignment of Door.Door Repaired. W/900430 Ltr ML20012D5341990-03-16016 March 1990 LER 90-003-01:on 900201,RCIC Isolation Signal Occurred During Warmup.Caused by Spurious High Steam Flow Signal.Rcic Sys Piping Integrity Verified & Isolation Logic Reset.W/ 900316 Ltr ML20012D5371990-03-16016 March 1990 LER 90-002-01:on 900129,oil in Diesel Generator Governor 1A Found to Be Low & Could Not Be Seen in Sight Glass.Caused by Slow Leak from Compensation Needle Valve Plug.Proper Amount of Oil Added & Operability Test performed.W/900316 Ltr ML20012C4931990-03-15015 March 1990 LER 90-004-00:on 900213,control Room B HVAC Intake Radiation Monitor Lost Power Causing auto-start of Emergency make-up Train B.Caused by Blown Fuses.Fuses Replaced.Logic Revs for Radiation Monitors Will Be installed.W/900315 Ltr ML20012B6501990-03-0909 March 1990 LER 90-002-00:on 900209,Operating Surveillance LOS-TG-W1 Determined to Have Exceeded Required Testing Interval,Per Tech Spec 3/4.7.10.Caused by Personnel Error.Personnel Counseled & Ref Procedures Will Be revised.W/900309 Ltr ML20012B5521990-03-0808 March 1990 LER 90-001-00:on 900206,full Reactor Scram Occurred During Instrument Surveillance Testing.Caused by Actuation of APRM E Trip Circuitry.Shutdown Margin Revised & Caution Card Placed on Control Room Bench board.W/900308 Ltr ML20011F8251990-03-0202 March 1990 LER 90-003-00:on 900201,RCIC Received Div 2 Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal Generated When Steam/Water Mixture Admitted to RCIC Steam Line.Isolation Logic reset.W/900302 Ltr ML20011F5551990-02-28028 February 1990 LER 90-002-00:on 900129,after Filling Diesel Generator 1A Governor W/Oil,Generator Started & Declared Inoperable. Caused by Slow Leak Coming from Compensation Needle Valve Plug.Oil Added & Plug Washer replaced.W/900228 Ltr ML20006F5951990-02-21021 February 1990 LER 90-001-00:on 900122,RWCU Sys Received Div 1 Leakage Detection Ambient Temp High Isolation Signal,Causing Trips of RWCU Pumps a & C.Caused by Broken Thermocouple Input Lead.Lead Wire Reconnected & Isolation reset.W/900221 Ltr ML20011F4921990-02-16016 February 1990 LER 89-013-01:on 890907,Group I Isolation Received During Performance of Instrument Surveillance LIS-MS-401.Caused by Depressurization of Main Steam Line Low Pressure Switch. Surveillance Revised to Split Into Two parts.W/900216 Ltr ML20006E4501990-02-15015 February 1990 LER 89-010-01:on 890715 & 17,voltage Oscillations Noted on Div II Battery Charger,Resulting in Inoperability of HPCS Sys.Caused by Failure of Charger in High Voltage Shutdown Relay.Charger Energized & Relay replaced.W/900215 Ltr ML20006E4451990-02-14014 February 1990 LER 89-009-01:on 890619,diaphragm Leak Discovered in RCIC Steam Line High Flow Isolation Switch.Caused by 1 & 1/2-inch Tear in Diaphragm.Pressure Differential Switch Replaced & Calibr.Reported Per NRC Bulletin 86-002.W/900214 Ltr ML20006E3981990-02-14014 February 1990 LER 89-008-01:on 890228,reactor Vessel Low Water Level 2 Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.Channel Placed in Tripped Condition & All Static-O-Ring Pressure Switches to Be replaced.W/900214 Ltr ML20006E3951990-02-14014 February 1990 LER 89-010-01:on 890303,automatic Depressurization Sys Permissive Switch Found W/Setpoint in Excess of Reject Limit.Caused by Setpoint Drift.All Static-O-Ring Reactor Vessel Level Switches Will Be replaced.W/900214 Ltr ML19354D8361990-01-15015 January 1990 LER 89-018-00:on 891216,plant 250-volt Battery & RCIC Sys Declared Inoperable Due to Low Battery Electrolyte Temps. Caused by Failure of Div I Switchgear Heat Removal Sys Damper Actuators.Air Intake Dampers closed.W/900115 Ltr ML20042D3921990-01-0404 January 1990 LER 89-011-01:on 890826,spurious Reactor Protection Sys Actuation Occurred.Definite Cause of Trip Not Determined. Brief Disturbance in Reactor Protection Sys Allowed Some Contactors to Trip.Procedure revised.W/900104 Ltr ML20005E2741989-12-22022 December 1989 LER 89-028-00:on 891204,RHR Shutdown Cooling Suction Header Outboard Isolation Valve Automatically Isolated.Caused by Miscommunication Between Technician & Station Operator.Task Force Developed to Review event.W/891222 Ltr ML19351A6301989-12-15015 December 1989 LER 89-006-01:on 890214,reactor Vessel Low Water Level 3 Switch Setpoint Found Out of Tolerance.Caused by Setpoint Drift.Level Switch to Be Replaced by Analog Trip Sys During First Quarter 1990.W/891215 Ltr ML20011D1341989-12-14014 December 1989 LER 89-017-00:on 891117,flow Switch FS-2E22-N006 Found W/ Setpoint Out of Tolerance Above Reject Limit.Caused by Setpoint Drift.Work Request Written to Replace Flow Switch. W/891214 Ltr ML19351A6751989-12-12012 December 1989 LER 89-027-00:on 891113,primary Containment Isolation Sys Group I Isolation Occurred While Performing Instrument Surveillance.Caused by Loss of Power to Leak Detection Sys Logic.Isolation reset.W/891213 Ltr ML19332F0081989-12-0808 December 1989 LER 89-016-00:on 891109,RWCU Isolation Occurred While Instrument Surveillance on Ventilation Differential Temp Isolation Functional Test in Progress.Caused by Faulty Thermocouple.Thermocouple repaired.W/891208 Ltr ML20005D6621989-12-0606 December 1989 LER 89-026-00:on 891106,inadvertent Primary Containment Isolation Actuation Occurred While Clearing out-of-svc. Caused by Inadequate Logic Setup During Mod Installation. Trip Status & Output Switches repositioned.W/891206 Ltr ML19332F2431989-12-0101 December 1989 LER 89-025-00:on 891101,sys Auxiliary Transformer Feed to Bus 142Y Tripped Open When Equipment Operator Closed Door Containing Relays.Caused by Misalignment of Door.Isolations Reset,Bus Energized & Circuit Logic tested.W/891201 Ltr ML19332E6581989-11-29029 November 1989 LER 89-015-00:on 891030,shift Control Room Engineer Noted That Quarterly Standby Liquid Control Operating Surveillance LOS-SC-Q1 Was Past Critical Date.Caused by Clerical Data Entry Error.Missed Surveillance performed.W/891129 Ltr ML19332D5181989-11-22022 November 1989 LER 89-018-01:on 890515,RCIC Received Div I & Div II Isolation on RCIC High Steam Line Flow.Caused by Spurious High Steam Flow Signal When Steam Added to RCIC Steam Line. Special Test Initiated.Isolation Logic reset.W/891122 Ltr ML19327C2601989-11-17017 November 1989 LER 89-014-00:on 891020,primary Containment Isolation Sys Group 4 Isolation Occurred Causing Isolation Dampers to Close.Caused by Opening of Div 2 125-volt Dc Breaker.Power Supply replaced.W/891117 Ltr ML19325F3411989-11-13013 November 1989 LER 89-024-00:on 891013 & 30,unsealed Openings in Main Control Room Floor & Main Control Room West Wall Discovered. Caused by Wide Gap Between Structural Beam & Cable Tray. Openings Sealed & Fire Watch established.W/891113 Ltr ML19324C1751989-11-0808 November 1989 LER 89-012-01:on 890309,diaphragm Leak Found in Pressure Differential Switch 1E31-N013BB.Caused by Tear Found in Diaphragm.Replacement Switch Installed,Calibr & Functionally Tested satisfactorily.W/891108 Ltr ML20024E9121983-08-26026 August 1983 LER 83-093/03L-0:on 830801,discovered full-in Indication on Core Display for Control Rod 34-47 Inoperable.Caused by Failed Switching Transistor on Data Memory Board 19.Data Memory Board replaced.W/830826 Ltr ML20024B8381983-07-0505 July 1983 LER 83-060/03L-0:on 830606,following Turbine Trip & Scram Due to High Vibration on Main Turbine,Reactor Recirculation Breaker 4B Closed.Cause Undetermined.Auxiliary Contacts cleaned.W/830705 Ltr ML20024B0721983-06-16016 June 1983 Updated LER 83-012/03X-1:on 830210,w/reactor in Cold Shutdown,Setpoints for Switches 1E31-N612A/B Found Above Tech Spec Limits.Cause Unknown.Switches calibr.W/830616 Ltr ML20024A6961983-06-14014 June 1983 LER 83-051/03L-0:on 830516,reactor Protection Sys Trip Channel H2 Limit Switch Failed to Operate Properly.Cause Unknown.Limit Switch readjusted.W/830614 Ltr 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217C9121999-10-12012 October 1999 SER Input Authorizing Licensee Proposed Request to Modify Definition of Core Alteration in Section 1.0 of TS & Update Sections 3/4.1,3.4.3 & 3/4.9 to Reflect Proposed Definition Change ML20217F9091999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for LaSalle County Stations,Units 1 & 2.With ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212C4501999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for LaSalle County Station,Units 1 & 2.With ML20210R0671999-07-31031 July 1999 Monthly Operating Repts for July 1999 for LaSalle County Station,Units 1 & 2.With ML20210C1681999-07-0909 July 1999 Seventh Refueling Outage ASME Section XI Summary Rept ML20209H1501999-06-30030 June 1999 Monthly Operating Repts for June 1999 for LaSalle County Station,Units 1 & 2.With ML20195J7871999-05-31031 May 1999 Monthly Operating Repts for May 1999 for LaSalle County Station,Units 1 & 2.With ML20209E1431999-05-31031 May 1999 Cycle 8 COLR, for May 1999 ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations ML20206N2071999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for LaSalle County Station,Units 1 & 2.With ML20205L8421999-03-31031 March 1999 Rev 2 to EMF-96-125, LaSalle Unit 2 Cycle 8 Reload Analysis ML20205L8301999-03-31031 March 1999 Administrative Technical Requirements App B (Amend 26) LaSalle Unit 2 Cycle 8 COLR & Reload Transient Analysis Results, for Mar 1999 ML20205R2721999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for LaSalle County Station,Units 1 & 2.With ML20205L8391999-03-22022 March 1999 Rev 2 to 960103, Neutronics Licensing Rept for LaSalle Unit 2,Cycle 8 ML20204C8141999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for LaSalle County Station,Units 1 & 2.With ML20199E4601998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for LaSalle County Station,Units 1 & 2.With ML20207C7371998-12-31031 December 1998 Annual Rept for LaSalle County Station for Jan 1998 Through Dec 1998 ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with ML20198B3801998-12-14014 December 1998 SER Accepting one-time Request for Relief from Certain Provisions of Section XI of ASME Boiler & Pressure Vessel Code,Per 10CFR50.55a for Certain Plant Safety/Relief Valves ML20206N2261998-12-0909 December 1998 LER 98-S03-00:on 981116,protected Area Was Entered Without Current Authorization for Unescorted Access Due to Programmatic Deficiency Error.Changed Badge Control Process ML20197K0981998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for LaSalle County Station,Unts 1 & 2.With ML20196B1441998-11-23023 November 1998 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Bindings of Safety-Related Power-Operated Gate Valves ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB ML20195D3191998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for LaSalle County Station.With ML20154H6781998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20153D0191998-09-18018 September 1998 Part 21 Rept Re Defect in Gap Conductance Analyses for co- Resident BWR Fuel.Initially Reported on 980917.Corrective Analyses Performed Demonstrating That Current Operating Limits Bounding from BOC to Cycle Exposure of 8 Gwd/Mtu ML20153C7621998-09-18018 September 1998 Safety Evaluation Acceping NRC Bulletin 95-002, Unexpected Clogging of RHR Pump Strainer While Operating in Suppression Pool Cooling Mode ML20153C6771998-09-17017 September 1998 Part 21 Rept Re Defect Relative to MCPR Operating Limits as Impacted by Gap Conductance of co-resident BWR Fuel at Facilities.Operating Limit for LaSalle Unit 2 & Quad Cities Unit 2 Will Be Revised as Listed ML20151W0241998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for LaSalle County Station.With ML20237E2921998-08-21021 August 1998 Special Rept:On 980811,channel 5 of Lpms Became Inoperable. Caused by Channel Failed pre-amplifier Located Inside Primary Containment at Inboard Side of Electrical Penetration E-19.Initiated Repairs of Channel ML20237E2331998-08-21021 August 1998 Revised Pages of Section 20 of Rev 66 to CE-1-A, QA Topical Rept ML20237B4861998-07-31031 July 1998 Monthly Operating Repts for July 1998 for LaSalle County Nuclear Power Station Units 1 & 2 ML20236V7701998-07-31031 July 1998 Revised LaSalle Unit 1 Cycle 8 COLR & Reload Transient Analysis Results ML20236P8231998-07-14014 July 1998 Special Rept:From 980614-17,various Fire Rated Assemblies Were Inoperable for Period Greater than Seven Days.Caused by Test Equipment Being Routed Through Fire Doors.Established Fire Watches & on 980619 Assemblies Were Declared Operable ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20236L8041998-07-0606 July 1998 Safety Evaluation Granting Licensee 980304 Request for Second 10-yr Interval Pump & Valve IST Program Plan,Rev 2, Including Changes to 2 ASME Boiler & Pressure Vessel Code Relief Requests Previously Submitted in Rev 1 ML20236P3611998-06-30030 June 1998 Monthly Operating Repts for June 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20249C4891998-06-22022 June 1998 Special Rept:On 980522,Fire Detection Zone 1-31 Was Noted out-of-service for More than 14 Days.Detection Sys Was Taken out-of-service on 980508 to Prevent False Alarms During Hot Work Activities.Sys Was Returned to Operable Status 980528 ML20248M3101998-05-31031 May 1998 Monthly Operating Repts for May 1998 for LaSalle County Nuclear Power Station,Units 1 & 2 ML20236V7771998-05-31031 May 1998 Rev 1 to 24A5180, Supplemental Reload Licensing Rept for LaSalle County Station Unit 1 Reload 7 Cycle 8 ML20217Q7041998-05-0404 May 1998 Safety Evaluation Accepting Util Request to Leave Leak Chase Channels Plugged During Performance of Containment ILRT ML20247M4491998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for LaSalle County Station ML20216F4941998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for LaSalle County Station,Units 1 & 2 ML20217N6581998-03-30030 March 1998 Special Rept on Fire Detection,Deluge Sys & Fire Rated Assemblies During Period of 980303-25.Established Fire Watches Until Affected Equipment Is Returned to Operable Status ML20216D9511998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for LaSalle County Station,Units 1 & 2 ML20247M4631998-02-28028 February 1998 Rev Monthly Operating Rept for Feb 1998 for LaSalle County Station ML20203D7241998-02-20020 February 1998 Special Rept:On 980118,Fire Detection Zones 1-18 & 2-18 Taken out-of-svc to Prevent False Alarms During Hot Work Activities on Auxiliary Electric Equipment Room Ventilation Sys.Fire Watches Will Remain in Place ML20202G9851998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for LaSalle County Station,Units 1 & 2 ML20199K1651998-01-23023 January 1998 Rev 65h to Topical Rept CE-1-A, Comm Ed QA Tr 1999-09-30
[Table view] |
Text
f; ,; r c
. p --~~ .
i
'I LaSalle County Nuct:ar Station
'f RuralRoute #1, Box 220
'l v Marseilles, Illinois 61341
\ Telephone 815/357 6761 March 9, 1990 a
Director of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission Mail Station F1-137 Washington, D.C. 20555
Dear Sir:
Licensee Event Report #90-002-00, Docket #050-374 is being submitted to your office in accordance with 10CFR50.73(a)(2)(i).
O G
hl.J.Diederich station Manager LaSalle County station GJD/DAC/kg Enclosure xc: Nuclear Licensing Administrator NRC Resident Inspector NRC Region III Administrator IMPO - Records Center l.
l l
t I 31 '
p s (
e.
i LICENSEE EVENT RF, PORT (LER)
F P LO Docket thseer (2) Pane (3) ]
F'acility Name (1)
Iatalle County Station Unit 2 015101010131714 1 ofl0l6 Title (4)
Surveillance Not PerfwmJ Within Recuired Time Interval Out to Personnel Error and Procedural Inadecuacles Event Date (5) LER thster (6) Report Date (T) Other Facilities involved (8) l Month Day Year Year fy/ // Sequential //j Revision / Month Day Year Facility Neues Docket thseer(s) ;
! /// thseer y//
/ thster 01 51 01 01 01 I I l 01 2 01 9 91 0 91 0 01012
~
01 0 013 01 9 91 0 01 51 01 01 01 1 I ;
THls REPORT IS SUBMITTED PUR$U4NT TO THE REQUIREMENTS OF 10CFR
" (cwt one or more of the followina) (11)
" 1 20.402(b) ,,,,_ 20.405(c) ,,,,,, 50.73(a)(2)(lv) 73.71(b)
POER , 20.405(a)(1)(l) ,,,,,,_ 50.36(c)(1) _ 50.73(a)(2)(v) _ 73.71(c) 20.405(a)(1)(ll) 50.36(c)(2) 50.73(a)(2)(vil) Other (Specify !
LEVEL i i ,,,,,, .,,,_ ,,,,
(10) 01 41 0 _ 20.40$(a)(1)(lli) .x ,, 50.73(a)(2)(l) _ 50.73(a)(2)(vill)(A) in Abstract !
50.73(a)(2)(ll) 50.73(a)(2)(vill)(B) below and in
/ /////// ////'///'//////, _ 20.405(a)(1)(lv) ,,,,,_
50.73(a)(2)(lli) 50.73(a)(2)(x) Text)
/'/ 20.405(a)(1)(v)
/// }'ff3/// /
/ /' /
'f fffff /'ff
//'/'//// _ ,,,,,, _,,,_
tlCENSEE CONTACT FOR THis LER (12)
TELEPHONE NUISER Name AREA CODE Don Crevi. Reoulatory Assurance extension 2e60 8 I i 15 315111-l6171611 C0pFLETE ONE LINE FOR EACH (XWFONENT FAILURE DESCRf tED IN THIS REPORT (13)
C0pFONENT MANUFAC. REPORTA8LE CAUSE SYSTEM COMPONENT MANUFAC- REPORTA8LE CAUSE SYSTEM '
TURER 10 IIPRDS TURER TO NPRDS A l l l l l l l N l l l l l l l }
0 I I I I l l l N I I I I I I I .
SUPPLE 8 ENTAL REPORT EXPECTED (14) Expected Month l Day l Year Submission
~
lyes (if ves, conDiete EXPECTED SUBMISSION DATE) YlNO l ll !l '
l ABSTRACT (Limit to 1400 spaces, i.e, approximately fifteen single-space typewritten Innes) (16)
On february 9, 1990 with Unit 2 in the Run Mode (Operational Condition 1) the LaSalle Operating Surveillance LOS-TG-W1. " Turbine Weekly Surveillance," was detemined to have exceeded its required testing interval as established in Technical Specification 3/4.7.10.
On february 8,1990 at 2045 hours0.0237 days <br />0.568 hours <br />0.00338 weeks <br />7.781225e-4 months <br /> the 7 day +25% period to perfom LOS-TG-W1 as required by Technical specification 4.7.10 was exceeded. The Operating personnel inadvertently allowed the surveillance frequency '
to be exceeded without declaring the bypass valves inoperable due to inattention to detall.
Neither LaSalle Operating Procedure LOP TG-02, " Turbine Generator Startup," nor LaSalle General Procedure, LGP-1-1, 'Nomal Unit Startup," indicate any specific power level requirement which could not be exceeded prior to perfoming Loi-TG411 during a unit startup. LOP-1-1 did Indicate that the surveillance should be started at 15% power. This contributed to allowing Operating personnel miss the requirement for perfoming this surveillance prior to exceeding 25% power.
LOS-TG-W1 was successfully perfomed on february 9,1990 at 0415 hours0.0048 days <br />0.115 hours <br />6.861772e-4 weeks <br />1.579075e-4 months <br /> without further event.
Personnel involved in this event were counselled on attention to details. Procedures LGP-1-1 and LOP-TG-02 will be revised to aid to prevent recurrence of this type of event in the future.
This event is being submitted pursuant to the requirements of 10CFR50.73(a)(2)(l) due to exceeding the required surveillance test time interval.
1 L W 8 EVENT KpcRT (Lit) TEXT CaffilaaATi m Fom Rev 2.0 l pACILlif NRpE (1) DOCKET NueER (2) LER IM WER (6) Peae (3) l Voor /// Sequentia) /,/,/, Revision ;
/// thster - T// thader j
- 11e County Statlan unit 2 015Io1010131114 910 - 01012 - 0I 0 01 2 cF 01 6 !
TEXT Energy Industry identification System (Ells) codes are identified in the test as [XX] l
)
PLANT AND $YSTEM 10EWilFICA110N t
General Electric - telling teater Reactor Energy Industry identification System (Ells) codes are identified in the test as [XX).
.j A. CONDlil0N PRIOR 10 EVEW1 Unit (s): 2 Event Date: 2/9/90 Event ilme: 0000 Hours Reactor Mode (s): 1 Mode (s) ieme: Run PowerLevel(s): ,_,4,,E ,
f S. OESCRIFil0N OF EVENT $
l On February 9,1990 with Unit 2 in the Run Mode (Operational Condition 1) the LaSalle Operating Surveillance LOS-1G41, "Tuttine Weekly Surveillance,' was detemined to have escoeded its required i testing interval as estabitshed in Technical Specification 3/4.7.10.
Technical Specification 3.7.10 requires the Main Turbine (1G) [1A) bypass valves to be operable when I therms) power is greater than 295 of rated themel power and Technical Specification 4.7.10 requires the l bypass valves to be demonstrated operable at least once per 7 days by cycline each valve through at !
least one couplete cycle of full travel.
Listed below is a chronological description of events:
I January 31,1990 Lo$-1G41 was successfully completed.
I February 6,1990 Unit 2 scranned during the performance of LaSalle Instroent Surveillance LIS-NR l
403,- ' Wit 2 Average Power Range Monitor, Rod Block Monitor and Scra Functional Test." W 1e testin0AveragePowerRangeMonitor(APRM,NR)[lG)ChannelF.ReactorProtectionSystem(RPS
- Channel B) flow biased thermal trip which Initiates 1/2 scrm, another 1/2 scrm was received from APRM Channel E (RPS Channel A). This completed the logic for a full reactor scrm (LER 374/90-001-00).
't 1 February 7,1990 LOS-1G41 was scheduled to be performed. This surveillance is not required when
! the unit is shutdown and could not be performed until the Main Turbine was operating at rated speed.
February 7,1990 Unit 2 startup was commenced in accordance with LaSalle General Procedure LOP-1-1,
- " Normal Unit Startup."
j February 8,1990 LOS-TG41 was scheduled to be critical (includes 25% grace period; this is the date the surveillance must be perfomed or the system is declared inoperable).
L1csaem EWimi IEp0RT (LER) 1Exf OWillRIAfle Fem hev 2.0 fACIL11Y MlWE (1) 00CEt1 Nupett (2) LER GRpmER (6) Peae (3)
Year // 5eguential // Revision l
// th e er /j/j/
f
/ th e er I
% 11e county Station unit 2 0 1 5 1 0 1 0 1 0 1 31 71 4 910 - 01012 - 01 0 01 3 0F 01 6 l lItxt Energy Industry identification system (tils) codes are identified in the test as [xx) !
i S. Ot$CRIPiloll 0F EVtW1 (Continued) i I
Following shift turnover at the beginning of day shift 40700-1500 hours), a review of the l surveillance schedule and a review of LGP-l-1 was perfomed by the Unit 2 Shift Forsman ($F, l Ilcensed Senior Reactor Operator). The Unit 2 SF determined that Lo$-TG41, LOS-AP43, ' Turbine .l 1
Stop Valve Scram functional," and LOS-AP-M4, 'Tuttine Control Valve Monthly Survelliance," would need to be performed once the Main Turbine was on line, f At 1056 hours0.0122 days <br />0.293 hours <br />0.00175 weeks <br />4.01808e-4 months <br /> the reactor mode switch was placed in the Run Mode (Operational Condition 1) in l
accordance with LGP-1-1.
l l
At.1323 hours0.0153 days <br />0.368 hours <br />0.00219 weeks <br />5.034015e-4 months <br /> the Main forbine was placed on line and the Main Generator was loaded to the grid, reactorpowerwassubsequentlyincreasedto235bywithdrawingcontrolrods(RD)(AA).
At 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />, shift turnover took place. The same Unit 2 SF renalned on duty. The Unit 2 5F was aware that LOS-TG41, LOS-AP43 and LOS-AP-M4 needed to be performed as required by LGP-1-1, but, was not aware of the requirement to dauenstrate operability of the tuttine bypass valves prior to i reaching 25E thermal power. LOP-1-1 did not Indicate this requirement. ,
j At 1650 hours0.0191 days <br />0.458 hours <br />0.00273 weeks <br />6.27825e-4 months <br /> control rod withdrawal was stopped for the performance of control rod scram time l testing; reactor power was 24.55 of rated thermal power at this time.
Getween 1700 and 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br />, the Unit 2 Shift Foreman had issued the surveillances to be peformed [
to the Unit 2 Nuclear Station Operator (WSo, licensed Reactor Operator). !
-At 2015 hours0.0233 days <br />0.56 hours <br />0.00333 weeks <br />7.667075e-4 months <br /> control rod scram time testing was completed.
At 2045 hcurs the critical time to perform LOS-1G41 was exceeded and the Unit 2 Main Turbine '
Bypass Valves became Inoperable due to exceeding their required surveillance testing time interva) per Technical Specification 4.7.10. Control rod withdrawal was reestabilshed for the purpose of ,
raising reactor power per LGP-1-1.
At 2110 hours0.0244 days <br />0.586 hours <br />0.00349 weeks <br />8.02855e-4 months <br /> reactor power was increased to greater than 25% of rated thermal power, without performance of LOS-TG41 as required by Technical Specification 3.7.10.
At the end of the afternoon shift (1500-2300 hours) the Unit 2 SF questioned the Unit 2 NSO on whether or not the surveillance was performed. The NSO indicated that the surveillance was not done and would have to be completed on the nemt shift. .
At 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br /> the afternoon shift turned over to the midnight shift (2300-0700 hours). The written turnover had indicated that LOS-TG41, LOS-RP-M3 and LOS-AP-M4 needed to be performed.
At 0415 hours0.0048 days <br />0.115 hours <br />6.861772e-4 weeks <br />1.579075e-4 months <br /> on February 9, 1990, LOS-1G 41 was satisfactorily coupleted. At this time the Technical Specification timeclock was exceeded by approminately 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> and 5 minutes. (The action ,
statement of specification 3.7.10 allows 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> to restore the bypass valves to operable status.)
]
l i
I L P2 ant! Evidfi REptuti (LIR) 1EHT Ciuf11NuAT10N Form nov 2.0- i Fame (3) j FACIL11Y INfE (1) 00CKE1 Nu mER (2) LER NWWER (6) __
Year /// Sequential Revision i ff fff
/// thster //)/
// thater l tda11e County statlan unit 2 0 1 5 1 0 1 0 1 0 1 31 71 4 910 - 01012 - 0I o 01 4 0F 01 6 l TEXT Energy Industry identification System (Ells) codes are identified in the text as (KK)
J
- 8. Df.5CRIPiloN OF EVENT (Continued)
During a subsequent review of coupleted surveillances performed on February 14, 1990, it was I determined that the Limiting Condition for Operating per Technical Specification 3.7.10 was enceeded.
This event is being submitted pursuant to the requirements of 10CFR$0.73(a)(2)(l) due to enceeding the required surveillance test time interval.
C. APPARENT CAU$E OF EVENT l
the cause of this event was due to inattention to detall in that a surveillance was allowed to exceed the critical date without declaring the associated equipment inoperable.
l A contributing factor was that the surveillance could not be performed while the unit was shutdown with the Main Steam isolation valves open. $1nce the Main furtine bypass valves are not required to be operable with the reactor less than 25 power, this was not a problem and the 745ay surveillance requirement did not need to be met. However, under these conditions the surveillance must have been i done prior to exceeding 25 power (if the bypass valves wre to remain operable). ,
It is not required to complete one step of the normal unit startup procedure before continuing on with ,
the rest of the procedure. LGP.1-1 currently has a signoff step prior to the step for increasing reactor power to greater than 15 which requires verification that LOS-TG4f1 has been performed. This i
was not done untl) the midnight shift because the Turbine Generator was still being placed on line in accordance with LDP-1G-02. There is no specific guidance in LGP-1-1 that this verification means that the bypass valves must have been tested in the previous 7 days prior to exceeding 2M power.
t Other factors wre identified and listed below:
- 1. The Unit 2 Shift Forseln and Unit 2 NSO were not aware of the Technical Specification requirement l to perform LOS-TG4dl prior to exceeding 25 of rated thermal power, ,
- 2. Neither LGP-1-1, "Notaal Unit Startup," or LDP-TG-02, " Turbine GeMrator Startup," Identified the {
requirement.
- 3. The surveillances wre noted in the last step of LOP-TG-02 after placing the Monsture Separator ,
L Reheater's (MS) [$8), on line.
- 4. TheUnit2SFandExtraSROwereintheprocessofplacingfeedwaterheaters(HD)($M) inservice i_ during shift turnover from the day shift to the afternoon shift. This prevented them from actually participating in the shift (crew) briefing. ,
l l
l
, , . . ~_ -. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ -.
[
i LF8mL88 EVENT REpeni (LER) TEHT CONilenahT10N Fem her 2.0 DOCKET IRpSER (2) LER 1RWe m (6) Pee Cl) I hlCILITY IllfE (1) !
fear /jff Sequential / Revision
//
F/ thsher [/f thsher .[
Lasalle cannty station unit 2 015101010131il4 910 - 01012 - 01 0 01 5 0F 01 6 TEXT Energy ladustry Identification System (Ell 5) codes are identified in the tent as [KX]
\
- 0. SAFETY AleALY$15 0F EVENT ),
The tJ41ne bypass system is not required to effect or support safe shutdown of the reactor or to :
perfom in the operation of reactor safety features. The tuelne bypass system is designed to control reactor pressure as follows: .l l
a) during the reactor heatup to rated pressure while the turbine generator is being brought up to ;
speed and synchrontred,
.b) during power opera *.lon when the reactor steam generation exceeds the transient tustne stean requirements, and
}
c) during reactor cooldown.
t the allowable tolerance for perfoming surveillance activities is sufficiently restrictive to ensure !
that the reliability associated with the surveillance activity is not significantly degraded beyond that ,
obtained from the nominal survelliance interval, too degradation was observed when the surveillance was i perfomed. :
l i
l E.- CORRECTIVE ACTIONS l
At 0415 hours0.0048 days <br />0.115 hours <br />6.861772e-4 weeks <br />1.579075e-4 months <br /> on february 9,1990 LOS-TG41 was satisfactorily completed. .
Personnel involved were counselled on this event. ,
LGP-1-1, LGP-1-3, "Startup from Hot Standby to Power Operations," and LOP-TG-42 will be revised to J include the requirement to perfo m LOS-TG 41 prior to exceeding 25% power per Technical Specifications. J Operating procedures such as startup of the Off-Gas system will be reviewed to detemine if there Is any other Technical Specificatien related equipment where a slallar problem could occur. Action item Record ]
(AIR) 374-200-90-00001 will be issueJ to track the completion of this corre:tive action. .j All licensed operators will be tallgated on this event. Emphasis will be placed on the need to perfom !
all surveillances by the critical date or declare associated equipment inoperable and take the associated actions. AIR 374-200-90-00002 will be Issued to track the completion of this corrective action.
'The LaSalle Aeninistrative Procedure LAP-1600-2, " Conduct of Operations," will be revised to require a discussion of any critical surveillances due in shift briefings. AIR 314-200-90-00003 will be issued to track the completion of this corrective action.
--..y- . . _ _ . . , . , _ ._ . . . _ - . . . , . _ . ,
,y.*
I 1
LVM53 EWEdif REPORT (LER) TERT CiuffitalAf tm Form her 2.0 LER th5GER (6) Paas (3)
'PACillif II W (1) DOCKET tR5GER (2)
Year / Sequential g/// Ilusher g/ hevision
""r
///
l Lasalle County station unit 2 015Io1010131714 910 - 01012 - 01 0 01 6 0F 01 6 TEXT Energy industry identification System (Ell 5) codes are identified in the tent as (XX) l l
i F. PREVIOUS EVENTS !
LER Number Title i
373/M-06140 Failure to Run 1A Olesel Generator Within I Hour Timectock ,
373/95-069 4 0 Missed Fire Protection Surveillance by Mechanical Maintenance Department l 373/M-003 00 Missed Surveillance on heactor Water pil Due to Personnel Error l 373/E 406-00 Unit 1 Reactor Water Conductivity Missed Sample Due to Misunderstanding the j Technical Specification nequirements 373/N-02640 Frequency of Prime y Contalament Air Lock Leakage Rate Test Enceeded 373 4 7-000-00 Missed off Gas Hydrogen Sample Due to Personnel Error 373/87-019 4 0 Failure to Cycle Interundlate Control hads During Surveillance Due to Personnel Error 374/N41040 Failure to Perforn Surveillance on had Worth Minlalzer and mod Serpence control System Durin0 Pouer noduction 374/80 4 04-00 Missed Technical Specification Surveillance Due to Personnel Error 374/08-006-00 Missed Loose Parts Monitor Survelliance Due to Personnel Error G. CopFONENT FAILURE DATA hot appilcable.
[
l l
I l
_